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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6571994-05-0606 May 1994 LER 94-005-00:on 940407,chain Locking Mechanism on CP Suction Isolation Valve,Was Found Broken.Caused by Personnel Error.Corrective Action:New Chain Placed on Valve Handwheel & Chain Locking Mechanism intacted.W/940506 Ltr ML20029D8031994-05-0404 May 1994 LER 94-003-00:on 940404,two Flow Orifices Were Improperly Installed.Caused by Improper Installation of All Accessible Flow Orifices.Personnel Performed Procedure Ost 1.6.4 Correcting Improperly Installed orifices.W/940504 Ltr ML20046B5481993-07-30030 July 1993 LER 93-012-00:on 930702,discovered That Hydrogen Analyzer Inoperable During Quarterly Performance of Calibration Procedure.Test Personnel Contributed to Cause of Event.Test & Calibration Procedures Will Be revised.W/930730 Ltr ML20045J1201993-07-19019 July 1993 LER 93-011-00:on 930619,ESF Actuation Letdown Isolation Occurred While Synchronizing Main Unit Generator.Caused by Cooldown of RCS Due to Steam Demand.Plant Stabilized within Three Minutes & Pressurizer Level restored.W/930719 Ltr ML20045G4591993-07-0808 July 1993 LER 93-010-00:on 930614,determined That TS Surveillance on SI Accumulator Samples Missed Due to Draining & Refilling Accumulators Several Times During Outage.Accumulators a & C Immediately sampled.W/930708 Ltr ML20045F4711993-07-0202 July 1993 LER 93-009-00:on 930607,high Radiation Area Barrier Was Unlocked Due to Personnel Error.Comprehensive Confirmation Survey Performed,Personnel Interviewed & Task Force Formed. W/930702 Ltr ML20044F1541993-05-21021 May 1993 LER 93-007-00:on 930423,discoverd That Original Piping Did Not Conform to Design Code Requirement.Caused by Design Deficiency.Headers Fitted W/Code Approved End Caps & Tested & Now Conform to Design requirements.W/930521 Ltr ML20044F1521993-05-21021 May 1993 LER 93-008-00:on 930423,leakage Detected Through Two Check Valves in Chlorine Injection Line.Caused by Failure to Include Valves in ASME Section XI Testing Program.Check Valves Added to ASME Testing program.W/930521 Ltr ML20044D5251993-05-14014 May 1993 LER 93-006-00:on 930415,two Operators Entered Posted Area W/O Radiation Monitoring Device & Entered Locked High Radiation Area & Left Barrier Open.Caused by Personnel Error in Judgement.Operators counseled.W/930514 Ltr ML20024H1191991-05-15015 May 1991 LER 91-012-00:on 910415,excessive Max Operating Pressure Differential for Selected Solenoid Operated Valves Noted. Caused by Design Deficiencies.Equipment Mod Initiated to Replace Solenoid valve.W/910515 Ltr ML20029B2541991-03-0404 March 1991 LER 91-005-00:on 910131,steam Leakage in Auxiliary Feedwater Pumproom Caused ESF Actuation.Caused by Personnel Error. Control Room Operator Closed Steam Supply Isolation Valve to Stop Steam Leaking & Event Will Be reviewed.W/910304 Ltr ML17286B2651991-02-14014 February 1991 LER 90-006-01:on 900605,containment Isolation Valves Exceeded Stroke Time Limit,Per Tech Spec 3.6.3.1.Caused by Deficient Surveillance Program.Surveillance Procedures Revised to Include Stroke Time requirements.W/910214 Ltr ML20028H7391991-01-23023 January 1991 LER 90-007-01:on 900622,containment Entry Performed to Determine If Flanges Installed,Per Info Notice 90-019. Flanges Immediately Removed.Caused by Procedural Deficiency. Transfer Canal Draining Procedures revised.W/910123 Ltr ML20024F7441990-12-14014 December 1990 LER 90-021-00:on 901113,ESF Actuation & Feedwater Isolation Occurred During MSIV Stroke Testing.Caused by Operator Error.Feedwater Isolation Signal Reset & Isolation Valves reopened.W/901214 Ltr ML20024F7431990-12-14014 December 1990 LER 90-023-00:on 901114,ESF Actuation & Feedwater Isolation Occurred in Response to Opening Condenser Steam Dump Valve. Caused by Operation of Steam Dump Sys in Steam Pressure Control Mode.Signal reset.W/901214 Ltr ML17285B4731990-07-18018 July 1990 LER 90-007-00:on 900622,refueling Cavity Drain Flanges Found to Be Installed During Operation.Caused by Deficiency in Transfer Canal Draining Procedure.Procedure Revised to Verify Removal of Flanges After Canal drained.W/900717 Ltr ML20043G5771990-06-15015 June 1990 LER 89-017-02:on 891218,atmospheric Steam Relief Valve C Opened to Lower MSIV C.Caused by Swell Phenomena Experienced After Opening MSIV C.Feedwater Isolation Signal Reset. W/900615 Ltr ML20043B5171990-05-23023 May 1990 LER 90-004-00:on 900423,inadvertent ESF Actuation Occurred During Safeguards Protection Sys Testing.Caused by Personnel Closing Breaker Before Resetting Safety Injection Sys Signal.Signal reset.W/900523 Ltr ML20043B5201990-05-23023 May 1990 LER 90-005-00:on 900423,inadvertent ESF Actuation Occurred During Quench Spray Flow Switch Calibr.Caused by Error in Procedure Resulting in Installation of Two Leads on Same Terminal.Discharge Valves opened.W/900523 Ltr ML20043A4991990-05-16016 May 1990 LER 88-005-01:on 880219,startup Feedwater Pump Started, Causing Current Surge That Actuated Overcurrent Relay for Emergency Response Facility Transformer 3B.Caused by Faulty Transformer Relay.Relay replaced.W/900516 Ltr ML20012E6681990-03-29029 March 1990 LER 90-006-00:on 900227,plant Operation in Excess of Licensing Basis.Caused by Failure of Computer to Synchronize File Addresses in Task 3D.Heat Balance Calculations Reverified Using Data from Plant Variable Computer ML20012C4141990-03-14014 March 1990 LER 90-002-00:on 900117,steam Generator B Channel 3 Pressure Transmitter Failed Low & Declared Inoperable.On 900119, Discovered That Channel Returned to Svc W/O Completing Required Time Response Testing on transmitter.W/900314 Ltr ML20012C7271990-03-14014 March 1990 LER 90-002-00:on 900217,steam Generator B Channel 3 Pressure Transmitter Failed Low & Declared Inoperable.Caused by Failure to Complete Tech Spec Required post-maint Test. Post-maint Test Procedure revised.W/900314 Ltr ML20012C0631990-03-0808 March 1990 LER 90-005-01:on 900209,defect Found in Casing of Limitorque Model HBC-1 Gear Operators,Causing Valve Motion to Cease Prematurely in Open Direction.Caused by Excess Matl on Housings.Also Reported Per Part 21.W/900308 Ltr ML20012C0651990-03-0808 March 1990 LER 90-003-01:on 900110,determined That Recirculation Spray HX River Water Radiation Monitor Sample Line Lacked Automatic,Remote Manual or Locked Shut Containment Isolation Valve.Request for Exemption Submitted to NRC.W/900308 Ltr ML20011F2761990-02-23023 February 1990 LER 90-004-00:on 900124:discovered That Control Rod Positions Not Recorded on Operator Logs on 890425 When Control Rod Insertion Limit Monitor & Deviation Alarm Out of Svc.Cause Not Stated.Personnel counseled.W/900223 Ltr ML20006F2041990-02-20020 February 1990 LER 90-002-00:on 900114,120-volt Ac Inverter for Vital Bus 3 Experienced Blown Dc Input Fuse When Inverter Bypassed & Aligned to 480-volt Ac Emergency Power.Caused by Mgt Action. Administrative Guidance issued.W/900220 Ltr ML20011E6341990-02-14014 February 1990 LER 90-005-00:on 900209,six Limitorque Corp Gear Operators, Model HBC-1,found to Contain Defect in Casting of Limit Stop Housing.Housings Machined to Remove Excess Matl.Item Reportable Per Part 21.W/900214 Ltr ML17223A7461990-02-0909 February 1990 LER 90-003-00:on 900110,determined That Recirculation Spray HX River Water Radiation Monitor Sample Lines Lacked Automatic,Remote Manual or Locked Shut Isolation Valve. Exemption Request from GDC 57 initiated.W/900209 Ltr ML20011E2501990-02-0606 February 1990 LER 90-001-00:on 900107,high Radiation Alarm Received on Steam Generator Blowdown (SGBD) Sample Radiation Monitor, Causing SGBD Sys Isolation.Caused by Crud Particles Swept Into Monitor.Monitor Purged & Returned to svc.W/890206 Ltr ML20006B4031990-01-26026 January 1990 LER 89-018-01:on 891227,reactor Trip Occurred Following Initial Startup from Refueling Outage.Caused by Trip of 480 Volt Ac Feeder Breaker to Rod Drive Motor Generator Sets. Installed Spare Breaker tested.W/900126 Ltr ML20006A8711990-01-23023 January 1990 LER 89-019-00:on 891227,discovered That Manual Reactor Trip Operating Surveillance Test Not Performed within Required Frequency Prior to Previous Reactor start-up on 891224. Caused by Inadequate start-up procedures.W/900123 Ltr ML20006A8901990-01-23023 January 1990 LER 89-014-01:on 891101,routine Radiation Barrier Check Identified Faulty Door Locking Mechanism.Caused by Weld Latching Mechanism Plate Interfering W/Locking Action of Door.Mechanism Modified & Latch removed.W/900123 Ltr ML20006A8721990-01-23023 January 1990 LER 89-009-01:on 890413,temporary Protection Covers Found on Five Temp Elements During Test of High Energy Line Break Temp Elements.Caused by Deficiency in Surveillance Program. Covers Immediately Removed from Temp elements.W/900123 Ltr ML20006A8691990-01-23023 January 1990 LER 89-017-01:on 891218,feedwater Isolation ESF Actuation, Caused by Swell Phenomena Experienced After Opening of C Msiv.Feedwater Isolation Signal Reset & Restored to Prefeedwater Isolation conditions.W/900118 Ltr ML19354E1551990-01-17017 January 1990 LER 89-017-00:on 891218,feedwater Isolation Occurred Due to Erroneous Level Transmitter Root Valve Position Indication. Operations Personnel Reset Feedwater Isolation Signal. W/900117 Ltr ML19354E1071990-01-16016 January 1990 LER 89-016-00:on 891215 & 16,erratic Level Transmitter Behavior Caused Steam Generator B hi-hi Level Feedwater Isolation.Caused by Inner Plugs Remaining Partially Inserted After Valves Opened.Plugs Freed from seats.W/900116 Ltr ML20005F8901990-01-12012 January 1990 LER 89-015-01:on 891213,operator Incorrectly Restored Solid State Protection Sys Generating Low Steamline Pressure Safety Injection Signal.Caused by Operator Error.Plant Restored to pre-safety Injection condition.W/900112 Ltr ML19332F5051989-12-12012 December 1989 LER 89-013-00:on 891112,4 Kv Bus 1A Power Supply Breaker Tripped on Phase overcurrent,de-energizing Emergency Bus 1A. Caused by Incorrect Tap Setting on Overcurrrent Relay.Relay Taps Reset & Breaker replaced.W/891211 Ltr ML20005D6631989-12-0606 December 1989 LER 89-027-00:on 891106,Train a Svc Water Pump Seal Water Supply Automatically Transferred to Backup Supply Due to Low Pressure.Caused by Seal Water Normal Supply Inadvertently Isolating While de-energizing.Manual revised.W/891206 Ltr ML19332E4931989-12-0101 December 1989 LER 89-014-00:on 891108,routine Radiation Barrier Check Identified Faulty Door Locking Mechanism on North Door to East Valve Trench Area.Caused by Welded Latching Mechanism. Locking Mechanism modified.W/891201 Ltr ML19332D2321989-11-20020 November 1989 LER 89-026-00:on 891020,automatic Start of Auxiliary Feedwater Pumps Caused Steam Generator Blowdown Isolation. Caused by Inadequate Communications & Radiation Monitor Setpoint.Setpoint adjusted.W/891120 Ltr ML19325F1821989-11-0808 November 1989 LER 89-012-00:on 891010,in-core Instrumentation Guide Thimble Tubes Identified W/Degradation in Excess of 60% Wall Thickness.Caused by Mechanical Wear of Thimbles Against Reactor Vessel Internals.Tubes isolated.W/891108 Ltr ML19327B8701989-10-31031 October 1989 LER 89-014-01:on 890506,supply Breaker to 480 Volt Essential Bus J Opened & Alternate Bus J Supply Breaker Did Not Close. Caused by Spurious Trip Due to Broken Circuit.Reset Button Returned to Normal Position & Breaker closed.W/891031 Ltr ML19324C3741989-10-30030 October 1989 LER 88-002-01:on 880127,radiation Monitors for Control Room Deenergized,Resulting in Actuation of Control Room Emergency Bottled Air Pressurization Sys.Cause Not Determined.Pressure Transmitter to Be replaced.W/891030 Ltr ML19327B1851989-10-20020 October 1989 LER 89-011-00:on 890920,engineering Determined That Rupture Restraint Gaps Were Opened to Greater than Original Design Analysis.Caused by Alignment Performed During Hot Functional Testing.Design Change Mod to Be performed.W/891020 Ltr ML19325C6321989-10-10010 October 1989 LER 89-025-00:on 890910,high Temps on Steam Generators B & C Auxiliary Feedwater Lines Identified.Caused by Improper Seating of Auxiliary Feedwater Check Valves.Procedure Initiated to Verify & Correct condition.W/891010 Ltr ML19325C8851989-09-0909 September 1989 LER 89-010-00:on 890907,UL Test Results Indicated That Horizontally Mounted Prototype Fire Dampers Failed to Comply W/Requirements of Ul Std 555-1968.Caused by Discrepancies Between as-fabricated & Required specs.W/891009 Ltr ML18041A1891989-04-21021 April 1989 LER 89-005-00:on 890322,safety Injection Occurred Due to Low Pressurizer Pressure.Caused by Deficiencies in Safety Accumulator Check Valve Surveillance Test.Refueling Outage Calibr Procedures pre-reviewed by operators.W/890421 Ltr ML18041A1881989-03-14014 March 1989 LER 89-003-00:on 890212,noticed Erratic Operation of Main Feedwater Regulating Valve C & Turbine Trip/Reactor Trip Occurred Due to High Water Level in Steam Generator C.Caused by Valve Vibration & Hydraulic forces.W/890314 Ltr 1994-05-06
[Table view] Category:RO)
MONTHYEARML20029D6571994-05-0606 May 1994 LER 94-005-00:on 940407,chain Locking Mechanism on CP Suction Isolation Valve,Was Found Broken.Caused by Personnel Error.Corrective Action:New Chain Placed on Valve Handwheel & Chain Locking Mechanism intacted.W/940506 Ltr ML20029D8031994-05-0404 May 1994 LER 94-003-00:on 940404,two Flow Orifices Were Improperly Installed.Caused by Improper Installation of All Accessible Flow Orifices.Personnel Performed Procedure Ost 1.6.4 Correcting Improperly Installed orifices.W/940504 Ltr ML20046B5481993-07-30030 July 1993 LER 93-012-00:on 930702,discovered That Hydrogen Analyzer Inoperable During Quarterly Performance of Calibration Procedure.Test Personnel Contributed to Cause of Event.Test & Calibration Procedures Will Be revised.W/930730 Ltr ML20045J1201993-07-19019 July 1993 LER 93-011-00:on 930619,ESF Actuation Letdown Isolation Occurred While Synchronizing Main Unit Generator.Caused by Cooldown of RCS Due to Steam Demand.Plant Stabilized within Three Minutes & Pressurizer Level restored.W/930719 Ltr ML20045G4591993-07-0808 July 1993 LER 93-010-00:on 930614,determined That TS Surveillance on SI Accumulator Samples Missed Due to Draining & Refilling Accumulators Several Times During Outage.Accumulators a & C Immediately sampled.W/930708 Ltr ML20045F4711993-07-0202 July 1993 LER 93-009-00:on 930607,high Radiation Area Barrier Was Unlocked Due to Personnel Error.Comprehensive Confirmation Survey Performed,Personnel Interviewed & Task Force Formed. W/930702 Ltr ML20044F1541993-05-21021 May 1993 LER 93-007-00:on 930423,discoverd That Original Piping Did Not Conform to Design Code Requirement.Caused by Design Deficiency.Headers Fitted W/Code Approved End Caps & Tested & Now Conform to Design requirements.W/930521 Ltr ML20044F1521993-05-21021 May 1993 LER 93-008-00:on 930423,leakage Detected Through Two Check Valves in Chlorine Injection Line.Caused by Failure to Include Valves in ASME Section XI Testing Program.Check Valves Added to ASME Testing program.W/930521 Ltr ML20044D5251993-05-14014 May 1993 LER 93-006-00:on 930415,two Operators Entered Posted Area W/O Radiation Monitoring Device & Entered Locked High Radiation Area & Left Barrier Open.Caused by Personnel Error in Judgement.Operators counseled.W/930514 Ltr ML20024H1191991-05-15015 May 1991 LER 91-012-00:on 910415,excessive Max Operating Pressure Differential for Selected Solenoid Operated Valves Noted. Caused by Design Deficiencies.Equipment Mod Initiated to Replace Solenoid valve.W/910515 Ltr ML20029B2541991-03-0404 March 1991 LER 91-005-00:on 910131,steam Leakage in Auxiliary Feedwater Pumproom Caused ESF Actuation.Caused by Personnel Error. Control Room Operator Closed Steam Supply Isolation Valve to Stop Steam Leaking & Event Will Be reviewed.W/910304 Ltr ML17286B2651991-02-14014 February 1991 LER 90-006-01:on 900605,containment Isolation Valves Exceeded Stroke Time Limit,Per Tech Spec 3.6.3.1.Caused by Deficient Surveillance Program.Surveillance Procedures Revised to Include Stroke Time requirements.W/910214 Ltr ML20028H7391991-01-23023 January 1991 LER 90-007-01:on 900622,containment Entry Performed to Determine If Flanges Installed,Per Info Notice 90-019. Flanges Immediately Removed.Caused by Procedural Deficiency. Transfer Canal Draining Procedures revised.W/910123 Ltr ML20024F7441990-12-14014 December 1990 LER 90-021-00:on 901113,ESF Actuation & Feedwater Isolation Occurred During MSIV Stroke Testing.Caused by Operator Error.Feedwater Isolation Signal Reset & Isolation Valves reopened.W/901214 Ltr ML20024F7431990-12-14014 December 1990 LER 90-023-00:on 901114,ESF Actuation & Feedwater Isolation Occurred in Response to Opening Condenser Steam Dump Valve. Caused by Operation of Steam Dump Sys in Steam Pressure Control Mode.Signal reset.W/901214 Ltr ML17285B4731990-07-18018 July 1990 LER 90-007-00:on 900622,refueling Cavity Drain Flanges Found to Be Installed During Operation.Caused by Deficiency in Transfer Canal Draining Procedure.Procedure Revised to Verify Removal of Flanges After Canal drained.W/900717 Ltr ML20043G5771990-06-15015 June 1990 LER 89-017-02:on 891218,atmospheric Steam Relief Valve C Opened to Lower MSIV C.Caused by Swell Phenomena Experienced After Opening MSIV C.Feedwater Isolation Signal Reset. W/900615 Ltr ML20043B5171990-05-23023 May 1990 LER 90-004-00:on 900423,inadvertent ESF Actuation Occurred During Safeguards Protection Sys Testing.Caused by Personnel Closing Breaker Before Resetting Safety Injection Sys Signal.Signal reset.W/900523 Ltr ML20043B5201990-05-23023 May 1990 LER 90-005-00:on 900423,inadvertent ESF Actuation Occurred During Quench Spray Flow Switch Calibr.Caused by Error in Procedure Resulting in Installation of Two Leads on Same Terminal.Discharge Valves opened.W/900523 Ltr ML20043A4991990-05-16016 May 1990 LER 88-005-01:on 880219,startup Feedwater Pump Started, Causing Current Surge That Actuated Overcurrent Relay for Emergency Response Facility Transformer 3B.Caused by Faulty Transformer Relay.Relay replaced.W/900516 Ltr ML20012E6681990-03-29029 March 1990 LER 90-006-00:on 900227,plant Operation in Excess of Licensing Basis.Caused by Failure of Computer to Synchronize File Addresses in Task 3D.Heat Balance Calculations Reverified Using Data from Plant Variable Computer ML20012C4141990-03-14014 March 1990 LER 90-002-00:on 900117,steam Generator B Channel 3 Pressure Transmitter Failed Low & Declared Inoperable.On 900119, Discovered That Channel Returned to Svc W/O Completing Required Time Response Testing on transmitter.W/900314 Ltr ML20012C7271990-03-14014 March 1990 LER 90-002-00:on 900217,steam Generator B Channel 3 Pressure Transmitter Failed Low & Declared Inoperable.Caused by Failure to Complete Tech Spec Required post-maint Test. Post-maint Test Procedure revised.W/900314 Ltr ML20012C0631990-03-0808 March 1990 LER 90-005-01:on 900209,defect Found in Casing of Limitorque Model HBC-1 Gear Operators,Causing Valve Motion to Cease Prematurely in Open Direction.Caused by Excess Matl on Housings.Also Reported Per Part 21.W/900308 Ltr ML20012C0651990-03-0808 March 1990 LER 90-003-01:on 900110,determined That Recirculation Spray HX River Water Radiation Monitor Sample Line Lacked Automatic,Remote Manual or Locked Shut Containment Isolation Valve.Request for Exemption Submitted to NRC.W/900308 Ltr ML20011F2761990-02-23023 February 1990 LER 90-004-00:on 900124:discovered That Control Rod Positions Not Recorded on Operator Logs on 890425 When Control Rod Insertion Limit Monitor & Deviation Alarm Out of Svc.Cause Not Stated.Personnel counseled.W/900223 Ltr ML20006F2041990-02-20020 February 1990 LER 90-002-00:on 900114,120-volt Ac Inverter for Vital Bus 3 Experienced Blown Dc Input Fuse When Inverter Bypassed & Aligned to 480-volt Ac Emergency Power.Caused by Mgt Action. Administrative Guidance issued.W/900220 Ltr ML20011E6341990-02-14014 February 1990 LER 90-005-00:on 900209,six Limitorque Corp Gear Operators, Model HBC-1,found to Contain Defect in Casting of Limit Stop Housing.Housings Machined to Remove Excess Matl.Item Reportable Per Part 21.W/900214 Ltr ML17223A7461990-02-0909 February 1990 LER 90-003-00:on 900110,determined That Recirculation Spray HX River Water Radiation Monitor Sample Lines Lacked Automatic,Remote Manual or Locked Shut Isolation Valve. Exemption Request from GDC 57 initiated.W/900209 Ltr ML20011E2501990-02-0606 February 1990 LER 90-001-00:on 900107,high Radiation Alarm Received on Steam Generator Blowdown (SGBD) Sample Radiation Monitor, Causing SGBD Sys Isolation.Caused by Crud Particles Swept Into Monitor.Monitor Purged & Returned to svc.W/890206 Ltr ML20006B4031990-01-26026 January 1990 LER 89-018-01:on 891227,reactor Trip Occurred Following Initial Startup from Refueling Outage.Caused by Trip of 480 Volt Ac Feeder Breaker to Rod Drive Motor Generator Sets. Installed Spare Breaker tested.W/900126 Ltr ML20006A8711990-01-23023 January 1990 LER 89-019-00:on 891227,discovered That Manual Reactor Trip Operating Surveillance Test Not Performed within Required Frequency Prior to Previous Reactor start-up on 891224. Caused by Inadequate start-up procedures.W/900123 Ltr ML20006A8901990-01-23023 January 1990 LER 89-014-01:on 891101,routine Radiation Barrier Check Identified Faulty Door Locking Mechanism.Caused by Weld Latching Mechanism Plate Interfering W/Locking Action of Door.Mechanism Modified & Latch removed.W/900123 Ltr ML20006A8721990-01-23023 January 1990 LER 89-009-01:on 890413,temporary Protection Covers Found on Five Temp Elements During Test of High Energy Line Break Temp Elements.Caused by Deficiency in Surveillance Program. Covers Immediately Removed from Temp elements.W/900123 Ltr ML20006A8691990-01-23023 January 1990 LER 89-017-01:on 891218,feedwater Isolation ESF Actuation, Caused by Swell Phenomena Experienced After Opening of C Msiv.Feedwater Isolation Signal Reset & Restored to Prefeedwater Isolation conditions.W/900118 Ltr ML19354E1551990-01-17017 January 1990 LER 89-017-00:on 891218,feedwater Isolation Occurred Due to Erroneous Level Transmitter Root Valve Position Indication. Operations Personnel Reset Feedwater Isolation Signal. W/900117 Ltr ML19354E1071990-01-16016 January 1990 LER 89-016-00:on 891215 & 16,erratic Level Transmitter Behavior Caused Steam Generator B hi-hi Level Feedwater Isolation.Caused by Inner Plugs Remaining Partially Inserted After Valves Opened.Plugs Freed from seats.W/900116 Ltr ML20005F8901990-01-12012 January 1990 LER 89-015-01:on 891213,operator Incorrectly Restored Solid State Protection Sys Generating Low Steamline Pressure Safety Injection Signal.Caused by Operator Error.Plant Restored to pre-safety Injection condition.W/900112 Ltr ML19332F5051989-12-12012 December 1989 LER 89-013-00:on 891112,4 Kv Bus 1A Power Supply Breaker Tripped on Phase overcurrent,de-energizing Emergency Bus 1A. Caused by Incorrect Tap Setting on Overcurrrent Relay.Relay Taps Reset & Breaker replaced.W/891211 Ltr ML20005D6631989-12-0606 December 1989 LER 89-027-00:on 891106,Train a Svc Water Pump Seal Water Supply Automatically Transferred to Backup Supply Due to Low Pressure.Caused by Seal Water Normal Supply Inadvertently Isolating While de-energizing.Manual revised.W/891206 Ltr ML19332E4931989-12-0101 December 1989 LER 89-014-00:on 891108,routine Radiation Barrier Check Identified Faulty Door Locking Mechanism on North Door to East Valve Trench Area.Caused by Welded Latching Mechanism. Locking Mechanism modified.W/891201 Ltr ML19332D2321989-11-20020 November 1989 LER 89-026-00:on 891020,automatic Start of Auxiliary Feedwater Pumps Caused Steam Generator Blowdown Isolation. Caused by Inadequate Communications & Radiation Monitor Setpoint.Setpoint adjusted.W/891120 Ltr ML19325F1821989-11-0808 November 1989 LER 89-012-00:on 891010,in-core Instrumentation Guide Thimble Tubes Identified W/Degradation in Excess of 60% Wall Thickness.Caused by Mechanical Wear of Thimbles Against Reactor Vessel Internals.Tubes isolated.W/891108 Ltr ML19327B8701989-10-31031 October 1989 LER 89-014-01:on 890506,supply Breaker to 480 Volt Essential Bus J Opened & Alternate Bus J Supply Breaker Did Not Close. Caused by Spurious Trip Due to Broken Circuit.Reset Button Returned to Normal Position & Breaker closed.W/891031 Ltr ML19324C3741989-10-30030 October 1989 LER 88-002-01:on 880127,radiation Monitors for Control Room Deenergized,Resulting in Actuation of Control Room Emergency Bottled Air Pressurization Sys.Cause Not Determined.Pressure Transmitter to Be replaced.W/891030 Ltr ML19327B1851989-10-20020 October 1989 LER 89-011-00:on 890920,engineering Determined That Rupture Restraint Gaps Were Opened to Greater than Original Design Analysis.Caused by Alignment Performed During Hot Functional Testing.Design Change Mod to Be performed.W/891020 Ltr ML19325C6321989-10-10010 October 1989 LER 89-025-00:on 890910,high Temps on Steam Generators B & C Auxiliary Feedwater Lines Identified.Caused by Improper Seating of Auxiliary Feedwater Check Valves.Procedure Initiated to Verify & Correct condition.W/891010 Ltr ML19325C8851989-09-0909 September 1989 LER 89-010-00:on 890907,UL Test Results Indicated That Horizontally Mounted Prototype Fire Dampers Failed to Comply W/Requirements of Ul Std 555-1968.Caused by Discrepancies Between as-fabricated & Required specs.W/891009 Ltr ML18041A1891989-04-21021 April 1989 LER 89-005-00:on 890322,safety Injection Occurred Due to Low Pressurizer Pressure.Caused by Deficiencies in Safety Accumulator Check Valve Surveillance Test.Refueling Outage Calibr Procedures pre-reviewed by operators.W/890421 Ltr ML18041A1881989-03-14014 March 1989 LER 89-003-00:on 890212,noticed Erratic Operation of Main Feedwater Regulating Valve C & Turbine Trip/Reactor Trip Occurred Due to High Water Level in Steam Generator C.Caused by Valve Vibration & Hydraulic forces.W/890314 Ltr 1994-05-06
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARL-99-154, Monthly Operating Repts for Sept 199 for Bvps,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 199 for Bvps,Units 1 & 2. with L-99-139, LER 99-S01-00:on 990813,uncompensated Loss of Ability to Detect within Single Intrusion Security Detection Zone Occurred.Caused by Procedure non-compliance.Involved Personnel Received Counseling Re Event.With1999-09-0202 September 1999 LER 99-S01-00:on 990813,uncompensated Loss of Ability to Detect within Single Intrusion Security Detection Zone Occurred.Caused by Procedure non-compliance.Involved Personnel Received Counseling Re Event.With L-99-140, Monthly Operating Repts for Aug 1999 for Bvps,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Bvps,Units 1 & 2. with L-99-126, Monthly Operating Repts for Jul 1999 for Beaver Valley Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for Beaver Valley Power Station,Units 1 & 2.With L-99-107, Monthly Operating Repts for June 1999 for Bvps,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Bvps,Units 1 & 2. with ML20209D9531999-06-27027 June 1999 Inservice Insp Ninety-Day Rept Bvps,Unit 2 Outage 7,Year 1999 L-99-096, Monthly Operating Repts for May 1999 for BVPS Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for BVPS Units 1 & 2. with L-99-078, Special Rept:On 990326,seismic Monitoring Instruments Were Declared Inoperable.Caused by Resolution of Potential TS Compliance Issue & Work Scheduling Issue.Instrumentation Was Returned to Svc Following Calibr & Declared Operable1999-05-0303 May 1999 Special Rept:On 990326,seismic Monitoring Instruments Were Declared Inoperable.Caused by Resolution of Potential TS Compliance Issue & Work Scheduling Issue.Instrumentation Was Returned to Svc Following Calibr & Declared Operable L-99-079, Monthly Operating Repts for Apr 1999 for Beaver Valley Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Beaver Valley Power Station,Units 1 & 2.With ML20205L0401999-04-0909 April 1999 SER Accepting Util Relief Requests for Inservice Insp Second 10-year Interval for Beaver Valley Power Station, Unit 2 L-99-054, Special Rept:On 990320,meteorological Tower Wind Speed Sensors Were Declared Inoperable.Caused by Calibration Completed by Vendor Did Not Adequately Cover Full Operating Range of Sensors.Removed Sensors & Sent Offsite1999-04-0505 April 1999 Special Rept:On 990320,meteorological Tower Wind Speed Sensors Were Declared Inoperable.Caused by Calibration Completed by Vendor Did Not Adequately Cover Full Operating Range of Sensors.Removed Sensors & Sent Offsite L-99-058, Monthly Operating Repts for Mar 1999 for Bvps,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bvps,Units 1 & 2. with ML20196K7981999-03-25025 March 1999 Rev 4 to COLR, for Cycle 8 L-99-038, Monthly Operating Repts for Feb 1999 for Bvps,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Bvps,Units 1 & 2. with ML20203E1181999-02-10010 February 1999 SER Accepting Proposed Revs to Plant,Units 1 & 2 Quality Assurance Program Description L-99-019, Special Rept:On 990120,meteorological Tower Wind Speed Sensors Declared Inoperable.Caused by Processor Card for Sensor Locked Up & Needed to Be Reset.Heater That Fit Around Shaft of Sensor Replaced1999-02-0505 February 1999 Special Rept:On 990120,meteorological Tower Wind Speed Sensors Declared Inoperable.Caused by Processor Card for Sensor Locked Up & Needed to Be Reset.Heater That Fit Around Shaft of Sensor Replaced ML20196F7011999-01-31031 January 1999 BVPS Unit 2 Heatup & Cooldown Limit Curves During Normal Operation at 15 EFPY Using Code Case N-626 ML20203D4811999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Bvps,Units 1 & 2, in Accordance with NRC GL 97-02.With ML20207E6631999-01-28028 January 1999 Rev 0 to EMECH-0713-1, Operational Assessment of SG Tubing at Beaver Valley Unit 1,Cycle 13 ML20210G7041999-01-22022 January 1999 BVPS Unit 1 Facility Changes,Tests & Experiments for 980123-990122 ML20207E5861998-12-31031 December 1998 Annual Rept 1998 for Toledo Edison ML20207E5601998-12-31031 December 1998 Annual Rept 1998 for Pennpower ML20198B9021998-12-31031 December 1998 BVPS Unit 1 Simulator Four Yr Certification Rept for 1995-1998 ML20207E5901998-12-31031 December 1998 Dqe 1998 Annual Rept to Shareholders ML20199C9971998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Bvps,Units 1 & 2. with ML20207E5521998-12-31031 December 1998 Annual Rept 1998 for Ohio Edison ML20207E5761998-12-31031 December 1998 Annual Rept 1998 for Illuminating Co ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199F5341998-12-29029 December 1998 Safety Evaluation Granting Relief Requests 1-TYP-3-B3.140-1, 1-TYP-3-B5.70-1,1-TYP-3-RH-E-1-1,1-TYP-3-B-G-1, 1-TYP-3-APP-I-1,1-TYP-3-UT-1,1-TYP-3-N-509,1-TYP-3-N-521, 1-TYP-3-N-524,1-TYP-3-B3.120-1 & 1-TYP-3-C6.10-1 ML20198K8551998-12-21021 December 1998 SER Granting Relief Request PRR-5 for Third 10-year Inservice Testing for Beaver Valley Power Station,Unit 1 ML20198A1631998-12-0909 December 1998 SER Approving Implementation Program to Resolve USI A-46 at Facility That Has Adequately Addressed Purpose of 10CFR50.54(f) Request L-98-229, Monthly Operating Repts for Nov 1998 for Bvps,Units 1 & 2. with1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bvps,Units 1 & 2. with ML20195J3131998-11-12012 November 1998 Safety Evaluation Granting First & Second 10-yr Interval Inservice Insp Request for Relief L-98-210, Monthly Operating Repts for Oct 1998 for Bvps,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Bvps,Units 1 & 2. with ML20206G0291998-10-31031 October 1998 BVPS Unit 2 Facility Changes,Tests & Experiments for Period 971101-981031 ML20154R9121998-10-20020 October 1998 Safety Evaluation Accepting Proposed Changes to QA Program Description in Chapter 17.2 of BVPS-2 Ufsar.Proposed Changes Would Modify QA Organization to Allow Warehouse QC Inspectors to Report to Manager of Nuclear Procurement Dept ML20154P7491998-10-19019 October 1998 SE Accepting Second ten-year Interval Inservice Insp Request for Relief RR-1-TYP-2-B5.40-1,Rev 0,for Plant, Unit 1 ML20198F7611998-10-0606 October 1998 Duquesne Light Co,Beaver Valley Power Station 1998 Emergency Preparedness Ingestion Zone Exercise, Conducted on 981006 ML20154C6711998-10-0101 October 1998 Safety Evaluation Concluding That Revised Model Identified in Dl Submittal Was Appropriate for Analysis of Installed Conduit Ampacity Limits.Determined That There Are No Outstanding Safety Concerns with Respect to Ampacity ML20154D5001998-09-30030 September 1998 Special Rept on Overview of BVPS-1 & BVPS-2 TS Compliance Issues & Corrective Action Taken L-98-197, Monthly Operating Repts for Sept 1998 for Beaver Valley Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Beaver Valley Power Station,Units 1 & 2.With ML20154E2171998-09-28028 September 1998 Follow-up Part 21 Rept Re Defect with 1200AC & 1200BC Recorders Built Under Westronics 10CFR50 App B Program. Westronics Has Notified Bvps,Ano & RBS & Is Currently Making Arrangements to Implement Design Mods L-98-188, Special Rept:During 1998,Unit 2 SG Eddy Current exam,26 Tubes Were Improperly Encoded in SG 2RCS-SG21C During Previous Outage.Use of Independent Databases to Track New Indications Being Implemented as Preventive Measure1998-09-21021 September 1998 Special Rept:During 1998,Unit 2 SG Eddy Current exam,26 Tubes Were Improperly Encoded in SG 2RCS-SG21C During Previous Outage.Use of Independent Databases to Track New Indications Being Implemented as Preventive Measure L-98-178, Monthly Operating Repts for Aug 1998 for Bvps,Units 1 & 2. with1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Bvps,Units 1 & 2. with ML20155B5871998-08-28028 August 1998 Non-proprietary Rev 1 to 51-5001925-01, Risk Assessment for Installation of Electrosleeves at BVPS & Callaway Plant ML20236X2351998-08-0505 August 1998 Part 21 Rept Re Defect Associated W/Westronics 1200AC & 1200BC Recorders Built Under Westronics 10CFR50,App B Program.Beaver Valley,Arkansas Nuclear One & River Bend Station Notified.Design Mod Is Being Developed L-98-168, Monthly Operating Repts for July 1998 for Bvps,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Bvps,Units 1 & 2 L-98-157, Special Rept:On 980423,inoperability of Seismic Monitoring Instrument Noted.Caused by Obsolescence of Instrument & Inability to Obtain Necessary Spare Parts.Design Change Is Being Pursued to Obtain Replacement Product1998-07-29029 July 1998 Special Rept:On 980423,inoperability of Seismic Monitoring Instrument Noted.Caused by Obsolescence of Instrument & Inability to Obtain Necessary Spare Parts.Design Change Is Being Pursued to Obtain Replacement Product L-98-139, Monthly Operating Repts for June 1998 for Bvps,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Bvps,Units 1 & 2 L-98-119, Monthly Operating Repts for Bvps,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for Bvps,Units 1 & 2 1999-09-30
[Table view] |
Text
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Teernone #4m m4ooo
( Nuclear Group. !
P.O Don 4 I t,h.ppinoport PA nonaam October 10, 1989 i ND3MNO:1974 l V j i
L I
Beaver Valley Power Station, Unit No. 2
$' Docket No. 50-412, License No. NPF-73 LER 89-025.00 V
l United States Nuclear Regulatory Commission .
Document Control Desk Washington, DC 20555 i
Gentlemen:- -
In accordance with Appendix A, Beaver Valley Technical -
' Specifications, the following Licensee Event Report is submitted: !
LER 89-025-00, 10 CFR 50.73.a.2.ii.A, " Auxiliary l
~
Feedwater Intra-System Recirculation - Unanalyzed Condition".
I
/
T. P. Noonan General Manager Nuclear Operations cj ;
Attachment.
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8910170118 891olo [
PDR ADOCK 05000412 '
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'J. ; , October 10, 1989 l ND3NNO*1974 i Page two-
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cci Mr. William T. Russell l Regional Administrator tUnited States Nuclear Regulatory Commission J Region.1 ;
475 Allendals Road !
King of Prussia, PA 19406 J i
C. A. Roteck, Ohio Edison '
Mr. Peter Tam, BVPS Licensing Project Manager United States Nuclear Regulatory Commission
-Washington, DC 20555 ,
J. Beall, Nuclear Regulatory Commission, BVPS Senior Resident Inspector j CAPCO Nuclear Projects Coordinator Toledo Edison j INPO Records Center Suite 1500 -
1100 circle 75 Parkway Atlanta, GA 30339 i I
I G. E. Muckle, Factory Mutual Engineering, Pittsburgh ,
I Mr. J. N. Steinmetz, Operating Plant Projects Manager ,
Mid Atlantic Area Westinghouse Electric Corporation Energy Systems Service Division ,
Box 355 Pittsburgh, PA 15230 American Nuclear Insurers c/o'Dottie Sherman, ANI Library !
The Exchange Suite 245' 270 Farmington Avenue Farmington, CT 06032 ,
i Mr. Richard Janat3 Department of Environmental Resources P. O. Box 2063 16th Floor, Fulton Building , !
Harrisburg, PA 1*i120 Director, Safety E'ialuation & Control Virginia Electric & Power Co. ,
P.O. Box 26666 One James River P1.aza -
Richmond, VA 23251 4
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APPROVED DMS NO 3100 4'04 UCENSEE EVENT REPORT (LER) "aa'
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N1We TELEPHONE NuM018I Thomas P. Noonan, General Manager Nuclear Operation 41112 61413 l- l 1121518 COMPLtit ONE Liht F08i E ACM COMPONtNT P AILUht DthCRIDED IN TMit AtPORT 1936 t gay,g Cault tvsit u cou'ONtNY "$%l AC- Mjr0{,1Agg n ,, g7 g , goy,pggg, vggjAC nto,tAggt n
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on 9/10/89 at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, Ope 13tions personnel identified high temperatures on the "B" and "C" Steam Generator (SGB and SGC)
Auxiliary Feedwater (AFW) lines. Pyrometer readings (250 degrees Fahrenheit (F) to 328 F) indicated recirculation within the SGB and SGC AFW lines, apparently the result of AFW check valves not properly seated. Operations personnel initiated a procedure to verify and ccrrect this condition by flushing the AFW line with an AFW pump to reseat the check valves. Due to thermal considerations and potential waterhammer, engineering support was requested prior to performance of this procedure. The train I
"B" hydraulic control valve in the SGB AFW line was closed, at 1640 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.2402e-4 months <br />, to limit the backleakage. Engineering recommended that flushing be performed after the piping was below 200 F. At 2003 hours0.0232 days <br />0.556 hours <br />0.00331 weeks <br />7.621415e-4 months <br />, after the piping temperature was less than 200 F, I the "B" AFW line was flushed for two minutes, reducing the l piping temperature to 85 F and rescating the check valves. A l periodic trend of AFW piping temperature was initiated to verify no further leakage occurred. There were no safety implications as a result of this event. An Engineering evaluation showed that the elevated temperatures would not have impacted the AFW system's ability to perform its design function.
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FActu1V esamt en DOCM1 NUMDEn (H tt h WUMet fl 16) PAGE L38 vtaa "T8[,[, : [,N Be:ver Valley Power Station, Unit 2 0F 1 l510 l o l0 l 4 l1 l2 81 9 0 l215 -
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DESCRIPTION i
on 9/10/89 at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, Operations personnel were notified of an l
unusual oder in the South safeguards Area. Operators investigated '
and found that the odor was the result of the effects of high j temperatures in the "B" and "C" Steam Generator (SGB and SGC)
Auxiliary Feedwater (AFW) lines. The high temperatures were believed to be the result of backleakage past check valves 2FWE-100 and 2FWE-43B. The valves apparently did not resent after an earlier AFW surveillance test. The leakage flowpath was from the "B" Steam Generator AFW line, into the Train "B" AFW header ;
and into the "C" Steam Generator via the Train "B" AFW header.
This was determined via pyrometer readings on the AFW piping. The l-AFW line temperature at the containment penetration for the "B" Steam Generator was measured at 328 degrees Fahrenheit.
Temperatures gradually decreased along this flowpath due to ambient cooling, until at the penetration for the "C" Steam ;
l Generator the temperature was 250 degrees Fahrenheit (see Figure i 1). No backleakage was detected past the check valves into the
( '
Train "A" AFW header or past the "B" Motor Driven Auxiliary Feedwater Pump discharge check valve.
I Operations personnel than began preparations to perform a procedure to verify and correct this condition. This procedure would flush the AFW line, using an AFW pump, and reseat the check
' valves. Due to thermal considerations and potential waterhammer, engineering support was requested prior to performance of this procedure. Engineering recommended that flushing be performed -
after the piping was below 200 F. The hydraulic control valve in the "B" AFW line was closed, at 1640 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.2402e-4 months <br />, to stop the backleakage and allow the piping to cool. This action isolated Train "B" AFW to the "B" Steam Generator and placed the station into the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> Action Statement for Technical Specification 3.7.1.2 (one inoperable train of AFW). Train "B" AFW was still available to the other Steam Generators. Train "A" AFW was l operable and available to all Steam Generators throughout this event.
At 2003 hours0.0232 days <br />0.556 hours <br />0.00331 weeks <br />7.621415e-4 months <br />, after the piping temperature had decreased to below 200 degrees F, the hydraulic control valve was reopened and the station exited Technical Specification 3.7.1.2. The "B" AFW line was flushed using throttled flow, as per procedure, for two minutes. This reduced the maximum piping temperature to 85 F.
Operations personnel then initiated a periodic trend (once every 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />) to monitor the AFW piping temperatures to ensure that the check valves were seated. On 9/11/89, after verification that the AFW piping temperature was steadily decreasing to ambient area temperatures, the periodic trend frequency was decreased to a shiftly frequency.
NRC PoRM 368A *U.S. GPOs 1985.$20-599 000 70 C431 -
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- a " C'u n'." 00.0 Beaver Valley Power Station Unit 2 o l5 jo l0 l0 l 4l1l2 or 8l9 -
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'l The cause for this event was attributed to check valves in the SGB AFW line (2FWE-100: Walworth Co. Model 5350 WE valve, and 2FWE-43B: Atwood & Morrill Co. Inc. Model 1350-16H valve) which
'were not properly seated, allowing main feedwater flow into the ~
AFW piping. After flushing, the check valves reseated a.nd the leakage was eliminated. Work requests have been initiated to inspect these valves and perform any necessary corrective actions.
CORRECTIVE ACTIONS The following corrective actions have been or will be taken as a result of this event:
- 1. The hydraulic control valve for the SGB AFW line was closed to limit the backleakage in the piping.
- 2. Operations personnel performed procedure OM 2.24.4Q, to flush the SGB AFW line and reseat the check valves. '
- 3. A periodic trend was initiated to monitor AFW piping '
temperatures. i
- 4. Maintenance Work Requests were generated to inspect and repair the SGB AFW check valves (2FWE-100 and 2FWE-43B).
- 5. AFW piping temperatures are currently monitored at the ,
Auxiliary Feedwater Pumps to check for steam binding of the pumps. This practice will be revised to monitor the temperatures near the AFW containment penetrations. This will identify both steam binding and/or intra-system recirculation.
- 6. This event will be. included in the Operator Licensed Retraining Sessions and in the Technical Personnel Training for Testing personnel.
SAFETY IMPLICATIONS There were no safety implications as a result of this event. An Engineering evaluation of this event indicated that the high temperatures experienced by the AFW piping had no detrimental effects.
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0l 0 0l4 0F 0 l5 isxt w -e w a nea.< anaw unc r.m. snuw on REPORTABILITY This event was determined to be reportable in accordance with the requirement of 10CFR50.73.a.2.ii.A, as an unanalyzed condition.
An Engineering evaluation determined that plant safety was not significantly compromised, therefore this event was not reported in accordance with 10CFR50.72.b.ii.A.
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