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l L @l 0 ] 5 l 0 l 0 l 0 l 3 l 3 l 4 69@l 0EVENT                        l 3 DATE l 2 l 6 l 8 l 0 @l014l0l8]8l0l@
l L @l 0 ] 5 l 0 l 0 l 0 l 3 l 3 l 4 69@l 0EVENT                        l 3 DATE l 2 l 6 l 8 l 0 @l014l0l8]8l0l@
J4      15      REPORT OATE          40 8        8                    60            61            QOCnETsyv8ER              64 EVENT DESCRIPTION AND PRO 8ABLE CONSEQUENCES h o 2        l Plant operators were testing the temporary fire pump when a section of the fire main [
J4      15      REPORT OATE          40 8        8                    60            61            QOCnETsyv8ER              64 EVENT DESCRIPTION AND PRO 8ABLE CONSEQUENCES h o 2        l Plant operators were testing the temporary fire pump when a section of the fire main [
[
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l pi-lTj l f ailed. During performance of the surveillance test on the portable fire pump                                                                                  l l                                                                                                                                                    In fact, system l
l pi-lTj l f ailed. During performance of the surveillance test on the portable fire pump                                                                                  l l                                                                                                                                                    In fact, system l l o 14 l l mentioned above, there was a problem maintaining system pressure.                                                                                                    ,
!
l o 14 l l mentioned above, there was a problem maintaining system pressure.                                                                                                    ,
I i
I i
o s        l pressure never rose above 120 psig during a half-hour testing period prior to 1620 l 10 is 1 I hours when the failure occurred. The Hvdropneumatic Pressure Maintenance Pump                                                                                  i lo 171 l {FP-P-31 was running prior to and during this surveillance test.                                                                    Between the time I i o is l l period of 1610 hours to 1620 hours, while testing was in                                                                  (continued on attached)l 80 SYSTEM              CAU$E        CAUSE                                                    COMP.          VA LV E CODE                CODE      SUSCOCE                COMPONENT CODE                  ,U8C00E        SUSCODE l A lB l@ lE l@ lC l@ lP lI lP lE lX lX l@ 'D ]@ lZ                                                              l@                    ,
o s        l pressure never rose above 120 psig during a half-hour testing period prior to 1620 l 10 is 1 I hours when the failure occurred. The Hvdropneumatic Pressure Maintenance Pump                                                                                  i lo 171 l {FP-P-31 was running prior to and during this surveillance test.                                                                    Between the time I i o is l l period of 1610 hours to 1620 hours, while testing was in                                                                  (continued on attached)l 80 SYSTEM              CAU$E        CAUSE                                                    COMP.          VA LV E CODE                CODE      SUSCOCE                COMPONENT CODE                  ,U8C00E        SUSCODE l A lB l@ lE l@ lC l@ lP lI lP lE lX lX l@ 'D ]@ lZ                                                              l@                    ,
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           , 2      l this type. The failed section of piping has been replaced.                                                                                                g I      i L.' l.3! I                                                                                                                                                                      i l
           , 2      l this type. The failed section of piping has been replaced.                                                                                                g I      i L.' l.3! I                                                                                                                                                                      i l
i  4    I 80 7      8 9
i  4    I 80 7      8 9
                                       *bPowER                      OTHER STATUS              Dis O    RY                        DISCOVERY DESCRIPTION STA ITTi'l W@ l 0l 010l@lDesien Change                                                  l    l B l@l Visual: operator observation                                            l      l n w tage                  44      45        4e                                                                w
                                       *bPowER                      OTHER STATUS              Dis O    RY                        DISCOVERY DESCRIPTION STA ITTi'l W@ l 0l 010l@lDesien Change                                                  l    l B l@l Visual: operator observation                                            l      l n w tage                  44      45        4e                                                                w 8 ,cy,y,7y      co'j,,y,            12                                                                                                                                l LOCATION of RELEASE                                    I RELEASED OP RELE ASE                      AMOUNT OF ACTIVlTY i e                                                      3/A                    I          I                                      N/A                                l 7      8 9 LzJ @ LzJ@l    10          tt                                      44            45                                                                    80 PERSONNEL E RPO5URES NUV8ER                TYPE        DESCRIPTtON i 7 1010l0l@lZ]@l N/A a
      '
8 ,cy,y,7y      co'j,,y,            12                                                                                                                                l LOCATION of RELEASE                                    I RELEASED OP RELE ASE                      AMOUNT OF ACTIVlTY i e                                                      3/A                    I          I                                      N/A                                l 7      8 9 LzJ @ LzJ@l    10          tt                                      44            45                                                                    80 PERSONNEL E RPO5URES NUV8ER                TYPE        DESCRIPTtON
'
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                       ,ERsON~ELINJU4Es
                       ,ERsON~ELINJU4Es
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800D 5053L
800D 5053L


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      .
    ..
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Attachment To LER 80-18/01T Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 Event Description And Probable Consequences    (continued) progress, system pressure dropped to 95 psig, causing Diesel Driven Fire    ,
Attachment To LER 80-18/01T Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 Event Description And Probable Consequences    (continued) progress, system pressure dropped to 95 psig, causing Diesel Driven Fire    ,
Pump [FP-P-2] to start. The system pressure increased and the Diesel Pump (FP-P-2] was throttled back, again, system pressure dropped. The operator then increased the speed of {FP-P-2] again and, at approximately 1620 hours,
Pump [FP-P-2] to start. The system pressure increased and the Diesel Pump (FP-P-2] was throttled back, again, system pressure dropped. The operator then increased the speed of {FP-P-2] again and, at approximately 1620 hours, the system pressure dropped to 25 pounds. This is the point at which the fire main failed. There was a minimal safety hazard because the operators were aware of the failure and had it isolated in eight minutes.
                                                                                      '
the system pressure dropped to 25 pounds. This is the point at which the fire main failed. There was a minimal safety hazard because the operators were aware of the failure and had it isolated in eight minutes.
                                                                                       ;
                                                                                       ;
I
I
                                                                                      ,
                                                                                      !
                             .}}
                             .}}

Revision as of 13:32, 1 February 2020

LER 80-018/01T-0:on 800326,plant Operators Were Testing Temporary Fire Pump When Section of Fire Main Failed.Caused by Piping Failure.Failed Section of Piping Replaced
ML19305D797
Person / Time
Site: Beaver Valley
Issue date: 04/08/1980
From: Werling J
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19305D782 List:
References
LER-80-018-01T, LER-80-18-1T, NUDOCS 8004150534
Download: ML19305D797 (2)


Text

.

U , , .

U. S. NUCLE AR REGULATORY COMMISSION NRc F OCM %6

, P773 i LICENSEE EVENT REPORT (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION)

CONTROL SLOCK: l I

l l l l l lh 6

TOT'l i P lLICENSEE A \ BCODE l V l S l 1ISl@l 0 l 0 l-LICENSE l 0 l NuveER 0 l 0 l 0 l 0 l- 26l0 l 260 l@l4 LICENSEl1TYPE l1 l1JO l 1 $1l@l l

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8 8 9 le CON T 10IiI 3[,%

l L @l 0 ] 5 l 0 l 0 l 0 l 3 l 3 l 4 69@l 0EVENT l 3 DATE l 2 l 6 l 8 l 0 @l014l0l8]8l0l@

J4 15 REPORT OATE 40 8 8 60 61 QOCnETsyv8ER 64 EVENT DESCRIPTION AND PRO 8ABLE CONSEQUENCES h o 2 l Plant operators were testing the temporary fire pump when a section of the fire main [

[

l pi-lTj l f ailed. During performance of the surveillance test on the portable fire pump l l In fact, system l l o 14 l l mentioned above, there was a problem maintaining system pressure. ,

I i

o s l pressure never rose above 120 psig during a half-hour testing period prior to 1620 l 10 is 1 I hours when the failure occurred. The Hvdropneumatic Pressure Maintenance Pump i lo 171 l {FP-P-31 was running prior to and during this surveillance test. Between the time I i o is l l period of 1610 hours0.0186 days <br />0.447 hours <br />0.00266 weeks <br />6.12605e-4 months <br /> to 1620 hours0.0188 days <br />0.45 hours <br />0.00268 weeks <br />6.1641e-4 months <br />, while testing was in (continued on attached)l 80 SYSTEM CAU$E CAUSE COMP. VA LV E CODE CODE SUSCOCE COMPONENT CODE ,U8C00E SUSCODE l A lB l@ lE l@ lC l@ lP lI lP lE lX lX l@ 'D ]@ lZ l@ ,

o 9 12 13 18 19 20 7 8 9 to 11 SEQUENTIAL OCCUPRENCE REPORT REVISION EVENT YE AR R EPORT No. COCE TYPE No.

g R .Ro

@ ,a(jg l-l 10 11 18 l l-l 10 l 1 l lT l l-l Loj

._ l288l01 22 23 24 26 27 28 29 30 Ji 32 ON PL NT eN HOURS 22 $8 IT POR41 8. $UPPL E MANUPA TURER K N AC ON lAl@lZl@

33 34 J@

35 lZ 06 l@ l0 l0l0l0l 31 40 lenY l@ lNl@

42 l N j@

43 lZl9l9l9J@

44 47 l

CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h i i ; o i l The cause of the incident was piping failure. The piping section will be lab  ;

y l tested for further insight into the failure mode. This is the second failure of l

~

l

, 2 l this type. The failed section of piping has been replaced. g I i L.' l.3! I i l

i 4 I 80 7 8 9

  • bPowER OTHER STATUS Dis O RY DISCOVERY DESCRIPTION STA ITTi'l W@ l 0l 010l@lDesien Change l l B l@l Visual: operator observation l l n w tage 44 45 4e w 8 ,cy,y,7y co'j,,y, 12 l LOCATION of RELEASE I RELEASED OP RELE ASE AMOUNT OF ACTIVlTY i e 3/A I I N/A l 7 8 9 LzJ @ LzJ@l 10 tt 44 45 80 PERSONNEL E RPO5URES NUV8ER TYPE DESCRIPTtON i 7 1010l0l@lZ]@l N/A a

l

,ERsON~ELINJU4Es

~uv.ER oEsCRIPTioN@

7 i -

8 9 Iol0l0l@l it 12 N/A 80 l

7 E DE PT oN i 9 l,_Z_J@l N/A l gg 7 8 9 10 Om ,

G45CRiPTION 2 o IN 155UEI81 n/A i i i i i i i i i iiiil1 8 8 9 'O 64 69 30 5 J. A. Werling PHONE:

412-643-1258 2 NAME OF PREPARER _

800D 5053L

Attachment To LER 80-18/01T Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 Event Description And Probable Consequences (continued) progress, system pressure dropped to 95 psig, causing Diesel Driven Fire ,

Pump [FP-P-2] to start. The system pressure increased and the Diesel Pump (FP-P-2] was throttled back, again, system pressure dropped. The operator then increased the speed of {FP-P-2] again and, at approximately 1620 hours0.0188 days <br />0.45 hours <br />0.00268 weeks <br />6.1641e-4 months <br />, the system pressure dropped to 25 pounds. This is the point at which the fire main failed. There was a minimal safety hazard because the operators were aware of the failure and had it isolated in eight minutes.

I

.