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| number = ML16027A147
| number = ML16027A147
| issue date = 01/27/2016
| issue date = 01/27/2016
| title = Turkey Point Nuclear Generating Station - NRC Integrated Inspection Report 05000250/2015004, 05000251/2015004, October 1, 2015 to December 31, 2015
| title = NRC Integrated Inspection Report 05000250/2015004, 05000251/2015004, October 1, 2015 to December 31, 2015
| author name = Suggs L B
| author name = Suggs L
| author affiliation = NRC/RGN-II/DRP/RPB3
| author affiliation = NRC/RGN-II/DRP/RPB3
| addressee name = Nazar M
| addressee name = Nazar M
Line 14: Line 14:
| page count = 43
| page count = 43
}}
}}
See also: [[followed by::IR 05000250/2015004]]
See also: [[see also::IR 05000250/2015004]]


=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION  
{{#Wiki_filter:UNITED STATES
REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257
                                NUCLEAR REGULATORY COMMISSION
  January 27, 2016  
                                                REGION II
 
                            245 PEACHTREE CENTER AVENUE NE, SUITE 1200
Mr. Mano Nazar
                                      ATLANTA, GEORGIA 30303-1257
President and Chief Nuclear Officer  
                                          January 27, 2016
Mr. Mano Nazar
President and Chief Nuclear Officer
  Nuclear Division
NextEra Energy
P.O. Box 14000
Juno Beach, FL 33408-0420
SUBJECT: TURKEY POINT NUCLEAR GENERATING STATION - NRC INTEGRATED
              INSPECTION REPORT 05000250/2015004, 05000251/2015004
Dear Mr. Nazar:
On December 31, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an
inspection at your Turkey Point Nuclear Generating Station Units 3 and 4. On January 15,
2016, the NRC inspectors discussed the results of the inspection with Mr. Tom Summers and
other members of your staff. The inspectors documented the results of this inspection in the
enclosed inspection report.
NRC inspectors documented one self-revealing finding of very low safety significance (Green) in
this report. The finding involved a violation of NRC requirements. The NRC is treating this
violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement
Policy.
If you contest the violations or significance of these NCVs, you should provide a response within
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with
copies to the Regional Administrator Region II; the Director, Office of Enforcement, U.S. Nuclear
Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at
Turkey Point Nuclear Generating Station Units 3 and 4.
If you disagree with a cross-cutting aspect assignment, you should provide a response within 30
days of the date of this inspection report, with the basis for your disagreement, to the Regional
Administrator, Region II; and the NRC resident inspector at the Turkey Point Nuclear
Generating Station Units 3 and 4.


  Nuclear Division  
M. Nazar                                    2
NextEra Energy P.O. Box 14000 Juno Beach, FL  33408-0420
In accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections,
Exemptions, Requests for Withholding, of the NRCs Rules of Practice, a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
NRCs Public Document Room or from the Publicly Available Records (PARS) component of the
NRCs Agency wide Documents Access and Management System (ADAMS). ADAMS is
accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public
Electronic Reading Room).
                                            Sincerely,
                                            /RA/
                                            LaDonna B. Suggs, Chief
                                            Reactor Projects Branch 3
                                            Division of Reactor Projects
Docket Nos.: 50-250, 50-251
License Nos.: DPR-31, DPR-41
Enclosure:
IR 05000250/2015004, 05000251/2015004
  w/Attachment: Supplementary Information
cc Distribution via ListServ


SUBJECT: TURKEY POINT NUCLEAR GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000250/2015004, 05000251/2015004
Dear Mr. Nazar:


   
  ML16027A147                SUNSI REVIEW COMPLETE      FORM 665 ATTACHED
On December 31, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an
OFFICE                RII:DRP      RII:DRP        RII:DRS        RII:DRS        RII:DRS        RII:DRS      RII:DRS
inspection at your Turkey Point Nuclear Generating Station Units 3 and 4. On January 15, 2016, the NRC inspectors discussed the results of the inspection with Mr. Tom Summers and other members of your staff. The inspectors documented the results of this inspection in the
SIGNATURE          TLH4 via email MXE2 via email MAB7 via email REW1 via email  RXK3 /RA for/      RXK3    PGC1 via email
enclosed inspection report.
NAME                    THoeg      MEndress        MBates        RWilliams      BPursley        RKellner    PCapehart
DATE                  1/26/2016    1/26/2016      1/25/2016      1/26/2016      1/26/2016      1/26/2016    1/25/2016
E-MAIL COPY?        YES      NO  YES      NO    YES      NO    YES      NO    YES      NO    YES      NO  YES      NO
OFFICE                RII:DRP      RII:DRS        RII:DRS
SIGNATURE                LJB4    RXK3 /RA FOR/  CMD4 via email
NAME                  LSuggs        JPanfel        CDykes
DATE                  1/26/2016    1/26/2016      1/26/2016
E-MAIL COPY?        YES NO        YES NO        YES NO
       
M. Nazar                                3
Letter to Mano Nazar from LaDonna B. Suggs January 27, 2016
SUBJECT: TURKEY POINT NUCLEAR GENERATING STATION - NRC INTEGRATED
              INSPECTION REPORT 05000250/2015004, 05000251/2015004
DISTRIBUTION:
S. Price, RII
L. Gibson, RII
OE Mail
RIDSNRRDIRS
PUBLIC
RidsNrrPMTurkeyPoint Resource


   
              U.S. NUCLEAR REGULATORY COMMISSION
NRC inspectors documented one self-revealing finding of very low safety significance (Green) in this report. The finding involved a violation of NRC requirements.  The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement
                                  REGION II
Policy.
Docket Nos: 50-250, 50-251
   
License Nos: DPR-31, DPR-41
If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, U.S. Nuclear
Report Nos: 05000250/2015004, 05000251/2015004
Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at
Licensee:    Florida Power & Light Company (FP&L)
Turkey Point Nuclear Generating Station Units 3 and 4.
Facility:    Turkey Point Nuclear Generating Station, Units 3 & 4
Location:    9760 S. W. 344th Street
            Homestead, FL 33035
Dates:      October 1 to December 31, 2015
Inspectors: T. Hoeg, Senior Resident Inspector
            M. Endress, Resident Inspector
            M. Bates, Senior Operations Engineer
            R. Williams, Senior Reactor Inspector
            B. Pursley, Health Physicist
            C. Dykes, Health Physicist
            J. Panfel, Health Physicist
            B. Kellner, Senior Health Physicist
            P. Capehart, Senior Operations Engineer
Approved by: LaDonna B. Suggs, Chief
            Reactor Projects Branch 3
            Division of Reactor Projects
                                                                  Enclosure


                                              SUMMARY
If you disagree with a cross-cutting aspect assignment, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II; and the NRC resident inspector at the Turkey Point Nuclear
IR 05000250/2015004, 05000251/2015004; 10/01/2015 - 12/31/2015; Turkey Point Nuclear
Generating Station, Units 3 and 4; Refueling Outage & Other Outage Activities.
The report covered a three-month period of inspection by the resident inspectors and specialist
inspectors from the Region II office. One Green non-cited violation (NCV) was identified. The
significance of inspection findings are indicated by their color (i.e., greater than Green, or
Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609,
Significance Determination Process, (SDP) dated April 29, 2015. The cross-cutting aspects
were determined using IMC 0310, Aspects Within the Cross-Cutting Areas, dated December
4, 2014. All violations of NRC requirements were dispositioned in accordance with the NRCs
Enforcement Policy dated February 4, 2015. The NRCs program for overseeing the safe
operation of commercial nuclear power reactors is described in NUREG-1649, Reactor
Oversight Process, Revision 5.
NRC-Identified and Self-Revealing Findings
Cornerstone: Barrier Integrity
    *  Green: A self-revealing NCV of Technical Specification (TS) 6.8.1, Procedures and
        Programs, was identified when the licensee failed to properly implement procedure
        3-PMI-072.6, Steam Dump to Atmosphere Control Loop Calibration. Specifically, the
        licensee incorrectly installed a temporary electrical jumper in reactor operator console
        3C02 instead of 3C04, in contrast to Step 6.3.2 of 3-PMI-072.6. This action resulted in
        actuation of a 3B 4160 volt (V) vital bus lockout circuit causing loss of power to the B
        train of Unit 3 (U3) spent fuel pool (SFP) cooling. Immediate corrective actions were
        taken to remove the jumper and restore the B train of SFP cooling. The licensee
        entered the condition in its corrective action program (CAP) as action request (AR)
        02088911 and 02088914.
        The performance deficiency was determined to be more than minor because it was
        associated with the human performance attribute of the barrier integrity cornerstone and
        adversely affected the cornerstone objective to provide reasonable assurance that
        physical design barriers (fuel cladding, reactor coolant system (RCS), and containment)
        protect the public from radionuclide releases. In addition, the performance deficiency, if
        left uncorrected, had the potential to lead to a more significant safety concern. The
        finding was screened using IMC 0609, Significance Determination Process,
        Attachment 0609.04, Initial Characterization of Findings, Tables 2 and 3, dated July 1,
        2012, and Appendix G Attachment 1, Shutdown Operations Significance Determination
        Process Phase 1 Initial Screening and Characterization of Findings, Exhibit 4 for Barrier
        Integrity, dated May 9, 2014. The inspectors determined the finding was of very low
        safety significance (Green) because it was not associated with low temperature over
        pressurization, freeze seals, steam generator nozzle dams, criticality, drain down or
        leakage paths, or the containment barrier. Furthermore, one train of SFP cooling
        remained in operation, the rate of SFP temperature rise was low (~ 2 °F/hour), and
        additional methods remained available to limit SFP temperature rise. This finding was
        assigned a cross cutting aspect associated with the procedure adherence element of the
        human performance area because the licensee failed to correctly execute step 6.3.2 of
        procedure 3-PMI-072.6 (H.8). (Section 1R20)


Generating Station Units 3 and 4.
                                              3
M. Nazar 2
Licensee-Identified Violations
      Violations of very low safety or security significance or Severity Level IV that were
In accordance with Title 10 of the Code of Federal Regulations 2.390, "Public Inspections, Exemptions, Requests for Withholding," of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the  
      identified by the licensee have been reviewed by the NRC. Corrective actions taken or
NRC's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agency wide Documents Access and M
      planned by the licensee have been entered into the licensees CAP. These violations
anagement System (ADAMS).  ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
       and corrective action tracking numbers are listed in Section 4OA7 of this report.
       Sincerely,
      /RA/ 
      LaDonna B. Suggs, Chief      Reactor Projects Branch 3
      Division of Reactor Projects


                                        REPORT DETAILS
Docket Nos.: 50-250, 50-251 License Nos.: DPR-31, DPR-41
Summary of Plant Status
Unit 3 began this inspection period at 100 percent of Rated Thermal Power (RTP) where it
Enclosure:  
remained until October 19, 2015, when it was shut down for a scheduled refueling outage
IR 05000250/2015004, 05000251/2015004
(RFO). Unit 3 was restarted November 29, 2015, and returned to 100 percent of RTP on
   w/Attachment:  Supplementary Information
December 9, 2015, where it remained through the end of this inspection period.
Unit 4 (U4) began this inspection period at 100 percent of RTP where it remained through the
end of this inspection period.
1.      REACTOR SAFETY
        Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
1R01 Adverse Weather Protection (IP 71111.01)
.1      Readiness for Seasonal Extreme Weather Conditions
  a.    Inspection Scope
        During the month of December, the inspectors reviewed and verified the status of
        actions taken by the licensee for winter readiness prior to the onset of cool weather. The
        inspectors reviewed licensee procedure OP-AA-102-1002, Seasonal Readiness,
        Attachment 7, Cold Weather Readiness Check List, and Attachment 14, Turkey Point
        Site Specific Guidance. The inspectors reviewed system health reports and open CAP
        ARs for the emergency diesel generators (EDGs) and auxiliary feedwater (AFW) pumps
        to determine if any deficiencies existed that could affect operation of equipment
        immersion heaters. The inspectors performed walk downs of systems that could be
        affected by cold weather as outlined in the licensee site specific guidance including the
        following areas:
        *    U3 and U4 EDGs
        *    AFW pumps
        *    U3 and U4 charging pumps
        *    U3 and U4 boric acid storage tanks
b.      Findings
        No findings were identified.
1R04 Equipment Alignment (IP 71111.04)
.1      Partial Equipment Walk Downs (Quarterly)
   a.  Inspection Scope
        The inspectors conducted three partial alignment verifications of the safety-related
        systems listed below. These inspections included reviews using plant lineup
        procedures, operating procedures, and piping and instrumentation drawings, which were


cc Distribution via ListServ
                                              5
      compared with observed equipment configurations to verify that the critical portions of
      the systems were correctly aligned to support operability. The inspectors also verified
      that the licensee had identified and resolved, by entering them in the CAP, equipment
      alignment problems that could cause initiating events or impact the capability of
      mitigating systems or barriers. Documents reviewed are listed in the Attachment. This
      inspection constitutes three samples.
      *    4B EDG while 4A EDG was out of service (OOS)
      *    4A and 4B high head safety injection (HHSI) pumps while 3A and 3B HHSI pumps
          were OOS
      *    3B EDG while 3A EDG was OOS
  b. Findings
      No findings were identified.
1R05 Fire Protection (IP 71111.05)
.1    Fire Area Walk downs
  a. Inspection Scope
      The inspectors walked down the following five plant areas to evaluate conditions related
      to control of transient combustibles, ignition sources, material condition, and operational
      status of fire protection systems including fire barriers used to prevent fire damage and
      propagation. The inspectors reviewed these activities using provisions in the licensees
      procedure 0-ADM-016, Fire Protection Plan and 10 CFR Part 50, Appendix R. The
      inspectors routinely reviewed the licensees fire impairment lists and monitored the
      associated corrective actions for completion. The inspectors reviewed the AR report
      database to verify that fire protection problems were being identified and appropriately
      resolved in the CAP. The inspectors tours of the selected areas verified the fire
      protection equipment was installed as shown on the applicable fire plan drawings and
      appeared functional and ready for usage. This inspection constitutes five samples. The
      following areas were inspected:
      *    U4 Pipe and Valve Room, Fire Zone 030
      *    U3 Containment Building, Fire Zone 060
      *    U4 4B Vital Battery Room, Fire Zone 102
      *    U3 and U4 Mechanical Equipment Room, Fire Zone 097
      *    Auxiliary Building Electrical Equiptment Room, Fire Zone 025
  b. Findings
      No findings were identified.


ML16027A147  SUNSI REVIEW COMPLETE  FORM 665 ATTACHED OFFICE RII:DRP RII:DRP RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS SIGNATURE TLH4 via email MXE2 via email MAB7 via email REW1 via emailRXK3 /RA for/ RXK3 PGC1 via email
                                              6
NAME THoeg MEndress MBates RWilliams BPursley RKellner PCapehart DATE 1/26/2016 1/26/2016 1/25/2016 1/26/2016 1/26/2016 1/26/2016 1/25/2016 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO OFFICE RII:DRP RII:DRS RII:DRS    SIGNATURE LJB4 RXK3 /RA FOR/CMD4 via email    
.2    Fire Protection - Drill Observation
NAME LSuggs JPanfel CDykes    DATE 1/26/2016 1/26/2016 1/26/2016    E-MAIL COPY?    YES NO        YES NO        YES NO         
   a. Inspection Scope
M. Nazar 3
      On December 9, 2015, the inspectors observed an unannounced fire drill that took place
      within the station power block just outside the 3D31/4D31 non vital 125 VDC switchgear
Letter to Mano Nazar from LaDonna B. Suggs January 27, 2016
      room in the turbine building. The drill was observed to evaluate the readiness of the
SUBJECT: TURKEY POINT NUCLEAR GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000250/2015004, 05000251/2015004 
      plant fire brigade to fight fires and the control room to make the proper emergency action
DISTRIBUTION:  
      level (EAL) classification. The inspectors verified that the licensee staff identified
S. Price, RII 
      deficiencies, openly discussed them in a self-critical manner at the drill debrief meeting,
L. Gibson, RII  OE Mail 
      and took appropriate corrective actions as required. Specific attributes evaluated were:
RIDSNRRDIRS
      *  Proper wearing of fire protective gear and self-contained breathing apparatus
      *  Proper use and layout of fire hoses
      *  Employment of appropriate fire-fighting techniques
      *  Sufficient fire-fighting equipment brought to the scene
      *  Effectiveness of command and control
      *  Search for victims and propagation of the fire into other plant areas
      *  Smoke removal operations
      *  Utilization of pre-planned strategies
      *  Adherence to the pre-planned drill scenario
      *  Drill objective
      The inspectors also observed the placement and charging of the fire hoses used to
      simulate extinguishing the fire.
  b. Findings
      No findings were identified.
1R08 Inservice Inspection Activities (IP 71111.08)
  a. Inspection Scope
      Non-Destructive Examination Activities and Welding Activities
      From October 26-29, 2015, the inspectors conducted an onsite review of the
      implementation of the licensees inservice inspection (ISI) program for monitoring
      degradation of the RCS boundary, risk-significant piping and component boundaries,
      and containment boundaries in U3.
      The inspectors either directly observed or reviewed the following non-destructive
      examinations (NDEs) mandated by the American Society of Mechanical Engineers
      (ASME) Boiler and Pressure Vessel Code (Code of Record: 2007 Edition with 2008
      Addenda) to evaluate compliance with the ASME Code, Section XI and Section V
      requirements, and if any indications or defects were detected, to evaluate if they were
      dispositioned in accordance with the ASME Code or an NRC-approved alternative
      requirement. The inspectors also reviewed the qualifications of the NDE technicians
      performing the examinations, to determine whether they were current and in compliance
      with the ASME Code requirements.


PUBLIC
                                        7
RidsNrrPMTurkeyPoint Resource
*    Ultrasonic Examination of Loop B 18-inch Feedwater Nozzle-to-Pipe weld,
 
    Augmented Examination (observed)
Enclosure
*    Ultrasonic Examination (UT) of Loop B 14-inch Feedwater Pipe-to-Elbow weld,
U.S. NUCLEAR REGULATORY COMMISSION
    Augmented Examination (observed)
REGION II
*    Visual Examination of the Reactor Pressure Vessel bottom-mounted instrumentation
 
    penetrations (reviewed)
*    Visual Examination (VT-3) of Spring Hanger 3-RCH-27, Class 1 Support (observed)
Docket Nos:  50-250, 50-251
*    VT-3 of Dual Spring Hanger VS-1G-12, Class 1 Support (observed)
The inspectors either directly observed or reviewed the following welding activities,
qualification records, and associated documents in order to evaluate compliance with
procedures and the ASME Code, Section XI and Section IX requirements. Specifically,
the inspectors reviewed the work order (WO), repair and replacement plan, weld data
sheets, welding procedures, procedure qualification records, welder performance
qualification records, and NDE reports.
*    WO 4030098001, Repair of PZR HTR Sleeve #11, Class 1 (reviewed)
*    WO 4029647301, Valve 3-298C Replace Valve, Class 2 (reviewed)
During non-destructive surface and volumetric examinations performed since the
previous RFO, the licensee did not identify any relevant indications that were analytically
evaluated and accepted for continued service; therefore, no NRC review was completed
for this inspection procedure (IP) attribute.
Pressurized Water Reactor Vessel Upper Head Penetration Inspection Activities
The inspectors verified that for the U3 vessel head, a bare metal visual examination and
a volumetric examination were not required during this outage, in accordance with the
requirements of ASME Code Case N-729-1 and 10 CFR 50.55a(g)(6)(ii)(D).
The licensee did not identify any relevant indications that were accepted for continued
service. Additionally, the licensee did not perform any welding repairs to the vessel
head penetrations since the beginning of the last U3 RFO; therefore, no NRC review
was completed for these IP attributes.
Boric Acid Corrosion Control Inspection Activities
The inspectors reviewed the licensees boric acid corrosion control program activities to
determine if the activities were implemented in accordance with the commitments made
in response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor
Pressure Boundary Components in PWR Plants, and applicable industry guidance
documents. Specifically, the inspectors performed an onsite records review of
procedures, and the results of the licensees containment walkdown inspections
performed during the current RFO. The inspectors also interviewed the Boric Acid
Corrosion Control (BACC) program owner, conducted an independent walkdown of
containment to evaluate compliance with licensees BACC program requirements, and
verified that degraded or non-conforming conditions, such as boric acid leaks, were
properly identified and corrected in accordance with the licensees BACC and CAP.


                                          8
License Nos:  DPR-31, DPR-41
  The inspectors reviewed the following engineering evaluations, completed for evidence
  of boric acid leakage, to determine if the licensee properly applied applicable corrosion
  rates to the affected components; and properly assessed the effects of corrosion
Report Nos:  05000250/2015004, 05000251/2015004
  induced wastage on structural or pressure boundary integrity in accordance with the
  licensee procedures.
  *  AR 02014343, Boric Acid Evaluation
  *  AR 02021132, Boric Acid Evaluation
  *  AR 02025309, Boric Acid Evaluation
  *  AR 02038045, Boric Acid Evaluation
  The inspectors reviewed the following condition reports (CRs) and associated corrective
  actions related to evidence of boric acid leakage, to evaluate if the corrective actions
  completed were consistent with the requirements of the ASME Code and 10 CFR Part
  50, Appendix B, Criterion XVI.
  *  AR 02086287, CV-3-2819 has corrosion on electrical connection
  *  AR 02086292, MOV-3-866B inactive minor dry white boric acid at packing
  *  AR 02086231, 3-309D inactive minor dry white boric acid at packing
  *  AR 02086226, 3-306B inactive minor dry white boric acid at packing
  *  AR 02086218, 3-120G inactive dry white boric acid at D/S pipe cap
  *  AR 02086240, 3-572 inactive dry white boric acid at packing
  *  AR 02086239, 3-542, inactive dry white boric acid at packing
  Steam Generator Tube Inspection Activities
  The inspectors verified that for the U3 steam generator tubes, no inspection activities
  were required this RFO, in accordance with the requirements of the ASME Code, the
  licensees TS, and Nuclear Energy Institute (NEI) 97-06, Steam Generator Program
  Guidelines.
  Identification and Resolution of Problems
  The inspectors reviewed a sample of ISI-related issues entered into the CAP to
  determine if the licensee had appropriately described the scope of the problem, and
  had initiated corrective actions. The review also included the licensees consideration
  and assessment of operating experience events applicable to the plant. The inspectors
  performed this review to ensure compliance with 10 CFR Part 50, Appendix B, Criterion
  XVI, Corrective Action, requirements.
b. Findings
  No findings were identified.


  Licensee: Florida Power & Light Company (FP&L)  
                                              9
1R11 Licensed Operator Requalification Program (IP 71111.11)
.1    Licensed Operator Requalification Exam
  a. Inspection Scope
      Annual Review of Licensee Requalification Examination Results: On December 30,
      2015, the licensee completed the annual requalification operating examinations required
      to be administered to all licensed operators in accordance with 10 CFR 55.59(a)(2). The
      inspectors performed an in-office review of the overall pass/fail results of the individual
      operating examinations and the crew simulator operating examinations in accordance
      with IP 71111.11, Licensed Operator Requalification Program. These results were
      compared to the thresholds established in Section 3.02, Requalification Examination
      Results, of IP 71111.11.
  b. Findings
      No findings were identified.
.2    Resident Inspector Quarterly Review
  a. Inspection Scope
      The inspectors performed the following inspection sample of a simulator observation and
      assessed licensed operator performance while training. These observations included
      procedural use and adherence, response to alarms, communications, command and
      control, and coordination and control of the reactor plant operations.
      On October 8, 2015, the inspectors assessed licensed operator performance in the
      plant-specific simulator during a training evolution. The training scenario was started
      with the unit in Mode 1 at 100 percent power and included a fire lasting greater than 15
      minutes, a loss of reactor coolant accident (LOCA), a reactor trip, a safety injection, a
      residual heat removal (RHR) pump seal failure, and a radiological release to the
      environment.
      During this simulator observation, the simulator board configurations were compared
      with actual plant control board configurations reflecting recent plant changes or
      modifications. The inspectors specifically evaluated the following attributes related to
      operating crew performance and the licensee evaluation:
      *  Clarity and formality of communication
      *  Ability to take timely action to safely control the unit
      *  Prioritization, interpretation, and verification of alarms
      *  Correct use and implementation of off-normal and emergency operating procedures
          and emergency plan implementing procedures
      *  Control board operation and manipulation, including high-risk operator actions
      *  Oversight and direction provided by shift supervisor, including ability to identify and
          implement appropriate TS actions and emergency plan classification and notification
      *  Crew overall performance and interactions
      *  Evaluators control of the scenario and post scenario evaluation of crew performance


                                              10
  b. Findings
Facility:  Turkey Point Nuclear Generating Station, Units 3 & 4
      No findings were identified.
 
.3   Control Room Observations
Location:  9760 S. W. 344th Street
  a. Inspection Scope
Homestead, FL 33035
      The inspectors performed daily assessments of licensed operators in the control room
      during their performance of routine operations. These observations included daily
Dates:  October 1 to December 31, 2015 
      surveillance testing, log keeping, response to alarms, communications, shift turnovers,
      and coordination of plant activities. These observations were conducted to verify
      operator compliance with station operating guidelines, such as use of procedures,
Inspectors:  T. Hoeg, Senior Resident Inspector
      control and manipulation of components, and communications. The inspectors also
  M. Endress, Resident Inspector    M. Bates, Senior Operations Engineer    R. Williams, Senior Reactor Inspector
      performed the following three focused control room observations during reactivity
  B. Pursley, Health Physicist
      manipulations and Mode changes:
  C. Dykes, Health Physicist
      On November 19, 2015, the inspectors performed a focused observation on U4
  J. Panfel, Health Physicist
      consisting of a RCS primary water dilution per 0-OP-046, Enclosure 6, Chemical
  B. Kellner, Senior Health Physicist    P. Capehart, Senior Operations Engineer
      Volume Control System Boron Concentration Control. Specifically, the inspectors
   
      observed the reactor operators performance of the pre-job brief per 0-ADM-200,
Approved by: LaDonna B. Suggs, Chief
      Attachment 7, Planned Reactivity Manipulations for Maintaining Steady State Plant
  Reactor Projects Branch 3    Division of Reactor Projects 
      Conditions and verified the operators complied with the applicable procedure during the
 
      evolution.
  SUMMARY  IR 05000250/2015004, 05000251/2015004; 10/01/2015 - 12/31/2015; Turkey Point Nuclear
      On December 1, 2015 and December 2, 2015, the inspectors performed a focused
Generating Station, Units 3 and 4; Refueling Outage & Other Outage Activities.
      observation in the U3 control room during low power physics testing in accordance with
      procedure 0-OSP-040.19, Low Power Physics Testing. The inspectors observed the
The report covered a three-month period of inspection by the resident inspectors and specialist
      pre-evolution operating crew brief, control rod movements, monitoring of subcritical
inspectors from the Region II office.  One Green non-cited violation (NCV) was identified.  The
      multiplication, and data collection.
significance of inspection findings are indicated by their color (i.e., greater than Green, or
      On December 3, 2015, the inspectors performed a focused observation on U3 during a
Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," (SDP) dated April 29, 2015.  The cross-cutting aspects were determined using IMC 0310, "Aspects Within the Cross-Cutting Areas," dated December
      reactor startup per procedure 3-GOP-301, Hot Standby to Power Operations. The
4, 2014.  All violations of NRC requirements were
      inspectors reviewed the expected critical boron concentration calculation and the control
dispositioned in accordance with the NRC's
      rod pull sequence plan used during the observed reactor startup. The inspectors
Enforcement Policy dated February 4, 2015. The NRC's program for overseeing the safe
      reviewed the recorded reactor startup physics data to ensure it was as calculated by the
operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 5.
      licensee reactor engineering staff.
NRC-Identified and Self-Revealing Findings 
      This inspection constitutes three samples. The inspectors focused on the following
      conduct of operations attributes as appropriate:
Cornerstone:  Barrier Integrity 
      *  Operator compliance and use of procedures
* Green:  A self-revealing NCV of Technical Specification (TS) 6.8.1, "Procedures and Programs," was identified when the licensee failed to properly implement procedure 3-PMI-072.6, "Steam Dump to Atmosphere Control Loop Calibration."  Specifically, the  
      *  Control board manipulations
licensee incorrectly installed a temporary electrical jumper in reactor operator console
      *  Communication between crew members
3C02 instead of 3C04, in contrast to Step 6.3.2 of 3-PMI-072.6.  This action resulted in
      *  Use and interpretation of plant instruments, indications and alarms
actuation of a 3B 4160 volt (V) vital bus lockout circuit causing loss of power to the B
      *  Use of human error prevention techniques
train of Unit 3 (U3) spent fuel pool (SFP) cooling.  Immediate corrective actions were taken to remove the jumper and restore the B train of SFP cooling.  The licensee entered the condition in its corrective action program (CAP) as action request (AR)
      *  Documentation of activities, including initials and sign-offs in procedures
      *  Supervision of activities, including risk and reactivity management


02088911 and 02088914.  
                                              11
    b. Findings
      No findings were identified.
.4    Biennial Requalification
    a. Inspection Scope
      The inspectors reviewed the facility operating history and associated documents in
      preparation for this inspection. During the weeks of November 30, 2015 through
      December 21, 2015, the inspectors reviewed documentation associated with the
      licensees operator requalification program biennial written examinations. The activity
      performed by the inspectors was conducted to assess the licensees effectiveness in
      implementing requalification requirements identified in 10 CFR Part 55, Operators
      Licenses. The evaluations were also performed to determine if the licensee effectively
      implemented operator requalification guidelines established in NUREG-1021, Operator
      Licensing Examination Standards for Power Reactors, and IP 71111.11, Licensed
      Operator Requalification Program. Documentation reviewed included two biennial
      written examinations. The records were inspected using the criteria listed in IP
      71111.11. Documents reviewed during the inspection are documented in the List of
      Documents Reviewed.
      The sample is now complete because the remainder of this sample was previously
      inspected and documented in the third quarter integrated inspection report
      (05000250&251/2015003).
    b. Findings
      No findings were identified.
1R12  Maintenance Effectiveness (IP 71111.12)
    a. Inspection Scope
      The inspectors reviewed known equipment problems associated with the U3 steam
      generator steam flow module FM-3-474D affecting the maintenance rule program and
      equipment performance history trends associated with the equipment. Specifically, the
      inspectors reviewed AR 02081538.
      The inspectors reviewed the licensees activities to meet the requirements of 10 CFR
      50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power
      Plants, and licensee procedure NAP-415, Maintenance Rule Program Administration.
      The inspectors focused on maintenance rule scoping, characterization of maintenance
      problems and failed components, risk significance, determination of a(1) or a(2)
      performance criteria classification, corrective actions, and the appropriateness of
      established performance goals and monitoring criteria. The inspectors also interviewed
      responsible engineers and observed or reviewed corrective maintenance activities. The
      inspectors verified that equipment problems were being identified and appropriately
      entered into the licensees CAP. The inspectors used the licensee maintenance rule


   
                                            12
The performance deficiency was determined to be more than minor because it was associated with the human performance attribute of the barrier integrity cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that
    database, system health reports, maintenance rule unavailability status reports, and the
physical design barriers (fuel cladding, reactor coolant system (RCS), and containment) protect the public from radionuclide releases.  In addition, the performance deficiency, if
    CAP as sources of information on tracking and resolution of issues. This inspection
left uncorrected, had the potential to lead to a more significant safety concern. The  
    constitutes one sample.
finding was screened using IMC 0609, "Significance Determination Process," Attachment 0609.04, "Initial Characterization of Findings," Tables 2 and 3, dated July 1, 2012, and Appendix G Attachment 1, "Shutdown Operations Significance Determination
    *  U3 FM-3-474D Flow Module Bias Potentiometer
Process Phase 1 Initial Screening and Characterization of Findings," Exhibit 4 for Barrier
b. Findings
Integrity, dated May 9, 2014.  The inspectors determined the finding was of very low
    No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (IP 71111.13)
a.  Inspection Scope
    The inspectors completed in-office reviews and control room inspections of the
    licensees risk assessment of five emergent or planned maintenance activities. The
    inspectors verified the licensees risk assessment and risk management activities using
    the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management
    and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of
    Maintenance at Nuclear Power Plants, Revision 3; and procedures 0-ADM-068, Work
    Week Management; WM-AA-1000, Work Activity Risk Management; and 0-ADM-225,
    On Line Risk Assessment and Management. The inspectors also reviewed the
    effectiveness of the licensees contingency actions to mitigate increased risk resulting
    from the degraded equipment and the licensee is assessment of aggregate risk using
    procedure OP-AA-104-1007, Online Aggregate Risk. The inspectors discussed the on-
    line risk monitor (OLRM) results with the control room operators and verified all
    applicable OOS equipment was included in the OLRM calculation. The inspectors
    evaluated the following five risk assessment samples during the inspection period:
    *  U3 3A 4kV Bus, U3 Startup Transformer (SUT), and 3A and 3B HHSI pumps OOS
    *  U3 3A 4kV Bus, U3 SUT, and 3D Vital 480V Motor Control Cabinet (MCC) OOS
    *  U3 3-312A Valve Inspection and Repair with Freeze Seal (WO 40411630)
    *  U3 SUT OOS, U3 3A Sequencer OOS, and 3A and 3B EDGs Running
    *  U3 Train 2 AFW, U4 Train 2 AFW, and U3 3B Emergency Containment Cooler OOS
b.  Findings
    No findings were identified.
1R15 Operability Determinations and Functionality Assessments (IP 71111.15)
aInspection Scope
    The inspectors evaluated the technical adequacy of the licensee evaluations to ensure
    that TS operability was properly justified and the subject component or system remained
    available such that no unrecognized increase in risk occurred for the five operability
    evaluations described in the ARs listed below. The inspectors reviewed applicable
    sections of the updated Final Safety Anaylsis Report (UFSAR) to determine if the system
    or component remained available to perform its intended function. In addition, when
    applicable, the inspectors reviewed compensatory measures implemented to verify that


safety significance (Green) because it was not associated with low temperature over pressurization, freeze seals, steam generator nozzle dams, criticality, drain down or leakage paths, or the containment barrier. Furthermore, one train of SFP cooling
                                          13
remained in operation, the rate of SFP temperature rise was low (~ 2 °F/hour), and  
    the affected equipment remained capable of performing its intended design function.
additional methods remained available to limit SFP temperature riseThis finding was
    The inspectors also reviewed a sampling of CRs to verify that the licensee routinely
assigned a cross cutting aspect associated with the procedure adherence element of the human performance area because the licensee failed to correctly execute step 6.3.2 of procedure 3-PMI-072.6 (H.8).  (Section 1R20)
    identifed and corrected any deficiencies associated with operability evaluations. This
3    Licensee-Identified Violations
    inspection constitutes five samples.
Violations of very low safety or security significance or Severity Level IV that were identified by the licensee have been reviewed by the NRC. Corrective actions taken or
    *  AR 02083336, U3 RHR Gas Voids
planned by the licensee have been entered into the licensee's CAP. These violations
    *  AR 02082853, Pressurizer Steam Sample Line Containment Isolation Valve (CV-4-
and corrective action tracking numbers are listed in Section 4OA7 of this report.
        951) OOS
    
    *  AR 02053124, 3B EDG Oil Leak
   REPORT DETAILS Summary of Plant Status
    *  AR 02086176, 3A FT-3-414 Bent and Unsupported
   
    *  AR 02093957, 4B EDG TS-4-6132 Broken
Unit 3 began this inspection period at 100 percent of Rated Thermal Power (RTP) where it remained until October 19, 2015, when it was shut down for a scheduled refueling outage
bFindings
(RFO)Unit 3 was restarted November 29, 2015, and returned to 100 percent of RTP on
    No findings were identified.
December 9, 2015, where it remained through the end of this inspection period.  
1R18 Plant Modifications (IP 71111.18)
    Permanent Plant Modifications
aInspection Scope
    The inspectors reviewed the following two permanent plant modifications. The
    inspectors reviewed the 10 CFR 50.59 screening and technical evaluation to verify that
    the modifications had not affected system operability or availability. The inspectors
    reviewed associated plant drawings, design analyses, and UFSAR documents impacted
    by these modifications and discussed the changes with licensee personnel to verify that
    the modifications were consistent with the WO and associated documents. The
    inspectors observed portions of the modifications and surrounding areas to determine if
    conditions resulted in any potential unsafe conditions not described in the engineering
    change documentation. Additionally, the inspectors reviewed and verified that any
    conditions associated with the modifications were being identified and entered into the
    CAP. This inspection constitutes two samples.
    *   EC 280399, U3 Reactor Coolant Pump (RCP) Seal Replacmement Modification
    *   EC 285012, FT-4-494 U4 Steam Generator C Steam Flow Detector Line
        Replacement
  b.  Findings
    No findings were identified.
1R19 Post Maintenance Testing (IP 71111.19)
a.  Inspection Scope
    For the five post maintenance tests and associated WOs listed below, the inspectors
    reviewed the test procedures and either witnessed the testing or reviewed test records to
    determine whether the scope of testing adequately verified that the work performed was
    completed satisfactorily and demonstrated that the affected equipment was operable.


                                            14
Unit 4 (U4) began this inspection period at 100 percent of RTP where it remained through the end of this inspection period.  
      The inspectors verified that the requirements in licensee procedure 0-ADM-737, Post
      Maintenance Testing, were incorporated into the test requirements. The inspectors
1. REACTOR SAFETY
      reviewed the following WOs consisting of five inspection samples:
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity 
      *  WO 40281614, U3 Pressurizer Pressure Operated Relief Valve PCV-3-455C
      *  WO 40419666, U4 Steam Generator C Steam Flow Detector FT-4-494
      *  WO 40371127, 3B Containment Spray Pump Check Valve Inspection
      *  WO 40419961, Reactor Protection System 3-P7-1-B Relay Replacement
      *  WO 40161059, 3B50 Load Center Relay Replacements
  b. Findings
      No findings were identified.
1R20 Refueling and Other Outage Activities (IP 71111.20)
.1    Unit 3 Refueling Outage PT3-28 (one sample)
  a. Inspection Scope
      Outage Planning, Control and Risk Assessment
      During daily outage planning activities by the licensee, the inspectors reviewed the risk
      reduction methodology employed by the licensee during RFO PT3-28 meetings including
      outage control center (OCC) morning meetings, operations daily team meetings, and
      schedule performance update meetings. The inspectors examined the licensee
      implementation of shutdown safety assessments during PT3-28 in accordance with
      administrative procedure ADM-051, Outage Risk Assessment and Control, to verify if a
      defense in depth concept was in place to ensure safe operations and avoid unnecessary
      risk. In addition, the inspectors regularly monitored outage planning and control
      activities in the OCC, and interviewed responsible OCC management personnel during
      the outage to ensure system, structure, and component configurations, and work scope
      were consistent with TS requirements, site procedures, and outage risk controls.
      Monitoring of Shutdown Activities
      The inspectors performed walk downs of important systems and components used for
      RHR from the reactor core and SFP during the shutdown period, including the intake
      cooling water system, component cooling water (CCW) system, and SFP cooling
      system.
      Outage Activities
      The inspectors examined outage activities to verify that they were conducted in
      accordance with TS, licensee procedures, and the licensees outage risk control plan.
      Some of the more significant inspection activities accomplished by the inspectors were
      as follows:


1R01 Adverse Weather Protection (IP 71111.01)  
                                            15
  *  Walked down selected safety-related equipment clearance orders
.1 Readiness for Seasonal Extreme Weather Conditions
  *  Verified operability of RCS pressure, level, flow, and temperature instruments during
   a. Inspection Scope
      various modes of operation
  During the month of December, the inspectors reviewed and verified the status of
  *  Verified electrical systems availability and alignment
actions taken by the licensee for winter readiness prior to the onset of cool weather. The  
  *  Verified shutdown cooling system and SFP cooling system operation
inspectors reviewed licensee procedure OP-AA-102-1002, "Seasonal Readiness,"
  *  Evaluated implementation of reactivity controls
Attachment 7, "Cold Weather Readiness Check List," and Attachment 14, "Turkey Point Site Specific Guidance.The inspectors reviewed system health reports and open CAP ARs for the emergency diesel generators (E
  *  Reviewed control of containment penetrations
DGs) and auxiliary feedwater (AFW) pumps to determine if any deficiencies existed that could affect operation of equipment immersion heaters. The inspectors performed walk downs of systems that could be
  *  Examined foreign material exclusion (FME) controls put in place inside containment
affected by cold weather as outlined in the licensee site specific guidance including the following areas:
      (e.g., around the refueling cavity, near sensitive equipment and RCS breaches) and
* U3 and U4 EDGs
      around the SFP
* AFW pumps
  *  Observed fuel loading and unloading in the SFP and in containment
* U3 and U4 charging pumps 
  Monitoring of Plant Heat up and Containment Closure Activities
* U3 and U4 boric acid storage tanks       
  The inspectors examined the applicable TS, license conditions, and verified
b. Findings
  administrative prerequisites were being met prior to reactor plant mode changes. The
  inspectors reviewed measured RCS leak rates, and verified containment integrity was
No findings were identified.  
   properly established. The inspectors performed a containment closeout inspection prior
  to the reactor plant startup to verify no evidence of leakage or debris were left in
  containment that could affect plant operations.
  Reactor Startup and Mode Changes
  On December 2, 2015, the inspectors observed the U3 reactor startup and turbine
  synchronization to the electrical grid and associated Mode changes. The inspectors
  reviewed the recorded reactor startup physics data in order to determine it was as-
  calculated by the licensee reactor engineering staff. The inspectors determined that
  startup and Mode changes were performed in accordance with licensee procedures 0-
  OSP-040.16, Initial Criticality After Refueling Outage and Nuclear Design Verification,
  and 3-GOP-301, Mode 3 to Power Operations.
  Corrective Action Program
  The inspectors reviewed ARs generated during PT3-28 to evaluate the licensees
  threshold for initiating ARs. The inspectors reviewed CRs to verify priorities, Mode
  holds, and significance levels were assigned as required. Resolution and
  implementation of corrective actions of several ARs were also reviewed for
  completeness. The inspectors routinely reviewed the results of site oversight of daily
  surveillances of outage activities.
b. Findings
  Introduction: A Green self-revealing NCV of TS 6.8.1, Procedures and Programs, was
  identified for the licensees failure to correctly execute procedure 3-PMI-072.6, Steam
  Dump to Atmosphere Control Loop Calibration. The failure resulted in actuation of a 3B
  4160 V vital bus lockout circuit causing loss of power to the B train of U3 SFP cooling.
  Description: On November 4, 2015, at 2112 hours, Instrumentation and Controls
  technicians were performing procedure 3-PMI-072.6, Steam Dump to Atmosphere
  Control Loop Calibration, when a temporary electrical jumper was incorrectly installed in


                                        16
1R04 Equipment Alignment (IP 71111.04)
the control room reactor operator console 3C02 instead of 3C04, in contrast to step 6.3.2
.1 Partial Equipment Walk Downs (Quarterly)
of 3-PMI-072.6. At the time of the event, U3 was defueled with all of its fuel temporarily
    a. Inspection Scope
relocated to the SFP. The 3A 4160 V vital bus was de-energized for planned
The inspectors conducted three partial alignment verifications of the safety-related
maintenance and all 480 V vital load centers were powered by the 3B 4160 V vital bus.
systems listed below. These inspections included reviews using plant lineup procedures, operating procedures, and piping and instrumentation drawings, which were
Separate load centers provided power to two separate trains of U3 SFP cooling pumps,
5  compared with observed equipment configurations to verify that the critical portions of the systems were correctly aligned to support operability. The inspectors also verified
and the 3A train pump was powered from Unit 4 electrical switchgear.
that the licensee had identified and resolved, by entering them in the CAP, equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers. Documents reviewed are listed in the Attachment. This
The incorrectly placed jumper actuated a 3B 4160 V vital bus lockout circuit causing all
inspection constitutes three samples.  
associated Unit 3 480 V vital load and motor control centers to de-energize. Numerous
* 4B EDG while 4A EDG was out of service (OOS)
equipment was rendered OOS including the B SFP cooling pump and the 3B CCW
* 4A and 4B high head safety injection (HHSI) pumps while 3A and 3B HHSI pumps
pump. The 3B CCW pump provided cooling to both U3 SFP cooling heat exchangers.
were OOS * 3B EDG while 3A EDG was OOS
Upon loss of the 3B CCW pump, the standby 3C CCW pump started on low pressure as
    b. Findings
designed, providing cooling to the 3A SFP cooling train. Immediate corrective action
  No findings were identified.  
was taken to remove the jumper and restore the B train of SFP cooling. However, the
loss of one train of SFP cooling for approximately four hours caused the SFP
1R05 Fire Protection (IP 71111.05)
temperature to rise from approximately 110 °F to 117 °F. The licensee restored U3 load
and motor control centers at 0207 hours on November 5, 2015, and by 0300 hours the
.1 Fire Area Walk downs
SFP temperature had returned to normal.
    a. Inspection Scope
The licensee entered the condition in its CAP as AR 02088911 and 02088914.
The inspectors walked down the following five plant areas to evaluate conditions related
Corrective actions included site-wide briefings of lessons learned from the event, quality
to control of transient combustibles, ignition sources, material condition, and operational
reviews of procedure 3-PMI-072.6, and enhanced oversight of maintenance activities.
status of fire protection systems including fire barriers used to prevent fire damage and propagation. The inspectors reviewed these activities using provisions in the licensee's procedure 0-ADM-016, "Fire Protection Plan" and 10 CFR Part 50, Appendix R.  The
Analysis: The inspectors determined that the failure to correctly implement maintenance
inspectors routinely reviewed the licensee's fire impairment lists and monitored the
procedure 3-PMI-072.6 was a performance deficiency. The performance deficiency was
associated corrective actions for completion. The inspectors reviewed the AR report
determined to be more than minor because it was associated with the human
database to verify that fire protection problems were being identified and appropriately
performance attribute of the barrier integrity cornerstone and adversely affected the
resolved in the CAP. The inspectors' tours of the selected areas verified the fire protection equipment was installed as shown on the applicable fire plan drawings and appeared functional and ready for usage. This inspection constitutes five samples. The
cornerstone objective to provide reasonable assurance that physical design barriers (fuel
following areas were inspected:
cladding, RCS, and containment) protect the public from radionuclide releases.
Specifically, the licensees failure to correctly execute step 6.3.2 of procedure
3-PMI-072.6 rendered one of two SFP cooling trains OOS, causing the SFP temperature
to rise from approximately 110 °F to 117 °F over a four-hour period. While the
performance deficiency did not directly challenge the integrity of the fuel cladding, if left
uncorrected, the SFP temperature would have continued to increase, potentially
affecting SFP inventory.
The finding was screened using IMC 0609, Significance Determination Process,
Attachment 0609.04, Initial Characterization of Findings, Tables 2 and 3, dated July 1,
2012, and Appendix G Attachment 1, Shutdown Operations Significance Determination
Process Phase 1 Initial Screening and Characterization of Findings, Exhibit 4 for Barrier
Integrity, dated May 9, 2014. The inspectors determined the finding was of very low
safety significance (Green) because it was not associated with low temperature over
pressurization, freeze seals, steam generator nozzle dams, criticality, drain down or
leakage paths, or the containment barrier. Furthermore, one train of SFP cooling
remained in operation, the rate of SFP temperature rise was low (~2 °F/hour), and
additional diverse compensatory methods remained available to limit SFP temperature
rise. This finding was assigned a cross cutting aspect associated with the procedure
adherence element of the human performance area because the licensee failed to
correctly execute step 6.3.2 of procedure 3-PMI-072.6 (H.8).


  * U4 Pipe and Valve Room, Fire Zone 030
                                            17
* U3 Containment Building, Fire Zone 060
    Enforcement: Technical Specification 6.8.1 requires that procedures required by the
* U4 4B Vital Battery Room, Fire Zone 102
    licensees Quality Assurance Topical Report (QATR) be established, implemented, and
* U3 and U4 Mechanical Equipment Room, Fire Zone 097
    maintained. The QATR includes procedures listed in Appendix A of NRC Regulatory
* Auxiliary Building Electrical Equiptment Room, Fire Zone 025
    Guide 1.33, Revision 2, dated February 1978, including procedures for calibrations. The
    b. Findings  
    licensee implements TS 6.8.1 requirements, in part, using procedure 3-PMI-072.6,
  No findings were identified.  
    Steam Dump to Atmosphere Control Loop Calibration. Step 6.3.2 of procedure
    3-PMI-072.6, requires that a jumper be installed in reactor operator console 3C02.
    Contrary to this requirement, on November 4, 2015, at 2112 hours, a maintenance
    technician mistakenly installed a jumper in reactor operator console 3C04. This action
    resulted in actuation of a 3B 4160 V vital bus lockout circuit causing loss of power to the
    B train of U3 SFP cooling. The licensee took immediate corrective action to remove the
    jumper. This violation is being treated as an NCV, consistent with Section 2.3.2 of the
    Enforcement Policy, because it was of very low safety significance and was entered in
    the licensees CAP as AR 02088911 and 02088914. (NCV 05000250/2015004-01,
    Failure to correctly follow procedure 3-PMI-072.6, Steam Dump to Atmosphere Control
    Loop Calibration.)
1R22 Surveillance Testing (IP 71111.22)
a. Inspection Scope
    The inspectors either reviewed or observed the following five surveillance tests to verify
    that the tests met the TS requirements, the UFSAR description, the licensees
    procedural requirements, and demonstrated that systems were capable of performing
    their intended safety functions and operational readiness. In addition, the inspectors
    evaluated the effect of the testing activities on the plant to ensure that conditions were
    adequately addressed by the licensee staff and that after completion of the testing
    activities, equipment was returned to the status required for the system to perform its
    safety function. The inspectors verified that any surveillance deficiencies were
    documented in the licensees CAP. This inspection constitutes two surveillance test
    samples, one inservice testing (IST) sample, and two containment isolation valve leak
    test samples. The inspectors reviewed the following tests:
    Surveillance Test:
    * 0-OSP-059.13, U4 Flux Map
    * 3-OSP-072.5, U3 Main Steam Safey Valve Setpoint Verification
    In-Service Tests:
    * 3-OSP-206.1, Component Cooling Water MOV-3-1418 Valve Test (IST)
    Containment Isolation Valve Test:
    * 3-OSP-051.5, U3 Local Leak Rate Test, Penetration 8 CV-3-951
    * 3-OSP-051.5, U3 Local Leak Rate Test, Penetration 14 CV-3-204
b. Findings
    No findings were identified.


                                              18
 
      Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation (IP 71114.06)
 
.1    Emergency Preparedness Drill
.2 Fire Protection - Drill Observation
  a. Inspection Scope
    a. Inspection Scope  
      On October 8, 2015, the inspectors observed an emergency preparedness drill and the
On December 9, 2015, the inspectors observed an unannounced fire drill that took place
      performance of the licensees emergency response organization. The drill included a
within the station power block just outside the 3D31/4D31 non vital 125 VDC switchgear
      simulated fire in the U4 laydown area, a LOCA inside containment, followed by a RHR
      pump seal failure and radiological release to the environment. The fire, lasting greater
      than 15 minutes, required an unusual event emergency declaration and notification to
      state and local county officials and the NRC per licensee procedure 0-EPIP-20101,
      Duties of the Emergency Coordinator. The scenario progressed to a loss of two RCS
      barriers with the loss or potential loss of a third barrier requiring a general emergency
      declaration and an additional notification. The inspectors observed the crew in the plant
      simulator, including simulated implementation of emergency procedures. The inspectors
      observed the emergency response organization staff in the control room simulator and
      technical support center while they implemented the event classification guidelines and
      emergency response procedures. The inspectors determined that the emergency
      classification and notifications were made in accordance with the licensee emergency
      plan implementing procedure 0-EPIP-20101. The inspectors attended the licensees
      post drill critique, reviewed the licensees critique items, and discussed inspector
      observations with the licensee to verify that drill issues were identified and captured in
      the licensees CAP. This inspection constitutes one sample.
  b. Findings
      No findings were identified.
2.    RADIATION SAFETY (RS)
      Cornerstones: Public Radiation Safety and Occupational Radiaition Safety
2RS1 Radiological Hazard Assessment and Exposure Controls (IP 71124.01)
  a. Inspection Scope
      Hazard Assessment and Instructions to Workers. During facility tours, the inspectors
      directly observed labeling of radioactive material and postings for radiation areas, high
      radiation areas, and airborne radioactivity areas established within the radiologically
      controlled area (RCA) of the U3 containment building, auxiliary building, the Independent
      Spent Fuel Storage Installation (ISFSI), and radioactive waste processing and storage
      locations. The inspectors independently measured radiation dose rates or directly
      observed conduct of licensee radiation surveys for selected RCA areas. The inspectors
      reviewed survey records for several plant areas including surveys for alpha emitters,
      airborne radioactivity, gamma surveys with a range of dose rate gradients, and pre-job
      surveys for upcoming tasks. The inspectors also discussed changes to plant operations
      that could contribute to changing radiological conditions since the last inspection. For
      selected outage jobs, the inspectors attended pre-job briefings and reviewed Radiation


room in the turbine building.  The drill was observed to evaluate the readiness of the plant fire brigade to fight fires and the control room to make the proper emergency action
                                          19
level (EAL) classification. The inspectors verified that the licensee staff identified deficiencies, openly discussed them in a self-critical manner at the drill debrief meeting, and took appropriate corrective actions as required. Specific attributes evaluated were: 
  Work Permit (RWP) details to assess communication of radiological control
* Proper wearing of fire protective gear and self-contained breathing apparatus
  requirements and current radiological conditions to workers.
* Proper use and layout of fire hoses
  Hazard Control and Work Practices. The inspectors evaluated access barrier
* Employment of appropriate fire-fighting techniques
  effectiveness for selected Locked High Radiation Area (LHRA) locations and discussed
* Sufficient fire-fighting equipment brought to the scene
  changes to procedural guidance for LHRA and Very High Radiation Area controls with
* Effectiveness of command and control
  Radiation Protection (RP) supervisors. The inspectors observed and evaluated controls
* Search for victims and propagation of the fire into other plant areas
  for the storage of irradiated material within the SFP. Established radiological controls
* Smoke removal operations
  (including airborne controls) were evaluated for selected U3 RFO 28 (U3R28) tasks
* Utilization of pre-planned strategies
  including RCP seal replacements, reactor cavity decontamination and reactor sump
* Adherence to the pre-planned drill scenario
  demobilization activities. In addition, the inspectors reviewed licensee controls for areas
* Drill objective
  where dose rates could change significantly as a result of plant shutdown and refueling
The inspectors also observed the placement and charging of the fire hoses used to
  operations.
simulate extinguishing the fire.  
  Through direct observations and interviews with licensee staff, the inspectors evaluated
    b. Findings  
  occupational workers adherence to selected RWPs and RP technician proficiency in
No findings were identified.  
  providing job coverage. Electronic dosimeter (ED) alarm set points and worker stay
  times were evaluated against area radiation survey results for selected U3 RFO jobs,
  including the reactor sump demobilization and reactor cavity decontamination. The
  inspectors discussed the use of personnel dosimetry (extremity dosimetry and
  multibadging in high dose rate gradients) with RP staff. The inspectors also evaluated
  worker response to dose and dose rate alarms during selected work activities.
  Control of Radioactive Material. The inspectors observed surveys of material and
  personnel being released from the RCA using small article monitor (SAM), personnel
  contamination monitor (PCM), and portal monitor instruments. As part of IP 71124.05,
  the inspectors reviewed the last two calibration records for selected release point survey
  instruments and discussed equipment sensitivity, alarm setpoints, and release program
  guidance with licensee staff. The inspectors reviewed records of leak tests on selected
  sealed sources and discussed nationally tracked source transactions with licensee staff.
  Problem Identification and Resolution. The inspectors reviewed CAP documents
  associated with radiological hazard assessment and exposure control. The inspectors
  evaluated the licensees ability to identify and resolve the issues in accordance with
  licensee procedures. The inspectors also reviewed recent self-assessment results.
  Radiation protection activities were evaluated against the requirements of the UFSAR
  Section 11; TS Sections 6.8 Procedures and Programs and 6.12 High Radiation Area;
  10 CFR Parts 19 and 20; Regulatory Guide 8.38, Control of Access to High and Very
  High Radiation Areas in Nuclear Power Plants; and approved licensee procedures.
  Licensee programs for monitoring materials and personnel released from the RCA were
  evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of Radioactively
  Contaminated Material. Documents reviewed are listed in the Attachment.
b. Findings
  No findings were identified.


1R08 Inservice Inspection Activities (IP 71111.08)  
                                            20
    a. Inspection Scope  
2RS2 Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls
Non-Destructive Examination Acti
    (IP 71124.02)
vities and Welding Activities
a. Inspection Scope
From October 26-29, 2015, the inspectors conducted an onsite review of the
    Work Planning and Exposure Tracking. The inspectors reviewed work activities and their
implementation of the licensee's inservice inspection (ISI) program for monitoring degradation of the RCS boundary, risk-significant piping and component boundaries,  
    collective exposure estimates for U3 RFO. The inspectors reviewed ALARA planning
and containment boundaries in U3.  
    packages for the following high collective exposure tasks: SG cleaning (including bundle
The inspectors either directly observed or reviewed the following non-destructive
    flushing, sludge lancing, and foreign object search and retrieval); refueling activities;
examinations (NDEs) mandated by the American Society of Mechanical Engineers
    RCP seal replacement; bottom mounted inspection, and; various valve work. For the
(ASME) Boiler and Pressure Vessel Code (Code of Record:  2007 Edition with 2008
    selected tasks, the inspectors reviewed established dose goals and discussed
Addenda) to evaluate compliance with the ASME Code, Section XI and Section V
    assumptions regarding the bases for the current estimates with responsible ALARA
requirements, and if any indications or defects were detected, to evaluate if they were dispositioned in accordance with the ASME Code or an NRC-approved alternative requirement. The inspectors also reviewed the qualifications of the NDE technicians
    planners. The inspectors evaluated the incorporation of exposure reduction initiatives
performing the examinations, to determine whether they were current and in compliance
    and operating experience. Adjustments made to planned doses were also reviewed,
with the ASME Code requirements.
    along with the basis of those adjustments. Post-job reviews from both the current and
7  * Ultrasonic Examination of Loop B 18-inch Feedwater Nozzle-to-Pipe weld, Augmented Examination (observed)
    previous RFO were assessed. Where applicable, the inspectors discussed changes to
* Ultrasonic Examination (UT) of Loop B 14-inch Feedwater Pipe-to-Elbow weld, Augmented Examination (observed)
    established estimates with ALARA planners and evaluated them against work scope
* Visual Examination of the Reactor Pressure Vessel bottom-mounted instrumentation
    changes or unanticipated elevated dose rates.
penetrations (reviewed)
    Source Term Reduction and Control. The inspectors reviewed the collective exposure
* Visual Examination (VT-3) of Spring Hanger 3-RCH-27, Class 1 Support (observed)
    three-year rolling average from 2012-2014 and reviewed historical collective exposure
* VT-3 of Dual Spring Hanger VS-1G-12, Class 1 Support (observed)
    trends. The inspectors evaluated historical dose rate trends and compared them to
The inspectors either directly observed or reviewed the following welding activities,
    current data.
qualification records, and associated documents in order to evaluate compliance with  
    Radiation Worker Performance. In conjunction with IP 71124.01, radiation worker
procedures and the ASME Code, Section XI and Section IX requirements. Specifically,  
    performance was evaluated during several tasks both within containment and the
the inspectors reviewed the work order (WO), repair and replacement plan, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports.  
    auxiliary building. The inspectors specifically evaluated both the use of ALARA briefings
    and remote technologies, including teledosimetry and remote visual monitoring, to
    reduce dose.
    Problem Identification and Resolution. The inspectors reviewed and discussed selected
    CAP documents associated with ALARA program implementation. The inspectors
    evaluated the licensees ability to identify and resolve the issues in accordance with
    licensee procedures. The inspectors also reviewed recent self-assessment results.
    ALARA program activities were evaluated against the requirements of the UFSAR
    Section 11, applicable TS Sections 6.8 and 6.12, 10 CFR Part 20, and approved
    licensee procedure. Records reviewed are listed in the Attachment.
b.  Findings
    No findings were identified.
2RS3 In-Plant Airborne Radioactivity Control and Mitigation (IP 71124.03)
a.  Inspection Scope
    Engineering Controls: Licensee engineering controls used to control and mitigate
    airborne radioactivity were reviewed and discussed. The inspectors evaluated selected
    U3 engineering controls including temporary High Efficiency Particulate Air (HEPA)
    filtration systems for selected outage tasks with the potential for generating airborne


* WO 4030098001, Repair of PZR HTR Sleeve #11, Class 1 (reviewed)
                                      21
* WO 4029647301, Valve 3-298C Replace Valve, Class 2 (reviewed)
activity conditions. The evaluations included procedural guidance, operability testing,
During non-destructive surface and volumetric examinations performed since the
and established configurations during specific outage tasks. In addition, plant guidance
previous RFO, the licensee did not identify any relevant indications that were analytically
and its implementation for the monitoring of potential airborne beta-gamma and alpha-
evaluated and accepted for continued service; therefore, no NRC review was completed for this inspection procedure (IP) attribute.  
emitting radionuclides for outage tasks associated with refueling activities, head
disassembly, and valve maintenance were reviewed and discussed with cognizant
Pressurized Water Reactor Vessel Upper Head Penetration Inspection Activities
licensee representatives.
Use of Respiratory Protection Devices: Program guidance for issuance and use of
The inspectors verified that for the U3 vessel head, a bare metal visual examination and a volumetric examination were not required during this outage, in accordance with the requirements of ASME Code Case N-729-1 and 10 CFR 50.55a(g)(6)(ii)(D).  
respiratory protection devices were reviewed and discussed with responsible licensee
representatives. The inspectors reviewed Total Effective Dose Equivalent (TEDE)
ALARA evaluations conducted for select U3 outage tasks. Use of respiratory protective
equipment was evaluated for selected workers involved in U3 outage activities. The
inspectors toured selected onsite compressors available for supplying breathing air for
current outage activities and reviewed Grade D or greater air certification for permanent
and temporary on-site compressors used for supplied-line breathing air and self-
contained breathing apparatus (SCBA) bottle fill-station activities. Training, fit testing,
and medical qualifications for selected RP, maintenance, and operations using
respiratory protection for outage activities were reviewed and discussed with cognizant
licensee representatives.
Self-Contained Breathing Apparatus for Emergency Use: The inspectors reviewed
current status, operability and availability of select respiratory and SCBA equipment
maintained within the U3 and U4 control rooms, B5B lockers, and U3 and U4 reactor
auxiliary building locations. Maintenance activities for selected respiratory protective
equipment (e.g., compressed gas cylinders, regulators, valves, and hose couplings), by
certified vendor technicians were reviewed for selected SCBA units. Training, fit testing,
and medical qualifications for selected RP, maintenance, and operations staff assigned
Emergency Response Organization duties were reviewed and discussed with cognizant
licensee representatives. For selected U3 and U4 control room operators, the
inspectors discussed and reviewed annual hands-on SCBA training activities, including
donning, doffing, and functionally checking SCBA equipment, bottle change out, and
also reviewed availability of corrective lens, as applicable, for on-shift personnel.
Problem Identification and Resolution: The inspectors reviewed selected CAP
documents within the area of radiological airborne controls and respiratory protection
activities. The inspectors evaluated the licensees ability to identify and resolve the
issues in accordance with licensee procedures PI-AA-104-1000, Corrective Action, Rev.
6, and 0-ADM-533, Corrective Action Program Guidance, Rev. 14. The inspectors also
evaluated the scope of the licensees internal audit program and reviewed recent
assessment results. Specific licensee CAP documents reviewed for airborne
radionuclide concentration monitoring and mitigation are listed in the Attachment.
Radiation Protection program activities associated with airborne radioactivity monitoring
and controls were evaluated against details and requirements documented in the
UFSAR, TS Section 3/4.9.9, Containment Ventilation System, 3/4.9.13, Radiation
Monitoring, and 6.8.1, Procedures and Programs; 10 CFR Part 20, and also approved
licensee procedures. Documents reviewed are listed in the Attachment.
The inspectors completed all specified line-items detailed in IP 71124.03.


   
                                          22
The licensee did not identify any relevant indications that were accepted for continued
  b.  Findings
service. Additionally, the licensee did not perform any welding repairs to the vessel head penetrations since the beginning of the last U3 RFO; therefore, no NRC review was completed for these IP attributes.  
    No findings were identified.
2RS4 Occupational Dose Assessment (IP 71124.04)
Boric Acid Corrosion Control Inspection Activities
a.  Inspection Scope
    The inspector evaluated current RP program guidance and its implementation for
The inspectors reviewed the licensee's boric acid corrosion control program activities to determine if the activities were implemented in accordance with the commitments made in response to NRC Generic Letter 88-05, "Boric Acid Corrosion of Carbon Steel Reactor
    monitoring and assessing occupational workers internal and external radiation
Pressure Boundary Components in PWR Plants," and applicable industry guidance
    exposure. The review included quality assurance activities, results, and responses to
documents. Specifically, the inspectors performed an onsite records review of  
    identified issues; and individual dose results for selected occupational workers.
procedures, and the results of the licensee's containment walkdown inspections
    External Dosimetry: The inspector reviewed and discussed RP program guidance for
performed during the current RFO. The inspectors also interviewed the
    monitoring external and internal radiation exposures of occupational workers. The
  Boric Acid Corrosion Control (BACC) program owner, conducted an independent walkdown of containment to evaluate compliance with licensee's BACC program requirements, and  
    inspector verified National Voluntary Laboratory Accreditation Program certification data
verified that degraded or non-conforming conditions, such as boric acid leaks, were  
    and discussed program guidance for storage, processing and results for dosimeters
properly identified and corrected in accordance with the licensee's BACC and CAP.  
    currently in use. The inspector also reviewed and discussed the comparison between
    ED and thermoluminescent dosimeter data.
    Internal Dosimetry: Program guidance, instrument detection capabilities, and select
    results for assessing internally deposited radionuclides were reviewed and discussed in
    detail. The inspector evaluated licensee follow-up in vivo monitoring results and dose
    assignment for three workers involved in contamination events having the potential for
    internal deposition of radioactive material. In addition, the current licensee and contract
    vendor laboratory analysis capabilities for the collection and analysis of in vitro samples
    were reviewed and discussed in detail.
    Special Dosimetric Situations: The inspector reviewed monitoring conducted and results
    for two declared pregnant workers since the last inspection. The methodology and
    results of monitoring occupational workers within non-uniform external dose fields and
    assignment of effective dose equivalent results were discussed in detail. In addition, the
    adequacy of dosimetry program guidance and its implementation for shallow dose
    assessments and supporting calculations for an individual involved in a select
    contamination event were evaluated. Neutron monitoring guidance and implementation
    for select at power containment entries were reviewed and discussed. RP staff
    proficiency involved in conducting skin dose assessments, neutron monitoring, and
    whole body counter (WBC) operations were evaluated through review and discussions
    of completed records and supporting data.
    Problem Identification and Resolution: The inspectors reviewed and discussed selected
    CAP documents associated with occupational dose assessment. The reviewed items
    included ARs, self-assessments, and quality assurance audit documents. The
    inspectors evaluated the licensees ability to identify, characterize, prioritize, and resolve
    the identified issues in accordance with licensee procedures PI-AA-104-1000, Corrective
    Action, Rev. 6, and 0-ADM-533, Corrective Action Program Guidance, Rev. 14.
    Radiation protection program occupational dose assessment guidance and activities
    were evaluated against the requirements of the UFSAR Section 11; TS Sections 6.8.1,
    Procedures and Programs, and 6.12, High Radiation Area; 10 CFR Parts 19 and 20; and
    approved licensee procedures. Records reviewed are listed in the Attachment.


 
                                            23
The inspectors reviewed the following engineering evaluations, completed for evidence of boric acid leakage, to determine if the licensee properly applied applicable corrosion
    The inspectors completed all specified line-items detailed in IP 71124.04.
rates to the affected components; and properly assessed the effects of corrosion induced wastage on structural or pressure boundary integrity in accordance with the licensee procedures.  
b.  Findings
    No findings were identified.
2RS5 Radiation Monitoring Instrumentation (IP 71124.05)
a.  Inspection Scope
    Radiation Monitoring Instrumentation: During tours of the auxiliary building, turbine
    building, SFP areas, and RCA exit point, the inspectors observed installed radiation
    detection equipment including the following instrument types: area radiation monitors
    (ARMs), airborne monitors, liquid and gaseous effluent monitors, PCMs, SAMs, and
    portal monitors. The inspectors observed the physical location of the components, and
    noted the material condition.
    In addition to equipment walkdowns, the inspectors observed source checks and alarm
    setpoint testing of various portable and fixed detection instruments, including ion
    chambers, telepoles, PCMs, SAMs, and portal monitors. For the portable instruments,
    the inspectors observed the use of a high-range check source and reviewed records of
    periodic output value testing for a calibration source. The inspectors reviewed recent
    calibration records and evaluated alarm setpoint values for selected ARMs, PCMs, portal
    monitors, SAMs, effluent monitors, and a WBC. This included a sampling of instruments
    used for post-accident monitoring such as containment high-range ARMs and effluent
    monitor high-range noble gas and iodine channels. Radioactive sources used to
    calibrate selected ARMs and effluent monitors were evaluated for traceability to national
    standards. Calibration stickers on portable survey instruments and air samplers were
    noted during inspection of storage areas for ready-to-use equipment. The inspectors
    also reviewed countroom quality assurance records for gamma ray spectrometry
    equipment and liquid scintillation detectors.
    Problem Identification and Resolution: Selected licensee CAP documents associated
    with instrumentation were reviewed and assessed. The inspectors evaluated the
    licensees ability to identify and resolve the identified issues in accordance with licensee
    procedures. The inspectors also reviewed recent self-assessment results.
    Operability and reliability of selected radiation detection instruments were reviewed
    against details documented in the following: 10 CFR Part 20; NUREG-0737,
    Clarification of Three Mile Island Action Plan Requirements; TS Section 3; UFSAR
    Chapters 11; and applicable licensee procedures. Documents reviewed during the
    inspection are listed in the Attachment.
b.  Findings
    No findings were identified.


  * AR 02014343, Boric Acid Evaluation
                                            24
* AR 02021132, Boric Acid Evaluation
4OA1 Performance Indicator Verification (IP 71151)
* AR 02025309, Boric Acid Evaluation
.1  Barrier Integrity Cornerstone
* AR 02038045, Boric Acid Evaluation
  a. Inspection Scope
  The inspectors reviewed the following condition reports (CRs) and associated corrective actions related to evidence of boric acid leakage, to evaluate if the corrective actions
      The inspectors reviewed licensee submittals for the U3 and U4 Performance Indicators
completed were consistent with the requirements of the ASME Code and 10 CFR Part
      (PI) listed below for the period October 1, 2014, through September 30, 2015, to verify
50, Appendix B, Criterion XVI.  
      the accuracy of the PI data reported during that period. Performance indicator
      definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance
      Indicator Guideline, and licensee procedure 0-ADM-032, NRC Performance Indicators
      Turkey Point, were used to check the reporting for each data element. The inspectors
      checked operator logs, plant status reports, CRs, system health reports, and PI data
      sheets to verify that the licensee had identified the required data, as applicable. The
      inspectors interviewed licensee personnel associated with PI data collection, evaluation,
      and distribution. This inspection constitutes four samples.
      *   U3 Mitigating Systems PIs
      *   U4 Mitigating Systems PIs
  b. Findings
      No findings were identified.
.2  Radiation Safety Cornerstones
  a. Inspection Scope
      Occupational Radiation Safety Cornerstone: The inspectors reviewed recent
      Occupational Exposure Control Effectiveness PI results for the occupational radiation
      safety cornerstone, and reviewed PI records generated from October 2014 through
      October 2015. For the assessment period, the inspectors reviewed ED alarm logs and
      selected CRs related to controls for exposure significant areas. Documents reviewed
      are listed in the Attachment.
      Public Radiation Safety Cornerstone: The inspectors reviewed recent radiological
      control effluent release occurrences PI results for the public radiation safety cornerstone,
      and reviewed PI records generated from October 2014 through October 2015. For the
      assessment period, the inspectors reviewed cumulative and projected doses to the
      public contained in liquid and gaseous release permits and CRs related to radiological
      effluent TS/Offsite Dose Calculation Manual issues. Documents reviewed are listed in
      the Attachment.
  b. Findings
      No findings were identified.


* AR 02086287, CV-3-2819 has corrosion on electrical connection
                                            25
* AR 02086292, MOV-3-866B inactive minor dry white boric acid at packing
4OA2 Problem Identification and Resolution (IP 71152)
* AR 02086231, 3-309D inactive minor dry white boric acid at packing
.1    Daily Review
* AR 02086226, 3-306B inactive minor dry white boric acid at packing
  a. Inspection Scope
* AR 02086218, 3-120G inactive dry white boric acid at D/S pipe cap
      As required by IP 71152, Identification and Resolution of Problems, and to help identify
* AR 02086240, 3-572 inactive dry white boric acid at packing
      repetitive equipment failures or specific human performance issues for follow-up, the
* AR 02086239, 3-542, inactive dry white boric acid at packing
      inspectors performed a screening of items entered daily into the licensees CAP. This
Steam Generator Tube Inspection Activities
      review was accomplished by reviewing daily printed summaries of ARs and by reviewing
The inspectors verified that for the U3 steam generator tubes, no inspection activities
      the licensees electronic AR database. Additionally, RCS unidentified leakage was
      checked on a daily basis to verify no substantive or unexplained changes. Documents
      reviewed are listed in the Attachment.
  b. Findings
      No findings were identified.
.2    Annual Sample: Missed Fire Watch Tours
  a. Inspection Scope
      The inspectors selected AR 02056905, Missed Fire Watch Tours for a more in-depth
      review of the circumstances and the corrective actions that followed. The AR report was
      reviewed to ensure that an appropriate evaluation was performed and corrective actions
      were specified and prioritized in accordance with the licensees program. Other
      attributes checked included disposition of operability and resolution of the problem,
      including cause determination, past operability determination, and corrective actions.
      The inspectors interviewed plant personnel and evaluated the CR in accordance with the
      requirements of the licensees corrective actions process as specified in licensees
      procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205,
      Condition Evaluation and Corrective Action. This inspection constitutes one sample.
  b. Findings and Observations
      No inspector findings were identified. A licensee-identified violation of very low safety
      significance (Green) is documented in Section 4OA7 of this report. The licensee
      identified that employees failed to perform hourly required fire watch roves. The
      inspectors noted that the licensees evaluation for the missed fire watch roves concluded
      that there was no violation of any TS requirement since TS do not require fire watches
      for degraded fire protection features. The licensee concluded that the missed roves
      represented a reduction in the effectiveness of the Fire Protection Program (FPP) and
      the loss of a defense-in-depth feature.
      The licensee determined the root cause of the event to be that operations management
      was not engaged with the fire watch program. The licensee also determined that a
      direct cause was that fire watch employees willfully chose non-compliance with fire
      protection requirements. Immediate corrective actions for this event included the
      immediate denial of site access for the individuals who failed to conduct the roves. The
      licensee also updated the fire protection procedure, 0-ADM-016.4, to include Operations


were required this RFO, in accordance with the requirements of the ASME Code, the
                                              26
licensee's TS, and Nuclear Energy Institute (NEI) 97-06, "Steam Generator Program
      Management Responsibilities and Oversight that requires observations, audits, and
Guidelines."
      assessments to ensure regulatory requirements are met. The licensee also conducted
Identification and Resolution of Problems
      an extent of condition and determined that no other missed tours were present in other
      departments based on data collected and security access logs.
The inspectors reviewed a sample of ISI-related issues entered into the CAP to  
.3    Semi-Annual Trend
determine if the licensee had appropriately described the scope of the problem, and  had initiated corrective actions. The review also included the licensee's consideration and assessment of operating experience events applicable to the plant. The inspectors
  a. Inspection Scope
performed this review to ensure compliance with 10 CFR Part 50, Appendix B, Criterion
      The inspectors performed a review of the licensees records including ARs, CAP health
      reports, apparent cause evaluation reports, and various corrective action review board
      reports to asses an adverse trend in the performance of reactor protection transmitters.
      The inspectors reviewed licensee AR 02088175, which identified an adverse trend in
      protection transmitter calibration check results. The inspectors evaluated the
      effectiveness of the licensees corrective actions and the significance of the problems,
      including attributes such as accurate documentation, reportability, evaluation, corrective
      actions, and problem resolution. This inspection constitutes one sample.
  b. Findings and Observations
      No inspector findings were identified. The licensee noted that the transmitters in
      question, Rosemount pressure transmitters, are expected to drift a slight amount. The
      licensee also noted that both the transmitter age and replacement of components tended
      to exacerbate the transmitter drift through the calibration cycle. The licensee concluded
      that even with the noted transmitter drift, the transmitters still performed satisfactorily
      and were within TS compliance. The inspectors did not identify any additional trends not
      observed by the licensees trending activities.
4OA5 Other Activities
.1    Independent Spent Fuel Storage Facility Walk down (IP 60855.1)
  a. Inspection Scope
      On December 17, 2015, the inspector conducted a walk down of the ISFSI protected
      area per IP 60855.1, Operation of an ISFSI at Operating Plants. The inspectors
      observed each cask building temperature indicator and passive ventilation system to be
      free of any obstruction, allowing natural draft convection decay heat removal through the
      air inlet and air outlet openings. The inspectors observed associated cask building
      structures to be structurally intact and radiation protection access and security controls
      to the ISFSI area to be satisfactory.
  b. Findings
      No findings were identified.


XVI, "Corrective Action," requirements.
                                            27
4OA6 Meetings
  b. Findings
    The resident inspectors presented the inspection results to Mr. Tom Summers and other
    members of licensee management on January 15, 2016. The inspectors asked the
No findings were identified.  
    licensee whether any of the material examined during the inspection should be
    considered proprietary information. The licensee did not identify any proprietary
    information.
 
4OA7 Licensee-identified Violation
    The following violation of very low safety significance (Green) was identified by the
 
    licensee and is a violation of NRC requirements which meets the criteria of the NRC
9  1R11 Licensed Operator Requalification Program (IP 71111.11)  
    Enforcement Policy for being dispositioned as an NCV.
.1 Licensed Operator Requalification Exam
    10 CFR 50.48 states that each operating nuclear power plant must have a fire protection
    plan that satisfies Criterion 3 of Appendix A of this part. Turkey Point Renewed
  a. Inspection Scope
    Operating License condition D, for Units 3 and 4, states that the licensee shall
Annual Review of Licensee Requalification Examination Results:  On December 30, 2015, the licensee completed the annual requalification operating examinations required
    implement and maintain in effect all provisions of the approved FPP as described in the
to be administered to all licensed operators in accordance with 10 CFR 55.59(a)(2). The inspectors performed an in-office review of the overall pass/fail results of the individual operating examinations and the crew simulator operating examinations in accordance
    UFSAR Appendix 9.6A. The approved FPP is implemented, in part, by 0-ADM-016, Fire
with IP 71111.11, "Licensed Operator Requalification Program."  These results were
    Protection Program, as referenced in Section 7.2 of UFSAR Appendix 9.6A. Section 5.6
compared to the thresholds established in Section 3.02, "Requalification Examination Results," of IP 71111.11.  
    of 0-ADM-016 requires that, for non-functional post-fire safe shutdown components,
    b. Findings
    engineering evaluations should identify appropriate compensatory actions, including
No findings were identified.
    hourly fire roves. Contrary to the above, between May 1st, 2014, and April 23rd, 2015,
    hourly fire watch patrols were not conducted on numerous occasions in fire zones that
    required regular hourly tours due to fire protection equipment impairment. The failure to
    perform the fire watch tours did not cause the inoperability of any equipment but resulted
    in the loss of a defense-in-depth feature for fire detection in fire zones affected by an
    impaired or non-functional fire safety component or feature. This violation was
    associated with the Mitigating Systems Cornerstone and affected the cornerstone
    objective of ensuring the availability, reliability and capability of the systems that respond
    to initiating events to prevent undesirable consequences. The inspectors determined the
    finding to be of very low safety significance (Green) after performing a detailed risk
    evaluation in accordance with Manual Chapter 0609, Appendix A, because the missed
    fire watch tours reflected a low degradation of the Fire Prevention and Administrative
    Controls FPP element in that other area fire protection defense-in-depth features such
    as automatic fire detection (smoke detectors), automatic fire suppression capability
    (sprinklers), manual suppression capability (fire brigade), and safe shutdown capability
    from the main control room were still available. The licensee entered this violation into
    their CAP as AR 02056905.
ATTACHMENT: SUPPLEMENTARY INFORMATION


.2 Resident Inspector Quarterly Review
                              SUPPLEMENTARY INFORMATION
    a. Inspection Scope
                                KEY POINTS OF CONTACT
The inspectors performed the following inspection sample of a simulator observation and
Licensee Personnel:
assessed licensed operator performance while training. These observations included procedural use and adherence, response to alarms, communications, command and control, and coordination and control of the reactor plant operations.  
F. Banks, Quality Manager
On October 8, 2015, the inspectors assessed licensed operator performance in the
C. Cashwell, Training Manager
plant-specific simulator during a training evolution. The training scenario was started with the unit in Mode 1 at 100 percent power and included a fire lasting greater than 15 minutes, a loss of reactor coolant accident (LOCA), a reactor trip, a safety injection, a
P. Czaya, Licensing
residual heat removal (RHR) pump seal failure, and a radiological release to the
C. Domingos, Plant General Manager
environment.  
T. Eck, Security Manager
M. Guth, Licensing Manager
O. Hanek, Licensing Engineer
A. Katz, Projects Manager
G. Melin, Operations Manager
S. Mihalakea, Licensing
K. Ohara, Emergency Preparedness Manager
J. Pallin, Engineering Director
D. Sluszka, Work Controls Manager
B. Stamp, Operations Director
T. Summers, Site Vice-President
D. Barrow, Maintenance Director
R. Hess, General Operations Training Supervisor
M. Wilson, Operations Training Supervisor
NRC Personnel:
B. Bishop, Senior Project Engineer
A. Beaston, Project Engineer
A. Vargas, Project Engineer
                    LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Opened and Closed
05000251/2015004-01                NCV        Failure to correctly follow procedure
                                                3-PMI-072.6, Steam Dump to
                                                Atmosphere Control Loop Calibration.
                                                (Section 1R20)
                                                                                  Attachment


                              LIST OF DOCUMENTS REVIEWED
During this simulator observation, the simulator board configurations were compared with actual plant control board configurations reflecting recent plant changes or modifications.  The inspectors specifically evaluated the following attributes related to
Section 1R01: Adverse Weather
operating crew performance and the licensee evaluation:
0-ONOP-103.3, Severe Weather Preparations
* Clarity and formality of communication 
Section 1R04: Equipment Alignment
* Ability to take timely action to safely control the unit
3-NOP-022, Emergency Diesel Generator Fuel Oil System
* Prioritization, interpretation, and verification of alarms
3-NOP-023, Emergency Diesel Generator
* Correct use and implementation of off-normal and emergency operating procedures
4-NOP-022, Emergency Diesel Generator Fuel Oil System
and emergency plan implementing procedures
4-NOP-023, Emergency Diesel Generator
* Control board operation and manipulation, including high-risk operator actions
3-OP-201, Filling/Draining the Refueling Cavity and the SFP Transfer Canal
* Oversight and direction provided by shift supervisor, including ability to identify and implement appropriate TS actions and emergency plan classification and notification
4-OP-201, Filling/Draining the Refueling Cavity and the SFP Transfer Canal
* Crew overall performance and interactions
P&ID 5613-M-3022, Emergency Diesel Engine and Oil System
* Evaluator's control of the scenario and post scenario evaluation of crew performance 
P&ID 5613-M-3062, Safety Injection System
10      b. Findings
P&ID 5614-M-3062, Safety Injection System
  No findings were identified.
Section 1R05: Fire Protection
.3 Control Room Observations 
0-ONOP-016.10, Pre-Fire Plan Guidelines and Safe Shutdown Manual Actions
Section 1R08: Inservice Inspection Activities
  a. Inspection Scope
Procedures:
The inspectors performed daily assessments of licensed operators in the control room during their performance of routine operations.  These observations included daily  surveillance testing, log keeping, response to alarms, communications, shift turnovers,
0-ADM-537, Boric Acid Corrosion Control Program, Rev. 11
and coordination of plant activities.  These observations were conducted to verify
3-OSP-045.1, ASME Section XI Quality Group A Bolting Examination, Rev. 2
operator compliance with station operating guidelines, such as use of procedures,
MA-AA-1000, Plant Leak Management Procedure, Rev. 6
control and manipulation of components, and communications.  The inspectors also performed the following three focused control room observations during reactivity manipulations and Mode changes: 
NDE 4.15, Visual Examination (VE) ASME Section XI Code Case N-722-1 and N-729-1, Rev. 4
 
NDE 4.2, Visual Examination VT-2 Conducted During System Pressure Tests, Rev. 10
NDE 4.3, Visual Examination VT-3, Rev. 12
On November 19, 2015, the inspectors performed a focused observation on U4
NDE 5.16, Ultrasonic Examination Technique for the Detection of Cracking in Feedwater Piping,
consisting of a RCS primary water dilution per 0-OP-046, Enclosure 6, "Chemical Volume Control System Boron Concentration
  Rev. 10
Control."  Specifically, the inspectors observed the reactor operators' performance of the pre-job brief per 0-ADM-200,
NDE 5.18, Ultrasonic Thickness Measurement, Rev. 8
Attachment 7, "Planned Reactivity Manipulations for Maintaining Steady State Plant
Calculations:
Conditions" and verified the operators complied with the applicable procedure during the
EC 284178, Review of Degradation and Operational Assessments at End-of-Cycle 27 for
 
  Turkey Point Unit 3
evolution. 
Work Orders/Work Requests:
 
WO 4029647301, Valve 3-298C Replace Valve
On December 1, 2015 and December 2, 2015, the inspectors performed a focused observation in the U3 control room during low power physics testing in accordance with
WO 4030098001, Repair of PZR HTR Sleeve #11
procedure 0-OSP-040.19, "Low Power Physics Testing."  The inspectors observed the
CAP Documents:
pre-evolution operating crew brief, control rod movements, monitoring of subcritical multiplication, and data collection.       
AR 1771920, Audit shows no self-assessments performed on the welding control program
On December 3, 2015, the inspectors performed a focused observation on U3 during a
reactor startup per procedure 3-GOP-301, "Hot Standby to Power Operations."  The
inspectors reviewed the expected critical boron concentration calculation and the control
rod pull sequence plan used during the observed reactor startup.  The inspectors
reviewed the recorded reactor startup physics data to ensure it was as calculated by the licensee reactor engineering staff.
This inspection constitutes three samples.  The inspectors focused on the following
conduct of operations attributes as appropriate:
* Operator compliance and use of procedures
* Control board manipulations
* Communication between crew members
* Use and interpretation of plant instruments, indications and alarms
* Use of human error prevention techniques
* Documentation of activities, including initials and sign-offs in procedures
* Supervision of activities, including risk and reactivity management
 
11      b. Findings
  No findings were identified.
.4 Biennial Requalification
  a. Inspection Scope
The inspectors reviewed the facility operating history and associated documents in preparation for this inspection.  During the weeks of November 30, 2015 through December 21, 2015, the inspectors reviewed documentation associated with the
licensee's operator requalification program biennial written examinations.  The activity
performed by the inspectors was conducted to assess the licensee's effectiveness in implementing requalification requirements identified in 10 CFR Part 55, "Operators' Licenses."  The evaluations were also performed to determine if the licensee effectively implemented operator requalification guidelines established in NUREG-1021, "Operator Licensing Examination Standards for Power Reactors," and IP 71111.11, "Licensed
Operator Requalification Program."  Documentation reviewed included two biennial
written examinations.  The records were inspected using the criteria listed in IP 71111.11.  Documents reviewed during the inspection are documented in the List of Documents Reviewed.
 
The sample is now complete because the remainder of this sample was previously
inspected and documented in the third quarter integrated inspection report
(05000250&251/2015003).
    b. Findings
No findings were identified.
 
1R12 Maintenance Effectiveness (IP 71111.12)
    a. Inspection Scope
The inspectors reviewed known equipment problems associated with the U3 steam
generator steam flow module FM-3-474D  affecting the maintenance rule program and equipment performance history trends associated with the equipment.  Specifically, the inspectors reviewed AR 02081538. 
 
The inspectors reviewed the licensee's activities to meet the requirements of 10 CFR
50.65, "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," and licensee procedure NAP-415, "Maintenance Rule Program Administration."  The inspectors focused on maintenance rule scoping, characterization of maintenance
problems and failed components, risk significance, determination of a(1) or a(2)
performance criteria classification, corrective actions, and the appropriateness of
established performance goals and monitoring criteria.  The inspectors also interviewed
responsible engineers and observed or reviewed corrective maintenance activities.  The inspectors verified that equipment problems were being identified and appropriately entered into the licensee's CAP.  The inspectors used the licensee maintenance rule 
12  database, system health reports, maintenance rule unavailability status reports, and the CAP as sources of information on tracking and resolution of issues.  This inspection
constitutes one sample.
* U3 FM-3-474D Flow Module Bias Potentiometer
    b. Findings
No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (IP 71111.13)
  a. Inspection Scope
The inspectors completed in-office reviews and control room inspections of the
licensee's risk assessment of five emergent or planned maintenance activities.  The
inspectors verified the licensee's risk assessment and risk management activities using the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management
and Resource Council 93-01, "Industry Guidelines for Monitoring the Effectiveness of
Maintenance at Nuclear Power Plants," Revision 3; and procedures 0-ADM-068, "Work
Week Management;" WM-AA-1000, "Work Activity Risk Management;" and 0-ADM-225, "On Line Risk Assessment and Management."  The inspectors also reviewed the effectiveness of the licensee's contingency actions to mitigate increased risk resulting from the degraded equipment and the licensee is assessment of aggregate risk using
procedure OP-AA-104-1007, "Online Aggregate Risk."  The inspectors discussed the on-
line risk monitor (OLRM) results with the control room operators and verified all
applicable OOS equipment was included in the OLRM calculation.  The inspectors evaluated the following five risk assessment samples during the inspection period:
* U3 3A 4kV Bus, U3 Startup Transformer (SUT), and 3A and 3B HHSI pumps OOS
* U3 3A 4kV Bus, U3 SUT, and 3D Vital 480V Motor Control Cabinet (MCC) OOS
* U3 3-312A Valve Inspection and Repair with Freeze Seal (WO 40411630)
* U3 SUT OOS, U3 3A Sequencer OOS, and 3A and 3B EDGs Running
* U3 Train 2 AFW, U4 Train 2 AFW, and U3 3B Emergency Containment Cooler OOS
    b. Findings
No findings were identified.
 
1R15 Operability Determinations and Functionality Assessments (IP 71111.15)
  a. Inspection Scope
The inspectors evaluated the technical adequacy of the licensee evaluations to ensure
that TS operability was properly justified and the subject component or system remained
available such that no unrecognized increase in risk occurred for the five operability
evaluations described in the ARs listed below.  The inspectors reviewed applicable sections of the updated Final Safety Anaylsis
Report (UFSAR) to determine if the system or component remained available to perform its intended function.  In addition, when
applicable, the inspectors reviewed compensatory measures implemented to verify that 
13  the affected equipment remained capable of performing its intended design function.  The inspectors also reviewed a sampling of CRs to verify that the licensee routinely
identifed and corrected any deficiencies associated with operability evaluations.  This inspection constitutes five samples.
* AR 02083336, U3 RHR Gas Voids
* AR 02082853, Pressurizer Steam Sample Line Containment Isolation Valve (CV-4-
951) OOS * AR 02053124, 3B EDG Oil Leak
* AR 02086176, 3A FT-3-414 Bent and Unsupported
* AR 02093957, 4B EDG TS-4-6132 Broken
    b. Findings
No findings were identified.
 
1R18 Plant Modifications (IP 71111.18)
  Permanent Plant Modifications
    a. Inspection Scope
The inspectors reviewed the following two permanent plant modifications.  The
inspectors reviewed the 10 CFR 50.59 screening and technical evaluation to verify that the modifications had not affected system operability or availability.  The inspectors reviewed associated plant drawings, design analyses, and UFSAR documents impacted
by these modifications and discussed the changes with licensee personnel to verify that
the modifications were consistent with the WO and associated documents.  The
inspectors observed portions of the modifications and surrounding areas to determine if conditions resulted in any potential unsafe conditions not described in the engineering change documentation.  Additionally, the inspectors reviewed and verified that any
conditions associated with the modifications were being identified and entered into the
CAP.  This inspection constitutes two samples.
 
* EC 280399, U3 Reactor Coolant Pump (RCP) Seal Replacmement Modification
* EC 285012, FT-4-494 U4 Steam Generator C Steam Flow Detector Line
Replacement
    b. Findings
No findings were identified.
1R19 Post Maintenance Testing (IP 71111.19)
    a. Inspection Scope
For the five post maintenance tests and associated WOs listed below, the inspectors
reviewed the test procedures and either witnessed the testing or reviewed test records to
determine whether the scope of testing adequately verified that the work performed was  completed satisfactorily and demonstrated that the affected equipment was operable. 
14  The inspectors verified that the requirem
ents in licensee procedure 0-ADM-737, "Post Maintenance Testing," were incorporated into the test requirements.  The inspectors
reviewed the following WOs consisting of five inspection samples:
* WO 40281614, U3 Pressurizer Pressure Operated Relief Valve PCV-3-455C 
* WO 40419666, U4 Steam Generator C Steam Flow Detector FT-4-494
* WO 40371127, 3B Containment Spray Pump Check Valve Inspection
* WO 40419961, Reactor Protection System 3-P7-1-B Relay Replacement
* WO 40161059, 3B50 Load Center Relay Replacements 
    b. Findings
No findings were identified.
1R20 Refueling and Other Outage Activities (IP 71111.20)
.1 Unit 3 Refueling Outage PT3-28 (one sample)
    a. Inspection Scope
Outage Planning, Control and Risk Assessment
During daily outage planning activities by the licensee, the inspectors reviewed the risk
reduction methodology employed by the licensee during RFO PT3-28 meetings including outage control center (OCC) morning meetings, operations daily team meetings, and schedule performance update meetings.  The inspectors examined the licensee
implementation of shutdown safety assessments during PT3-28 in accordance with
administrative procedure ADM-051, "Outage Risk Assessment and Control," to verify if a defense in depth concept was in place to ensure safe operations and avoid unnecessary risk.  In addition, the inspectors regularly monitored outage planning and control activities in the OCC, and interviewed responsible OCC management personnel during
the outage to ensure system, structure, and component configurations, and work scope
were consistent with TS requirements, site procedures, and outage risk controls.
Monitoring of Shutdown Activities
The inspectors performed walk downs of important systems and components used for RHR from the reactor core and SFP during t
he shutdown period, including the intake cooling water system, component cooling water (CCW) system, and SFP cooling
system.  Outage Activities
The inspectors examined outage activities to verify that they were conducted in
accordance with TS, licensee procedures, and the licensee's outage risk control plan.  Some of the more significant inspection activities accomplished by the inspectors were
as follows:
 
 
15  * Walked down selected safety-related equipment clearance orders 
* Verified operability of RCS pressure, level, flow, and temperature instruments during various modes of operation
* Verified electrical systems availability and alignment
* Verified shutdown cooling system and SFP cooling system operation
* Evaluated implementation of reactivity controls
* Reviewed control of containment penetrations
* Examined foreign material exclusion (FME) controls put in place inside containment (e.g., around the refueling cavity, near sensitive equipment and RCS breaches) and
around the SFP
* Observed fuel loading and unloading in the SFP and in containment
Monitoring of Plant Heat up and Containment Closure Activities
The inspectors examined the applicable TS, license conditions, and verified
administrative prerequisites were being met prior to reactor plant mode changes.  The
inspectors reviewed measured RCS leak rates, and verified containment integrity was properly established.  The inspectors performed a containment closeout inspection prior
to the reactor plant startup to verify no evidence of leakage or debris were left in containment that could affect plant operations.
Reactor Startup and Mode Changes
On December 2, 2015, the inspectors observed the U3 reactor startup and turbine synchronization to the electrical grid and associated Mode changes.  The inspectors reviewed the recorded reactor startup physics data in order to determine it was as-
calculated by the licensee reactor engineering staff.  The inspectors determined that
startup and Mode changes were performed in accordance with licensee procedures 0-
OSP-040.16, "Initial Criticality After Refueling Outage and Nuclear Design Verification,"
and 3-GOP-301, "Mode 3 to Power Operations."   
Corrective Action Program 
The inspectors reviewed ARs generated during PT3-28 to evaluate the licensee's
threshold for initiating ARs.  The inspectors reviewed CRs to verify priorities, Mode holds, and significance levels were assigned as required.  Resolution and implementation of corrective actions of several ARs were also reviewed for
completeness.  The inspectors routinely reviewed the results of site oversight of daily surveillances of outage activities.
    b. Findings
Introduction:  A Green self-revealing NCV of TS 6.8.1, "Procedures and Programs," was identified for the licensee's failure to correctly execute procedure 3-PMI-072.6, "Steam
Dump to Atmosphere Control Loop Calibration."  The failure resulted in actuation of a 3B
4160 V vital bus lockout circuit causing loss of power to the B train of U3 SFP cooling. 
Description:  On November 4, 2015, at 2112 hours, Instrumentation and Controls technicians were performing procedure 3-PMI-072.6, "Steam Dump to Atmosphere
Control Loop Calibration," when a temporary electrical jumper was incorrectly installed in 
16  the control room reactor operator console 3C02 instead of 3C04, in contrast to step 6.3.2 of 3-PMI-072.6.  At the time of the event, U3 was defueled with all of its fuel temporarily
relocated to the SFP.  The 3A 4160 V vital bus was de-energized for planned maintenance and all 480 V vital load centers were powered by the 3B 4160 V vital bus.  Separate load centers provided power to two separate trains of U3 SFP cooling pumps,
and the 3A train pump was powered from Unit 4 electrical switchgear.
 
The incorrectly placed jumper actuated a 3B 4160 V vital bus lockout circuit causing all
associated Unit 3 480 V vital load and motor control centers to de-energize.  Numerous equipment was rendered OOS including the B SFP cooling pump and the 3B CCW pump.  The 3B CCW pump provided cooling to both U3 SFP cooling heat exchangers. 
Upon loss of the 3B CCW pump, the standby 3C CCW pump started on low pressure as
designed, providing cooling to the 3A SFP cooling train.  Immediate corrective action
was taken to remove the jumper and restore the B train of SFP cooling.  However, the loss of one train of SFP cooling for approximately four hours caused the SFP temperature to rise from approximately 110 °F to 117 °F.  The licensee restored U3 load
and motor control centers at 0207 hours on November 5, 2015, and by 0300 hours the
SFP temperature had returned to normal. 
 
The licensee entered the condition in its CAP as AR 02088911 and 02088914.  Corrective actions included site-wide briefings of lessons learned from the event, quality
reviews of procedure 3-PMI-072.6, and enhanced oversight of maintenance activities.
 
Analysis:  The inspectors determined that the failure to correctly implement maintenance procedure 3-PMI-072.6 was a performance deficiency.  The performance deficiency was determined to be more than minor because it was associated with the human performance attribute of the barrier integrity cornerstone and adversely affected the
cornerstone objective to provide reasonable assurance that physical design barriers (fuel
cladding, RCS, and containment) protect the public from radionuclide releases. 
Specifically, the licensee's failure to correctly execute step 6.3.2 of procedure 3-PMI-072.6 rendered one of two SFP cooling trains OOS, causing the SFP temperature to rise from approximately 110 °F to 117 °F over a four-hour period.  While the
performance deficiency did not directly challenge the integrity of the fuel cladding, if left
uncorrected, the SFP temperature would have continued to increase, potentially
affecting SFP inventory. 
 
The finding was screened using IMC 0609, "Significance Determination Process," Attachment 0609.04, "Initial Characterization of Findings," Tables 2 and 3, dated July 1,
2012, and Appendix G Attachment 1, "Shutdown Operations Significance Determination
Process Phase 1 Initial Screening and Characterization of Findings," Exhibit 4 for Barrier
Integrity, dated May 9, 2014.  The inspectors determined the finding was of very low
safety significance (Green) because it was not associated with low temperature over pressurization, freeze seals, steam generator nozzle dams, criticality, drain down or
leakage paths, or the containment barrier.  Furthermore, one train of SFP cooling
remained in operation, the rate of SFP temperature rise was low (~2 °F/hour), and
additional diverse compensatory methods remained available to limit SFP temperature
rise.  This finding was assigned a cross cutting aspect associated with the procedure adherence element of the human performance area because the licensee failed to correctly execute step 6.3.2 of procedure 3-PMI-072.6 (H.8). 
 
 
17  Enforcement:  Technical Specification 6.8.1
requires that procedures required by the licensee's Quality Assurance Topical Repor
t (QATR) be established, implemented, and maintained.  The QATR includes procedures listed in Appendix A of NRC Regulatory Guide 1.33, Revision 2, dated February 1978, including procedures for calibrations.  The licensee implements TS 6.8.1 requirements, in part, using procedure 3-PMI-072.6, "Steam Dump to Atmosphere Control Loop Calibration."  Step 6.3.2 of procedure
3-PMI-072.6, requires that a jumper be installed in reactor operator console 3C02. 
Contrary to this requirement, on November 4, 2015, at 2112 hours, a maintenance
technician mistakenly installed a jumper in reactor operator console 3C04.  This action resulted in actuation of a 3B 4160 V vital bus lockout circuit causing loss of power to the B train of U3 SFP cooling.  The licensee took immediate corrective action to remove the
jumper.  This violation is being treated as an NCV, consistent with Section 2.3.2 of the
Enforcement Policy, because it was of very low safety significance and was entered in
the licensee's CAP as AR 02088911 and 02088914. (NCV 05000250/2015004-01, Failure to correctly follow procedure 3-PMI-072.6, "Steam Dump to Atmosphere Control
Loop Calibration.") 
1R22 Surveillance Testing (IP 71111.22)
    a. Inspection Scope
The inspectors either reviewed or observed the following five surveillance tests to verify
that the tests met the TS requirements, the UFSAR description, the licensee's
procedural requirements, and demonstrated that systems were capable of performing their intended safety functions and operational readiness.  In addition, the inspectors evaluated the effect of the testing activities on the plant to ensure that conditions were adequately addressed by the licensee staff and that after completion of the testing
activities, equipment was returned to the status required for the system to perform its
safety function.  The inspectors verified that any surveillance deficiencies were
 
documented in the licensee's CAP.  This inspection constitutes two surveillance test samples, one inservice testing (IST) sample, and two containment isolation valve leak test samples.  The inspectors reviewed the following tests: 
 
Surveillance Test:
* 0-OSP-059.13, U4 Flux Map
* 3-OSP-072.5, U3 Main Steam Safey Valve Setpoint Verification
In-Service Tests:
* 3-OSP-206.1, Component Cooling Water MOV-3-1418 Valve Test (IST) Containment Isolation Valve Test:
* 3-OSP-051.5, U3 Local Leak Rate Test, Penetration 8 CV-3-951
* 3-OSP-051.5, U3 Local Leak Rate Test, Penetration 14 CV-3-204 
  b. Findings
No findings were identified. 
18  Cornerstone:  Emergency Preparedness
1EP6 Drill Evaluation (IP 71114.06)
.1 Emergency Preparedness Drill
  a. Inspection Scope
On October 8, 2015, the inspectors observed an emergency preparedness drill and the performance of the licensee's emergency response organization.  The drill included a simulated fire in the U4 laydown area, a LOCA inside containment, followed by a RHR
pump seal failure and radiological release to the environment.  The fire, lasting greater
than 15 minutes, required an unusual event emergency declaration and notification to
 
state and local county officials and the NRC per licensee procedure 0-EPIP-20101, "Duties of the Emergency Coordinator."  The scenario progressed to a loss of two RCS barriers with the loss or potential loss of a third barrier requiring a general emergency
declaration and an additional notification.  The inspectors observed the crew in the plant
simulator, including simulated implementation of emergency procedures.  The inspectors
observed the emergency response organization staff in the control room simulator and technical support center while they implemented the event classification guidelines and emergency response procedures.  The inspectors determined that the emergency
classification and notifications were made in accordance with the licensee emergency
plan implementing procedure 0-EPIP-20101.  The inspectors attended the licensee's
post drill critique, reviewed the licensee's critique items, and discussed inspector
observations with the licensee to verify that drill issues were identified and captured in the licensee's CAP.  This inspection constitutes one sample.
  b. Findings
No findings were identified.
2. RADIATION SAFETY (RS)
Cornerstones: Public Radiation Safety and Occupational Radiaition Safety
2RS1 Radiological Hazard Assessment and Exposure Controls (IP 71124.01)
   
  a. Inspection Scope
Hazard Assessment and Instructions to Workers.  During facility tours, the inspectors directly observed labeling of radioactive material and postings for radiation areas, high radiation areas, and airborne radioactivity areas established within the radiologically controlled area (RCA) of the U3 containment building, auxiliary building, the Independent
Spent Fuel Storage Installation (ISFSI), and radioactive waste processing and storage
locations.  The inspectors independently measured radiation dose rates or directly
observed conduct of licensee radiation surveys for selected RCA areas.  The inspectors reviewed survey records for several plant areas including surveys for alpha emitters, airborne radioactivity, gamma surveys with a range of dose rate gradients, and pre-job surveys for upcoming tasks.  The inspectors also discussed changes to plant operations
that could contribute to changing radiological conditions since the last inspection.  For
selected outage jobs, the inspectors attended pre-job briefings and reviewed Radiation 
19  Work Permit (RWP) details to assess communication of radiological control requirements and current radiological conditions to workers.
 
Hazard Control and Work Practices.  The inspectors evaluated access barrier effectiveness for selected Locked High Radiation Area (LHRA) locations and discussed changes to procedural guidance for LHRA and Very High Radiation Area controls with
Radiation Protection (RP) supervisors.  The inspectors observed and evaluated controls
for the storage of irradiated material within the SFP.  Established radiological controls
(including airborne controls) were evaluated for selected U3 RFO 28 (U3R28) tasks including RCP seal replacements, reactor cavity decontamination and reactor sump demobilization activities.  In addition, the inspectors reviewed licensee controls for areas
where dose rates could change significantly as a result of plant shutdown and refueling
operations. 
 
Through direct observations and interviews with licensee staff, the inspectors evaluated occupational workers' adherence to selected RWPs and RP technician proficiency in
providing job coverage.  Electronic dosimeter (ED) alarm set points and worker stay
times were evaluated against area radiation survey results for selected U3 RFO jobs,
including the reactor sump demobilization and reactor cavity decontamination.  The inspectors discussed the use of personnel dosimetry (extremity dosimetry and multibadging in high dose rate gradients) with RP staff.  The inspectors also evaluated
worker response to dose and dose rate alarms during selected work activities. 
Control of Radioactive Material.  The inspectors observed surveys of material and personnel being released from the RCA using small article monitor (SAM), personnel contamination monitor (PCM), and portal monitor instruments.  As part of IP 71124.05, the inspectors reviewed the last two calibration records for selected release point survey
instruments and discussed equipment sensitivity, alarm setpoints, and release program
guidance with licensee staff.  The inspectors reviewed records of leak tests on selected
sealed sources and discussed nationally tracked source transactions with licensee staff.
Problem Identification and Resolution.  The inspectors reviewed CAP documents associated with radiological hazard assessment and exposure control.  The inspectors
evaluated the licensee's ability to identify and resolve the issues in accordance with
licensee procedures.  The inspectors also reviewed recent self-assessment results. 
Radiation protection activities were evaluated against the requirements of the UFSAR Section 11; TS Sections 6.8 Procedures and Programs and 6.12 High Radiation Area;
10 CFR Parts 19 and 20; Regulatory Guide 8.38, "Control of Access to High and Very
High Radiation Areas in Nuclear Power Plants"; and approved licensee procedures. 
Licensee programs for monitoring materials and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, "Control of Radioactively Contaminated Material."  Documents reviewed are listed in the Attachment.
  b. Findings
No findings were identified.
 
 
20  2RS2 Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls  (IP 71124.02)
    a. Inspection Scope
Work Planning and Exposure Tracking.  The inspectors reviewed work activities and their
collective exposure estimates for U3 RFO. The inspectors reviewed
ALARA planning packages for the following high collective exposure tasks: SG cleaning (including bundle flushing, sludge lancing, and foreign object search and retrieval); refueling activities; RCP seal replacement; bottom mounted inspection, and; various valve work.  For the selected tasks, the inspectors reviewed established dose goals and discussed assumptions regarding the bases for the current estimates with responsible ALARA
planners.  The inspectors evaluated the incorporation of exposure reduction initiatives
and operating experience.  Adjustments made to planned doses were also reviewed, along with the basis of those adjustments. Post-job reviews from both the current and previous RFO were assessed.  Where applicable, the inspectors discussed changes to
established estimates with ALARA planners and evaluated them against work scope
changes or unanticipated
elevated dose rates.
Source Term Reduction and Control.  The inspectors reviewed the collective exposure
three-year rolling average from 2012-2014 and reviewed historical collective exposure
trends.  The inspectors evaluated historical dose rate trends and compared them to
current data. 
Radiation Worker Performance.  In conjunction with IP 71124.01, radiation worker
performance was
evaluated during several tasks both within containment and the auxiliary building.  The inspectors specifically evaluated both the use of ALARA briefings and remote technologies, including teledosimetry and remote visual monitoring, to
reduce dose.
 
Problem Identification and Resolution.  The inspectors reviewed and discussed selected CAP documents associated with ALARA program implementation.  The inspectors evaluated the licensee's ability to identify and resolve the issues in accordance with
licensee procedures.  The inspectors also reviewed recent self-assessment results. 
ALARA program activities were evaluated against the requirements of the UFSAR Section 11, applicable TS Sections 6.8 and 6.12, 10 CFR Part 20, and approved licensee procedure.  Records reviewed are listed in the Attachment.
 
    b. Findings
No findings were identified.
2RS3 In-Plant Airborne Radioactivity Control and Mitigation (IP 71124.03)
  a. Inspection Scope
Engineering Controls:  Licensee engineering controls used to control and mitigate airborne radioactivity were reviewed and discussed.  The inspectors evaluated selected U3 engineering controls including temporary High Efficiency Particulate Air (HEPA)
filtration systems for selected outage tasks with the potential for generating airborne 
21  activity conditions.  The evaluations included procedural guidance, operability testing, and established configurations during specific outage tasks.  In addition, plant guidance
and its implementation for the monitoring of potential airborne beta-gamma and alpha-emitting radionuclides for outage tasks associated with refueling activities, head disassembly, and valve maintenance were reviewed and discussed with cognizant
licensee representatives.
 
Use of Respiratory Protection Devices:  Program guidance for issuance and use of respiratory protection devices were reviewed and discussed with responsible licensee representatives.  The inspectors reviewed Total Effective Dose Equivalent (TEDE) ALARA evaluations conducted for select U3 outage tasks.  Use of respiratory protective
equipment was evaluated for selected workers involved in U3 outage activities.  The
inspectors toured selected onsite compressors available for supplying breathing air for
current outage activities and reviewed Grade D or greater air certification for permanent and temporary on-site compressors used for supplied-line breathing air and self-contained breathing apparatus (SCBA) bottle fill-station activities.  Training, fit testing,
and medical qualifications for selected RP, maintenance, and operations using
respiratory protection for outage activities were reviewed and discussed with cognizant
licensee representatives.
Self-Contained Breathing Apparatus for Emergency Use:  The inspectors reviewed current status, operability and availability of select respiratory and SCBA equipment
 
maintained within the U3 and U4 control rooms, B5B lockers, and U3 and U4 reactor
auxiliary building locations.  Maintenance activities for selected respiratory protective
equipment (e.g., compressed gas cylinders, regulators, valves, and hose couplings), by certified vendor technicians were reviewed for selected SCBA units.  Training, fit testing, and medical qualifications for selected RP, maintenance, and operations staff assigned
Emergency Response Organization duties were reviewed and discussed with cognizant
licensee representatives.  For selected U3 and U4 control room operators, the
inspectors discussed and reviewed annual hands-on SCBA training activities, including donning, doffing, and functionally checking SCBA equipment, bottle change out, and also reviewed availability of corrective lens, as applicable, for on-shift personnel. 
 
Problem Identification and Resolution:  The inspectors reviewed selected CAP documents within the area of radiological airborne controls and respiratory protection
activities.  The inspectors evaluated the licensee's ability to identify and resolve the issues in accordance with licensee procedures PI-AA-104-1000, Corrective Action, Rev. 6, and 0-ADM-533, Corrective Action Program Guidance, Rev. 14.  The inspectors also
evaluated the scope of the licensee's internal audit program and reviewed recent
assessment results.  Specific licensee CAP documents reviewed for airborne
radionuclide concentration monitoring and mitigation are listed in the Attachment.
Radiation Protection program activities associated with airborne radioactivity monitoring and controls were evaluated against details and requirements documented in the
UFSAR, TS Section 3/4.9.9, Containment Ventilation System, 3/4.9.13, Radiation
Monitoring, and 6.8.1, Procedures and Programs; 10 CFR Part 20, and also approved
licensee procedures.  Documents reviewed are listed in the Attachment.
The inspectors completed all specified line-items detailed in IP 71124.03.
 
 
22      b. Findings
No findings were identified.
2RS4 Occupational Dose Assessment (IP 71124.04)
  a. Inspection Scope
The inspector evaluated current RP program guidance and its implementation for monitoring and assessing occupational workers' internal and external radiation exposure.  The review included quality assurance activities, results, and responses to
identified issues; and individual dose results for selected occupational workers. 
External Dosimetry:  The inspector reviewed and discussed RP program guidance for monitoring external and internal radiation exposures of occupational workers.  The
inspector verified National Voluntary Laboratory Accreditation Program certification data
and discussed program guidance for storage, processing and results for dosimeters
currently in use.  The inspector also reviewed and discussed the comparison between
 
ED and thermoluminescent dosimeter data.
Internal Dosimetry:  Program guidance, instrument detection capabilities, and select results for assessing internally deposited radionuclides were reviewed and discussed in
detail.  The inspector evaluated licensee follow-up
in vivo monitoring results and dose assignment for three workers involved in contamination events having the potential for
internal deposition of radioactive material.  In addition, the current licensee and contract vendor laboratory analysis capabilities for the collection and analysis of in vitro samples were reviewed and discussed in detail.
 
Special Dosimetric Situations:  The inspector reviewed monitoring conducted and results for two declared pregnant workers since the last inspection.  The methodology and results of monitoring occupational workers within non-uniform external dose fields and assignment of effective dose equivalent results were discussed in detail.  In addition, the
adequacy of dosimetry program guidance and its implementation for shallow dose
assessments and supporting calculations for an individual involved in a select
contamination event were evaluated.  Neutron monitoring guidance and implementation for select "at power" containment entries were reviewed and discussed.  RP staff proficiency involved in conducting skin dose assessments, neutron monitoring, and whole body counter (WBC) operations were evaluated through review and discussions
of completed records and supporting data. 
 
Problem Identification and Resolution:  The inspectors reviewed and discussed selected CAP documents associated with occupational dose assessment.  The reviewed items
included ARs, self-assessments, and quality assurance audit documents.  The
inspectors evaluated the licensee's ability to identify, characterize, prioritize, and resolve
the identified issues in accordance with licensee procedures PI-AA-104-1000, Corrective
Action, Rev. 6, and 0-ADM-533, Corrective Action Program Guidance, Rev. 14.
 
Radiation protection program occupational dose assessment guidance and activities were evaluated against the requirements of the UFSAR Section 11; TS Sections 6.8.1,
Procedures and Programs, and 6.12, High Radiation Area; 10 CFR Parts 19 and 20; and
approved licensee procedures.  Records reviewed are listed in the Attachment. 
23    The inspectors completed all specified line-items detailed in IP 71124.04.
      b. Findings
No findings were identified.
 
2RS5 Radiation Monitoring Instrumentation (IP 71124.05) 
    a. Inspection Scope
Radiation Monitoring Instrumentation:  During tours of the auxiliary building, turbine building, SFP areas, and RCA exit point, the inspectors observed installed radiation
detection equipment including the following instrument types: area radiation monitors (ARMs), airborne monitors, liquid and gaseous effluent monitors, PCMs, SAMs, and
portal monitors.  The inspectors observed the physical location of the components, and noted the material condition. 
In addition to equipment walkdowns, the inspectors observed source checks and alarm setpoint testing of various portable and fixed detection instruments, including ion chambers, telepoles, PCMs, SAMs, and portal monitors.  For the portable instruments,
the inspectors observed the use of a high-range check source and reviewed records of
periodic output value testing for a calibration source.  The inspectors reviewed recent
calibration records and evaluated alarm setpoint values for selected ARMs, PCMs, portal
monitors, SAMs, effluent monitors, and a WBC.  This included a sampling of instruments used for post-accident monitoring such as containment high-range ARMs and effluent monitor high-range noble gas and iodine channels.  Radioactive sources used to
calibrate selected ARMs and effluent monitors were evaluated for traceability to national
standards.  Calibration stickers on portable survey instruments and air samplers were
noted during inspection of storage areas for ready-to-use equipment.  The inspectors also reviewed countroom quality assurance records for gamma ray spectrometry equipment and liquid scintillation detectors. 
      Problem Identification and Resolution:  Selected licensee CAP documents associated
with instrumentation were reviewed and assessed.  The inspectors evaluated the
licensee's ability to identify and resolve the identified issues in accordance with licensee procedures.  The inspectors also reviewed recent self-assessment results. 
Operability and reliability of selected radiation detection instruments were reviewed
against details documented in the following: 10 CFR Part 20; NUREG-0737,
"Clarification of Three Mile Island Action Plan Requirements"; TS Section 3; UFSAR Chapters 11; and applicable licensee procedures.  Documents reviewed during the inspection are listed in the Attachment. 
  b. Findings
No findings were identified.
 
 
24  4OA1 Performance Indicator Verification (IP 71151)
.1 Barrier Integrity Cornerstone
    a. Inspection Scope
The inspectors reviewed licensee submittals for the U3 and U4 Performance Indicators
(PI) listed below for the period October 1, 2014, through September 30, 2015, to verify
the accuracy of the PI data reported during that period.  Performance indicator definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," and licensee procedure 0-ADM-032, "NRC Performance Indicators Turkey Point," were used to check the reporting for each data element.  The inspectors
checked operator logs, plant status reports, CRs, system health reports, and PI data
sheets to verify that the licensee had identified the required data, as applicable.  The inspectors interviewed licensee personnel associated with PI data collection, evaluation, and distribution.  This inspection constitutes four samples.
 
* U3 Mitigating Systems PIs
* U4 Mitigating Systems PIs
    b. Findings
No findings were identified.
.2 Radiation Safety Cornerstones
  a. Inspection Scope
Occupational Radiation Safety Cornerstone:  The inspectors reviewed recent Occupational Exposure Control Effectiveness PI results for the occupational radiation safety cornerstone, and reviewed PI records generated from October 2014 through
October 2015.  For the assessment period, the inspectors reviewed ED alarm logs and
selected CRs related to controls for exposure significant areas.  Documents reviewed
are listed in the Attachment.
Public Radiation Safety Cornerstone:  The inspectors reviewed recent radiological control effluent release occurrences PI results for the public radiation safety cornerstone,
and reviewed PI records generated from October 2014 through October 2015.  For the
assessment period, the inspectors reviewed cumulative and projected doses to the
public contained in liquid and gaseous release permits and CRs related to radiological effluent TS/Offsite Dose Calculation Manual issues.  Documents reviewed are listed in
the Attachment.
  b. Findings
No findings were identified.
 
25  4OA2 Problem Identification and Resolution (IP 71152)
.1 Daily Review
  a. Inspection Scope
As required by IP 71152, "Identification and Resolution of Problems," and to help identify
 
repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of items entered daily into the licensee's CAP.  This review was accomplished by reviewing daily printed summaries of ARs and by reviewing
the licensee's electronic AR database.  Additionally, RCS unidentified leakage was
checked on a daily basis to verify no substantive or unexplained changes.  Documents reviewed are listed in the Attachment.
    b. Findings
No findings were identified.
 
.2 Annual Sample:  Missed Fire Watch Tours
    a. Inspection Scope
  The inspectors selected AR 02056905, "Missed Fire Watch Tours" for a more in-depth review of the circumstances and the corrective actions that followed.  The AR report was reviewed to ensure that an appropriate evaluation was performed and corrective actions were specified and prioritized in accordance with the licensee's program.  Other attributes checked included disposition of operability and resolution of the problem,
including cause determination, past operability determination, and corrective actions. 
The inspectors interviewed plant personnel and evaluated the CR in accordance with the requirements of the licensee's corrective actions process as specified in licensee's procedures PI-AA-204, "Condition Identification and Screening Process," and PI-AA-205,
"Condition Evaluation and Corrective Action."  This inspection constitutes one sample.
    b. Findings and Observations
No inspector findings were identified.  A licensee-identified violation of very low safety significance (Green) is documented in Section 4OA7 of this report.  The licensee
identified that employees failed to perform hourly required fire watch roves.  The
inspectors noted that the licensee's evaluation for the missed fire watch roves concluded
that there was no violation of any TS requirement since TS do not require fire watches for degraded fire protection features.  The licensee concluded that the missed roves represented a reduction in the effectiveness of the Fire Protection Program (FPP) and
the loss of a defense-in-depth feature.   
 
The licensee determined the root cause of the event to be that operations management
was not engaged with the fire watch program.  The licensee also determined that a direct cause was that fire watch employees willfully chose non-compliance with fire protection requirements.  Immediate corrective actions for this event included the
immediate denial of site access for the individuals who failed to conduct the roves.  The
licensee also updated the fire protection procedure, 0-ADM-016.4, to include Operations 
26  Management Responsibilities and Oversight that requires observations, audits, and assessments to ensure regulatory requirements are met.  The licensee also conducted
an extent of condition and determined that no other missed tours were present in other departments based on data collected and security access logs.     
.3 Semi-Annual Trend
    a.  Inspection Scope
The inspectors performed a review of the licensee's records including ARs, CAP health reports, apparent cause evaluation reports, and various corrective action review board
reports to asses an adverse trend in the performance of reactor protection transmitters.  The inspectors reviewed licensee AR 02088175, which identified an adverse trend in
protection transmitter calibration check results.  The inspectors evaluated the effectiveness of the licensee's corrective actions and the significance of the problems, including attributes such as accurate documentation, reportability, evaluation, corrective
actions, and problem resolution.  This inspection constitutes one sample.
  b. Findings and Observations
No inspector findings were identified.  The licensee noted that the transmitters in
question, Rosemount pressure transmitters, are expected to drift a slight amount.  The
licensee also noted that both the transmitter age and replacement of components tended
to exacerbate the transmitter drift through the calibration cycle.  The licensee concluded
that even with the noted transmitter drift, the transmitters still performed satisfactorily and were within TS compliance.  The inspectors did not identify any additional trends not observed by the licensee's trending activities.
4OA5 Other Activities
.1 Independent Spent Fuel Storage Facility Walk down (IP 60855.1)
    a. Inspection Scope
On December 17, 2015, the inspector conducted a walk down of the ISFSI protected
area per IP 60855.1, "Operation of an ISFSI at Operating Plants."  The inspectors
observed each cask building temperature indicator and passive ventilation system to be free of any obstruction, allowing natural draft convection decay heat removal through the
air inlet and air outlet openings.  The inspectors observed associated cask building
structures to be structurally intact and radiation protection access and security controls
to the ISFSI area to be satisfactory.
    b. Findings
No findings were identified.
 
 
27  4OA6 Meetings
The resident inspectors presented the inspection results to Mr. Tom Summers and other members of licensee management on January 15, 2016.  The inspectors asked the licensee whether any of the material examined during the inspection should be
considered proprietary information.  The licensee did not identify any proprietary
 
information.
4OA7  Licensee-identified Violation
The following violation of very low safety significance (Green) was identified by the
licensee and is a violation of NRC requirements which meets the criteria of the NRC
Enforcement Policy for being dispositioned as an NCV.
10 CFR 50.48 states that each operating nuclear power plant must have a fire protection plan that satisfies Criterion 3 of Appendix A of this part.  Turkey Point Renewed
Operating License condition D, for Units 3 and 4, states that the licensee shall
implement and maintain in effect all provisions of the approved FPP as described in the UFSAR Appendix 9.6A.  The approved FPP is implemented, in part, by 0-ADM-016, Fire Protection Program, as referenced in Section 7.2 of UFSAR Appendix 9.6A.  Section 5.6 of 0-ADM-016 requires that, for non-functional post-fire safe shutdown components,
engineering evaluations should identify appropriate compensatory actions, including
hourly fire roves.  Contrary to the above, between May 1st, 2014, and April 23rd, 2015,
hourly fire watch patrols were not conducted on numerous occasions in fire zones that
required regular hourly tours due to fire protection equipment impairment.  The failure to perform the fire watch tours did not cause the inoperability of any equipment but resulted in the loss of a defense-in-depth feature for fire detection in fire zones affected by an
impaired or non-functional fire safety component or feature.  This violation was
associated with the Mitigating Systems Cornerstone and affected the cornerstone
objective of ensuring the availability, reliability and capability of the systems that respond to initiating events to prevent undesirable consequences.  The inspectors determined the finding to be of very low safety significance (Green) after performing a detailed risk
 
evaluation in accordance with Manual Chapter 0609, Appendix A, because the missed
fire watch tours reflected a low degradation of the Fire Prevention and Administrative
Controls FPP element in that other area fire protection defense-in-depth features such
as automatic fire detection (smoke detectors), automatic fire suppression capability (sprinklers), manual suppression capability (fire brigade), and safe shutdown capability from the main control room were still available.  The licensee entered this violation into
 
their CAP as AR 02056905.
ATTACHMENT:  SUPPLEMENTARY INFORMATION
 
Attachment SUPPLEMENTARY INFORMATION
  KEY POINTS OF CONTACT
  Licensee Personnel:
F. Banks, Quality Manager
 
C. Cashwell, Training Manager
P. Czaya, Licensing C. Domingos, Plant General Manager  T. Eck, Security Manager
 
M. Guth, Licensing Manager
O. Hanek, Licensing Engineer
 
A. Katz, Projects Manager
G. Melin, Operations Manager S. Mihalakea, Licensing
 
K. Ohara, Emergency Preparedness Manager
J. Pallin, Engineering Director
D. Sluszka, Work Controls Manager
B. Stamp, Operations Director T. Summers, Site Vice-President 
D. Barrow, Maintenance Director
R. Hess, General Operations Training Supervisor
M. Wilson, Operations Training Supervisor
 
  NRC Personnel:
B. Bishop, Senior Project Engineer
 
A. Beaston, Project Engineer
 
A. Vargas, Project Engineer
  LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
  Opened and Closed
05000251/2015004-01
NCV 
Failure to correctly follow procedure 3-PMI-072.6, "Steam Dump to
Atmosphere Control Loop Calibration."
(Section 1R20)
 
 
  LIST OF DOCUMENTS REVIEWED  
Section 1R01: Adverse Weather 0-ONOP-103.3, Severe Weather Preparations  
Section 1R04: Equipment Alignment 3-NOP-022, Emergency Diesel Generator Fuel Oil System 3-NOP-023, Emergency Diesel Generator  
4-NOP-022, Emergency Diesel Generator Fuel Oil System 4-NOP-023, Emergency Diesel Generator 3-OP-201, Filling/Draining the Refueling Cavity and the SFP Transfer Canal  
4-OP-201, Filling/Draining the Refueling Cavity and the SFP Transfer Canal  
P&ID 5613-M-3022, Emergency Diesel Engine and Oil System  
P&ID 5613-M-3062, Safety Injection System P&ID 5614-M-3062, Safety Injection System  
Section 1R05: Fire Protection 0-ONOP-016.10, Pre-Fire Plan Guidelines and Safe Shutdown Manual Actions  
Section 1R08: Inservice Inspection Activities  
Procedures: 0-ADM-537, Boric Acid Corrosion Control Program, Rev. 11  
3-OSP-045.1, ASME Section XI Quality Group A Bolting Examination, Rev. 2  
MA-AA-1000, Plant Leak Management Procedure, Rev. 6 NDE 4.15, Visual Examination (VE) ASME Section XI Code Case N-722-1 and N-729-1, Rev. 4 NDE 4.2, Visual Examination VT-2 Conducted During System Pressure Tests, Rev. 10  
NDE 4.3, Visual Examination VT-3, Rev. 12  
NDE 5.16, Ultrasonic Examination Technique for the Detection of Cracking in Feedwater Piping, Rev. 10 NDE 5.18, Ultrasonic Thickness Measurement, Rev. 8  
Calculations: EC 284178, Review of Degradation and Operational Assessments at End-of-Cycle 27 for  
Turkey Point Unit 3  
Work Orders/Work Requests: WO 4029647301, Valve 3-298C Replace Valve WO 4030098001, Repair of PZR HTR Sleeve #11  
 
CAP Documents: AR 1771920, Audit shows no self-assessments performed on the welding control program  
AR 1858601, BOP, ISI and FAC Quick Hit Self-Assessment for 2012 Outages (SL-1-24, SL-2-
AR 1858601, BOP, ISI and FAC Quick Hit Self-Assessment for 2012 Outages (SL-1-24, SL-2-
20, TP-3-26, TP-4-27) AR 2086224, Inconsistent gaps were identified bet
  20, TP-3-26, TP-4-27)
ween CRDM/RPI plates and the seismic plate  
AR 2086224, Inconsistent gaps were identified between CRDM/RPI plates and the seismic plate
bumper AR 2086933, Debris inside spring hanger  
  bumper
Miscellaneous Documents: 2012 Welding May 2012 Quality Assurance Assessment  
AR 2086933, Debris inside spring hanger
3  AES 13118520-2Q-3, Condition Monitoring and Operational Assessment for the Turkey Point Unit 3 Steam Generators Based on Eddy Current Examination End of Cycle 26, March 2014 Calibration Data Sheet for UT Instruments SN: 136P1106C031381, K07639 Calibration Data Sheet No.: 5.16-002 Certificate of Conformity NDE Probe SN: SE1110
Miscellaneous Documents:
Certificate of Personnel Qualification ID No.: D0360, C2231, C6756
2012 Welding May 2012 Quality Assurance Assessment
ENG-CSI -2.3, Steam Generator Integrity Program Administration, Rev. 32 ENG-CSI-2.2, Planning and Reporting Results of Steam Generator Tubing Examinations,  Rev. 44 ER-AP-116, Boric Acid Corrosion Control, Rev. 0 Focused Self-Assessment Report 1837244, Boric Acid Corrosion Control Program 
Krautkramer Transducer Certificate of Conformity SN: 012Y39
Personnel Certification Statement:  T. Thomas, B. Thompson, M. Smith, and M. Johnson
Quick Hit Assessment Report 1892958, Boric Acid Corrosion Control Leak Evaluations Ultrasonic Instrument Calibration Data Record and Certification SN: 01R6B7 Visual Examination Evaluation Sheet: 4.3.001
Visual Examination Record Data Sheets: #4.3-008 and #4.3-009
Section 1R11:  Licensed Operator Requalification Process 0-ADM-211, Emergency and Off-Normal Operating Procedure Usage
TR-AA-230-1007, Conduct of Simulator Training and Evaluation 
TR-AA-220-1004, Licensed Operator Continuing Training Annual Operating and Biennial   
 
  Written Exams, Revision 1
TR-AA-230-1004, SAT Implementation, Revision 5
PTN OPS LOC15 SRO EXM1, Administered 10/06/2015 PTN OPS LOC15 SRO EXM2, Administered 11/29/2015
Section 1R15:  Operability Evaluations 0-ADM-213, Technical Specification Related Equipment Out of Service Logbook 0-ADM-226, Operability Screening and Condition Reports EN-AA-203-1001, Operability Determinations and Assessments
Section 1R18:  Plant Modifications 5610-M-410-40, NX Seal Assembly SPEC-C-021, Turkey Point Units 3 & 4 Tubing and Tubing Supports
 
WO 40419666 
Section 1R19:  Post Maintenance Testing 0-ADM-737, Post Maintenance Testing MA-AA-203-1000, Maintenance Functional Testing
 
Section 1R20:  Refueling and Other Outage Activities
0-ADM-009, Containment Closeout Inspection MA-AA-101-1000, Foreign Material Exclusion Procedure
0-ADM-556, Fuel Assembly and Insert Shuffles
 
Section 2RS1:  Radiological Hazard Assessment and Exposure Controls
  Procedures, Guidance Documents, and Manuals 0-HPA-001, Radiation Work Permit Initiation and Termination, Rev. 4 
4  RP-AA-102-1000, Alpha Monitoring, Rev. 2
RP-AA-103-1006, Conduct of Radiological Diving Operations, Rev. 1
RP-AA-107, Radioactive Material Control Program, Rev. 0 RP-AA-107-1003, Unconditional and Conditional Release of Material, Rev. 1 RP-SR-103-1001, Posting Requirements for Radiological Hazards, Rev. 2
RP-SR-103-1002, High Radiation Area Controls, Rev. 3
RP-SR-103-1008, Remote Monitoring, Rev. 5
0-HPS-025.2, Posting and Survey Requirements for Fuel Movement, Rev. 4B
0-HPS-027.1, Work Controls in Hot Particle Areas, Rev. 0 0-HPS-106, Survey & Posting Guidelines for Plant Evolutions, Rev. 5
Records and Data Reviewed 2015 NSTS Annual Inventory Reconciliation, Dated 01/15/15
 
Radioactive Source Leak Test Results, Dated 10/15/2015 Air Calculation Sheet, (ACS) A/S Log Ref No. P1-15-1023, U3 RCB REACTOR Sump During Demob, Dated 11/17/2015 ACS, A/S Log Ref No. P0-15-1011, U3 RCB 30' 6" Routine, Dated 11/17/2015
ACS, A/S Log Ref No. P0-15-1013, Vac Shack During Tool & Respirator Decon, Dated
11/17/2015 ACS, A/S Log Ref No. P0-15-1021, U3 RCB 58' By REACTOR Head Stand, Dated 11/17/2015 ACS, A/S Log Ref No. P0-15-1025, U3 RCB Upper REACTOR Cavity, Dated 11/17/2015
PTN-M-20150604-3, U4 10 Foot Pipeway, Dated 06/04/2015
PTN-M-20150930-2, U4 10 Foot Pipeway, Dated 09/30/2015
PTN-M-20150914-1, U3 10 Foot Pipeway, Dated 09/14/2015
PTN-M-20150930-3, U3 10 Foot Pipeway, Dated 09/30/2015 PTN-M-20150711-25, U4 "B" RHR Pump Room, Dated 07/11/2015 PTN-M-20151010-2, U4 "B" RHR Pump Room, Dated 10/10/2015
PTN-M-20150918-5, U4 Charging Pump Room, Dated 09/18/2015
PTN-M-20151011-7, U4 Charging Pump Room, Dated 10/11/2015
PTN-M-20141120-6, Unit 4 "B" RHR Dose Alarm Follow-up, Dated 11/20/2014 PTN-M-20151020-6, Aux Bldg 3-240 Valve, Dated 10/20/2015 PTN-M-20151021-25, U3 Containment 14 ft elev Inside Biowall, Dated 10/21/2015
PTN-M-20151022-15, U3 Containment 14 ft elev Inside Biowall, Dated 10/22/2015
PTN-M-20151027-30, U3 Containment 14 ft elev Inside Biowall, Dated 10/27/2015
PTN-M-20150311-6, ISFSI Pad Semi-Annual, Dated 03/11/2015
PTN-M- 20150918-6, ISFSI Pad Semi-Annual, Dated 09/18/2015 RWP Number (No.) 15-3000 U3R28 Initial Containment Entry and when Containment is posted as a Locked High Radiation Area, Rev. 0 RWP No. 15-3008, Containment General Outage Maintenance (Bulk Work), Rev 0
RWP No. 15-3013, Regenerative Heat Exchanger Room Work (Bulk Work), Rev. 0
RWP No. 15-3014, Reactor Sump - Non Legacy Boric Acid Work, Rev. 0 RWP No. 15-3018, RCP Work (Bulk Work), Rev. 0 RWP No. 15-3205, Outage Locked High Radiation Area Work, Rev. 0
 
CAP Documents Nuclear Oversight Report # PTN-14-002, Radiation Protection and Radwaste, Dated
08/18/2014
AR 01996578
AR 01997251
 
AR 01997991 
5  AR 02006239
 
AR 02008430
 
AR 02009674
AR 02020231
AR 02024963
 
AR 02029276
 
AR 02033046
 
AR 02033644
 
AR 02044544
AR 02044742
AR 02049552
 
AR 02058970
Section 2RS2:  ALARA
Procedures and Guidance Documents 0-HPA-001, Radiation Work Permit Initiation and Termination, Rev. 04
0-HPA-072, Installation, Control, and Removal of Permanent and Temporary Shielding, Rev. 03
RP-AA-104, ALARA Program, Rev. 04 RP-AA-104-100, ALARA Implementing Procedure, Rev. 06
RP-AA-104-2003, Five Year ALARA Plan Template, Rev. 01
Primary Strategic Water Chemistry Plan, FPL PTN Units 3 & 4, 08/15/2013
 
Records and Data Reviewed 10 CFR Applicability Determination Form, TSR 15-03, Temporary Lead Shielding Installation on Containment 14' Cavity Drain Valves, 10/18/15 ALARA Review No. 2015-006, U3R28 Refueling Activities, Including Ultra-Sonic Fuel Cleaning, Rev. 0 ALARA Review No. 2015-007, Generator Bundle Flush, Sludge Lance, and FOSAR, Rev. 0
ALARA Review No. 2015-008, U3 A, B, C RCP Seal Replacement - Fukushima Upgrade - A Motor Replacement, and PMs. Rev. 0 ALARA Review No. 2015-010, U3 BMI (Bottom Mounted Inspection), Rev. 0
ALARA Review No. 2015-013, PCV-3-455A and PCV-3-455B, Rev. 0
Job-In-Progress Review No. 2015-007, S/G secondary sludge lancing and FOSAR, Rev. 0
Job-In-Progress Review No. 2015-008, U3 A,B,C RCP Seal Replacement, Rev. 0
Job-In-Progress Review No. 2015-010, U3 BMI, Rev. 0 PTN ALARA Review Board Meeting Minutes, 03/23/15, 06/29/15, 09/04/15
PTN Nuclear Oversight Report #PTN-14-002, Subject: Radiological Protection and Radwaste, 05/09/14 PTN Quick Hit Assessment Report #1938751/1927754, "Self Assessment of ALARA", 04/23/14
PTN-3-R28 Refueling Outage 0500 Turnover 11/03/15, 11/05/15 PTN-3-R28 Refueling Outage 1700 Turnover 11/12/15 PTN 5-Year ALARA Plan 2015-2020 
RP Survey #PTN-M-20151029-34, Unit 3 Regenerative Heat Exchangers 14', 10/29/2015 RP Survey #PTN-M-20151029-27, Unit 3 Regenerative Heat Exchangers 14', 10/28/2015 RP Survey #PTN-M-20151028-36, U3 Containment 14' Inside Biowall, 10/28/2015 RP Survey #PTN-M-20151026-22, U3 Containment 14' Inside Biowall, 10/26/2015 RP Survey #PTN-M-20151020-19, U3 Containment 14' Inside Biowall, 10/20/2015
 
6  Temporary Shielding Request (TSR) No. 2015-03, U3 RCB, 14' Elevation, Cavity Drain Valves, 07/20/2015 TSR No. 2015-17, U3 RCB, 14' Regen. Heat Exchanger Room, 07/22/2015
CAP Documents
AR 01921887
 
AR 01997991
 
AR 01909707
 
AR 02072141
AR 01997680
AR 02043416
 
AR 02038064
 
Section 2RS3:  In-Plant Airborne Radioactivity Control and Mitigation
Procedures and Guidance Documents 0-ADM-041, PTN Respiratory Protection Plan, Rev. 9
0-ADM-533, Corrective Action Program Guidance, Rev. 14
0-ADM-605, Control of Radioactive Material, Rev. 4 0-HPA-028, High Efficiency Particulate Air (HEPA) Filtration Ventilation Systems in the Radiation Controlled Area, Rev. 2A 0-HPS-062.2, Use of the Self-Contained Breathing Apparatus, Rev.1 
0-HPS-063.2, Maintenance and Accountability of Respiratory Protective Equipment, Rev. 7 
0-HPS-063.4, Selection and Issuance of Respiratory Protection Equipment, Rev. 3
0-HPS-065.2, Operation and Maintenance of the Respirator Fit-Test System, Rev. 4 0-HPS-090, Inventory of Radiation Protection Emergency Equipment, Rev. 2 PI-AA-104-1000, Corrective Action, Rev. 6
RP-AA-102-1000, Alpha Monitoring, Rev. 2
RP-TP-102-1001, Radiological Air Sample Assay, Rev. 4
 
Records and Data Reviewed  Air Sample Log, for the period 10/1 thru 11/5/2015 Air Calculation Sheet and Gamma Spectroscopy Analysis, Air Sample # P1-I1-15-0405, U-3 RCB Lower Reactor Cavity, 10/26/2015 Certificate of Testing, PortaCount Bench 2, S/N 8030111513, 07/08/2015; and S/N 8030111601, 06/10/2015 HP-90, SCBA Inventory, Inspection, and Repair Records, September and October 2015 HP-93Respirator, Inventory, Inspection, and Repair Record, September and October 2015
HP-93.1, SCBA Air Bottle Inspection and Inventory Records, September and October 2015
HP-93.6, Air Quality Certificate, Bauer Air Compressor, Dated 08/05/2015, and 05/11/2015
List of SCBA Qualified Operations, Maintenance, and Health Physics Personnel, 10/01/2015 Scott Authorized Service Center Certificates for selected vendor employees, Dated 08/22/2014 Scott PosiChek3, Visual/Functional Test Results, Regulators:  89200090, Dated 09/22/2015; 89200100, Dated 09/23/2015; 89200101, Dated 09/22/2015; 89200109, Dated
09/22/2015; and 89200149, Dated 09/23/2015; Unitech Service Group, DOP Test Results, HEPA Unit Type, Portable, HEPA S/N 018, Dated 06/23/2015; S/N 033, Dated 06/23/2015; and S/N 040, Dated 06/24/2015 Vendor Laboratory Compressed Air/Gas Quality Testing Report Results, Bauer Air Compressor, Dated 08/05/2015, and 07/31/2015
 
7  CAP Documents Quick Hit/Department Assessment Report, 2014 Respiratory Protection Program Annual Review (AR 2014222), 04/07/2015
AR 01911462
AR 01845706
 
AR 01877007
 
AR 01889000
 
AR 01900277
 
AR 01964422
AR 01997251
AR 01938504
 
AR 02057725
 
AR 02020932
Section 2RS4: Occupational Dose Assessment
  Procedures and Guidance Documents 0-HPA-030, Personnel Monitoring of External Dose, Rev. 3
0-HPS-023, Environmental Radiation Monitoring, Rev. 1 0-HPS-026.2, Response Protocols for Whole Body Counting Entrance and Exit, Rev. 3 0-HPS-031.1, Whole Body Dosimetry Issue, Rev. 3A
0-HPS-031.2, Multibadge Exposure Monitoring, Rev. 0B
RP-AA-101-2004, Method for Monitoring and Assigning Effective Dose Equivalent (EDE) for 
High Dose Gradient Work, Rev. 3
RP-SR-101-1003, Personnel Contamination Monitoring and Decontamination, Rev. 3 RP-TP-101-1005, Internal Dose Assessment, Rev. 1
RP-TP-101-1000, Exposure Investigations, Rev. 0A
RP-TP-102-1002, Hard to Detect Radionuclides and Contamination Controls, Rev. 1
RP-TP-105-3008, Operation of the Radiation Protection Apex-In Vivo Whole Body Counting 
Equipment, Rev. 2
Records and Data Reviewed  ABACOS-2000 Nuclide Libraries, 11/05/2015
Alpha Smear Log, 01/08/2015 thru 11/05/2015
Dosimetry Task Matrix, Daily Fastscan QC Check, October 2015
Extended Fastscan QA File Control Charts, 10/06/2015 thru 11/04/2015 Extended Fastscan WBC System Calibration Report, System # 97-7040, 10/23/2013 and
10/22/2014 EDE Multibadge Datasheets, Pack ID# 5010 and 5012, 11/04/2015
"Fastscan 1" WBC System Calibration Report, System # 97-7040, 10/23/2013 and 10/22/2014
 
HP-55A, Turkey Point Plant Environmental Radiation Controlled Area Radiation Levels Results Log [including ISFSI], 06/24/14 thru 12/26/14
HP-55A, Turkey Point Plant Environmental Radiation Controlled Area Radiation Levels Results Log [including ISFSI], 12/26/14 thru 6/23/15 NVLAP Lab Code 100555-0, On-Site Assessment Report and Accreditation Certificate, 06/11/2015 QA 1000 File, "2013 Alpha Smear Summary: Unit 4 R27 Refueling Outage", 06/13/2014 Sensitivity Study of Personnel Contamination Monitors used at Turkey Point Nuclear Station, 02/10/2010
 
8  Technical Support Document No. 15-058, Rev 00, Neutron Dosimetry Evaluation at Turkey Point Nuclear Power Plant, 08/21/2015 Report, Turkey Point 2015 Site TEDE Dose, Top 25, 11/04/2015
Report, Turkey Point 2015 Annual (all sites) TEDE, Top 25, 11/04/2015
CAP Documents
AR 01861722
 
AR 01940206
 
AR 01959134
AR 01979141
AR 02013453
 
AR 02024069
 
AR 02076960
 
2RS5:  Radiation Monitoring Instrumentation
Procedures 0-HPT-072, Calibration and Operation of Canberra Personnel Monitors, Rev. 2
0-HPT-018, Calibration of Survey Instruments, Rev. 4 0-HPT-010, Radiation Protection Instrument Plan, Rev. 6 RP-TP-105-3007, Operation and Calibration of the GEM-5 Gamma Exit Monitor, Rev 4
 
Calibrations and Data Work Order 40033883, ARMS Cal Inside Containment (RD-1401-03), 02/2012
Work Order 40323168, ARMS Cal Inside Containment (RD-1401-03), 03/2014 Work Order 40170223, T.S R-4-19 S/G Liquid Sample PRMS Cal, 05/2013 Work Order 40280868, T.S R-4-19 S/G Liquid Sample PRMS Channel CAL, 12/2014
Work Order 40273313, T.S. Plt Vent SPING Rad-6304 PM Cal, 09/2014
Work Order 40113819, T.S. Plt Vent SPING Rad-6304 PM Cal, 12/2012
Work Order 40161233, T.S. RAD-6311 A/B Cont HI Range ARMS CAL Per 3-PMI-066.3, 02/2013 Work Order 40219065, T.S. RAD-6311 A/B Cont HI Range ARMS CAL Per 3-PMI-066.3, 03/2014 Work Order 40323168, T.S. RD-4-15 SJAE 18 Monthly PM CAL, 01/2015
Work Order 40247970, T.S. RD-4-15 SJAE Spiking cause alarms, 07/2013
Calibration of the FASTSCAN WBC System #97-7040, 10/2013 & 10/2014 HP-7:5.4 CRONOS Calibration Records for #1302-27, 09/24/14 & 03/19/14; #0912-039 , 10/02/2014 & 10/11/2013; #1005-048 05/26/2015 & 06/09/2014; #1005-049 04/27/2015 &
04/29/2014; #1006-037 06/15/2015 & 06/20/2014; #1302-029 07/22/2015 & 07/22/2014;
#1302-028 01/13/12015 & 07/23/2014. GEM-5 Calibration Certificates: #1423, #1424, 07/2014 & 07/2013; #1425 07/2014 & 06/2015 Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-107, 03/2015 Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-107, 03/2014
Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-107, 01/2014
Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-108, 07/2015
Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-108, 01/2015
Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #1107-185, 03/2015 Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #1107-185, 02/2015 System Health Report 07/01/2015-09/30/2015
F & J Model LV-14M Calibration Record Serial #s 4029, 4030, 4031, 06/2015 
9  Calibration of the Count Room MCA System, Detector Two, 06/2014
RADECO H809V/C Air Sampler Calibration Record, HPI# 1485E 02/2015
Controlled Settings- Eberline AMS 4, #1847, 10/2015; #2551, 10/2015; #1836 10/2015,  #1283 8/2015, #1080 08/2015, #12872 05/2015, #1638 08/2015, #1079 08/2015 Radiation Detection Instrument Calibration and Maintenance Record, Telepole #6605-081, 11/12/2015 & 05/07/2015; RO-20 #105 10/22/2015 HP-7-21, Shepard Model 89 Shielded Range Calibrator Certification Form, 02/2015
 
CAP Documents PTN-14-002, Radiological Protection and Radwaste Audit, 03/03/2014


AR 01895614
                                              3
AES 13118520-2Q-3, Condition Monitoring and Operational Assessment for the Turkey Point
  Unit 3 Steam Generators Based on Eddy Current Examination End of Cycle 26, March 2014
Calibration Data Sheet for UT Instruments SN: 136P1106C031381, K07639
Calibration Data Sheet No.: 5.16-002
Certificate of Conformity NDE Probe SN: SE1110
Certificate of Personnel Qualification ID No.: D0360, C2231, C6756
ENG-CSI -2.3, Steam Generator Integrity Program Administration, Rev. 32
ENG-CSI-2.2, Planning and Reporting Results of Steam Generator Tubing Examinations,
  Rev. 44
ER-AP-116, Boric Acid Corrosion Control, Rev. 0
Focused Self-Assessment Report 1837244, Boric Acid Corrosion Control Program
Krautkramer Transducer Certificate of Conformity SN: 012Y39
Personnel Certification Statement: T. Thomas, B. Thompson, M. Smith, and M. Johnson
Quick Hit Assessment Report 1892958, Boric Acid Corrosion Control Leak Evaluations
Ultrasonic Instrument Calibration Data Record and Certification SN: 01R6B7
Visual Examination Evaluation Sheet: 4.3.001
Visual Examination Record Data Sheets: #4.3-008 and #4.3-009
Section 1R11: Licensed Operator Requalification Process
0-ADM-211, Emergency and Off-Normal Operating Procedure Usage
TR-AA-230-1007, Conduct of Simulator Training and Evaluation
TR-AA-220-1004, Licensed Operator Continuing Training Annual Operating and Biennial
Written Exams, Revision 1
TR-AA-230-1004, SAT Implementation, Revision 5
PTN OPS LOC15 SRO EXM1, Administered 10/06/2015
PTN OPS LOC15 SRO EXM2, Administered 11/29/2015
Section 1R15: Operability Evaluations
0-ADM-213, Technical Specification Related Equipment Out of Service Logbook
0-ADM-226, Operability Screening and Condition Reports
EN-AA-203-1001, Operability Determinations and Assessments
Section 1R18: Plant Modifications
5610-M-410-40, NX Seal Assembly
SPEC-C-021, Turkey Point Units 3 & 4 Tubing and Tubing Supports
WO 40419666
Section 1R19: Post Maintenance Testing
0-ADM-737, Post Maintenance Testing
MA-AA-203-1000, Maintenance Functional Testing
Section 1R20: Refueling and Other Outage Activities
0-ADM-009, Containment Closeout Inspection
MA-AA-101-1000, Foreign Material Exclusion Procedure
0-ADM-556, Fuel Assembly and Insert Shuffles
Section 2RS1: Radiological Hazard Assessment and Exposure Controls
Procedures, Guidance Documents, and Manuals
0-HPA-001, Radiation Work Permit Initiation and Termination, Rev. 4


AR 02035780
                                          4
RP-AA-102-1000, Alpha Monitoring, Rev. 2
RP-AA-103-1006, Conduct of Radiological Diving Operations, Rev. 1
RP-AA-107, Radioactive Material Control Program, Rev. 0
RP-AA-107-1003, Unconditional and Conditional Release of Material, Rev. 1
RP-SR-103-1001, Posting Requirements for Radiological Hazards, Rev. 2
RP-SR-103-1002, High Radiation Area Controls, Rev. 3
RP-SR-103-1008, Remote Monitoring, Rev. 5
0-HPS-025.2, Posting and Survey Requirements for Fuel Movement, Rev. 4B
0-HPS-027.1, Work Controls in Hot Particle Areas, Rev. 0
0-HPS-106, Survey & Posting Guidelines for Plant Evolutions, Rev. 5
Records and Data Reviewed
2015 NSTS Annual Inventory Reconciliation, Dated 01/15/15
Radioactive Source Leak Test Results, Dated 10/15/2015
Air Calculation Sheet, (ACS) A/S Log Ref No. P1-15-1023, U3 RCB REACTOR Sump During
        Demob, Dated 11/17/2015
ACS, A/S Log Ref No. P0-15-1011, U3 RCB 30 6 Routine, Dated 11/17/2015
ACS, A/S Log Ref No. P0-15-1013, Vac Shack During Tool & Respirator Decon, Dated
        11/17/2015
ACS, A/S Log Ref No. P0-15-1021, U3 RCB 58 By REACTOR Head Stand, Dated 11/17/2015
ACS, A/S Log Ref No. P0-15-1025, U3 RCB Upper REACTOR Cavity, Dated 11/17/2015
PTN-M-20150604-3, U4 10 Foot Pipeway, Dated 06/04/2015
PTN-M-20150930-2, U4 10 Foot Pipeway, Dated 09/30/2015
PTN-M-20150914-1, U3 10 Foot Pipeway, Dated 09/14/2015
PTN-M-20150930-3, U3 10 Foot Pipeway, Dated 09/30/2015
PTN-M-20150711-25, U4 B RHR Pump Room, Dated 07/11/2015
PTN-M-20151010-2, U4 B RHR Pump Room, Dated 10/10/2015
PTN-M-20150918-5, U4 Charging Pump Room, Dated 09/18/2015
PTN-M-20151011-7, U4 Charging Pump Room, Dated 10/11/2015
PTN-M-20141120-6, Unit 4 B RHR Dose Alarm Follow-up, Dated 11/20/2014
PTN-M-20151020-6, Aux Bldg 3-240 Valve, Dated 10/20/2015
PTN-M-20151021-25, U3 Containment 14 ft elev Inside Biowall, Dated 10/21/2015
PTN-M-20151022-15, U3 Containment 14 ft elev Inside Biowall, Dated 10/22/2015
PTN-M-20151027-30, U3 Containment 14 ft elev Inside Biowall, Dated 10/27/2015
PTN-M-20150311-6, ISFSI Pad Semi-Annual, Dated 03/11/2015
PTN-M- 20150918-6, ISFSI Pad Semi-Annual, Dated 09/18/2015
RWP Number (No.) 15-3000 U3R28 Initial Containment Entry and when Containment is posted
        as a Locked High Radiation Area, Rev. 0
RWP No. 15-3008, Containment General Outage Maintenance (Bulk Work), Rev 0
RWP No. 15-3013, Regenerative Heat Exchanger Room Work (Bulk Work), Rev. 0
RWP No. 15-3014, Reactor Sump - Non Legacy Boric Acid Work, Rev. 0
RWP No. 15-3018, RCP Work (Bulk Work), Rev. 0
RWP No. 15-3205, Outage Locked High Radiation Area Work, Rev. 0
CAP Documents
Nuclear Oversight Report # PTN-14-002, Radiation Protection and Radwaste, Dated
        08/18/2014
AR 01996578
AR 01997251
AR 01997991


AR 01945528
                                          5
AR 02006239
AR 02008430
AR 02009674
AR 02020231
AR 02024963
AR 02029276
AR 02033046
AR 02033644
AR 02044544
AR 02044742
AR 02049552
AR 02058970
Section 2RS2: ALARA
Procedures and Guidance Documents
0-HPA-001, Radiation Work Permit Initiation and Termination, Rev. 04
0-HPA-072, Installation, Control, and Removal of Permanent and Temporary Shielding, Rev. 03
RP-AA-104, ALARA Program, Rev. 04
RP-AA-104-100, ALARA Implementing Procedure, Rev. 06
RP-AA-104-2003, Five Year ALARA Plan Template, Rev. 01
Primary Strategic Water Chemistry Plan, FPL PTN Units 3 & 4, 08/15/2013
Records and Data Reviewed
10 CFR Applicability Determination Form, TSR 15-03, Temporary Lead Shielding Installation on
  Containment 14 Cavity Drain Valves, 10/18/15
ALARA Review No. 2015-006, U3R28 Refueling Activities, Including Ultra-Sonic Fuel Cleaning,
  Rev. 0
ALARA Review No. 2015-007, Generator Bundle Flush, Sludge Lance, and FOSAR, Rev. 0
ALARA Review No. 2015-008, U3 A, B, C RCP Seal Replacement - Fukushima Upgrade - A
  Motor Replacement, and PMs. Rev. 0
ALARA Review No. 2015-010, U3 BMI (Bottom Mounted Inspection), Rev. 0
ALARA Review No. 2015-013, PCV-3-455A and PCV-3-455B, Rev. 0
Job-In-Progress Review No. 2015-007, S/G secondary sludge lancing and FOSAR, Rev. 0
Job-In-Progress Review No. 2015-008, U3 A,B,C RCP Seal Replacement, Rev. 0
Job-In-Progress Review No. 2015-010, U3 BMI, Rev. 0
PTN ALARA Review Board Meeting Minutes, 03/23/15, 06/29/15, 09/04/15
PTN Nuclear Oversight Report #PTN-14-002, Subject: Radiological Protection and Radwaste,
  05/09/14
PTN Quick Hit Assessment Report #1938751/1927754, Self Assessment of ALARA, 04/23/14
PTN-3-R28 Refueling Outage 0500 Turnover 11/03/15, 11/05/15
PTN-3-R28 Refueling Outage 1700 Turnover 11/12/15
PTN 5-Year ALARA Plan 2015-2020
RP Survey #PTN-M-20151029-34, Unit 3 Regenerative Heat Exchangers 14, 10/29/2015
RP Survey #PTN-M-20151029-27, Unit 3 Regenerative Heat Exchangers 14, 10/28/2015
RP Survey #PTN-M-20151028-36, U3 Containment 14 Inside Biowall, 10/28/2015
RP Survey #PTN-M-20151026-22, U3 Containment 14 Inside Biowall, 10/26/2015
RP Survey #PTN-M-20151020-19, U3 Containment 14 Inside Biowall, 10/20/2015


AR 02042545
                                              6
AR 02009932
Temporary Shielding Request (TSR) No. 2015-03, U3 RCB, 14 Elevation, Cavity Drain Valves,
Section 4OA1: Performance Indicator Verification 0-ADM-032, NRC Performance Indicators Turkey Point, Rev. 5  
  07/20/2015
List of Dose and Dose Rate Alarms October 1, 2014 to September 30, 2015 Monthly Gaseous Dose Report, October 2015  
TSR No. 2015-17, U3 RCB, 14 Regen. Heat Exchanger Room, 07/22/2015
Monthly Liquid Dose Report, October 2015  
CAP Documents
AR 01921887
AR 01997991
AR 01909707
AR 02072141
AR 01997680
AR 02043416
AR 02038064
Section 2RS3: In-Plant Airborne Radioactivity Control and Mitigation
Procedures and Guidance Documents
0-ADM-041, PTN Respiratory Protection Plan, Rev. 9
0-ADM-533, Corrective Action Program Guidance, Rev. 14
0-ADM-605, Control of Radioactive Material, Rev. 4
0-HPA-028, High Efficiency Particulate Air (HEPA) Filtration Ventilation Systems in the
        Radiation Controlled Area, Rev. 2A
0-HPS-062.2, Use of the Self-Contained Breathing Apparatus, Rev.1
0-HPS-063.2, Maintenance and Accountability of Respiratory Protective Equipment, Rev. 7
0-HPS-063.4, Selection and Issuance of Respiratory Protection Equipment, Rev. 3
0-HPS-065.2, Operation and Maintenance of the Respirator Fit-Test System, Rev. 4
0-HPS-090, Inventory of Radiation Protection Emergency Equipment, Rev. 2
PI-AA-104-1000, Corrective Action, Rev. 6
RP-AA-102-1000, Alpha Monitoring, Rev. 2
RP-TP-102-1001, Radiological Air Sample Assay, Rev. 4
Records and Data Reviewed
Air Sample Log, for the period 10/1 thru 11/5/2015
Air Calculation Sheet and Gamma Spectroscopy Analysis, Air Sample # P1-I1-15-0405, U-3
        RCB Lower Reactor Cavity, 10/26/2015
Certificate of Testing, PortaCount Bench 2, S/N 8030111513, 07/08/2015; and S/N
        8030111601, 06/10/2015
HP-90, SCBA Inventory, Inspection, and Repair Records, September and October 2015
HP-93Respirator, Inventory, Inspection, and Repair Record, September and October 2015
HP-93.1, SCBA Air Bottle Inspection and Inventory Records, September and October 2015
HP-93.6, Air Quality Certificate, Bauer Air Compressor, Dated 08/05/2015, and 05/11/2015
List of SCBA Qualified Operations, Maintenance, and Health Physics Personnel, 10/01/2015
Scott Authorized Service Center Certificates for selected vendor employees, Dated 08/22/2014
Scott PosiChek3, Visual/Functional Test Results, Regulators: 89200090, Dated 09/22/2015;
        89200100, Dated 09/23/2015; 89200101, Dated 09/22/2015; 89200109, Dated
        09/22/2015; and 89200149, Dated 09/23/2015;
Unitech Service Group, DOP Test Results, HEPA Unit Type, Portable, HEPA S/N 018, Dated
        06/23/2015; S/N 033, Dated 06/23/2015; and S/N 040, Dated 06/24/2015
Vendor Laboratory Compressed Air/Gas Quality Testing Report Results, Bauer Air Compressor,
        Dated 08/05/2015, and 07/31/2015


2014 Annual Radioactive Effluent Report  
                                            7
CAP Documents
Quick Hit/Department Assessment Report, 2014 Respiratory Protection Program Annual
        Review (AR 2014222), 04/07/2015
AR 01911462
AR 01845706
AR 01877007
AR 01889000
AR 01900277
AR 01964422
AR 01997251
AR 01938504
AR 02057725
AR 02020932
Section 2RS4: Occupational Dose Assessment
Procedures and Guidance Documents
0-HPA-030, Personnel Monitoring of External Dose, Rev. 3
0-HPS-023, Environmental Radiation Monitoring, Rev. 1
0-HPS-026.2, Response Protocols for Whole Body Counting Entrance and Exit, Rev. 3
0-HPS-031.1, Whole Body Dosimetry Issue, Rev. 3A
0-HPS-031.2, Multibadge Exposure Monitoring, Rev. 0B
RP-AA-101-2004, Method for Monitoring and Assigning Effective Dose Equivalent (EDE) for
  High Dose Gradient Work, Rev. 3
RP-SR-101-1003, Personnel Contamination Monitoring and Decontamination, Rev. 3
RP-TP-101-1005, Internal Dose Assessment, Rev. 1
RP-TP-101-1000, Exposure Investigations, Rev. 0A
RP-TP-102-1002, Hard to Detect Radionuclides and Contamination Controls, Rev. 1
RP-TP-105-3008, Operation of the Radiation Protection Apex-In Vivo Whole Body Counting
  Equipment, Rev. 2
Records and Data Reviewed
ABACOS-2000 Nuclide Libraries, 11/05/2015
Alpha Smear Log, 01/08/2015 thru 11/05/2015
Dosimetry Task Matrix, Daily Fastscan QC Check, October 2015
Extended Fastscan QA File Control Charts, 10/06/2015 thru 11/04/2015
Extended Fastscan WBC System Calibration Report, System # 97-7040, 10/23/2013 and
  10/22/2014
EDE Multibadge Datasheets, Pack ID# 5010 and 5012, 11/04/2015
Fastscan 1 WBC System Calibration Report, System # 97-7040, 10/23/2013 and 10/22/2014
HP-55A, Turkey Point Plant Environmental Radiation Controlled Area Radiation Levels Results
  Log [including ISFSI], 06/24/14 thru 12/26/14
HP-55A, Turkey Point Plant Environmental Radiation Controlled Area Radiation Levels Results
  Log [including ISFSI], 12/26/14 thru 6/23/15
NVLAP Lab Code 100555-0, On-Site Assessment Report and Accreditation Certificate,
  06/11/2015
QA 1000 File, 2013 Alpha Smear Summary: Unit 4 R27 Refueling Outage, 06/13/2014
Sensitivity Study of Personnel Contamination Monitors used at Turkey Point Nuclear Station,
  02/10/2010


AR 01909707
                                            8
Technical Support Document No. 15-058, Rev 00, Neutron Dosimetry Evaluation at Turkey
    Point Nuclear Power Plant, 08/21/2015
Report, Turkey Point 2015 Site TEDE Dose, Top 25, 11/04/2015
Report, Turkey Point 2015 Annual (all sites) TEDE, Top 25, 11/04/2015
CAP Documents
AR 01861722
AR 01940206
AR 01959134
AR 01979141
AR 02013453
AR 02024069
AR 02076960
2RS5: Radiation Monitoring Instrumentation
Procedures
0-HPT-072, Calibration and Operation of Canberra Personnel Monitors, Rev. 2
0-HPT-018, Calibration of Survey Instruments, Rev. 4
0-HPT-010, Radiation Protection Instrument Plan, Rev. 6
RP-TP-105-3007, Operation and Calibration of the GEM-5 Gamma Exit Monitor, Rev 4
Calibrations and Data
Work Order 40033883, ARMS Cal Inside Containment (RD-1401-03), 02/2012
Work Order 40323168, ARMS Cal Inside Containment (RD-1401-03), 03/2014
Work Order 40170223, T.S R-4-19 S/G Liquid Sample PRMS Cal, 05/2013
Work Order 40280868, T.S R-4-19 S/G Liquid Sample PRMS Channel CAL, 12/2014
Work Order 40273313, T.S. Plt Vent SPING Rad-6304 PM Cal, 09/2014
Work Order 40113819, T.S. Plt Vent SPING Rad-6304 PM Cal, 12/2012
Work Order 40161233, T.S. RAD-6311 A/B Cont HI Range ARMS CAL Per 3-PMI-066.3,
    02/2013
Work Order 40219065, T.S. RAD-6311 A/B Cont HI Range ARMS CAL Per 3-PMI-066.3,
    03/2014
Work Order 40323168, T.S. RD-4-15 SJAE 18 Monthly PM CAL, 01/2015
Work Order 40247970, T.S. RD-4-15 SJAE Spiking cause alarms, 07/2013
Calibration of the FASTSCAN WBC System #97-7040, 10/2013 & 10/2014
HP-7:5.4 CRONOS Calibration Records for #1302-27, 09/24/14 & 03/19/14; #0912-039 ,
    10/02/2014 & 10/11/2013; #1005-048 05/26/2015 & 06/09/2014; #1005-049 04/27/2015 &
    04/29/2014; #1006-037 06/15/2015 & 06/20/2014; #1302-029 07/22/2015 & 07/22/2014;
    #1302-028 01/13/12015 & 07/23/2014.
GEM-5 Calibration Certificates: #1423, #1424, 07/2014 & 07/2013; #1425 07/2014 & 06/2015
Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-107, 03/2015
Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-107, 03/2014
Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-107, 01/2014
Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-108, 07/2015
Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-108, 01/2015
Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #1107-185, 03/2015
Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #1107-185, 02/2015
System Health Report 07/01/2015-09/30/2015
F & J Model LV-14M Calibration Record Serial #s 4029, 4030, 4031, 06/2015


AR 02063559  
                                            9
Calibration of the Count Room MCA System, Detector Two, 06/2014
RADECO H809V/C Air Sampler Calibration Record, HPI# 1485E 02/2015
Controlled Settings- Eberline AMS 4, #1847, 10/2015; #2551, 10/2015; #1836 10/2015, #1283
    8/2015, #1080 08/2015, #12872 05/2015, #1638 08/2015, #1079 08/2015
Radiation Detection Instrument Calibration and Maintenance Record, Telepole #6605-081,
    11/12/2015 & 05/07/2015; RO-20 #105 10/22/2015
HP-7-21, Shepard Model 89 Shielded Range Calibrator Certification Form, 02/2015
CAP Documents
PTN-14-002, Radiological Protection and Radwaste Audit, 03/03/2014
AR 01895614
AR 02035780
AR 01945528
AR 02042545
AR 02009932
Section 4OA1: Performance Indicator Verification
0-ADM-032, NRC Performance Indicators Turkey Point, Rev. 5
List of Dose and Dose Rate Alarms October 1, 2014 to September 30, 2015
Monthly Gaseous Dose Report, October 2015
Monthly Liquid Dose Report, October 2015
2014 Annual Radioactive Effluent Report
AR 01909707
AR 02063559
AR 02083253
Section 4OA2: Problem Identification and Resolution
AR 2046565, Engineering CAP Indicator for Quality of Cause Analysis
AR 02038459, Safety Issue, No Safety Chain on Emergency Ladder
AR 02039495, Unable To Complete 0-GME-005.03 for 4AD07 SBO Breaker
AR 02039635, Station Blackout Tie Breaker Testing
AR 02040240, RCS A HI Tave Alarmed Early Following Dilution
AR 02040257, 4A Charging Pump Needs Oil
AR 02040258, 3B Charging Pump Fluid Drive Needs Oil
AR 02040265, 4B Turbo Oil Pump Minor Oil Seal Leak
AR 02041403, Time Delay Actuation Outside Acceptable Band
AR 02041408, Time Delay Actuation Outside Acceptable Band
AR 02041612, 3P253A 3A 4KV Room Sump Pump Does Not Turn Off
AR 02041798, Spalling Concrete in Unit 4 Spent Fuel Pool Room
AR 02041864, 3A EDG Coolant Reservoir Stained With Coolant
AR 02044844, 4KV Switchgear Sump High Level
AR 02044936, Performed Level 3 Leak Rate Investigation on Unit 3
AR 02044977, Unit 3 Gamma Metric Channel Alarm Causing a Distraction
AR 02045014, N-3-31 Detector Replacement
AR 02045085, 3B RCP Motor Has Oil Leak and Needs Replacement
AR 02046549, Active Boric Acid Leak at Bonnet of 4-873B
AR 02046555, Maintenance Rule A(1) Status for NIS Source Range Detectors
AR 02047770, Errors in Unit 4 Post Trip Review Restart Report
AR 02047817, Coolant Leak From the 3B EDG
AR 02049161, Excessive Ripple on the 22 Vdc Power Supply


AR 02083253
                                          10
Section 4OA2: Problem Identification and Resolution
AR 02049180, Missing Bolt and Washer on 3B Belt Guard
AR 2046565, Engineering CAP Indicator for Quality of Cause Analysis AR 02038459, Safety Issue, No Safety Chain on Emergency Ladder 
AR 02049269, 10 CFR 50.59 Screening for Rod Control System Monitoring
AR 02039495, Unable To Complete 0-GME-005.03 for 4AD07 SBO Breaker  AR 02039635, Station Blackout Tie Breaker Testing  AR 02040240, RCS A HI Tave Alarmed Early Following Dilution
AR 02049306, FME Found in 4P212A Pump Casing
AR 02040257, 4A Charging Pump Needs Oil
AR 20241958, U4 RHR Pump High Radiation Barrier Is Unsafe
AR 02040258, 3B Charging Pump Fluid Drive Needs Oil
AR 02097053, Level 3 Mispositioning Event
AR 02040265, 4B Turbo Oil Pump Minor Oil Seal Leak
AR 02097144, RHR Pump Testing
AR 02041403, Time Delay Actuation Outside Acceptable Band AR 02041408, Time Delay Actuation Outside Acceptable Band AR 02041612, 3P253A 3A 4KV Room Sump Pump Does Not Turn Off
AR 02041798, Spalling Concrete in Unit 4 Spent Fuel Pool Room
AR 02041864, 3A EDG Coolant Reservoir Stained With Coolant 
AR 02044844, 4KV Switchgear Sump High Level  AR 02044936, Performed Level 3 Leak Rate Investigation on Unit 3 AR 02044977, Unit 3 Gamma Metric Channel Alarm Causing a Distraction 


AR 02045014, N-3-31 Detector Replacement  
                    LIST OF ACRONYMS
AR 02045085, 3B RCP Motor Has Oil Leak and Needs Replacement  
AFW  Auxiliary Feedwater
AR 02046549, Active Boric Acid Leak at Bonnet of 4-873B
ALARA As Low As Reasonably Achievable
AR   Action Request
ARM  Area Radiation Monitor
ASME  American Society of Mechanical Engineers
CAP  Corrective Action Program
CCW  Component Cooling Water
CFR  Code of Federal Regulations
CR    Condition Report
EAL  Emergency Action Level
ED    Electronic Dosimeter
EDG  Emergency Diesel Generator
FME  Foreign Material Exclusion
FPP  Fire Protection Program
GOP  General Operating Procedure
HEPA  High Efficiency Particulate Air
HHSI  High Head Safety Injection
ICW  Intake Cooling Water
IP    Inspection Procedure
ISFSI Independent Spent Fuel Storage Installation
IST  Inservice Testing
LCO  Limiting Condition of Operation
LER  Licensee Event Report
LHRA  Locked High Radiation Area
LOCA  Loss of Coolant Accident
NAP  Nuclear Administrative Procedure
NCV  Non-Cited Violation
NDE  Non-Destructive Examination
NEI  Nuclear Energy Institute
NRC  Nuclear Regulatory Commission
OCC  Outage Control Center
OLRM  On-Line Risk Monitor
ONOP Off Normal Operating Procedure
OOS  Out of Service
OSP  Operations Surveillance Procedure
P&ID  Piping and Instrumentation Drawing
PCM  Personnel Contamination Monitor
PI    Performance Indicator
PW    Primary Water
QATR Quality Assurance Topical Report
RCA  Radiologically Controlled Area
RCE  Root Cause Evaluation
RCP  Reactor Coolant Pump
RCS  Reactor Coolant System
RFO  Refueling Outage
RHR  Residual Heat Removal
RP    Radiation Protection


AR 02046555, Maintenance Rule A(1) Status for NIS Source Range Detectors AR 02047770, Errors in Unit 4 Post Trip Review Restart Report 
                            12
AR 02047817, Coolant Leak From the 3B EDG
RTP   Rated Thermal Power
AR 02049161, Excessive Ripple on the 22 Vdc Power Supply 
RWP   Radiation Work Permit
10  AR 02049180, Missing Bolt and Washer on 3B Belt Guard 
SAM   Small Article Monitor
AR 02049269, 10 CFR 50.59 Screening for Rod Control System Monitoring 
SCBA Self-Contained Breathing Apparatus
AR 02049306, FME Found in 4P212A Pump Casing  AR 20241958, U4 RHR Pump High Radiation Barrier Is Unsafe  AR 02097053, Level 3 Mispositioning Event 
SDP   Significance Determination Process
AR 02097144, RHR Pump Testing 
SFP   Spent Fuel Pool
  LIST OF ACRONYMS 
SAM   Small Article Monitor
AFW Auxiliary Feedwater ALARA As Low As Reasonably Achievable AR  Action Request
SCBA Self-Contained Breathing Apparatus
ARM  Area Radiation Monitor
SDP   Significance Determination Process
ASME  American Society of Mechanical Engineers
SG   Steam Generator
CAP  Corrective Action Program
SFP   Spent Fuel Pool
CCW  Component Cooling Water CFR  Code of Federal Regulations CR  Condition Report
SI   Safety Injection
EAL  Emergency Action Level
SUT   Startup Transformer
ED  Electronic Dosimeter
TEDE Total Effective Dose Equivalent
EDG  Emergency Diesel Generator FME  Foreign Material Exclusion FPP  Fire Protection Program
TS   Technical Specifications
GOP  General Operating Procedure
U3   Unit 3
HEPA  High Efficiency Particulate Air
U4   Unit 4
HHSI High Head Safety Injection ICW Intake Cooling Water IP Inspection Procedure
UFSAR Updated Final Safety Analysis Report
ISFSI Independent Spent Fuel Storage Installation 
WBC   Whole Body Counter
IST  Inservice Testing
WO   Work Order
LCO  Limiting Condition of Operation
LER  Licensee Event Report LHRA  Locked High Radiation Area LOCA  Loss of Coolant Accident
NAP  Nuclear Administrative Procedure
NCV  Non-Cited Violation
NDE  Non-Destructive Examination NEI  Nuclear Energy Institute NRC  Nuclear Regulatory Commission
OCC Outage Control Center
OLRM On-Line Risk Monitor
ONOP  Off Normal Operating Procedure
OOS Out of Service OSP  Operations Surveillance Procedure P&ID  Piping and Instrumentation Drawing
PCM  Personnel Contamination Monitor
PI  Performance Indicator
PW Primary Water QATR Quality Assurance Topical Report RCA Radiologically Controlled Area
RCE  Root Cause Evaluation
RCP  Reactor Coolant Pump
RCS  Reactor Coolant System RFO  Refueling Outage RHR Residual Heat Removal
RP Radiation Protection
12  
RTP Rated Thermal Power  
RWP Radiation Work Permit SAM Small Article Monitor SCBA Self-Contained Breathing Apparatus  
SDP Significance Determination Process  
SFP Spent Fuel Pool  
SAM Small Article Monitor  
SCBA Self-Contained Breathing Apparatus SDP Significance Determination Process SG Steam Generator  
SFP Spent Fuel Pool  
SI Safety Injection  
SUT Startup Transformer TEDE Total Effective Dose Equivalent TS   Technical Specifications  
U3   Unit 3  
U4   Unit 4  
UFSAR Updated Final Safety Analysis Report WBC Whole Body Counter WO   Work Order
}}
}}

Latest revision as of 19:44, 4 December 2019

NRC Integrated Inspection Report 05000250/2015004, 05000251/2015004, October 1, 2015 to December 31, 2015
ML16027A147
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 01/27/2016
From: Ladonna Suggs
NRC/RGN-II/DRP/RPB3
To: Nazar M
Nextera Energy
References
IR 2015004
Download: ML16027A147 (43)


See also: IR 05000250/2015004

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

245 PEACHTREE CENTER AVENUE NE, SUITE 1200

ATLANTA, GEORGIA 30303-1257

January 27, 2016

Mr. Mano Nazar

President and Chief Nuclear Officer

Nuclear Division

NextEra Energy

P.O. Box 14000

Juno Beach, FL 33408-0420

SUBJECT: TURKEY POINT NUCLEAR GENERATING STATION - NRC INTEGRATED

INSPECTION REPORT 05000250/2015004, 05000251/2015004

Dear Mr. Nazar:

On December 31, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Turkey Point Nuclear Generating Station Units 3 and 4. On January 15,

2016, the NRC inspectors discussed the results of the inspection with Mr. Tom Summers and

other members of your staff. The inspectors documented the results of this inspection in the

enclosed inspection report.

NRC inspectors documented one self-revealing finding of very low safety significance (Green) in

this report. The finding involved a violation of NRC requirements. The NRC is treating this

violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement

Policy.

If you contest the violations or significance of these NCVs, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with

copies to the Regional Administrator Region II; the Director, Office of Enforcement, U.S. Nuclear

Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at

Turkey Point Nuclear Generating Station Units 3 and 4.

If you disagree with a cross-cutting aspect assignment, you should provide a response within 30

days of the date of this inspection report, with the basis for your disagreement, to the Regional

Administrator, Region II; and the NRC resident inspector at the Turkey Point Nuclear

Generating Station Units 3 and 4.

M. Nazar 2

In accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections,

Exemptions, Requests for Withholding, of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRCs Public Document Room or from the Publicly Available Records (PARS) component of the

NRCs Agency wide Documents Access and Management System (ADAMS). ADAMS is

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public

Electronic Reading Room).

Sincerely,

/RA/

LaDonna B. Suggs, Chief

Reactor Projects Branch 3

Division of Reactor Projects

Docket Nos.: 50-250, 50-251

License Nos.: DPR-31, DPR-41

Enclosure:

IR 05000250/2015004, 05000251/2015004

w/Attachment: Supplementary Information

cc Distribution via ListServ

ML16027A147 SUNSI REVIEW COMPLETE FORM 665 ATTACHED

OFFICE RII:DRP RII:DRP RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS

SIGNATURE TLH4 via email MXE2 via email MAB7 via email REW1 via email RXK3 /RA for/ RXK3 PGC1 via email

NAME THoeg MEndress MBates RWilliams BPursley RKellner PCapehart

DATE 1/26/2016 1/26/2016 1/25/2016 1/26/2016 1/26/2016 1/26/2016 1/25/2016

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

OFFICE RII:DRP RII:DRS RII:DRS

SIGNATURE LJB4 RXK3 /RA FOR/ CMD4 via email

NAME LSuggs JPanfel CDykes

DATE 1/26/2016 1/26/2016 1/26/2016

E-MAIL COPY? YES NO YES NO YES NO

M. Nazar 3

Letter to Mano Nazar from LaDonna B. Suggs January 27, 2016

SUBJECT: TURKEY POINT NUCLEAR GENERATING STATION - NRC INTEGRATED

INSPECTION REPORT 05000250/2015004, 05000251/2015004

DISTRIBUTION:

S. Price, RII

L. Gibson, RII

OE Mail

RIDSNRRDIRS

PUBLIC

RidsNrrPMTurkeyPoint Resource

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos: 50-250, 50-251

License Nos: DPR-31, DPR-41

Report Nos: 05000250/2015004, 05000251/2015004

Licensee: Florida Power & Light Company (FP&L)

Facility: Turkey Point Nuclear Generating Station, Units 3 & 4

Location: 9760 S. W. 344th Street

Homestead, FL 33035

Dates: October 1 to December 31, 2015

Inspectors: T. Hoeg, Senior Resident Inspector

M. Endress, Resident Inspector

M. Bates, Senior Operations Engineer

R. Williams, Senior Reactor Inspector

B. Pursley, Health Physicist

C. Dykes, Health Physicist

J. Panfel, Health Physicist

B. Kellner, Senior Health Physicist

P. Capehart, Senior Operations Engineer

Approved by: LaDonna B. Suggs, Chief

Reactor Projects Branch 3

Division of Reactor Projects

Enclosure

SUMMARY

IR 05000250/2015004, 05000251/2015004; 10/01/2015 - 12/31/2015; Turkey Point Nuclear

Generating Station, Units 3 and 4; Refueling Outage & Other Outage Activities.

The report covered a three-month period of inspection by the resident inspectors and specialist

inspectors from the Region II office. One Green non-cited violation (NCV) was identified. The

significance of inspection findings are indicated by their color (i.e., greater than Green, or

Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process, (SDP) dated April 29, 2015. The cross-cutting aspects

were determined using IMC 0310, Aspects Within the Cross-Cutting Areas, dated December

4, 2014. All violations of NRC requirements were dispositioned in accordance with the NRCs

Enforcement Policy dated February 4, 2015. The NRCs program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 5.

NRC-Identified and Self-Revealing Findings

Cornerstone: Barrier Integrity

Programs, was identified when the licensee failed to properly implement procedure

3-PMI-072.6, Steam Dump to Atmosphere Control Loop Calibration. Specifically, the

licensee incorrectly installed a temporary electrical jumper in reactor operator console

3C02 instead of 3C04, in contrast to Step 6.3.2 of 3-PMI-072.6. This action resulted in

actuation of a 3B 4160 volt (V) vital bus lockout circuit causing loss of power to the B

train of Unit 3 (U3) spent fuel pool (SFP) cooling. Immediate corrective actions were

taken to remove the jumper and restore the B train of SFP cooling. The licensee

entered the condition in its corrective action program (CAP) as action request (AR)

02088911 and 02088914.

The performance deficiency was determined to be more than minor because it was

associated with the human performance attribute of the barrier integrity cornerstone and

adversely affected the cornerstone objective to provide reasonable assurance that

physical design barriers (fuel cladding, reactor coolant system (RCS), and containment)

protect the public from radionuclide releases. In addition, the performance deficiency, if

left uncorrected, had the potential to lead to a more significant safety concern. The

finding was screened using IMC 0609, Significance Determination Process,

Attachment 0609.04, Initial Characterization of Findings, Tables 2 and 3, dated July 1,

2012, and Appendix G Attachment 1, Shutdown Operations Significance Determination

Process Phase 1 Initial Screening and Characterization of Findings, Exhibit 4 for Barrier

Integrity, dated May 9, 2014. The inspectors determined the finding was of very low

safety significance (Green) because it was not associated with low temperature over

pressurization, freeze seals, steam generator nozzle dams, criticality, drain down or

leakage paths, or the containment barrier. Furthermore, one train of SFP cooling

remained in operation, the rate of SFP temperature rise was low (~ 2 °F/hour), and

additional methods remained available to limit SFP temperature rise. This finding was

assigned a cross cutting aspect associated with the procedure adherence element of the

human performance area because the licensee failed to correctly execute step 6.3.2 of

procedure 3-PMI-072.6 (H.8). (Section 1R20)

3

Licensee-Identified Violations

Violations of very low safety or security significance or Severity Level IV that were

identified by the licensee have been reviewed by the NRC. Corrective actions taken or

planned by the licensee have been entered into the licensees CAP. These violations

and corrective action tracking numbers are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 3 began this inspection period at 100 percent of Rated Thermal Power (RTP) where it

remained until October 19, 2015, when it was shut down for a scheduled refueling outage

(RFO). Unit 3 was restarted November 29, 2015, and returned to 100 percent of RTP on

December 9, 2015, where it remained through the end of this inspection period.

Unit 4 (U4) began this inspection period at 100 percent of RTP where it remained through the

end of this inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection (IP 71111.01)

.1 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

During the month of December, the inspectors reviewed and verified the status of

actions taken by the licensee for winter readiness prior to the onset of cool weather. The

inspectors reviewed licensee procedure OP-AA-102-1002, Seasonal Readiness,

Attachment 7, Cold Weather Readiness Check List, and Attachment 14, Turkey Point

Site Specific Guidance. The inspectors reviewed system health reports and open CAP

ARs for the emergency diesel generators (EDGs) and auxiliary feedwater (AFW) pumps

to determine if any deficiencies existed that could affect operation of equipment

immersion heaters. The inspectors performed walk downs of systems that could be

affected by cold weather as outlined in the licensee site specific guidance including the

following areas:

  • U3 and U4 charging pumps

b. Findings

No findings were identified.

1R04 Equipment Alignment (IP 71111.04)

.1 Partial Equipment Walk Downs (Quarterly)

a. Inspection Scope

The inspectors conducted three partial alignment verifications of the safety-related

systems listed below. These inspections included reviews using plant lineup

procedures, operating procedures, and piping and instrumentation drawings, which were

5

compared with observed equipment configurations to verify that the critical portions of

the systems were correctly aligned to support operability. The inspectors also verified

that the licensee had identified and resolved, by entering them in the CAP, equipment

alignment problems that could cause initiating events or impact the capability of

mitigating systems or barriers. Documents reviewed are listed in the Attachment. This

inspection constitutes three samples.

  • 4A and 4B high head safety injection (HHSI) pumps while 3A and 3B HHSI pumps

were OOS

b. Findings

No findings were identified.

1R05 Fire Protection (IP 71111.05)

.1 Fire Area Walk downs

a. Inspection Scope

The inspectors walked down the following five plant areas to evaluate conditions related

to control of transient combustibles, ignition sources, material condition, and operational

status of fire protection systems including fire barriers used to prevent fire damage and

propagation. The inspectors reviewed these activities using provisions in the licensees

procedure 0-ADM-016, Fire Protection Plan and 10 CFR Part 50, Appendix R. The

inspectors routinely reviewed the licensees fire impairment lists and monitored the

associated corrective actions for completion. The inspectors reviewed the AR report

database to verify that fire protection problems were being identified and appropriately

resolved in the CAP. The inspectors tours of the selected areas verified the fire

protection equipment was installed as shown on the applicable fire plan drawings and

appeared functional and ready for usage. This inspection constitutes five samples. The

following areas were inspected:

  • U4 Pipe and Valve Room, Fire Zone 030
  • U3 Containment Building, Fire Zone 060
  • U4 4B Vital Battery Room, Fire Zone 102
  • U3 and U4 Mechanical Equipment Room, Fire Zone 097
  • Auxiliary Building Electrical Equiptment Room, Fire Zone 025

b. Findings

No findings were identified.

6

.2 Fire Protection - Drill Observation

a. Inspection Scope

On December 9, 2015, the inspectors observed an unannounced fire drill that took place

within the station power block just outside the 3D31/4D31 non vital 125 VDC switchgear

room in the turbine building. The drill was observed to evaluate the readiness of the

plant fire brigade to fight fires and the control room to make the proper emergency action

level (EAL) classification. The inspectors verified that the licensee staff identified

deficiencies, openly discussed them in a self-critical manner at the drill debrief meeting,

and took appropriate corrective actions as required. Specific attributes evaluated were:

  • Proper wearing of fire protective gear and self-contained breathing apparatus
  • Proper use and layout of fire hoses
  • Employment of appropriate fire-fighting techniques
  • Sufficient fire-fighting equipment brought to the scene
  • Effectiveness of command and control
  • Search for victims and propagation of the fire into other plant areas
  • Smoke removal operations
  • Utilization of pre-planned strategies
  • Adherence to the pre-planned drill scenario
  • Drill objective

The inspectors also observed the placement and charging of the fire hoses used to

simulate extinguishing the fire.

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities (IP 71111.08)

a. Inspection Scope

Non-Destructive Examination Activities and Welding Activities

From October 26-29, 2015, the inspectors conducted an onsite review of the

implementation of the licensees inservice inspection (ISI) program for monitoring

degradation of the RCS boundary, risk-significant piping and component boundaries,

and containment boundaries in U3.

The inspectors either directly observed or reviewed the following non-destructive

examinations (NDEs) mandated by the American Society of Mechanical Engineers

(ASME) Boiler and Pressure Vessel Code (Code of Record: 2007 Edition with 2008

Addenda) to evaluate compliance with the ASME Code,Section XI and Section V

requirements, and if any indications or defects were detected, to evaluate if they were

dispositioned in accordance with the ASME Code or an NRC-approved alternative

requirement. The inspectors also reviewed the qualifications of the NDE technicians

performing the examinations, to determine whether they were current and in compliance

with the ASME Code requirements.

7

  • Ultrasonic Examination of Loop B 18-inch Feedwater Nozzle-to-Pipe weld,

Augmented Examination (observed)

  • Ultrasonic Examination (UT) of Loop B 14-inch Feedwater Pipe-to-Elbow weld,

Augmented Examination (observed)

penetrations (reviewed)

  • Visual Examination (VT-3) of Spring Hanger 3-RCH-27, Class 1 Support (observed)
  • VT-3 of Dual Spring Hanger VS-1G-12, Class 1 Support (observed)

The inspectors either directly observed or reviewed the following welding activities,

qualification records, and associated documents in order to evaluate compliance with

procedures and the ASME Code,Section XI and Section IX requirements. Specifically,

the inspectors reviewed the work order (WO), repair and replacement plan, weld data

sheets, welding procedures, procedure qualification records, welder performance

qualification records, and NDE reports.

During non-destructive surface and volumetric examinations performed since the

previous RFO, the licensee did not identify any relevant indications that were analytically

evaluated and accepted for continued service; therefore, no NRC review was completed

for this inspection procedure (IP) attribute.

Pressurized Water Reactor Vessel Upper Head Penetration Inspection Activities

The inspectors verified that for the U3 vessel head, a bare metal visual examination and

a volumetric examination were not required during this outage, in accordance with the

requirements of ASME Code Case N-729-1 and 10 CFR 50.55a(g)(6)(ii)(D).

The licensee did not identify any relevant indications that were accepted for continued

service. Additionally, the licensee did not perform any welding repairs to the vessel

head penetrations since the beginning of the last U3 RFO; therefore, no NRC review

was completed for these IP attributes.

Boric Acid Corrosion Control Inspection Activities

The inspectors reviewed the licensees boric acid corrosion control program activities to

determine if the activities were implemented in accordance with the commitments made

in response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor

Pressure Boundary Components in PWR Plants, and applicable industry guidance

documents. Specifically, the inspectors performed an onsite records review of

procedures, and the results of the licensees containment walkdown inspections

performed during the current RFO. The inspectors also interviewed the Boric Acid

Corrosion Control (BACC) program owner, conducted an independent walkdown of

containment to evaluate compliance with licensees BACC program requirements, and

verified that degraded or non-conforming conditions, such as boric acid leaks, were

properly identified and corrected in accordance with the licensees BACC and CAP.

8

The inspectors reviewed the following engineering evaluations, completed for evidence

of boric acid leakage, to determine if the licensee properly applied applicable corrosion

rates to the affected components; and properly assessed the effects of corrosion

induced wastage on structural or pressure boundary integrity in accordance with the

licensee procedures.

The inspectors reviewed the following condition reports (CRs) and associated corrective

actions related to evidence of boric acid leakage, to evaluate if the corrective actions

completed were consistent with the requirements of the ASME Code and 10 CFR Part

50, Appendix B, Criterion XVI.

  • AR 02086287, CV-3-2819 has corrosion on electrical connection

Steam Generator Tube Inspection Activities

The inspectors verified that for the U3 steam generator tubes, no inspection activities

were required this RFO, in accordance with the requirements of the ASME Code, the

licensees TS, and Nuclear Energy Institute (NEI) 97-06, Steam Generator Program

Guidelines.

Identification and Resolution of Problems

The inspectors reviewed a sample of ISI-related issues entered into the CAP to

determine if the licensee had appropriately described the scope of the problem, and

had initiated corrective actions. The review also included the licensees consideration

and assessment of operating experience events applicable to the plant. The inspectors

performed this review to ensure compliance with 10 CFR Part 50, Appendix B, Criterion

XVI, Corrective Action, requirements.

b. Findings

No findings were identified.

9

1R11 Licensed Operator Requalification Program (IP 71111.11)

.1 Licensed Operator Requalification Exam

a. Inspection Scope

Annual Review of Licensee Requalification Examination Results: On December 30,

2015, the licensee completed the annual requalification operating examinations required

to be administered to all licensed operators in accordance with 10 CFR 55.59(a)(2). The

inspectors performed an in-office review of the overall pass/fail results of the individual

operating examinations and the crew simulator operating examinations in accordance

with IP 71111.11, Licensed Operator Requalification Program. These results were

compared to the thresholds established in Section 3.02, Requalification Examination

Results, of IP 71111.11.

b. Findings

No findings were identified.

.2 Resident Inspector Quarterly Review

a. Inspection Scope

The inspectors performed the following inspection sample of a simulator observation and

assessed licensed operator performance while training. These observations included

procedural use and adherence, response to alarms, communications, command and

control, and coordination and control of the reactor plant operations.

On October 8, 2015, the inspectors assessed licensed operator performance in the

plant-specific simulator during a training evolution. The training scenario was started

with the unit in Mode 1 at 100 percent power and included a fire lasting greater than 15

minutes, a loss of reactor coolant accident (LOCA), a reactor trip, a safety injection, a

residual heat removal (RHR) pump seal failure, and a radiological release to the

environment.

During this simulator observation, the simulator board configurations were compared

with actual plant control board configurations reflecting recent plant changes or

modifications. The inspectors specifically evaluated the following attributes related to

operating crew performance and the licensee evaluation:

  • Clarity and formality of communication
  • Ability to take timely action to safely control the unit
  • Prioritization, interpretation, and verification of alarms
  • Correct use and implementation of off-normal and emergency operating procedures

and emergency plan implementing procedures

  • Control board operation and manipulation, including high-risk operator actions
  • Oversight and direction provided by shift supervisor, including ability to identify and

implement appropriate TS actions and emergency plan classification and notification

  • Crew overall performance and interactions
  • Evaluators control of the scenario and post scenario evaluation of crew performance

10

b. Findings

No findings were identified.

.3 Control Room Observations

a. Inspection Scope

The inspectors performed daily assessments of licensed operators in the control room

during their performance of routine operations. These observations included daily

surveillance testing, log keeping, response to alarms, communications, shift turnovers,

and coordination of plant activities. These observations were conducted to verify

operator compliance with station operating guidelines, such as use of procedures,

control and manipulation of components, and communications. The inspectors also

performed the following three focused control room observations during reactivity

manipulations and Mode changes:

On November 19, 2015, the inspectors performed a focused observation on U4

consisting of a RCS primary water dilution per 0-OP-046, Enclosure 6, Chemical

Volume Control System Boron Concentration Control. Specifically, the inspectors

observed the reactor operators performance of the pre-job brief per 0-ADM-200,

Attachment 7, Planned Reactivity Manipulations for Maintaining Steady State Plant

Conditions and verified the operators complied with the applicable procedure during the

evolution.

On December 1, 2015 and December 2, 2015, the inspectors performed a focused

observation in the U3 control room during low power physics testing in accordance with

procedure 0-OSP-040.19, Low Power Physics Testing. The inspectors observed the

pre-evolution operating crew brief, control rod movements, monitoring of subcritical

multiplication, and data collection.

On December 3, 2015, the inspectors performed a focused observation on U3 during a

reactor startup per procedure 3-GOP-301, Hot Standby to Power Operations. The

inspectors reviewed the expected critical boron concentration calculation and the control

rod pull sequence plan used during the observed reactor startup. The inspectors

reviewed the recorded reactor startup physics data to ensure it was as calculated by the

licensee reactor engineering staff.

This inspection constitutes three samples. The inspectors focused on the following

conduct of operations attributes as appropriate:

  • Operator compliance and use of procedures
  • Control board manipulations
  • Communication between crew members
  • Use and interpretation of plant instruments, indications and alarms
  • Use of human error prevention techniques
  • Documentation of activities, including initials and sign-offs in procedures
  • Supervision of activities, including risk and reactivity management

11

b. Findings

No findings were identified.

.4 Biennial Requalification

a. Inspection Scope

The inspectors reviewed the facility operating history and associated documents in

preparation for this inspection. During the weeks of November 30, 2015 through

December 21, 2015, the inspectors reviewed documentation associated with the

licensees operator requalification program biennial written examinations. The activity

performed by the inspectors was conducted to assess the licensees effectiveness in

implementing requalification requirements identified in 10 CFR Part 55, Operators

Licenses. The evaluations were also performed to determine if the licensee effectively

implemented operator requalification guidelines established in NUREG-1021, Operator

Licensing Examination Standards for Power Reactors, and IP 71111.11, Licensed

Operator Requalification Program. Documentation reviewed included two biennial

written examinations. The records were inspected using the criteria listed in IP

71111.11. Documents reviewed during the inspection are documented in the List of

Documents Reviewed.

The sample is now complete because the remainder of this sample was previously

inspected and documented in the third quarter integrated inspection report

(05000250&251/2015003).

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (IP 71111.12)

a. Inspection Scope

The inspectors reviewed known equipment problems associated with the U3 steam

generator steam flow module FM-3-474D affecting the maintenance rule program and

equipment performance history trends associated with the equipment. Specifically, the

inspectors reviewed AR 02081538.

The inspectors reviewed the licensees activities to meet the requirements of 10 CFR

50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power

Plants, and licensee procedure NAP-415, Maintenance Rule Program Administration.

The inspectors focused on maintenance rule scoping, characterization of maintenance

problems and failed components, risk significance, determination of a(1) or a(2)

performance criteria classification, corrective actions, and the appropriateness of

established performance goals and monitoring criteria. The inspectors also interviewed

responsible engineers and observed or reviewed corrective maintenance activities. The

inspectors verified that equipment problems were being identified and appropriately

entered into the licensees CAP. The inspectors used the licensee maintenance rule

12

database, system health reports, maintenance rule unavailability status reports, and the

CAP as sources of information on tracking and resolution of issues. This inspection

constitutes one sample.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (IP 71111.13)

a. Inspection Scope

The inspectors completed in-office reviews and control room inspections of the

licensees risk assessment of five emergent or planned maintenance activities. The

inspectors verified the licensees risk assessment and risk management activities using

the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management

and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of

Maintenance at Nuclear Power Plants, Revision 3; and procedures 0-ADM-068, Work

Week Management; WM-AA-1000, Work Activity Risk Management; and 0-ADM-225,

On Line Risk Assessment and Management. The inspectors also reviewed the

effectiveness of the licensees contingency actions to mitigate increased risk resulting

from the degraded equipment and the licensee is assessment of aggregate risk using

procedure OP-AA-104-1007, Online Aggregate Risk. The inspectors discussed the on-

line risk monitor (OLRM) results with the control room operators and verified all

applicable OOS equipment was included in the OLRM calculation. The inspectors

evaluated the following five risk assessment samples during the inspection period:

  • U3 3A 4kV Bus, U3 Startup Transformer (SUT), and 3A and 3B HHSI pumps OOS
  • U3 3A 4kV Bus, U3 SUT, and 3D Vital 480V Motor Control Cabinet (MCC) OOS
  • U3 3-312A Valve Inspection and Repair with Freeze Seal (WO 40411630)
  • U3 Train 2 AFW, U4 Train 2 AFW, and U3 3B Emergency Containment Cooler OOS

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments (IP 71111.15)

a. Inspection Scope

The inspectors evaluated the technical adequacy of the licensee evaluations to ensure

that TS operability was properly justified and the subject component or system remained

available such that no unrecognized increase in risk occurred for the five operability

evaluations described in the ARs listed below. The inspectors reviewed applicable

sections of the updated Final Safety Anaylsis Report (UFSAR) to determine if the system

or component remained available to perform its intended function. In addition, when

applicable, the inspectors reviewed compensatory measures implemented to verify that

13

the affected equipment remained capable of performing its intended design function.

The inspectors also reviewed a sampling of CRs to verify that the licensee routinely

identifed and corrected any deficiencies associated with operability evaluations. This

inspection constitutes five samples.

  • AR 02082853, Pressurizer Steam Sample Line Containment Isolation Valve (CV-4-

951) OOS

b. Findings

No findings were identified.

1R18 Plant Modifications (IP 71111.18)

Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed the following two permanent plant modifications. The

inspectors reviewed the 10 CFR 50.59 screening and technical evaluation to verify that

the modifications had not affected system operability or availability. The inspectors

reviewed associated plant drawings, design analyses, and UFSAR documents impacted

by these modifications and discussed the changes with licensee personnel to verify that

the modifications were consistent with the WO and associated documents. The

inspectors observed portions of the modifications and surrounding areas to determine if

conditions resulted in any potential unsafe conditions not described in the engineering

change documentation. Additionally, the inspectors reviewed and verified that any

conditions associated with the modifications were being identified and entered into the

CAP. This inspection constitutes two samples.

Replacement

b. Findings

No findings were identified.

1R19 Post Maintenance Testing (IP 71111.19)

a. Inspection Scope

For the five post maintenance tests and associated WOs listed below, the inspectors

reviewed the test procedures and either witnessed the testing or reviewed test records to

determine whether the scope of testing adequately verified that the work performed was

completed satisfactorily and demonstrated that the affected equipment was operable.

14

The inspectors verified that the requirements in licensee procedure 0-ADM-737, Post

Maintenance Testing, were incorporated into the test requirements. The inspectors

reviewed the following WOs consisting of five inspection samples:

  • WO 40281614, U3 Pressurizer Pressure Operated Relief Valve PCV-3-455C

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities (IP 71111.20)

.1 Unit 3 Refueling Outage PT3-28 (one sample)

a. Inspection Scope

Outage Planning, Control and Risk Assessment

During daily outage planning activities by the licensee, the inspectors reviewed the risk

reduction methodology employed by the licensee during RFO PT3-28 meetings including

outage control center (OCC) morning meetings, operations daily team meetings, and

schedule performance update meetings. The inspectors examined the licensee

implementation of shutdown safety assessments during PT3-28 in accordance with

administrative procedure ADM-051, Outage Risk Assessment and Control, to verify if a

defense in depth concept was in place to ensure safe operations and avoid unnecessary

risk. In addition, the inspectors regularly monitored outage planning and control

activities in the OCC, and interviewed responsible OCC management personnel during

the outage to ensure system, structure, and component configurations, and work scope

were consistent with TS requirements, site procedures, and outage risk controls.

Monitoring of Shutdown Activities

The inspectors performed walk downs of important systems and components used for

RHR from the reactor core and SFP during the shutdown period, including the intake

cooling water system, component cooling water (CCW) system, and SFP cooling

system.

Outage Activities

The inspectors examined outage activities to verify that they were conducted in

accordance with TS, licensee procedures, and the licensees outage risk control plan.

Some of the more significant inspection activities accomplished by the inspectors were

as follows:

15

  • Walked down selected safety-related equipment clearance orders
  • Verified operability of RCS pressure, level, flow, and temperature instruments during

various modes of operation

  • Verified electrical systems availability and alignment
  • Evaluated implementation of reactivity controls
  • Reviewed control of containment penetrations

(e.g., around the refueling cavity, near sensitive equipment and RCS breaches) and

around the SFP

  • Observed fuel loading and unloading in the SFP and in containment

Monitoring of Plant Heat up and Containment Closure Activities

The inspectors examined the applicable TS, license conditions, and verified

administrative prerequisites were being met prior to reactor plant mode changes. The

inspectors reviewed measured RCS leak rates, and verified containment integrity was

properly established. The inspectors performed a containment closeout inspection prior

to the reactor plant startup to verify no evidence of leakage or debris were left in

containment that could affect plant operations.

Reactor Startup and Mode Changes

On December 2, 2015, the inspectors observed the U3 reactor startup and turbine

synchronization to the electrical grid and associated Mode changes. The inspectors

reviewed the recorded reactor startup physics data in order to determine it was as-

calculated by the licensee reactor engineering staff. The inspectors determined that

startup and Mode changes were performed in accordance with licensee procedures 0-

OSP-040.16, Initial Criticality After Refueling Outage and Nuclear Design Verification,

and 3-GOP-301, Mode 3 to Power Operations.

Corrective Action Program

The inspectors reviewed ARs generated during PT3-28 to evaluate the licensees

threshold for initiating ARs. The inspectors reviewed CRs to verify priorities, Mode

holds, and significance levels were assigned as required. Resolution and

implementation of corrective actions of several ARs were also reviewed for

completeness. The inspectors routinely reviewed the results of site oversight of daily

surveillances of outage activities.

b. Findings

Introduction: A Green self-revealing NCV of TS 6.8.1, Procedures and Programs, was

identified for the licensees failure to correctly execute procedure 3-PMI-072.6, Steam

Dump to Atmosphere Control Loop Calibration. The failure resulted in actuation of a 3B

4160 V vital bus lockout circuit causing loss of power to the B train of U3 SFP cooling.

Description: On November 4, 2015, at 2112 hours0.0244 days <br />0.587 hours <br />0.00349 weeks <br />8.03616e-4 months <br />, Instrumentation and Controls

technicians were performing procedure 3-PMI-072.6, Steam Dump to Atmosphere

Control Loop Calibration, when a temporary electrical jumper was incorrectly installed in

16

the control room reactor operator console 3C02 instead of 3C04, in contrast to step 6.3.2

of 3-PMI-072.6. At the time of the event, U3 was defueled with all of its fuel temporarily

relocated to the SFP. The 3A 4160 V vital bus was de-energized for planned

maintenance and all 480 V vital load centers were powered by the 3B 4160 V vital bus.

Separate load centers provided power to two separate trains of U3 SFP cooling pumps,

and the 3A train pump was powered from Unit 4 electrical switchgear.

The incorrectly placed jumper actuated a 3B 4160 V vital bus lockout circuit causing all

associated Unit 3 480 V vital load and motor control centers to de-energize. Numerous

equipment was rendered OOS including the B SFP cooling pump and the 3B CCW

pump. The 3B CCW pump provided cooling to both U3 SFP cooling heat exchangers.

Upon loss of the 3B CCW pump, the standby 3C CCW pump started on low pressure as

designed, providing cooling to the 3A SFP cooling train. Immediate corrective action

was taken to remove the jumper and restore the B train of SFP cooling. However, the

loss of one train of SFP cooling for approximately four hours caused the SFP

temperature to rise from approximately 110 °F to 117 °F. The licensee restored U3 load

and motor control centers at 0207 hours0.0024 days <br />0.0575 hours <br />3.422619e-4 weeks <br />7.87635e-5 months <br /> on November 5, 2015, and by 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br /> the

SFP temperature had returned to normal.

The licensee entered the condition in its CAP as AR 02088911 and 02088914.

Corrective actions included site-wide briefings of lessons learned from the event, quality

reviews of procedure 3-PMI-072.6, and enhanced oversight of maintenance activities.

Analysis: The inspectors determined that the failure to correctly implement maintenance

procedure 3-PMI-072.6 was a performance deficiency. The performance deficiency was

determined to be more than minor because it was associated with the human

performance attribute of the barrier integrity cornerstone and adversely affected the

cornerstone objective to provide reasonable assurance that physical design barriers (fuel

cladding, RCS, and containment) protect the public from radionuclide releases.

Specifically, the licensees failure to correctly execute step 6.3.2 of procedure

3-PMI-072.6 rendered one of two SFP cooling trains OOS, causing the SFP temperature

to rise from approximately 110 °F to 117 °F over a four-hour period. While the

performance deficiency did not directly challenge the integrity of the fuel cladding, if left

uncorrected, the SFP temperature would have continued to increase, potentially

affecting SFP inventory.

The finding was screened using IMC 0609, Significance Determination Process,

Attachment 0609.04, Initial Characterization of Findings, Tables 2 and 3, dated July 1,

2012, and Appendix G Attachment 1, Shutdown Operations Significance Determination

Process Phase 1 Initial Screening and Characterization of Findings, Exhibit 4 for Barrier

Integrity, dated May 9, 2014. The inspectors determined the finding was of very low

safety significance (Green) because it was not associated with low temperature over

pressurization, freeze seals, steam generator nozzle dams, criticality, drain down or

leakage paths, or the containment barrier. Furthermore, one train of SFP cooling

remained in operation, the rate of SFP temperature rise was low (~2 °F/hour), and

additional diverse compensatory methods remained available to limit SFP temperature

rise. This finding was assigned a cross cutting aspect associated with the procedure

adherence element of the human performance area because the licensee failed to

correctly execute step 6.3.2 of procedure 3-PMI-072.6 (H.8).

17

Enforcement: Technical Specification 6.8.1 requires that procedures required by the

licensees Quality Assurance Topical Report (QATR) be established, implemented, and

maintained. The QATR includes procedures listed in Appendix A of NRC Regulatory

Guide 1.33, Revision 2, dated February 1978, including procedures for calibrations. The

licensee implements TS 6.8.1 requirements, in part, using procedure 3-PMI-072.6,

Steam Dump to Atmosphere Control Loop Calibration. Step 6.3.2 of procedure

3-PMI-072.6, requires that a jumper be installed in reactor operator console 3C02.

Contrary to this requirement, on November 4, 2015, at 2112 hours0.0244 days <br />0.587 hours <br />0.00349 weeks <br />8.03616e-4 months <br />, a maintenance

technician mistakenly installed a jumper in reactor operator console 3C04. This action

resulted in actuation of a 3B 4160 V vital bus lockout circuit causing loss of power to the

B train of U3 SFP cooling. The licensee took immediate corrective action to remove the

jumper. This violation is being treated as an NCV, consistent with Section 2.3.2 of the

Enforcement Policy, because it was of very low safety significance and was entered in

the licensees CAP as AR 02088911 and 02088914. (NCV 05000250/2015004-01,

Failure to correctly follow procedure 3-PMI-072.6, Steam Dump to Atmosphere Control

Loop Calibration.)

1R22 Surveillance Testing (IP 71111.22)

a. Inspection Scope

The inspectors either reviewed or observed the following five surveillance tests to verify

that the tests met the TS requirements, the UFSAR description, the licensees

procedural requirements, and demonstrated that systems were capable of performing

their intended safety functions and operational readiness. In addition, the inspectors

evaluated the effect of the testing activities on the plant to ensure that conditions were

adequately addressed by the licensee staff and that after completion of the testing

activities, equipment was returned to the status required for the system to perform its

safety function. The inspectors verified that any surveillance deficiencies were

documented in the licensees CAP. This inspection constitutes two surveillance test

samples, one inservice testing (IST) sample, and two containment isolation valve leak

test samples. The inspectors reviewed the following tests:

Surveillance Test:

  • 0-OSP-059.13, U4 Flux Map
  • 3-OSP-072.5, U3 Main Steam Safey Valve Setpoint Verification

In-Service Tests:

  • 3-OSP-206.1, Component Cooling Water MOV-3-1418 Valve Test (IST)

Containment Isolation Valve Test:

  • 3-OSP-051.5, U3 Local Leak Rate Test, Penetration 8 CV-3-951
  • 3-OSP-051.5, U3 Local Leak Rate Test, Penetration 14 CV-3-204

b. Findings

No findings were identified.

18

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation (IP 71114.06)

.1 Emergency Preparedness Drill

a. Inspection Scope

On October 8, 2015, the inspectors observed an emergency preparedness drill and the

performance of the licensees emergency response organization. The drill included a

simulated fire in the U4 laydown area, a LOCA inside containment, followed by a RHR

pump seal failure and radiological release to the environment. The fire, lasting greater

than 15 minutes, required an unusual event emergency declaration and notification to

state and local county officials and the NRC per licensee procedure 0-EPIP-20101,

Duties of the Emergency Coordinator. The scenario progressed to a loss of two RCS

barriers with the loss or potential loss of a third barrier requiring a general emergency

declaration and an additional notification. The inspectors observed the crew in the plant

simulator, including simulated implementation of emergency procedures. The inspectors

observed the emergency response organization staff in the control room simulator and

technical support center while they implemented the event classification guidelines and

emergency response procedures. The inspectors determined that the emergency

classification and notifications were made in accordance with the licensee emergency

plan implementing procedure 0-EPIP-20101. The inspectors attended the licensees

post drill critique, reviewed the licensees critique items, and discussed inspector

observations with the licensee to verify that drill issues were identified and captured in

the licensees CAP. This inspection constitutes one sample.

b. Findings

No findings were identified.

2. RADIATION SAFETY (RS)

Cornerstones: Public Radiation Safety and Occupational Radiaition Safety

2RS1 Radiological Hazard Assessment and Exposure Controls (IP 71124.01)

a. Inspection Scope

Hazard Assessment and Instructions to Workers. During facility tours, the inspectors

directly observed labeling of radioactive material and postings for radiation areas, high

radiation areas, and airborne radioactivity areas established within the radiologically

controlled area (RCA) of the U3 containment building, auxiliary building, the Independent

Spent Fuel Storage Installation (ISFSI), and radioactive waste processing and storage

locations. The inspectors independently measured radiation dose rates or directly

observed conduct of licensee radiation surveys for selected RCA areas. The inspectors

reviewed survey records for several plant areas including surveys for alpha emitters,

airborne radioactivity, gamma surveys with a range of dose rate gradients, and pre-job

surveys for upcoming tasks. The inspectors also discussed changes to plant operations

that could contribute to changing radiological conditions since the last inspection. For

selected outage jobs, the inspectors attended pre-job briefings and reviewed Radiation

19

Work Permit (RWP) details to assess communication of radiological control

requirements and current radiological conditions to workers.

Hazard Control and Work Practices. The inspectors evaluated access barrier

effectiveness for selected Locked High Radiation Area (LHRA) locations and discussed

changes to procedural guidance for LHRA and Very High Radiation Area controls with

Radiation Protection (RP) supervisors. The inspectors observed and evaluated controls

for the storage of irradiated material within the SFP. Established radiological controls

(including airborne controls) were evaluated for selected U3 RFO 28 (U3R28) tasks

including RCP seal replacements, reactor cavity decontamination and reactor sump

demobilization activities. In addition, the inspectors reviewed licensee controls for areas

where dose rates could change significantly as a result of plant shutdown and refueling

operations.

Through direct observations and interviews with licensee staff, the inspectors evaluated

occupational workers adherence to selected RWPs and RP technician proficiency in

providing job coverage. Electronic dosimeter (ED) alarm set points and worker stay

times were evaluated against area radiation survey results for selected U3 RFO jobs,

including the reactor sump demobilization and reactor cavity decontamination. The

inspectors discussed the use of personnel dosimetry (extremity dosimetry and

multibadging in high dose rate gradients) with RP staff. The inspectors also evaluated

worker response to dose and dose rate alarms during selected work activities.

Control of Radioactive Material. The inspectors observed surveys of material and

personnel being released from the RCA using small article monitor (SAM), personnel

contamination monitor (PCM), and portal monitor instruments. As part of IP 71124.05,

the inspectors reviewed the last two calibration records for selected release point survey

instruments and discussed equipment sensitivity, alarm setpoints, and release program

guidance with licensee staff. The inspectors reviewed records of leak tests on selected

sealed sources and discussed nationally tracked source transactions with licensee staff.

Problem Identification and Resolution. The inspectors reviewed CAP documents

associated with radiological hazard assessment and exposure control. The inspectors

evaluated the licensees ability to identify and resolve the issues in accordance with

licensee procedures. The inspectors also reviewed recent self-assessment results.

Radiation protection activities were evaluated against the requirements of the UFSAR

Section 11; TS Sections 6.8 Procedures and Programs and 6.12 High Radiation Area;

10 CFR Parts 19 and 20; Regulatory Guide 8.38, Control of Access to High and Very

High Radiation Areas in Nuclear Power Plants; and approved licensee procedures.

Licensee programs for monitoring materials and personnel released from the RCA were

evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of Radioactively

Contaminated Material. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

20

2RS2 Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls

(IP 71124.02)

a. Inspection Scope

Work Planning and Exposure Tracking. The inspectors reviewed work activities and their

collective exposure estimates for U3 RFO. The inspectors reviewed ALARA planning

packages for the following high collective exposure tasks: SG cleaning (including bundle

flushing, sludge lancing, and foreign object search and retrieval); refueling activities;

RCP seal replacement; bottom mounted inspection, and; various valve work. For the

selected tasks, the inspectors reviewed established dose goals and discussed

assumptions regarding the bases for the current estimates with responsible ALARA

planners. The inspectors evaluated the incorporation of exposure reduction initiatives

and operating experience. Adjustments made to planned doses were also reviewed,

along with the basis of those adjustments. Post-job reviews from both the current and

previous RFO were assessed. Where applicable, the inspectors discussed changes to

established estimates with ALARA planners and evaluated them against work scope

changes or unanticipated elevated dose rates.

Source Term Reduction and Control. The inspectors reviewed the collective exposure

three-year rolling average from 2012-2014 and reviewed historical collective exposure

trends. The inspectors evaluated historical dose rate trends and compared them to

current data.

Radiation Worker Performance. In conjunction with IP 71124.01, radiation worker

performance was evaluated during several tasks both within containment and the

auxiliary building. The inspectors specifically evaluated both the use of ALARA briefings

and remote technologies, including teledosimetry and remote visual monitoring, to

reduce dose.

Problem Identification and Resolution. The inspectors reviewed and discussed selected

CAP documents associated with ALARA program implementation. The inspectors

evaluated the licensees ability to identify and resolve the issues in accordance with

licensee procedures. The inspectors also reviewed recent self-assessment results.

ALARA program activities were evaluated against the requirements of the UFSAR

Section 11, applicable TS Sections 6.8 and 6.12, 10 CFR Part 20, and approved

licensee procedure. Records reviewed are listed in the Attachment.

b. Findings

No findings were identified.

2RS3 In-Plant Airborne Radioactivity Control and Mitigation (IP 71124.03)

a. Inspection Scope

Engineering Controls: Licensee engineering controls used to control and mitigate

airborne radioactivity were reviewed and discussed. The inspectors evaluated selected

U3 engineering controls including temporary High Efficiency Particulate Air (HEPA)

filtration systems for selected outage tasks with the potential for generating airborne

21

activity conditions. The evaluations included procedural guidance, operability testing,

and established configurations during specific outage tasks. In addition, plant guidance

and its implementation for the monitoring of potential airborne beta-gamma and alpha-

emitting radionuclides for outage tasks associated with refueling activities, head

disassembly, and valve maintenance were reviewed and discussed with cognizant

licensee representatives.

Use of Respiratory Protection Devices: Program guidance for issuance and use of

respiratory protection devices were reviewed and discussed with responsible licensee

representatives. The inspectors reviewed Total Effective Dose Equivalent (TEDE)

ALARA evaluations conducted for select U3 outage tasks. Use of respiratory protective

equipment was evaluated for selected workers involved in U3 outage activities. The

inspectors toured selected onsite compressors available for supplying breathing air for

current outage activities and reviewed Grade D or greater air certification for permanent

and temporary on-site compressors used for supplied-line breathing air and self-

contained breathing apparatus (SCBA) bottle fill-station activities. Training, fit testing,

and medical qualifications for selected RP, maintenance, and operations using

respiratory protection for outage activities were reviewed and discussed with cognizant

licensee representatives.

Self-Contained Breathing Apparatus for Emergency Use: The inspectors reviewed

current status, operability and availability of select respiratory and SCBA equipment

maintained within the U3 and U4 control rooms, B5B lockers, and U3 and U4 reactor

auxiliary building locations. Maintenance activities for selected respiratory protective

equipment (e.g., compressed gas cylinders, regulators, valves, and hose couplings), by

certified vendor technicians were reviewed for selected SCBA units. Training, fit testing,

and medical qualifications for selected RP, maintenance, and operations staff assigned

Emergency Response Organization duties were reviewed and discussed with cognizant

licensee representatives. For selected U3 and U4 control room operators, the

inspectors discussed and reviewed annual hands-on SCBA training activities, including

donning, doffing, and functionally checking SCBA equipment, bottle change out, and

also reviewed availability of corrective lens, as applicable, for on-shift personnel.

Problem Identification and Resolution: The inspectors reviewed selected CAP

documents within the area of radiological airborne controls and respiratory protection

activities. The inspectors evaluated the licensees ability to identify and resolve the

issues in accordance with licensee procedures PI-AA-104-1000, Corrective Action, Rev.

6, and 0-ADM-533, Corrective Action Program Guidance, Rev. 14. The inspectors also

evaluated the scope of the licensees internal audit program and reviewed recent

assessment results. Specific licensee CAP documents reviewed for airborne

radionuclide concentration monitoring and mitigation are listed in the Attachment.

Radiation Protection program activities associated with airborne radioactivity monitoring

and controls were evaluated against details and requirements documented in the

UFSAR, TS Section 3/4.9.9, Containment Ventilation System, 3/4.9.13, Radiation

Monitoring, and 6.8.1, Procedures and Programs; 10 CFR Part 20, and also approved

licensee procedures. Documents reviewed are listed in the Attachment.

The inspectors completed all specified line-items detailed in IP 71124.03.

22

b. Findings

No findings were identified.

2RS4 Occupational Dose Assessment (IP 71124.04)

a. Inspection Scope

The inspector evaluated current RP program guidance and its implementation for

monitoring and assessing occupational workers internal and external radiation

exposure. The review included quality assurance activities, results, and responses to

identified issues; and individual dose results for selected occupational workers.

External Dosimetry: The inspector reviewed and discussed RP program guidance for

monitoring external and internal radiation exposures of occupational workers. The

inspector verified National Voluntary Laboratory Accreditation Program certification data

and discussed program guidance for storage, processing and results for dosimeters

currently in use. The inspector also reviewed and discussed the comparison between

ED and thermoluminescent dosimeter data.

Internal Dosimetry: Program guidance, instrument detection capabilities, and select

results for assessing internally deposited radionuclides were reviewed and discussed in

detail. The inspector evaluated licensee follow-up in vivo monitoring results and dose

assignment for three workers involved in contamination events having the potential for

internal deposition of radioactive material. In addition, the current licensee and contract

vendor laboratory analysis capabilities for the collection and analysis of in vitro samples

were reviewed and discussed in detail.

Special Dosimetric Situations: The inspector reviewed monitoring conducted and results

for two declared pregnant workers since the last inspection. The methodology and

results of monitoring occupational workers within non-uniform external dose fields and

assignment of effective dose equivalent results were discussed in detail. In addition, the

adequacy of dosimetry program guidance and its implementation for shallow dose

assessments and supporting calculations for an individual involved in a select

contamination event were evaluated. Neutron monitoring guidance and implementation

for select at power containment entries were reviewed and discussed. RP staff

proficiency involved in conducting skin dose assessments, neutron monitoring, and

whole body counter (WBC) operations were evaluated through review and discussions

of completed records and supporting data.

Problem Identification and Resolution: The inspectors reviewed and discussed selected

CAP documents associated with occupational dose assessment. The reviewed items

included ARs, self-assessments, and quality assurance audit documents. The

inspectors evaluated the licensees ability to identify, characterize, prioritize, and resolve

the identified issues in accordance with licensee procedures PI-AA-104-1000, Corrective

Action, Rev. 6, and 0-ADM-533, Corrective Action Program Guidance, Rev. 14.

Radiation protection program occupational dose assessment guidance and activities

were evaluated against the requirements of the UFSAR Section 11; TS Sections 6.8.1,

Procedures and Programs, and 6.12, High Radiation Area; 10 CFR Parts 19 and 20; and

approved licensee procedures. Records reviewed are listed in the Attachment.

23

The inspectors completed all specified line-items detailed in IP 71124.04.

b. Findings

No findings were identified.

2RS5 Radiation Monitoring Instrumentation (IP 71124.05)

a. Inspection Scope

Radiation Monitoring Instrumentation: During tours of the auxiliary building, turbine

building, SFP areas, and RCA exit point, the inspectors observed installed radiation

detection equipment including the following instrument types: area radiation monitors

(ARMs), airborne monitors, liquid and gaseous effluent monitors, PCMs, SAMs, and

portal monitors. The inspectors observed the physical location of the components, and

noted the material condition.

In addition to equipment walkdowns, the inspectors observed source checks and alarm

setpoint testing of various portable and fixed detection instruments, including ion

chambers, telepoles, PCMs, SAMs, and portal monitors. For the portable instruments,

the inspectors observed the use of a high-range check source and reviewed records of

periodic output value testing for a calibration source. The inspectors reviewed recent

calibration records and evaluated alarm setpoint values for selected ARMs, PCMs, portal

monitors, SAMs, effluent monitors, and a WBC. This included a sampling of instruments

used for post-accident monitoring such as containment high-range ARMs and effluent

monitor high-range noble gas and iodine channels. Radioactive sources used to

calibrate selected ARMs and effluent monitors were evaluated for traceability to national

standards. Calibration stickers on portable survey instruments and air samplers were

noted during inspection of storage areas for ready-to-use equipment. The inspectors

also reviewed countroom quality assurance records for gamma ray spectrometry

equipment and liquid scintillation detectors.

Problem Identification and Resolution: Selected licensee CAP documents associated

with instrumentation were reviewed and assessed. The inspectors evaluated the

licensees ability to identify and resolve the identified issues in accordance with licensee

procedures. The inspectors also reviewed recent self-assessment results.

Operability and reliability of selected radiation detection instruments were reviewed

against details documented in the following: 10 CFR Part 20; NUREG-0737,

Clarification of Three Mile Island Action Plan Requirements; TS Section 3; UFSAR

Chapters 11; and applicable licensee procedures. Documents reviewed during the

inspection are listed in the Attachment.

b. Findings

No findings were identified.

24

4OA1 Performance Indicator Verification (IP 71151)

.1 Barrier Integrity Cornerstone

a. Inspection Scope

The inspectors reviewed licensee submittals for the U3 and U4 Performance Indicators

(PI) listed below for the period October 1, 2014, through September 30, 2015, to verify

the accuracy of the PI data reported during that period. Performance indicator

definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance

Indicator Guideline, and licensee procedure 0-ADM-032, NRC Performance Indicators

Turkey Point, were used to check the reporting for each data element. The inspectors

checked operator logs, plant status reports, CRs, system health reports, and PI data

sheets to verify that the licensee had identified the required data, as applicable. The

inspectors interviewed licensee personnel associated with PI data collection, evaluation,

and distribution. This inspection constitutes four samples.

b. Findings

No findings were identified.

.2 Radiation Safety Cornerstones

a. Inspection Scope

Occupational Radiation Safety Cornerstone: The inspectors reviewed recent

Occupational Exposure Control Effectiveness PI results for the occupational radiation

safety cornerstone, and reviewed PI records generated from October 2014 through

October 2015. For the assessment period, the inspectors reviewed ED alarm logs and

selected CRs related to controls for exposure significant areas. Documents reviewed

are listed in the Attachment.

Public Radiation Safety Cornerstone: The inspectors reviewed recent radiological

control effluent release occurrences PI results for the public radiation safety cornerstone,

and reviewed PI records generated from October 2014 through October 2015. For the

assessment period, the inspectors reviewed cumulative and projected doses to the

public contained in liquid and gaseous release permits and CRs related to radiological

effluent TS/Offsite Dose Calculation Manual issues. Documents reviewed are listed in

the Attachment.

b. Findings

No findings were identified.

25

4OA2 Problem Identification and Resolution (IP 71152)

.1 Daily Review

a. Inspection Scope

As required by IP 71152, Identification and Resolution of Problems, and to help identify

repetitive equipment failures or specific human performance issues for follow-up, the

inspectors performed a screening of items entered daily into the licensees CAP. This

review was accomplished by reviewing daily printed summaries of ARs and by reviewing

the licensees electronic AR database. Additionally, RCS unidentified leakage was

checked on a daily basis to verify no substantive or unexplained changes. Documents

reviewed are listed in the Attachment.

b. Findings

No findings were identified.

.2 Annual Sample: Missed Fire Watch Tours

a. Inspection Scope

The inspectors selected AR 02056905, Missed Fire Watch Tours for a more in-depth

review of the circumstances and the corrective actions that followed. The AR report was

reviewed to ensure that an appropriate evaluation was performed and corrective actions

were specified and prioritized in accordance with the licensees program. Other

attributes checked included disposition of operability and resolution of the problem,

including cause determination, past operability determination, and corrective actions.

The inspectors interviewed plant personnel and evaluated the CR in accordance with the

requirements of the licensees corrective actions process as specified in licensees

procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205,

Condition Evaluation and Corrective Action. This inspection constitutes one sample.

b. Findings and Observations

No inspector findings were identified. A licensee-identified violation of very low safety

significance (Green) is documented in Section 4OA7 of this report. The licensee

identified that employees failed to perform hourly required fire watch roves. The

inspectors noted that the licensees evaluation for the missed fire watch roves concluded

that there was no violation of any TS requirement since TS do not require fire watches

for degraded fire protection features. The licensee concluded that the missed roves

represented a reduction in the effectiveness of the Fire Protection Program (FPP) and

the loss of a defense-in-depth feature.

The licensee determined the root cause of the event to be that operations management

was not engaged with the fire watch program. The licensee also determined that a

direct cause was that fire watch employees willfully chose non-compliance with fire

protection requirements. Immediate corrective actions for this event included the

immediate denial of site access for the individuals who failed to conduct the roves. The

licensee also updated the fire protection procedure, 0-ADM-016.4, to include Operations

26

Management Responsibilities and Oversight that requires observations, audits, and

assessments to ensure regulatory requirements are met. The licensee also conducted

an extent of condition and determined that no other missed tours were present in other

departments based on data collected and security access logs.

.3 Semi-Annual Trend

a. Inspection Scope

The inspectors performed a review of the licensees records including ARs, CAP health

reports, apparent cause evaluation reports, and various corrective action review board

reports to asses an adverse trend in the performance of reactor protection transmitters.

The inspectors reviewed licensee AR 02088175, which identified an adverse trend in

protection transmitter calibration check results. The inspectors evaluated the

effectiveness of the licensees corrective actions and the significance of the problems,

including attributes such as accurate documentation, reportability, evaluation, corrective

actions, and problem resolution. This inspection constitutes one sample.

b. Findings and Observations

No inspector findings were identified. The licensee noted that the transmitters in

question, Rosemount pressure transmitters, are expected to drift a slight amount. The

licensee also noted that both the transmitter age and replacement of components tended

to exacerbate the transmitter drift through the calibration cycle. The licensee concluded

that even with the noted transmitter drift, the transmitters still performed satisfactorily

and were within TS compliance. The inspectors did not identify any additional trends not

observed by the licensees trending activities.

4OA5 Other Activities

.1 Independent Spent Fuel Storage Facility Walk down (IP 60855.1)

a. Inspection Scope

On December 17, 2015, the inspector conducted a walk down of the ISFSI protected

area per IP 60855.1, Operation of an ISFSI at Operating Plants. The inspectors

observed each cask building temperature indicator and passive ventilation system to be

free of any obstruction, allowing natural draft convection decay heat removal through the

air inlet and air outlet openings. The inspectors observed associated cask building

structures to be structurally intact and radiation protection access and security controls

to the ISFSI area to be satisfactory.

b. Findings

No findings were identified.

27

4OA6 Meetings

The resident inspectors presented the inspection results to Mr. Tom Summers and other

members of licensee management on January 15, 2016. The inspectors asked the

licensee whether any of the material examined during the inspection should be

considered proprietary information. The licensee did not identify any proprietary

information.

4OA7 Licensee-identified Violation

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements which meets the criteria of the NRC

Enforcement Policy for being dispositioned as an NCV.

10 CFR 50.48 states that each operating nuclear power plant must have a fire protection

plan that satisfies Criterion 3 of Appendix A of this part. Turkey Point Renewed

Operating License condition D, for Units 3 and 4, states that the licensee shall

implement and maintain in effect all provisions of the approved FPP as described in the

UFSAR Appendix 9.6A. The approved FPP is implemented, in part, by 0-ADM-016, Fire

Protection Program, as referenced in Section 7.2 of UFSAR Appendix 9.6A. Section 5.6

of 0-ADM-016 requires that, for non-functional post-fire safe shutdown components,

engineering evaluations should identify appropriate compensatory actions, including

hourly fire roves. Contrary to the above, between May 1st, 2014, and April 23rd, 2015,

hourly fire watch patrols were not conducted on numerous occasions in fire zones that

required regular hourly tours due to fire protection equipment impairment. The failure to

perform the fire watch tours did not cause the inoperability of any equipment but resulted

in the loss of a defense-in-depth feature for fire detection in fire zones affected by an

impaired or non-functional fire safety component or feature. This violation was

associated with the Mitigating Systems Cornerstone and affected the cornerstone

objective of ensuring the availability, reliability and capability of the systems that respond

to initiating events to prevent undesirable consequences. The inspectors determined the

finding to be of very low safety significance (Green) after performing a detailed risk

evaluation in accordance with Manual Chapter 0609, Appendix A, because the missed

fire watch tours reflected a low degradation of the Fire Prevention and Administrative

Controls FPP element in that other area fire protection defense-in-depth features such

as automatic fire detection (smoke detectors), automatic fire suppression capability

(sprinklers), manual suppression capability (fire brigade), and safe shutdown capability

from the main control room were still available. The licensee entered this violation into

their CAP as AR 02056905.

ATTACHMENT: SUPPLEMENTARY INFORMATION

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel:

F. Banks, Quality Manager

C. Cashwell, Training Manager

P. Czaya, Licensing

C. Domingos, Plant General Manager

T. Eck, Security Manager

M. Guth, Licensing Manager

O. Hanek, Licensing Engineer

A. Katz, Projects Manager

G. Melin, Operations Manager

S. Mihalakea, Licensing

K. Ohara, Emergency Preparedness Manager

J. Pallin, Engineering Director

D. Sluszka, Work Controls Manager

B. Stamp, Operations Director

T. Summers, Site Vice-President

D. Barrow, Maintenance Director

R. Hess, General Operations Training Supervisor

M. Wilson, Operations Training Supervisor

NRC Personnel:

B. Bishop, Senior Project Engineer

A. Beaston, Project Engineer

A. Vargas, Project Engineer

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened and Closed

05000251/2015004-01 NCV Failure to correctly follow procedure

3-PMI-072.6, Steam Dump to

Atmosphere Control Loop Calibration.

(Section 1R20)

Attachment

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather

0-ONOP-103.3, Severe Weather Preparations

Section 1R04: Equipment Alignment

3-NOP-022, Emergency Diesel Generator Fuel Oil System

3-NOP-023, Emergency Diesel Generator

4-NOP-022, Emergency Diesel Generator Fuel Oil System

4-NOP-023, Emergency Diesel Generator

3-OP-201, Filling/Draining the Refueling Cavity and the SFP Transfer Canal

4-OP-201, Filling/Draining the Refueling Cavity and the SFP Transfer Canal

P&ID 5613-M-3022, Emergency Diesel Engine and Oil System

P&ID 5613-M-3062, Safety Injection System

P&ID 5614-M-3062, Safety Injection System

Section 1R05: Fire Protection

0-ONOP-016.10, Pre-Fire Plan Guidelines and Safe Shutdown Manual Actions

Section 1R08: Inservice Inspection Activities

Procedures:

0-ADM-537, Boric Acid Corrosion Control Program, Rev. 11

3-OSP-045.1, ASME Section XI Quality Group A Bolting Examination, Rev. 2

MA-AA-1000, Plant Leak Management Procedure, Rev. 6

NDE 4.15, Visual Examination (VE) ASME Section XI Code Case N-722-1 and N-729-1, Rev. 4

NDE 4.2, Visual Examination VT-2 Conducted During System Pressure Tests, Rev. 10

NDE 4.3, Visual Examination VT-3, Rev. 12

NDE 5.16, Ultrasonic Examination Technique for the Detection of Cracking in Feedwater Piping,

Rev. 10

NDE 5.18, Ultrasonic Thickness Measurement, Rev. 8

Calculations:

EC 284178, Review of Degradation and Operational Assessments at End-of-Cycle 27 for

Turkey Point Unit 3

Work Orders/Work Requests:

WO 4029647301, Valve 3-298C Replace Valve

WO 4030098001, Repair of PZR HTR Sleeve #11

CAP Documents:

AR 1771920, Audit shows no self-assessments performed on the welding control program

AR 1858601, BOP, ISI and FAC Quick Hit Self-Assessment for 2012 Outages (SL-1-24, SL-2-

20, TP-3-26, TP-4-27)

AR 2086224, Inconsistent gaps were identified between CRDM/RPI plates and the seismic plate

bumper

AR 2086933, Debris inside spring hanger

Miscellaneous Documents:

2012 Welding May 2012 Quality Assurance Assessment

3

AES 13118520-2Q-3, Condition Monitoring and Operational Assessment for the Turkey Point

Unit 3 Steam Generators Based on Eddy Current Examination End of Cycle 26, March 2014

Calibration Data Sheet for UT Instruments SN: 136P1106C031381, K07639

Calibration Data Sheet No.: 5.16-002

Certificate of Conformity NDE Probe SN: SE1110

Certificate of Personnel Qualification ID No.: D0360, C2231, C6756

ENG-CSI -2.3, Steam Generator Integrity Program Administration, Rev. 32

ENG-CSI-2.2, Planning and Reporting Results of Steam Generator Tubing Examinations,

Rev. 44

ER-AP-116, Boric Acid Corrosion Control, Rev. 0

Focused Self-Assessment Report 1837244, Boric Acid Corrosion Control Program

Krautkramer Transducer Certificate of Conformity SN: 012Y39

Personnel Certification Statement: T. Thomas, B. Thompson, M. Smith, and M. Johnson

Quick Hit Assessment Report 1892958, Boric Acid Corrosion Control Leak Evaluations

Ultrasonic Instrument Calibration Data Record and Certification SN: 01R6B7

Visual Examination Evaluation Sheet: 4.3.001

Visual Examination Record Data Sheets: #4.3-008 and #4.3-009

Section 1R11: Licensed Operator Requalification Process

0-ADM-211, Emergency and Off-Normal Operating Procedure Usage

TR-AA-230-1007, Conduct of Simulator Training and Evaluation

TR-AA-220-1004, Licensed Operator Continuing Training Annual Operating and Biennial

Written Exams, Revision 1

TR-AA-230-1004, SAT Implementation, Revision 5

PTN OPS LOC15 SRO EXM1, Administered 10/06/2015

PTN OPS LOC15 SRO EXM2, Administered 11/29/2015

Section 1R15: Operability Evaluations

0-ADM-213, Technical Specification Related Equipment Out of Service Logbook

0-ADM-226, Operability Screening and Condition Reports

EN-AA-203-1001, Operability Determinations and Assessments

Section 1R18: Plant Modifications

5610-M-410-40, NX Seal Assembly

SPEC-C-021, Turkey Point Units 3 & 4 Tubing and Tubing Supports

WO 40419666

Section 1R19: Post Maintenance Testing

0-ADM-737, Post Maintenance Testing

MA-AA-203-1000, Maintenance Functional Testing

Section 1R20: Refueling and Other Outage Activities

0-ADM-009, Containment Closeout Inspection

MA-AA-101-1000, Foreign Material Exclusion Procedure

0-ADM-556, Fuel Assembly and Insert Shuffles

Section 2RS1: Radiological Hazard Assessment and Exposure Controls

Procedures, Guidance Documents, and Manuals

0-HPA-001, Radiation Work Permit Initiation and Termination, Rev. 4

4

RP-AA-102-1000, Alpha Monitoring, Rev. 2

RP-AA-103-1006, Conduct of Radiological Diving Operations, Rev. 1

RP-AA-107, Radioactive Material Control Program, Rev. 0

RP-AA-107-1003, Unconditional and Conditional Release of Material, Rev. 1

RP-SR-103-1001, Posting Requirements for Radiological Hazards, Rev. 2

RP-SR-103-1002, High Radiation Area Controls, Rev. 3

RP-SR-103-1008, Remote Monitoring, Rev. 5

0-HPS-025.2, Posting and Survey Requirements for Fuel Movement, Rev. 4B

0-HPS-027.1, Work Controls in Hot Particle Areas, Rev. 0

0-HPS-106, Survey & Posting Guidelines for Plant Evolutions, Rev. 5

Records and Data Reviewed

2015 NSTS Annual Inventory Reconciliation, Dated 01/15/15

Radioactive Source Leak Test Results, Dated 10/15/2015

Air Calculation Sheet, (ACS) A/S Log Ref No. P1-15-1023, U3 RCB REACTOR Sump During

Demob, Dated 11/17/2015

ACS, A/S Log Ref No. P0-15-1011, U3 RCB 30 6 Routine, Dated 11/17/2015

ACS, A/S Log Ref No. P0-15-1013, Vac Shack During Tool & Respirator Decon, Dated

11/17/2015

ACS, A/S Log Ref No. P0-15-1021, U3 RCB 58 By REACTOR Head Stand, Dated 11/17/2015

ACS, A/S Log Ref No. P0-15-1025, U3 RCB Upper REACTOR Cavity, Dated 11/17/2015

PTN-M-20150604-3, U4 10 Foot Pipeway, Dated 06/04/2015

PTN-M-20150930-2, U4 10 Foot Pipeway, Dated 09/30/2015

PTN-M-20150914-1, U3 10 Foot Pipeway, Dated 09/14/2015

PTN-M-20150930-3, U3 10 Foot Pipeway, Dated 09/30/2015

PTN-M-20150711-25, U4 B RHR Pump Room, Dated 07/11/2015

PTN-M-20151010-2, U4 B RHR Pump Room, Dated 10/10/2015

PTN-M-20150918-5, U4 Charging Pump Room, Dated 09/18/2015

PTN-M-20151011-7, U4 Charging Pump Room, Dated 10/11/2015

PTN-M-20141120-6, Unit 4 B RHR Dose Alarm Follow-up, Dated 11/20/2014

PTN-M-20151020-6, Aux Bldg 3-240 Valve, Dated 10/20/2015

PTN-M-20151021-25, U3 Containment 14 ft elev Inside Biowall, Dated 10/21/2015

PTN-M-20151022-15, U3 Containment 14 ft elev Inside Biowall, Dated 10/22/2015

PTN-M-20151027-30, U3 Containment 14 ft elev Inside Biowall, Dated 10/27/2015

PTN-M-20150311-6, ISFSI Pad Semi-Annual, Dated 03/11/2015

PTN-M- 20150918-6, ISFSI Pad Semi-Annual, Dated 09/18/2015

RWP Number (No.) 15-3000 U3R28 Initial Containment Entry and when Containment is posted

as a Locked High Radiation Area, Rev. 0

RWP No. 15-3008, Containment General Outage Maintenance (Bulk Work), Rev 0

RWP No. 15-3013, Regenerative Heat Exchanger Room Work (Bulk Work), Rev. 0

RWP No. 15-3014, Reactor Sump - Non Legacy Boric Acid Work, Rev. 0

RWP No. 15-3018, RCP Work (Bulk Work), Rev. 0

RWP No. 15-3205, Outage Locked High Radiation Area Work, Rev. 0

CAP Documents

Nuclear Oversight Report # PTN-14-002, Radiation Protection and Radwaste, Dated

08/18/2014

AR 01996578

AR 01997251

AR 01997991

5

AR 02006239

AR 02008430

AR 02009674

AR 02020231

AR 02024963

AR 02029276

AR 02033046

AR 02033644

AR 02044544

AR 02044742

AR 02049552

AR 02058970

Section 2RS2: ALARA

Procedures and Guidance Documents

0-HPA-001, Radiation Work Permit Initiation and Termination, Rev. 04

0-HPA-072, Installation, Control, and Removal of Permanent and Temporary Shielding, Rev. 03

RP-AA-104, ALARA Program, Rev. 04

RP-AA-104-100, ALARA Implementing Procedure, Rev. 06

RP-AA-104-2003, Five Year ALARA Plan Template, Rev. 01

Primary Strategic Water Chemistry Plan, FPL PTN Units 3 & 4, 08/15/2013

Records and Data Reviewed

10 CFR Applicability Determination Form, TSR 15-03, Temporary Lead Shielding Installation on

Containment 14 Cavity Drain Valves, 10/18/15

ALARA Review No. 2015-006, U3R28 Refueling Activities, Including Ultra-Sonic Fuel Cleaning,

Rev. 0

ALARA Review No. 2015-007, Generator Bundle Flush, Sludge Lance, and FOSAR, Rev. 0

ALARA Review No. 2015-008, U3 A, B, C RCP Seal Replacement - Fukushima Upgrade - A

Motor Replacement, and PMs. Rev. 0

ALARA Review No. 2015-010, U3 BMI (Bottom Mounted Inspection), Rev. 0

ALARA Review No. 2015-013, PCV-3-455A and PCV-3-455B, Rev. 0

Job-In-Progress Review No. 2015-007, S/G secondary sludge lancing and FOSAR, Rev. 0

Job-In-Progress Review No. 2015-008, U3 A,B,C RCP Seal Replacement, Rev. 0

Job-In-Progress Review No. 2015-010, U3 BMI, Rev. 0

PTN ALARA Review Board Meeting Minutes, 03/23/15, 06/29/15, 09/04/15

PTN Nuclear Oversight Report #PTN-14-002, Subject: Radiological Protection and Radwaste,

05/09/14

PTN Quick Hit Assessment Report #1938751/1927754, Self Assessment of ALARA, 04/23/14

PTN-3-R28 Refueling Outage 0500 Turnover 11/03/15, 11/05/15

PTN-3-R28 Refueling Outage 1700 Turnover 11/12/15

PTN 5-Year ALARA Plan 2015-2020

RP Survey #PTN-M-20151029-34, Unit 3 Regenerative Heat Exchangers 14, 10/29/2015

RP Survey #PTN-M-20151029-27, Unit 3 Regenerative Heat Exchangers 14, 10/28/2015

RP Survey #PTN-M-20151028-36, U3 Containment 14 Inside Biowall, 10/28/2015

RP Survey #PTN-M-20151026-22, U3 Containment 14 Inside Biowall, 10/26/2015

RP Survey #PTN-M-20151020-19, U3 Containment 14 Inside Biowall, 10/20/2015

6

Temporary Shielding Request (TSR) No. 2015-03, U3 RCB, 14 Elevation, Cavity Drain Valves,

07/20/2015

TSR No. 2015-17, U3 RCB, 14 Regen. Heat Exchanger Room, 07/22/2015

CAP Documents

AR 01921887

AR 01997991

AR 01909707

AR 02072141

AR 01997680

AR 02043416

AR 02038064

Section 2RS3: In-Plant Airborne Radioactivity Control and Mitigation

Procedures and Guidance Documents

0-ADM-041, PTN Respiratory Protection Plan, Rev. 9

0-ADM-533, Corrective Action Program Guidance, Rev. 14

0-ADM-605, Control of Radioactive Material, Rev. 4

0-HPA-028, High Efficiency Particulate Air (HEPA) Filtration Ventilation Systems in the

Radiation Controlled Area, Rev. 2A

0-HPS-062.2, Use of the Self-Contained Breathing Apparatus, Rev.1

0-HPS-063.2, Maintenance and Accountability of Respiratory Protective Equipment, Rev. 7

0-HPS-063.4, Selection and Issuance of Respiratory Protection Equipment, Rev. 3

0-HPS-065.2, Operation and Maintenance of the Respirator Fit-Test System, Rev. 4

0-HPS-090, Inventory of Radiation Protection Emergency Equipment, Rev. 2

PI-AA-104-1000, Corrective Action, Rev. 6

RP-AA-102-1000, Alpha Monitoring, Rev. 2

RP-TP-102-1001, Radiological Air Sample Assay, Rev. 4

Records and Data Reviewed

Air Sample Log, for the period 10/1 thru 11/5/2015

Air Calculation Sheet and Gamma Spectroscopy Analysis, Air Sample # P1-I1-15-0405, U-3

RCB Lower Reactor Cavity, 10/26/2015

Certificate of Testing, PortaCount Bench 2, S/N 8030111513, 07/08/2015; and S/N

8030111601, 06/10/2015

HP-90, SCBA Inventory, Inspection, and Repair Records, September and October 2015

HP-93Respirator, Inventory, Inspection, and Repair Record, September and October 2015

HP-93.1, SCBA Air Bottle Inspection and Inventory Records, September and October 2015

HP-93.6, Air Quality Certificate, Bauer Air Compressor, Dated 08/05/2015, and 05/11/2015

List of SCBA Qualified Operations, Maintenance, and Health Physics Personnel, 10/01/2015

Scott Authorized Service Center Certificates for selected vendor employees, Dated 08/22/2014

Scott PosiChek3, Visual/Functional Test Results, Regulators: 89200090, Dated 09/22/2015;

89200100, Dated 09/23/2015; 89200101, Dated 09/22/2015; 89200109, Dated

09/22/2015; and 89200149, Dated 09/23/2015;

Unitech Service Group, DOP Test Results, HEPA Unit Type, Portable, HEPA S/N 018, Dated

06/23/2015; S/N 033, Dated 06/23/2015; and S/N 040, Dated 06/24/2015

Vendor Laboratory Compressed Air/Gas Quality Testing Report Results, Bauer Air Compressor,

Dated 08/05/2015, and 07/31/2015

7

CAP Documents

Quick Hit/Department Assessment Report, 2014 Respiratory Protection Program Annual

Review (AR 2014222), 04/07/2015

AR 01911462

AR 01845706

AR 01877007

AR 01889000

AR 01900277

AR 01964422

AR 01997251

AR 01938504

AR 02057725

AR 02020932

Section 2RS4: Occupational Dose Assessment

Procedures and Guidance Documents

0-HPA-030, Personnel Monitoring of External Dose, Rev. 3

0-HPS-023, Environmental Radiation Monitoring, Rev. 1

0-HPS-026.2, Response Protocols for Whole Body Counting Entrance and Exit, Rev. 3

0-HPS-031.1, Whole Body Dosimetry Issue, Rev. 3A

0-HPS-031.2, Multibadge Exposure Monitoring, Rev. 0B

RP-AA-101-2004, Method for Monitoring and Assigning Effective Dose Equivalent (EDE) for

High Dose Gradient Work, Rev. 3

RP-SR-101-1003, Personnel Contamination Monitoring and Decontamination, Rev. 3

RP-TP-101-1005, Internal Dose Assessment, Rev. 1

RP-TP-101-1000, Exposure Investigations, Rev. 0A

RP-TP-102-1002, Hard to Detect Radionuclides and Contamination Controls, Rev. 1

RP-TP-105-3008, Operation of the Radiation Protection Apex-In Vivo Whole Body Counting

Equipment, Rev. 2

Records and Data Reviewed

ABACOS-2000 Nuclide Libraries, 11/05/2015

Alpha Smear Log, 01/08/2015 thru 11/05/2015

Dosimetry Task Matrix, Daily Fastscan QC Check, October 2015

Extended Fastscan QA File Control Charts, 10/06/2015 thru 11/04/2015

Extended Fastscan WBC System Calibration Report, System # 97-7040, 10/23/2013 and

10/22/2014

EDE Multibadge Datasheets, Pack ID# 5010 and 5012, 11/04/2015

Fastscan 1 WBC System Calibration Report, System # 97-7040, 10/23/2013 and 10/22/2014

HP-55A, Turkey Point Plant Environmental Radiation Controlled Area Radiation Levels Results

Log [including ISFSI], 06/24/14 thru 12/26/14

HP-55A, Turkey Point Plant Environmental Radiation Controlled Area Radiation Levels Results

Log [including ISFSI], 12/26/14 thru 6/23/15

NVLAP Lab Code 100555-0, On-Site Assessment Report and Accreditation Certificate,

06/11/2015

QA 1000 File, 2013 Alpha Smear Summary: Unit 4 R27 Refueling Outage, 06/13/2014

Sensitivity Study of Personnel Contamination Monitors used at Turkey Point Nuclear Station,

02/10/2010

8

Technical Support Document No.15-058, Rev 00, Neutron Dosimetry Evaluation at Turkey

Point Nuclear Power Plant, 08/21/2015

Report, Turkey Point 2015 Site TEDE Dose, Top 25, 11/04/2015

Report, Turkey Point 2015 Annual (all sites) TEDE, Top 25, 11/04/2015

CAP Documents

AR 01861722

AR 01940206

AR 01959134

AR 01979141

AR 02013453

AR 02024069

AR 02076960

2RS5: Radiation Monitoring Instrumentation

Procedures

0-HPT-072, Calibration and Operation of Canberra Personnel Monitors, Rev. 2

0-HPT-018, Calibration of Survey Instruments, Rev. 4

0-HPT-010, Radiation Protection Instrument Plan, Rev. 6

RP-TP-105-3007, Operation and Calibration of the GEM-5 Gamma Exit Monitor, Rev 4

Calibrations and Data

Work Order 40033883, ARMS Cal Inside Containment (RD-1401-03), 02/2012

Work Order 40323168, ARMS Cal Inside Containment (RD-1401-03), 03/2014

Work Order 40170223, T.S R-4-19 S/G Liquid Sample PRMS Cal, 05/2013

Work Order 40280868, T.S R-4-19 S/G Liquid Sample PRMS Channel CAL, 12/2014

Work Order 40273313, T.S. Plt Vent SPING Rad-6304 PM Cal, 09/2014

Work Order 40113819, T.S. Plt Vent SPING Rad-6304 PM Cal, 12/2012

Work Order 40161233, T.S. RAD-6311 A/B Cont HI Range ARMS CAL Per 3-PMI-066.3,

02/2013

Work Order 40219065, T.S. RAD-6311 A/B Cont HI Range ARMS CAL Per 3-PMI-066.3,

03/2014

Work Order 40323168, T.S. RD-4-15 SJAE 18 Monthly PM CAL, 01/2015

Work Order 40247970, T.S. RD-4-15 SJAE Spiking cause alarms, 07/2013

Calibration of the FASTSCAN WBC System #97-7040, 10/2013 & 10/2014

HP-7:5.4 CRONOS Calibration Records for #1302-27, 09/24/14 & 03/19/14; #0912-039 ,

10/02/2014 & 10/11/2013; #1005-048 05/26/2015 & 06/09/2014; #1005-049 04/27/2015 &

04/29/2014; #1006-037 06/15/2015 & 06/20/2014; #1302-029 07/22/2015 & 07/22/2014;

  1. 1302-028 01/13/12015 & 07/23/2014.

GEM-5 Calibration Certificates: #1423, #1424, 07/2014 & 07/2013; #1425 07/2014 & 06/2015

Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-107, 03/2015

Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-107, 03/2014

Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-107, 01/2014

Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-108, 07/2015

Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #0904-108, 01/2015

Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #1107-185, 03/2015

Canberra Personnel Monitor Calibration Data Sheet Argos 5AB Serial #1107-185, 02/2015

System Health Report 07/01/2015-09/30/2015

F & J Model LV-14M Calibration Record Serial #s 4029, 4030, 4031, 06/2015

9

Calibration of the Count Room MCA System, Detector Two, 06/2014

RADECO H809V/C Air Sampler Calibration Record, HPI# 1485E 02/2015

Controlled Settings- Eberline AMS 4, #1847, 10/2015; #2551, 10/2015; #1836 10/2015, #1283

8/2015, #1080 08/2015, #12872 05/2015, #1638 08/2015, #1079 08/2015

Radiation Detection Instrument Calibration and Maintenance Record, Telepole #6605-081,

11/12/2015 & 05/07/2015; RO-20 #105 10/22/2015

HP-7-21, Shepard Model 89 Shielded Range Calibrator Certification Form, 02/2015

CAP Documents

PTN-14-002, Radiological Protection and Radwaste Audit, 03/03/2014

AR 01895614

AR 02035780

AR 01945528

AR 02042545

AR 02009932

Section 4OA1: Performance Indicator Verification

0-ADM-032, NRC Performance Indicators Turkey Point, Rev. 5

List of Dose and Dose Rate Alarms October 1, 2014 to September 30, 2015

Monthly Gaseous Dose Report, October 2015

Monthly Liquid Dose Report, October 2015

2014 Annual Radioactive Effluent Report

AR 01909707

AR 02063559

AR 02083253

Section 4OA2: Problem Identification and Resolution

AR 2046565, Engineering CAP Indicator for Quality of Cause Analysis

AR 02038459, Safety Issue, No Safety Chain on Emergency Ladder

AR 02039495, Unable To Complete 0-GME-005.03 for 4AD07 SBO Breaker

AR 02039635, Station Blackout Tie Breaker Testing

AR 02040240, RCS A HI Tave Alarmed Early Following Dilution

AR 02040257, 4A Charging Pump Needs Oil

AR 02040258, 3B Charging Pump Fluid Drive Needs Oil

AR 02040265, 4B Turbo Oil Pump Minor Oil Seal Leak

AR 02041403, Time Delay Actuation Outside Acceptable Band

AR 02041408, Time Delay Actuation Outside Acceptable Band

AR 02041612, 3P253A 3A 4KV Room Sump Pump Does Not Turn Off

AR 02041798, Spalling Concrete in Unit 4 Spent Fuel Pool Room

AR 02041864, 3A EDG Coolant Reservoir Stained With Coolant

AR 02044844, 4KV Switchgear Sump High Level

AR 02044936, Performed Level 3 Leak Rate Investigation on Unit 3

AR 02044977, Unit 3 Gamma Metric Channel Alarm Causing a Distraction

AR 02045014, N-3-31 Detector Replacement

AR 02045085, 3B RCP Motor Has Oil Leak and Needs Replacement

AR 02046549, Active Boric Acid Leak at Bonnet of 4-873B

AR 02046555, Maintenance Rule A(1) Status for NIS Source Range Detectors

AR 02047770, Errors in Unit 4 Post Trip Review Restart Report

AR 02047817, Coolant Leak From the 3B EDG

AR 02049161, Excessive Ripple on the 22 Vdc Power Supply

10

AR 02049180, Missing Bolt and Washer on 3B Belt Guard

AR 02049269, 10 CFR 50.59 Screening for Rod Control System Monitoring

AR 02049306, FME Found in 4P212A Pump Casing

AR 20241958, U4 RHR Pump High Radiation Barrier Is Unsafe

AR 02097053, Level 3 Mispositioning Event

AR 02097144, RHR Pump Testing

LIST OF ACRONYMS

AFW Auxiliary Feedwater

ALARA As Low As Reasonably Achievable

AR Action Request

ARM Area Radiation Monitor

ASME American Society of Mechanical Engineers

CAP Corrective Action Program

CCW Component Cooling Water

CFR Code of Federal Regulations

CR Condition Report

EAL Emergency Action Level

ED Electronic Dosimeter

EDG Emergency Diesel Generator

FME Foreign Material Exclusion

FPP Fire Protection Program

GOP General Operating Procedure

HEPA High Efficiency Particulate Air

HHSI High Head Safety Injection

ICW Intake Cooling Water

IP Inspection Procedure

ISFSI Independent Spent Fuel Storage Installation

IST Inservice Testing

LCO Limiting Condition of Operation

LER Licensee Event Report

LHRA Locked High Radiation Area

LOCA Loss of Coolant Accident

NAP Nuclear Administrative Procedure

NCV Non-Cited Violation

NDE Non-Destructive Examination

NEI Nuclear Energy Institute

NRC Nuclear Regulatory Commission

OCC Outage Control Center

OLRM On-Line Risk Monitor

ONOP Off Normal Operating Procedure

OOS Out of Service

OSP Operations Surveillance Procedure

P&ID Piping and Instrumentation Drawing

PCM Personnel Contamination Monitor

PI Performance Indicator

PW Primary Water

QATR Quality Assurance Topical Report

RCA Radiologically Controlled Area

RCE Root Cause Evaluation

RCP Reactor Coolant Pump

RCS Reactor Coolant System

RFO Refueling Outage

RHR Residual Heat Removal

RP Radiation Protection

12

RTP Rated Thermal Power

RWP Radiation Work Permit

SAM Small Article Monitor

SCBA Self-Contained Breathing Apparatus

SDP Significance Determination Process

SFP Spent Fuel Pool

SAM Small Article Monitor

SCBA Self-Contained Breathing Apparatus

SDP Significance Determination Process

SG Steam Generator

SFP Spent Fuel Pool

SI Safety Injection

SUT Startup Transformer

TEDE Total Effective Dose Equivalent

TS Technical Specifications

U3 Unit 3

U4 Unit 4

UFSAR Updated Final Safety Analysis Report

WBC Whole Body Counter

WO Work Order