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{{Adams|number = ML103020254}}
{{Adams
| number = ML103130239
| issue date = 11/09/2010
| title = IR 05000440-10-004, on 07/01/2010 09/30/2010, Surveillance Testing, Problem Identification and Resolution
| author name = Cameron J
| author affiliation = NRC/RGN-III/DRP/B6
| addressee name = Bezilla M
| addressee affiliation = FirstEnergy Nuclear Operating Co
| docket = 05000440
| license number = NPF-058
| contact person =
| document report number = IR-10-004
| document type = Inspection Report, Letter
| page count = 5
}}


{{IR-Nav| site = 05000440 | year = 2010 | report number = 004 }}
{{IR-Nav| site = 05000440 | year = 2010 | report number = 004 }}


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:ber 9, 2010
[[Issue date::October 29, 2010]]


Mr. Mark Bezilla Site Vice President FirstEnergy Nuclear Operating Company Perry Nuclear Power Plant P. O. Box 97, 10 Center Road, A-PY-A290 Perry, OH 44081-0097
==SUBJECT:==
 
ERRATA FOR PERRY NUCLEAR POWER PLANT NRC INTEGRATED INSPECTION REPORT 05000440/2010004
SUBJECT: PERRY NUCLEAR POWER PLANT NRC INTEGRATED INSPECTION REPORT 05000440/2010004


==Dear Mr. Bezilla:==
==Dear Mr. Bezilla:==
On September 30, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Perry Nuclear Power Plant. The enclosed report documents the inspection findings which were discussed on October 6, 2010, with you and members of your staff.
On October 29, 2010, the U.S. Nuclear Regulatory Commission (NRC) issued Integrated Inspection Report 05000440/2010004 (ML103020254). A cross-cutting aspect associated with a non-cited violation was inadvertently incorrectly characterized in the Integrated Inspection Report Summary of Findings. Please insert the attached errata where appropriate into Integrated Inspection Report 05000440/2010004.
 
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
 
Based on the results of this inspection, two NRC-identified findings of very low safety significance (Green) were identified. Both of the findings were determined to involve a violation of NRC requirements, however, because the findings were of very low safety significance and because the issues were entered into your corrective action program, the NRC is treating the findings as non-cited violations (NCVs) consistent with Section 2.3.2 of the NRC Enforcement Policy.
 
If you contest the subject or severity of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Perry Nuclear Power Plant.
 
In addition, if you disagree with the cross-cutting aspect of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Perry Nuclear Power Plant. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
Sincerely,/RA/ Jamnes L. Cameron, Chief Branch 6 Division of Reactor Projects Docket No. 50-440 License No. NPF-58


===Enclosure:===
We apologize for any inconvenience to you and your staff.
Inspection Report 05000440/2010004


===w/Attachment:===
Sincerely,
Supplemental Information cc w/encl: Distribution via ListServ Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION III Docket No: 50-440 License No: NPF-58 Report No: 050000440/2010004 Licensee: FirstEnergy Nuclear Operating Company (FENOC)
/RA/
Facility: Perry Nuclear Power Plant, Unit 1 Location: Perry, Ohio Dates: July 1, 2010, through September 30, 2010 Inspectors: M. Marshfield, Senior Resident Inspector T. Hartman, Resident Inspector R. Edwards, Reactor Inspector L. Jones, Reactor Engineer M. Phalen, Senior Health Physicist, DRS W. Slawinski, Senior Health Physicist, DRS P. Smagacz, Reactor Engineer
Jamnes L. Cameron, Chief Branch 6 Division of Reactor Projects Docket No. 50-440 License No. NPF-58 Enclosure: Errata for Inspection Report 05000440/2010004 cc w/encl: Distribution via ListServ


Observers: V. Myers, Nuclear Safety Professional Development Program R. Leidy, Ohio Department of Health Approved by: Jamnes L. Cameron, Chief Branch 6 Division of Reactor Projects Enclosure
Errata for Inspection Report 05000440/2010004 SUMMARY OF FINDINGS IR 05000440/2010004; 07/01/2010 - 09/30/2010; Surveillance Testing; Problem Identification and Resolution.


=SUMMARY OF FINDINGS=
The inspection was conducted by resident and regional inspectors. The inspection report (IR) covers a 3-month period of resident inspection. Two green findings which were NCVs were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter (IMC) 0609 Significance Determination Process (SDP). Cross-cutting aspects were determined using IMC 0310, "Components Within The Cross-Cutting Areas." Findings for which the SDP does not apply may be "Green," or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
........................................................................................................... 1


=REPORT DETAILS=
A. Inspector-Identified and Self-Revealed Findings Cornerstone: Mitigating Systems
  ....................................................................................................................... 3Summary of Plant Status
  * Green. The inspectors identified a finding of very low safety significance and associated NCV of 10 CFR 50, Appendix B, Criterion XI, Test Control, for the unacceptable preconditioning of the 'A' residual heat removal (RHR) pump minimum flow valve prior to quarterly in-service testing. Specifically, the licensee performed a surveillance that cycled the valve prior to performing stroke time testing, and had not previously performed an evaluation assessing the sequence for preconditioning. The licensee entered the issue into their corrective action program.


==REACTOR SAFETY==
The inspectors determined that unacceptably preconditioning the RHR minimum flow valve was a performance deficiency that affected the Mitigating Systems Cornerstone because it can mask the true as-found condition of a component designed to mitigate accidents. The performance deficiency was determined to be more than minor because, if left uncorrected, it could lead to a more significant safety concern. The finding was of very low safety significance because it was not a design/qualification deficiency, did not represent a loss of system safety function, did not result in a loss of function of a single train for greater than its Technical Specification (TS)-allowable outage time, did not result in a loss of function of nonsafety-related risk-significant equipment and was not risk significant due to external events. This finding has a cross-cutting aspect in the work control planning component of the Human Performance area (per IMC 0310 H.3(a)), because the licensee did not appropriately plan work activities for plant structures, systems, and components. Specifically, the licensee did not schedule the surveillance tests in the proper sequence to prevent unacceptable preconditioning of the valve. (Section 1R22)
....................................................................................................... 31R01Adverse Weather Protection (71111.01) ............................................................. 31R04Equipment Alignment (71111.04Q) ..................................................................... 31R05Fire Protection (71111.05Q) ................................................................................ 51R06Flood Protection Measures (71111.06) ............................................................... 51R11Licensed Operator Requalification Program (71111.11) ..................................... 61R12Maintenance Effectiveness (71111.12Q) ............................................................ 61R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) ......... 71R15Operability Evaluations (71111.15) ..................................................................... 81R18Temporary Plant Modifications (71111.18) ......................................................... 91R19Post-Maintenance Testing (71111.19) ................................................................ 91R22Surveillance Testing (71111.22)
* Green. The inspectors identified a finding of very low safety significance and associated NCV for a failure to comply with TS 3.0.2 by not entering TS Limiting Condition for Operation (LCO) 3.3.5.1 Condition A and TS LCO 3.3.6.1 Condition A when required.


==RADIATION SAFETY==
The inspectors determined that the licensee incorrectly utilized a TS Surveillance Requirement Note that allows a delay in entering the Conditions and Required Actions for the given TS LCO. As a result, the licensee failed to correctly enter the Conditions 1  Enclosure
................................................................................................... 132RS1Radiological Hazard Assessment and Exposure Controls (71124.01) ............. 132RS3In-Plant Airborne Radioactivity Control and Mitigation (71124.03) ................... 172RS4Occupational Dose Assessment (71124.04)


==OTHER ACTIVITIES==
and Required Actions when reactor level instruments were declared inoperable to perform testing in support of planned maintenance. The licensee entered the issue associated with the failure to comply with TS into their corrective action program.
..................................................................................................... 214OA1Performance Indicator Verification (71151) ....................................................... 214OA2Problem Identification and Resolution (71152) ................................................. 234OA3Follow-up of Events and Notices of Enforcement Discretion (71153) ............... 264OA5Other Activities .................................................................................................. 274OA6Meetings............................................................................................................ 284OA7Licensee-Identified Violations ........................................................................... 28


=SUPPLEMENTAL INFORMATION=
This performance deficiency was determined to be more than minor because it impacted the Equipment Performance attribute of the Mitigating Systems Cornerstone, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage); and if left uncorrected it could lead to a more significant safety concern. This finding is of very low safety significance because it was not a design/qualification deficiency, did not represent a loss of system safety function, did not result in a loss of function of a single train for greater than its TS-allowable outage time, did not result in a loss of function of nonsafety-related risk-significant equipment and was not risk significant due to external events. This finding has a cross-cutting aspect in the decision making component of Human Performance cross-cutting area (per IMC 0310 H.1(b)), because the licensee did not use conservative assumptions to ensure the proposed action was safe. Specifically, the licensee incorrectly used the TS Surveillance Requirement Note to satisfy maintenance requirements. (Section 4OA2)
B. Licensee-Identified Violations One violation of very low safety significance was identified by the licensee and has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and its corrective action tracking number are listed in Section 4OA7 of this report.


==KEY POINTS OF CONTACT==
2  Enclosure
Licensee 
: [[contact::M. Bezilla]], Vice President Nuclear
: [[contact::D. Evans]], Work and Outage Management Director
: [[contact::J. Grabnar]], Site Engineering Director
: [[contact::H. Hanson]], Performance Improvement Director
: [[contact::T. Jardine]], Operations Manager
: [[contact::K. Krueger]], Plant General Manager
: [[contact::P. McNulty]], Radiation Protection Manager
: [[contact::M. Stevens]], Maintenance Director
: [[contact::J. Tufts]], Chemistry Manager
Other 
: [[contact::C. O'Clare]], Ohio Department of Health 


==LIST OF ITEMS==
UNITED STATES ovember 9, 2010
OPENED, CLOSED AND DISCUSSED
===Opened and Closed===
: 05000440/2010004-01 NCV Unacceptable Preconditioning of RHR Valve Prior to ASME In-Service Testing (1R22)
: 05000440/2010004-02 NCV Failure to Comply with Technical Specification LCOs When Reactor Vessel Level Instruments Were Declared
Inoperable (4OA2.4) 


===Closed===
==SUBJECT:==
: [[Closes finding::05000440/FIN-2010003-06]] URI Failure to Hydrostatically Test Replacement Components in Accordance with ASME (Section 4OA5.1)
ERRATA FOR PERRY NUCLEAR POWER PLANT NRC INTEGRATED INSPECTION REPORT 05000440/2010004
: [[Closes LER::05000440/LER-2010-003]] LER Loss of Control Rod Drive Header Pressure Results in Manual RPS Actuation (Section 4OA3.1) 
: Discussed 45815 EN Retraction of Event Notification 45815: Loss of Safety Function to Control the Release of Radioactive Material (Section 4OA3.2) 
: Attachment
==LIST OF DOCUMENTS REVIEWED==
The following is a partial list of documents reviewed during the inspection.
: Inclusion on this list does not imply that the NRC inspector reviewed the documents in their entirety, but rather that selected sections or portions of the documents were evaluated as part of the overall inspection effort.
: Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.
: 1R01 Adverse Weather
: CR 10-80444; Security Project - North-Side Concrete 'T' Wall Installation Issues Drawing 743-0013-00000; Topography and Storm Drain Composite; Revision D
: EER 600631290; Perform Evaluation to Determine Locations of Drainage Gaps in Installed T-Walls; dated August 4, 2010 1R04 Equipment Alignment
: CR 08-42257; Annulus Exhaust Gas Treatment System (AGETS) "A" Train Low Flow Adjustment; dated June 20, 2008
: CR 10-72614; Unplanned Fire Suppression Impairment for Annulus Exhaust Gas Treatment System; dated March 4, 2010
: CR 08-34483; Annulus Exhaust Gas Treatment System Flow Indication Low Flow; dated January 29, 2008
: CR 07-31871; AEGTS B Discharge Damper Is Not Functioning Correctly; dated December 21, 2007 Drawing 912-0605-00000; Reactor Building Annulus Exhaust Gas Treatment; Revision W
: PYBP-POS-2-2; Annulus Exhaust Gas Treatment System A (B) Outage Protected Equipment Posting Checklist; Revision 10 PNPP No. 10392; Annulus Exhaust Gas Treatment System A (B) Outage Protected Equipment Posting Checklist; dated July 14, 2009
: SOI-M15; AEGTS System; Revision 8
: VLI-M23/24; MCC, Switchgear and Miscellaneous Electrical Equipment Area HVAC System; Revision 7
: CR 10-82114; 0M23C0002B Did Not Trip with a B Train Trip Signal Present; dated September 2, 2010
: CR 10-82118; Replacement Solenoid Valve Mount Screw Holes Are Not Threaded; dated August 31, 2010 Drawing 912-0609-00000; MCC Switchgear and Misc Electrical Equipment Areas HVAC System and Battery Room Exhaust; Revision AA Perry Plant Health Report 2010-2 for P42 - Emergency Closed Cooling System
: SOI-P42; Emergency Closed Cooling System; Revision 16
: VLI-P42; Emergency Closed Cooling System; Revision 15 Drawing 302-0621-00000; Emergency Closed Cooling System; Revision SS
: Drawing 208-0041-00002; Reactor Protection System MG Set S001B
: Drawing 208-0041-00001; Reactor Protection System MG Set S001A
: CR 10-81707; Overheating on Voltage Regulator for RPS MG Set B; dated August 25, 2010 
: Attachment 1R05 Fire Protection (Annual/Quarterly)
: PAP-1910; Fire Protection Program; Revision 19 P54-24; Calculation of Combustible Loading and Allowable Limits for Fire Loading; Revision 4
: FPI-0IB; Pre-Fire Plan Instruction - Intermediate Building; Revision 5
: FPI-0CC; Pre-Fire Plan Instruction - Control Complex; Revision 8
: CR 10-80981; Documentation of NRC Questions; dated August 9, 2010
: CR 10-81985; Response to Questions from the NRC Resident Inspector; dated August 27, 2010
: FPI-1AB; Pre-Fire Plan Instruction - Auxiliary Building; Revision 3
: CR 10-82504; NRC Question Regarding Pen Seals in
: AX 620' West; dated September 10, 2010 
: 1R06 Internal Flooding
: PAP-0204; Housekeeping/Cleanliness Control Program; Revision 24
: ARI-H13-P601-0018; Leak Detection; Revision 13
: NOP-OP-1012; Material Readiness and Housekeeping Inspection Program; Revision 5
: CR 10-77685; Various Through Wall Piping Leaks on N71; dated June 3, 2010 Drawing 911-0617; Auxiliary Building Drains; Revision F 1R11 Licensed Operator Requalification Program
: PYBP-PTS-0005; Operator Continuing Training Program Administration; Revision 25
: PYBP-POS-0027; Operator Actions from Memory; Revision 0, dated December 3, 2008
: Simulator Exercise Guide
: OTLC-3058201010_PY_SGC1; Cycle 10 2010 Evaluated Scenario C1; Revision 0
: CR 10-80980; Unsat Training Observation - Ops Performance Improvement Time Not Properly Used; dated August 9, 2010
: CR 10-81725; Unqualified Individuals Signing as Training Coordinators; dated August 25, 2010 1R12 Maintenance Effectiveness
: WO 200284303; Chg Oil Fltrs Combustion Gas Purge Unit; dated July 21, 2010
: CR 10-79817; Wrong Oil Added to CGMC Reservoir; dated July 17, 2010
: CR 10-80089;
: NRC-ID. No FME High Risk Brief Sheet in Work Order; dated July 22, 2010
: CR 10-80169; Failed PMT for CGMC B Aux Oil Pump; dated July 24, 2010
: Clearance
: EPY-M25-0005; Control Room HVAC Supply Plenum; dated September 1, 2010 LCOTR# A10-M25-032; M25/26 Inoperable, Period 5 Week 10; dated August 30, 2010
: CR 10-81952; Relay Contacts do not Change State; dated August 30, 2010
: CR 10-81957; Loose Fittings on Low Flow Switch; dated August 30, 2010
: Drawing 912-0610-00000; Control Room HVAC and Emergency Recirculation System; Revision FF
: CR 10-82639; Maintenance HPCS Work Start Deficiencies; dated September 13, 2010
: CR 10-82715; Inadequate Order for Div 3 Fuel Oil Day Tank Work; dated September 16, 2010
: CR 10-82864; Grease Fitting Damaged during Disassembly; dated September 19, 2010
: CR 10-82970; Less Than Adequate Contingency Planning for Div 3 DG Inspections; dated September 21, 2010
: CR 10-82989; FME Concerns Identified in Div 3 DG Room; dated September 20, 2010
: CR 10-83194; PMT Could Not Be Worked as Written; dated September 24, 2010
: WO 200430281; Rebuild Ball Valves to Small and Large Seals
: CR 10-83134; Lower Airlock Door Air Supply Flex Hoses Possibly Defective
: CR 10-82842; Lower Airlock Pneumatic System Pressure Drop Test Failed Attachment
: CR 10-76252; Lower Containment Airlock Reactor Door
: CR 09-69338; Upper Containment Airlock Reactor Door
: 1R13 Maintenance Risk Assessments and Emergent Work Control
: NOP-OP-1007; Risk Management; Revision 7
: CR 10-80396; Perry Not Notified of Conservative Grid Ops; dated July 28, 2010
: CR 10-81724; Finding - Fuel Oil Samples not Analyzed per Tech Specs; dated August 25, 2010
: CR 10-81727; Diesel Fuel Oil Sample Analysis Completion Dates Inconsistent; dated August 25, 2010
: CR 10-81733; Procedure Steps Signed as Performed Inappropriately; dated August 25, 2010
: CR 10-82658; Water/Steam Leak From 1N27F505D (RFBP D Discharge Check Valve); dated September 15, 2010
: WO 200430709; Wire Wrap/Inject Inspection Flange; dated September 17, 2010
: WO 200430710; Remove Insulation @ Valve; dated September 16, 2010
: ECP 10-0570-000; Leak Sealant Device on Reactor Feedwater Booster Pump 'D' Discharge Check Valve (1N27F0505D); Revision 0
: ECP 10-0570-001; Install and Inject Leak Sealant Device on Reactor Feedwater Booster Pump 'D' Discharge Check Valve (1N27F0505D); Revision 1
: CR 10-82682; Div 3 DG Generator Inter Pole Side Plate Movement; dated September 15, 2010
: CR 10-82992; Div 3 Diesel Generator - Migrating Exciter Field Core Plates; dated September 22, 2010
: WO 200430766; Remove Generator Rotor, Inspect for Loose Wedge Studs; dated September 15, 2010 1R15 Operability Evaluations
: CR 10-78672; 1M43 Agastat Relay Qualification Issue; dated June 22, 2010
: CR 10-81023; M52 Turning Vanes Degraded; dated August 10, 2010 Prompt Functionality Assessment for Degraded TSC Ventilation Supply Fan Turning Vanes; dated August 13, 2010 Prompt Operability Determination for Diesel Generator Building Ventilation Systems; dated July 15, 2010
: CR 10-81973; No Insulation Inside Plenum; dated August 30, 2010 eSOMS Narrative Logs dated September 2, 2010
: Prompt Operability Determination for ECC to FPCC Heat Exchanger Bypass Valve Stroke Time Testing Failure; August 24, 2010
: CR 10-81623; OP42F0255B Failed Stroke Closed Test; dated August 23, 2010
: 1R18 Permanent/Temporary Modifications Perry Plant Health Report 2010-2 for Temporary Modifications
: NOP-CC-2003; Engineering Changes; Revision 14
: NORM-CC-2001; Engineering Change Process Flowcharts; Revision 00
: ECP 10-0020-0000; Reference Documents - Hot Surge Tank Low Level Alarm from Level Transmitter Signal; Revision 0
: ECP 10-0020-0001; Hot Surge Tank Low Level Alarm from Level Transmitter Signal; Revision 3
: WO 200399695; Hot Surge Tank Low Level Alarm; dated May 15, 2010
: NOBP-ER-3003-01; Temporary Modification Review Checklist; Revision 00
: CR 09-67788; Host Surge Tank (HST) Level Low Alarm Locked In; dated November 15, 2009 Drawing 302-0081-00000; Feedwater; Revision BBB 
: Attachment Drawing 302-0101-00000; Condensate System; Revision TT Drawing 208-0149-00002; MDFP Auto Start Logic & RFBP Auto Start Logic; Revision S
: CR 10-82802; Potential Single Failure Vulnerability with Hot Surge Tank Temp Mod; dated September 16, 2010 1R19 Post-Maintenance Testing
: SVI-B21-T0137F; ECCS Drywell Pressure High Channel "F" Functional for 1B21-N694F; Revision 5
: PTI-M23-P0005; Emergency Service Water Pump House Ventilation System Train B Damper
: Stroking; Revision 5
: WO 200323496; Replace Rosemount MTU Card; dated August 11, 2010
: WO 200323644; Replace Keylock Control Switch 1B21C-S27A; dated August 4, 2010
: WO 200340398; Replace and Perform Calibration Check of 1M15D0001B Instrumentation; dated August 25, 2010
: WO 200327715; Replace AEGT Fan 'B' Motor; dated August 25, 2010
: WO 200290571; Replace SLS/MTR/Oil Hydramotor at ESW "B" Outlet Damper; dated September 6, 2010
: WO 200333304; MERP - Replace Utility Station w/NUS; dated September 6, 2010
: CR 10-81632; Temperature Switch Found Tripped; dated August 23, 2010
: CR 10-81633; RFACR: Damaged Field Conductor to Motor; dated August 23, 2010
: WO 200328863; Replace Cntrl Relays in EH1304 Cubicle; dated September 20, 2010
: SOI-R22; Metal Clad Switchgear 5-15 KV; Revision 25
: CR 10-82852; Unexpected Reading Obtained during Functional Testing; dated September 19, 2010
: SVI-E22-T1319; Diesel Generator Start and Load Division 3; Revision 15
: CR 10-83148; Div 3 Emergency Diesel Generator Failure to Start During Testing; dated September 24, 2010
: CR 10-83163; Generator Stator Temperature Monitor is Erratic and Unreliable; dated September 24, 2010
: CR 10-83181; Div 3 DG Additional Tagging Points Requested; dated September 24, 2010
: 1R22 Surveillance Testing
: SVI-E12-T2001; RHR A Pump and Valve Operability Test; Revision 26
: SVI-E12-T1194; LPCI Pump A Discharge Low Flow (Bypass) Channel Functional for 1E12-N652A; Revision 8
: SVI-E51-T2001; RCIC Pump and Valve Operability Test; Revision 32
: CR 01-79624;
: NRC-Identified Concern for Pre-conditioning Valve During Surveillance Testing; dated July 12, 2010
: NOP-ER-3204; Inservice Testing Program; Revision 1
eSOMS Narrative Logs dated July 7-8, 2010
: SVI-P45-T2002; ESW Pump B and Valve Operability Test; Revision 26
: SVI-R10-T5227; Off-Site Power Availability Verification; Revision 2
: Attachment 2RS1 Radiological Hazard Assessment and Exposure Controls
: CR 09-56065; Containment Vessel Drywell Purge Degraded Flows Impacting Refuel Floor; dated March 25, 2009
: CR 09-57294; Boundary Exceeded Radiological Controlled Area (RCA); dated April 16, 2009
: CR 09-60436; Dose Rates in the P5480405 Condensate Backwash Receiving Tanl Higher than Expected; dated June 11, 2009
: CR 09-62628; Radioactive Material Found Outside the RCA; dated August 2, 2009
: CR 09-63398 and Associated Apparent Cause Evaluation; Platform Found Outside with Fixed Contamination; dated August 18, 2009
: CR 09-66069; RISB Radioactive Material Inventory Discrepancies; dated October 16, 2009
: CR 10-76774; Radiological Issues Associated with Division 2 ECC LOCA Initiation; dated May 11, 2010
: CR-09-54403;
: RFO-12 Elevated Airborne Levels During Separator Lift; dated February 28, 2009
: HPI-C0014; Radlock key Issue; Revision 01
: HPI-H0004; Identification of Radioactive Materials and Release of Materials from RCAs; Revision 22
: HPI-K0009; Operation of the WARF, RISB and OSSC Yard; Revision 0
: HPI-L0004; Source Control Documentation and Inventory; Revision 8
: NOPB-NF-3102; Control of Non-Special Nuclear Material in the Fuel Pools; Revision 00
: NOP-OP-4101; Access Controls for Radiologically Controlled Areas; Revision 01
: NOP-OP-4102; Radiological Postings, Labeling, and Markings; Revision 05
: NOP-OP-4107; Radiation Work Permit; Revisions 4 and 5
: NRC Form 748; National Source Tracking Transaction Report; dated January 12, 2009
: NSTS Annual Inventory Reconciliation; dated September 9, 2009, and January 29, 2010 PNPP No. 10280; Sealed Source Leak Test Data Sheet
: HPI-L0004; dated January 13, 2010 PNPP No. 7445; Sealed Source Leak Test Data Sheet ORM 6.4.2; dated January 13, 2010
: SVI-E31-T5190; Sealed Source Leak Test and Inventory; Revision 5
: TEDE ALARA Evaluations for ALARA Plan Nos. 09-6018-02, 09-6041-00 and 10-0066; dates October 2008 and February 2010 2RS3 In-Plant Airborne Radioactivity Control and Mitigation
: Air Sample Records/Collection and Evaluation Forms for Various Work Activities and Locations; Various Dates in March and April 2009
: CR 09-57025; Air Sampling Equipment Found with Expired Calibration; dated April 09, 2009
: EP-Emergency Plan for Perry Nuclear Power Plant Docket Nos. 50-440; Revision 30
: HPI-G0007; Maintenance of Respiratory Protective Equipment and Operation of the Respirator Cleaning / Issue Facilities; Revision 21
: HPI-G0008; Requalification of Respirators; Revision 07
: HPI-L0003; Equipment History; Revision 06
: HRI-0003; Respirator Qualification Health Assessment; Revision 02
: NOP-OP-4301; Respiratory Protection Program; Revision 01
: NOP-OP-4302; Issuing Respiratory Protection; Revision 00
: NOP-OP-4303; Respirator Quantitative Fit Test Portacount
: PRO 8030; Revision 01
: NOP-OP-4310; Firehawk M7 Self Contained Breathing Apparatus; Revision 04
: NOP-OP-4702; Air Sampling; Revision 01
: PSI-0022; Emergency Plan Training program; Revision 03
: PYBP-RPS-0038; Radiologically Controlled Area HEPA Ventilation and HEPA Vacuum Unit Program; Revision 01 
: Attachment 2RS4 Occupational Dose Assessment 
: ALARA Plan 09-6040; Suppression Pool Cleaning and Inspection; Revision 03
: NOP-OP-4204; Special External Exposure Monitoring; Revision 03
: NOP-OP-4204-04; Effective Dose Equivalent Dose Determination; Revision 01
: NOP-OP-4205; Dose Assessment; Revision 03
: NOP-OP-4206; Bioassay Program; Revision 00
: NOP-OP-4503; Personnel Contamination Monitoring; Revision 02
: Radiological Engineering Assessment; Source term Determination for Cycle 12 Operations; Undated
: RWP 09-6040;
: RFO-12 Suppression Pool Diving Activities; Revision 03
: 4OA1 Performance Indicator Verification
: NOBP-LP-4012; NRC Performance Indicators; Revision 3
: NOBP-LP-4012-06; MSPI Data Sheets for Heat Removal System from July 2009 to June 2010; Revision 2
: NOBP-LP-4012-07; MSPI Data Sheets for Residual Heat Removal System from July 2009 to June 2010; Revision 2
: NOBP-LP-4012-19; MSPI Data Sheets for Emergency Service Water from July 2009 to June 2010; Revision 2 Mitigating Systems Performance Index Basis Document; Revision 4
: PYBP-DES-0011; Mitigating Systems Performance Index; Revision 1
eSOMS Narrative Logs; July 2009 to June 2010
: List of CRs for all MSPI monitored systems; July 2009 to June 2010 MSPI Derivation Reports for all MSPI monitored systems; June 2010 
: 4OA2 Identification and Resolution of Problems 
: CRs for the period January 1, 2010, through June 30, 2010
: CR 10-81162; Potential Misapplication of TS Note; dated August 12, 2010 eSOMS Narrative Logs; July 2010, to August 2010
eSOMS Action Tracking; July 2010 to August 2010
: WO 200322765; PDP - "New PM" Replace Rosemount STU Card; dated August 9, 2010
: SVI-B21-T0187C, ECCS/HPCS RPV Water Level 2 and Level 8 Channel C Functional for
: 1B21-N673C; Revision 6 4OA3 Follow-up of Events and Notices of Enforcement Discretion
: LER 2010-003; Loss of Control Rod Drive Header Pressure Result in Manual RPS Actuation; dated July 12, 2010
: CR 10-74904; During
: SVI-E12T0146 Performance, Operations Received Unexpected Annunciators; dated April 4, 2010
: 4OA7 Licensee-Identified Findings
: CR 10-81724; Fuel Oil Samples not Analyzed per Tech Specs; dated August 25, 2010 
: Attachment
==LIST OF ACRONYMS==
: [[USED]] [[]]
: [[AEGTS]] [[annulus exhaust gas treatment system]]
: [[ALA]] [[]]
: [[RA]] [[as-low-as-reasonably-achievable]]
: [[AS]] [[]]
: [[ME]] [[American Society of Mechanical Engineers]]
: [[CAP]] [[corrective action program]]
CFR  Code of Federal Regulations CR  condition report
ECC  emergency closed cooling
: [[EDG]] [[emergency diesel generator]]
: [[ESW]] [[emergency service water]]
: [[FENOC]] [[FirstEnergy Nuclear Operating Company]]
: [[HE]] [[]]
PA  high-efficiency particulate air
: [[HP]] [[health physics]]
: [[HP]] [[]]
CS  high pressure core spray
: [[HRA]] [[high radiation area]]
: [[IMC]] [[Inspection Manual Chapter]]
IP  Inspection Procedure IR  Inspection Report
IST  inservice testing
: [[LCO]] [[limiting condition for operation]]
: [[LER]] [[Licensee Event Report]]
: [[LPCI]] [[low pressure core injection]]
: [[MS]] [[]]
PI  mitigating systems performance index
NCV  non-cited violation
: [[NEI]] [[Nuclear Energy Institute]]
: [[NIOSH]] [[/]]
: [[MSSHA]] [[National Institute for Occupational Safety and Health/  Mine Safety and Health Administration]]
: [[NOP]] [[Nuclear Operating Procedure]]
NRC  Nuclear Regulatory Commission
ONI  Off-Normal Instruction
: [[PI]] [[performance indicator]]
: [[PM]] [[post-maintenance]]
RCIC  reactor core isolation cooling RHR  residual heat removal
RP  radiation protection
RPS  reactor protection system
: [[RWP]] [[radiation work permit]]
: [[SCBA]] [[self-contained breathing apparatus]]
SDP  Significance Determination Process SR  surveillance requirement
SSC  structure, system, or component
: [[SVI]] [[Surveillance Instruction]]
: [[TS]] [[Technical Specification]]
: [[USAR]] [[Updated Safety Analysis Report]]
: [[VH]] [[]]
RA  very high radiation area
WO  work order
M. Bezilla    -2-
In accordance with
: [[10 CFR]] [[2.390 of the]]
: [[NRC]] [['s "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the]]
: [[NRC]] [[Public Document Room or from the Publicly Available Records (]]
: [[PARS]] [[) component of]]
: [[NRC]] [['s document system (]]
ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). Sincerely, 
      /RA/  Jamnes L. Cameron, Chief
Branch 6
Division of Reactor Projects  Docket No. 50-440
License No. NPF-58


Enclosure: Inspection Report 05000440/2010004  w/Attachment:  Supplemental Information cc w/encl: Distribution via ListServ 
Dear M
}}
}}

Latest revision as of 07:24, 13 November 2019

IR 05000440-10-004, on 07/01/2010 09/30/2010, Surveillance Testing, Problem Identification and Resolution
ML103130239
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 11/09/2010
From: Jamnes Cameron
NRC/RGN-III/DRP/B6
To: Bezilla M
FirstEnergy Nuclear Operating Co
References
IR-10-004
Download: ML103130239 (5)


Text

ber 9, 2010

SUBJECT:

ERRATA FOR PERRY NUCLEAR POWER PLANT NRC INTEGRATED INSPECTION REPORT 05000440/2010004

Dear Mr. Bezilla:

On October 29, 2010, the U.S. Nuclear Regulatory Commission (NRC) issued Integrated Inspection Report 05000440/2010004 (ML103020254). A cross-cutting aspect associated with a non-cited violation was inadvertently incorrectly characterized in the Integrated Inspection Report Summary of Findings. Please insert the attached errata where appropriate into Integrated Inspection Report 05000440/2010004.

We apologize for any inconvenience to you and your staff.

Sincerely,

/RA/

Jamnes L. Cameron, Chief Branch 6 Division of Reactor Projects Docket No. 50-440 License No. NPF-58 Enclosure: Errata for Inspection Report 05000440/2010004 cc w/encl: Distribution via ListServ

Errata for Inspection Report 05000440/2010004 SUMMARY OF FINDINGS IR 05000440/2010004; 07/01/2010 - 09/30/2010; Surveillance Testing; Problem Identification and Resolution.

The inspection was conducted by resident and regional inspectors. The inspection report (IR) covers a 3-month period of resident inspection. Two green findings which were NCVs were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter (IMC) 0609 Significance Determination Process (SDP). Cross-cutting aspects were determined using IMC 0310, "Components Within The Cross-Cutting Areas." Findings for which the SDP does not apply may be "Green," or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

A. Inspector-Identified and Self-Revealed Findings Cornerstone: Mitigating Systems

  • Green. The inspectors identified a finding of very low safety significance and associated NCV of 10 CFR 50, Appendix B, Criterion XI, Test Control, for the unacceptable preconditioning of the 'A' residual heat removal (RHR) pump minimum flow valve prior to quarterly in-service testing. Specifically, the licensee performed a surveillance that cycled the valve prior to performing stroke time testing, and had not previously performed an evaluation assessing the sequence for preconditioning. The licensee entered the issue into their corrective action program.

The inspectors determined that unacceptably preconditioning the RHR minimum flow valve was a performance deficiency that affected the Mitigating Systems Cornerstone because it can mask the true as-found condition of a component designed to mitigate accidents. The performance deficiency was determined to be more than minor because, if left uncorrected, it could lead to a more significant safety concern. The finding was of very low safety significance because it was not a design/qualification deficiency, did not represent a loss of system safety function, did not result in a loss of function of a single train for greater than its Technical Specification (TS)-allowable outage time, did not result in a loss of function of nonsafety-related risk-significant equipment and was not risk significant due to external events. This finding has a cross-cutting aspect in the work control planning component of the Human Performance area (per IMC 0310 H.3(a)), because the licensee did not appropriately plan work activities for plant structures, systems, and components. Specifically, the licensee did not schedule the surveillance tests in the proper sequence to prevent unacceptable preconditioning of the valve. (Section 1R22)

  • Green. The inspectors identified a finding of very low safety significance and associated NCV for a failure to comply with TS 3.0.2 by not entering TS Limiting Condition for Operation (LCO) 3.3.5.1 Condition A and TS LCO 3.3.6.1 Condition A when required.

The inspectors determined that the licensee incorrectly utilized a TS Surveillance Requirement Note that allows a delay in entering the Conditions and Required Actions for the given TS LCO. As a result, the licensee failed to correctly enter the Conditions 1 Enclosure

and Required Actions when reactor level instruments were declared inoperable to perform testing in support of planned maintenance. The licensee entered the issue associated with the failure to comply with TS into their corrective action program.

This performance deficiency was determined to be more than minor because it impacted the Equipment Performance attribute of the Mitigating Systems Cornerstone, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage); and if left uncorrected it could lead to a more significant safety concern. This finding is of very low safety significance because it was not a design/qualification deficiency, did not represent a loss of system safety function, did not result in a loss of function of a single train for greater than its TS-allowable outage time, did not result in a loss of function of nonsafety-related risk-significant equipment and was not risk significant due to external events. This finding has a cross-cutting aspect in the decision making component of Human Performance cross-cutting area (per IMC 0310 H.1(b)), because the licensee did not use conservative assumptions to ensure the proposed action was safe. Specifically, the licensee incorrectly used the TS Surveillance Requirement Note to satisfy maintenance requirements. (Section 4OA2)

B. Licensee-Identified Violations One violation of very low safety significance was identified by the licensee and has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and its corrective action tracking number are listed in Section 4OA7 of this report.

2 Enclosure

UNITED STATES ovember 9, 2010

SUBJECT:

ERRATA FOR PERRY NUCLEAR POWER PLANT NRC INTEGRATED INSPECTION REPORT 05000440/2010004

Dear M