IR 05000255/2019002

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Integrated Inspection Report 05000255/2019002
ML19210D321
Person / Time
Site: Palisades 
Issue date: 07/26/2019
From: Chuck Norton
NRC/RGN-III
To: Arnone C
Entergy Nuclear Operations
References
IR 2019002
Download: ML19210D321 (33)


Text

July 26, 2019

SUBJECT:

PALISADES NUCLEAR PLANT, UNIT 1INTEGRATED INSPECTION REPORT 05000255/2019002

Dear Mr. Arnone:

On June 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Palisades Nuclear Plant, Unit 1. On July 9, 2019, the NRC inspectors discussed the results of this inspection with Mr. D. Corbin, Acting Site Vice President and other members of your staff.

The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Palisades.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Palisades. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Charles H. Norton, Acting Chief Branch 2 Division of Reactor Projects

Docket No. 05000255 License No. DPR-20

Enclosure:

As stated

Inspection Report

Docket Number:

05000255

License Number:

DPR-20

Report Number:

05000255/2019002

Enterprise Identifier: I-2019-002-0061

Licensee:

Entergy Nuclear Operations, Inc.

Facility:

Palisades Nuclear Plant

Location:

Covert, MI

Inspection Dates:

April 1, 2019 to June 30, 2019

Inspectors:

B. Bartlett, Project Engineer

N. Feliz-Adorno, Senior Reactor Inspector

E. Fernandez, Reactor Inspector

M. Holmberg, Senior Reactor Inspector

M. Jones, Reactor Inspector

P. Laflamme, Senior Resident Inspector

J. Mancuso, Resident Inspector

V. Myers, Senior Health Physicist

J. Winslow, Resident Inspector

Approved By:

Charles H. Norton, Acting Chief

Branch 2

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Palisades Nuclear Plant in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Inadequate Ultrasonic Examination of Reactor Head Nozzles Results in Operation with Pressure Boundary Leakage Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000255/2019002-01 Open/Closed

[H.2] - Field Presence 71111.08P The inspectors identified a Green finding and associated Non-Cited Violation (NCV) of Technical Specification (TS) 3.4.13.a, Reactor Coolant System Operational Leakage, for the licensees failure to place the plant in Mode 3 (Hot Standby) within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode 5 (Cold Shutdown) within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> with the plant in Mode 1 (Power Operation) during a portion of operating Cycle 26 with pressure boundary LEAKAGE present at reactor vessel closure head (RVCH) penetration nozzle 25. In particular, the licensees UT contractor mischaracterized flaw indications, and thus had not identified them as flaws before they resulted in operation with the pressure boundary LEAKAGE. The inspectors determined the condition was reasonably foreseeable and preventable by the licensee as there were several weaknesses in the licensees oversight of its contractor that mischaracterized the nozzle flaw indications.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000255/2013005-06 Qualification Basis for Safety-Related Agastat Relays and Molded Case Circuit Breakers 71152 Closed LER 05000255/2018003-00 LER 2018-003-00 Indications Identified in Reactor Pressure Vessel Head Nozzle Penetrations 71111.08P Closed URI 05000255/2018004-01 Potential Failure to Identify/Correct Rejectable Flaws in Reactor Pressure Vessel Head Penetration 71111.08P Closed

PLANT STATUS

The plant began the inspection period at rated thermal power, and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.04) (1 Sample)

(1) The inspectors evaluated readiness to cope with external flooding from May 23 to May 28, 2019

Summer Readiness Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated summer readiness of offsite and alternate alternating current (AC) power systems on May 28, 2019

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Right Train Control Room Heating, Ventilation, and Air Conditioning (CRHVAC)during Left Train CRHVAC maintenance on May 8 and 9, 2019
(2) Safeguards Transformer 1-1 System on May 28, 2019
(3) P-66A, Right Train High Pressure Safety Inspection System following check valve testing on June 27, 2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Fire Area 9: Screen House/Intake Structure during the week of April 1, 2019
(2) Fire Area 24: Auxiliary Feed Water (AFW) Pump Room during the week of April 1, 2019
(3) Fire Area 1: Control Room and Fire Area 33: Technical Support Center during the week of April 1, 2019
(4) Fire Area 29-31: Mechanical Equipment Rooms, on May 24, 2019
(5) Fire Area 4: 1C 2.4KV Switchgear Room on June 20, 2019

71111.07T - Heat Sink Performance Triennial Review (IP Section 02.02)

The inspectors evaluated heat exchanger/sink performance on the following:

(1) Containment Air Coolers VHX-1, VHX-2, VHX-3, Cooled by Service Water
(2) Diesel Generator 1-2 Jacket Water Heat Exchanger, Cooled by Service Water
(3) Ultimate Heat Sink, IP 71111.07T Sections 02.02.d.5 and 02.02.d.6 were completed

===71111.08P - Inservice Inspection Activities (PWR)

PWR Inservice Inspection Activities Sample (IP Section 03.01) (1 Partial)

(1)

(Partial)

The inspectors verified that the reactor coolant system boundary, steam generator tubes, reactor vessel internals, risk-significant piping system boundaries, and containment boundary are appropriately monitored for degradation and that repairs and replacements were appropriately fabricated, examined and accepted by reviewing the following activities from June 17, 2019 to June 27, 2019:

03.01.b - Pressurized-Water Reactor Vessel Upper Head Penetration Examination Activities

  • Reactor head penetration nozzle nonvisual examinations completed during the 2018 refueling outage and during previous outages

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Training/Examinations (IP Section 03.02)===

(1) The inspectors observed and evaluated a Licensed Operator Requalification As Found Exam on June 4, 2019

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (2 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Control Room Ventilation System during the week of April 1, 2019
(2) Chemical and Volume Control System on June 24, 2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Elevated risk for breaker 52-1214, Motor Control Center 22 and 24 480 volt feeder breaker maintenance on May 1, 2019
(2) Elevated risk due to geomagnetic storm, planned battery charger #1 maintenance and testing, and dry fuel cask inspections during the week of May 13, 2019
(3) Elevated risk for planned P-7B, Service Water Pump maintenance and emergent maintenance on 1-1 Emergency Diesel Generator (EDG) during the week of May 6, 2019
(4) Elevated Risk due to 1-1 EDG speed droop relay replacement on June 20, 2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (4 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Evaluation of 2.4 KV Safeguards Power Supply on April 25, 2019 (2)1-1 EDG operability determination after failure to start during surveillance testing on May 7, 2019
(3) Evaluation of Right Channel Safety Injection Actuation System test circuitry on May 24, 2019
(4) Evaluation of 1-1 EDG Indicating Lights for Parallel/Unit Selector Switch on June 4, 2019

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Engineering Change (EC) 81531, Main Transformer Cooler Bank 5 Pump from Temporary Power and EC 82148 Supplemental Cooling to EX-10 Main Transformer from May 31 through June 20, 2019

71111.19 - Post-Maintenance Testing

Post Maintenance Test Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the following post maintenance tests:

(1) QO-5 after CV-3070, P-66B High Pressure Safety Injection Pump Subcooling Valve Actuator maintenance on April 8, 2019
(2) MO-33B after Right Train CRHVAC maintenance on April 19, 2019 (3)1-1 EDG Engine A Start Relay replacement on May 8, 2019
(4) Testing after Battery Charger #1 preventative maintenance on May 13, 2019 (5)1-1 EDG speed droop relay replacement on June 20, 2019

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

FLEX Testing (IP Section 03.02)

(1) P-1003, FLEX Pump One Year Operational Test as documented in WO 52817904 on April 16, 2019

Inservice Testing (IP Section 03.01) (1 Sample)

(1) QO-20A, Low Pressure Safety Injection Pumps on June 18, 2019

Surveillance Tests (other) (IP Section 03.01) (3 Samples)

(1) QO-34, Control Rod Exercising on April 23, 2019
(2) QI-39, Auxiliary Feedwater Actuation System Logic Test on May 15, 2019
(3) RE-132, Diesel Generator 1-2 Load Reject Test on May 20, 2019

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (2 Samples)

(1) The inspectors evaluated an Emergency Response Organization (ERO) Drill on April 10, 2019
(2) The inspectors evaluated an ERO Drill on May 22,

RADIATION SAFETY

71124.05 - Radiation Monitoring Instrumentation

Calibration and Testing Program (IP Section 02.02) (1 Partial)

The inspectors evaluated the calibration and testing program implementation.

(1)

(Partial)

The inspectors completed all items in section 02.02 with the exception of 02.02(c):

Alarm Setpoint and Calibration Method Check of Personnel Contamination Monitors, Portal Monitors and Small Article Monitors

  • SAM 54, SN 285662
  • GEM-5, SN 1712-186
  • ARGOS-5AB, SN 1712-183

Failure to Meet Calibration or Source Check Acceptance Criteria

  • Telepole 6605-093, 01/28/2019
  • HD-09A Air Sampler 23697, 01/10/2019
  • HD-09A Air Sampler 17380, 01/10/2019

Walk Downs and Observations (IP Section 02.01) (1 Sample)

The inspectors evaluated radiation monitoring instrumentation during plant walkdowns.

(1) The inspectors reviewed the following:

Portable Survey Instruments

  • Ludlum 12-4, SN 326407
  • Telepole, SN 6600-038
  • RO-20, SN 11838
  • Ludlum 117, SN 12045
  • Ludlum 43-92, SN 273222
  • AMP 100, SN 600798

Source Check Demonstration

  • Telepole, SN 6600-038
  • RO-20, SN 11838
  • Ludlum 12-4, SN 326407

Area Radiation Monitors and Continuous Air Monitors

  • Area monitor for radiologically controlled area hallway
  • Area monitor for radioactive waste processing area East
  • Area monitor for radioactive waste processing area West
  • Air monitoring system for truckbay
  • Air monitoring system for hot machine shop
  • Air monitoring system for tool decon area Personnel Contamination Monitors, Portal Monitors and Small Article Monitors
  • SAM 54, SN 285662
  • ARGOS-5AB, SN 1712-185
  • GEM-5, SN 091

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Instrumentation and Equipment (IP Section 02.04) (1 Sample)

The inspectors reviewed the following radioactive effluent discharge system surveillance test results:

(1) The inspectors reviewed effluent flow measurements, air cleaning systems, and accident range effluent monitors

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10)===

(1) Unit 1 (10/01/2018-03/31/2019)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (1 Sample)

(1) Unit 1 (April 1, 2018 - March 31, 2019)

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (1 Sample)

(1) Unit 1 (April 1, 2018 - March 31, 2019)

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) Unit 1 (10/01/2018-03/31/2019)

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample.

(IP Section 02.16) (1 Sample)

(1) Unit 1 (10/01/2018-03/31/2019)

71152 - Problem Identification and Resolution

Annual Follow-Up of Selected Issues (IP Section 02.03) (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Licensee Cause Evaluation for Missed Flaw Indications Identified in Reactor Pressure Vessel Head Nozzle Penetrations as documented in CR-PLP-2018-05857 between June 17 and June 27, 2019
(2) Adverse Cause Analysis for RPS Channel B Failure Resulting in an Automatic Reactor Trip on January 9, 2019, as documented in CR-PLP-2019-00117

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends with a focus on human performance issues that might be indicative of a more significant safety issue during the period from January 1, 2019 to June 30, 2019

71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000255/2018-003-00 Indications Identified in Reactor Pressure Vessel Head Nozzle Penetrations. ADAMS Accession: ML19003A239 The circumstances surrounding this LER are documented in the Results Section of this Report

INSPECTION RESULTS

Observation: Semi-Annual Trend Review 71152 The inspectors review was focused on human performance issues, but also considered the results of daily inspector CAP item screening and licensee trending efforts. The inspectors review nominally considered the 6 month period of January 2019 through June 2019, although some examples expanded beyond those dates when warranted by the scope of the trend.

The inspectors reviewed condition reports, trend reports, and human performance evaluations to address performance oversight at the site. During the inspection period, the NRC inspectors noted a few challenges where low level human performance errors occurred in multiple departments, including Operations, Maintenance, and Projects. Examples included an inadvertent fuse disconnect during maintenance activities which resulted in an unanticipated momentary loss of the 1D DC distribution system during live-dead-live checks, component cooling water system miss-alignment to two control rod drive mechanism housings resulting in a 40F increase in housing temperatures, bumping open a Main Steam Isolation Valve Bypass Valve motor power supply breaker with a fire hose during a planned fired drill, and hanging a danger tag on the wrong drain valve on the plant heating boiler system and then not identifying the error until after maintenance had been completed.

Although the above examples did not challenge safety function or equipment reliability, these issues illustrated a decline in the use of human performance tools to prevent errors while performing work in the field and signs of complacency; all of which could potentially impact nuclear safety.

The licensee appropriately entered these issues into the CAP and completed timely evaluations of these issues to determine the causes of the performance decline. Corrective actions included training, site-wide communications reinforcing standards and expectations, and a re-emphasis on the following human performance tools: pre-job briefs; procedure use and adherence; and verification and validation activities. The inspectors determined that the corrective actions taken to date appeared to be effective at addressing the identified gaps and plan to continue to evaluate these actions during routine observations and inspections.

Observation: RPS Channel B Failure Resulting in an Automatic Reactor Trip 71152 On January 9, 2019, the licensee experienced an automatic reactor trip and valid actuation of the auxiliary feedwater (AFW) system. The direct cause of the event was identified to be a loss of all power to the reactor protection system (RPS) BD matrix due to shorted capacitors associated with the RPS B channel and a blown fuse association with the RPS D channel BD matrix power supply. The inspectors reviewed the licensee's final adverse cause analysis after a failure evaluation of the RPS D channel BD matrix power supply and fuse was conducted.

The inspectors reviewed the results of the failure evaluation and discussed these results with the licensee. Using the results of the failure evaluation, the licensee identified that the RPS D channel BD matrix power supply module was no longer meeting its efficiency rating and was a causal factor. Additional corrective actions from the failure evaluation included creation of a periodic maintenance activity to perform periodic thermography on the power supplies to identify potential vulnerabilities to similar failure modes. The inspectors determined that the corrective actions were appropriate and timely based on the safety significance of the issue.

Observation: Licensee Cause Determination - Missed Flaw Indications Identified in Reactor Pressure Vessel Head Nozzle Penetrations 71152 On November 10, 2018, with the plant in Mode 6, during bare metal visual inspections of the reactor vessel closure head (RVCH), dried boric acid was identified in the area of reactor head nozzle 25, indicative of a through-wall flaw. The licensees contractor had recently completed ultrasonic (UT) examinations of this nozzle and the inspectors inquired if the licensees contractor had identified flaw indications or evidence of leakage during this examination. The inspectors questions prompted the licensees contractor to re-review nozzle 25 UT data and the contractor staff subsequently identified an inside diameter (ID)connected flaw indication and UT indications of leakage within the annulus behind nozzle 25 (e.g. UT leak path). Subsequently, the contractor performed a re-review of all nozzle UT data and subsequently applied an eddy current (ET) technique to the ID surface of nozzles 34 and 36 and identified an additional two nozzles with ID flaw indications (nozzles 33 and 36).

The results of the licensee's 2018 RVCH UT examination were documented in report 180-9291875-000 Palisades Unit 1, 1RO26 Reactor Head Inspection Report and included the following information: penetration nozzle 25 had an inside diameter connected axial 100 percent through-wall flaw indication with a 1.4 inch length; penetration nozzle 33 contained an inside diameter connected axial part through-wall flaw indication with a 0.890 inch length; and penetration nozzle 36 had two inside diameter connected part through-wall off-axis flaws that were recorded as 0.514 inch and 0.729 inch in length respectively. As a corrective action, the licensee performed just-in-time training on the flaw characteristics observed in nozzles 25 and 33 and this training was applied to re-inspection of the remainder of the reactor head nozzle population to ensure all flawed nozzles were identified. The licensee repaired the affected nozzles 25, 33 and 36 utilizing the contractor's (Framatome) half-nozzle replacement method prior to returning the RVCH to service. On January 3, 2019, the licensee issued LER 2018-003-00 Indications Identified in Reactor Pressure Vessel Head Nozzle Penetrations and reported this in accordance with 50.73(a)(2)(ii)(A) as a condition of the nuclear power plant, including its principal safety barriers, being seriously degraded. Additional information on the event can be found in Section 71153 of this report.

The licensee documented an apparent cause evaluation (ACA) for boric acid found at control rod drive nozzle 25 in CR-PLP-2018-05857. In this ACA, the licensee identified two direct causes of the boric acid deposit found at control rod drive nozzle 25: Direct Cause 1 - the Palisades head nozzle material (Inconel Alloy 600) which is susceptible to primary water stress corrosion cracking (PWSCC), resulted in a through-wall flaw in nozzle 25, and Direct Cause 2 - the contractor examiners failure to resolve the ID surface initiated flaw in nozzle 25. Additionally, the licensee identified two causal factors: Causal Factor 1 - Flaws that initiate on the outside diameter are the primary area of focus during head penetration exams, resulting in the examiner failing to identify specific characteristics of ID initiated flaws. As a result, the ID initiated flaws were not identified and corrected prior to the through-wall flaw in

1R26 (a.k.a. - Palisades 2018 refueling outage); and Causal Factor 2 - ET was removed as

an examination technique and therefore, the ID initiated flaws were not resolved prior to developing a through-wall flaw in 1R26.

The inspectors reviewed the licensees cause investigation, extent of condition, and extent of cause for this event associated with the identification of degraded nozzles in the RVCH to ensure that the licensee identified the full extent of performance errors and had established actions to correct these errors. Additionally, the NRC Vendor Inspection Branch completed a review of the contractors root cause investigation and corrective actions for this event as this issue potentially impacted other licensees (reference NRC report 99901300/2019-201). The inspectors confirmed the licensee established an adequate basis for the Direct Causes 1 and 2 in the ACA completed under CR-PLP-2018-05857. However, Causal Factor 2 associated with the removal of the ET technique, did not have a sufficient basis for the inspectors to independently confirm this as a causal factor because both ET and UT are qualified to detect ID flaws. Specifically, the UT technique applied was demonstrated as qualified to detect ID flaws and ET was also qualified to detect ID flaws, so either method would be sufficient to detect PWSCC. Therefore, the inspectors could not substantiate Causal Factor 2 and considered this a weakness in the licensees ACA. Additionally, the scope of the licensees ACA was limited to planar flaws within the RVCH nozzles and did not include the contractors failure to identify evidence of a UT leak path signal at nozzle 25. The UT leak path method is relied on to identify flaws that may exist in the J-groove weld of a nozzle and which may not be detected by visual examinations looking for evidence of leakage on the RVCH. To address this issue, the licensees contractor assigned an action to correct this error during the 2018 outage (e.g. just in time training and procedure changes) and therefore the inspectors were not concerned that the narrow scope of the licensees ACA had adversely impacted the ability to detect the full extent of degraded RVCH nozzles and J-groove welds.

In response to the missed flaw indications, the licensee conducted a self-assessment of the programs for contractor oversight of the vessel head inspections. Specifically, in CR-HQN-2019-00577 Fleet NDE oversight of RVCH examinations the licensee identified causal factors and conclusions as they related to programs for oversight of the contractor head UT examinations. In this document, the licensee identified program weaknesses which included:

No governing standard existed for oversight of RVCH inspections; Fleet Inspection Services did not rigorously challenge the implementation of the contractor procedure requirements for two specific areas - pre-job briefings and UT data analyst independence, and no formal operating experience screening was performed for a similar missed flaw event that occurred in 2013 at the Shearon Harris Plant. The licensee concluded that had these insights been realized prior to the examinations, Entergy would have been less vulnerable to missed indications.

The inspectors reviewed the licensees self-assessment as documented in CR-HQN-2019-00577 and confirmed the licensee established an adequate basis for its program findings but noted that the licensee had not reviewed the Indian Point Unit 2 (IP2) nozzle leakage event which occurred within the prior 6 months of the Palisades head leak (reference IP2 licensee event report (LER) 05000-247-2018-001-00, Penetration Indications Discovered During Reactor Pressure Vessel Head Inspection). The lack of a review of the IP2 event to gain insights on program performance indicated a narrow scope of review for related operating experience, in particular since the IP2 site is owned and operated by the Palisades licensee.

Minor Violation 71153 Minor Violation: On January 21, 2019, the licensee was informed by the reactor vessel closure head (RVCH) examination contractor of a Part 21 deviation in contracted services based on a vendor reanalysis of ultrasonic (UT) exam data completed in November of 2018 (reference Framatome CR 2018-9955). The contractor identified a Part 21 deviation from contracted services in RVCH examinations associated with the results the contractors re-review of UT data, for past outages. Specifically, an axially oriented flaw indication was present in the nozzle 25 material that had not been reported as a flaw indication during previous RVCH examinations. As of June 27, 2019, the licensee had not applied site procedure EN-LI-1008-01 10 CFR 21 Evaluations And Reporting in response to the contractors identification of a Part 21 deviation. Specifically, the licensee did not follow Section 5.2 of procedure EN-LI-1008-01 which stated If it is determined that the deficiency/condition does constitute 10 CFR 21 discovery of a Technical Specification Safety Limit related issue, deviation or failure to comply, then the Responsible Department Manager documents the bases of the determination and proceeds to Section 5.3. and Assign a corrective action to the Responsible Department Manager to complete Attachment 9.3 as soon as practicable, and in all cases within 60 calendar days of determining that the deficiency/condition does constitute discovery of a deviation or failure to comply (i.e., the determination of answers to Attachment 9.2). The licensees failure to follow procedure EN-LI-1008-01 and complete an evaluation of the contractor identified Part 21 deviation, represented a violation of 10 CFR Appendix B, Criterion V Instructions, Procedures, and Drawings, which requires in part that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.

Screening: The inspectors determined the performance deficiency was minor. For this issue, the licensees contractor completed a Part 21 evaluation and concluded that although this issue met the definition of a Part 21 deviation, the missed UT indication in nozzle 25 did not pose a substantial safety hazard or a risk of violating a safety limit (as defined in 10 CFR Part 21) associated with the integrity of the reactor coolant pressure boundary and was therefore not a defect as defined in Part 21. Based on substantial margins that existed until reaching a critical (e.g. unstable) crack size for nozzle 25 and the absence of corrosion induced wastage of the RVCH, the inspectors agreed with the licensees contractor assessment that this issue did not pose a substantial safety hazard. With this result, the inspectors applied the IMC 0612, Appendix B Issue Screening process and answered no to the more than minor questions for this violation because no loss of safety function occurred. Additionally, the inspectors considered this to be this similar to minor Example F of Section 4 Insignificant Procedural Errors of IMC 0612, Appendix E Examples of Minor Issues.

Enforcement:

This failure to comply with 10 CFR Appendix B, Criterion V constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

Minor Violation 71153 Minor Violation: On November 10, 2018, with the plant in Mode 6, during bare metal visual inspections of the reactor vessel closure head, dried boric acid was identified in the area of reactor head nozzle 25, indicative of a through-wall flaw. On January 3, 2019, the licensee issued a licensee event report (LER) 2018-003-00 Indications Identified in Reactor Pressure Vessel Head Nozzle Penetrations and reported this in accordance with 10 CFR Part 50.73(a)(2)(ii)(A) as a condition of the nuclear power plant, including its principal safety barriers, being seriously degraded. However, the licensee did not perform an investigation to determine if the accumulation of a boric acid deposit at nozzle 25 was indicative of plant operation with through-wall pressure boundary leakage and as such was prohibited by Technical Specification (TS) LCO 3.4.13, which states that operational LEAKAGE shall be limited to: No pressure boundary LEAKAGE. The licensees failure to report plant operation prohibited by TS to the NRC in an LER represented a violation of 10 CFR Part 50.73(a)(2)(i)(B).

Screening: The inspectors determined the performance deficiency was minor. Consistent with the guidance in Inspection Manual Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, the inspectors determined the performance deficiency was not a finding of more than minor significance based on No answers to the more-than-minor screening questions. The inspectors also reviewed the examples of minor issues in IMC 0612, Appendix E, Examples of Minor Issues and found no examples related to this issue. Additionally, based on review of Section 2.2.2 Traditional Enforcement of the NRCs Enforcement Policy, this issue represents a minor violation because failure to make this report resulted in no appreciable potential safety consequence and was less significant than a SL IV violation.

Enforcement:

This failure to comply with Part 50.73(a)(2)(i)(B) constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

Unresolved Item (Closed)

Qualification Basis for Safety-Related Agastat Relays and Molded Case Circuit Breakers05000255/2013005-06 71152

Description:

On February 12, 2014, the NRC issued Inspection Report 05000255/2013005 documenting Unresolved Item (URI)05000255/2013005-06. This URI was associated with safety-related molded case circuit breakers (MCCBs) and Agastat relays installed in mild environments which appeared to not have preventive maintenance (PM) schedules for inspection or replacement to address their specified lifetime. Since then, the NRC undertook efforts, such as training, to assist inspectors in dispositioning issues related to how long safety-related components remain in service and to clarify the applicability of various regulations and industry standards. As part of this effort, the NRC determined current agency regulations require the establishment of quality assurance programs and supporting procedures that, among other things, set PM schedules for the inspection or replacement of parts having a specific lifetime.

During the NRC's previous inspection, the inspectors determined the licensee had developed PM schedules and associated procedures for the inspection of the MCCBs. However, the appropriateness of the schedule and procedures to detect degradation prior to the MCCB experiencing a loss of safety function was not readily evident. While the NRC undertook the training efforts previously described, the licensee replaced the MCCBs installed beyond their specified life and created recurring work tasks to replace MCCBs prior to the breakers exceeding their specified life as documented in CR-PLP-2015-1914 and CR-PLP-2013-4010.

Because these actions reasonably ensured the continued quality of the MCCBs during their specified lifetime, the inspectors determined further efforts to evaluate the appropriateness of the procedures in effect at the time the URI was issued were no longer needed to provide reasonable assurance of adequate protection of public health and safety.

Regarding the Agastat relays, the inspectors determined the licensee had developed PM schedules and associated procedures to manage the service life of safety-related Agastat relays prior to the issuance of this URI. Specifically, on January 1, 2009, the licensee initiated corrective action document CR-PLP-2009-00346 to address a deficiency regarding their PM strategy for safety-related Agastat relays. The associated corrective actions included the development of EC20559, Validate Selective Agastat Relays Setpoint Data, Revision 0, which validated and/or established inspection acceptance criteria intended to detect degradation prior to loss of safety function. These acceptance criteria were included in calibration sheets which are implemented during periodic PM activities.

Based on the above, no performance deficiency or violation of regulatory requirements was identified. This review did not represent an inspection sample.

Corrective Action Reference(s): CR-PLP-2015-1914 and CR-PLP-2013-4010

Unresolved Item (Closed)

Potential Failure to Identify/Correct Rejectable Flaws in Reactor Pressure Vessel Head Penetration 05000255/2018004-01 71111.08P

Description:

This was closed to a Green NCV.

Inadequate Ultrasonic Examination of Reactor Head Nozzles Results in Operation with Pressure Boundary Leakage Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events

Green NCV 05000255/2019002-01 Open/Closed

[H.2] - Field Presence 71111.08P The inspectors identified a Green finding and associated Non-Cited Violation (NCV) of Technical Specification (TS) 3.4.13.a, Reactor Coolant System Operational Leakage, for the licensees failure to place the plant in Mode 3 (Hot Standby) within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode 5 (Cold Shutdown) within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> with the plant in Mode 1 (Power Operation) during a portion of operating Cycle 26 with pressure boundary LEAKAGE present at reactor vessel closure head (RVCH) penetration nozzle 25. In particular, the licensees UT contractor mischaracterized flaw indications, and thus had not identified them as flaws before they resulted in operation with the pressure boundary LEAKAGE. The inspectors determined the condition was reasonably foreseeable and preventable by the licensee as there were several weaknesses in the licensees oversight of its contractor that mischaracterized the nozzle flaw indications.

Description:

On November 10, 2018, with the plant in Mode 6, during bare metal visual inspections of the RVCH, dried boric acid was identified in the area of nozzle 25, indicative of a primary coolant system (PCS) leakage from a through-wall flaw. The licensees contractor (Framatome) had recently completed UT examinations of nozzle 25 and the NRC inspectors inquired if the contractor had identified flaw indications or evidence of leakage during this UT examination. The inspectors questions prompted the licensees contractor to re-review nozzle 25 UT data and the contractor staff subsequently identified an inside diameter (ID)connected axial thru-wall flaw indication and UT indications of leakage within the annulus behind nozzle 25 (e.g. UT leak path). Subsequently, the contractor performed a re-review of all nozzle UT data and then applied an eddy current examination technique to the ID surface of nozzles 34, and 36 and identified additional ID connected flaws in nozzles 33 and 36. In licensee event report (LER) 2018-003-00, the licensee determined the cause of these flaws to be primary water stress corrosion cracking (PWSCC) based on the nozzle material (Inconel Alloy 600) which is known to be susceptible to PWSCC. Additionally, the licensee reported that the reactor head UT contractor performed an in-depth summary of the prior data reviews on reactor head nozzles 25, 33, and 36 and that the result of this review shows that the ID-initiated axial flaws were present and detectible with the demonstrated inspection method in 2007, 2009, 2010, and 2012. The licensees contractor staff had not observed ID initiated flaws since the 2001-2002 timeframe, and thus the UT examinations of the RVCH were focused on identification of outside diameter (OD) initiated flaws.

Each of the RVCH nozzle UT examinations dating back to 2007 were completed by the same contractor (Framatome) in accordance with procedure 54-ISI-604 Automated Ultrasonic Examination of Open Tube Reactor Pressure Vessel Closure Head Penetrations (Revisions 3 through 13) and this procedure was required to be qualified for detection of flaws in vessel head penetration nozzles in accordance with applicable NRC requirements (e.g. NRC Order EA 03-009 Establishing Interim Inspection Requirements for Reactor Pressure Vessel Heads at Pressurized Water Reactors, 10 CFR 50.55a Codes and Standards, Code Cases 729-1 and Code Case N-729-4). Procedure 54-ISI-604 included instructions for identification of ID connected flaws and the contractor staff that applied this procedure had demonstrated the capability to detect ID flaws with this procedure. Specifically, certification records (Performance Demonstration Qualification Records issued by the Electric Power Research Institute (EPRI)) existed for each of the contractor staff that performed inspections of nozzles 25, 33 and 36 confirming that the contractor staff member had demonstrated the ability to detect and size flaws that originated at both the ID and OD surface of mockup RVCH nozzles.

However, the procedure steps for classifying UT indications as ID flaws were not properly applied by the licensees contractor staff during each of the 7 times that the RVCH nozzles were examined from 2007 through 2018. As a result, the flaw indications present in nozzles 25, 33 and 36 were previously mischaracterized by the contractor staff and thus not identified as flaws.

Upon discovery of the through-wall leak on nozzle 25, the licensee determined that the leak was present for a maximum of the duration of operating cycle 26 and that refinement of that leakage duration was immaterial to cause investigation, corrective action determination, or repair plans. Therefore, the licensee did not conduct an evaluation to determine a more precise leakage duration. Based on the presence of a through-wall flaw in nozzle 25, in conjunction with a confirmed UT leak path signal, and dried boric acid deposit present at the outside vessel head surface at nozzle 25, the inspectors concluded leakage existed well in excess of 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> during operating cycle 26.

In response to the missed flaw indications, the licensee conducted a self-assessment of the programs for contractor oversight of the vessel head inspections. Specifically, in CR-HQN-2019-00577 Fleet NDE oversight of RVCH examinations the licensee identified causal factors and conclusions as they related to programs for oversight of the contractor head UT examinations. In this document, the licensee identified a number of program weaknesses which included: No governing standard existed for oversight of RVCH inspections; Fleet Inspection Services did not rigorously challenge the implementation of the contractor procedure requirements for two specific areas - pre-job briefings and UT data analyst independence, and no formal operating experience screening occurred for a similar 2013 missed flaw event that occurred at the Shearon Harris Plant. The licensee concluded that had these insights been realized prior to the RVCH examinations, Entergy would have been less vulnerable to missed indications. Therefore, the licensee missed opportunities to strengthen oversight of the Palisades UT examination process that could have precluded extended operation with a through-wall flaw at nozzle 25 as revealed during the 2018 Palisades outage (e.g. the leakage event at Palisades was reasonably foreseeable and preventable).

Corrective Actions: The licensees contractor staff completed training on the flaw characteristics observed in nozzles 25 and 33 and applied lessons learned from this training to the remainder of the reactor head nozzle population during the 2018 refueling outage to ensure all flawed nozzles were identified and the licensee repaired each of the flawed nozzles (25, 33 and 36) prior to returning the RVCH to service. The inspectors identified that the licensee had operated during cycle 26 with pressure boundary LEAKAGE which is prohibited by TS LCO 3.4.13 and the licensee entered this TS violation into the corrective action program for further corrective action.

Corrective Action References: CR-PLP-2019-02516

Performance Assessment:

Performance Deficiency: The licensees failure to change plant operating conditions from Mode 1 (Power Operation) to Mode 3 (Hot Standby) within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and Mode 5 (Cold Shutdown) within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />, with pressure boundary LEAKAGE at RVCH nozzle 25 during operating cycle 26 was contrary to TS LCO 3.4.13 and a performance deficiency. In particular, the licensees UT contractor mischaracterized flaw indications, and thus had not identified them as flaws before they resulted in operation with the pressure boundary LEAKAGE. The inspectors determined the condition was reasonably foreseeable and preventable by the licensee as there were several weaknesses in the licensees oversight of its contractor that mischaracterized the nozzle flaw indications.

Screening: The inspectors determined the performance deficiency was more than minor because if left uncorrected, it would have the potential to lead to a more significant safety concern. Specifically, continued operation with pressure boundary LEAKAGE at RVCH nozzle 25 if not corrected, would result in wastage of the RVCH which would increase the chance for a loss-of-coolant (LOCA) event and rod ejection.

Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors screened the safety significance as Green using IMC 0609, Appendix A, Exhibit 1, LOCA Initiators, because, after a reasonable assessment of degradation, it was determined that the violation did not result in exceeding the PCS leak rate for a small-break LOCA and did not affect any other systems used to mitigate a LOCA that could result in a total loss of function. Although, the licensee's UT examination was not successful in identifying the flaw in nozzle 25 before minor leakage occurred, the licensees bare metal visual exam was successful in identifying the leakage condition, and the licensee's timely corrective actions prevented this condition from becoming a more safety significant concern. Therefore, the inspectors determined that the issue is of very low safety significance (Green).

Cross-Cutting Aspect: H.2 - Field Presence: Leaders are commonly seen in the work areas of the plant observing, coaching, and reinforcing standards and expectations. Deviations from standards and expectations are corrected promptly. Senior managers ensure supervisory and management oversight of work activities, including contractors and supplemental personnel. In this case, the licensee failed to establish adequate oversight of the contractor during UT examinations of RVCH nozzles which resulted in extended operation with an undetected flaw in nozzle 25 that progressed through-wall and caused pressure boundary LEAKAGE [Item H.2].

Enforcement:

Violation: TS LCO 3.4.13 requires in part, PCS operational LEAKAGE shall be limited to: a.

No pressure boundary LEAKAGE; with the reactor in Modes 1, 2 3 and 4.

TS LCO 3.4.13.b Action statements for Condition Pressure boundary LEAKAGE exists include: B.1 - Be in MODE 3 completion time - 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and B.2 - Be in MODE 5 completion time - 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

Contrary to the above, since approximately May of 2017 thru October 13, 2018, with the plant in Mode 1 (Power Operation) and pressure boundary LEAKAGE present through a nonisolable fault in a PCS component (reactor vessel head penetration nozzle 25), the licensee failed to place the plant in Mode 3 (Hot Standby) within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode 5 (Cold Shutdown) within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

Enforcement Action: This violation is being treated as an non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

The disposition of this finding and associated violation closes URI: 05000255/2018004-01.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On April 11, 2019, the inspectors presented the Triennial Heat Sink to Mr. D. Lucy, Assistant General Manager of Plant Operations and other members of the licensee staff.
  • On May 29, 2019, the inspectors presented the Debrief for Unresolved Item 05000255/2013005-06 to Mr. O. Gustafson, Director of Regulatory and Performance Improvement and other members of the licensee staff.
  • On June 6, 2019, the inspectors presented the radiation protection baseline inspection results to Mr. D. Corbin, General Manager Plant Operations, and other members of the licensee staff.
  • On July 9, 2019, the inspectors presented the integrated inspection results to Mr. D. Corbin, Acting Site Vice President and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Corrective Action

Documents

CR-PLP-2019-

2146

Unsecured Compressed Cylinder Protective Cap Sitting on

Post Near Safeguards Transformer 1-1

05/28/2019

CR-PLP-2019-

2150

Nitrogen Bottle Found Unsecured Outside the 590' Elevation

North Entrance to the Turbine Building

05/29/2019

Miscellaneous

PLP-RPT-12-

00142

Palisades Nuclear Plant Flooding Walkdown Submittal

Report for Resolution of Fukushima Near-Term Task Force

Recommendation 2.3: Flooding

Procedures

Admin 4.00

Operations Organization, Responsibilities, and Conduct

Admin 4.02

Control of Equipment

AOP-38

Acts of Nature

SOP-30

Station Power

Work Orders

WO 52775537

Annual Inspection of Watertight Barriers

08/07/2018

71111.04

Corrective Action

Documents

CR-PLP-2019-

2404

150/151-115 (Z-Phase) Component Cooling Pump P-52C

OC Relay Flag Actuated

06/17/2019

CR-PLP-2019-

2477

Level 2 Oil Leak from VC-10 Compressor Shaft Seal

06/20/2019

CR-PLP-2019-

2528

Safeguards Transformer Found Power Available Light was

not Illuminated Gas-in-Oil Monitor

06/25/2019

Drawings

M-218, Sheet 6

Piping & Instrument Diagram, Heating, Ventilation and Air-

Conditioning Control Room

M-218, Sheet 6A

Piping & Instrument Diagram Heating, Ventilation and Air-

Conditioning Control Room

M-218, Sheet 7

Piping & Instrument Diagram, Heating, Ventilation and Air-

Conditioning Control room

Procedures

SOP-24

Ventilation and Air Conditioning System

SPS-E-28

Safeguards Transformer 1-1 (EX-07) Load Tap Changer

Voltage Settings

Work Orders

WO52825095

Safeguards Transfer EX-07 Load Tap Changer Set

05/24/2019

WO52825095

EX-07: Load Tap Changer Controller, Replace 1K Rheostat

04/19/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.05Q Fire Plans

Pre Fire Plan 4,

34, 35, & 36 /

Rooms 116A,

190, 191, & 192

1-C Switchgear Room and Manhole 1, 2, & 3 / Elevation 590

71111.07T

Calculations

EA-C-PAL-99-

209B-01

Generation of Flow Rate Acceptance Criteria for Technical

Specification Surveillance Test RO-216

2/06/2012

EA-EAR-2000-

0119-01

Instrument Uncertainty Calculation for TI-1319, Critical

Service Water Temperature Indication

08/21/2000

EA-EC28106-03

Diesel Generator Lube Oil Cooler Tube Plugging

2/27/2013

EA-GL-96-06-

SWS-02

Service Water GL 96-06 Waterhammer Assessment

08/12/2004

EA-GOTHIC-04-

Containment Response to a LOCA Using GOTHIC 7.2a

10/21/2010

EA-GOTHIC-04-

Containment Response to a MSLB Using GOTHIC 7.2a

10/21/2010

EAR-98-0512

Establish 85* as the Design Basis Service Water Inlet

Temperature Limit

07/24/2001

EC26869

E031A/B Lube Oil and E-22A/B Jacket Water Coolers Tube

Plugging Allowance

2/14/2011

EC62697

EDG Jacket Water Cooler Tube Plugging Revision

2/02/2016

Corrective Action

Documents

CR-PLP-2015-

05318

Pre-NRC UHS Assessment

10/26/2015

CR-PLP-2015-

4504

RO-216 Acceptance Criteria for EDG1-1 Not Met

09/30/2015

CR-PLP-2017-

226

RO-216, Service Water Flow Verification, Actual

Containment Air Cooler Service Water Flow Was

Outside of the Containment +/- 10 % Air Cooler Flow Band

05/05/2017

CR-PLP-2018-

00313

E-22B, 1-2 D/G Jacket Water Cooler 12 Partially Blocked

Tubes

01/16/2018

CR-PLP-2018-

00318

E-22B, D/G 1-2 Jacket Water Cooler, Eddy Current

Inspection Identified Tubes for Plugging

01/17/2018

CR-PLP-2018-

06058

VHX-3 Inspection Identified Tube Blockage

11/15/2018

Miscellaneous

RU14-021

Inspection of Raw Water Intake Pipe

10/30/2015

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

UCC Job # 02-07-

203.97

Spring 2018 Inspection and Cleaning

04/24/2018

UCC Job # 02-07-

203.99

Fall 2018 Inspection and Cleaning

09/30/2018

Procedures

AOP-21

EDG 1-2 Malfunctions

Revision 3

ARP-20B

Diesel Generator 1-2 Scheme EK-30

08/18/14

DWO-1

Operators Daily/Weekly Items MODEs 1, 2, 3, and 4

07/20/2017

EN-DC-316

Heat Exchanger Performance and Conditioning Monitoring

Revision 11

MO-29

Engineered Safety System Alignment

Revision 40

SEP-HX-PLP-001

Heat Exchanger Condition Assessment Program

Revision 3

SEP-SW-PLP-

2

Service Water and Fire Protection Inspection Program

Revision 6

SEP-UIP-005

Underground Component Inspection Plan

Revision 5

Work Orders

WO00429037

RO-144 - IST P-7A,B,C SWS PMP Comprehensive Test

05/08/2017

WO00429039

RO-216 Service Water Flow Verification

05/11/2017

WO00443731

VHX-2, Inspection for Tube Fouling

05/04/2017

WO00496138

E-11B; Replace Jacket Water Cooler HT Exchanger Tube

Bundle

07/17/2018

WO52537659

RO-216 Service Water Flow Verification

09/30/2015

WO52544850

VHX-1, Inspection for Tube Fouling and Eddy Current Test

10/16/2015

WO52560090

VHX-1, Containment Air Cooler Air Side Inspection

09/22/2015

WO52562743

VHX-2, Containment Air Cooler Air Side Inspection

09/22/2015

WO52641426

QO-6 1R25 Cold Shutdown Valve Test Procedure (18 month

Reg)

07/19/2018

WO52673149

VHX-3, Containment Air Cooler Inspection

04/25/2017

WO52673320

VHX-1, Containment Air Cooler Air Side Inspection

04/24/2017

WO52673321

VHX-2, Containment Air Cooler Air Side Inspection

05/10/2017

WO52741815

E-22B, Eddy Current Testing of EDG Jacket Water Cooler

05/03/2018

WO52759701

VHX-3, Inspection for Tube Fouling

11/16/2018

WO52776895

VHX-1, Containment Air Cooler Air Side Inspection

10/29/2018

WO52779143

RO-144 -IST P-7A,B,C SWS Pmp Comprehensive Test

11/12/2018

WO52780058

RO-216 Service Water Flow Verification

11/18/2018

WO52780063

VHX-2, Containment Air Cooler Air Side Inspection

11/13/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

WO52780492

QO-6 - Cold Shutdown Valve Test Procedure

2/20/2018

WO52809269

QO-14A - P-7A, IST Service Water Pump

06/01/2018

WO52824503

QO-14A - P-7A IST Service Water Pump

08/20/2018

WO52827609

QO-14C -P-7C, IST Service Water Pump

09/18/2018

WO52838248

QO-14A - P-7A IST Service Water Pump

11/27/2018

WO52843635

QO-14C -P-7C, IST Service Water Pump

2/29/2018

WO52848008

MO-29 Engineering Safety System Alignment

2/26/2019

WO52848499

MO-7A-2 Emergency Diesel Generator 1-2

2/19/2019

WO52849692

MO-29 Engineering Safety System Alignment

03/26/2019

71111.08P

Corrective Action

Documents

Resulting from

Inspection

CR-PLP-2019-

2516

The NRC is Proposing a Green Finding and Associated NCV

of TS 3.4.13.

06/25/2019

NDE Reports

1075

Performance Demonstration Program Qualification for

Jeffery Grigsby

08/20/2014

180-9247379-000

Palisades Unit 1, 1 R024 Reactor Head Inspection Report

180-9271125-000

Palisades Unit 1, 1RO25 Reactor Head Inspection Report

180-9291875-000

Palisades Unit 1, 1RO26 Reactor Head Inspection Report

180-9291875-000

Palisades Unit 1, 1RO26 Reactor Head Inspection Report

2/04/2018

384

Performance Demonstration Program Qualification for Scott

R. Breiholz

08/20/2014

407

Performance Demonstration Program Qualification for

Vladimir Zado

08/28/2014

498

Performance Demonstration Program Qualification for

Michael W. Key

08/25/2014

- 9062418 -

000

Palisades Unit 1, RO19 Reactor Head Inspection Report

- 9110490 -

000

Palisades Unit 1, RO20 Reactor Head Inspection Report

- 9181224 -

000

Palisades Unit 1, 1RO22 Reactor Head Inspection Report

- 9218473 -

000

Palisades Unit 1, RO23 Reactor Head Inspection Report

51-9147146-000

Palisades Unit 1, 1RO21 Reactor Head Inspection Report

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

671

Performance Demonstration Program Qualification for

Hrvoje Bezlaj

08/19/2014

939

Performance Demonstration Program for Rickie L. Rose

08/26/2014

Procedures

54-ISI-604-013

Automated Ultrasonic Examination of Open Tube RPV

Closure Head Penetrations

08/31/2006

71111.11Q

PLSEG-LOR-

19B-01

Licensed Operator Re-qualification Cycle 19B as Found

Scenario

71111.12

Corrective Action

Documents

CR-PLP-2017-

257

Maintenance Rule Evaluation

2/23/2017

CR-PLP-2017-

00634

VC-11 Control Room HVAC Refrigeration Condensing Unit

did not Automatically Start in Auto as Expected Following

the Swap

2/22/2017

CR-PLP-2017-

04335

P-55B Low Oil Pressure During CVCO-4

09/21/2017

CR-PLP-2017-

05085

P-55C Unusual Noises in P-55A Cube with P-55C Running

11/03/2017

CR-PLP-2017-

05188

VC-11 Failed to Start After Being Returned to Auto

11/09/2017

CR-PLP-2017-

299

VC-11 Control Room HVAC Refrigeration Condensing Unit

Failed to Start

11/17/2017

CR-PLP-2017-

05599

P-55C Input Shaft Oil Leaks

2/08/2017

CR-PLP-2017-

05668

P-55A Exhibited Loud Banging Noises

2/12/2017

CR-PLP-2018-

221

Returning the Charging Pumps to Active (a)(1) Status with

Corrective Actions

01/11/2018

CR-PLP-2018-

00932

While Swapping CRHVAC Trains for MO-33B, VC-11 did not

Pump Down as Expected

2/22/2018

CR-PLP-2018-

00939

Air Handling Unit V-96 Outside Air Damper was Slow to

Open

2/23/2018

CR-PLP-2018-

00940

CR HVAC Testing, FIS-1681, Air Handling Unit V-95

Discharge Flow Indicator was Reading 5000 CFM

2/23/2018

CR-PLP-2018-

01050

Visual Inspection of RT-85D-B Control Room Emergency

Ventilation Filtration Testing - B Train

2/28/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CR-PLP-2018-

03154

VC-11, Control Room HVAC Refrigeration Condensing Unit

not Running

07/03/2018

CR-PLP-2019-

00327

Multiple Equipment Failures Associated with the Control

Room Ventilation System Over the Past Several Years

01/23/2019

CR-PLP-2019-

00383

V-95 Control Room Ventilation Main Supply Fan Tripped

Unexpectedly

CR-PLP-2019-

00785

Control Room HVAC System (VAS-CRV) is Maintenance

Rule "Near (a)(1)" Due to Experiencing Two (2) Functional

Failures

2/22/2019

CR-PLP-2019-

2512

Tracking CR for Maintenance Rule Evaluations (Failure

Determinations) of Low Safety Significant Equipment

Performance Issues

06/25/2019

Engineering

Evaluations

EN-LI-118,

9.9

Equipment Failure Evaluation

01/25/2019

Miscellaneous

Q1-2019 System

Health Report

Chemical Volume Control - Charging/Letdown

06/28/2019

Q3-2018

Control Room HVAC System Health Report

03/26/2019

Q4-2018

Chemical Volume Control - Charging/Letdown System

Health Report

06/28/2019

Q4-2018

Control Room HVAC System Health Report

03/26/2019

Procedures

EN-DC-336

Control Room Ventilation System Reliability

71111.13

Drawings

E-5, Sheet 5B

Relay Diagram 480 Volt Motor Control Centers

Miscellaneous

Operators Risk Report

05/01/2019

Procedures

Admin 4.02

Control of Equipment

AOP-38

Acts of Nature

71111.15

Corrective Action

Documents

CR-PLP-2019-

01671

High Pressure Safety Injection (HPSI) Pumps Operability

Evaluation

04/24/2019

CR-PLP-2019-

01863

1-1 EDG Failed to Start

05/06/2019

CR-PLP-2019-

01871

G1-1/ESR1 Relay Coil was Found with a Cracked Housing

with a White Substance Emanating From It

05/07/2019

CR-PLP-2019-

2108

Preconditioning Evaluation for MO-7A-1 Emergency Diesel

Generator

05/23/2019

CR-PLP-2019-

The TS/PB-R, SIS Test Button CKT No 2, was Momentarily

05/23/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2114

Released during Step 5.4.13 of QO-1 Safety Injection

System Testing

CR-PLP-2019-

238

"Parallel" Light did not Light when G1-1/DSR Parallel/Unit

Selector was Placed in Parallel

06/04/2019

Drawings

E 17, Sheet 13

Diesel Generator Breakers

E-17, Sheet 12

Diesel Engine Control Trips and Alarms

VEN-M12, Sheet

Control Equipment Schematic, Excitation Relaying &

Metering

VEN-M12, Sheet

98(1)

Engine Control Diesel Generator 1-1

VEN-M12; Sheet

Wiring Diagram Engine Exciter Panel C22 DG 1-1

VEN-M12; Sheet

98(1)

Schematic Diagram Engine Control DG 1-1

Miscellaneous

DBD-5.01

Diesel Engine and Auxiliary Systems

Procedures

MO-7A-1

Emergency Diesel Generator 1-1

71111.18

Engineering

Changes

81531

EX-10 Oil Cooler; Feed Cooler Bank 5 Pump from

Temporary Power / and Connect Wavebook to Monitor

Current

2148

Supplemental Cooling to EX-10 Main Transformer

Miscellaneous

PLP-RPT-19-

00025

EX-10 Main Transformer - GSU Transformer Thermal

Evaluation

PLP-RPT-19-

00028

Zones of Influence for Temporary Cooling Equipment in the

Palisades Plant Yard Area

Procedures

SOP-8

Main Turbine and Generating Systems

110

Work Orders

WO 517052

Breaker 8-5 (EX-10), Oil Pump Tripped for Bank #5

01/25/2019

71111.19

Corrective Action

Documents

CR-PLP-2019-

2458

An N/O Set of Contacts on the Droop Relay G1-1/DR was

Hanging up and not fully Changing States

06/20/2019

CR-PLP-2019-

2474

Unloaded Field Voltage Lower than Normal During MO-7A-1

for EDG 1-1

06/20/2019

Miscellaneous

Work Instruction

WI-EPS-E-01

Battery Charger Maintenance

Work Instruction,

WI-EPS-E-04

Calibration Testing of Electrical Meters

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Procedures

SOP-22

Emergency Diesel Generators

Work Orders

WO 525968

G1-1/DR; Parallel Light did not Light

06/20/2019

WO 52769842

ML-3070, Post-Maintenance Test: Inspect/Repair Oiler, Adj

W/QO-5

05/09/2019

WO 52783497

Battery Charger Maintenance

05/13/2019

WO 52788631

VC-10, Condenser Overhaul Post-Maintenance

04/16/2019

WO 52788632

Check Calibration of EAI-48

5/13/2019

WO 52858408

MO-33B - Perform MO-33B for 'B' CRHVAC

04/19/2019

71111.22

Corrective Action

Documents

CR-PLP-2019-

00145

CRD-24 did not Move with the Group

01/10/2019

CR-PLP-2019-

01645

Control Rod #23 Temperature was Observed Rising

04/23/2019

CR-PLP-2019-

01788

Question was Raised as to Whether the 1 Year Flex Pump

Standby PMs Required a 2 Hour Run or a 30 Minute Run

05/01/2019

CR-PLP-2019-

2061

Hi NO Alarm on the Portable NO Detector During MO-7A-2

05/20/2019

Procedures

EN-OP-201-05

Palisades FLEX Program Document

QI-39

Auxiliary Feedwater Actuation System Logic Test

QO-20

Inservice Test Procedure - Low Pressure Safety Injection

Pumps

QO-34

Control Rod Exercising

RE-132

Diesel Generator 1-2 Load Reject

SOP-22

K-16 Security Diesel Generator Checklist

Work Orders

WO 52817904

FLEX Standby PM: P-1003 One Year Operational Test (FSB

A)

04/10/2019

WO 52859570

QO-34 - Control Rod Exercising

04/23/2019

WO 52873536

QO-20A P-67A Inservice Test Low Pressure Safety Injection

Pump

06/18/2019

WO 52881915

K-16, Security Diesel Generator Monthly Start Test

06/10/2019

71114.06

Corrective Action

Documents

CR-PLP-2018-

2083

Plant Public Address Announcements are not Being Heard

at Warehouse 2

05/22/2019

CR-PLP-2019-

2084

Central Alarm Station (CAS) Secondary Work Station Would

not Communicate with the CAS Printer

05/22/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CR-PLP-2019-

2110

General Performance of the Provided EP Radios was Poor

During Drill

05/23/2019

Miscellaneous

May 22, 2019, Emergency Planning Drill Scenario Narrative

71124.05

Calibration

Records

Calibration Record For GEM-5 Serial Number 1712-186

08/24/2018

Calibration Record For ARGOS Serial Number 1712-183

08/30/2018

M-54 Calibration Data Sheet For Serial Number 285662

03/31/2019

Calibration Record For AMP-200 Serial Number 7704.032

06/01/2018

Calibration Record For RAS-1 Serial Number 19529

05/02/2018

Calibration Record For iSolo Serial Number 1047346

06/10/2018

2018-B2.28-

CALDAT-06948

Calibration Record for RO-20 Serial Number 1492

10/10/2018

2018-B2.28-

CALDAT-07015

Calibration Record For LM-177 Serial Number 273222

10/11/2018

2019-B2.28-

CALDAT-02731

Calibration Record For AMS-4 Serial Number 121

03/27/2019

2019-B2.28-

CALDAT-02950

Calibration Record For Telepole Serial Number 6600-019

04/03/2019

Miscellaneous

Gamma Spectroscopy Detector's 2018 Annual

Efficiency/Lower Limit of Detection Verifications

01/03/2019

71124.06

DABD-03

Palisades - Stack Release Rate Calculations

06/24/2002

Procedures

RT-85C

Fuel Handling Area Ventilation System Filter Testing

03/01/2018

Self-Assessments LO-PLPLO-2018-

00014

Radiation Monitor Functionality Assessment

Work Orders

2641428

Hi Range Noble Gas Effluent Monitor RIA-2327 Calibration

04/03/2017

71151

Miscellaneous

NRC Performance Indicator Data Sheet, Initiating Events -

Unplanned Power Changes per 7,000 Critical Hours (IE03);

Second Quarter 2018 through Second Quarter 2019

04/01/2018

to

06/30/2019

NRC Indicator Safety System Functional Failures (MS05)

Technique/Data Sheet; 2nd Quarter 2018 to 1st Quarter

2019

04/01/2019

to

03/31/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152

Corrective Action

Documents

CR-PLP-2009-

00346

Agastat Time Delay Relays Not Included in Site Calibration

Sheet Database

01/28/2009

CR-PLP-2018-

05857

Bare Metal Visual Examination of the Reactor Pressure

Vessel Head per Work Order 52779311 Identified

Recordable Boron Indications at Head Penetration Number

25. Samples of the Leakage Confirmed a High Boron

Concentration.

2/17/2018

CR-PLP-2019-

00063

As Found Condition Verified that CRDM Housing #37 & #28

Component Cooling Water Cooling Lines are Installed

Incorrectly.

01/04/2019

CR-PLP-2019-

00117

Plant Trip due to RPS BD Matrix Loss of Power

2/26/2019

CR-PLP-2019-

01676

The Process to Review changes in Plant Design,

Procedures/Processes and New Equipment has not been

Consistently Implemented

04/04/2019

CR-PLP-2019-

01678

Objectives from Department Rollups are not Creating Clear

Specific Gap Identification for Focused Coaching by

Supervisors

04/18/2019

CR-PLP-2019-

01832

Identified Trend of Failure to Coach When an Issue was

Identified by Non-consequential Procedure Compliance

Issues

05/03/2019

CR-PLP-2019-

241

Station Identified Leadership did not Act Promptly to More

Broadly Address Subtle Signs of Performance Decline

06/04/2019

CR-PLP-2019-

2175

During Fire Drill Operator Inadvertently Made Contact with

and Opened a Breaker

05/29/2019

CR-PLP-32019-

2520

Control Rod Drive Seal Leakage Measurement

06/25/2019

Corrective Action

Documents

Resulting from

Inspection

CR-PLP-2013-

04010

2013 NRC Aging Management Inspection - Three MCCBs

Are Exceeding Their Service Life

09/11/2013

CR-PLP-2013-

04344

Agastat Timing Relay Service Life Not Defined

10/03/2013

CR-PLP-2015-

01914

Resolution of Service Life TIA

05/08/2015

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Engineering

Changes

EC20559

Validate Selective Agastat Relays Setpoint Data

Miscellaneous

Performance Improvement Integrated Matrix (PIM) May

2019

DPRM/APRM

Report

Palisades Performance Improvement May 2019

Human

Performance

Evaluation for

CR-PLP-2019-

01120

Received Alarm EK-0524, Load Shedding/Safeguards Bus

Control CKT Undervoltage, Unexpectedly

03/18/2019

Procedures

1707-01

Framatome Procedure Implementation of 10 CFR 21

2/06/2019

EN-LI-108-01

CFR 21 Evaluations And Reporting

Revision 10

EN-LI-118

Performance Analysis Template

Self-Assessments EN-LI-121,

9.1

Palisades Performance Improvement

May 2019

EN-LI-121,

9.3

Aggregate Performance Issue Worksheet for Failure to

Provide Reinforcement of Some Expectations from

Supervisors

71153

Corrective Action

Documents

CR-HQN-2019-

00577

Fleet NDE Oversight of RXVCH Examinations

04/24/2019

CR-PLP-2018-

05857

Bare Metal Visual Examination of the Reactor Pressure

Vessel Head per Work Order 52779311 Identified

Recordable Boron Indications at Head Penetration

Number 25.

11/10/2018

CR-PLP-2018-

05895

Framatome Indication Notification Report RVCH-ISI-INR-

1R026-2018-002 Provides Notification of a Change in

Material Condition of Reactor Head Penetration Number 33.

11/21/2018

CR-PLP-2018-

225

Framatome Indication Notification Report RVCH-ISI-INR-

1R026-2018-003 Rev O Provides Notification of a Change in

Material Condition of Reactor Head Penetration Number 36.

11/21/2018

Corrective Action

Documents

Resulting from

CR-PLP-2019-

2460

The LER Should have also Included Reporting Criteria for 10 CFR 73(a)(2)(B) for Operation in a Condition that was

Prohibited by Tech Specs.

06/20/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Inspection

CR-PLP-2019-

2468

The inspector Identified that a Review Under 10 CFR 21,

Required by EN-LI-108-01, 10 CFR 21 Evaluations and

Reporting, was not Properly Conducted by the Site.

06/20/2019

Miscellaneous

05000255/2018-

003-00

Licensee Event Report-Indications Identified in Reactor

Pressure Vessel Head Nozzle Penetrations

01/30/2019