ML20128J555: Difference between revisions

From kanterella
Jump to navigation Jump to search
(StriderTol Bot insert)
 
(StriderTol Bot change)
 
Line 1: Line 1:
#REDIRECT [[IR 05000445/2020001]]
{{Adams
| number = ML20128J555
| issue date = 05/07/2020
| title = Integrated Inspection Report 05000445/2020001 and 05000446/2020001
| author name = O'Keefe N
| author affiliation = NRC/RGN-IV/DRP/RPB-B
| addressee name = Peters K
| addressee affiliation = Vistra Operations Company, LLC
| docket = 05000445, 05000446
| license number = NPF-087, NPF-089
| contact person =
| document report number = IR 2020001
| document type = Inspection Report, Letter
| page count = 24
}}
See also: [[see also::IR 05000445/2020001]]
 
=Text=
{{#Wiki_filter:May 7, 2020
Mr. Ken Peters
Senior Vice President and Chief Nuclear Officer
VISTRA Operations Company, LLC
P.O. Box 1002
Glen Rose, TX 76043
SUBJECT:        COMANCHE PEAK NUCLEAR POWER PLANT, UNITS 1 AND 2 -
                INTEGRATED INSPECTION REPORT 05000445/2020001 AND
                05000446/2020001
Dear Mr. Peters:
On March 31, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection
at Comanche Peak Nuclear Power Plant, Units 1 and 2. On April 2, 2020, the NRC inspectors
discussed the results of this inspection with Mr. T. McCool, Site Vice President, and other
members of your staff. The results of this inspection are documented in the enclosed report.
One finding of very low safety significance (Green) is documented in this report. This finding
involved a violation of NRC requirements. We are treating this violation as a non-cited
violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.
If you contest the violation or the significance or severity of the violation documented in this
inspection report, you should provide a response within 30 days of the date of this inspection
report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional
Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector
at Comanche Peak Nuclear Power Plant, Units 1 and 2.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the
NRC Resident Inspector at Comanche Peak Nuclear Power Plant, Units 1 and 2.
 
K. Peters                                        2
This letter, its enclosure, and your response (if any) will be made available for public inspection
and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document
Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public
Inspections, Exemptions, Requests for Withholding.
                                                Sincerely,
                                                Cornelius    Digitally signed by
                                                            Cornelius F. O'Keefe
                                                F. O'Keefe  Date: 2020.05.07
                                                            14:50:23 -05'00'
                                                Neil F. O'Keefe, Chief
                                                Reactor Projects Branch B
                                                Division of Reactor Projects
Docket Nos. 05000445 and 05000446
License Nos. NPF-87 and NPF-89
Enclosure:
As stated
cc w/ encl: Distribution via LISTSERV
 
 
ML20128J555
                              Non-Sensitive                    Publicly Available
        SUNSI Review
                              Sensitive                        Non-Publicly Available
  OFFICE SRI:DRP/B      RI:DRP/B              DRS/IPAT  DRS/EB1
  NAME    JEllegood    NDay                  AAgrawal  VGaddy
  DATE    05/01/2020  05/04/2020            05/01/2020 05/04/2020
  OFFICE DRS/EB2        DRS/OB                DRS/RCB    DNMS/RxIB
  NAME    NTaylor      GWerner                MHaire    GWarnick
  DATE    05/04/2020  05/04/2020            05/01/2020 05/04/2020
  OFFICE SPE/DRP/B      BC:DRP/B
  NAME    DProulx      NOKeefe
  DATE    05/04/2020  05/07/2020
                               
                          U.S. NUCLEAR REGULATORY COMMISSION
                                        Inspection Report
Docket Numbers:        05000445 and 05000446
License Numbers:      NPF-87 and NPF-89
Report Numbers:        05000445/2020001 and 05000446/2020001
Enterprise Identifier: I-2020-001-0010
Licensee:              VISTRA Operations Company, LLC
Facility:              Comanche Peak Nuclear Power Plant, Units 1 and 2
Location:              Glen Rose, TX 76043
Inspection Dates:      January 1 to March 31, 2020
Inspectors:            J. Ellegood, Senior Resident Inspector
                      D. Antonangeli, Health Physicist
                      B. Baca, Health Physicist
                      N. Day, Resident Inspector
                      N. Greene, Senior Health Physicist
                      J. Melfi, Project Engineer
                      J. O'Donnell, Senior Health Physicist
Approved By:          Neil F. O'Keefe, Chief
                      Reactor Projects Branch B
                      Division of Reactor Projects
                                                                        Enclosure
 
                                              SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees
performance by conducting an integrated inspection at Comanche Peak Nuclear Power Plant,
Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight
Process is the NRCs program for overseeing the safe operation of commercial nuclear power
reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
                                List of Findings and Violations
  Manual Reactor Trip Due to Loss of both Main Feed Pumps
  Cornerstone          Significance                              Cross-Cutting    Report
                                                                  Aspect            Section
  Initiating Events    Green                                      [H.12] - Avoid    71153
                        NCV 05000446/2020001-01                    Complacency
                        Open/Closed
  A self-revealed finding and associated non-cited violation (NCV) of very low safety
  significance occurred when the licensee failed to implement procedures for operation of the
  feed and condensate system as required by Technical Specification 5.4.1.a. Specifically,
  while adjusting flow to the auxiliary condensers for the Unit 2 main feed pumps, the operators
  isolated circulating water flow to the condensers, causing a loss of both Unit 2 main feedwater
  pumps. Control room operators manually insert a plant trip in response to the loss of
  feedwater.
                                    Additional Tracking Items
  Type        Issue Number                Title                          Report Section  Status
  LER        05000446/2018-002-01        LER 2018-002-01 for            71153            Closed
                                          Comanche Peak, Unit 2,
                                          Automatic Actuation of
                                          Auxiliary Feedwater System.
  LER        05000446/2019-002-00        LER 2019-002-00 for            71153            Closed
                                          Comanche Peak Nuclear
                                          Power Plant, Unit 2,
                                          Automatic Actuation of
                                          Auxiliary Feedwater System.
                                                  2
 
PLANT STATUS
Unit 1 began the inspection period at rated thermal power and remained there throughout the
inspection period.
Unit 2 began the inspection period at rated thermal power. On January 1, 2020, the licensee
inserted a manual trip in response to a loss of both main feed pumps while adjusting circulating
water flow to the auxiliary condensers. The licensee took the reactor critical and synchronized
to the grid on January 3, 2020. The licensee reached 100 percent power on January 4, 2020,
and remained at or near rated thermal power for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
complete when the IP requirements most appropriate to the inspection activity were met
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
Program - Operations Phase. From January 1 - March 19, 2020, the inspectors performed
plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine
reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed
selected procedures and records, observed activities, and interviewed personnel to assess
licensee performance and compliance with Commission rules and regulations, license
conditions, site procedures, and standards.
Starting on March 20, 2020, in response to the National Emergency declared by the President
of the United States on the public health risks of the coronavirus (COVID-19), resident
inspectors were directed to begin telework and to remotely access licensee information using
available technology. During this time the resident inspectors performed periodic site visits
each week and during that time conducted plant status activities as described in IMC 2515,
Appendix D; and observed risk-significant activities when warranted. In addition, resident and
regional baseline inspections were evaluated to determine if all or portions of the objectives and
requirements stated in the IP could be performed remotely. If the inspections could be
performed remotely, they were conducted per the applicable IP. In the cases where it was
determined the objectives and requirements could not be performed remotely, management
elected to postpone and reschedule the inspection to a later date.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Impending Severe Weather Sample (IP Section 03.02) (1 Sample)
    (1)    The inspectors evaluated the adequacy of the overall preparations to protect
            risk-significant systems from forecasted thunderstorms on January 10, 2020
                                                  3
 
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (1 Sample)
    The inspectors evaluated system configurations during partial walkdowns of the following
    systems/trains:
    (1)    Unit 2, chemical and volume control system on February 6, 2020
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)
    The inspectors evaluated the implementation of the fire protection program by conducting a
    walkdown and performing a review to verify program compliance, equipment functionality,
    material condition, and operational readiness of the following fire areas:
    (1)    Unit 1, turbine building basement on January 17, 2020
    (2)    Unit 2, turbine building basement on January 17, 2020
    (3)    Unit 2, emergency diesel generator A room on January 23, 2020
    (4)    Service water intake structure building on March 26, 2020
Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)
    (1)    The inspectors evaluated the onsite fire brigade training and performance during an
          unannounced fire drill on March 3, 2020
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1
Sample)
    (1)    The inspectors observed and evaluated licensed operator performance in the control
          room during turbine start and synchronization to the grid on January 3, 2020
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
    (1)    The inspectors observed and evaluated licensed operators for just in time training for
          a reactor startup on January 2, 2020
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (1 Sample)
    The inspectors evaluated the effectiveness of maintenance to ensure the following
    structures, systems, and components (SSCs) remain capable of performing their intended
    function:
    (1)    Unit 2, auxiliary feedwater system on February 25, 2020
                                                4
 
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)
  The inspectors evaluated the accuracy and completeness of risk assessments for the
  following planned and emergent work activities to ensure configuration changes and
  appropriate work controls were addressed;
  (1)    Realignment of the Units 1 and 2 circulating water system on January 15, 2020
  (2)    Planned yellow risk for Unit 1 auxiliary feedwater valve strokes concurrent with
          emergent work to restore the Unit 1 emergency diesel generator A to operable status
          on February 14, 2020
  (3)    Risk associated with switchyard work and troubleshooting of Unit 2 circulating water
          pump on February 7, 2020
  (4)    Risk associated with starting the Unit 2 circulating water pump 2 on March 5, 2020
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)
  The inspectors evaluated the licensee's justifications and actions associated with the
  following operability determinations and functionality assessments:
  (1)    Unit 1, residual heat removal systems A and B, due to increasing pressures as
          described in condition report CR-2019-009779 on January 9, 2020
  (2)    Unit 2, emergency diesel generator A, due to a degraded time delay device as
          described in condition report CR-2020-001295 on February 24, 2020
  (3)    Unit 2, safety chiller 2-06, tripping due to a shorting bulb socket assembly as
          described in condition report CR 2020-001502 on March 2, 2020
  (4)    Unit 2, control rods from potential thermal sleeve cracking as described in Part 21
          report LTR-NRC-19-79, and corrective action document TR 2020-1247
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (4 Samples)
  The inspectors evaluated the following post maintenance test activities to verify system
  operability and functionality:
  (1)    Repair of disconnected wires and replacement of components in the Unit 2 safeguard
          sequencer system per Work Order 5840776 on February 20, 2020
  (2)    Replacement of cell 22 on battery 1DT4 per Work Order 5848383 on January 31,
          2020
  (3)    Repair of failed switch on neutron flux power ranch channel N-42 per Work
          Order 5866789 on February 28, 2020
  (4)    As found testing, calibration, and installation of Unit 2 safeguard sequencer B
          undervoltage relays per Work Order 5666818 on March 4, 2020.
                                                  5
 
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Surveillance Tests (other) (IP Section 03.01) (4 Samples)
    (1) Unit 2, emergency diesel generator monthly load test per Procedure OPT 214B, Diesel
        Generator Operability Test, Revision 16, on January 22, 2020
    (2) Unit 2, at power end of core life reactivity test per Work Order 5659452 on February 10,
        2020
    (3) Unit 1, monthly control rod exercise surveillance per Work Order 5829754 on
        January 24, 2020
    (4) Unit 1, train A slave relay K609 actuation test per Work Order 5656218 on March 11,
        2020
71114.06 - Drill Evaluation
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01)
(1 Sample)
    (1)    The blue team emergency preparedness drill on February 19, 2020.
RADIATION SAFETY
71124.05 - Radiation Monitoring Instrumentation
Walk Downs and Observations (IP Section 02.01) (1 Sample)
    The inspectors evaluated the following radiation detection instrumentation during plant
    walkdowns:
    (1)    Portable Survey Instruments
              * RM-177, HP-1461
              * RM-177, HP-1113
              * RM-177, HP-1145
              * RM-177, HP-2400
              * RM-177, HP-1464
              * RM-177, HP-1081
              * RM-177, HP-1026
              * AMS-4, HP-2166
              * 3030E, HP-3270
          Source Check Demonstration
              * Rad Eye G, HP-3112
              * Telepole, HP-1906
              * Rad Eye GX, HP-4045
              * Ludlum Model 3000, HP-3166
          Area Radiation Monitors and Continuous Air Monitors
              * 2-RE-6253
                                                  6
 
                *  2-RE-6259A
                *  2-RE-6297
                *  X-RE-5896A
                *  X-RE-5895B
                *  1-RE-6256
                *  1-RE-6295
            Personnel Contamination Monitors, Portal Monitors and Small Article Monitors
                * SAM, HP-0063
                * GEM-5, HP-0075
                * SAM, HP-0055
                * GEM-5, HP-0076
Calibration and Testing Program (IP Section 02.02) (1 Sample)
    The inspectors evaluated the calibration and testing of the following radiation detection
    instruments:
    (1)    Alarm Setpoint and Calibration Method Check of Personnel Contamination Monitors,
            Portal Monitors and Small Article Monitors
                * GEM-5, HP-0075
                * SAM, HP-0063
            Failure to Meet Calibration or Source Check Acceptance Criteria
                * Telepole, HP-1907
                * ARGOS, HP-0065
                * RO-20AA, HP-4123
                * AMS-4, HP-2166
71124.06 - Radioactive Gaseous and Liquid Effluent Treatment
Walk Downs and Observations (IP Section 02.01) (1 Sample)
    The inspectors walked down the following gaseous and liquid radioactive effluent monitoring
    and filtered ventilation systems to assess the material condition and verify proper alignment
    according to plant design:
    (1)        *  Plant Vent Stack Radiation Monitoring System
                *  Liquid Waste Processing Radiation Monitoring System
                *  Turbine Sump Radiation Monitoring System
                *  Station Service Water to Discharge Canal Radiation Monitoring System
Calibration and Testing Program (Process & Effluent Monitors) (IP Section 02.02) (1 Sample)
    The inspectors reviewed the following gaseous and liquid effluent monitor instrument
    calibrations and tests:
    (1)        *  WO 5360001, X-RE-5567A, South Plant Vent Stack Radiation Monitor
                    Calibration, 07/30/2018
                                                7
 
              *  WO 5590739, X-RE-5570B, North Plant Vent Stack WRGM Radiation Monitor
                  Calibration, 10/01/2019
              *  WO 5585319, X-RE-5253, Liquid Waste Processing Discharge Radiation
                  Monitor Calibration, 10/28/2019
              *  WO 5556086, 2-RE-5100, Turbine Sump 2-04 Radiation Monitor Calibration,
                  06/12/2019
              *  WO 5421935, 1-RE-4269, Unit 1 Station Service Water Train A to Discharge
                  Canal Radiation Monitor Calibration, 10/24/2018
              *  WO 5631300, 1-RE-4270, Unit 1 Station Service Water Train B to Discharge
                  Canal Radiation Monitor Calibration, 01/14/2020
              *  WO 5576336, 2-RE-4269, Unit 2 Station Service Water Train A to Discharge
                  Canal Radiation Monitor Calibration, 09/25/2019
              *  WO 5447947, X-FT-5288, LWPS LHMT X-01/X-02 Discharge to VD System
                  Flow Transmitter Calibration, 09/27/2018
Sampling and Analysis (IP Section 02.03) (1 Sample)
    The inspectors reviewed the following:
    (1)    Radioactive Effluent Sampling and Analysis Activities
              * Plant Ventilation Weekly Sampling, 01/27/2020
              * Containment Ventilation Sampling, 01/30/2020
          Effluent Discharge Permits
              * G2018-034, Unit 1 Containment Vent, 02/27/2018
              * G2018-208, Plant Vent Stack B, 12/09/2018
              * G2018-210, Non-Routine Gas Normal, 12/10/2018
              * G2019-046, Plant Vent Stack B, 03/12/2019
              * G2019-193, Unit 2 Containment Vent, 11/24/2019
              * G2019-216, Plant Vent Stack A, 12/31/2019
              * L2018-023, Plant Effluent Tank 1, 07/05/2018
              * L2018-040, Plant Effluent Tank 2, 10/24/2018
              * L2018-051, Low Volume Waste Pond (LVWP), 12/01/2018
              * L2019-016, Plant Effluent Tank 1, 02/14/2019
              * L2019-055, Squaw Creek Reservoir, 08/01/2019
              * L2019-072, Plant Effluent Tank 2, 12/12/2019
Instrumentation and Equipment (IP Section 02.04) (1 Sample)
    The inspectors reviewed the following radioactive effluent discharge system surveillance test
    results:
    (1)        *  WO 5319196, Primary Plant Ventilation Exhaust Filter Unit X-16 - Carbon
                  Analysis B Train, 01/13/2018
              *  WO 5377734, Primary Plant Ventilation Exhaust Filter Unit X-01 - ESF Filter
                  Test A Train, 10/31/2018
              *  WO 5431297, Primary Plant Ventilation Exhaust Filter Unit X-02 - ESF Filter
                  Test B Train, 11/07/2018
                                                8
 
              *  WO 5558463, Primary Plant Ventilation Exhaust Filter Unit X-02 - Carbon
                  Analysis B Train, 09/18/2019
Dose Calculations (IP Section 02.05) (1 Sample)
    The inspectors reviewed the following to asses public dose:
    (1)  Liquid and Gaseous Discharge Permits
              * G2018-034, Unit 1 Containment Vent, 02/27/2018
              * G2018-208, Plant Vent Stack B, 12/09/2018
              * G2018-210, Non-Routine Gas Normal, 12/10/2018
              * G2019-046, Plant Vent Stack B, 03/12/2019
              * G2019-193, Unit 2 Containment Vent, 11/24/2019
              * G2019-216, Plant Vent Stack A, 12/31/2019
              * L2018-023, Plant Effluent Tank 1, 07/05/2018
              * L2018-040, Plant Effluent Tank 2, 10/24/2018
              * L2018-051, Low Volume Waste Pond (LVWP), 12/01/2018
              * L2019-016, Plant Effluent Tank 1, 02/14/2019
              * L2019-055, Squaw Creek Reservoir, 08/01/2019
              * L2019-072, Plant Effluent Tank 2, 12/12/2019
          Annual Radiological Effluent Release Reports
              * 2017 Annual Radioactive Effluent Release Report, 03/12/2018
              * 2018 Annual Radioactive Effluent Release Report, 04/20/2019
          Abnormal Gaseous or Liquid Tank Discharges
              * None were available for review during this inspection
71124.07 - Radiological Environmental Monitoring Program
Site Inspection (IP Section 02.01) (1 Sample)
    The inspectors evaluated the radiological environmental monitoring program
    implementation.
    (1)  The inspectors reviewed the following:
          Walkdowns, Calibrations, and Maintenance Record Review
              * Air sampling stations: A1, A2, A3, A4, A5, A6, A7, A8
              * Thermoluminescent dosimeter (TLD) monitoring stations: R1, R4, R11, R13,
                  R22, R25, R27, R29, R30, R36
              * Calibrations of selected air sample pumps: 2178, 2196B, 2214, and 2224
          Environmental Sample Collections and Preparation Observation
              * Air particulate (A1, A2, A3, A4, A5, A6, A7, A8)
              * Air charcoal (A1, A2, A3, A4, A5, A6, A7, A8)
              * Broad leaf (BL1, BL2, BL3)
              * Surface water (SW1, SW2, SW3, SW4, SW5)
                                                9
 
        Licensee Actions in Response to Missed Sample, Inoperable Sampler, Lost
        Thermoluminescent Dosimeter (TLD) or Anomalous Measurement
        The inspectors reviewed the licensee's response to 13 missing or anomalous TLD
        results. The inspectors reviewed 6 inoperable samplers as noted in corrective action
        documents since May 2017 and noted in the 2017 and 2018 Annual Environmental
        Operating Reports. The majority of inoperable samplers were attributed to loss of
        power due to external events, such as weather and power line work.
        Sampling Program for the Potential of Licensed Material Entering Groundwater
            * Groundwater Monitoring Wells: 9, 10, 11, 12, 14, 15, 16, 19, 25, CP-A, CP-B,
                CP-C
Groundwater Protection Initiative (GPI) Implementation (IP Section 02.02) (1 Sample)
    (1)  The inspectors evaluated the licensee's voluntary groundwater protection initiative.
        A few observations were as follows:
            * The general maintenance and material condition of the groundwater
                monitoring wells was adequate with the general area around the well was
                kept clear of any obstructions.
            * Most monitoring wells had enough water for samples to be taken.
            * Monitoring well locations 11 and CP-A had results of 835 and 1700 pCi/L,
                respectively, which are both below their lower limit of detection (LLD)
                requirements. The remaining well location samples all tested below the
                minimum detectable activity.
            * The licensee implemented additional surface water sampling of the drainage
                flow catch basin to track the potential impact of a water treatment filtered
                water storage tank leak. The licensee has corrective actions in progress to
                address the identified leak.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) (2 Samples)
    (1)  Unit 1 January 1, 2019, to December 31, 2019
    (2)  Unit 2 January 1, 2019, to December 31 2019
IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02)
(2 Samples)
    (1)  Unit 1 January 1, 2019, to December 31, 2019
    (2)  Unit 2 January 1, 2019, to December 31, 2019
                                                10
 
IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)
    (1)    Unit 1 January 1, 2019, to December 31, 2019
    (2)    Unit 2 January 1, 2019, to December 31, 2019
71153 - Follow-up of Events and Notices of Enforcement Discretion
Event Follow-up (IP Section 03.01) (1 Sample)
    (1)    The inspectors evaluated licensee response to a Unit 2 reactor trip on January 1,
            2020.
Event Report (IP Section 03.02) (2 Samples)
    The inspectors evaluated the following licensee event reports (LERs):
    (1)    LER 05000446/2019-002-00, Automatic Actuation of Auxiliary Feedwater System
            (ADAMS Accession No. ML19199A033). The inspectors determined that it was not
            reasonable to foresee or correct the cause discussed in the LER; therefore, no
            performance deficiency was identified. The inspectors did not identify a violation of
            NRC requirements.
    (2)    LER 05000446/2018-002-01, Automatic Actuation of Auxiliary Feedwater System
            (ADAMS Accession No. ML 19199A032). The inspectors determined that it was not
            reasonable to foresee or correct the cause discussed in the LER; therefore, no
            performance deficiency was identified. The inspectors did not identify a violation of
            NRC requirements.
INSPECTION RESULTS
  Manual Reactor Trip Due to Loss of both Main Feed Pumps
  Cornerstone          Significance                              Cross-Cutting      Report
                                                                  Aspect              Section
  Initiating Events    Green                                    [H.12] - Avoid      71153
                        NCV 05000446/2020001-01                  Complacency
                        Open/Closed
  A self-revealed finding and associated non-cited violation (NCV) of very low safety
  significance occurred when the licensee failed to implement procedures for operation of the
  feed and condensate system as required by Technical Specification 5.4.1a. Specifically,
  while adjusting flow to the auxiliary condensers for the Unit 2 main feed pumps, the licensee
  isolated circulating water flow to the condensers, causing a loss of both Unit 2 main
  feedwater pumps. Control room operators manually insert a plant trip in response to the loss
  of feedwater.
  Description: On January 1, 2020, the Comanche Peak on-shift operations crew decided to
  secure a running circulating water pump for Unit 2. Although securing the pump was not on
  the plan of the day schedule, the shift manager added the activity into the shift's work
  activities to support planned work the following week. The inspectors noted that the activity
  would use normal circulating water system operating Procedure SOP-310B, Circulating
  Water, Revision 18, and the work schedule provided enough time to prepare for and conduct
  the evolution. The procedure was structured to secure one circulating water pump, adjust
                                                11
 
flow as needed to the main condenser, and then to adjust flow to the two main feedwater
pump auxiliary condensers. There are two steam driven main feedwater pumps.
The auxiliary condensers support operation of the two main feedwater pumps by condensing
the steam used by the feedwater pump turbines. Flow was being adjusted to optimize plant
thermal efficiency.
The crew successfully secured the circulating water pump and adjusted main condenser flow.
The crew then proceeded to the auxiliary condensers to adjust circulating water flow. A field
operator was stationed at each of the two auxiliary condenser outlet valves and a third field
operator was communicating with the main control room staff. In addition, a senior reactor
operator provided local oversight of the evolution. The crew intended to adjust the throttle
position of the circulating water with a final position directed by the reactor operator in the
control room. The reactor operator directed the valve operators to slowly close their
respective valves (simultaneously) to his mark while he monitored water box outlet
temperature. The valves were initially in a throttled position at the start and they reached the
fully closed position shortly after starting. Without any flow to the auxiliary condensers, both
main feedwater pumps automatically tripped on low vacuum to protect the pumps. Control
room staff immediately inserted a manual trip from 100 percent power. The control room
operators stabilized the plant in mode 3 using Emergency Procedure E-0, Reactor Trip and
Safety Injection, and normal operating procedures without further issue.
Personnel directly involved in the task failed to recognize that condenser vacuum would
respond quickly to reduced cooling water flow, but there would be delays before condensate
temperature would be reduced as the circulating water was adjusted due to mixing. In
addition, the personnel directly involved in the task did not recognize that the auxiliary
condenser outlet valves were two turns from full closed at the start of the evolution. These
factors led the field operators to erroneously fully close the valves prior to control room
direction to stop throttling the valves. The inspectors noted that the auxiliary condenser outlet
valves had large valve position indicators to provided system configuration information to the
local operators.
Comanche Peak performed a root cause evaluation to understand the event. The review
identified several weaknesses in crew performance that contributed to the event. Weakness
identified as the root cause were an over-reliance on process (i.e., procedures) coupled with
a failure to address gaps in behaviors and standards. This resulted in a lack of critical
thinking by plant staff as well as a failure to understand and address risks associated with the
proposed activities. During this evolution, operators failed to recognize the potential to lose
vacuum for the feed pumps due to a lack in understanding system operation and
fundamentals. The crew considered the throttling of cooling water flow to be a routine activity
and, therefore, the task preparations did not trigger a focused brief to discuss the evolution.
However, changing the circulating water pump configuration only occurs during winter months
to allow for maintenance on the pumps. The operators assigned to the task had a lack of
proficiency as none of the operators directly involved with adjusting flow on the auxiliary
condensers had secured a circulating water pump before. Furthermore, the operations shift
included three operators that had performed this evolution previously, but none were directly
involved in adjusting flow to the auxiliary condensers. The inspectors noted that their direct
involvement could have reduced the likelihood of an error during the evolution. In addition,
periodic throttling of the auxiliary condenser outlet valve flow occurred with regularity;
however, the adjustments were normally made in small increments with time between valve
movements to allow the system to equilibrate.
                                                12
 
The inspectors performed walkdowns of the evolution after the event, interviewed the
personnel involved, reviewed plant operating procedures, and reviewed the root cause
evaluation. The inspectors noted that although Comanche Peak used the correct procedure
and the procedure had been used successfully previously, weaknesses in preparation for the
activity and oversight led to the loss of the feed pumps. Weaknesses included a failure to
recognize the risks associated with throttling auxiliary condenser circulating water flow,
adjusting flow to two condensers simultaneously, giving a non-standard order (throttle slowly
closed to my mark), not understanding the throttling characteristics of a butterfly valve, not
establishing the initial valve positions and closely monitoring the position as it was adjusted,
not monitoring the most applicable system parameters for the expected changes, and failure
to recognize and compensate for a lack of proficiency of the operators in performing this
evolution.
Corrective Actions: As an immediate corrective action, Comanche Peak operators tripped the
Unit 2 reactor and stabilized the plant in mode 3. Personnel involved were removed from
on-shift duties pending remedial training. Longer term actions included additional oversite of
operations activities. Additional actions are discussed on AR 2020-00008.
Corrective Action References: CR-2020-00008
Performance Assessment:
Performance Deficiency: The failure to adequately supervise component manipulations and
control system parameters within procedure limits while adjusting circulating water flow
through the auxiliary condensers was a performance deficiency. Specifically, operators failed
to adequately prepare for adjusting circulating water flow to the Unit 2 main feedwater pump
auxiliary condenser outlet valves, which caused inappropriate valve manipulation during the
evolution and created a condition that required a Unit 2 reactor trip.
Screening: The inspectors determined the performance deficiency was more than minor
because it was associated with the human performance attribute of the Initiating Events
Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events
that upset plant stability and challenge critical safety functions during shutdown as well as
power operations. Specifically, the failure to adequately supervise component manipulations
and maintain system parameters within procedural limits led to the loss of both running main
feedwater pumps and a plant trip.
Significance: The inspectors assessed the significance of the finding using Appendix A, The
Significance Determination Process (SDP) for Findings At-Power. In accordance with
IMC 0609, Appendix A, Exhibit 1, the inspectors determined that the finding required a
detailed risk evaluation because the loss of feedwater caused operators to manually trip the
reactor and the loss of main feedwater constituted a loss of mitigation equipment used to
transition the plant to a stable shutdown condition.
The senior reactor analyst performed a detailed risk evaluation by treating the finding as an
initiating event and using the conditional core damage probability for a loss of main feedwater
as called for in Section 8.0, Initiating Event Analyses, of the Risk Assessment of Operational
Events Handbook. The analyst used Comanche Peak SPAR model version 8.58, run on
SAPHIRE, software version 8.2.1, for the evaluation.
The model was modified to reflect probabilistic recovery of a main feedwater pump. To
accomplish this, the analyst adjusted Basic Event MFW-XHE-XL-TRIP, Operator Fails to
                                                13
 
Restart Main Feedwater Flow, used in Fault Tree MFW, Main Feedwater System, from
TRUE to a SPAR-H human reliability model derived value of 4.40E-2. In this human reliability
analysis, the analyst assigned high stress to both diagnosis and action and moderate
complexity to both diagnosis and action for the recovery. All other performance shaping
factors were set to nominal. Also, the analyst credited the use of the licensees diverse and
flexible coping strategies (FLEX) equipment. Performance of the initiating event analysis with
these modifications yielded an estimate of the increase in core damage frequency of 7.8E-7
per year from internal events. Loss of main feedwater events were the dominant sequences
and were mitigated by the auxiliary feedwater system.
The analyst noted that this detailed risk assessment evaluates an actual event in which no
external events occurred. Additionally, the period that the events impacted plant equipment
was small enough that the probability of an external initiator occurring during this time would
be negligible. Therefore, the analyst assumed that the risk from external events, given the
subject performance deficiency, was essentially zero. This resulted a total estimate in the
increase of core damage frequency of 7.8E-7 per year, making the finding of very low safety
significance (Green).
The increase in large early release frequency from this finding was determined to be of very
low safety significance using IMC 0609, Appendix H, Containment Integrity Significance
Determination Process, because loss of main feedwater sequences screen as having low
safety significance in pressurized water reactors with large dry containments.
Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the
possibility of mistakes, latent issues, and inherent risk, even while expecting successful
outcomes. Individuals implement appropriate error reduction tools. The licensee identified in
their root cause analysis that operations did not recognize nor understand the risks
associated with the evolution. The inspectors concluded that as a result, operators did not
plan for the possibility of mistakes or implement appropriate error reduction tools.
Enforcement:
Violation: Technical Specification Section 5.4.1.a requires, in part, that written procedures
shall be established, implemented, and maintained covering the applicable procedures
recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
NRC Regulatory Guide 1.33, Revision 2, Appendix A, Section 3, addresses Procedures for
Startup, Operation, and Shutdown or Safety-Related PWR Systems and Section 3.K,
addresses Feedwater System. The licensee established Procedure SOP-310B, Circulating
Water, Revision 18, to address operation of the circulating water system, including adjusting
flow to the auxiliary condensers which support operation of main feedwater system.
Procedure SOP-310B, Revision 18, step 5.3.7, requires operators to slowly adjust the
auxiliary condenser differential pressure to between 1- and 10 feet H2O. Contrary to the
above, on January 1, 2020, the licensee failed to slowly adjust the auxiliary condenser
differential pressure and maintain it between 1- and 10 feet H2O when operators fully closed
the valves, causing a condition (dual feedwater pump trips on low vacuum) that required a
reactor trip.
Enforcement Action: This violation is being treated as a non-cited violation, consistent with
Section 2.3.2 of the Enforcement Policy.
                                              14
 
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
  *  On January 31, 2020, the inspectors presented the radiation safety exit meeting
      inspection results to Mr. T. McCool, Site Vice President, and other members of the
      licensee staff.
  *  On April 2, 2020, the inspectors presented the integrated inspection results to
      Mr. T. McCool and other members of the licensee staff.
                                                15
 
DOCUMENTS REVIEWED
Inspection Type              Designation    Description or Title                                        Revision or
Procedure                                                                                              Date
71111.04  Procedures        SOP-103B      Chemical and Volume Control System                          13
71111.05  Fire Plans        FPI-105B      U-2, train B Diesel generator and Equipment Elevation, 810' 2
            Miscellaneous                    Fire Hazard Analysis Report Sections 5.9.7 and 5.6          32
                              Drill 20-15-01 Fire Drill Scenario for EDG 2-02 810' Fuel Oil Transfer Pit March 3,
                                                                                                        2020
71111.12  Corrective Action TR-YYYY-NNNN  2016-008019
            Documents
            Miscellaneous                    Maintence Rule Summary Report for Unit 1 and Unit 2        02/18/2020
                                            Auxillary Feedwater
                                            Auxiliary Feedwater System Status                          2nd Quarter
                                                                                                        FY19
71111.13  Drawings          E2-0026        6.9KV Three Line Diagram Normal Buses                      13
            Miscellaneous    STI-600.01-1  Guarded Equipment Management Posting Log                    February 12,
                                                                                                        2020
            Procedures        SOP-310B      Circulating water System                                    18
            Work Orders      5835726        Auxiliary Feedwater Pump Turbine 2-01Govenor Stroke        02/13/2020
71111.15  Corrective Action CR            2019-9530                                                  12/13/2019
            Documents        TR            2020-1247                                                  February 19,
                                                                                                        2020
            Drawings          M2-2760        Diesel Engine Start/Stop Logic                              15
            Operability                      FSAR Table 8.3-1, Loading Requirements for Loss of          104
            Evaluations                      Coolant Accident Coincident with Loss of Offsite Power
                              CR-            2020-001295
71111.19  Corrective Action CR-YYYY-NNNN  2019-009453
            Documents        IR-2020-001597 Multiple Relays Out of Tolerance on Unit 2 Train B
                                            Sequencer
            Procedures        INC-7393A      CH Cal Neutron Flux Power Range ION Current Gain and        6
                                            Summing Level Amplifier
                              MSE-S2-0673B  Unit 2 Train B Sequencer Under Voltage Relay Surveillance  5
            Work Orders      WO 5666818    Perform MSE-S2-0673B, TR B Sequencer UV Relay
                              WO 5840776    Troubleshoot and Repair Sequence Alarm Circuit as
                                            documented in IR-2019-009453
                                                        16
 
Inspection Type          Designation Description or Title                                        Revision or
Procedure                                                                                        Date
                        WO 5848383  Replace Cell 22 on BT1D4 at Power
                        WO 5866715  Perform CCAL IAW INC-7393A
                        WO 5866789  Troubleshoot test signal going to zero described in CR 2020-
                                    001447
71111.20  Miscellaneous            BEACON 3D Reactivity Projection for Unit 2 Forced Outage    01/01/2020
                                    Startup
71111.22  Procedures    ETP-106    Monthly RCCA Repositioning                                  1
                        OPT-106A    Control Rod Exercise                                        12
                        OPT-467A    Train A Safeguards Slave realy K609 Actuation Test          Revision 5
          Work Orders  WO 5656218  Solid State Protection System Slave Relay Test              March 11,
                                                                                                  2020
                        WO 5659452  Perform NUC 202 AT-Power MTC Measurement
                        WO 5829754  OPT-106A, Control Rod Exercise Test
                        WO 5846000  Monthly RCCA Reposit ETP-106
                        WO 5852752  IR-2020-000542 Troubleshoot 2-01 EDG Volt Reg TRBL
71114.06  Miscellaneous            ERO team Exercise                                            February 9,
                                                                                                  2020
71124.05  Calibration  3443188    X-RE-5700 ICI-4998, CCAL FB VNT EXH                          06/24/2009
          Records      3648653    2-RE-6297, ICI-4961 Channel Calibration                      09/30/2010
                        391556      1-RE-6295 ICI-4961, CCAL                                    03/16/2009
                        4373552    1-RE-6295 ICI-4961, CCAL                                    04/12/2016
                        4374577    2-RE-6297 ICI-4961, CCAL                                    05/10/2017
                        4426655    X-RE-5700 ICI-4998, CCAL FB VNT EXH                          01/22/2015
                        4520934    1-RE-6256 ICI-4959 CCAL HRAM                                06/09/2015
                        5371788    X-RE-5701 INC-4915X, CCAL AB VNT GPRM                        07/18/2019
                        5522342    1-RE-6290A INC-7079, CCAL CNTMT HRRM                        05/16/2019
                        5522458    1-RE-6290B INC-7079, CCAL CNTMT HRRM                        05/02/2019
                        5526341    1-RUK-2326A/2328A INC-4916 CCAL                              07/17/2019
                        ASCAN      WBC System Calibration Data Package                          11/20/2019
                        FSCAN      WBC System Calibration Data Package                          09/12/2019
                        HP-0058    Argos/Sirius Calibration Data Sheet                          11/10/2019
                        HP-0063    NE Technology SAM Calibration Data Sheet                    10/22/2018
                        HP-0075    GEM-5 Calibration Data Sheet                                02/04/2019
                                                17
 
Inspection Type              Designation    Description or Title                                          Revision or
Procedure                                                                                                Date
                            HP-1206        Ludlum Model 177 Frisker Calibration Data Sheet              01/27/2020
                            HP-2166        AMS-4 Calibration Data Sheet                                  10/04/2019
                            HP-4124        Thermo RO-20AA Calibration Data Sheet                        01/29/2020
                            HP-5002        Low Volume Air Sampler Calibration Data Sheet                10/12/2018
                            HP-711812      RDS-31 Calibration Data Sheet                                10/07/2019
          Corrective Action CR-YYYY-NNNN  2011-006222, 2016-001350, 2018-003694, 2018-006522,
          Documents                        2018-006631, 2018-007217, 2019-000184, 2019-001550,
                                            2019-004125, 2019-004570, 2019-005318, 2019-007716,
                                            2019-008045, 2019-008114, 2019-008129
                            TR-YYYY-NNNN  2018-006999, 2018-007197, 2018-007846, 2019-001511,
                                            2019-003201, 2019-003405, 2019-003992, 2019-004146,
                                            2019-004149, 2019-004221, 2019-005656, 2020-000063
          Corrective Action CR-YYYY-NNNN  2020-000750, 2020-000783, 2020-000814
          Documents
          Resulting from
          Inspection
          Miscellaneous    1-RE-6290A    Last Detector Primary Calibration                            05/15/2019
                            19-001 through Calibration Well Source Charts                                08/08/2019
                            19-007
                            2Qtr FY19      CPNPP System Status: Radiation Monitoring
                            T190990        RadCal 2026C and 1800cc, 180cc, and 6cc detectors            05/29/2019
          Procedures        CLI-782        APEX Gamma Spectroscopy Counting System                      2
                            ICI-4959      Channel Calibration - High Range Area Radiation Monitors      4
                            ICI-4961      Channel Calibration - Digital High Range Area Monitors        4
                            ICI-4998      Channel Calibration - Gas Process Radiation Monitor          4
                            INC-7079      Channel Calibration -                                        6
                                            Containment High Range Radiation Monitor Channels
                                            1-RE-6290A/B and 2-RE-6290A/B
                            RPI-301        Portable Survey Instruments                                  13
                            RPI-800        Control of Radiation Protection Equipment                    17
                            RPI-802        Performance of Source Checks                                  28
                            RPI-862        Calibration of the Argos/Sirius Personnel Contamination      14
                                            Monitor and Gem-5 Gamma Exit Monitor
                            STA-619        Administrative Control of Digital Radiation Monitoring System 7
                                                      18
 
Inspection Type              Designation  Description or Title                                      Revision or
Procedure                                                                                            Date
                            STA-650      General Health Physics Plan                                8
                            STA-658      Radiation Protection Equipment Calibration Program        12
                            STA-677      Preventative Maintenance Program                          13
                            STA-700      Surveillance Frequency Control Program                    1
                            STI-677.01    PM Change Processing                                      2
          Self-Assessments  EVAL-2018-006 Work Management/Radiation Protection Audit                08/02/2018
                            EVAL-2019-007 Chemistry Control and Chemistry Measurement & Analysis    11/21/2019
71124.06  Calibration      WO 5360001    X-RE-5567A, South Plant Vent Stack Radiation Monitor      07/30/2018
          Records                        Calibration
                            WO 5421935    1-RE-4269, Unit 1 Station Service Water Train A to        10/24/2018
                                          Discharge Canal Radiation Monitor Calibration
                            WO 5447947    X-FT-5288, LWPS LHMT X-01/X-02 Discharge to VD System      09/27/2018
                                          Flow Transmitter Calibration
                            WO 5556086    2-RE-5100, Turbine Sump 2-04 Radiation Monitor Calibration 06/12/2019
                            WO 5576336    2-RE-4269, Unit 2 Station Service Water Train A to        09/25/2019
                                          Discharge Canal Radiation Monitor Calibration
                            WO 5585319    X-RE-5253, Liquid Waste Processing Discharge Radiation    10/28/2019
                                          Monitor Calibration
                            WO 5590739    X-RE-5570B, North Plant Vent Stack WRGM Radiation          10/01/2019
                                          Monitor Calibration
                            WO 5631300    1-RE-4270, Unit 1 Station Service Water Train B to        01/14/2020
                                          Discharge Canal Radiation Monitor
          Corrective Action CR-YYYY-NNNN  2019-008687, 2019-008794
          Documents        TR-YYYY-NNNN  2017-000757, 2018-003362, 2019-001642, 2019-005866,
                                          2019-006713, 2019-008605
          Corrective Action TR-YYYY-NNNN  2020-000766, 2020-000815, 2020-000817
          Documents        TR-YYYY-NNNN  2020-000766, 2020-000815, 2020-000817
          Resulting from
          Inspection
          Miscellaneous                  CPSES Offsite Dose Calculation Manual, Unit 1 and Unit 2  34
                                          2017 Annual Radioactive Effluent Release Report            03/12/2018
                                          2018 Annual Radioactive Effluent Release Report            04/20/2019
                            G2018-034    Gaseous Discharge Permit - Unit 1 Containment Vent        02/27/2018
                            G2018-208    Gaseous Discharge Permit - Plant Vent Stack B              12/09/2018
                                                      19
 
Inspection Type              Designation  Description or Title                                      Revision or
Procedure                                                                                            Date
                            G2018-210    Gaseous Discharge Permit - Non-Routine Gas Normal          12/10/2018
                            G2019-046    Gaseous Discharge Permit - Plant Vent Stack B              03/12/2019
                            G2019-193    Gaseous Discharge Permit - Unit 2 Containment Vent        11/24/2019
                            G2019-216    Gaseous Discharge Permit - Plant Vent Stack A              12/31/2019
                            L2018-023    Liquid Discharge Permit - Plant Effluent Tank 1            07/05/2018
                            L2018-040    Liquid Discharge Permit - Plant Effluent Tank 2            10/24/2018
                            L2018-051    Liquid Discharge Permit - Low Volume Waste Pond (LVWP)    12/01/2018
                            L2019-016    Liquid Discharge Permit - Plant Effluent Tank 1            02/14/2019
                            L2019-055    Liquid Discharge Permit - Squaw Creek Reservoir            08/01/2019
                            L2019-072    Liquid Discharge Permit - Plant Effluent Tank 2            12/12/2019
          Procedures        CHM-170      Liquid and Gaseous Effluent Program                        4
                            CHM-230      Guidelines for Sample Collection                          3
                            CLI-744      Radioactive Effluent Pre-Release Permit Processing        2
                            CLI-745      Radioactive Effluent Post-Release Permit Processing and    3
                                          Surveillance Tracking
                            STA-603      Control of Station Radioactive Effluents                  21
                            STA-619      Administrative Control of the Digital Radiation Monitoring 7
                                          System
                            STA-677      Preventive Maintenance Program                            13
          Self-Assessments  EVAL-2019-007 Radioactive Waste, Effluents, Environmental, and Chemistry 11/21/2019
                                          Programs
          Work Orders      WO 5319196    Primary Plant Ventilation Exhaust Filter Unit X-16        01/31/2018
                            WO 5377734    Primary Plant Ventilation Exhaust Filter Unit X-01        10/03/2018
                            WO 5431297    Primary Plant Ventilation Exhaust Filter Unit X-02        11/17/2018
                            WO 5558463    Primary Plant Ventilation Exhaust Filter Unit X-02        09/18/2019
71124.07  Corrective Action CR-YYYY-NNNN  2018-001574, 2018-001611, 2018-001760, 2018-004523,
          Documents                      2019-002077
                            TR-YYYY-NNNN  2018-001867, 2018-004228, 2019-001642, 2019-007287
                                          2019-008284, 2019-009052, 2019-009165
          Corrective Action CR-YYYY-NNNN  2020-000748
          Documents
          Resulting from
          Inspection
                                                      20
 
Inspection Type            Designation  Description or Title                                      Revision or
Procedure                                                                                            Date
          Miscellaneous                  2017 Annual Radiological Environmental Operating Report    04/30/2018
                                          2018 Annual Radiological Environmental Operating Report    04/01/2019
                            NUPIC Audit  GEL Laboratories (JQA-14-097)                              05/29/2014
                            23724
                            NUPIC Audit  GEL Laboratories (NOD-19-018)                              08/29/2019
                            24747
                            (NOV2019-069)
                            ODCM          Comanche Peak Steam Electric Station Offsite Dose          34
                                          Calculation Manual Unit 1 and Unit 2
                            RPI-714-1-    2018 Land Use Census                                      07/31/2018
                            20180715
                            RPI-714-1-    2019 Land Use Census                                      07/25/2019
                            20190620
          Procedures      RPI-538      Process Environmental Badges                              9
                            RPI-710      Radiological Environmental Monitoring, Sampling, and      22
                                          Analysis Program
                            RPI-713      Collection, Preparation, and Shipment of Radiological      19
                                          Environmental Samples
                            RPI-714      Land Use Census                                            6
                            RPI-888      Calibration of Portable Air Sample Equipment              5
                            STA-653      Contamination Control Program                              20
                            STA-654      Groundwater Protection Program                            9
          Self-Assessments EVAL-2019-007 Radioactive Waste, Effluents, Environmental, amd Chemistry 11/21/2019
                                          PRgrams
          Work Orders      WO-          4938991, 4965490, 5052258, 5080201, 5490927,
                                          5651858, 5654059, 5654081, 5654093, 5654106,
                                          5654119, 5654136, 5659602, 5659645, 5667801,
                                          5736155, 5736168, 5736197, 5736232, 5736248,
                                          5736282, 5736299, 5741625, 5747140
                                                    21
}}

Latest revision as of 21:13, 21 August 2022

Integrated Inspection Report 05000445/2020001 and 05000446/2020001
ML20128J555
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 05/07/2020
From: O'Keefe N
NRC/RGN-IV/DRP/RPB-B
To: Peters K
Vistra Operations Company
References
IR 2020001
Download: ML20128J555 (24)


See also: IR 05000445/2020001

Text

May 7, 2020

Mr. Ken Peters

Senior Vice President and Chief Nuclear Officer

VISTRA Operations Company, LLC

P.O. Box 1002

Glen Rose, TX 76043

SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT, UNITS 1 AND 2 -

INTEGRATED INSPECTION REPORT 05000445/2020001 AND

05000446/2020001

Dear Mr. Peters:

On March 31, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at Comanche Peak Nuclear Power Plant, Units 1 and 2. On April 2, 2020, the NRC inspectors

discussed the results of this inspection with Mr. T. McCool, Site Vice President, and other

members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding

involved a violation of NRC requirements. We are treating this violation as a non-cited

violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector

at Comanche Peak Nuclear Power Plant, Units 1 and 2.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the

NRC Resident Inspector at Comanche Peak Nuclear Power Plant, Units 1 and 2.

K. Peters 2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

Cornelius Digitally signed by

Cornelius F. O'Keefe

F. O'Keefe Date: 2020.05.07

14:50:23 -05'00'

Neil F. O'Keefe, Chief

Reactor Projects Branch B

Division of Reactor Projects

Docket Nos. 05000445 and 05000446

License Nos. NPF-87 and NPF-89

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

ML20128J555

Non-Sensitive Publicly Available

SUNSI Review

Sensitive Non-Publicly Available

OFFICE SRI:DRP/B RI:DRP/B DRS/IPAT DRS/EB1

NAME JEllegood NDay AAgrawal VGaddy

DATE 05/01/2020 05/04/2020 05/01/2020 05/04/2020

OFFICE DRS/EB2 DRS/OB DRS/RCB DNMS/RxIB

NAME NTaylor GWerner MHaire GWarnick

DATE 05/04/2020 05/04/2020 05/01/2020 05/04/2020

OFFICE SPE/DRP/B BC:DRP/B

NAME DProulx NOKeefe

DATE 05/04/2020 05/07/2020

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers: 05000445 and 05000446

License Numbers: NPF-87 and NPF-89

Report Numbers: 05000445/2020001 and 05000446/2020001

Enterprise Identifier: I-2020-001-0010

Licensee: VISTRA Operations Company, LLC

Facility: Comanche Peak Nuclear Power Plant, Units 1 and 2

Location: Glen Rose, TX 76043

Inspection Dates: January 1 to March 31, 2020

Inspectors: J. Ellegood, Senior Resident Inspector

D. Antonangeli, Health Physicist

B. Baca, Health Physicist

N. Day, Resident Inspector

N. Greene, Senior Health Physicist

J. Melfi, Project Engineer

J. O'Donnell, Senior Health Physicist

Approved By: Neil F. O'Keefe, Chief

Reactor Projects Branch B

Division of Reactor Projects

Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Comanche Peak Nuclear Power Plant,

Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight

Process is the NRCs program for overseeing the safe operation of commercial nuclear power

reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Manual Reactor Trip Due to Loss of both Main Feed Pumps

Cornerstone Significance Cross-Cutting Report

Aspect Section

Initiating Events Green [H.12] - Avoid 71153

NCV 05000446/2020001-01 Complacency

Open/Closed

A self-revealed finding and associated non-cited violation (NCV) of very low safety

significance occurred when the licensee failed to implement procedures for operation of the

feed and condensate system as required by Technical Specification 5.4.1.a. Specifically,

while adjusting flow to the auxiliary condensers for the Unit 2 main feed pumps, the operators

isolated circulating water flow to the condensers, causing a loss of both Unit 2 main feedwater

pumps. Control room operators manually insert a plant trip in response to the loss of

feedwater.

Additional Tracking Items

Type Issue Number Title Report Section Status

LER 05000446/2018-002-01 LER 2018-002-01 for 71153 Closed

Comanche Peak, Unit 2,

Automatic Actuation of

Auxiliary Feedwater System.

LER 05000446/2019-002-00 LER 2019-002-00 for 71153 Closed

Comanche Peak Nuclear

Power Plant, Unit 2,

Automatic Actuation of

Auxiliary Feedwater System.

2

PLANT STATUS

Unit 1 began the inspection period at rated thermal power and remained there throughout the

inspection period.

Unit 2 began the inspection period at rated thermal power. On January 1, 2020, the licensee

inserted a manual trip in response to a loss of both main feed pumps while adjusting circulating

water flow to the auxiliary condensers. The licensee took the reactor critical and synchronized

to the grid on January 3, 2020. The licensee reached 100 percent power on January 4, 2020,

and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. From January 1 - March 19, 2020, the inspectors performed

plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine

reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed

selected procedures and records, observed activities, and interviewed personnel to assess

licensee performance and compliance with Commission rules and regulations, license

conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President

of the United States on the public health risks of the coronavirus (COVID-19), resident

inspectors were directed to begin telework and to remotely access licensee information using

available technology. During this time the resident inspectors performed periodic site visits

each week and during that time conducted plant status activities as described in IMC 2515,

Appendix D; and observed risk-significant activities when warranted. In addition, resident and

regional baseline inspections were evaluated to determine if all or portions of the objectives and

requirements stated in the IP could be performed remotely. If the inspections could be

performed remotely, they were conducted per the applicable IP. In the cases where it was

determined the objectives and requirements could not be performed remotely, management

elected to postpone and reschedule the inspection to a later date.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the adequacy of the overall preparations to protect

risk-significant systems from forecasted thunderstorms on January 10, 2020

3

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1) Unit 2, chemical and volume control system on February 6, 2020

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1) Unit 1, turbine building basement on January 17, 2020

(2) Unit 2, turbine building basement on January 17, 2020

(3) Unit 2, emergency diesel generator A room on January 23, 2020

(4) Service water intake structure building on March 26, 2020

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the onsite fire brigade training and performance during an

unannounced fire drill on March 3, 2020

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1

Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control

room during turbine start and synchronization to the grid on January 3, 2020

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operators for just in time training for

a reactor startup on January 2, 2020

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components (SSCs) remain capable of performing their intended

function:

(1) Unit 2, auxiliary feedwater system on February 25, 2020

4

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed;

(1) Realignment of the Units 1 and 2 circulating water system on January 15, 2020

(2) Planned yellow risk for Unit 1 auxiliary feedwater valve strokes concurrent with

emergent work to restore the Unit 1 emergency diesel generator A to operable status

on February 14, 2020

(3) Risk associated with switchyard work and troubleshooting of Unit 2 circulating water

pump on February 7, 2020

(4) Risk associated with starting the Unit 2 circulating water pump 2 on March 5, 2020

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1) Unit 1, residual heat removal systems A and B, due to increasing pressures as

described in condition report CR-2019-009779 on January 9, 2020

(2) Unit 2, emergency diesel generator A, due to a degraded time delay device as

described in condition report CR-2020-001295 on February 24, 2020

(3) Unit 2, safety chiller 2-06, tripping due to a shorting bulb socket assembly as

described in condition report CR 2020-001502 on March 2, 2020

(4) Unit 2, control rods from potential thermal sleeve cracking as described in Part 21

report LTR-NRC-19-79, and corrective action document TR 2020-1247

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the following post maintenance test activities to verify system

operability and functionality:

(1) Repair of disconnected wires and replacement of components in the Unit 2 safeguard

sequencer system per Work Order 5840776 on February 20, 2020

(2) Replacement of cell 22 on battery 1DT4 per Work Order 5848383 on January 31,

2020

(3) Repair of failed switch on neutron flux power ranch channel N-42 per Work

Order 5866789 on February 28, 2020

(4) As found testing, calibration, and installation of Unit 2 safeguard sequencer B

undervoltage relays per Work Order 5666818 on March 4, 2020.

5

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01) (4 Samples)

(1) Unit 2, emergency diesel generator monthly load test per Procedure OPT 214B, Diesel

Generator Operability Test, Revision 16, on January 22, 2020

(2) Unit 2, at power end of core life reactivity test per Work Order 5659452 on February 10,

2020

(3) Unit 1, monthly control rod exercise surveillance per Work Order 5829754 on

January 24, 2020

(4) Unit 1, train A slave relay K609 actuation test per Work Order 5656218 on March 11,

2020

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01)

(1 Sample)

(1) The blue team emergency preparedness drill on February 19, 2020.

RADIATION SAFETY

71124.05 - Radiation Monitoring Instrumentation

Walk Downs and Observations (IP Section 02.01) (1 Sample)

The inspectors evaluated the following radiation detection instrumentation during plant

walkdowns:

(1) Portable Survey Instruments

  • RM-177, HP-1461
  • RM-177, HP-1113
  • RM-177, HP-1145
  • RM-177, HP-2400
  • RM-177, HP-1464
  • RM-177, HP-1081
  • RM-177, HP-1026
  • AMS-4, HP-2166
  • 3030E, HP-3270

Source Check Demonstration

  • Rad Eye G, HP-3112
  • Telepole, HP-1906
  • Rad Eye GX, HP-4045
  • Ludlum Model 3000, HP-3166

Area Radiation Monitors and Continuous Air Monitors

  • 2-RE-6253

6

  • 2-RE-6259A
  • 2-RE-6297
  • X-RE-5896A
  • X-RE-5895B
  • 1-RE-6256
  • 1-RE-6295

Personnel Contamination Monitors, Portal Monitors and Small Article Monitors

  • GEM-5, HP-0075
  • GEM-5, HP-0076

Calibration and Testing Program (IP Section 02.02) (1 Sample)

The inspectors evaluated the calibration and testing of the following radiation detection

instruments:

(1) Alarm Setpoint and Calibration Method Check of Personnel Contamination Monitors,

Portal Monitors and Small Article Monitors

  • GEM-5, HP-0075

Failure to Meet Calibration or Source Check Acceptance Criteria

  • Telepole, HP-1907
  • ARGOS, HP-0065
  • RO-20AA, HP-4123
  • AMS-4, HP-2166

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Walk Downs and Observations (IP Section 02.01) (1 Sample)

The inspectors walked down the following gaseous and liquid radioactive effluent monitoring

and filtered ventilation systems to assess the material condition and verify proper alignment

according to plant design:

(1) * Plant Vent Stack Radiation Monitoring System

  • Liquid Waste Processing Radiation Monitoring System
  • Turbine Sump Radiation Monitoring System
  • Station Service Water to Discharge Canal Radiation Monitoring System

Calibration and Testing Program (Process & Effluent Monitors) (IP Section 02.02) (1 Sample)

The inspectors reviewed the following gaseous and liquid effluent monitor instrument

calibrations and tests:

(1) * WO 5360001, X-RE-5567A, South Plant Vent Stack Radiation Monitor

Calibration, 07/30/2018

7

Calibration, 10/01/2019

  • WO 5585319, X-RE-5253, Liquid Waste Processing Discharge Radiation

Monitor Calibration, 10/28/2019

  • WO 5556086, 2-RE-5100, Turbine Sump 2-04 Radiation Monitor Calibration,

06/12/2019

Canal Radiation Monitor Calibration, 10/24/2018

Canal Radiation Monitor Calibration, 01/14/2020

Canal Radiation Monitor Calibration, 09/25/2019

  • WO 5447947, X-FT-5288, LWPS LHMT X-01/X-02 Discharge to VD System

Flow Transmitter Calibration, 09/27/2018

Sampling and Analysis (IP Section 02.03) (1 Sample)

The inspectors reviewed the following:

(1) Radioactive Effluent Sampling and Analysis Activities

  • Plant Ventilation Weekly Sampling, 01/27/2020
  • Containment Ventilation Sampling, 01/30/2020

Effluent Discharge Permits

  • G2018-034, Unit 1 Containment Vent, 02/27/2018
  • G2018-208, Plant Vent Stack B, 12/09/2018
  • G2018-210, Non-Routine Gas Normal, 12/10/2018
  • G2019-046, Plant Vent Stack B, 03/12/2019
  • G2019-193, Unit 2 Containment Vent, 11/24/2019
  • G2019-216, Plant Vent Stack A, 12/31/2019
  • L2018-023, Plant Effluent Tank 1, 07/05/2018
  • L2018-040, Plant Effluent Tank 2, 10/24/2018
  • L2018-051, Low Volume Waste Pond (LVWP), 12/01/2018
  • L2019-016, Plant Effluent Tank 1, 02/14/2019
  • L2019-055, Squaw Creek Reservoir, 08/01/2019
  • L2019-072, Plant Effluent Tank 2, 12/12/2019

Instrumentation and Equipment (IP Section 02.04) (1 Sample)

The inspectors reviewed the following radioactive effluent discharge system surveillance test

results:

(1) * WO 5319196, Primary Plant Ventilation Exhaust Filter Unit X-16 - Carbon

Analysis B Train, 01/13/2018

  • WO 5377734, Primary Plant Ventilation Exhaust Filter Unit X-01 - ESF Filter

Test A Train, 10/31/2018

  • WO 5431297, Primary Plant Ventilation Exhaust Filter Unit X-02 - ESF Filter

Test B Train, 11/07/2018

8

Analysis B Train, 09/18/2019

Dose Calculations (IP Section 02.05) (1 Sample)

The inspectors reviewed the following to asses public dose:

(1) Liquid and Gaseous Discharge Permits

  • G2018-034, Unit 1 Containment Vent, 02/27/2018
  • G2018-208, Plant Vent Stack B, 12/09/2018
  • G2018-210, Non-Routine Gas Normal, 12/10/2018
  • G2019-046, Plant Vent Stack B, 03/12/2019
  • G2019-193, Unit 2 Containment Vent, 11/24/2019
  • G2019-216, Plant Vent Stack A, 12/31/2019
  • L2018-023, Plant Effluent Tank 1, 07/05/2018
  • L2018-040, Plant Effluent Tank 2, 10/24/2018
  • L2018-051, Low Volume Waste Pond (LVWP), 12/01/2018
  • L2019-016, Plant Effluent Tank 1, 02/14/2019
  • L2019-055, Squaw Creek Reservoir, 08/01/2019
  • L2019-072, Plant Effluent Tank 2, 12/12/2019

Annual Radiological Effluent Release Reports

Abnormal Gaseous or Liquid Tank Discharges

  • None were available for review during this inspection

71124.07 - Radiological Environmental Monitoring Program

Site Inspection (IP Section 02.01) (1 Sample)

The inspectors evaluated the radiological environmental monitoring program

implementation.

(1) The inspectors reviewed the following:

Walkdowns, Calibrations, and Maintenance Record Review

  • Air sampling stations: A1, A2, A3, A4, A5, A6, A7, A8
  • Thermoluminescent dosimeter (TLD) monitoring stations: R1, R4, R11, R13,

R22, R25, R27, R29, R30, R36

  • Calibrations of selected air sample pumps: 2178, 2196B, 2214, and 2224

Environmental Sample Collections and Preparation Observation

  • Air particulate (A1, A2, A3, A4, A5, A6, A7, A8)
  • Air charcoal (A1, A2, A3, A4, A5, A6, A7, A8)
  • Broad leaf (BL1, BL2, BL3)
  • Surface water (SW1, SW2, SW3, SW4, SW5)

9

Licensee Actions in Response to Missed Sample, Inoperable Sampler, Lost

Thermoluminescent Dosimeter (TLD) or Anomalous Measurement

The inspectors reviewed the licensee's response to 13 missing or anomalous TLD

results. The inspectors reviewed 6 inoperable samplers as noted in corrective action

documents since May 2017 and noted in the 2017 and 2018 Annual Environmental

Operating Reports. The majority of inoperable samplers were attributed to loss of

power due to external events, such as weather and power line work.

Sampling Program for the Potential of Licensed Material Entering Groundwater

  • Groundwater Monitoring Wells: 9, 10, 11, 12, 14, 15, 16, 19, 25, CP-A, CP-B,

CP-C

Groundwater Protection Initiative (GPI) Implementation (IP Section 02.02) (1 Sample)

(1) The inspectors evaluated the licensee's voluntary groundwater protection initiative.

A few observations were as follows:

  • The general maintenance and material condition of the groundwater

monitoring wells was adequate with the general area around the well was

kept clear of any obstructions.

  • Most monitoring wells had enough water for samples to be taken.
  • Monitoring well locations 11 and CP-A had results of 835 and 1700 pCi/L,

respectively, which are both below their lower limit of detection (LLD)

requirements. The remaining well location samples all tested below the

minimum detectable activity.

  • The licensee implemented additional surface water sampling of the drainage

flow catch basin to track the potential impact of a water treatment filtered

water storage tank leak. The licensee has corrective actions in progress to

address the identified leak.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) (2 Samples)

(1) Unit 1 January 1, 2019, to December 31, 2019

(2) Unit 2 January 1, 2019, to December 31 2019

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02)

(2 Samples)

(1) Unit 1 January 1, 2019, to December 31, 2019

(2) Unit 2 January 1, 2019, to December 31, 2019

10

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)

(1) Unit 1 January 1, 2019, to December 31, 2019

(2) Unit 2 January 1, 2019, to December 31, 2019

71153 - Follow-up of Events and Notices of Enforcement Discretion

Event Follow-up (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated licensee response to a Unit 2 reactor trip on January 1,

2020.

Event Report (IP Section 03.02) (2 Samples)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000446/2019-002-00, Automatic Actuation of Auxiliary Feedwater System

(ADAMS Accession No. ML19199A033). The inspectors determined that it was not

reasonable to foresee or correct the cause discussed in the LER; therefore, no

performance deficiency was identified. The inspectors did not identify a violation of

NRC requirements.

(2) LER 05000446/2018-002-01, Automatic Actuation of Auxiliary Feedwater System

(ADAMS Accession No. ML 19199A032). The inspectors determined that it was not

reasonable to foresee or correct the cause discussed in the LER; therefore, no

performance deficiency was identified. The inspectors did not identify a violation of

NRC requirements.

INSPECTION RESULTS

Manual Reactor Trip Due to Loss of both Main Feed Pumps

Cornerstone Significance Cross-Cutting Report

Aspect Section

Initiating Events Green [H.12] - Avoid 71153

NCV 05000446/2020001-01 Complacency

Open/Closed

A self-revealed finding and associated non-cited violation (NCV) of very low safety

significance occurred when the licensee failed to implement procedures for operation of the

feed and condensate system as required by Technical Specification 5.4.1a. Specifically,

while adjusting flow to the auxiliary condensers for the Unit 2 main feed pumps, the licensee

isolated circulating water flow to the condensers, causing a loss of both Unit 2 main

feedwater pumps. Control room operators manually insert a plant trip in response to the loss

of feedwater.

Description: On January 1, 2020, the Comanche Peak on-shift operations crew decided to

secure a running circulating water pump for Unit 2. Although securing the pump was not on

the plan of the day schedule, the shift manager added the activity into the shift's work

activities to support planned work the following week. The inspectors noted that the activity

would use normal circulating water system operating Procedure SOP-310B, Circulating

Water, Revision 18, and the work schedule provided enough time to prepare for and conduct

the evolution. The procedure was structured to secure one circulating water pump, adjust

11

flow as needed to the main condenser, and then to adjust flow to the two main feedwater

pump auxiliary condensers. There are two steam driven main feedwater pumps.

The auxiliary condensers support operation of the two main feedwater pumps by condensing

the steam used by the feedwater pump turbines. Flow was being adjusted to optimize plant

thermal efficiency.

The crew successfully secured the circulating water pump and adjusted main condenser flow.

The crew then proceeded to the auxiliary condensers to adjust circulating water flow. A field

operator was stationed at each of the two auxiliary condenser outlet valves and a third field

operator was communicating with the main control room staff. In addition, a senior reactor

operator provided local oversight of the evolution. The crew intended to adjust the throttle

position of the circulating water with a final position directed by the reactor operator in the

control room. The reactor operator directed the valve operators to slowly close their

respective valves (simultaneously) to his mark while he monitored water box outlet

temperature. The valves were initially in a throttled position at the start and they reached the

fully closed position shortly after starting. Without any flow to the auxiliary condensers, both

main feedwater pumps automatically tripped on low vacuum to protect the pumps. Control

room staff immediately inserted a manual trip from 100 percent power. The control room

operators stabilized the plant in mode 3 using Emergency Procedure E-0, Reactor Trip and

Safety Injection, and normal operating procedures without further issue.

Personnel directly involved in the task failed to recognize that condenser vacuum would

respond quickly to reduced cooling water flow, but there would be delays before condensate

temperature would be reduced as the circulating water was adjusted due to mixing. In

addition, the personnel directly involved in the task did not recognize that the auxiliary

condenser outlet valves were two turns from full closed at the start of the evolution. These

factors led the field operators to erroneously fully close the valves prior to control room

direction to stop throttling the valves. The inspectors noted that the auxiliary condenser outlet

valves had large valve position indicators to provided system configuration information to the

local operators.

Comanche Peak performed a root cause evaluation to understand the event. The review

identified several weaknesses in crew performance that contributed to the event. Weakness

identified as the root cause were an over-reliance on process (i.e., procedures) coupled with

a failure to address gaps in behaviors and standards. This resulted in a lack of critical

thinking by plant staff as well as a failure to understand and address risks associated with the

proposed activities. During this evolution, operators failed to recognize the potential to lose

vacuum for the feed pumps due to a lack in understanding system operation and

fundamentals. The crew considered the throttling of cooling water flow to be a routine activity

and, therefore, the task preparations did not trigger a focused brief to discuss the evolution.

However, changing the circulating water pump configuration only occurs during winter months

to allow for maintenance on the pumps. The operators assigned to the task had a lack of

proficiency as none of the operators directly involved with adjusting flow on the auxiliary

condensers had secured a circulating water pump before. Furthermore, the operations shift

included three operators that had performed this evolution previously, but none were directly

involved in adjusting flow to the auxiliary condensers. The inspectors noted that their direct

involvement could have reduced the likelihood of an error during the evolution. In addition,

periodic throttling of the auxiliary condenser outlet valve flow occurred with regularity;

however, the adjustments were normally made in small increments with time between valve

movements to allow the system to equilibrate.

12

The inspectors performed walkdowns of the evolution after the event, interviewed the

personnel involved, reviewed plant operating procedures, and reviewed the root cause

evaluation. The inspectors noted that although Comanche Peak used the correct procedure

and the procedure had been used successfully previously, weaknesses in preparation for the

activity and oversight led to the loss of the feed pumps. Weaknesses included a failure to

recognize the risks associated with throttling auxiliary condenser circulating water flow,

adjusting flow to two condensers simultaneously, giving a non-standard order (throttle slowly

closed to my mark), not understanding the throttling characteristics of a butterfly valve, not

establishing the initial valve positions and closely monitoring the position as it was adjusted,

not monitoring the most applicable system parameters for the expected changes, and failure

to recognize and compensate for a lack of proficiency of the operators in performing this

evolution.

Corrective Actions: As an immediate corrective action, Comanche Peak operators tripped the

Unit 2 reactor and stabilized the plant in mode 3. Personnel involved were removed from

on-shift duties pending remedial training. Longer term actions included additional oversite of

operations activities. Additional actions are discussed on AR 2020-00008.

Corrective Action References: CR-2020-00008

Performance Assessment:

Performance Deficiency: The failure to adequately supervise component manipulations and

control system parameters within procedure limits while adjusting circulating water flow

through the auxiliary condensers was a performance deficiency. Specifically, operators failed

to adequately prepare for adjusting circulating water flow to the Unit 2 main feedwater pump

auxiliary condenser outlet valves, which caused inappropriate valve manipulation during the

evolution and created a condition that required a Unit 2 reactor trip.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the human performance attribute of the Initiating Events

Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events

that upset plant stability and challenge critical safety functions during shutdown as well as

power operations. Specifically, the failure to adequately supervise component manipulations

and maintain system parameters within procedural limits led to the loss of both running main

feedwater pumps and a plant trip.

Significance: The inspectors assessed the significance of the finding using Appendix A, The

Significance Determination Process (SDP) for Findings At-Power. In accordance with

IMC 0609, Appendix A, Exhibit 1, the inspectors determined that the finding required a

detailed risk evaluation because the loss of feedwater caused operators to manually trip the

reactor and the loss of main feedwater constituted a loss of mitigation equipment used to

transition the plant to a stable shutdown condition.

The senior reactor analyst performed a detailed risk evaluation by treating the finding as an

initiating event and using the conditional core damage probability for a loss of main feedwater

as called for in Section 8.0, Initiating Event Analyses, of the Risk Assessment of Operational

Events Handbook. The analyst used Comanche Peak SPAR model version 8.58, run on

SAPHIRE, software version 8.2.1, for the evaluation.

The model was modified to reflect probabilistic recovery of a main feedwater pump. To

accomplish this, the analyst adjusted Basic Event MFW-XHE-XL-TRIP, Operator Fails to

13

Restart Main Feedwater Flow, used in Fault Tree MFW, Main Feedwater System, from

TRUE to a SPAR-H human reliability model derived value of 4.40E-2. In this human reliability

analysis, the analyst assigned high stress to both diagnosis and action and moderate

complexity to both diagnosis and action for the recovery. All other performance shaping

factors were set to nominal. Also, the analyst credited the use of the licensees diverse and

flexible coping strategies (FLEX) equipment. Performance of the initiating event analysis with

these modifications yielded an estimate of the increase in core damage frequency of 7.8E-7

per year from internal events. Loss of main feedwater events were the dominant sequences

and were mitigated by the auxiliary feedwater system.

The analyst noted that this detailed risk assessment evaluates an actual event in which no

external events occurred. Additionally, the period that the events impacted plant equipment

was small enough that the probability of an external initiator occurring during this time would

be negligible. Therefore, the analyst assumed that the risk from external events, given the

subject performance deficiency, was essentially zero. This resulted a total estimate in the

increase of core damage frequency of 7.8E-7 per year, making the finding of very low safety

significance (Green).

The increase in large early release frequency from this finding was determined to be of very

low safety significance using IMC 0609, Appendix H, Containment Integrity Significance

Determination Process, because loss of main feedwater sequences screen as having low

safety significance in pressurized water reactors with large dry containments.

Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the

possibility of mistakes, latent issues, and inherent risk, even while expecting successful

outcomes. Individuals implement appropriate error reduction tools. The licensee identified in

their root cause analysis that operations did not recognize nor understand the risks

associated with the evolution. The inspectors concluded that as a result, operators did not

plan for the possibility of mistakes or implement appropriate error reduction tools.

Enforcement:

Violation: Technical Specification Section 5.4.1.a requires, in part, that written procedures

shall be established, implemented, and maintained covering the applicable procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

NRC Regulatory Guide 1.33, Revision 2, Appendix A, Section 3, addresses Procedures for

Startup, Operation, and Shutdown or Safety-Related PWR Systems and Section 3.K,

addresses Feedwater System. The licensee established Procedure SOP-310B, Circulating

Water, Revision 18, to address operation of the circulating water system, including adjusting

flow to the auxiliary condensers which support operation of main feedwater system.

Procedure SOP-310B, Revision 18, step 5.3.7, requires operators to slowly adjust the

auxiliary condenser differential pressure to between 1- and 10 feet H2O. Contrary to the

above, on January 1, 2020, the licensee failed to slowly adjust the auxiliary condenser

differential pressure and maintain it between 1- and 10 feet H2O when operators fully closed

the valves, causing a condition (dual feedwater pump trips on low vacuum) that required a

reactor trip.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

14

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 31, 2020, the inspectors presented the radiation safety exit meeting

inspection results to Mr. T. McCool, Site Vice President, and other members of the

licensee staff.

  • On April 2, 2020, the inspectors presented the integrated inspection results to

Mr. T. McCool and other members of the licensee staff.

15

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.04 Procedures SOP-103B Chemical and Volume Control System 13

71111.05 Fire Plans FPI-105B U-2, train B Diesel generator and Equipment Elevation, 810' 2

Miscellaneous Fire Hazard Analysis Report Sections 5.9.7 and 5.6 32

Drill 20-15-01 Fire Drill Scenario for EDG 2-02 810' Fuel Oil Transfer Pit March 3,

2020

71111.12 Corrective Action TR-YYYY-NNNN 2016-008019

Documents

Miscellaneous Maintence Rule Summary Report for Unit 1 and Unit 2 02/18/2020

Auxillary Feedwater

Auxiliary Feedwater System Status 2nd Quarter

FY19

71111.13 Drawings E2-0026 6.9KV Three Line Diagram Normal Buses 13

Miscellaneous STI-600.01-1 Guarded Equipment Management Posting Log February 12,

2020

Procedures SOP-310B Circulating water System 18

Work Orders 5835726 Auxiliary Feedwater Pump Turbine 2-01Govenor Stroke 02/13/2020

71111.15 Corrective Action CR 2019-9530 12/13/2019

Documents TR 2020-1247 February 19,

2020

Drawings M2-2760 Diesel Engine Start/Stop Logic 15

Operability FSAR Table 8.3-1, Loading Requirements for Loss of 104

Evaluations Coolant Accident Coincident with Loss of Offsite Power

CR- 2020-001295

71111.19 Corrective Action CR-YYYY-NNNN 2019-009453

Documents IR-2020-001597 Multiple Relays Out of Tolerance on Unit 2 Train B

Sequencer

Procedures INC-7393A CH Cal Neutron Flux Power Range ION Current Gain and 6

Summing Level Amplifier

MSE-S2-0673B Unit 2 Train B Sequencer Under Voltage Relay Surveillance 5

Work Orders WO 5666818 Perform MSE-S2-0673B, TR B Sequencer UV Relay

WO 5840776 Troubleshoot and Repair Sequence Alarm Circuit as

documented in IR-2019-009453

16

Inspection Type Designation Description or Title Revision or

Procedure Date

WO 5848383 Replace Cell 22 on BT1D4 at Power

WO 5866715 Perform CCAL IAW INC-7393A

WO 5866789 Troubleshoot test signal going to zero described in CR 2020-

001447

71111.20 Miscellaneous BEACON 3D Reactivity Projection for Unit 2 Forced Outage 01/01/2020

Startup

71111.22 Procedures ETP-106 Monthly RCCA Repositioning 1

OPT-106A Control Rod Exercise 12

OPT-467A Train A Safeguards Slave realy K609 Actuation Test Revision 5

Work Orders WO 5656218 Solid State Protection System Slave Relay Test March 11,

2020

WO 5659452 Perform NUC 202 AT-Power MTC Measurement

WO 5829754 OPT-106A, Control Rod Exercise Test

WO 5846000 Monthly RCCA Reposit ETP-106

WO 5852752 IR-2020-000542 Troubleshoot 2-01 EDG Volt Reg TRBL

71114.06 Miscellaneous ERO team Exercise February 9,

2020

71124.05 Calibration 3443188 X-RE-5700 ICI-4998, CCAL FB VNT EXH 06/24/2009

Records 3648653 2-RE-6297, ICI-4961 Channel Calibration 09/30/2010

391556 1-RE-6295 ICI-4961, CCAL 03/16/2009

4373552 1-RE-6295 ICI-4961, CCAL 04/12/2016

4374577 2-RE-6297 ICI-4961, CCAL 05/10/2017

4426655 X-RE-5700 ICI-4998, CCAL FB VNT EXH 01/22/2015

4520934 1-RE-6256 ICI-4959 CCAL HRAM 06/09/2015

5371788 X-RE-5701 INC-4915X, CCAL AB VNT GPRM 07/18/2019

5522342 1-RE-6290A INC-7079, CCAL CNTMT HRRM 05/16/2019

5522458 1-RE-6290B INC-7079, CCAL CNTMT HRRM 05/02/2019

5526341 1-RUK-2326A/2328A INC-4916 CCAL 07/17/2019

ASCAN WBC System Calibration Data Package 11/20/2019

FSCAN WBC System Calibration Data Package 09/12/2019

HP-0058 Argos/Sirius Calibration Data Sheet 11/10/2019

HP-0063 NE Technology SAM Calibration Data Sheet 10/22/2018

HP-0075 GEM-5 Calibration Data Sheet 02/04/2019

17

Inspection Type Designation Description or Title Revision or

Procedure Date

HP-1206 Ludlum Model 177 Frisker Calibration Data Sheet 01/27/2020

HP-2166 AMS-4 Calibration Data Sheet 10/04/2019

HP-4124 Thermo RO-20AA Calibration Data Sheet 01/29/2020

HP-5002 Low Volume Air Sampler Calibration Data Sheet 10/12/2018

HP-711812 RDS-31 Calibration Data Sheet 10/07/2019

Corrective Action CR-YYYY-NNNN 2011-006222, 2016-001350, 2018-003694, 2018-006522,

Documents 2018-006631, 2018-007217, 2019-000184, 2019-001550,

2019-004125, 2019-004570, 2019-005318, 2019-007716,

2019-008045, 2019-008114, 2019-008129

TR-YYYY-NNNN 2018-006999, 2018-007197, 2018-007846, 2019-001511,

2019-003201, 2019-003405, 2019-003992, 2019-004146,

2019-004149, 2019-004221, 2019-005656, 2020-000063

Corrective Action CR-YYYY-NNNN 2020-000750, 2020-000783, 2020-000814

Documents

Resulting from

Inspection

Miscellaneous 1-RE-6290A Last Detector Primary Calibration 05/15/2019

19-001 through Calibration Well Source Charts 08/08/2019

19-007

2Qtr FY19 CPNPP System Status: Radiation Monitoring

T190990 RadCal 2026C and 1800cc, 180cc, and 6cc detectors 05/29/2019

Procedures CLI-782 APEX Gamma Spectroscopy Counting System 2

ICI-4959 Channel Calibration - High Range Area Radiation Monitors 4

ICI-4961 Channel Calibration - Digital High Range Area Monitors 4

ICI-4998 Channel Calibration - Gas Process Radiation Monitor 4

INC-7079 Channel Calibration - 6

Containment High Range Radiation Monitor Channels

1-RE-6290A/B and 2-RE-6290A/B

RPI-301 Portable Survey Instruments 13

RPI-800 Control of Radiation Protection Equipment 17

RPI-802 Performance of Source Checks 28

RPI-862 Calibration of the Argos/Sirius Personnel Contamination 14

Monitor and Gem-5 Gamma Exit Monitor

STA-619 Administrative Control of Digital Radiation Monitoring System 7

18

Inspection Type Designation Description or Title Revision or

Procedure Date

STA-650 General Health Physics Plan 8

STA-658 Radiation Protection Equipment Calibration Program 12

STA-677 Preventative Maintenance Program 13

STA-700 Surveillance Frequency Control Program 1

STI-677.01 PM Change Processing 2

Self-Assessments EVAL-2018-006 Work Management/Radiation Protection Audit 08/02/2018

EVAL-2019-007 Chemistry Control and Chemistry Measurement & Analysis 11/21/2019

71124.06 Calibration WO 5360001 X-RE-5567A, South Plant Vent Stack Radiation Monitor 07/30/2018

Records Calibration

WO 5421935 1-RE-4269, Unit 1 Station Service Water Train A to 10/24/2018

Discharge Canal Radiation Monitor Calibration

WO 5447947 X-FT-5288, LWPS LHMT X-01/X-02 Discharge to VD System 09/27/2018

Flow Transmitter Calibration

WO 5556086 2-RE-5100, Turbine Sump 2-04 Radiation Monitor Calibration 06/12/2019

WO 5576336 2-RE-4269, Unit 2 Station Service Water Train A to 09/25/2019

Discharge Canal Radiation Monitor Calibration

WO 5585319 X-RE-5253, Liquid Waste Processing Discharge Radiation 10/28/2019

Monitor Calibration

WO 5590739 X-RE-5570B, North Plant Vent Stack WRGM Radiation 10/01/2019

Monitor Calibration

WO 5631300 1-RE-4270, Unit 1 Station Service Water Train B to 01/14/2020

Discharge Canal Radiation Monitor

Corrective Action CR-YYYY-NNNN 2019-008687, 2019-008794

Documents TR-YYYY-NNNN 2017-000757, 2018-003362, 2019-001642, 2019-005866,

2019-006713, 2019-008605

Corrective Action TR-YYYY-NNNN 2020-000766, 2020-000815, 2020-000817

Documents TR-YYYY-NNNN 2020-000766, 2020-000815, 2020-000817

Resulting from

Inspection

Miscellaneous CPSES Offsite Dose Calculation Manual, Unit 1 and Unit 2 34

2017 Annual Radioactive Effluent Release Report 03/12/2018

2018 Annual Radioactive Effluent Release Report 04/20/2019

G2018-034 Gaseous Discharge Permit - Unit 1 Containment Vent 02/27/2018

G2018-208 Gaseous Discharge Permit - Plant Vent Stack B 12/09/2018

19

Inspection Type Designation Description or Title Revision or

Procedure Date

G2018-210 Gaseous Discharge Permit - Non-Routine Gas Normal 12/10/2018

G2019-046 Gaseous Discharge Permit - Plant Vent Stack B 03/12/2019

G2019-193 Gaseous Discharge Permit - Unit 2 Containment Vent 11/24/2019

G2019-216 Gaseous Discharge Permit - Plant Vent Stack A 12/31/2019

L2018-023 Liquid Discharge Permit - Plant Effluent Tank 1 07/05/2018

L2018-040 Liquid Discharge Permit - Plant Effluent Tank 2 10/24/2018

L2018-051 Liquid Discharge Permit - Low Volume Waste Pond (LVWP) 12/01/2018

L2019-016 Liquid Discharge Permit - Plant Effluent Tank 1 02/14/2019

L2019-055 Liquid Discharge Permit - Squaw Creek Reservoir 08/01/2019

L2019-072 Liquid Discharge Permit - Plant Effluent Tank 2 12/12/2019

Procedures CHM-170 Liquid and Gaseous Effluent Program 4

CHM-230 Guidelines for Sample Collection 3

CLI-744 Radioactive Effluent Pre-Release Permit Processing 2

CLI-745 Radioactive Effluent Post-Release Permit Processing and 3

Surveillance Tracking

STA-603 Control of Station Radioactive Effluents 21

STA-619 Administrative Control of the Digital Radiation Monitoring 7

System

STA-677 Preventive Maintenance Program 13

Self-Assessments EVAL-2019-007 Radioactive Waste, Effluents, Environmental, and Chemistry 11/21/2019

Programs

Work Orders WO 5319196 Primary Plant Ventilation Exhaust Filter Unit X-16 01/31/2018

WO 5377734 Primary Plant Ventilation Exhaust Filter Unit X-01 10/03/2018

WO 5431297 Primary Plant Ventilation Exhaust Filter Unit X-02 11/17/2018

WO 5558463 Primary Plant Ventilation Exhaust Filter Unit X-02 09/18/2019

71124.07 Corrective Action CR-YYYY-NNNN 2018-001574, 2018-001611, 2018-001760, 2018-004523,

Documents 2019-002077

TR-YYYY-NNNN 2018-001867, 2018-004228, 2019-001642, 2019-007287

2019-008284, 2019-009052, 2019-009165

Corrective Action CR-YYYY-NNNN 2020-000748

Documents

Resulting from

Inspection

20

Inspection Type Designation Description or Title Revision or

Procedure Date

Miscellaneous 2017 Annual Radiological Environmental Operating Report 04/30/2018

2018 Annual Radiological Environmental Operating Report 04/01/2019

NUPIC Audit GEL Laboratories (JQA-14-097) 05/29/2014

23724

NUPIC Audit GEL Laboratories (NOD-19-018) 08/29/2019

24747

(NOV2019-069)

ODCM Comanche Peak Steam Electric Station Offsite Dose 34

Calculation Manual Unit 1 and Unit 2

RPI-714-1- 2018 Land Use Census 07/31/2018

20180715

RPI-714-1- 2019 Land Use Census 07/25/2019

20190620

Procedures RPI-538 Process Environmental Badges 9

RPI-710 Radiological Environmental Monitoring, Sampling, and 22

Analysis Program

RPI-713 Collection, Preparation, and Shipment of Radiological 19

Environmental Samples

RPI-714 Land Use Census 6

RPI-888 Calibration of Portable Air Sample Equipment 5

STA-653 Contamination Control Program 20

STA-654 Groundwater Protection Program 9

Self-Assessments EVAL-2019-007 Radioactive Waste, Effluents, Environmental, amd Chemistry 11/21/2019

PRgrams

Work Orders WO- 4938991, 4965490, 5052258, 5080201, 5490927,

5651858, 5654059, 5654081, 5654093, 5654106,

5654119, 5654136, 5659602, 5659645, 5667801,

5736155, 5736168, 5736197, 5736232, 5736248,

5736282, 5736299, 5741625, 5747140

21