IR 05000269/2006006: Difference between revisions
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{{#Wiki_filter: | {{#Wiki_filter:ril 27, 2006 | ||
==SUBJECT:== | |||
OCONEE NUCLEAR STATION - NRC COMPONENT DESIGN BASES INSPECTION REPORT 05000269/2006006, 05000270/2006006, 05000287/2006006 | |||
==Dear Mr. Hamilton:== | ==Dear Mr. Hamilton:== | ||
On March 16, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an | On March 16, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Oconee Nuclear Station. The enclosed report documents the inspection findings which were discussed on March 16, 2006, with Mr. David Baxter, Station Manager and other members of your staff. | ||
The inspection examined activities conducted under your licenses as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your licenses. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. | |||
The report documents one NRC-identified finding of very low safety significance (Green). This finding was determined to involve a violation of NRC requirements. However, because of its very low safety significance and because it had been entered into your corrective action program, the NRC is treating this issue as a non-cited violation in accordance with Section VI.A.1 of the NRCs Enforcement Policy. If you deny this non-cited violation you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. | |||
20555-0001, with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Oconee Nuclear Station. | |||
DEC 2 In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | |||
Sincerely, Charles R. Ogle, | Sincerely, Charles R. Ogle, Chief Engineering Branch 1 Division of Reactor Safety Docket Nos.: 50-269, 50-270, 50-287 License Nos.: DPR-38, DPR-47, DPR-55 | ||
===Enclosure:=== | ===Enclosure:=== | ||
NRC Inspection Report 05000269/2006006,05000270/2006006,05000287/2006006 w/Attachment: Supplemental Information | NRC Inspection Report 05000269/2006006,05000270/2006006, 05000287/2006006 w/Attachment: Supplemental Information | ||
_________________________ | |||
OFFICE RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS SIGNATURE /RA/ /RA/ via phone /RA/via email /RA/ /RA/via email /RA/via email /RA/ | |||
NAME Mmaymi MScott MMichel BMiller LHajos HCampbell CJulian DATE 4/18 /2006 4/18 /2006 4/17 /2006 4/18/2006 4/18 /2006 4/18/2006 4/18 /2006 E-MAIL COPY? YES YES YES YES NO NO YES OFFICE RII/DRP SIGNATURE /RA/ DCPayne for NAME MErnestes DATE 4/21/06 E-MAIL COPY? YES YES NO YES NO YES NO YES NO | |||
REGION | DEC 3 | ||
REGION II== | |||
Docket Nos.: 50-269, 50-270, 50-287 License Nos.: DPR-38, DPR-47, DPR-55 Report No.: 50-269/2006006, 50-270/2006006, 50-287/2006006 Licensee: Duke Energy Corporation Facility: Oconee Nuclear Station, Units 1, 2, and 3 Location: 7800 Rochester Highway Seneca, SC 29672 Dates: February 13, 2006 - March 16, 2006 Inspectors: C. Julian, Team leader M. Maymi, Reactor Inspector M. Scott, Sr. Reactor Inspector H. Cambell, Contract Inspector L. Hajos, Contractor Inspector B. Miller, Reactor Inspector Trainee E. Michel, Reactor Inspector Trainee Approved by: Charles R. Ogle, Chief Engineering Branch 1 Division of Reactor Safety Enclosure | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
IR 05000269/2006006, 05000270/2006006, 05000287/2006006; 02/13/2006 - 03/16/2006; | IR 05000269/2006006, 05000270/2006006, 05000287/2006006; 02/13/2006 - 03/16/2006; | ||
White, Yellow, Red) using IMC 0609, | Oconee Nuclear Station, Units 1, 2, and 3; Component Design Bases Inspection. | ||
This inspection was conducted by a team of five NRC inspectors from the Region II office and two NRC contract inspectors. One Green finding, which was a non-cited violation, was identified during this inspection. The significance of most findings is indicated by their color (Green, | |||
White, Yellow, Red) using IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000. | |||
===NRC-Identified and Self-Revealing Findings=== | ===NRC-Identified and Self-Revealing Findings=== | ||
Line 43: | Line 60: | ||
===Cornerstone: Mitigating Systems=== | ===Cornerstone: Mitigating Systems=== | ||
: '''Green.''' | : '''Green.''' | ||
The team identified a Green, non-cited violation (NCV) of Technical Specification 5.4.1.b for a non-conservative operator action setpoint in the Emergency | The team identified a Green, non-cited violation (NCV) of Technical Specification 5.4.1.b for a non-conservative operator action setpoint in the Emergency Operating Procedures. Specifically, the 6 foot level setpoint for operator action to complete the BWST to Reactor Building Emergency Sump (RBES) swap over by closing the BWST suction valves did not include enough margin to preclude degradation or damage to the pumps due to vortex formation in the BWST in all cases. When the NRC notified the licensee of this condition, the licensee entered it into the corrective action program. | ||
=== | This finding is greater than minor because it is associated with the procedure quality attribute of the Mitigating Systems cornerstone and affected the cornerstone objective of ensuring reliable, available, and capable systems that respond to initiating events to prevent undesirable consequences. This finding is of very low safety significance because no actual loss of safety function occurred and operators have been trained to identify loss of pump suction. This finding has been entered into the licensees corrective action program as PIP O-06-01374. (Section 1R21.2.1.1 ) | ||
None | |||
===Licensee-Identified Violations=== | |||
None | |||
=REPORT DETAILS= | =REPORT DETAILS= | ||
Equipment reliability issues were also considered in | ==REACTOR SAFETY== | ||
Cornerstones: Mitigating Systems and Barrier Integrity {{a|1R21}} | |||
==1R21 Component Design Bases Inspection== | |||
{{IP sample|IP=IP 71111.21}} | |||
===.1 Inspection Sample Selection Process=== | |||
The team selected risk significant components and operator actions for review using information contained in the licensees Probabilistic Risk Assessment (PRA). In general, this included components and operator actions that had a risk achievement worth factor greater than two or Birnbaum value greater than 1E-6. The components selected were located within the high and low pressure safety injection, Borated Water Storage Tank, Keowee hydroelectric emergency power units, Standby Shutdown Facility, and vital electrical distribution systems. The sample selection included 25 components, seven operator actions, and six operating experience items. Additionally, the team reviewed two modifications by performing activities identified in IP 71111.17, Permanent Plant Modifications, Section 02.02.a. and IP 71111.02, Evaluations of Changes, Tests, or Experiments. | |||
The team performed a margin assessment and detailed review of the selected risk-significant components to verify that the design bases have been correctly implemented and maintained. This design margin assessment considered original design issues, margin reductions due to modification, or margin reductions identified as a result of material condition issues. Equipment reliability issues were also considered in the selection of components for detailed review. These included items such as failed performance test results, significant corrective action, repeated maintenance, Maintenance Rule (a)1 status, degraded conditions, NRC resident inspector input , | |||
system health reports, industry operating experience and licensee problem equipment lists. Consideration was also given to the uniqueness and complexity of the design, operating experience, and the available defense in depth margins. An overall summary of the reviews performed and the specific inspection findings identified are included in the following sections of the report. A specific list of documents reviewed is included in the attachment to this report. | |||
===.2 Results of Detailed Reviews=== | |||
===.2.1 Detailed Component Reviews=== | |||
===.2.1.1 Borated Water Storage Tank (BWST) Level Transmitters=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed relevant portions of the Updated Final Safety Analysis Report(UFSAR), Technical Specifications (TS), uncertainty calculations, Problem Investigation | The inspectors reviewed relevant portions of the Updated Final Safety Analysis Report (UFSAR), Technical Specifications (TS), uncertainty calculations, Problem Investigation Process reports (PIPs), work orders and completed surveillances related to the BWST level transmitters. Although specific scaling calculations were not available, the combination of calibration procedures and physical layout diagrams allowed for verification of transmitter elevations and resultant scaling. Further, the external layout and configuration of the transmitters was examined to the extent possible. A significant portion of the review was devoted to calculation OSC-2820, Emergency Procedure Guidelines Setpoint, Rev. 31, where several operator actions regarding BWST level were evaluated. | ||
====b. Findings==== | ====b. Findings==== | ||
=====Introduction:===== | =====Introduction:===== | ||
The team identified a Green, non-cited violation (NCV) of TS 5.4.1.b for | The team identified a Green, non-cited violation (NCV) of TS 5.4.1.b for a non-conservative operator action setpoint in the Emergency Operating Procedures. | ||
Specifically, the 6 foot level setpoint for operator action to complete the BWST to Reactor Building Emergency Sump (RBES) swap over by closing the BWST suction valves did not include enough margin to preclude degradation or damage to the pumps due to vortex formation in the BWST in all cases. | |||
=====Description:===== | |||
In response to a Loss Of Coolant Accident (LOCA), the High Pressure Injection (HPI), Low Pressure Injection (LPI) and Reactor Building Spray (RBS) systems pump borated water from the BWST until the tank is nearly empty. Suction for the ECCS systems must then be transferred from the BWST to the Reactor Building Emergency Sump (RBES). The Oconee Emergency Operating Procedures (EOPs)direct the operators to monitor the decreasing BWST level, at 9 feet to open the suction valves to the RBES, and at 6 feet to close the suction valves from the BWST. Appendix E of calculation OSC-2820 used a methodology developed by Harleman, and contained in a reference included in the List of Documents Reviewed attached to this report, to calculate the BWST level margin that should be allowed to prevent vortex formation and potential air ingestion into the safety related pumps. The calculation concluded that a water level depth of 14.2 inches above the top of the BWST suction line was sufficient to adequately protect the pumps from subsequent potential air ingestion and potential degradation. When operator action times, valve stroke times and BWST level measurement uncertainties were included, an action setpoint of 6 feet BWST level was determined to be acceptable. At this level the operators were directed by the EOPs to begin closing the BWST suction valves LP-21 and LP-22. | |||
The inspectors questioned if the vortex margin calculation was sufficiently conservative. | |||
The inspectors recognized that there are several analytical approaches for determining adequate suction water levels to avoid potential vortex-induced pump damage. When the conservative Hydraulics Institute method, contained in a reference included in the List of Documents Reviewed attached to this report, was applied, a depth margin of over 10 feet is recommended to preclude vortex creation for the specific tank suction geometry and high flow conditions at Oconee. | |||
The licensee acknowledged that use of the Harleman method was not sufficiently conservative for pump protection and documented this deficiency in their corrective action program by initiating PIP 06-01374. | |||
Using the Reddy-Pickford methodology, contained in a reference included in the List of Documents Reviewed attached to this report, the licensee concluded that vortex prevention will require approximately 5.1 feet level remaining in the BWST. The PIP addressed current operability of the BWST by stating that BWST isolation will be initiated at 6 feet and simulator validation has shown that the level will not decrease below 3.32 feet worst case. The licensee consulted with the pump vendors and were told that the pumps can tolerate up to 5% gas by volume without distress and 5% to 10% gas by volume for up to an hour. A conservative calculation assuming total voiding of the BWST suction piping with additional pump suction from the sump flow path, predicted a 7.5% void fraction. A short term corrective action documented in the PIP is to raise the BWST normal level and the operator action setpoints to ensure that the RBES swap occurs above levels in which air entraining vortexing is expected to occur. | |||
A longer term action as documented in the PIP at the end of the inspection is to perform a plant modification to install a vortex suppressor in the BWSTs of all three units. | |||
=====Analysis:===== | |||
Failing to provide adequate procedure guidance to preclude damage or degradation to the RBS, LPI and HPI pumps on BWST to RBES swap over in the EOPs is a performance deficiency. This finding is greater than minor because it is related to the procedure quality attribute of the Mitigating Systems cornerstone and affects the objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. This finding is of very low safety significance because although the RBS, LPI and HPI pumps could be damaged or degraded during a LOCA, the actual safety system function is not lost due to the availability of third standby LPI and HPI pumps and the tolerance of LPI pumps to short term air entrainment. Additionally, the procedures caution the operators to monitor pump parameters for indication of suction loss and the operators receive training on this phenomenon. | |||
=====Enforcement:===== | |||
TS 5.4.1.b requires that written procedures shall be established covering Emergency Operating Procedures. Procedures EP/1, 2, 3/A/1800/001 Emergency Operating Procedure, were written, in part, to fulfill this requirement. Contrary to TS 5.4.1.b, appropriate instructions were not provided in procedures EP/1, 2, 3/A/1800/001 Emergency Operating Procedure, for operator actions setpoint for BWST to RBES swap over at a level in the BWST that would preclude pump damage or degradation due to vortex formation in the BWST in all cases. Because the licensee took actions to enter this item into their corrective action program (PIP O-06-01374), this violation is identified as a non-cited violation (NCV) consistent with Section VI.A of the NRC Enforcement Policy, and is identified as NCV 05000269, 270, 287/2006006-01, Non-Conservative EOP Procedure Setpoint for Operator Action to Accomplish BWST to RBES Swap Over on Low BWST Level. | |||
===.2.1.2 Keowee Hydroelectric Generator Wheel Pit (Turbine) Vacuum Breaker/Air Admission=== | |||
Valve | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the operation, testing, and maintenance of vacuum | The inspectors reviewed the operation, testing, and maintenance of vacuum breaker valves MT-25 installed on the Keowee Hydro Units. This included a review of calculations, maintenance and corrective action documents, and discussions with cognizant licensee personnel. This review was performed to verify that the valves continue to operate in accordance with their design basis. | ||
====b. Findings==== | ====b. Findings==== | ||
The licensee could not provide the inspectors an analysis of the potential | The licensee could not provide the inspectors an analysis of the potential consequences to Keowee operability of the vacuum breaker valves failing open or failing to open. | ||
Available design documentation (calculation KC-0085 and technical manual KM-200-158) state that these valves are required to open following a load rejection from power to limit vacuum inside the turbine case. This action is to prevent the turbine from being exposed to a water column separation. Following a column separation, flooding or back slapping of the turbine could occur. This action could damage the turbine thrust bearing and cause the unit to fail. The inspectors determined that these vacuum breakers have not been included in a preventive maintenance program (PIP 06-01183)and have not been in scope for the maintenance rule and license renewal. The inspectors were concerned that normal operational testing may not be adequate to detect valve degradation. In addition, design aspects of the MT-25 vacuum breakers such as possible failure modes and significance were not available for review by the inspectors. This issue remains unresolved pending the inspectors review of the licensees determination of any impacts the potential vacuum breaker failures could have on the Keowee emergency power function. Accordingly, this item is identified as URI 05000269, 270, 287/2006006-002, Possible Vacuum Breaker Failure Impact to Keowee Emergency Power Function. | |||
===.2.1.3 LPI to HPI Pump Suction Header Manual Valves LP-54 and LP-56=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Manual valves LP-54 and LP-56 are normally open valves in the flow path used to | Manual valves LP-54 and LP-56 are normally open valves in the flow path used to align the HPI pumps in piggyback mode. The team reviewed preventive and corrective maintenance work order history, and corrective action documents to verify the reliability and availability of manual valves LP-54 and LP-56. In addition, the team reviewed Design Basis Documents (DBD), periodic test and operating procedures that manipulate these manual valves to verify the configuration of these valve was adequately controlled. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
===.2.1.4 Reactor Building Sump Suction Isolation Valves LP-19 and LP-20=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Motor operated valves (MOV) LP-19 and LP-20 are used to align LPI pump suction | Motor operated valves (MOV) LP-19 and LP-20 are used to align LPI pump suction to the containment recirculation sump. The team reviewed preventive and corrective maintenance work order history, maintenance rule component status, and corrective action documents to verify the reliability and availability of MOVs LP-19 and LP-20. | ||
In addition, the team reviewed DBDs, periodic stroke time test procedures, stroke time trends, actuator open/close thrust margin calculations, and test acceptance criteria to verify these were consistent with system design bases. The team also reviewed common cause failure issues to verify these were addressed and corrective actions were adequate. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.5 LPI Pump Discharge Check Valves LP-31, LP-33, and LP-35=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Check valves LP-31, 33, and 35 are used during LPI pump operation and | Check valves LP-31, 33, and 35 are used during LPI pump operation and prevent backflow through the pump when the pump is not running and the LPI headers are cross-connected. The team reviewed corrective maintenance work order history, and corrective action documents to verify the check valves were reliable and periodically inspected. In addition, the team reviewed DBDs, and completed test procedures to verify that the check valves stroked open allowing sufficient flow from the LPI pump, and prevented backflow. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.6 RCS/LPI Isolation LP-1 and LPI Hot Leg Suction Isolation LP-2=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed preventive and corrective maintenance work order history,maintenance rule component status and corrective action documents to verify the reliability and availability of MOVs LP-1 and LP-2. These MOVs are used to align | The team reviewed preventive and corrective maintenance work order history, maintenance rule component status and corrective action documents to verify the reliability and availability of MOVs LP-1 and LP-2. These MOVs are used to align the Reactor Coolant System (RCS) for decay heat removal. In addition, the team reviewed DBDs, periodic stroke time test procedures, stroke time trends, actuator open/close thrust margin calculations, and test acceptance criteria to verify these were consistent with system design bases. The team also reviewed an LP-1 pressure interlock, which prevents an inadvertent opening of the MOV during normal operation, signal testing and calibration procedures to verify that the interlock setpoint is being maintained and tested. | ||
====b. Findings==== | ====b. Findings==== | ||
Line 102: | Line 165: | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The LPI coolers are cooled by the Low Pressure Service Water (LPSW) system. | The LPI coolers are cooled by the Low Pressure Service Water (LPSW) system. The team reviewed DBDs, performance test calculations that verify heat removal capability, system health reports, and test acceptance criteria to verify they were consistent with design basis. In addition the team reviewed LPSW flow test and flow balance verification procedures, LPSW corrective action documents, completed flow test results, and adequate flow verification calculations to verify availability and reliability of LPSW to the LPI coolers, and to verify degraded conditions are being addressed. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.8 Standby Shutdown Facility (SSF) Auxiliary Service Water (ASW) Pump to Steam=== | |||
Generator (SG) Throttle Valve CCW-268 | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed preventive and corrective maintenance work order history,maintenance rule component status, and corrective action documents to verify the reliability and availability of MOV CCW-268. This MOV is a normally closed valve | The team reviewed preventive and corrective maintenance work order history, maintenance rule component status, and corrective action documents to verify the reliability and availability of MOV CCW-268. This MOV is a normally closed valve used to throttle flow to the SGs when the SSF ASW system is required. In addition, the team reviewed DBDs, valve data sheet calculations, actuator open/close thrust margin calculations, a valve replacement modification, stroke test procedure, test acceptance criteria, and MOV trend reports to verify acceptance criteria were consistent with system design bases, and to verify MOV design margins were being maintained. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.9 SSF Sump Pump Discharge Check Valves CCW-312 and CCW-313=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Check valves CCW-312 and 313 are credited for closing during a seismically | Check valves CCW-312 and 313 are credited for closing during a seismically induced Turbine Building Flood to prevent back flow from the yard drain system into the SSF pump room. The team reviewed preventive and corrective maintenance work order history, preventive maintenance procedures and completed work orders, and corrective action documents to verify the check valves were reliable and periodically inspected. | ||
In addition, the team reviewed DBDs, and a completed temporary test procedure that verified the check valves stroked open, and also prevented backleakage when operating the alternate sump pump. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.1 0 MOVs HP-24 & HP-25: BWST to HPI Pump Suction Valves=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), | The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), Technical Specifications (TS), DBDs, and associated drawings to determine the design basis performance requirements of these valves. Further, PIPs, work orders, system health reports and surveillances were reviewed to assess the operating history and general performance of these valves. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.1 1 MOVs LP-15 & LP-16: LPI Discharge to HPI Suction Valves, (PiggyBack Valves)=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the UFSAR, TS, DBDs, and associated drawings to | The inspectors reviewed the UFSAR, TS, DBDs, and associated drawings to determine the design basis performance requirements of these valves. Further, PIPs, work orders, system health reports and surveillances were reviewed to assess the operating history and general performance of these valves. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.1 2 LPI PUMPS=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the UFSAR, TS, DBDs, and associated drawings to | The inspectors reviewed the UFSAR, TS, DBDs, and associated drawings to determine the design basis performance requirements of these pumps. Also, TAC documentation (Test Acceptance Criteria), PIPs, work orders, system health reports and surveillances were reviewed to assess the operating history and general performance of these pumps. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | |||
===.2.1.1 3 LP-28, Manual BWST Isolation Valves=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
These valves are locked open on each unit to align the BWST to the suction of | These valves are locked open on each unit to align the BWST to the suction of the ECCS pumps. Further, they must be capable of being closed after a postulated tornado event, as well as to prevent reverse flow from the containment sump during a LOCA. | ||
The LPI DBD, TS 3.5.3, flow diagrams and surveillance procedures were reviewed | The LPI DBD, TS 3.5.3, flow diagrams and surveillance procedures were reviewed by the inspectors to establish design basis performance requirements. In addition, PIPs, work orders and system health reports were reviewed to assess the operating history and general performance of these valves. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.1 4 MOVs LP-103 & LP-104: Post-LOCA Boron Dilution Isolation Valves=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the DBD, and associated drawings to determine the | The inspectors reviewed the DBD, and associated drawings to determine the design basis performance requirements of these valves. Further, PIPs, work orders, system health reports and surveillances were reviewed to assess the operating history and general performance of these valves. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.1 5 High Pressure Injection (HPI) Pump and Motor Coolers=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed the UFSAR, DBDs, TS, Selected Licensee Commitments (SLC),calculations, and drawings to identify design basis information for the HPI pumps and the pump motor cooler cooling sources. The team also reviewed HPI pump flow tests, bearing oil analysis, vibration data trends, HPI system health reports, bearing and | The team reviewed the UFSAR, DBDs, TS, Selected Licensee Commitments (SLC),calculations, and drawings to identify design basis information for the HPI pumps and the pump motor cooler cooling sources. The team also reviewed HPI pump flow tests, bearing oil analysis, vibration data trends, HPI system health reports, bearing and stator temperature data trends, flow rate and differential pressure trends, and corrective action documents. These documents were reviewed to verify HPI pump design margins were being maintained and to confirm that the licensee was entering problems which could affect system performance into the corrective action program, and initiating appropriate corrective actions. | ||
The team also verified that the HPI pump motor coolers had adequate cooling by reviewing the availability and reliability of all cooling sources. The review included motor cooler flow rate trends, completed procedures which verified minimum required flow to the motor coolers from the LPSW and HPSW sources, and which also verified system check valves function to open and/or prevent backflow. In addition, LPSW to HPI cooler maintenance rule a(1) status and associated corrective actions were reviewed to verify these were adequate and commensurate with risk significance. | |||
To verify the availability of the Auxiliary Service Water (ASW) system cooling flow path to the HPI pump motor coolers, the team reviewed the completed temporary procedures performed to verify adequate flow and check valve operation. The team also reviewed ASW to LPSW flow path check valve preventive maintenance and piping inspections that verified sections of piping that were not maintained dry were not degraded by fouling or blockage. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
===.2.1.1 | ===.2.1.1 6 LPI to HPI Pump Suction Header Check Valves LP-55 and LP-57=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Check valves LP-55 and LP-57 are used when aligning HPI pumps in piggyback | Check valves LP-55 and LP-57 are used when aligning HPI pumps in piggyback mode to allow flow from LPI discharge header to the suction of the HPI pumps. The team reviewed preventive and corrective maintenance work order history, and corrective action documents to verify the check valves were reliable and periodically inspected. In addition, the team reviewed DBDs, and completed test procedures that verified the check valves stroked open allowing sufficient flow to the HPI pump suction, and prevented backleakage from the opposite train when closed. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.1 7 Pressurizer Power Operated Relief and High Point Primary Vent Valves=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed DBDs to establish the design basis equipment capability of | The team reviewed DBDs to establish the design basis equipment capability of the pressurizer power operated relief and primary high point vent valves. These valves are used in the emergency procedures for forced cooling. The team reviewed testing and operational history of the valves. Also, the team reviewed the corrective action documents for the valves for the past three years. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.1 8 Main Turbine Generator Condenser Isolation Valves and the Circulating Water Pump=== | |||
Isolation Valves | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed the design basis and equipment capability for the main | The team reviewed the design basis and equipment capability for the main generator condenser isolation and the circulating water pump discharge isolation valves. | ||
The team reviewed the turbine flood design basis documents and corrective action documents for the last 10 years and work orders for the last 3 years. Select problems with the valves were reviewed in depth including periodic testing results. The team discussed technical details with maintenance personnel, valve engineers, operators, and system engineers. | The team reviewed the turbine flood design basis documents and corrective action documents for the last 10 years and work orders for the last 3 years. Select problems with the valves were reviewed in depth including periodic testing results. The team discussed technical details with maintenance personnel, valve engineers, operators, and system engineers. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.1 9 Keowee Hydroelectric Generator Wheel Pit (Turbine) Sump Pumps=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed the design basis and equipment capability for the two turbine | The team reviewed the design basis and equipment capability for the two turbine sump pumps located in the wheel pit. The sump pumps empty the wheel pit and keep turbine shaft packing water out of the shafts lower guide bearing. The team verified the safety-related power sources, reviewed the adequacy of equipment performance testing and maintenance work orders, and assessed potential common cause failure mechanisms. | ||
System related corrective action documents were reviewed to assess the recent performance history of the equipment. | System related corrective action documents were reviewed to assess the recent performance history of the equipment. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.2 0 BWST: Structural Considerations of the Tank=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the UFSAR, structural calculations and relevant PRA data | The inspectors reviewed the UFSAR, structural calculations and relevant PRA data to determine the tank design basis. The inspectors also reviewed past Civil/Coating Inspection Reports of the tanks for all three units, PIPs, and work orders, to verify that the tanks continue to meet their design basis. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
===.2.1.2 1 Transformers CT-3 and=== | ===.2.1.2 1 Transformers CT-3 and CT-4=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed work orders, procedures, PIPs, and test records for | The team reviewed work orders, procedures, PIPs, and test records for transformers CT-3 and CT-4. The cognizant system engineer was interviewed and a work order addressing replacement of wiring in CT-4 control cabinet was reviewed (98573929-01). | ||
Also, affected design calculations were reviewed and the team performed a partial system walk-down of Unit 1, 2 and 3 Main Step Up and Start Up transformers. | Also, affected design calculations were reviewed and the team performed a partial system walk-down of Unit 1, 2 and 3 Main Step Up and Start Up transformers. This review was accomplished to verify that the components continue to perform to their documented design basis. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.2 2 HPI Pump C, Switchgear TD, Circuit Breakers N1, N2, E1, E2, S1 and S2=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed calculations, drawings, maintenance procedures, and vendor | The team reviewed calculations, drawings, maintenance procedures, and vendor data on the equipment that supplies power from offsite to engineered safety feature buses. | ||
The team reviewed the protective relaying calculations for the 4 kilovolt (kV) Class 1E service motors to determine if the protection and coordination were within the motors | The team reviewed the protective relaying calculations for the 4 kilovolt (kV) Class 1E service motors to determine if the protection and coordination were within the motors allowable thermal limits and operating conditions. The team performed a partial system walk-down of the Unit 1, 2 and 3 4 kilovolt (V) and 480volt (V) switchgears, located in the turbine building. The team reviewed the licensing commitments contained in the UFSAR to determine the requirements for the settings of the degraded and loss of voltage relays. | ||
The team reviewed the basis for the setpoint, whether the settings allow for proper operation of all loads, and whether all required loads were analyzed to operate successfully during the period of set time delay. The team reviewed the surveillance procedures for the loss of voltage relays to determine compliance with the pick up and drop out limits. The team reviewed two years of maintenance history records on the 4kV breakers. This review was accomplished to verify that the components continue to perform to their documented design basis. | The team reviewed the basis for the setpoint, whether the settings allow for proper operation of all loads, and whether all required loads were analyzed to operate successfully during the period of set time delay. The team reviewed the surveillance procedures for the loss of voltage relays to determine compliance with the pick up and drop out limits. The team reviewed two years of maintenance history records on the 4kV breakers. This review was accomplished to verify that the components continue to perform to their documented design basis. | ||
Line 220: | Line 312: | ||
No findings of significance were identified. | No findings of significance were identified. | ||
===.2.1.2 3 Emergency Power Switching Logic=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed the logic diagrams and test procedures for circuits that control | The team reviewed the logic diagrams and test procedures for circuits that control the Emergency Power Switching Logic. Logic diagrams were reviewed to determine whether the switching between various sources of power would occur as described in the UFSAR and DBD. The setpoint, time delays and the associated tolerances for relays were reviewed to determine whether the scheme would perform properly and would avoid spurious trips. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.2 4 Auto Transfer Features=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed logic diagrams, test procedures and calculations for circuits | The team reviewed logic diagrams, test procedures and calculations for circuits that control the automatic transfer of power sources for the engineered safety feature buses. | ||
Logic diagrams were reviewed to determine whether the transfer from station | Logic diagrams were reviewed to determine whether the transfer from station auxiliary power to offsite startup power would occur immediately for unit trip scenarios, and after main generator trip for accident scenarios. The setpoint, time delays and the associated tolerances for voltage relays were reviewed to determine whether the transfer scheme would allow sufficient voltage decay to preclude damage to motors, but still avoid spurious transfer to the onsite emergency source. The team also reviewed elementary and logic diagrams, and calculations for the fast transfer of non-engineered safety feature buses to the offsite source to determine whether it would result in spurious actuation of engineered safety feature bus under-voltage protection, protect the motors or disrupt load sequencing on the engineered safety feature buses. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2.1. | No findings of significance were identified. | ||
===.2.1.2 5 Engineered Safety Feature Bus Load Shed, Load Sequencing, and Breaker=== | |||
Coordination/Fault Protection | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed calculations, drawings, relay setting and test reports to | The team reviewed calculations, drawings, relay setting and test reports to determine whether engineered safety feature load shed schemes, load sequencing, and bus protection were adequate to assure availability of engineered safety feature loads within the times assumed in the safety analysis, and to prevent spurious tripping of buses. | ||
The team reviewed the setpoints and time delays for undervoltage relays used in the load shed scheme, as well as power supplies and setpoints for the discrete timing relays | The team reviewed the setpoints and time delays for undervoltage relays used in the load shed scheme, as well as power supplies and setpoints for the discrete timing relays used in motor starting circuits. The team also reviewed surveillance procedures and test reports for time delay relays to determine whether actual setpoints were consistent with the intended design. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified.. | No findings of significance were identified. | ||
===.3 Review of Low Margin Operator Actions=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team performed a margin assessment of a sample of risk significant, time critical operator actions. Where possible, margins were determined by the review of the assumed design basis, engineering modeling, and UFSAR stated response times and job performance times. For the selected operator actions, the team performed a walk through of associated Emergency Procedures, Abnormal Procedures, Annunciator Response Procedures, and other operations procedures with appropriate training personnel or plant operators to assess operator knowledge level, adequacy of procedures, and availability of special equipment when required. The following | The team performed a margin assessment of a sample of risk significant, time critical operator actions. Where possible, margins were determined by the review of the assumed design basis, engineering modeling, and UFSAR stated response times and job performance times. For the selected operator actions, the team performed a walk through of associated Emergency Procedures, Abnormal Procedures, Annunciator Response Procedures, and other operations procedures with appropriate training personnel or plant operators to assess operator knowledge level, adequacy of procedures, and availability of special equipment when required. The following operator actions were reviewed: | ||
High pressure recirculation - operator failure to initiate | |||
* Low pressure recirculation - operator failure to initiate | |||
* High pressure injection - failure to throttle HPI pumps | * High pressure injection - failure to throttle HPI pumps | ||
* Flooding - auxiliary and turbine | * Flooding - auxiliary and turbine building Borated water storage tank - failure to make up during piping break | ||
* Decay heat removal - operator response to loss of DHR Turbine bypass valves - failure to close on | * Decay heat removal - operator response to loss of DHR Turbine bypass valves - failure to close on demand The licensee had validated the time critical actions (TCA) in a performed surveillance run by operations support personnel. The team compared the times generated in the surveillance against the model times in a engineering developed model and subsequent calculation (OSC-2820). The inspectors walked down several EP action locations in the plant, observing for usability of instructions and equipment and observing that the time critical valves are appropriately tagged as time critical. Job performance measures developed by training for the non-licensed operators were observed in the plant during walk downs. | ||
The inspectors observed unpracticed and cold-to-the-scenario operator training personnel performance on the above asterisked actions. The observation occurred on the Oconee control room simulator. The training personnel were checking the scenarios to be used during operator annual requalification testing for problems. The TCAs imbedded in the scenarios were timed for comparison to those times found in the validation surveillance. | |||
Activity points in the emergency procedures and abnormal procedures were compared with the basis documents. The loss of DHR was discussed with operations support personnel procedure writers. The discussion covered the differences between the units, sequence of actions, and timeliness of the operator actions and their options. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified.. | No findings of significance were identified. | ||
===.4 Review of Industry Operating Experience=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed selected operating experience issues that had occurred at | The team reviewed selected operating experience issues that had occurred at several other nuclear facilities for applicability to this facility. The issues that received review by the team were: | ||
NRC Generic Letter 98-02, Loss of Reactor Coolant Inventory and Associated Potential for Loss of Emergency Mitigation Functions While In a Shutdown Condition. | |||
NRC Information Notice 95-03, Supplements 1 & 2, Loss of Reactor Coolant Inventory and Potential Loss of Emergency Mitigation Functions While In a Shutdown Condition. | |||
NRC Generic Letter 88-17, Loss of Decay Heat Removal.NRC Information Notice 90-55, Recent Operating Experience on Loss of | NRC Bulletin 88-10, Nonconforming Molded-Case Circuit Breakers. | ||
NRC Bulletin 88-04, Potential Safety Related Pump Loss, Minimum Flow Concerns. | |||
NRC Generic Letter 88-17, Loss of Decay Heat Removal. | |||
NRC Information Notice 90-55, Recent Operating Experience on Loss of Reactor Coolant Inventory While in Shutdown Condition. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified.. | No findings of significance were identified. | ||
===.5 Review of Permanent Plant Modifications=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed two modifications related to the selected risk significant | The team reviewed two modifications related to the selected risk significant components in detail to verify that the design bases, licensing bases, and performance capability of the components have not been degraded through modifications. The team reviewed the modification package, implementation procedure, 50.59 evaluation, calculations, post-modification testing results, corrective action documents, and performed an independent walkdown of the observable portions of the modification. The team reviewed the modifications in accordance with IP 71111.17, Permanent Plant Modifications, Section 02.02.a and IP 71111.02, Evaluations of Changes, Tests, or Experiments. | ||
The following modifications were reviewed: | |||
Modification NSM ON-33106, Emergency Sump Return Line. | |||
Modification NSM ON-23093, LPI Passive Cross-Connect Modification. | Modification NSM ON-23093, LPI Passive Cross-Connect Modification. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
==OTHER ACTIVITIES== | |||
4AO6 Meetings, Including Exit | |||
===Exit Meeting Summary=== | |||
On March 16, 2006, the team presented the inspection results to Mr. D. Baxter, Station Manager, and other members of the licensee staff. Licensee representatives acknowledged their understanding of the inspection results. No proprietary information was reviewed during this inspection or included in the report. | |||
=SUPPLEMENTAL INFORMATION= | =SUPPLEMENTAL INFORMATION= | ||
==KEY POINTS OF CONTACT== | ==KEY POINTS OF CONTACT== | ||
Licensee: | Licensee: | ||
: [[contact::K. Alter]], Engineering Supervisor | : [[contact::K. Alter]], Engineering Supervisor | ||
: [[contact::D. Baxter]], Station Manager | : [[contact::D. Baxter]], Station Manager | ||
: [[contact:: | C. Brown System Engineer AC systems | ||
: [[contact::N. Clarkson]], Sr. Engineer, Regulatory Compliance | |||
: [[contact::T. Grant]], Engineering Supervisor | : [[contact::T. Grant]], Engineering Supervisor | ||
: [[contact::L. Nicholson]], Manager, Safety Assurance | : [[contact::L. Nicholson]], Manager, Safety Assurance | ||
Line 290: | Line 417: | ||
: [[contact::E. Riggs]], Resident Inspector | : [[contact::E. Riggs]], Resident Inspector | ||
: [[contact::M. Shannon]], Senior Resident Inspector | : [[contact::M. Shannon]], Senior Resident Inspector | ||
==ITEMS OPENED, CLOSED, AND DISCUSSED== | ==ITEMS OPENED, CLOSED, AND DISCUSSED== | ||
Open/ | |||
: 05000269, 270, 287/2006006- | Open/Closed NCV | ||
swap over on Low BWST Level (Section | : 05000269, 270, 287/2006006-01 Non-Conservative EOP Procedure Setpoint for Operator Action to accomplish BWST to RBES swap over on Low BWST Level (Section 1R21.2.1.1) | ||
1R21.2.1.1) | Open URI | ||
Open | : 05000269, 270, 287/2006006-02 Possible Vacuum Breaker Failure Impact to Keowee Emergency Power Function (Section 1R21.2.1.2) | ||
URI | |||
: 05000269, 270, 287/2006006- | |||
1R21.2.1.2) | |||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
}} | }} |
Latest revision as of 14:36, 22 December 2019
ML061180004 | |
Person / Time | |
---|---|
Site: | Oconee |
Issue date: | 04/27/2006 |
From: | Ogle C NRC/RGN-II/DRS/EB1 |
To: | Brandi Hamilton Duke Energy Corp |
References | |
IR-06-006 | |
Download: ML061180004 (31) | |
Text
ril 27, 2006
SUBJECT:
OCONEE NUCLEAR STATION - NRC COMPONENT DESIGN BASES INSPECTION REPORT 05000269/2006006, 05000270/2006006, 05000287/2006006
Dear Mr. Hamilton:
On March 16, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Oconee Nuclear Station. The enclosed report documents the inspection findings which were discussed on March 16, 2006, with Mr. David Baxter, Station Manager and other members of your staff.
The inspection examined activities conducted under your licenses as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your licenses. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
The report documents one NRC-identified finding of very low safety significance (Green). This finding was determined to involve a violation of NRC requirements. However, because of its very low safety significance and because it had been entered into your corrective action program, the NRC is treating this issue as a non-cited violation in accordance with Section VI.A.1 of the NRCs Enforcement Policy. If you deny this non-cited violation you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C.
20555-0001, with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Oconee Nuclear Station.
DEC 2 In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely, Charles R. Ogle, Chief Engineering Branch 1 Division of Reactor Safety Docket Nos.: 50-269, 50-270, 50-287 License Nos.: DPR-38, DPR-47, DPR-55
Enclosure:
NRC Inspection Report 05000269/2006006,05000270/2006006, 05000287/2006006 w/Attachment: Supplemental Information
_________________________
OFFICE RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS SIGNATURE /RA/ /RA/ via phone /RA/via email /RA/ /RA/via email /RA/via email /RA/
NAME Mmaymi MScott MMichel BMiller LHajos HCampbell CJulian DATE 4/18 /2006 4/18 /2006 4/17 /2006 4/18/2006 4/18 /2006 4/18/2006 4/18 /2006 E-MAIL COPY? YES YES YES YES NO NO YES OFFICE RII/DRP SIGNATURE /RA/ DCPayne for NAME MErnestes DATE 4/21/06 E-MAIL COPY? YES YES NO YES NO YES NO YES NO
DEC 3
REGION II==
Docket Nos.: 50-269, 50-270, 50-287 License Nos.: DPR-38, DPR-47, DPR-55 Report No.: 50-269/2006006, 50-270/2006006, 50-287/2006006 Licensee: Duke Energy Corporation Facility: Oconee Nuclear Station, Units 1, 2, and 3 Location: 7800 Rochester Highway Seneca, SC 29672 Dates: February 13, 2006 - March 16, 2006 Inspectors: C. Julian, Team leader M. Maymi, Reactor Inspector M. Scott, Sr. Reactor Inspector H. Cambell, Contract Inspector L. Hajos, Contractor Inspector B. Miller, Reactor Inspector Trainee E. Michel, Reactor Inspector Trainee Approved by: Charles R. Ogle, Chief Engineering Branch 1 Division of Reactor Safety Enclosure
SUMMARY OF FINDINGS
IR 05000269/2006006, 05000270/2006006, 05000287/2006006; 02/13/2006 - 03/16/2006;
Oconee Nuclear Station, Units 1, 2, and 3; Component Design Bases Inspection.
This inspection was conducted by a team of five NRC inspectors from the Region II office and two NRC contract inspectors. One Green finding, which was a non-cited violation, was identified during this inspection. The significance of most findings is indicated by their color (Green,
White, Yellow, Red) using IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
NRC-Identified and Self-Revealing Findings
Cornerstone: Mitigating Systems
- Green.
The team identified a Green, non-cited violation (NCV) of Technical Specification 5.4.1.b for a non-conservative operator action setpoint in the Emergency Operating Procedures. Specifically, the 6 foot level setpoint for operator action to complete the BWST to Reactor Building Emergency Sump (RBES) swap over by closing the BWST suction valves did not include enough margin to preclude degradation or damage to the pumps due to vortex formation in the BWST in all cases. When the NRC notified the licensee of this condition, the licensee entered it into the corrective action program.
This finding is greater than minor because it is associated with the procedure quality attribute of the Mitigating Systems cornerstone and affected the cornerstone objective of ensuring reliable, available, and capable systems that respond to initiating events to prevent undesirable consequences. This finding is of very low safety significance because no actual loss of safety function occurred and operators have been trained to identify loss of pump suction. This finding has been entered into the licensees corrective action program as PIP O-06-01374. (Section 1R21.2.1.1 )
Licensee-Identified Violations
None
REPORT DETAILS
REACTOR SAFETY
Cornerstones: Mitigating Systems and Barrier Integrity
1R21 Component Design Bases Inspection
.1 Inspection Sample Selection Process
The team selected risk significant components and operator actions for review using information contained in the licensees Probabilistic Risk Assessment (PRA). In general, this included components and operator actions that had a risk achievement worth factor greater than two or Birnbaum value greater than 1E-6. The components selected were located within the high and low pressure safety injection, Borated Water Storage Tank, Keowee hydroelectric emergency power units, Standby Shutdown Facility, and vital electrical distribution systems. The sample selection included 25 components, seven operator actions, and six operating experience items. Additionally, the team reviewed two modifications by performing activities identified in IP 71111.17, Permanent Plant Modifications, Section 02.02.a. and IP 71111.02, Evaluations of Changes, Tests, or Experiments.
The team performed a margin assessment and detailed review of the selected risk-significant components to verify that the design bases have been correctly implemented and maintained. This design margin assessment considered original design issues, margin reductions due to modification, or margin reductions identified as a result of material condition issues. Equipment reliability issues were also considered in the selection of components for detailed review. These included items such as failed performance test results, significant corrective action, repeated maintenance, Maintenance Rule (a)1 status, degraded conditions, NRC resident inspector input ,
system health reports, industry operating experience and licensee problem equipment lists. Consideration was also given to the uniqueness and complexity of the design, operating experience, and the available defense in depth margins. An overall summary of the reviews performed and the specific inspection findings identified are included in the following sections of the report. A specific list of documents reviewed is included in the attachment to this report.
.2 Results of Detailed Reviews
.2.1 Detailed Component Reviews
.2.1.1 Borated Water Storage Tank (BWST) Level Transmitters
a. Inspection Scope
The inspectors reviewed relevant portions of the Updated Final Safety Analysis Report (UFSAR), Technical Specifications (TS), uncertainty calculations, Problem Investigation Process reports (PIPs), work orders and completed surveillances related to the BWST level transmitters. Although specific scaling calculations were not available, the combination of calibration procedures and physical layout diagrams allowed for verification of transmitter elevations and resultant scaling. Further, the external layout and configuration of the transmitters was examined to the extent possible. A significant portion of the review was devoted to calculation OSC-2820, Emergency Procedure Guidelines Setpoint, Rev. 31, where several operator actions regarding BWST level were evaluated.
b. Findings
Introduction:
The team identified a Green, non-cited violation (NCV) of TS 5.4.1.b for a non-conservative operator action setpoint in the Emergency Operating Procedures.
Specifically, the 6 foot level setpoint for operator action to complete the BWST to Reactor Building Emergency Sump (RBES) swap over by closing the BWST suction valves did not include enough margin to preclude degradation or damage to the pumps due to vortex formation in the BWST in all cases.
Description:
In response to a Loss Of Coolant Accident (LOCA), the High Pressure Injection (HPI), Low Pressure Injection (LPI) and Reactor Building Spray (RBS) systems pump borated water from the BWST until the tank is nearly empty. Suction for the ECCS systems must then be transferred from the BWST to the Reactor Building Emergency Sump (RBES). The Oconee Emergency Operating Procedures (EOPs)direct the operators to monitor the decreasing BWST level, at 9 feet to open the suction valves to the RBES, and at 6 feet to close the suction valves from the BWST. Appendix E of calculation OSC-2820 used a methodology developed by Harleman, and contained in a reference included in the List of Documents Reviewed attached to this report, to calculate the BWST level margin that should be allowed to prevent vortex formation and potential air ingestion into the safety related pumps. The calculation concluded that a water level depth of 14.2 inches above the top of the BWST suction line was sufficient to adequately protect the pumps from subsequent potential air ingestion and potential degradation. When operator action times, valve stroke times and BWST level measurement uncertainties were included, an action setpoint of 6 feet BWST level was determined to be acceptable. At this level the operators were directed by the EOPs to begin closing the BWST suction valves LP-21 and LP-22.
The inspectors questioned if the vortex margin calculation was sufficiently conservative.
The inspectors recognized that there are several analytical approaches for determining adequate suction water levels to avoid potential vortex-induced pump damage. When the conservative Hydraulics Institute method, contained in a reference included in the List of Documents Reviewed attached to this report, was applied, a depth margin of over 10 feet is recommended to preclude vortex creation for the specific tank suction geometry and high flow conditions at Oconee.
The licensee acknowledged that use of the Harleman method was not sufficiently conservative for pump protection and documented this deficiency in their corrective action program by initiating PIP 06-01374.
Using the Reddy-Pickford methodology, contained in a reference included in the List of Documents Reviewed attached to this report, the licensee concluded that vortex prevention will require approximately 5.1 feet level remaining in the BWST. The PIP addressed current operability of the BWST by stating that BWST isolation will be initiated at 6 feet and simulator validation has shown that the level will not decrease below 3.32 feet worst case. The licensee consulted with the pump vendors and were told that the pumps can tolerate up to 5% gas by volume without distress and 5% to 10% gas by volume for up to an hour. A conservative calculation assuming total voiding of the BWST suction piping with additional pump suction from the sump flow path, predicted a 7.5% void fraction. A short term corrective action documented in the PIP is to raise the BWST normal level and the operator action setpoints to ensure that the RBES swap occurs above levels in which air entraining vortexing is expected to occur.
A longer term action as documented in the PIP at the end of the inspection is to perform a plant modification to install a vortex suppressor in the BWSTs of all three units.
Analysis:
Failing to provide adequate procedure guidance to preclude damage or degradation to the RBS, LPI and HPI pumps on BWST to RBES swap over in the EOPs is a performance deficiency. This finding is greater than minor because it is related to the procedure quality attribute of the Mitigating Systems cornerstone and affects the objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. This finding is of very low safety significance because although the RBS, LPI and HPI pumps could be damaged or degraded during a LOCA, the actual safety system function is not lost due to the availability of third standby LPI and HPI pumps and the tolerance of LPI pumps to short term air entrainment. Additionally, the procedures caution the operators to monitor pump parameters for indication of suction loss and the operators receive training on this phenomenon.
Enforcement:
TS 5.4.1.b requires that written procedures shall be established covering Emergency Operating Procedures. Procedures EP/1, 2, 3/A/1800/001 Emergency Operating Procedure, were written, in part, to fulfill this requirement. Contrary to TS 5.4.1.b, appropriate instructions were not provided in procedures EP/1, 2, 3/A/1800/001 Emergency Operating Procedure, for operator actions setpoint for BWST to RBES swap over at a level in the BWST that would preclude pump damage or degradation due to vortex formation in the BWST in all cases. Because the licensee took actions to enter this item into their corrective action program (PIP O-06-01374), this violation is identified as a non-cited violation (NCV) consistent with Section VI.A of the NRC Enforcement Policy, and is identified as NCV 05000269, 270, 287/2006006-01, Non-Conservative EOP Procedure Setpoint for Operator Action to Accomplish BWST to RBES Swap Over on Low BWST Level.
.2.1.2 Keowee Hydroelectric Generator Wheel Pit (Turbine) Vacuum Breaker/Air Admission
Valve
a. Inspection Scope
The inspectors reviewed the operation, testing, and maintenance of vacuum breaker valves MT-25 installed on the Keowee Hydro Units. This included a review of calculations, maintenance and corrective action documents, and discussions with cognizant licensee personnel. This review was performed to verify that the valves continue to operate in accordance with their design basis.
b. Findings
The licensee could not provide the inspectors an analysis of the potential consequences to Keowee operability of the vacuum breaker valves failing open or failing to open.
Available design documentation (calculation KC-0085 and technical manual KM-200-158) state that these valves are required to open following a load rejection from power to limit vacuum inside the turbine case. This action is to prevent the turbine from being exposed to a water column separation. Following a column separation, flooding or back slapping of the turbine could occur. This action could damage the turbine thrust bearing and cause the unit to fail. The inspectors determined that these vacuum breakers have not been included in a preventive maintenance program (PIP 06-01183)and have not been in scope for the maintenance rule and license renewal. The inspectors were concerned that normal operational testing may not be adequate to detect valve degradation. In addition, design aspects of the MT-25 vacuum breakers such as possible failure modes and significance were not available for review by the inspectors. This issue remains unresolved pending the inspectors review of the licensees determination of any impacts the potential vacuum breaker failures could have on the Keowee emergency power function. Accordingly, this item is identified as URI 05000269, 270, 287/2006006-002, Possible Vacuum Breaker Failure Impact to Keowee Emergency Power Function.
.2.1.3 LPI to HPI Pump Suction Header Manual Valves LP-54 and LP-56
a. Inspection Scope
Manual valves LP-54 and LP-56 are normally open valves in the flow path used to align the HPI pumps in piggyback mode. The team reviewed preventive and corrective maintenance work order history, and corrective action documents to verify the reliability and availability of manual valves LP-54 and LP-56. In addition, the team reviewed Design Basis Documents (DBD), periodic test and operating procedures that manipulate these manual valves to verify the configuration of these valve was adequately controlled.
b. Findings
No findings of significance were identified.
.2.1.4 Reactor Building Sump Suction Isolation Valves LP-19 and LP-20
a. Inspection Scope
Motor operated valves (MOV) LP-19 and LP-20 are used to align LPI pump suction to the containment recirculation sump. The team reviewed preventive and corrective maintenance work order history, maintenance rule component status, and corrective action documents to verify the reliability and availability of MOVs LP-19 and LP-20.
In addition, the team reviewed DBDs, periodic stroke time test procedures, stroke time trends, actuator open/close thrust margin calculations, and test acceptance criteria to verify these were consistent with system design bases. The team also reviewed common cause failure issues to verify these were addressed and corrective actions were adequate.
b. Findings
No findings of significance were identified.
.2.1.5 LPI Pump Discharge Check Valves LP-31, LP-33, and LP-35
a. Inspection Scope
Check valves LP-31, 33, and 35 are used during LPI pump operation and prevent backflow through the pump when the pump is not running and the LPI headers are cross-connected. The team reviewed corrective maintenance work order history, and corrective action documents to verify the check valves were reliable and periodically inspected. In addition, the team reviewed DBDs, and completed test procedures to verify that the check valves stroked open allowing sufficient flow from the LPI pump, and prevented backflow.
b. Findings
No findings of significance were identified.
.2.1.6 RCS/LPI Isolation LP-1 and LPI Hot Leg Suction Isolation LP-2
a. Inspection Scope
The team reviewed preventive and corrective maintenance work order history, maintenance rule component status and corrective action documents to verify the reliability and availability of MOVs LP-1 and LP-2. These MOVs are used to align the Reactor Coolant System (RCS) for decay heat removal. In addition, the team reviewed DBDs, periodic stroke time test procedures, stroke time trends, actuator open/close thrust margin calculations, and test acceptance criteria to verify these were consistent with system design bases. The team also reviewed an LP-1 pressure interlock, which prevents an inadvertent opening of the MOV during normal operation, signal testing and calibration procedures to verify that the interlock setpoint is being maintained and tested.
b. Findings
No findings of significance were identified.
.2.1.7 LPI Coolers (Decay Heat Removal Coolers)
a. Inspection Scope
The LPI coolers are cooled by the Low Pressure Service Water (LPSW) system. The team reviewed DBDs, performance test calculations that verify heat removal capability, system health reports, and test acceptance criteria to verify they were consistent with design basis. In addition the team reviewed LPSW flow test and flow balance verification procedures, LPSW corrective action documents, completed flow test results, and adequate flow verification calculations to verify availability and reliability of LPSW to the LPI coolers, and to verify degraded conditions are being addressed.
b. Findings
No findings of significance were identified.
.2.1.8 Standby Shutdown Facility (SSF) Auxiliary Service Water (ASW) Pump to Steam
Generator (SG) Throttle Valve CCW-268
a. Inspection Scope
The team reviewed preventive and corrective maintenance work order history, maintenance rule component status, and corrective action documents to verify the reliability and availability of MOV CCW-268. This MOV is a normally closed valve used to throttle flow to the SGs when the SSF ASW system is required. In addition, the team reviewed DBDs, valve data sheet calculations, actuator open/close thrust margin calculations, a valve replacement modification, stroke test procedure, test acceptance criteria, and MOV trend reports to verify acceptance criteria were consistent with system design bases, and to verify MOV design margins were being maintained.
b. Findings
No findings of significance were identified.
.2.1.9 SSF Sump Pump Discharge Check Valves CCW-312 and CCW-313
a. Inspection Scope
Check valves CCW-312 and 313 are credited for closing during a seismically induced Turbine Building Flood to prevent back flow from the yard drain system into the SSF pump room. The team reviewed preventive and corrective maintenance work order history, preventive maintenance procedures and completed work orders, and corrective action documents to verify the check valves were reliable and periodically inspected.
In addition, the team reviewed DBDs, and a completed temporary test procedure that verified the check valves stroked open, and also prevented backleakage when operating the alternate sump pump.
b. Findings
No findings of significance were identified.
.2.1.1 0 MOVs HP-24 & HP-25: BWST to HPI Pump Suction Valves
a. Inspection Scope
The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), Technical Specifications (TS), DBDs, and associated drawings to determine the design basis performance requirements of these valves. Further, PIPs, work orders, system health reports and surveillances were reviewed to assess the operating history and general performance of these valves.
b. Findings
No findings of significance were identified.
.2.1.1 1 MOVs LP-15 & LP-16: LPI Discharge to HPI Suction Valves, (PiggyBack Valves)
a. Inspection Scope
The inspectors reviewed the UFSAR, TS, DBDs, and associated drawings to determine the design basis performance requirements of these valves. Further, PIPs, work orders, system health reports and surveillances were reviewed to assess the operating history and general performance of these valves.
b. Findings
No findings of significance were identified.
.2.1.1 2 LPI PUMPS
a. Inspection Scope
The inspectors reviewed the UFSAR, TS, DBDs, and associated drawings to determine the design basis performance requirements of these pumps. Also, TAC documentation (Test Acceptance Criteria), PIPs, work orders, system health reports and surveillances were reviewed to assess the operating history and general performance of these pumps.
b. Findings
No findings of significance were identified.
.2.1.1 3 LP-28, Manual BWST Isolation Valves
a. Inspection Scope
These valves are locked open on each unit to align the BWST to the suction of the ECCS pumps. Further, they must be capable of being closed after a postulated tornado event, as well as to prevent reverse flow from the containment sump during a LOCA.
The LPI DBD, TS 3.5.3, flow diagrams and surveillance procedures were reviewed by the inspectors to establish design basis performance requirements. In addition, PIPs, work orders and system health reports were reviewed to assess the operating history and general performance of these valves.
b. Findings
No findings of significance were identified.
.2.1.1 4 MOVs LP-103 & LP-104: Post-LOCA Boron Dilution Isolation Valves
a. Inspection Scope
The inspectors reviewed the DBD, and associated drawings to determine the design basis performance requirements of these valves. Further, PIPs, work orders, system health reports and surveillances were reviewed to assess the operating history and general performance of these valves.
b. Findings
No findings of significance were identified.
.2.1.1 5 High Pressure Injection (HPI) Pump and Motor Coolers
a. Inspection Scope
The team reviewed the UFSAR, DBDs, TS, Selected Licensee Commitments (SLC),calculations, and drawings to identify design basis information for the HPI pumps and the pump motor cooler cooling sources. The team also reviewed HPI pump flow tests, bearing oil analysis, vibration data trends, HPI system health reports, bearing and stator temperature data trends, flow rate and differential pressure trends, and corrective action documents. These documents were reviewed to verify HPI pump design margins were being maintained and to confirm that the licensee was entering problems which could affect system performance into the corrective action program, and initiating appropriate corrective actions.
The team also verified that the HPI pump motor coolers had adequate cooling by reviewing the availability and reliability of all cooling sources. The review included motor cooler flow rate trends, completed procedures which verified minimum required flow to the motor coolers from the LPSW and HPSW sources, and which also verified system check valves function to open and/or prevent backflow. In addition, LPSW to HPI cooler maintenance rule a(1) status and associated corrective actions were reviewed to verify these were adequate and commensurate with risk significance.
To verify the availability of the Auxiliary Service Water (ASW) system cooling flow path to the HPI pump motor coolers, the team reviewed the completed temporary procedures performed to verify adequate flow and check valve operation. The team also reviewed ASW to LPSW flow path check valve preventive maintenance and piping inspections that verified sections of piping that were not maintained dry were not degraded by fouling or blockage.
b. Findings
No findings of significance were identified.
.2.1.1 6 LPI to HPI Pump Suction Header Check Valves LP-55 and LP-57
a. Inspection Scope
Check valves LP-55 and LP-57 are used when aligning HPI pumps in piggyback mode to allow flow from LPI discharge header to the suction of the HPI pumps. The team reviewed preventive and corrective maintenance work order history, and corrective action documents to verify the check valves were reliable and periodically inspected. In addition, the team reviewed DBDs, and completed test procedures that verified the check valves stroked open allowing sufficient flow to the HPI pump suction, and prevented backleakage from the opposite train when closed.
b. Findings
No findings of significance were identified.
.2.1.1 7 Pressurizer Power Operated Relief and High Point Primary Vent Valves
a. Inspection Scope
The team reviewed DBDs to establish the design basis equipment capability of the pressurizer power operated relief and primary high point vent valves. These valves are used in the emergency procedures for forced cooling. The team reviewed testing and operational history of the valves. Also, the team reviewed the corrective action documents for the valves for the past three years.
b. Findings
No findings of significance were identified.
.2.1.1 8 Main Turbine Generator Condenser Isolation Valves and the Circulating Water Pump
Isolation Valves
a. Inspection Scope
The team reviewed the design basis and equipment capability for the main generator condenser isolation and the circulating water pump discharge isolation valves.
The team reviewed the turbine flood design basis documents and corrective action documents for the last 10 years and work orders for the last 3 years. Select problems with the valves were reviewed in depth including periodic testing results. The team discussed technical details with maintenance personnel, valve engineers, operators, and system engineers.
b. Findings
No findings of significance were identified.
.2.1.1 9 Keowee Hydroelectric Generator Wheel Pit (Turbine) Sump Pumps
a. Inspection Scope
The team reviewed the design basis and equipment capability for the two turbine sump pumps located in the wheel pit. The sump pumps empty the wheel pit and keep turbine shaft packing water out of the shafts lower guide bearing. The team verified the safety-related power sources, reviewed the adequacy of equipment performance testing and maintenance work orders, and assessed potential common cause failure mechanisms.
System related corrective action documents were reviewed to assess the recent performance history of the equipment.
b. Findings
No findings of significance were identified.
.2.1.2 0 BWST: Structural Considerations of the Tank
a. Inspection Scope
The inspectors reviewed the UFSAR, structural calculations and relevant PRA data to determine the tank design basis. The inspectors also reviewed past Civil/Coating Inspection Reports of the tanks for all three units, PIPs, and work orders, to verify that the tanks continue to meet their design basis.
b. Findings
No findings of significance were identified.
.2.1.2 1 Transformers CT-3 and CT-4
a. Inspection Scope
The team reviewed work orders, procedures, PIPs, and test records for transformers CT-3 and CT-4. The cognizant system engineer was interviewed and a work order addressing replacement of wiring in CT-4 control cabinet was reviewed (98573929-01).
Also, affected design calculations were reviewed and the team performed a partial system walk-down of Unit 1, 2 and 3 Main Step Up and Start Up transformers. This review was accomplished to verify that the components continue to perform to their documented design basis.
b. Findings
No findings of significance were identified.
.2.1.2 2 HPI Pump C, Switchgear TD, Circuit Breakers N1, N2, E1, E2, S1 and S2
a. Inspection Scope
The team reviewed calculations, drawings, maintenance procedures, and vendor data on the equipment that supplies power from offsite to engineered safety feature buses.
The team reviewed the protective relaying calculations for the 4 kilovolt (kV) Class 1E service motors to determine if the protection and coordination were within the motors allowable thermal limits and operating conditions. The team performed a partial system walk-down of the Unit 1, 2 and 3 4 kilovolt (V) and 480volt (V) switchgears, located in the turbine building. The team reviewed the licensing commitments contained in the UFSAR to determine the requirements for the settings of the degraded and loss of voltage relays.
The team reviewed the basis for the setpoint, whether the settings allow for proper operation of all loads, and whether all required loads were analyzed to operate successfully during the period of set time delay. The team reviewed the surveillance procedures for the loss of voltage relays to determine compliance with the pick up and drop out limits. The team reviewed two years of maintenance history records on the 4kV breakers. This review was accomplished to verify that the components continue to perform to their documented design basis.
b. Findings
No findings of significance were identified.
.2.1.2 3 Emergency Power Switching Logic
a. Inspection Scope
The team reviewed the logic diagrams and test procedures for circuits that control the Emergency Power Switching Logic. Logic diagrams were reviewed to determine whether the switching between various sources of power would occur as described in the UFSAR and DBD. The setpoint, time delays and the associated tolerances for relays were reviewed to determine whether the scheme would perform properly and would avoid spurious trips.
b. Findings
No findings of significance were identified.
.2.1.2 4 Auto Transfer Features
a. Inspection Scope
The team reviewed logic diagrams, test procedures and calculations for circuits that control the automatic transfer of power sources for the engineered safety feature buses.
Logic diagrams were reviewed to determine whether the transfer from station auxiliary power to offsite startup power would occur immediately for unit trip scenarios, and after main generator trip for accident scenarios. The setpoint, time delays and the associated tolerances for voltage relays were reviewed to determine whether the transfer scheme would allow sufficient voltage decay to preclude damage to motors, but still avoid spurious transfer to the onsite emergency source. The team also reviewed elementary and logic diagrams, and calculations for the fast transfer of non-engineered safety feature buses to the offsite source to determine whether it would result in spurious actuation of engineered safety feature bus under-voltage protection, protect the motors or disrupt load sequencing on the engineered safety feature buses.
b. Findings
No findings of significance were identified.
.2.1.2 5 Engineered Safety Feature Bus Load Shed, Load Sequencing, and Breaker
Coordination/Fault Protection
a. Inspection Scope
The team reviewed calculations, drawings, relay setting and test reports to determine whether engineered safety feature load shed schemes, load sequencing, and bus protection were adequate to assure availability of engineered safety feature loads within the times assumed in the safety analysis, and to prevent spurious tripping of buses.
The team reviewed the setpoints and time delays for undervoltage relays used in the load shed scheme, as well as power supplies and setpoints for the discrete timing relays used in motor starting circuits. The team also reviewed surveillance procedures and test reports for time delay relays to determine whether actual setpoints were consistent with the intended design.
b. Findings
No findings of significance were identified.
.3 Review of Low Margin Operator Actions
a. Inspection Scope
The team performed a margin assessment of a sample of risk significant, time critical operator actions. Where possible, margins were determined by the review of the assumed design basis, engineering modeling, and UFSAR stated response times and job performance times. For the selected operator actions, the team performed a walk through of associated Emergency Procedures, Abnormal Procedures, Annunciator Response Procedures, and other operations procedures with appropriate training personnel or plant operators to assess operator knowledge level, adequacy of procedures, and availability of special equipment when required. The following operator actions were reviewed:
High pressure recirculation - operator failure to initiate
- Low pressure recirculation - operator failure to initiate
- High pressure injection - failure to throttle HPI pumps
- Flooding - auxiliary and turbine building Borated water storage tank - failure to make up during piping break
- Decay heat removal - operator response to loss of DHR Turbine bypass valves - failure to close on demand The licensee had validated the time critical actions (TCA) in a performed surveillance run by operations support personnel. The team compared the times generated in the surveillance against the model times in a engineering developed model and subsequent calculation (OSC-2820). The inspectors walked down several EP action locations in the plant, observing for usability of instructions and equipment and observing that the time critical valves are appropriately tagged as time critical. Job performance measures developed by training for the non-licensed operators were observed in the plant during walk downs.
The inspectors observed unpracticed and cold-to-the-scenario operator training personnel performance on the above asterisked actions. The observation occurred on the Oconee control room simulator. The training personnel were checking the scenarios to be used during operator annual requalification testing for problems. The TCAs imbedded in the scenarios were timed for comparison to those times found in the validation surveillance.
Activity points in the emergency procedures and abnormal procedures were compared with the basis documents. The loss of DHR was discussed with operations support personnel procedure writers. The discussion covered the differences between the units, sequence of actions, and timeliness of the operator actions and their options.
b. Findings
No findings of significance were identified.
.4 Review of Industry Operating Experience
a. Inspection Scope
The team reviewed selected operating experience issues that had occurred at several other nuclear facilities for applicability to this facility. The issues that received review by the team were:
NRC Generic Letter 98-02, Loss of Reactor Coolant Inventory and Associated Potential for Loss of Emergency Mitigation Functions While In a Shutdown Condition.
NRC Information Notice 95-03, Supplements 1 & 2, Loss of Reactor Coolant Inventory and Potential Loss of Emergency Mitigation Functions While In a Shutdown Condition.
NRC Bulletin 88-10, Nonconforming Molded-Case Circuit Breakers.
NRC Bulletin 88-04, Potential Safety Related Pump Loss, Minimum Flow Concerns.
NRC Generic Letter 88-17, Loss of Decay Heat Removal.
NRC Information Notice 90-55, Recent Operating Experience on Loss of Reactor Coolant Inventory While in Shutdown Condition.
b. Findings
No findings of significance were identified.
.5 Review of Permanent Plant Modifications
a. Inspection Scope
The team reviewed two modifications related to the selected risk significant components in detail to verify that the design bases, licensing bases, and performance capability of the components have not been degraded through modifications. The team reviewed the modification package, implementation procedure, 50.59 evaluation, calculations, post-modification testing results, corrective action documents, and performed an independent walkdown of the observable portions of the modification. The team reviewed the modifications in accordance with IP 71111.17, Permanent Plant Modifications, Section 02.02.a and IP 71111.02, Evaluations of Changes, Tests, or Experiments.
The following modifications were reviewed:
Modification NSM ON-33106, Emergency Sump Return Line.
Modification NSM ON-23093, LPI Passive Cross-Connect Modification.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4AO6 Meetings, Including Exit
Exit Meeting Summary
On March 16, 2006, the team presented the inspection results to Mr. D. Baxter, Station Manager, and other members of the licensee staff. Licensee representatives acknowledged their understanding of the inspection results. No proprietary information was reviewed during this inspection or included in the report.
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee:
- K. Alter, Engineering Supervisor
- D. Baxter, Station Manager
C. Brown System Engineer AC systems
- N. Clarkson, Sr. Engineer, Regulatory Compliance
- T. Grant, Engineering Supervisor
- L. Nicholson, Manager, Safety Assurance
- J. Rowell, Electrical Engineer
- J. Smith, Technical Specialist, Regulatory Compliance
- J. Stevens, System Engineer DC systems
- J. Weast, Engineer, Regulatory Compliance
NRC
- A. Hutto, Resident Inspector
- E. Riggs, Resident Inspector
- M. Shannon, Senior Resident Inspector
ITEMS OPENED, CLOSED, AND DISCUSSED
Open/Closed NCV
- 05000269, 270, 287/2006006-01 Non-Conservative EOP Procedure Setpoint for Operator Action to accomplish BWST to RBES swap over on Low BWST Level (Section 1R21.2.1.1)
Open URI
- 05000269, 270, 287/2006006-02 Possible Vacuum Breaker Failure Impact to Keowee Emergency Power Function (Section 1R21.2.1.2)