IR 05000255/2006006: Difference between revisions

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| issue date = 10/27/2006
| issue date = 10/27/2006
| title = IR 05000255-06-006 and 05000255-06-012; 07/01/2006 - 09/30/2006; Palisades Nuclear Plant; Operator Performance During Non-Routine Evolutions and Event Follow-up
| title = IR 05000255-06-006 and 05000255-06-012; 07/01/2006 - 09/30/2006; Palisades Nuclear Plant; Operator Performance During Non-Routine Evolutions and Event Follow-up
| author name = Lipa C A
| author name = Lipa C
| author affiliation = NRC/RGN-III/DRP/RPB4
| author affiliation = NRC/RGN-III/DRP/RPB4
| addressee name = Harden P A
| addressee name = Harden P
| addressee affiliation = Nuclear Management Co, LLC
| addressee affiliation = Nuclear Management Co, LLC
| docket = 05000255
| docket = 05000255
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=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:October 27, 2006Mr. Paul A. HardenSite Vice President Nuclear Management Company, LLC Palisades Nuclear Plant 27780 Blue Star Memorial Highway Covert, MI 49043-9530SUBJECT:PALISADES NUCLEAR PLANT NRC INTEGRATED INSPECTIONREPORT 05000255/2006006 and 05000255/2006012
[[Issue date::October 27, 2006]]
 
Mr. Paul A. HardenSite Vice President Nuclear Management Company, LLC Palisades Nuclear Plant 27780 Blue Star Memorial Highway Covert, MI 49043-9530
 
SUBJECT: PALISADES NUCLEAR PLANT NRC INTEGRATED INSPECTIONREPORT 05000255/2006006 and 05000255/2006012


==Dear Mr. Harden:==
==Dear Mr. Harden:==
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P. Harden-2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letterand its enclosure will be available electronically for public inspection in the NRC PublicDocument Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
P. Harden-2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letterand its enclosure will be available electronically for public inspection in the NRC PublicDocument Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/Christine A. Lipa, ChiefBranch 4 Division of Reactor ProjectsDocket No. 50-255License No. DPR-20
Sincerely,
 
/RA/Christine A. Lipa, ChiefBranch 4 Division of Reactor ProjectsDocket No. 50-255License No. DPR-20Enclosure:Inspection Report 05000255/2006006 and 0500025/2006012 w/Attachment: Supplemental Informationcc w/encl:J. Cowan, Executive Vice President and Chief Nuclear Officer R. Fenech, Senior Vice President, Nuclear Fossil and Hydro Operations D. Cooper, Senior Vice President - Group Operations L. Lahti, Manager, Regulatory Affairs J. Rogoff, Vice President, Counsel and Secretary A. Udrys, Esquire, Consumers Energy Company S. Wawro, Director of Nuclear Assets, Consumers Energy Company Supervisor, Covert Township Office of the Governor State Liaison Office, State of Michigan L. Brandon, Michigan Department of Environmental Quality -
===Enclosure:===
Inspection Report 05000255/2006006 and 0500025/2006012
 
===w/Attachment:===
Supplemental Informationcc w/encl:J. Cowan, Executive Vice President and Chief Nuclear Officer R. Fenech, Senior Vice President, Nuclear Fossil and Hydro Operations D. Cooper, Senior Vice President - Group Operations L. Lahti, Manager, Regulatory Affairs J. Rogoff, Vice President, Counsel and Secretary A. Udrys, Esquire, Consumers Energy Company S. Wawro, Director of Nuclear Assets, Consumers Energy Company Supervisor, Covert Township Office of the Governor State Liaison Office, State of Michigan L. Brandon, Michigan Department of Environmental Quality -
Waste and Hazardous Materials Division
Waste and Hazardous Materials Division


Line 291: Line 281:


===Closed===
===Closed===
: [[Closes finding::05000255/FIN-2006006-01]]NCVThe licensee failed to demonstrate that the performance orcondition of High Pressure Injection System had been
05000255/2006006-01NCVThe licensee failed to demonstrate that the performance orcondition of High Pressure Injection System had been
effectively controlled (Section R12)
effectively controlled (Section R12)05000255/2006006-02NCVControl Valve CV-3070 Failed to Stroke (Section 4OA5.2)
: [[Closes finding::05000255/FIN-2006006-02]]NCVControl Valve CV-3070 Failed to Stroke (Section 4OA5.2)
: 05000255/2006004-07URIControl Valve CV-3070 Fails to Stroke (Section 4OA5.2)
: [[Closes finding::05000255/FIN-2006004-07]]URIControl Valve CV-3070 Fails to Stroke (Section 4OA5.2)
: 05000255/2005202-01URIVerification of contents of two storage tubes which containrod fragments from assembly 1-024 (Section 4OA5.1)
: [[Closes finding::05000255/FIN-2005202-01]]URIVerification of contents of two storage tubes which containrod fragments from assembly 1-024 (Section 4OA5.1)


===Discussed===
===Discussed===
Line 303: Line 292:
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
The following is a list of documents reviewed during the inspection.
The following is a list of documents reviewed during the inspection.
: Inclusion on this list doesnot imply that the NRC inspectors reviewed the documents in their entirety but rather that selected sections or portions of the documents were evaluated as part of the overall inspection effort.
: Inclusion on this list doesnot imply that the NRC inspectors reviewed the documents in their entirety but rather that
: Inclusion of a documents on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.
: 1R04Equipment AlignmentPalisades Nuclear Administrative Procedure 4.02, Control of Equipment, Revision 29SOP-15 Checklist 15.1, Service Water System Checklist - Critical, Revision 38
: SOP-22 Checklist 22.1, Diesel Generators System Checklist, Revision 40
: SOP-22 Checklist 22.2, Fuel Oil System Checklist, Revision 40
: SOP-22, Diesel Generator System, Revision 40
: SOP-12, Checklist 12.5, Auxiliary Feedwater System Checklist, Revision 47
: SOP-12, Checklist 12.6, K-8 Steam Supply Checklist, Revision 47
: SOP-3, Checklist 3.9, Engineered Safeguards Administrative Control Verification, Revision 68
: Piping and Instrument Diagram (P&ID) -216, Lube Oil, Fuel Oil and Diesel Generator Systems, Sheet 1, Revision 69
: DBD-1.02, Service Water System, Revision 7
: MO-29, Engineered Safety System Alignment, Revision 34
: T-190, Service Water Supply to Auxiliary Feedwater, Revision 0
: 1R05Fire ProtectionPalisades Nuclear Plant Fire Hazards Analysis, Revision 5FPP-95-49, Engineering Analysis:
: Evaluation of the Effects of a Fire on the Ceiling of the Auxiliary Feedwater Pump Room
: AR01041901, Questionable Separation of Service Water Pumps and Fire Pump
: 1R06Flood ProtectionDBD 7.08, Plant Protection Against Flooding, Revision 5MSM- M - 16, Inspection of Watertight Barriers, Revision 12
: 1R07Heat SinkT-390, Single Tube Testing of the CCW Heat Exchangers, Revision 2Master Heat Exchanger Testing Plan, Revision 4, July 27, 2006
: Palisades Raw Water Corrosion Program Report - Operational Cycle 18 and 2006 Refueling Outage, Revision 0, June 12, 2006
: Health and Status Report for Component Cooling Water System, August 29, 2006
: 1R11Licensed Operator RequalificationSimulator Exercise Guide, Revision 0
: EOP-2.0, Reactor Trip Recovery, Revision 12
: ONP-18, Pressurizer Pressure Control Malfunctions, Revision 17
: ONP-4.2, Loss of Containment Integrity, Revision 4
: 1R12 Maintenance EffectivenessEGAD-EP-10, Maintenance Rule (MR) Scoping Document - HPSI, Revision 4System Health and Status Report, HPSI, July 14, 2006 and September 21, 2006
: CAP048210,
: MO-3064, Redundant HPSI to Reactor Coolant Loop 2A, would not go closed,June 6, 2005
: ACE003585 - CAP048210,
: MO-3064, Redundant HPSI to Reactor Coolant Loop 2A, would notgo closed, June 9, 2005
: MRE000377, MR Evaluation for
: MO-3064, June 9, 2005
: AR01023338, Unsatisfactory HPSI MR Performance Trend, July 31, 2006
: CAP 049839, Possible Incorrect MR Functional Failure Determinations for
: MO-3064 Events, September 22, 2005
: CAP047828, Torque Switch Setting on
: MO-3064 Found Low During Testing, May 10, 2005
: CAP037030, Subcooling
: CV-3070 Failed to Open During
: QO-5 Valve Test Procedure, August 8, 2003
: CAP 01050615, High Pressure Injection System in Main Rule (a)(1), September 15, 2006
: CAP 01052257, MR (a)(1) Classification of HPSI Systems Potentially Untimely, Sept. 26, 2006
: EM-25, MR Program, Revision 5
: OPR 000108, Outside Ambient Air Temperature in Excess of 95
oF, Revision 0EGAD-EP-10, MR Scoping Document,125 Volt Vital DC Power, Revision 4
: Letter from K. Toner to D. Crutchfield, Palisades Plant- Heating , Ventilating and Air Conditioning- SEP Topic
: IX-5, Ventilation Systems- Submittal of Switchgear Room, CableSpreading room and AFWP Room Test Results, November 1, 1982
: 1R13Maintenance Risk Assessments and Emergent Work EvaluationWorkweek 0627, Scheduled Yellow Path 1-1 EDG Testing, July 2 through July 8, 2006
: 1R15Operability EvaluationsFP-OP-OL-1, Corporate Office Quality Procedures:
: Operability Determination, Revision 1EC-8337, Evaluation of T-394 Load Test and Ability to Meet DB Load Requirement, June 6, 2006
: MO-7A-2, EDG 1-2, Revision 60
: OPR 01041995, Pin-hole Leak Downstream of
: CV-0824 on
: HB-23-16, Service Water Return from Containment, Revision 0
: OPR 01044874, AFWP, P-8B, Revision 0
: CAP01045286, Discrepancy exists between oil change procedures, August 18, 2006
: OPR 01050711, EDG 1-2, Revision 1
: 1R17Permanent Plant ModificationsEAR-2005-0063, Modification to Existing Design of Component Cooling Water Heat ExchangerService Water Outlet Valves, July 25, 2005
: 05-0652, 50.59 Screen for Modification to Existing Design of CCW Heat Exchanger SW Outlet Valve(s) CV-0823/6
: 1R19Post Maintenance TestingMO-7A-2, EDG 1-2, Revision 60WO
: 00293000-01, Unexpected Alarm EDG 1-2, troubleshoot and repair, August 22, 2004
: 1R22Surveillance TestingCOP-22A, Diesel Fuel Oil Testing Program, Revision 6DWG 96-7307F1B3, Diesel Fuel Oil Tank, Revision 0
: DWG C-228, Tank T-10A Foundation Section and Details, Revision 0
: QO-21, Inservice Test Procedure - AFWPs , Revision 28
: QO-5, Valve Test Procedure - Includes Containment Isolation Valves, Revision 70
: RT-202, Control Room HVAC Heat Removal Capability, Revision 5
: 1R23Temporary ModificationsEC 8290, Addition of Supplemental Diesel Generator & Breaker 152-403 at SafeguardsBus A14, Cubicle 4
: Screen 06-129, Install Temporary 2400V Diesel Generator, Revision 12OS1Access Control to Radiologically Significant Areas
:ACE003556, Items Suspended in Spent Fuel Pool Not Posted Correctly, August 8, 2005
: CE01007963-01, Locked High Rad Barrier no Secured as Tightly as Possible, Jan. 23, 2006
: ACE1034659-01, Higher that Expected Dose Rates Were Identified While Performing a Non-
: Routine Survey Around Advanced Liquid Processing System, August 4, 2006
: RCE1024675, Movement of Locked High Radiation Area Swing Gate, April 18, 2006
: ACE001023002, L-30 Crane Controls not Properly Secured and Controlled, April 25,2006
: HP 2.5, High Radiation Area Entry and Control, Revision 23
: HP 2.6, Containment Entry with the Reactor Critical, Revision 11
: HP 2.20, Radiation Safety Area Posting, Revision 20
: HP 2.33, Dose Investigation and Assessment, Revision 13
===Procedure===
: No. 5.09, Maintenance Cleanliness Standards, Revision 114OA1Performance Indicator Verification
:NRC PI Occupational Exposure Control Effectiveness (OR-1), July 2005 through July 2006
: NRC PI RETS / ODCM Radiological Effluent Occurrence (PR-1), July 2005 through July 20064OA2 Problem Identification and ResolutionPalisades Management Review Meeting, August 2006Operations Department Monthly Performance Report, August 2006
: Administrative Procedure 4.12, Operator Work-around Program, Revision 4
: CAP 01014772, Potential to Lose PCS Inventory Makeup Capability in Appendix R Fire Area 13
: CAP 01014535, Design Basis Potentially not Fully Met for T2 and AFW Pumps
: CAP 01009099,
: CV-1059 Strokes Open to Close ` 54 Seconds
: CAP 01008006, Potential Operator Challenge During Containment Sump Drain T-60 Dirty Waste Drain Tanks
: CAP 01029671, P-50D Primary Coolant Pump Vapor Seal Leak4OA3Event Follow-upLER 05-07, Inoperable EDG for a Time Longer Than Permitted by TSs, Revision 0Letter from P. Harden to NRC, Cancellation of Licensee Event Report 05-007, July 7, 2006
: EC 8337, Evaluation of T-394 Load test and Ability to Meet DB Load Requirement, June 6,
: 2006
: EA-Elec-LDTAB-005, EDG 1-1 and 1-2 Steady State Loadings, Revision 7
: 54OA5OtherLetter from P. Harden to NRC Bulletin 2005-01, "Material Control and Accounting at Reactors  and Wet Spent Fuel Storage Facilities Commitment Closeout", June 30, 2006
: Palisades Assembly I-021, Rod S15 Material Accountability Sheet, August 25, 1993
: Fuel Rod Fragment Survey, April 17, 2006
: Selected Control Room Logs, January 2004 through September 2006
: Emergency Diesel Generator System Health Report
: EDG NRC Performance Indicators, 2005
: EDG Performance Indicators, First and Second Quarters 2006
: Critical Service Water System Health Report
: MSPI Validation Package for Cooling Water Systems Engineered Safety Systems Performance Indicators 2005
: Engineered Safety Systems Performance Indicators, First and Second Quarters 2006
: Palisades Baseline Planned Unavailability for MSPI Implementation database
: NMC Palisades Nuclear Plant MSPI Basis, July 25, 2006
: MSPI Derivation Report, Data Entry 3.0
: Auxiliary Feedwater Performance Indicators, 2005
: Auxiliary Feedwater Performance Indicators, First and Second Quarters 2006
: 6
==LIST OF ACRONYMS==
: [[USEDAD]] [[AMSAgency-Wide Document and Management SystemAFWPAuxiliary Feedwater Pump]]
: [[ALARAA]] [[Low As Is Reasonably Achievable]]
ARAction Request
CAPCorrective Action Program
CCWComponent Cooling Water
CFRCode of Federal Regulations
CRCondition Report
DCDirect Current
: [[DRSD]] [[ivision of Reactor Safety]]
: [[EDG]] [[Emergency Diesel Generator]]
HPSIHigh Pressure Safety Injection
IMCInspection Manual Chapter
IPInspection Procedure
LCOLimiting Condition of Operation
LERFLarge Early Release Frequency
LERLicensee Event Report
MPFFMaintenance Preventable Functional Failures
MRMaintenance Rule
: [[MSPIM]] [[itigating Systems Performance Index]]
: [[NCV]] [[Non-Cited Violation]]
ODCMOff-site Dose Calculation Manual
OPROperability Recommendations
PARSPublicly Available Records
PIPerformance Indicator
RIResident Inspector
RPRadiation Protection
SDPSignificance Determination Process
SITSafety Injection Tank
SRASenior Reactor Analyst
SSCStructures, Systems, and Components
SWService Water
TITemporary Instruction
TMTemporary Modification
TSTechnical Specification
UFSARUpdated Final Safety Analysis Report
: [[URIU]] [[nresolved Item]]
}}
}}

Revision as of 10:35, 13 July 2019

IR 05000255-06-006 and 05000255-06-012; 07/01/2006 - 09/30/2006; Palisades Nuclear Plant; Operator Performance During Non-Routine Evolutions and Event Follow-up
ML063040322
Person / Time
Site: Palisades Entergy icon.png
Issue date: 10/27/2006
From: Christine Lipa
NRC/RGN-III/DRP/RPB4
To: Harden P
Nuclear Management Co
References
IR-06-006, IR-06-012
Download: ML063040322 (30)


Text

October 27, 2006Mr. Paul A. HardenSite Vice President Nuclear Management Company, LLC Palisades Nuclear Plant 27780 Blue Star Memorial Highway Covert, MI 49043-9530SUBJECT:PALISADES NUCLEAR PLANT NRC INTEGRATED INSPECTIONREPORT 05000255/2006006 and 05000255/2006012

Dear Mr. Harden:

On September 30, 2006, the U. S. Nuclear Regulatory Commission (NRC) completed aninspection at your Palisades Nuclear Plant. The enclosed report documents the inspection findings which were discussed on September 26, 2006, with you and other members of your staff.The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.Based on the results of this inspection, two NRC-identified findings of very low safetysignificance (Green) were identified. Both of these findings were determined to involve a violation of NRC requirements. However, because the violations were of very low safety significance and because the issues have been entered into your corrective action program, the NRC is treating these findings as a non-cited violations (NCVs) consistent with Section VI.A.1 of the Enforcement Policy. If you contest the subject or severity of a NCV, you should provide a response with a basis for your denial, within 30 days of the date of this inspection report, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -

Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office ofEnforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Palisades facility.

P. Harden-2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letterand its enclosure will be available electronically for public inspection in the NRC PublicDocument Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/Christine A. Lipa, ChiefBranch 4 Division of Reactor ProjectsDocket No. 50-255License No. DPR-20Enclosure:Inspection Report 05000255/2006006 and 0500025/2006012 w/Attachment: Supplemental Informationcc w/encl:J. Cowan, Executive Vice President and Chief Nuclear Officer R. Fenech, Senior Vice President, Nuclear Fossil and Hydro Operations D. Cooper, Senior Vice President - Group Operations L. Lahti, Manager, Regulatory Affairs J. Rogoff, Vice President, Counsel and Secretary A. Udrys, Esquire, Consumers Energy Company S. Wawro, Director of Nuclear Assets, Consumers Energy Company Supervisor, Covert Township Office of the Governor State Liaison Office, State of Michigan L. Brandon, Michigan Department of Environmental Quality -

Waste and Hazardous Materials Division

SUMMARY OF FINDINGS

IR 05000255/2006006 and 05000255/2006012; 07/01/2006 - 09/30/2006; Palisades NuclearPlant; Operator Performance During Non-routine Evolutions and Event Follow-up.This report covers a 3-month period of baseline inspections. The inspections were conductedby Region III inspectors and resident inspectors. This report includes two green findings, both of which were NCVs. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process (SDP)." Findings for which the SDP does not apply may be "Green" or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.

A. NRC-Identified

and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified a finding of very low safety significance (Green) andan associated Non-Cited Violation (NCV) of 10 CFR 50.65 "Requirements for monitoring effectiveness of maintenance at nuclear power plants." Specifically, contrary to 50.65(a)(2), the licensee failed to demonstrate that the performance of condition of the HPSI System had been effectively controlled through performance of appropriate maintenance, and did not place the system in 50.65(a)(1) status when system performance deteriorated. The licensee subsequently placed the HPSI system in 50.65(a)(1) status and entered the finding into their corrective action program. The inspectors determined that not placing the system in (a)(1) status whenperformance deteriorated is more than minor because it matched an example in IMC 0612, Appendix E, "Examples of Minor Violations," as being more than minor.

The finding is of very low safety significance because the finding did not result in loss of a safety function. (Section 1R12)*Green. A Green NCV was self-revealed on March 29, 2006, when control valveCV-3070, left train HPSI sub-cooling valve for HPSI pump P-66B, failed to open during preventive maintenance. Subsequent investigation by the licensee identified that a design change had removed a support for the valve. The removal of this support caused the valve to bind. The finding is a violation of 10 CFR 50, Appendix B,

Criterion III. The licensee entered the finding into the corrective action program, repaired the valve and added additional support to prevent recurrence.The inspectors concluded that the issue is more than minor because it affected theoperability, reliability, and availability of a mitigating system. The inspectors concluded a phase 3 assessment was required based on the results of phase 1 and 2 assessments.

Following a phase 3 assessment, the Senior Reactor Analyst concluded that the finding is of very low safety significance. (Section 4OA5.2)

2

B.Licensee-Identified Violations

A violation of very low safety significance, which was identified by the licensee has beenreviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and corrective actions are listed in Section 4OA7 of this report.

3

REPORT DETAILS

Summary of Plant StatusThe plant operated at or near full Rated Thermal Power during the inspection period.1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, andEmergency Preparedness1R04Equipment Alignment.1 Partial Walkdowns (71111.04Q)

a. Inspection Scope

The inspectors completed five equipment alignment inspection samples by performingpartial walkdowns of the following risk-significant plant equipment:*Right train diesel 1-2 alignments including service water (SW) and fuel supportsystem while left train emergency diesel generator (EDG) was out for testing*EDG 1-2 during elevated risk due to adverse weather;

  • EDG 1-1 immediately following inoperability of the 1-2 EDG;
  • Steam driven auxiliary feedwater pump (AFWP) during inoperability of motordriven AFWP; and*"B" train high pressure injection system while "A" train was out of service formaintenance. During the walkdowns, the inspectors verified that power was available, that accessibleequipment and components were appropriately aligned, and that no open work orders for known equipment deficiencies existed which would impact system availability.The inspectors also reviewed selected condition reports (CRs) related to equipmentalignment problems and verified that identified problems were entered into the corrective action program. The documents reviewed during this inspection are listed in the attachment.

b. Findings

No findings of significance were identified..2Complete Walkdown (71111.04S)The inspectors completed one semi-annual equipment alignment inspectionsample by performing a complete walkdown of the SW system. Utilizing piping and instrumentation diagrams and system checklists, the inspectors verified that accessible system components were correctly aligned. The inspectors also 4reviewed open maintenance work orders to verify that the equipment's safety functionwas not adversely impacted by pending work. The inspectors reviewed selected CRs associated with the SW system to verify thatidentified problems were entered into the corrective action program with the appropriate significance characterization. The inspectors also verified that planned and completed corrective actions were appropriate.

b. Findings

No findings of significance were identified.

1R05 Fire Protection.1Fire Area Walkdowns

a. Inspection Scope

The inspectors completed six fire protection inspection samples by touring the followingareas in which a fire could affect safety-related equipment:AFWP room (Fire Area 24)Screenhouse - intake structure (Fire Area 9)Outside areas and post indicating valve positions1-C switchgear room (Fire Area 4)Control room (Fire Area 1)Turbine building 625' elevation (Fire Area 23D) The inspectors verified that transient combustibles and ignition sources wereappropriately controlled, and that the installed fire protection equipment in the fire areas corresponded with the equipment which was referenced in the Updated Final Safety Analysis Report (UFSAR), Section 9.6, "Fire Protection." The inspectors also assessed the material condition of fire suppression systems, manual fire fighting equipment, smoke detection systems, fire barriers and emergency lighting units. For selected areas, the inspectors reviewed documentation for completed surveillances to verify that fire protection equipment and fire barriers were tested as required to ensure availability.The inspectors reviewed selected CRs associated with fire protection to verify thatidentified problems were entered into the corrective action program with the appropriate significance characterization. The inspectors also verified that planned and completed corrective actions were appropriate. The documents reviewed during this inspection are listed in the attachment.

b. Findings

No findings of significance were identified.

51R06Flood Protection (71111.06)

a. Inspection Scope

The inspectors completed one inspection sample pertaining to flood protectionmeasures for internal flooding events. The inspectors performed a walkdown of the component cooling water (CCW) room and its flood barriers to verify the flood barriers were in acceptable condition. The inspectors reviewed the licensee's flood analysis for the CCW room and determined the analysis was consistent with configuration of the room. Further, the inspectors reviewed CRs to verify that corrective actions for previouslyidentified flood protection problems were appropriate and had been properly implemented.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance (71111.07A)

a. Inspection Scope

The inspectors reviewed heat exchanger performance for the component cooling watersystem. The inspectors checked the licensee's data for heat exchanger flow to verify no evidence of fouling existed. The inspectors also reviewed the licensee's program for monitoring and ensuring the operability of the plant's heat exchangers. In addition, the inspectors verified that the heat exchangers were correctly categorized under the Maintenance Rule and verified that they were receiving the required maintenance. This represents one sample.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11Q)

a. Inspection Scope

The inspectors completed one inspection sample of licensed operator requalificationtraining by observing a crew of licensed operators during simulator training on August 30, 2006. The inspectors assessed the operators' response to the simulated events which included a loss of pressurizer control and a loss of containment integrity.The inspectors verified that the operators were able to effectively mitigate the eventsthrough accurate and timely implementation of applicable alarm response procedures; Off-Normal Procedure 4.2, "Loss of Containment Integrity," Off-Normal Procedure 18, "Pressurizer Pressure Control Malfunctions," and Emergency Operating Procedure 2.0, "Reactor Trip Recovery." The inspectors also observed the post-training critique to 6assess the licensee evaluators' and the crew's ability to self-identify performancedeficiencies.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12Q)

a. Inspection Scope

The inspectors completed two inspection samples pertaining to maintenanceeffectiveness by reviewing maintenance rule implementation activities for the following system and components:*High Pressure Safety Injection System*125 Volt Vital DC PowerThe inspectors reviewed the licensee's implementation of the maintenance rulerequirements to verify that component and equipment failures were evaluated and appropriately dispositioned. The inspectors also verified that the selected systems and components were scoped into the maintenance rule and properly categorized as (a)(1) or (a)(2) in accordance with 10 CFR 50.65.

b. Findings

IntroductionThe inspectors identified a finding of very low safety significance (Green) and anassociated NCV of 10 CFR 50.65 "Requirements for monitoring effectiveness of maintenance at nuclear power plants." Specifically, contrary to 50.65(a)(2), the licensee failed to demonstrate effective control of performance of the HPSI System and did not place the system in (a)(1) status, establish goals and commence monitoring performance or condition when system performance deteriorated. DescriptionWhile performing a Maintenance Effectiveness inspection of the HPSI system inaccordance with Inspection Procedure (IP) 71111.12, the inspectors noted that from May 10, 2005, to March 29, 2006, the system had experienced four Maintenance Preventable Functional Failures (MPFFs). As specified by the licensee's Maintenance Rule Scoping Document, the licensee established performance criterion as less than two failures in a 24 month period. In addition, during the review of the HPSI system Maintenance Rule documents, the inspectors noted that the Mitigating Systems Performance Index (MSPI) evaluation resulted in White.

Following the fourth MPFF on March 29, 2006, the licensee wrote an Action Request(AR) to evaluate the HPSI system for placement in 10 CFR 50.65(a)(1). The licensee concluded that because the failures were not related to each other and corrective 7actions had been taken for failures, the HPSI system did not warrant placement in10 CFR 50.65(a)(1). The inspectors questioned the licensee's conclusion that the system should remain in 10 CFR 50.65(a)(2) given the number of failures and the licensee reiterated their conclusion. On August 24, 2006, the Maintenance Rule expert panel met and recommended to the engineering systems manager that the system be placed in 10 CFR 50.65(a)(1). Subsequently, the engineering systems manager approved the decision and placed the system in 10 CFR 50.65(a)(1) status on August 31, 2006 and commenced monitoring performance against licensee-established goals.

The inspectors concluded that effective control of the HPSI system performancehad not been demonstrated as evidenced by the four MPFFs in less than 12 months, compounded with a white MSPI. In addition, the inspectors concluded that the licensee had ample time and opportunities prior to the start of the inspection to appropriately evaluate the effectiveness of the maintenance of the system. Regardless of the causes for the four failures, the licensee should have established goals and commenced monitoring the performance or condition of the system under 10 CFR 50.65(a)(1) when the multiple MPFFs indicated that system performance was not being effectively controlled through appropriate maintenance, to ensure that the system remained capable of performing its intended safety function. The licensee's failure to place the system in 10 CFR 50.65(a)(1) status when performance deteriorated resulted in the system not being monitored against licensee-established goals.

AnalysisThe inspectors determined that the failure to place the HPSI System into10 CFR 50.65(a)(1) when performance was not being effectively controlled through preventive maintenance was a licensee performance deficiency that warranted review in accordance with the Significant Determination Process. Using the IMC 0612, Appendix E, "Examples of Minor Violations," the inspectors determined that the finding was more than minor. Specifically the finding matches example 7.b.,

in that violations of 10 CFR 50.65(a)(2), are not minor because they necessarily involve degraded system performance. To assess the significance of the finding, the inspectors used Appendix A, "Determiningthe Significance of Reactor Inspection Findings for At-Power Situations" of IMC 0609, "Significance Determination Process," dated November 22, 2005. The inspectors determined that the finding was of very low safety significance, in accordance with the Phase 1 screening worksheet, because:

(1) it did not represent an actual loss of safety function of a system;
(2) it did not represent an actual loss of safety function of a single train for greater than its Technical Specification (TS) allowed outage time;
(3) it did not represent an actual loss of safety function of one or more non-TS trains of equipment designated as risk-significant per 10 CFR 50.65 for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; and
(4) it did not screen as potentially risk significant due to a seismic, fire, flooding, or severe weather initiating event.

8Enforcement10 CFR 50.65(a)(1), requires, in part, that the holders of an operating licensee shallmonitor the performance or condition of structures, systems, or components (SSC's)within the scope of the rule as defined by 10 CFR 50.65(b), against licensee-established goals, in a manner sufficient to provide reasonable assurance that such structures, systems and components, are capable of fulfilling their intended functions.

10 CFR 50.65(a)(2) states, in part, that monitoring as specified in 10 CFR 50.65(a)(1) is not required where it has been demonstrated that the performance of condition of an SSC is being effectively controlled through the performance of appropriate preventive maintenance, such that the SSC remains capable of performing its intended function. Contrary to the above, the licensee failed to demonstrate that the performance orcondition of HPSI System had been effectively controlled through performance of appropriate maintenance, yet, did not monitor against licensee-established goals.

Specifically, from May 10, 2005, to March 29, 2006, the HPSI system experienced four MPFFs, which showed that performance was not being effectively controlled since the performance criterion specified for the system was less than two MPFFs in a 24 month period. Subsequently, on August 31, 2006, the licensee placed the system in 10 CFR 50.65(a)(1). However, because of the very low safety significance and because the issue has been entered into the licensee's corrective action program (AR 01052257), the issue is being treated as a Non-Cited Violation (NCV) consistent with Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000255/2006006-01)

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

The inspectors completed four inspection samples. The inspectors reviewed thefollowing four activities to verify that the appropriate risk assessments were performed prior to removing equipment for work. The inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4), and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors verified the appropriate use of the licensee's risk assessment tool and risk categories in accordance with Administrative Procedure 4.02, Control of Equipment, Revision 29, and Fleet Procedure FP-OP-RSK-01, Risk Monitoring and Risk Management, Revision 0.

Documents reviewed are listed in the attachment. *Yellow risk path due to emergent adverse weather and EDG maintenanceactivities *Yellow risk due to scheduled EDG maintenance activities

  • Emergent work on load center 13
  • Yellow risk due to EDG testing and main transformer workThe inspectors also verified that CRs related to emergent equipment problems wereentered into the corrective action program with the appropriate significance characterization. The inspectors reviewed selected CRs related to risk management 9during maintenance activities to verify that planned corrective actions were appropriateand had been implemented as scheduled.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

For the four operability evaluations described in the Operability Recommendations(OPRs) listed below, the inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors reviewed the UFSAR to verify that the system or component remained available to perform its intended function. In addition, the inspectors reviewed compensatory measures implemented to verify that the compensatory measures worked as stated and the measures were adequately controlled. In addition, the inspectors verified that the CRs generated for equipment operability issues were entered into the licensee's corrective action program with the appropriate significance characterization. Documents reviewed are listed in the attachment.*Operability of EDG 1-2 from October 28 to November 20, 2005*Operability of SW System with pin hole leak

  • Operability of AFWP with questionable oil sample results
  • Operability of EDG 1-2 with erratic fuel oil pressure profile

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications (71111.17A)

a. Inspection Scope

The inspectors reviewed one permanent plant modification package that involvedisolating instrument air to two SW supply valves. The inspectors reviewed the design change information, related design basis documents and the 10 CFR 50.59 screening evaluation to verify that the design bases, licensing bases and performance capability of the involved diesel generator system were not degraded by this modification. In addition, the inspectors reviewed applicable plant documents to verify that any appropriate changes were made. Documents reviewed are listed in the attachment.

b. Findings

No findings of significance were identified.

101R19Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors completed one inspection sample pertaining to post maintenancetesting by assessing testing activities that were conducted for the following maintenance activities:*Testing of EDG 1-2 after replacement of a temperature switch The inspectors observed portions of the post maintenance testing and revieweddocumentation to verify that the tests were performed as prescribed by the work orders and test procedures; that applicable testing prerequisites were met prior to the start of the tests; and the effect of testing on plant conditions was adequately addressed by the control room operators. The inspectors reviewed documentation to verify the test criteria and acceptance criteria were appropriate for the scope of work performed; reviewed test procedures to verify the tests adequately verified system operability; and reviewed documented test data to verify the data was complete, and that the equipment met the prescribed acceptance criteria. Further, the inspectors reviewed CRs to verify that post maintenance testing problems were entered into the corrective action program with the appropriate significance characterization. For select CRs, the inspectors verified that the corrective actions were appropriate and implemented as scheduled.b.FindingsNo findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors witnessed four surveillance tests and/or reviewed test data of selectedrisk-significant SSCs, listed below, to assess, as appropriate, whether the SSCs met the requirements of the TS; the USAR; Palisades Administrative Procedure 9.20, TS Surveillance and Special Testing Program; Engineering Manual EM-09-02 and EM-09-04, Inservice Testing of Plant Valves and Inservice Testing of selected safety-related pumps. One of the samples was an inservice test and one was an isolation valve. The inspectors also determined whether the testing effectively demonstrated that the SSCs were operationally ready and capable of performing their intended safety functions.

Further, the inspectors reviewed selected CRs regarding surveillance testing activities.

The inspectors verified that the identified problems were entered into the licensee's corrective action program with the appropriate significance characterization and that the planned and completed corrective actions were appropriate. Additional documents reviewed are listed in the attachment.COP-22A, Diesel Fuel Oil Testing ProgramQO-5, Valve Test Procedure - Includes Containment Isolation Valves(isolation valve)11QO-21, Inservice Test for AFWPs (IST)RT-202, Control Room HVAC Heat Removal Capability

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors completed one baseline inspection sample by reviewing the followingtemporary modification:*Installation of new non safety-related Diesel Generator 1-3 The inspectors reviewed the design documents and 10 CFR 50.59 safety screening toverify that the temporary modification did not affect the operability of the related systems and other interfacing systems. The inspectors reviewed documentation to verify that the modification was implemented as designed. Post modification testing results were reviewed to verify that the system functioned as intended after the modification was implemented.

b. Findings

No findings of significance were identified.1EP6Emergency Preparedness Drill Evaluation (71114.06)

a. Inspection Scope

The inspectors observed emergency response personnel in the Technical SupportCenter during an emergency planning drill on August 15, 2006. Emergency Preparedness personnel had pre-designated that the opportunities to classify the event and make protective action recommendations would be evaluated and included in the performance indicator data regarding drill and exercise performance.The inspectors verified the emergency classifications, notifications to offsite agencies,and the development of protective action recommendations were completed in an accurate and timely manner as required by the emergency plan implementing procedures The inspectors also verified that the drill was conducted in accordance with the prescribed sequence of events and that the drill objectives were met.The inspectors observed the post-drill critique in the Technical Support Center to verifythat emergency response personnel and drill evaluators adequately self-identified performance problems. The inspectors reviewed the post-drill critique report to verify that the data regarding the indicator for drill and exercise performance was accurate.

Condition reports generated for identified drill performance problems were reviewed to 12verify that the problems were entered into the corrective action program with theappropriate significance characterization. This represents one sample.

b. Findings

No findings of significance were identified.2.RADIATION SAFETYCornerstone: Occupational Radiation Safety2OS1Access Control to Radiologically Significant Areas (71121.01).1Plant Walkdowns/Boundary Verifications and Radiation Work Permit Reviews

a. Inspection Scope

The inspectors reviewed the licensee's physical and programmatic controls for highlyactivated and/or contaminated materials (non-fuel) that could be stored within the spent fuel pool. Specifically, applicable radiation protection (RP) procedures were reviewed, RP staff were interviewed, and a walkdown of the refuel floor was conducted. Although highly activated/contaminated materials are not stored in the spent fuel pool in a manner that readily allowed their inadvertent movement, the radiological controls for the storage of such materials was discussed with RP staff to ensure adequate barriers would be established should the licensee change its practices. This review represented one

sample.b.FindingsNo findings of significance were identified..2Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed the licensee's documentation for all potential PerformanceIndicator (PI) events occurring since the last radiological access control inspection in March 2004 to determine if any of these events involved dose rates greater than 25 Rem/hour at 30 centimeters or greater than 500 Rem/hour at 1 meter or involved unintended exposures greater than 100 millirem total effective dose equivalent (or greater than 5 Rem shallow dose equivalent or greater than 1.5 Rem lens dose equivalent). None were identified. This review represented one sample.

b. Findings

No findings of significance were identified.

13.3High Risk Significant, LHRA and Very High Radiation Area (VHRA) Access Controls

a. Inspection Scope

The inspectors discussed with RP staff the controls that were in place for areas thathad the potential to become high or locked high radiation areas during certain plant operations to determine if these plant operations required communication before hand with the RP group, so as to allow corresponding timely actions to properly post and control the radiation hazards. In particular, reactor operations procedures and RP procedures/job files developed to identify vulnerable areas subject to changing radiological conditions were reviewed and their implementation was discussed withRP supervisory staff. This review represented one sample.b.FindingsNo findings of significance were identified.4.OTHER ACTIVITIES (OA)4OA1Performance Indicator Verification (71151)Cornerstones: Occupational and Public Radiation Safety.1Radiation Safety Strategic Area

a. Inspection Scope

The inspectors sampled the licensee's PI submittals for the periods listed below. Theinspectors used PI definitions and guidance contained in Revision 3 of Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," to verify the accuracy of the PI data. The following PIs were reviewed:*Occupational Exposure Control Effectiveness:

The inspectors reviewed the licensee's assessment of the PI for occupational radiationsafety, to determine if indicator related data was adequately assessed and reported during the previous four quarters. The inspectors compared the licensee's PI data with the CR database, reviewed radiological restricted area exit electronic dosimetry transaction records, and conducted walkdowns of accessible locked high radiation area entrances to verify the adequacy of controls in place for these areas. Data collection and analysis methods for PIs were discussed with licensee representatives to determine if there were any unaccounted for occurrences in the Occupational Radiation Safety PI as defined in Revision 3 of Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline." This review represented one sample.*Radiological Environmental TS/Off-site Dose Calculation Manual (ODCM)Radiological Effluent Occurrences:

14The inspectors reviewed data associated with the RETS/ODCM PI to determine if theindicator was accurately assessed and reported. This review included the licensee's CR database for the previous four quarters, to identify any potential occurrences such as unmonitored, uncontrolled or improperly calculated effluent releases that may have impacted offsite dose. The inspectors also selectively reviewed gaseous and liquid effluent release data and the results of associated offsite dose calculations and quarterly PI verification records generated over the previous four quarters. Data collection and analyses methods for PIs were discussed with licensee representatives to determine if the process was implemented consistent with industry guidance in Revision 3 of Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline." This review represented one sample.b.FindingsNo findings of significance were identified.4OA2Identification and Resolution of Problems (71152).1Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issuesduring baseline inspection activities and plant status reviews to verify that CRs were being generated and entered into the corrective action program with the appropriate significance characterization. For select CRs, the inspectors also verified that identified corrective actions were appropriate and had been implemented or were scheduled to be implemented in a timely manner commensurate with the significance of the identified problem.

b. Findings

No findings of significance were identified..2Semi-Annual Trend Review

a. Inspection Scope

As required by IP 71152, "Identification and Resolution of Problems," the inspectorsperformed a review of the licensee's corrective action program (CAP) action requests to identify trends that could indicate the existence of a more significant safety issue. The inspectors also reviewed the Operations Department Monthly Performance Report dated March 2006, the Site DRUM Report for the 1 st Quarter of 2006 and the Corrective ActionProgram Performance Indicator Summary, dated May 2006. The inspectors' review for potential trends included the results from the daily inspector CAP item screening discussed in Section 4OA2.1. The plant CAP action request screening meetings were observed to review the licensee's level of effort in identifying potential trends, and any associated corrective actions that were planned or implemented. In addition, the 15inspectors reviewed issues documented outside the normal CAP that included,maintenance work orders, component status reports, performance indicators and Operations control room logs. The inspectors' review nominally considered the 6 month period of January through June 2006. The inspectors compared and contrasted their results with the results obtained by the licensee during previous internal reviews.

b. Findings

No findings of significance were identified..3Annual Sample for Follow-up Inspection

a. Inspection Scope

The inspectors completed one inspection sample for annual reviews of selected follow-up by reviewing the cumulative effects of operator work-arounds. The inspectors reviewed licensee practices for the identification, review and assessment of operator work-arounds including any cumulative impact. This inspection included review of the licensee's Administrative Procedure 4.12, "Operator Work-around Program" and biweekly "Palisades OPS Burden Status Report," which also addressed other "operator challenges," and discussions with operations supervisors about program implementation.

b. Findings

No findings of significance were identified.4OA3Event Follow-up (71153).1The inspectors reviewed Licensees Event Report (LER) 2005-07-00, "InoperableEmergency Diesel Generator for a Time Longer than Permitted by TSs" and subsequent correspondence that retracted the LER. The LER reported a condition where a failed snubber valve resulted in both diverting fuel from a single cylinder as well as spreading combustible fuel. In order to understand the licensee's rational for the LER retraction, the inspectors reviewed the basis documents prepared to support the retraction. Based on this review, the inspectors concluded additional information was needed to determined the acceptability of retracting the LER. Unresolved Item (URI)05000255/2006004-06 addressing assessment of the diesel operability remains open.

This LER remains open. 4OA5Other Activities.1(Closed) URI 05000255/2005202-01, "Verification of contents of two storage tubeswhich contain rod fragments from assembly 1-024 "The inspectors reviewed the licensee's response to the subject URI and discussed thisissue with the NRC Senior MC&A Physical Scientist who identified the issue originally.

The inspectors reviewed records developed in conjunction with the physical inventory of a failed fuel rod. The inspectors compared the results with documentation developed 16when the failed fuel was initially loaded into tubes. Based on these records, theinspectors concluded the licensee completed the physical inventories to verify the contents of storage tubes containing fuel pin fragments. These inventories confirmed the location of the fuel pins. This URI is closed..2(Closed) URI 05000255/2006004-07,"Control Valve CV-3070 Fails to Stoke"

a. Inspection Scope

In NRC Inspection Report 05000255/2006004, the inspectors documented URI05000255/2006004-07 regarding the failure of valve CV-3070, left train HPSI sub-cooling control valve, to stroke during maintenance. The licensee has performed and the NRC has reviewed the analysis of the valve's capability needed to close this URI. The licensee's analysis concluded the valve was not operable. This item is

closed.

b. Findings

IntroductionA Green NCV was self-revealed on March 29, 2006 when control valve CV-3070, lefttrain HPSI sub-cooling valve for HPSI pump P-66B, failed to open during preventive maintenance. Subsequent investigation by the licensee identified that a design change had removed a support for the valve. The removal of this support caused the valve to bind. DescriptionWhile performing maintenance to inspect and repair the valve's oiler, the licenseeattempted to test stroke the valve. Once the valve failed to stroke, the plant entered the applicable 72-hour limiting condition for operation action 3.5.2B.1, that requires the train to be restored to operable. After troubleshooting the failure, the licensee determined the valve could not be repaired within the Limiting Condition for Operation (LCO) action time and shut down the plant as required. Troubleshooting of the Control valve revealed the valve could open once it wasmechanically agitated. In addition, diagnostic testing of CV-3070 showed the stem movement of the valve was not smooth. These test results indicated internal valve component interference. Subsequent disassembly of the valve indicated the valves' stem was interacting with the back seat surface, increasing the force needed to open the valve. The licensee's causal analysis identified that in 1994 a support for the valve had beenremoved. A document search did not locate the design basis for the hanger. In addition, the licensee identified that the valve had also failed to stroke on 2003. The licensee concluded that inadequate support for the valve and its operator caused the internal components to bind and the valve to fail to stroke. Prior to restarting the reactor, the licensee repaired the valve and added additional support to prevent recurrence.

17AnalysisThe inspectors determined that the failure to adequately design the valve support was aperformance deficiency. The inspectors assessed this finding using the SDP. The inspectors reviewed the samples of minor issues in IMC 0612, "Power Reactor Inspection Reports," Appendix E, "Examples of Minor Issues," and determined that there were no examples related to this issue. Consistent with the guidance in IMC 0612, "Power Reactor Inspection Reports," Appendix B, "Issue Screening, "the inspectors determined that the finding was of more than minor significance because the failure of the valve to stroke is associated with the operability, reliability and availability of a mitigating system. Specifically, the sub-cooling valve is credited with maintaining subcooling of water to the HPSI pump when the plant is on sump recirculation.Phase 1 AssessmentThe inspectors performed a Phase 1 SDP review of this finding using the guidance provided in accordance with IMC 0609, Significance Determination Process, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-power Situations," Attachment 1. The inspectors determined that the finding represented an actual loss of safety function of a single train of safety-related equipment for greater than its TS allowed outage time and a Phase 2 SDP evaluation was warranted. Phase 2 AssessmentThe inspectors utilized all of the initiating event worksheets except the "AnticipatedTransient without Scram" and "Loss of Service Water " worksheets and solved only those sequences that involved the high pressure recirculation function with a duration of 3-30 days. Based on the results of the SDP worksheets, the inspectors determined that the finding was potentially of low to moderate safety significance (White). The regional senior reactor analyst (SRA) reviewed these results and determined that an SDP Phase 3 assessment was necessary to refine the risk characterization. Phase 3 AssessmentInternal Events - The SRA performed the risk evaluation using the PalisadesStandardized Plant Analysis Risk (SPAR) Model, Level 1, Revision 3P, Change 3.21, created October 2005. The SRA ran the SPAR model assuming failure of Valve CV-3070 to open throughout an exposure time of 672 hours0.00778 days <br />0.187 hours <br />0.00111 weeks <br />2.55696e-4 months <br /> (28 days). The SRA obtained a change in core damage frequency (CDF) of 4.9E-7 (Green) for internalevents. The dominant sequences involved loss of coolant accident scenarios with failure of high pressure recirculation. External Events

- The SRA reviewed the "Individual Plant Examination of ExternalEvents" report for Palisades dated February 1998 and the Palisades Fire Hazards Analysis Report, Revision 6, for insights on risk contribution from external events. In reviewing these documents, Valve CV-3070 was not shown to be needed or relied upon to support post-fire safe shutdown. The SRA determined that the risk contribution of this finding due to fire is insignificant. Regarding seismic and flooding contributors to risk, none of the dominant contributors involved Valve CV-3070. The SRA determined 18that the risk contribution of this finding due to seismic and flooding events was likewiseinsignificant. Large Early Release Frequency (LERF) - Using IMC 0609, Appendix H, "ContainmentIntegrity Significance Determination Process," the SRA determined that this was a Type "A" finding for a pressurized water reactor with large dry containment. Using Table 5.1, the SRA concluded that none of the accident sequences were contributors to LERF. The attributes considered in Table 5.1 were inter-system loss of coolant accidents and steam generator tube ruptures. None of these scenarios was impacted by this finding. The SRA concluded that the LERF was negligible and did notcontribute to the risk associated with this finding. Significance Determination Conclusion- -The SRA concluded that the total CDF for thisissue, considering internal events, external events, and LERF was estimated to be 4.9 E-7 (Green).Enforcement10 CFR 50 Appendix B Criterion III, requires, in part, that "Measures shall beestablished to assure that applicable regulatory requirements and the design basis, as defined in 50.2 and as specified in the licensee application , for those structures systems and components to which this appendix applies are correctly translated into specifications , drawings, procedures, and instructions...." Contrary to theserequirements, the licensee failed to include the hanger in design documentation. In addition, analysis to support removal of the hanger failed to recognize the potential for internal valve binding. As a result, the licensee removed the hanger, thus permitting the valve to bind. However, because this violation was of very low safety significance and because the issue was entered into the licensee's corrective action program as CAP01021152, this violation is being treated as an NCV, consistent with Section VI.A.1 of the Enforcement Policy (NCV 05000255/2006006-02). The licensee's initial corrective action included performing a plant shutdown..3Temporary Instruction (TI) 2515/169 Mitigating System Performance Index Verification

a. Inspection Scope

The inspectors reviewed the licensee's implementation of MSPI reporting guidance inaccordance with TI 2515/169. The inspectors reviewed a sample of procedures where unavailability was excluded due to either the short duration of the unavailability or where the licensee took credit for operator action to recover. For the MSPI systems, the inspectors verified the baseline planned unavailability hours and confirmed the hours were correctly translated into the basis document. In addition, the inspectors selected a sample of planned and unplanned unavailable hours and confirmed through operating logs, maintenance records or CRs that the data was accurate. Finally, the inspectors confirmed the accuracy of failure data on a sampling basis.The inspectors determined that the licensee accurately documented baseline plannedunavailability data; and accurately documented actual unavailability hours. The inspectors determined that one event related to the 1-2 EDG may result in an additional 19failure. If included, the failure would result in the Emergency AC Power MSPIindex crossing the Green/White threshold. This issue is already the subject of URI 05000255/2006004-06. No additional errors were identified in submitted data.

No significant discrepancies were identified in the basis document.

b. Findings

No findings of significance were identified.4OA6Meetings.1Exit MeetingThe inspectors presented the inspection results to Mr. P. Harden and other members oflicensee management on September 26, 2006. Licensee personnel acknowledged the findings presented. The inspectors asked licensee personnel whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified..2Interim Exit MeetingsAn interim exit meeting was conducted for:

  • Occupational radiation safety program for access control and PerformanceIndicator verification with Mr. B. Patrick and Ms. B. Dotson on October 3, 2006. 4OA7Licensee-Identified ViolationsThe following violation of very low safety significance was identified by the licenseeand is a violation of NRC requirements that meets the criteria of Section VI of the NRC Enforcement Policy for being dispositioned as an NCV.Cornerstone: Mitigating Systems

.1 On June 9, 2006, a Nuclear Control Operator (NCO) identified that LCO 3.0.3 had beeninadvertently entered due to two Safety Injection Tank (SIT) bottles being rendered

inoperable at the same time for approximately 40 seconds. Specifically, while performing RI-15C, SIT Level Channel Calibration on T-82B, the NCO vented T-82D due to a pressure rise. The Control Room Supervisor was subsequently made aware of the evolution. Technical Specification 5.4, requires procedures to be implemented and maintained for safety related equipment. Contrary to this requirement, the licensee failed to implement procedures to control operability of the SITs and unknowingly entered LCO 3.0.3. The inspectors reviewed the finding in accordance with IMC 0609 and concluded that since the two SITs were inoperable simultaneously for only 40 seconds and it was recognized promptly by the operating crew, the finding was of very low safety significance. The licensee entered this issue into their corrective action program as AR 01034847.ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

P. Harden, Site Vice President
G. Baustian, Training Manager
T. Blake, Nuclear Safety Assurance Manager
M. Carlson, Engineering Director
B. Dotson, Regulatory Compliance
G. Baustian, Training Manager
G. Hettel, Plant Manager
L. Lahti, Licensing Manager
D. Malone, Regulatory Affairs
C. Moeller, Radiation Protection General Supervisor - Ops
D. Nestle, Radiation Protection General Supervisor - Technical
B. Patrick, Radiation Protection & Chemistry Manager
K. Yeager, Assistant Operations Manager

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened05000255/2006006-01NCVThe licensee failed to demonstrate that the performance orcondition of High Pressure Injection System had been

effectively controlled per 10 CFR 50.65 (Section R12 )05000255/2006006-02NCV Control Valve CV-3070 Failed to Stroke (Section 4OA5.2)

Closed

05000255/2006006-01NCVThe licensee failed to demonstrate that the performance orcondition of High Pressure Injection System had been

effectively controlled (Section R12)05000255/2006006-02NCVControl Valve CV-3070 Failed to Stroke (Section 4OA5.2)

05000255/2006004-07URIControl Valve CV-3070 Fails to Stroke (Section 4OA5.2)
05000255/2005202-01URIVerification of contents of two storage tubes which containrod fragments from assembly 1-024 (Section 4OA5.1)

Discussed

05000255/2006004-06URIFailure of Component on 1-2 EDG Causes SurveillanceFailure (Section 4OA5.3)

2

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection.

Inclusion on this list doesnot imply that the NRC inspectors reviewed the documents in their entirety but rather that