IR 05000456/2021003: Difference between revisions

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=Text=
=Text=
{{#Wiki_filter:October 26, 2021
{{#Wiki_filter:
 
==SUBJECT:==
BRAIDWOOD STATION - INTEGRATED INSPECTION REPORT 05000456/2021003 AND 05000457/2021003
 
==Dear Mr. Rhoades:==
On September 30, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Braidwood Station. On October 13, 2021, the NRC inspectors discussed the results of this inspection with Mr. J. Keenan, the Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
 
No findings or violations of more than minor significance were identified during this inspection.
 
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
 
Sincerely, Signed by Peterson, Hironori on 10/26/21 Hironori Peterson, Chief Branch 3 Division of Reactor Projects Docket Nos. 05000456 and 05000457 License Nos. NPF-72 and NPF-77
 
===Enclosure:===
As stated
 
==Inspection Report==
Docket Numbers: 05000456 and 05000457 License Numbers: NPF-72 and NPF-77 Report Numbers: 05000456/2021003 and 05000457/2021003 Enterprise Identifier: I-2021-003-0059 Licensee: Exelon Generation Company, LLC Facility: Braidwood Station Location: Braceville, IL Inspection Dates: July 01, 2021 to September 30, 2021 Inspectors: B. Bartlett, Senior Operations Engineer G. Edwards, Health Physicist D. Kimble, Senior Resident Inspector J. Nance, Operations Engineer N. Shah, Project Engineer P. Smagacz, Resident Inspector Approved By: Hironori Peterson, Chief Branch 3 Division of Reactor Projects Enclosure
 
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Braidwood Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
 
===List of Findings and Violations===
 
No findings or violations of more than minor significance were identified.
 
===Additional Tracking Items===
None.
 
=PLANT STATUS=
 
Unit 1 began the inspection period operating at full power. With the exception of minor reductions in power to support scheduled testing activities and load changes requested by the transmission system dispatcher, the unit remained operating at or near full power for the entire inspection period.
 
Unit 2 began the inspection period operating at full power. On September 16, 2021, the unit reached the end of the fuel cycle and power coast down operations commenced in preparation for a planned refuel outage. The unit continued to reduce power in accordance with the licensees approved reactivity management plan, and was operating at approximately 91 percent power at the end of the inspection period.
 
==INSPECTION SCOPES==
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
 
Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident and regional inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week, increasing the amount of time on-site as local COVID-19 conditions permitted.
 
As part of their on-site activities, resident inspectors conducted plant status activities as described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution, observed risk significant activities; and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or a portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.
 
==REACTOR SAFETY==
 
==71111.04 - Equipment Alignment==
 
===Partial Walkdown Sample (IP Section 03.01) (4 Samples)===
The inspectors evaluated system configurations during partial physical alignment verifications of the following systems/trains:
: (1) 1A Residual Heat Removal (RH) Train during 1B RH Train maintenance during the week ending July 24, 2021.
: (2) 1B Safety Injection (SI) Train during 1A SI Train maintenance during the week ending August 28, 2021.
: (3) 2A Station Air Compressor during replacement of the Unit 0 Station Air Compressor replacement during the week ending September 4, 2021.
: (4) 2A Auxiliary Feedwater (AF) Train during 2B AF Train maintenance during the week ending September 11, 2021.
 
==71111.05 - Fire Protection==
 
===Fire Area Walkdown and Inspection Sample (IP Section 03.01) (3 Samples)===
The inspectors evaluated the implementation of the fire protection program by conducting physical inspections and reviews to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
: (1) Units 1 and 2 Auxiliary Building, 346' Elevation, General Area, during the week ending August 7, 2021.
: (2) Units 1 and 2 Auxiliary Building, 330' Elevation, 1A and 2A Essential Service Water (SX) Pump Room, during the week ending August 7, 2021.
: (3) Units 1 and 2 Auxiliary Building, 330' Elevation, 1B and 2B SX Pump Room, during the week ending August 7, 2021.
 
==71111.06 - Flood Protection Measures==
 
===Inspection Activities - Internal Flooding (IP Section 03.01) (2 Samples)===
The inspectors evaluated internal flooding mitigation protection features in the following plant areas:
: (1) Unit 1 Auxiliary Building, 330', 346', and 364' Elevations, during the week ending August 7, 2021.
: (2) Unit 2 Auxiliary Building, 330', 346', and 364' Elevations, during the week ending August 7, 2021.
 
==71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance==
 
===Requalification Examination Results (IP Section 03.03) (1 Sample)===
: (1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification annual operating exam and biennial written examination administered from August 9, 2021 through September 17, 2021.
 
==71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance==
 
===Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)===
: (1) Biennial Requalification Written Examinations The inspectors evaluated the quality of the licensed operator biennial requalification written examination administered between August 9, 2021 and September 17, 2021.
 
Annual Requalification Operating Tests The inspectors evaluated the adequacy of the facility licensees annual requalification operating test.
 
Administration of an Annual Requalification Operating Test The inspectors evaluated the effectiveness of the facility licensee in administering requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility licensee is effectively evaluating their licensed operators for mastery of training objectives.
 
Requalification Examination Security The inspectors evaluated the ability of the facility licensee to safeguard examination material, such that the examination is not compromised.
 
Remedial Training and Re-examinations The inspectors evaluated the effectiveness of remedial training conducted by the licensee, and reviewed the adequacy of re-examinations for licensed operators who did not pass a required requalification examination.
 
Operator License Conditions The inspectors evaluated the licensees program for ensuring that licensed operators meet the conditions of their licenses.
 
Control Room Simulator The inspectors evaluated the adequacy of the facility licensees control room simulator in modeling the actual plant, and for meeting the requirements contained in 10 CFR 55.46.
 
Problem Identification and Resolution The inspectors evaluated the licensees ability to identify and resolve problems associated with licensed operator performance.
 
==71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance==
 
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)
(1 Sample)
The inspectors observed and evaluated the following licensed operator activities in the control room:
: (1) Various activities involving on-watch operations crews. These activities included, but were not limited to:
End-of-cycle reactivity maneuvers leading into Unit 2 coast down operations for the A2R22 refuel outage during the week ending September 18, 2021.
 
4,160 Vac electric plant maneuvers in support of emergency diesel generator testing during the week ending September 18, 2021.
 
===Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)===
The inspectors observed and evaluated the following licensed operator training activity:
: (1) A complex casualty graded scenario involving a crew of licensed operators was observed in facility's simulator on September 7, 2021.
 
==71111.12 - Maintenance Effectiveness==
 
===Maintenance Effectiveness (IP Section 03.01) (3 Samples)===
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:
: (1) Maintenance effectiveness and performance history review of the Direct Current (DC)
Batteries and Distribution System during the weeks ending August 21 through August 28, 2021.
: (2) Maintenance effectiveness and performance history review of nuclear instrumentation during the week ending August 28, 2021.
: (3) Maintenance effectiveness and performance history review of Overpower Delta Temperature (OPDT) components during the weeks ending September 4 through September 30, 2021.
 
==71111.13 - Maintenance Risk Assessments and Emergent Work Control==
 
===Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)===
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
: (1) Evaluation of the activities and risk associated with emergent troubleshooting and repairs to the 1A Emergency Diesel Generator (EDG), as documented in Issue Report (IR) 4437474 during the week ending July 31, 2021.
: (2) Evaluation of the work activities and risk associated with planned maintenance on the 1B SI Recirculation Isolation Valve, 1SI8920, in conjunction with emergent work on 1HD026A, the 12A Feedwater Heater Normal Level Control Valve, during the week ending September 18, 2021.
: (3) Evaluation of the work activities and risk associated with several concurrent planned work activities, including acceptance testing for the 1A Station Air Compressor, 1A EDG monthly operability testing, 1A RH Train operability testing, and 2A Containment Spray Train operability testing during the week ending September 30, 2021.
 
==71111.15 - Operability Determinations and Functionality Assessments==
 
Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples 1 Partial)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
: (1) Evaluation of the availability of the 2B Start Up Feedwater Pump due to low oil pressure, as documented in IR 4428965 during the weeks ending July 10 through August 14, 2021.
: (2) Evaluation of the operability of the 2B RH system due to boric acid leakage on the 2FIS-0611 Recirculation Valve Controller, as documented in IR 4436953 during the weeks ending July 31 through August 14, 2021.
: (3) Evaluation of the operability of the 1A EDG after a failure to start during a monthly surveillance, as documented in IR 4437474 during the weeks ending August 7 through September 18, 2021.
: (4) Evaluation of the operability of the 2A EDG following identification of a sheared bolt associated with the 4L cylinder air manifold, as documented in IR 4443522 during the weeks ending September 4 through September 25, 2021.
 
  (5)    (Partial)
Continued evaluation of the operability of the source range nuclear instruments with their high flux trips bypassed during reactor startup, as documented in IR 4418688 during the weeks ending July 1 through September 25, 2021.
: (6) Review of Unit 1 Core Exit Thermocouple (CETC) operability following several issues, as documented in IRs 4419609, 4420610, and 4423740 during the weeks ending September 25 through September 30, 2021.
: (7) Review of the 0B Auxiliary Building Nonaccessible Area (NAC) Exhaust Filter Plenum Ventilation Train operability following identification of testing equipment being left installed since May 2021, as documented in IR 4447805 during the weeks ending July 10 through September 30, 2021.
 
==71111.19 - Post-Maintenance Testing==
 
===Post-Maintenance Test Sample (IP Section 03.01) (2 Samples)===
The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:
: (1) Testing of the 1SI8920 Mini-Flow Recirculation Valve after maintenance, as set forth in Work Order (WO) 4904903 during the week ending September 18, 2021.
: (2) Comprehensive functional and operational acceptance testing of the 1A Station Air Compressor following replacement and installation, as documented in station procedure SPP-21-002 during the weeks ending September 25 through September 30, 2021.
==71111.22 - Surveillance Testing==
 
The inspectors evaluated the following surveillance tests:
 
===Surveillance Tests (other) (IP Section 03.01)===
{{IP sample|IP=IP 71111.22|count=2}}
: (1) 2BwOSR 3.8.1.2-1, Technical Specification operability surveillance for the 2A EDG, during the weeks ending August 7 through August 14, 2021.
: (2) BwIP 2500-070, calibration of the 2B Steam Generator main steam atmospheric relief valve control loop, during the week ending August 14, 2021.
 
===Inservice Testing (IP Section 03.01) (1 Sample)===
: (1) 2BwOSR 5.5.8.RH, inservice testing for the 2B RH Train, during the weeks ending          August 14 through August 21, 2021.
 
==71114.04 - Emergency Action Level and Emergency Plan Changes==
 
===Inspection Review (IP Section 02.01-02.03) (1 Sample)===
: (1) The inspectors evaluated the following submitted Emergency Action Level and Emergency Plan changes.
 
Eval No. 20-71 Emergency Action Levels for Braidwood Station, EP-AA-1001, Addendum 3 This evaluation does not constitute NRC approval.
 
==71114.06 - Drill Evaluation==
 
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01)
(1 Sample)
The inspectors evaluated the following select emergency preparedness (EP) drill:
: (1) Observation and evaluation of the station's Emergency Response Organization during the performance of a full-scale site-wide EP drill on August 2, 2021.
 
===Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)===
The inspectors evaluated the following EP drill/training evolution:
: (1) Review of the implementation of the site's emergency plan by a crew of licensed operators during an evaluated emergency scenario in the facility's simulator on September 7,
 
==RADIATION SAFETY==
 
==71124.05 - Radiation Monitoring Instrumentation==
 
===Calibration and Testing Program (IP Section 03.02) (6 Samples)===
The inspectors evaluated the calibration and testing of the following radiation detection instruments:
: (1) Thermo Fisher RO20 SN#0013941
: (2) Eberline Model 3 SN#0017854
: (3) Ludlum 177 SN#0025821
: (4) Thermo Fisher RO20 SN#0018388
: (5) Eberline Model 3 SN#0014351
: (6) Ludlum 3030P SN#0015022
 
==71124.07 - Radiological Environmental Monitoring Program==
 
===Environmental Monitoring Equipment and Sampling (IP Section 03.01) (1 Sample)===
: (1) The inspectors evaluated environmental monitoring equipment and observed            collection of environmental samples.
 
===Radiological Environmental Monitoring Program (IP Section 03.02) (1 Sample)===
: (1) The inspectors evaluated the implementation of the licensees radiological            environmental monitoring program.
 
===GPI Implementation (IP Section 03.03) (1 Sample)===
: (1) The inspectors evaluated the licensees implementation of the Groundwater            Protection Initiative program to identify incomplete or discontinued program elements.
==71124.08 - Radioactive Solid Waste Processing & Radioactive Material Handling, Storage,==
 
& Transportation
 
===Radioactive Material Storage (IP Section 03.01)===
{{IP sample|IP=IP 71124.08|count=1}}
: (1) Inspectors evaluated the licensees performance in controlling, labeling, and securing radioactive materials. This included the radioactive waste storage portion of the facility.
 
===Radioactive Waste System Walkdown (IP Section 03.02) (1 Sample)===
: (1) Inspectors walked down accessible portions of the solid radioactive waste systems          and evaluated system configuration and functionality.
 
===Waste Characterization and Classification (IP Section 03.03) (2 Samples)===
: (1) The inspectors evaluated the licensees characterization and classification of radioactive waste. This included the resin waste streams at the facility.
: (2) The inspectors evaluated the licensees characterization and classification of radioactive waste. This included the dry activated waste (DAW) stream at the facility.
 
===Shipment Preparation (IP Section 03.04) (1 Sample)===
: (1) The inspectors observed that a shipment containing radioactive material is prepared according to requirements. The shipment identification number was RWS21-015 for seven B-25 Boxes of Condensate Polish Resin shipped on August 17, 2021.
 
===Shipping Records (IP Section 03.05) (3 Samples)===
The inspectors evaluated the following non-excepted radioactive material shipments through a record review:
: (1) Shipment RWS 21-001 UN3321 LSA-II; Resin Liner P0695283-14 in Cask 14-215.
: (2) Shipment RWS 20-015 UN3321 LSA-II; 14 DAW Legacy Waste in Cask 14-210.
: (3) Shipment RWS 20-018 UN2916 Type (B) Package; Resin Liner PO 692200-4.
 
==OTHER ACTIVITIES - BASELINE==
 
===71151 - Performance Indicator Verification The inspectors reviewed and verified selected portions of the licensee's performance indicator submittals listed below:
MS08: Heat Removal Systems (IP Section 02.07) ===
{{IP sample|IP=IP 71151|count=2}}
: (1) Unit 1 (July 1, 2020 through June 30, 2021)
: (2) Unit 2 (July 1, 2020 through June 30, 2021)
 
===MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)===
: (1) Unit 1 (July 1, 2020 through June 30, 2021)
: (2) Unit 2 (July 1, 2020 through June 30, 2021)
 
===MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)===
: (1) Unit 1 (July 1, 2020 through June 30, 2021)
: (2) Unit 2 (July 1, 2020 through June 30, 2021)
 
==71152 - Problem Identification and Resolution==
 
===Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)===
The inspectors conducted in-depth reviews of the licensees implementation of the CAP related to the following issues:
: (1) Review and assessment of the corrective actions for the spent fuel dry cask storage (DCS) system forced helium drying errors, as documented in IR 4364058 during the weeks ending August 7 through August 14, 2021.
: (2) Review and assessment of the corrective actions for the 1/2CC202B wrong unit valve operation, as documented in IR 4434922 during the weeks ending July 17 through September 30,
 
==INSPECTION RESULTS==
Observation: Forced Helium Drying Skid Issue During Dry Cask Processing                71152 The inspectors performed a detailed review of IR 4364058, Forced Helium Drying Skid Issue. Specifically, on August 19, 2020, a reactor services crew connected hoses incorrectly in preparation for Multi-Purpose Cannister (MPC) blowdown, resulting in an increased risk of the cask being over-pressurized due to bulk water boiling inside the cask. The inspectors chose this issue for an in-depth review of the licensee's actions within their corrective action program (CAP) due to the potential of cask failure and damage to the integrity of the fuel stored within the cask. Consequently, for this detailed Problem Identification and Resolution inspection sample, the inspectors focused on assessment of the licensee's corrective actions taken to address this condition.
 
The licensees evaluation concluded that the direct cause was the failure by the fuel handlers to verify that the correct hoses were properly attached to the MPC prior to starting work.
 
Contributing to this were inappropriate actions taken by supervision overseeing the work activities, in part, due to a culture of not reinforcing expectations for using human performance tools during previous work activities and workers not effectively challenging supervision when faced with potential issues.
 
Corrective actions included, but were not limited to, revising procedures to use color coded hoses to ensure correct connections and requiring that supervisors sign off on specific, key steps to ensure proper system setup. Additionally, coaching/training was provided to ensure fuel handling supervision understood the expectations for performing work observations and in how to identify and correct key behaviors. Further, fuel handling management verified the efficacy of these actions by holding monthly meetings to evaluate the observations performed and proffer feedback on their effectiveness.
 
The inspectors review did not identify any issues of note with the corrective actions taken; however, their effectiveness could not be confirmed as the licensee had not performed any cask handling activities since implementation.
 
No findings or violations of NRC requirements were identified by the inspectors in the course of this review.
 
Observation: 1/2CC202B Wrong Unit Error                                                71152 The inspectors performed a detailed review of IR 4434922, Level 4 Configuration Control -
Received Unexpected Alarm 1-2-E3. The issue involved the mistaken operation of 1CC202B, Motor-Operated Valve (MOV) 1B SX to CC Makeup Downstream Isolation, during what was planned to have been a post-maintenance stroke test of 2CC202B, MOV 2B SX to CC Makeup Downstream Isolation, on July 14, 2021. The inspectors determined that the mistaken operation of 1CC202B instead of the planned and briefed 2CC202B had constituted a violation of the requirements of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings. However, because the SX to Component Cooling (CC)emergency makeup line on each unit is protected from the effects of inadvertent valve operation by the use of two MOVs in series, the mistaken operation of the 1CC202B valve instead of the intended 2CC202B valve did not result in any adverse consequences.
 
Subsequently, the inspectors concluded that the violation had not adversely impacted the Reactor Safety Mitigating Systems Cornerstone objective and, therefore, constituted a violation of minor significance that was not subject to formal actions per Section 2.3.1 of the NRC Enforcement Policy.
 
The inspectors chose this issue for an in-depth review of the licensees actions within their CAP because of the inherent risk associated with wrong unit/wrong component operational errors. Consequently, for this detailed Problem Identification and Resolution inspection sample, the inspectors focused on assessment of the licensees corrective actions taken both for this specific error, as well as those targeted at the more generic issue of preventing wrong unit/wrong component operational errors.
 
The inspectors did not identify any issues with the licensees CAP actions taken. Actions targeting the more generic issue of wrong unit/wrong component operational errors were focused on reinforcing existing human performance tool use and appreciation by the workforce. Actions targeting this specific event included painting the control panels for the MOV hand switches involved in this event with the appropriate unit-specific color scheme - yellow for Unit 1 and green for Unit 2. At the time of the event, all of the control panels involved, all of which are located in the same physical area of the station, were painted with a non-distinct color.
 
No findings or violations of NRC requirements of more than minor safety significance were identified by the inspectors in the course of this review.
 
==EXIT MEETINGS AND DEBRIEFS==
The inspectors verified no proprietary information was retained or documented in this report.
 
On October 13, 2021, the inspectors presented the integrated inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.
 
On July 15, 2021, the inspectors presented the radiation protection inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.
 
On August 20, 2021, the inspectors presented the radiation protection inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.
 
On August 20, 2021, the inspectors presented the biennial requalification inspection results inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.
 
On October 1, 2021, the inspectors presented the EPlan and EAL Change Inspection Exit inspection results to Mr. D. Moore, Senior Manager, Emergency Preparedness, and other members of the licensee staff.
 
=DOCUMENTS REVIEWED=
 
Inspection Type              Designation      Description or Title                                        Revision or
Procedure                                                                                                  Date
71111.04  Corrective Action 4429000          SA SAC (2SA02C) Oil Temperature High                        06/12/2021
Documents        4436087          1RH8729A Lock Issues                                        07/20/2021
4436735          2SA02C Oil Temperature High                                  07/23/2021
4437788          2SA02C Margin Improvement Initiative                        07/29/2021
4443172          2SA01C FNL I/S Temperature is High                          08/28/2021
BwOP RH-M1        Operating Mechanical Lineup Unit 1 1A RH Train              14
Procedures        BwOP AF-E2        Electrical Lineup  Unit 2 Operating                        11
BwOP AF-M2        Operating Mechanical Lineup, Auxiliary Feedwater, Unit 2    18
BwOP RH-E1        Electrical Lineup  Unit 1 Operating                        10
BwOP SA-E2        Electrical Lineup  Unit 2 Station Air System Operating      5
BwOP SA-M2        Operating Mechanical Lineup Unit 2                          15
BwOP SI-E1        Electrical Lineup  Unit 1 Operating                        12
BwOP SI-M1        Operating Mechanical Lineup Unit 1                          27
71111.05  Fire Plans        Pre-Fire Plan No. Fire Zone 11.2-0; Auxiliary Building 346' Elevation,        3
101              Auxiliary Building General Area  South
Pre-Fire Plan No. Fire Zone 11.1A-0; Auxiliary Building 330' Elevation, Unit 1 2
Auxiliary Building Basement (1A/2A SX)
Pre-Fire Plan No. Fire Zone 11.1B-0; Auxiliary Building 330' Elevation, Unit 2 3
Auxiliary Building Basement (1B/2B SX)
Pre-Fire Plan No. Fire Zone 11.2-0; Auxiliary Building 346' Elevation,        3
Auxiliary Building General Area  Center
Pre-Fire Plan No. Fire Zone 11.2-0; Auxiliary Building 346' Elevation,        3
Auxiliary Building General Area  North
Procedures        BwAP 1110-1      Fire Protection Program System Requirements                  44
BwAP 1110-3      Plant Barrier Impairment Program                            39
BwOP PBI-1        Plant Barrier Impairment Program Pre-Evaluated Barrier      4
Matrix
CC-AA-201        Plant Barrier Control Program                                13
ER-AA-600-1069    High-Risk Fire Area Identification                          4
ER-BR-600-1069    Site List of High-Risk Fire Areas  Braidwood Unit 1 and    0
Unit 2
Inspection Type              Designation    Description or Title                                      Revision or
Procedure                                                                                            Date
OP-AA-201-008  Pre-Fire Plan Manual                                      4
OP-AA-201-009  Control of Transient Combustible Material                26
OP-AA-201-1001 Operations On-Line Fire Risk Management                  4
71111.06  Calculations      3C8-0685-002  Auxiliary Building Flood Level Calculation                16
3C8-0787-001  Confirmation of Safe Shutdown Capability After Auxiliary  4
Building Flooding
3C8-1281-001  Auxiliary Building Flood Level Calculations              4
Corrective Action 4355236        The Plug for the 0TR19P (Lime Sludge West Lagoon Sump    08/07/2020
Documents                        Pump) is Damaged and Needs to be Replaced
4366140        Unexpected Alarm 1-1-A2 Containment Drain Leak            08/29/2020
Detection Flow High
4391353        0TR19P WWT West Lime Sludge Lagoon #2 Sump Pump is        12/20/2020
Degraded
4405498        SD-191 Discrepancy During Watertight Door Surveillance    03/01/2021
4418893        WO 01785089-09 Stud Missing for Re-Installation of Flood  04/25/2021
Seal
22795        Procedural Guidance for Setting Cable Vault Sump Pumps    05/11/2021
27580        IAM for Sump Pump 0CP05P WO 5157026-01                    06/04/2021
28760        Received the Unit 1 SX Sump Level High High Alarm        06/11/2021
4438648        Door Operator Loose on Unit 2 SX Pump Room                08/03/2021
Miscellaneous    BB-PRA-012    Byron and Braidwood Probabilistic Risk Assessment,        9
Internal Flood Evaluation Summary Notebook
NEI 12-07      Guidelines for Performing Verification Walkdowns of Plant 0
Flood Protection Features
Procedures        0BwOA PRI-8    Auxiliary Building Flooding Unit 0                        9
ER-AA-450      Structures Monitoring                                    10
Work Orders      1860257        1DSFO06/08 Outage Flood Seals Surveillance                03/03/2017
1915060        2DSFSO06/08 Outage Flood Seals Surveillance              10/18/2017
4838070        Remove/Replace Flood Seal Covers                          03/25/2020
1DSFSO07 & 09  Auxiliary Feedwater Tunnel  Outage
5079981        Watertight Door Inspection                                03/18/2021
71111.11B  Corrective Action 4340246        4.0 Critique for Recent and Ramps                        05/012020
Documents        4398670        4.0 Critique U0 CC Heat Exchanger Side Drain Down        01/28/2021
Inspection Type              Designation    Description or Title                                      Revision or
Procedure                                                                                            Date
4418688        Level 3 Configuration Control SRNI's Required Function    04/24/2021
Bypassed
4430586        4.0 Critique U1 Reactor Trip Due to Generator Load Reject 06/21/2021
Corrective Action 4441641        NRC Identified Unattended Exam Material                  08/19/2021
Documents
Resulting from
Inspection
Fire Plans        Simulator Post 1A MFP Start (PMT)                                        03/05/2020
Event Testing
Miscellaneous    Simulator Post 1A MFP Start                                              11/06/2019
Event Testing
Simulator Post 2CC130 Issues / Drop 7 failure                            07/23/2021
Event Testing
Simulator Post 2CV131 - Securing Letdown Evolution                      07/14/2021
Event Testing
Simulator Post Unit 2A MFP Start 12/7/2020                              02/10/2021
Event Testing
TQ-AA-306      ATT 10 PWR Moderator Temperature Coefficient of          04/29/2021
Reactivity, Cycle 23 Compare to Plant Startup Data
TQ-AA-306      ATT 10 PWR Moderator Temperature Coefficient of          04/27/2021
Reactivity Cycle 23 New Core Test
TQ-AA-306      ATT 11 PWR Rod Worth Coefficient of Reactivity Cycle 23  04/27/2021
New Core Test
TQ-AA-306      ATT 12 PWR Boron Coefficient of Reactivity Cycle 23,      04/27/2021
New Core Test
TQ-AA-306      ATT 13 PWR Xenon Worths Cycle 23, New Core Test          04/27/2021
TQ-AA-306      ATT 16 PWR Approach to Criticality Using Boric Acid      04/29/2021
Cycle 23, Comparison to Plant Data
TQ-AA-306      ATT 16 PWR Approach to Criticality Using Boric Acid      04/27/2021
Cycle 23, New Core Test
TQ-AA-306      ATT 17 PWR Approach to Criticality Using Rods Cycle 23,  04/27/2021
New Core Test
TQ-BR-0115    Transient 10, Slow Primary Depressurization Due to Open  03/22/2021
PORV w/o Charging Pumps
Inspection Type            Designation    Description or Title                                      Revision or
Procedure                                                                                            Date
TQ-BR-302-0103 Braidwood Steady State Testing 100% and 75%                03/05/2020
TQ-BR-302-0103 FW/CV Letdown System Tuning 49%                            03/05/2020
TQ-BR-302-0106 Transient Test - 1, Manual Reactor Trip                    03/22/2021
TQ-BR-302-0107 Transient Test 2, Simultaneous Trip of All Main Feedwater  03/22/2021
Pumps
TQ-BR-302-0108 Transient Test 3, Simultaneous Closure of All Main Steam  03/22/2021
Isolation Valves
TQ-BR-302-0109 Transient Test 4, Simultaneous Trip of All Reactor Coolant 03/22/2021
Pumps
TQ-BR-302-0110 Transient Test 5, Trip of Any Single Reactor Coolant Pump  03/22/2021
TQ-BR-302-0111 Transient Test 6, Turbine Trip <br><P-8                    03/22/2021
TQ-BR-302-0112 Transient 7, Maximum Ramp Rate (100% to 75% to 100%)      03/22/2021
TQ-BR-302-0113 Transient 8, LBLOCA with LOOP                              03/22/2021
TQ-BR-302-0114 Transient 9, Maximum Size Main Steam Line Rupture          03/22/2021
TQ-BR-302-0116 Maximum Design Load Reject                                03/22/2021
Procedures      TQ-AA-10      Systematic Approach to Training Process Description        6
TQ-AA-150      Operator Training Programs                                20
TQ-AA-155      Conduct of Simulator Training and Evaluation              11
TQ-AA-201      Examination Security and Administration                    18
TQ-AA-306      Simulator Management                                      10
TQ-BR-201-0113 Braidwood Training Department Simulator Examination        23
Security Actions
Self-Assessments                Differences Between Braidwood Simulator and Braidwood      SRB 21-2
Unit 1
Work Orders                    Open Service Work Requests                                08/16/2021
71111.11Q Procedures        OP-AA-101-111- Operations Standards and Expectations                      27
1001
OP-AA-101-113  Operator Fundamentals                                      15
OP-AA-101-113- 4.0 Crew Critique Guidelines                              11
1006
OP-AA-103-102  Watch-Standing Practices                                  20
OP-AA-103-102- Strategies for Successful Transient Mitigation            2
1001
Inspection Type              Designation    Description or Title                                    Revision or
Procedure                                                                                          Date
OP-AA-103-103  Operation of Plant Equipment                            1
OP-AA-104-101  Communications                                          5
OP-AA-111-101  Operating Narrative Logs and Records                    18
OP-AA-300      Reactivity Management                                  14
71111.12  Corrective Action 1451512        Unit 2 Core Exit Thermocouple Nozzle 77 Connections    12/12/2012
Documents                        Swapped Affecting Indications
4370362        Recurring Equipment Reliability Issue Unit 1 D          09/18/2020
Incore Detector
4393580        Hairline Cracks in Tops of Battery Cells (1DC02E)      01/03/2021
4402276        Battery 211 Terminal Voltage High Out of Admin Limit    02/14/2021
4402279        Battery 112 Quarterly Temp Deviation High Out of Admin  02/14/2021
Limit
4403966        1D Incore Detector Issues                              02/22/2021
4411770        Failed Post-Maintenance Test 1D Incore                  03/26/2021
4413950        Battery 211 Has Cap Broken on Cell 56                  04/04/2021
4418835        1BwOS TRM 3.3.H.1 Failed Symmetric Core Exit            04/25/2021
Thermocouple Temperature Limits
4419609        Unit 1 Core Exit Thermocouple Nozzle 74 Connections    04/28/2021
Swapped Affecting Indications
21778        Unexpected Alarms 1-10-A5 and 1-114-A1 for OPDT        05/05/2021
23740        Unit 1 Core Exit Thermocouples Exceed Allowed Maximum  05/15/2021
Deviation
25470        DC111 Cracked Battery Cells                            05/25/2021
4436872        Pilot Cell for Battery 112 Specific Gravity Found Low  07/25/2021
4439676        Summary of Findings from Braidwood Unit 1 Source Range  08/09/2021
Nuclear Instrument Cable Testing
4440617        Unexpected BwAR 1-10-C3 Poer Range Flux Rate Trip Alert 08/13/2021
for N41
4440747        Battery 111 Average Cell Temp High                      08/15/2021
4441987        Unexpected Alarms 1-10-A5 and 1-14-A1 for 1C OPDT      08/22/2021
Operability      ER-AA-320-1001 Maintenance Rule 18-10  Scoping                        0
Evaluations
Procedures        ER-AA-312-1002 Maintenance Rule Functions  Safety Significant        3
Inspection Type              Designation    Description or Title                                  Revision or
Procedure                                                                                          Date
Classification
ER-AA-320      Maintenance Rule Implementation per NEI 18-10          0
ER-AA-320-1001 Maintenance Rule 18-10  Failure Definitions          0
ER-AA-320-1004 Maintenance Rule 18-10  Performance Monitoring and    1
Dispositioning Between (a)(1) and (a)(2)
71111.13  Corrective Action 4446169        Unexpected MRC Alarm; 12A HTR LO                      09/14/2021
Documents        4446232        1HD054A Continuous Operation Evaluation Required      09/14/2021
Miscellaneous                    1SI8920 Work Window Protected Equipment List          09/13/2021
Procedures        ER-AA-600      Risk Management                                        7
ER-AA-600-1042 On-Line Risk Management                                13
MA-AA-716-004  Conduct of Troubleshooting                            19
OP-AA-108-117  Protected Equipment Program                            7
WC-AA-101-1006 On-Line Risk Management and Assessment                4
71111.15  Corrective Action 1213984        A2R15LL: S/U FW PP Press Switch Isolation Leak-By      05/10/2011
Documents        320432        2PS-FW282A Isolation Valve Leaks-By                    04/02/2005
4419609        Unit 1 Core Exit Thermocouple Nozzle 74 - Connections  04/28/2021
Swapped Affecting Indications
20610        B Train Core Exit Thermocouples Not Communicating with 05/01/2021
Plant Process Computer
23740        Unit 1 Core Exit Thermocouples Exceed Allowed Maximum  05/15/2021
Deviation
28965        U-2 Startup Feedwater Pump Oil Pressure Low            06/12/2021
4436953        2FIS-0611 is Weeping Boric Acid                        07/26/2021
4437474        1SX169A Failed to Open on Slow Local Start of 1A DG    07/28/2021
4443522        2A DG Bolt on 4L Cylinder Sheared During Scheduled Run 08/30/2021
4447805        0B Non-Accessible Plenum Delay                        09/21/2021
Procedures        BwOP FW-24    Filling and Venting an Isolated Feedwater Pump        14
ER-AA-600-1012 Risk Management Documentation                          14
OP-AA-106-101- Operational Decision-Making Process                    23
1006
OP-AA-108-111  Adverse Condition Monitoring and Contingency Planning  15
OP-AA-108-115  Operability Determinations (CM-1)                      24
71111.19  Procedures        1BwOSR        Group A IST Requirements for 1B Safety Injection Pump  12
Inspection Type              Designation    Description or Title                                      Revision or
Procedure                                                                                              Date
5.5.8.SI-10B    (1SI01PB)
1BwOSR          Train B Safety Injection System Valve Stroke Surveillance  14
5.5.8.SI-1B
1BwOSR          Train B Safety Injection System Isolation Valve Indication 12
5.5.8.SI-2B    Surveillance
SPP-21-002      Modification Test of 1SA01CA Station Air Compressor        0
Work Orders      4762173        1SI8920 Motor Operated Valve Diagnostic Test              09/14/2021
5092650        Electrical  Replacement of U0 SAC EC 630879              10/06/2021
5175731        IST for 1SI8919A/B/8922B/8926  ASME Surveillance          09/14/2021
Requirements for 1SI01PM
71111.22  Corrective Action 4438884        2A DG Lower Lube Oil Cooler Oil Leak When Running          08/04/2021
Documents
Miscellaneous                    Calibration of Steam Generator 2B Main Steam Atmospheric  3
Relief Valve Control Loop Test Report Package
2P-MS042 BwIP 2500-070
Procedures        2BwOSR 3.8.1.2- Unit Two 2A Diesel Generator Operability Surveillance      51
2BwOSR          Group A IST Requirements for Residual Heat Removal        23
5.5.8.RH-5B    Pump 2RH01PB
BwIP 2500-070  Calibration of Steam Generator Main Steam Atmospheric      13
Relief Valve Control Loop
Work Orders      4718820        2P-MS042 S/G 2B Steam Outlet Pressure Loop                08/23/2021
71114.04  Miscellaneous    Eval No. 20-71  Emergency Action Levels for Braidwood Station,            09/08/2020
EP-AA-1001, Addendum 3
71114.06  Procedures        EP-AA-1000      Standardized Radiological Emergency Plan                  33
EP-AA-1001      Radiological Emergency Plan Annex for Braidwood Station    35
71124.05  Procedures        RP-AA-700      Controls for Radiation Protection Instrumentation          8
71124.07  Corrective Action AR 04359867    1st and 2nd Quarter REMP Samples to Document in            07/30/2020
Documents                        2020 AREOR
AR 04398177    BD-22                                                      01/26/2021
AR 04398679    3rd and 4th Quarter REMP Samples to Document in            01/28/2021
20 AREOR
Miscellaneous                    Braidwood Station Unit 1 and 2 Annual Radiological        05/2020
Environmental Operating Report 2019
Inspection Type              Designation Description or Title                                      Revision or
Procedure                                                                                          Date
Meteorological Tower Inspection Report                    06/2019
Meteorological Tower Inspection Report                    06/2020
Braidwood Nuclear Power Station Annual Radioactive        05/2021
Effluent Release Report (ARERR) 2020
Braidwood Station Unit 1 and 2 Annual Radiological        05/2021
Environmental Operating Report 2020
71124.08  Corrective Action AR 04364522 0B RW Demin Inlet Pressure High Out of Band                08/21/2020
Documents        AR 04375152 0PL01J, Liquid RW Control Panel, Alarm Check              10/07/2020
Unsatisfactory
AR 04403327 Lesson Learned: Dose Received During RW Resin Liner        02/18/2021
Survey
Miscellaneous                10 CFR 61 Analysis for Primary Resin Filters              04/16/2021
Procedures        RP-AA-600  Radioactive Material/Waste Shipments                      18
Shipping Records  RWS 20-015  UN3321 LSA-II; 14 DAW Legacy Waste in Cask 14-210          08/27/2020
RWS 20-018  UN2916 Type (B) Package; Resin Liner PO 692200-4          11/12/2020
RWS 21-001  UN3321 LSA-II; Resin Liner P0695283-14 in Cask 14-215      01/12/2021
RWS 21-015  UN2910 Limited Quantity of Material; Seven B-25 Boxes of  08/17/2021
CP Resin
71151      Miscellaneous                NRC Performance Indicator Data; Mitigating                07/01/2020 -
Systems  Mitigating System Performance Index for Heat    06/30/2021
Removal Systems
NRC Performance Indicator Data; Mitigating                07/01/2020 -
Systems  Mitigating System Performance Index for          06/30/2021
Residual Heat Removal Systems
NRC Performance Indicator Data; Mitigating                07/01/2020 -
Systems  Mitigating System Performance Index for          06/30/2021
Cooling Water Systems
Procedures        LS-AA-2001  Collecting and Reporting of NRC Performance Indicator Data 16
LS-AA-2200  Mitigating System Performance Index Data Acquisition and  7
Reporting
71152      Corrective Action 4364058    Forced Helium Drying Skid Issue                            08/19/2021
Documents        4433954    It Was Identified That Corrective Action 04364058-22 Had  07/08/2021
Been Extended Twice, In Reviewing the CA Template, the
Extensions and Their Approvals Were Not Documented
Inspection Type          Designation    Description or Title                                      Revision or
Procedure                                                                                        Date
4434922        Level 4 Configuration Control - Received Unexpected Alarm 07/14/2021
1-2-Ec
Drawings      M-66, Sheet 3A Diagram of Component Cooling Water, Units 1 and 2        AW
Miscellaneous                Gap Analysis for Braidwood DCS Human Performance Error    08/18/2020
Procedures    2BwOSR        Common Train Component Cooling Isolation Valve Stroke    10
5.5.8.CC-3    Surveillance
NO-AA-10      Quality Assurance Topical Report (QATR)                  97
OU-MW-671-300  MPC Processing Forced Helium Dehydration (FHD) for        16
PWRS (ISFSI)
PI-AA-120      Issue Identification and Screening Process                11
PI-AA-125      Corrective Action Program (CAP) Procedure                7
PI-AA-125-1001 Root Cause Analysis Manual                                6
PI-AA-125-1003 Corrective Action Program Evaluation Manual              6
PI-AA-125-1004 Effectiveness Review Manual                              2
2
}}
}}

Revision as of 18:43, 16 January 2022

Integrated Inspection Report 05000456/2021003 and 05000457/2021003
ML21299A077
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 10/26/2021
From: Hironori Peterson
Region 3 Branch 3
To: Rhoades D
Exelon Generation Co, Exelon Nuclear
References
IR 2021003
Download: ML21299A077 (24)


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