ML20062G279: Difference between revisions
StriderTol (talk | contribs) (StriderTol Bot insert) |
StriderTol (talk | contribs) (StriderTol Bot change) |
||
Line 17: | Line 17: | ||
=Text= | =Text= | ||
{{#Wiki_filter:}} | {{#Wiki_filter:- | ||
1 | |||
,. , OLOCK: l l l l l l (PLE ASE PRINT OR TYPE ALL REQUtnED INFOnMATIONI g- . l . ., ua,.atcone@lIHI l l al@lo O i 0[0l0l0l0l'ul0l0i010l@l4l1l1l1111@l := | |||
l lg i , uC=wa~< w a " t ~-6 " | |||
* 6 | |||
* u"a . | |||
leT | |||
; a | |||
,gC'" i Li@l Ol5 10 10 l 013I 2 l 1 !@l 0 ] 61019 l 7 l 8 !@l 0 l 6 ! 31017 I 8 l@ | |||
: E. , | |||
w os oENT oAn a a a j .. | |||
EVENT DESCniPTioN ANO pnODARLE CONSECUE*:CES Oc3ET 2.u w nuCaT OarE .I1 | |||
}! | |||
;g lWith the reactor in cold shutdown onh Procedure H.'IP-1-3902, " Safety Relief o-30-78, I l | |||
'g ; Valve Functional Test," was attempted unsatisfactorily cn B21-F013C and B21-F013L to I i | |||
g , functional test the solenoids installed per CCR 78-9. The solenoids had not creviousivl ! | |||
i | |||
;g ,been in service, and since the SRV's are not required to be acerable while the reactor i I i | |||
i 1 | |||
,T61 l s in cold shutdown, the SRV solenoids were not required to be ooerable and there was I , | |||
t | |||
.g ;no significance in.the failure of the SRV solenoid valves at the time of testino. I T51 IThis is a non-repetitive occurrence. l | |||
. . a t DE CO stoC E CO*.tPONENT CODE SUSC dE g g ~9 l Sl B j@ l E l@ l A l@ lV IA IL lV l 0! Pl@ l Xl@ @0 @ | |||
to 13 12 13 SL E 18 19 . | |||
' SEOUENTIAL OCCURRENCE REPO97 REVISION LE R 'RO EVENT YE AR REPORT NO. CODE TYPE NO. I J auC=T BER 17 I 81 l-l 10 14 13 I l-l lo I a l ILl l-l l 1l | |||
_ 21 22 2J ;4 26 27 28 23 30 31 22 CN A O O PLA T t T HOUR $ 58 IT F t d. SLP E htA N FACT RER j33E ig]34Z]@ l Zl@ l56Zl@ 10 i O! O! 01 It! l@ lY l@ [fLj@ lT 10 ! 21 Ol@ | |||
33 3/ 4J 43 42 43 44 47 CAuSE DESCRIPTION AND CORRECTIVE A0TICNS h i t, ; pf the eleven Target Rcck D. C. actuated solenoid valves tested. only two failed. One 1 : | |||
g ; failed from its plunger being bent out of adjustment and the other failed because its I plunger was not properly secured to the stem of the actuatina scrinas. Althouch nine i | |||
.of the solenoid valves passed the functional test and were found coroletely operable. | |||
I f; | |||
7 ;seven were found not to have the required locktite on the threads of the (cont. P. 2) r ' | |||
g vi 80 - | |||
IsI l El @$ l0 l 0 l 0 lgl | |||
% PC% E R OTHER $7ATUS N/A l 15 0 V l C Igl Functional Test O!$COVERY DESCRIPTION h l A TlVITY CO TENT RELE ASED 05 RELE ASE A41 CUNT OF ACTIVITY LOCATION OF RELEASE lca ]g W @ l Z [gl N/A l l tuA l ! | |||
:9 1 44 45 80 PERSONNEL E APOSvnES Nt* *M R Tvet CESCRIPTION - r | |||
'g l0l010l@lZl@l ft/A l | |||
: nnsO ma'iNJEs ! | |||
N n | |||
, p l0 luwtR0 l 0lgl EsCniPriON@ ft/A l s 9 11 12 20 Lot 0 C8 On oA*tAGF 70 F ACILtTY . ' | |||
TY8E C E SCIHP TION E l Zl@l tt/A l . | |||
t* | |||
Puott$rY ,,J MMWOMT Nac usE cNoy | |||
? | |||
TR d.,] FH@ | |||
l | |||
,o UE*CDIPTION fl/A I u mt I I l f I I I I I I I I I .', | |||
.o ; | |||
N AP.tE OF PREPARLil Tom Greene, Suot. of Plt. Eng. Serv. (912) 367-7731 Ext.121 2 PHCNE: 3 | |||
.cgia Power Company | |||
. ant E. I. Hatch Bax. ley, Georgia 31513 l | |||
Reportable Occurrence Report No. 50-321/1978-43 Cause Description and Corrective Actions (continued) | |||
I solenoid plungers. | |||
The failure of the two solenoids and lack of locktite | |||
: on seven solenoids can be contributed to poor QC control on the part of the solenoid manufacturer. All eleven SRV solenoid valves were removed, disassembled, i | |||
cleaned, and readjusted or replaced as deemed necessary by the Tcrget Rock a | |||
factory representative. The SRV solenoid valves were bench-tested, remounted, t | |||
and retested satisfactorily with no further action required. | |||
i 2 | |||
t f 'h f k , | |||
7" . | |||
. t C - | |||
5 i | |||
i I h | |||
e | |||
--}} |
Revision as of 23:49, 31 March 2020
ML20062G279 | |
Person / Time | |
---|---|
Site: | Hatch |
Issue date: | 06/30/1978 |
From: | Thomas Greene GEORGIA POWER CO. |
To: | |
Shared Package | |
ML20062G277 | List: |
References | |
LER-78-043-03L, LER-78-43-3L, NUDOCS 7812270285 | |
Download: ML20062G279 (2) | |
Text
-
1
,. , OLOCK: l l l l l l (PLE ASE PRINT OR TYPE ALL REQUtnED INFOnMATIONI g- . l . ., ua,.atcone@lIHI l l al@lo O i 0[0l0l0l0l'ul0l0i010l@l4l1l1l1111@l :=
l lg i , uC=wa~< w a " t ~-6 "
- 6
- u"a .
leT
- a
,gC'" i Li@l Ol5 10 10 l 013I 2 l 1 !@l 0 ] 61019 l 7 l 8 !@l 0 l 6 ! 31017 I 8 l@
- E. ,
w os oENT oAn a a a j ..
EVENT DESCniPTioN ANO pnODARLE CONSECUE*:CES Oc3ET 2.u w nuCaT OarE .I1
}!
- g lWith the reactor in cold shutdown onh Procedure H.'IP-1-3902, " Safety Relief o-30-78, I l
'g ; Valve Functional Test," was attempted unsatisfactorily cn B21-F013C and B21-F013L to I i
g , functional test the solenoids installed per CCR 78-9. The solenoids had not creviousivl !
i
- g ,been in service, and since the SRV's are not required to be acerable while the reactor i I i
i 1
,T61 l s in cold shutdown, the SRV solenoids were not required to be ooerable and there was I ,
t
.g ;no significance in.the failure of the SRV solenoid valves at the time of testino. I T51 IThis is a non-repetitive occurrence. l
. . a t DE CO stoC E CO*.tPONENT CODE SUSC dE g g ~9 l Sl B j@ l E l@ l A l@ lV IA IL lV l 0! Pl@ l Xl@ @0 @
to 13 12 13 SL E 18 19 .
' SEOUENTIAL OCCURRENCE REPO97 REVISION LE R 'RO EVENT YE AR REPORT NO. CODE TYPE NO. I J auC=T BER 17 I 81 l-l 10 14 13 I l-l lo I a l ILl l-l l 1l
_ 21 22 2J ;4 26 27 28 23 30 31 22 CN A O O PLA T t T HOUR $ 58 IT F t d. SLP E htA N FACT RER j33E ig]34Z]@ l Zl@ l56Zl@ 10 i O! O! 01 It! l@ lY l@ [fLj@ lT 10 ! 21 Ol@
33 3/ 4J 43 42 43 44 47 CAuSE DESCRIPTION AND CORRECTIVE A0TICNS h i t, ; pf the eleven Target Rcck D. C. actuated solenoid valves tested. only two failed. One 1 :
g ; failed from its plunger being bent out of adjustment and the other failed because its I plunger was not properly secured to the stem of the actuatina scrinas. Althouch nine i
.of the solenoid valves passed the functional test and were found coroletely operable.
I f;
7 ;seven were found not to have the required locktite on the threads of the (cont. P. 2) r '
g vi 80 -
IsI l El @$ l0 l 0 l 0 lgl
% PC% E R OTHER $7ATUS N/A l 15 0 V l C Igl Functional Test O!$COVERY DESCRIPTION h l A TlVITY CO TENT RELE ASED 05 RELE ASE A41 CUNT OF ACTIVITY LOCATION OF RELEASE lca ]g W @ l Z [gl N/A l l tuA l !
- 9 1 44 45 80 PERSONNEL E APOSvnES Nt* *M R Tvet CESCRIPTION - r
'g l0l010l@lZl@l ft/A l
- nnsO ma'iNJEs !
N n
, p l0 luwtR0 l 0lgl EsCniPriON@ ft/A l s 9 11 12 20 Lot 0 C8 On oA*tAGF 70 F ACILtTY . '
TY8E C E SCIHP TION E l Zl@l tt/A l .
t*
Puott$rY ,,J MMWOMT Nac usE cNoy
?
TR d.,] FH@
l
,o UE*CDIPTION fl/A I u mt I I l f I I I I I I I I I .',
.o ;
N AP.tE OF PREPARLil Tom Greene, Suot. of Plt. Eng. Serv. (912) 367-7731 Ext.121 2 PHCNE: 3
.cgia Power Company
. ant E. I. Hatch Bax. ley, Georgia 31513 l
Reportable Occurrence Report No. 50-321/1978-43 Cause Description and Corrective Actions (continued)
I solenoid plungers.
The failure of the two solenoids and lack of locktite
- on seven solenoids can be contributed to poor QC control on the part of the solenoid manufacturer. All eleven SRV solenoid valves were removed, disassembled, i
cleaned, and readjusted or replaced as deemed necessary by the Tcrget Rock a
factory representative. The SRV solenoid valves were bench-tested, remounted, t
and retested satisfactorily with no further action required.
i 2
t f 'h f k ,
7" .
. t C -
5 i
i I h
e
--