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#REDIRECT [[IR 05000382/2012008]]
{{Adams
| number = ML12310A497
| issue date = 11/05/2012
| title = IR 05000382-12-008, July 16, 2012 - September 24, 2012, Waterford 3 Biennial Baseline Inspection of the Identification and Resolution of Problems.
| author name = Kellar R
| author affiliation = NRC/RGN-IV/DRS
| addressee name = Jacobs D
| addressee affiliation = Entergy Operations, Inc
| docket = 05000382
| license number = NPF-038
| contact person =
| case reference number = EA-12-198
| document report number = IR-12-008
| document type = Inspection Report, Letter, Notice of Violation
| page count = 50
}}
See also: [[see also::IR 05000382/2012008]]
 
=Text=
{{#Wiki_filter:UNITED STATES
                                  NUC LEAR REGULATOR Y COMMI SSI ON
                                                      RE G IO N I V
                                                1600 EAST LAMAR BLVD
                                            ARL INGTON, TEXAS 76011- 4511
                                                November 5, 2012
EA-12-198
Donna Jacobs, Site Vice President, Operations
Entergy Operations, Inc.
Waterford Steam Electric Station, Unit 3
17265 River Road
Killona, LA 70057-0751
SUBJECT:        WATERFORD STEAM ELECTRIC STATION, UNIT 3 -
                NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION
                REPORT 05000382/2012008 AND NOTICE OF VIOLATION
Dear Ms. Jacobs:
On August 2, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem
Identification and Resolution biennial inspection at your Waterford Steam Electric Station,
Unit 3. The enclosed inspection report documents the inspection results that were discussed on
August 2, 2012, with Keith Nichols, Director of Engineering, and other members of your staff.
After additional in-office inspection, a final telephonic exit meeting was conducted on September
24, 2012 with Keith Nichols, Director of Engineering, and other members of your staff.
This inspection was an examination of activities conducted under your license as they relate to
problem identification and resolution and compliance with the Commissions rules and
regulations and the conditions of your license. Within these areas, the inspection involved
examination of selected procedures and representative records, observations of activities, and
interviews with personnel.
Based on the inspection sample, the inspection team concluded that the implementation of the
corrective action program and overall performance related to identifying, evaluating, and
resolving problems at Waterford Steam Electric Station, Unit 3, were adequate. Licensee
identified problems were entered into the corrective action program at a low threshold.
Problems were generally prioritized and evaluated commensurate with the safety significance of
the problems. Corrective actions were generally implemented in a timely manner
commensurate with their importance to safety and addressed the identified causes of problems.
Lessons learned from industry operating experience were generally reviewed and applied when
appropriate. Audits and self-assessments were effectively used to identify problems and
appropriate actions. Finally, the team determined that the station maintains a safety-conscious
work environment where employees feel free to raise nuclear safety concerns without fear of
retaliation.
Five NRC identified findings of very low safety significance (Green) were identified during this
inspection and are documented in the enclosed report. All five of these findings were
determined to involve a violation of NRC requirements. The NRC is treating four of the five
 
D. Jacobs                                      -2-
violations as non-cited violations (NCVs), consistent with Section 2.3.2 of the Enforcement
Policy. Additionally, a licensee-identified violation, which was determined to be of very low
safety significance, is listed in this report.
One of the findings that the NRC evaluated under the risk significance determination process as
having very low safety significance (Green) did not meet the criteria to be treated as a non-cited
violation. The violation associated with this issue was evaluated in accordance with the NRC
Enforcement Policy. The current version of this Policy is available on the NRC website at
(http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html). This violation is cited in
the enclosed Notice of Violation (Notice), and the circumstances surrounding it are described in
detail in the subject inspection report. The violation is being cited in the Notice in accordance
with Section 2.3.2 of the Enforcement Policy because you failed to restore compliance in a
reasonable period of time after the violation was previously identified as a non-cited violation.
You are required to respond to this letter and should follow the instructions specified in the
enclosed Notice when preparing your response. This reply should be clearly marked as a
"Reply to a Notice of Violation; EA-12-198" and should specifically include a firm commitment as
to when you will establish a design basis to determine the river level at which flood control
measures were to be initiated for closing the water tight doors as required in
Procedure OP-901-521, Severe Weather and Flooding. If you have additional information that
you believe the NRC should consider, you may provide it in your response to the Notice. The
NRC review of your response to the Notice will also determine whether further enforcement
action is necessary to ensure compliance with regulatory requirements.
If you contest these non-cited violations, you should provide a response within 30 days of the
date of this inspection report, with the basis for your denial, to the Nuclear Regulatory
Commission, ATTN: Document Control Desk, Washington DC 20555-0001, with copies to:
(1) the Regional Administrator, Region IV; (2) the Director, Office of Enforcement, United States
Nuclear Regulatory Commission, Washington, DC 20555-0001; and (3) NRC Resident
Inspector Office at Waterford Steam Electric Station, Unit 3.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the Regional Administrator, Region IV; and the NRC Resident Inspector at
Waterford Steam Electric Station, Unit 3.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, and your response will be available electronically for public inspection in the NRC
Public Document Room or from the Publicly Available Records (PARS) component of NRC's
Agency wide Document Access and Management System (ADAMS). ADAMS is accessible
from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic
Reading Room).
                                                Sincerely,
                                                /RA/
                                                Ray Kellar, P.E., Chief
                                                Technical Support Branch
                                                Division of Reactor Safety
 
D. Jacobs                                  -3-
Docket No.: 50-382
License No: NPF-38
Enclosures:
  1. Notice of Violation EA-12-198
  2. Inspection Report 05000382/2012008
        w/Attachments:
          1. Supplemental Information
          2. Information Request
cc w/enclosures: Electronic Distribution for Waterford 3
 
 
ML12310A497
SUNSI Rev Compl. Yes  No ADAMS                    Yes  No    Reviewer Initials    RLS
Publicly Avail.          Yes  No Sensitive        Yes  No    Sens. Type Initials
TL/SRI:DRP/C RI:DRP/E              PE:DRP/C    RI:DRS/EB1    ACES            BC:DRP/E
RSmith          DOverland          RKumana      MYoung        HGepford        DAllen
      -e-              -e-        /RA/        /RA/          /RA/            /RA/
10/23/2012      10/23/2012        10/13/2012  10/23/2012    10/26/2012      10/30/12
BC:DRS/TSB
RKellar
/RA/
11/5/2012
                                     
                                      NOTICE OF VIOLATION
Entergy Operations, Inc.                                                Docket No. 50-382
Waterford Steam Electric Station, Unit 2                                License No. NPF-38
                                                                        EA-12-198
During an NRC inspection conducted on July 16 through September 24, 2012, a violation of
NRC requirements was identified. In accordance with the NRC Enforcement Policy, the
violation is listed below:
        Title 10 of the Code of Federal Regulations Part 50, Appendix B, Criterion III, Design
        Control, states, in part, that measures shall be established to assure that applicable
        regulatory requirements and the design basis, as defined in 10 CFR 50.2, are correctly
        translated into specifications, procedures, and instructions.
        Contrary to the above, from March 10, 2011, to August 2, 2012, the licensee failed to
        establish measures to assure that applicable regulatory requirements and the design
        basis, as defined in 10 CFR 50.2, were correctly translated into specifications,
        procedures and instructions. Specifically, the licensee had not established a design
        basis to determine the river level at which flood control measures were to be initiated for
        closing the water tight doors as required in Procedure OP-901-521, Severe Weather
        and Flooding.
This violation is associated with a Green Significance Determination Process finding.
Pursuant to the provisions of 10 CFR 2.201, Entergy Operations is hereby required to submit a
written statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document
Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator,
Region IV, and a copy to the NRC Resident Inspector at the facility that is the subject of this
Notice, within 30 days of the date of the letter transmitting this Notice of Violation (Notice). This
reply should be clearly marked as a "Reply to a Notice of Violation; EA-12-198" and should
include for each violation: (1) the reason for the violation or, if contested, the basis for disputing
the violation or severity level, (2) the corrective steps that have been taken and the results
achieved, (3) the corrective steps that will be taken, and (4) the date when full compliance will
be achieved. Your response may reference or include previous docketed correspondence if the
correspondence adequately addresses the required response. If an adequate reply is not
received within the time specified in this Notice, an Order or a Demand for Information may be
issued as to why the license should not be modified, suspended, or revoked, or why such other
action as may be proper should not be taken. Where good cause is shown, consideration will
be given to extending the response time.
If you contest this enforcement action, you should also provide a copy of your response, with
the basis for your denial, to the Director, Office of Enforcement, United States Nuclear
Regulatory Commission, Washington, DC 20555-0001.
                                                -1-                              Enclosure 1
 
Because your response will be made available electronically for public inspection in the NRC
Public Document Room or from the NRCs document system (ADAMS), accessible from the
NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not
include any personal privacy, proprietary, or safeguards information so that it can be made
available to the public without redaction. If personal privacy or proprietary information is
necessary to provide an acceptable response, then please provide a bracketed copy of your
response that identifies the information that should be protected and a redacted copy of your
response that deletes such information. If you request withholding of such material, you must
specifically identify the portions of your response that you seek to have withheld and provide in
detail the bases for your claim of withholding (e.g., explain why the disclosure of information will
create an unwarranted invasion of personal privacy or provide the information required by
10 CFR 2.390(b) to support a request for withholding confidential commercial or financial
information). If safeguards information is necessary to provide an acceptable response, please
provide the level of protection described in 10 CFR 73.21.
In accordance with 10 CFR 19.11, you may be required to post this Notice within two working
days of receipt.
Dated this 5th day of November, 2012
                                                -2-                              Enclosure 1
 
                U.S. NUCLEAR REGULATORY COMMISSION
                                  REGION IV
Docket:      50-382
License:    NPF-38
Report:      05000382/2012008
Licensee:    Entergy Operations, Inc.
Facility:    Waterford Steam Electric Station, Unit 3
Location:    17265 River Road
            Killona, LA 70057-0751
Dates:      July 16 through September 24, 2012
Team Leader: R. Smith, Senior Resident Inspector, Grand Gulf
Inspectors:  D. Overland, Resident Inspector, Waterford 3
            R. Kumana, Project Engineer
            M. Young, Reactor Inspector
Approved By: Ray Kellar, P.E., Chief
            Technical Support Branch
            Division of Reactor Safety
                                    -1-                    Enclosure 2
 
                                      SUMMARY OF FINDINGS
IR 05000382/2012008; July 16, 2012 -September 24, 2012; Waterford 3 "Biennial Baseline
Inspection of the Identification and Resolution of Problems."
The team inspection was performed by one senior resident inspector, one resident inspector,
one reactor inspector, and one project engineer. One cited violation and four non-cited
violations of very low safety significance (Green) were identified during this inspection. The
significance of most findings is indicated by their color (Green, White, Yellow, Red) using
Inspection Manual Chapter 0609, "Significance Determination Process". Findings for which the
significance determination process does not apply may be Green or be assigned a severity level
after NRC management review. The NRC's program for overseeing the safe operation of
commercial nuclear power reactors is described in NUREG 1649, "Reactor Oversight Process,"
Revision 4, dated December 2006.
Identification and Resolution of Problems
The team reviewed approximately 350 condition reports, work orders, engineering evaluations,
root and apparent cause evaluations, and other supporting documentation to determine if
problems were being properly identified, characterized, and entered into the corrective action
program for evaluation and resolution. The team reviewed a sample of system health reports,
self-assessments, audits, trending reports and metrics, and various other documents related to
the corrective action program.
Based on these reviews, the team concluded that the licensees corrective action program and
its other processes to identify and correct nuclear safety problems were adequate to support
nuclear safety. However, the team noted at times the licensee staff did not always use the
corrective action program for problems that were perceived as minor. The team also noted
several challenges in correcting adverse conditions in a timely manner. Further, the licensee
had several long-standing issues, which had been in the corrective action process for over a
year without resolution.
The licensee appropriately evaluated industry operating experience for relevance to the facility
and entered applicable items in the corrective action program. However, there was one
example where the licensee failed to enter an information notice into their corrective action
program for evaluation of a condition adverse to quality. The licensee used industry operating
experience when performing root cause and apparent cause evaluations. The licensee
performed effective quality assurance audits and self-assessments, as demonstrated by self-
identification of poor corrective action program performance and identification of ineffective
corrective actions.
Finally, the team determined that the station continued to maintain a safety-conscious work
environment. Employees felt free to raise nuclear safety concerns to the attention of
management without fear of retaliation.
                                              -2-                              Enclosure 2
 
A. NRC-Identified and Self-Revealing Findings
  Cornerstone: Initiating Events
      *  Green. The team identified a non-cited violation of 10 CFR Part 50, Appendix B,
        Criterion V, Instructions, Procedures, and Drawings, for a failure to follow
        Procedure EN-OP-115, Conduct of Operations. Specifically, the licensee failed
        to ensure that control room operators knew the status of equipment at all times.
        While interviewing the person responsible for tracking plant deficiencies, the
        inspectors discovered that the licensee had two separate governing procedures.
        These two instructions had different definitions for categories of plant deficiencies
        and different databases for tracking them. The inspectors then interviewed the
        on-shift operators in the control room and reviewed both databases. The
        inspectors identified several issues, including lack of knowledge by the control
        room operators about which procedure to use, failure to track deficiencies in both
        databases, and inadequate classification of deficiencies. The inspectors
        determined that in March 2010, the licensee changed their process for tracking
        deficiencies to be consistent with their fleet reporting process. However, the
        licensee did not revise the procedure and did not train all affected personnel on
        the new process. As a result, control room operators did not have a complete
        and accurate knowledge of all plant deficiencies. This finding was entered into
        the licensees corrective action program as Condition Report CR-WF3-2012-
        03732.
        The failure to ensure that operators were aware of the status of all plant
        equipment was a performance deficiency. The performance deficiency was more
        than minor because it was associated with the procedure quality attribute of the
        Initiating Events Cornerstone and affected the cornerstone objective to limit the
        likelihood of those events that upset plant stability and challenge critical safety
        functions during shutdown as well as power operations. Specifically, the licensee
        failed to implement a procedure designed to ensure operators were aware of
        deficiencies in the instrumentation, controls, and operation of nuclear plant
        systems. In accordance with NRC Inspection Manual Chapter 0609,
        Attachment 4, "Initial Characterization of Findings," the issue was determined to
        affect the Initiating Events Cornerstone. In accordance with NRC Inspection
        Manual Chapter 0609, Appendix A, The Significance Determination Process
        (SDP) for Findings at Power, the issue was determined to have very low safety
        significance (Green) because it did not cause a reactor trip and did not cause the
        loss of mitigation equipment relied upon to transition the plant from the onset of
        the trip to a stable shutdown condition. This finding had a cross-cutting aspect in
        the human performance area, work practices component, in that the licensee
        failed to define and effectively communicate expectations regarding procedural
        compliance, and personnel did not follow procedures [H.4.b] (Section 4OA2.5.d).
      *  Green. The inspectors identified a non-cited violation of 10 CFR Part 50,
        Appendix B, Criterion XVI, Corrective Actions, because the licensee failed to
        determine the cause of a significant condition adverse to quality and take
                                        -3-                              Enclosure 2
 
      corrective actions to preclude repetition. Specifically, the licensee failed to
      assure that the cause of the condition was determined and corrective action
      taken to preclude repetition related to a contractors non-compliance with site
      procedural requirements. The corrective actions include developing additional
      training and provisions to provide additional contractor oversight. This finding
      was entered into the licensees corrective action program as Condition Reports
      CR-WF3-2012-03769 and CR-WF3-2012-03772.
      The failure to determine the cause of a significant condition adverse to quality
      and take corrective action to preclude repetition was a performance deficiency.
      The performance deficiency was more than minor because if left uncorrected, it
      could lead to more significant consequences; therefore, it is a finding.
      Specifically, failure to determine the cause of a significant condition adverse to
      quality and take corrective action to prevent recurrence can result in recurrence
      of the condition. In accordance with NRC Inspection Manual Chapter 0609,
      Attachment 4, "Initial Characterization of Findings," the issue was determined to
      affect the Initiating Events Cornerstone. In accordance with NRC Inspection
      Manual Chapter 0609, Appendix A, The Significance Determination Process
      (SDP) for Findings at Power, the issue was determined to have very low safety
      significance (Green) because the finding did not cause a reactor trip and the loss
      of mitigation equipment relied upon to transition the plant from the onset of the
      trip to a stable shutdown condition. This finding had a cross-cutting aspect in the
      human performance, work practice component, in that the licensee failed to
      follow guidance in the root cause evaluation procedure when developing
      appropriate corrective actions to prevent repetition [H.4(b)] (Section 4OA2.5.e).
Cornerstone: Mitigating Systems
  *  Green. The team identified a Green non-cited violation of 10 CFR Part 50,
      Appendix B, Criterion V, Instructions, Procedures, and Drawings, for a failure to
      follow the Operability Determination Process. Specifically, the licensee failed to
      determine the operability of the emergency diesel generators immediately upon
      discovery without delay and in a controlled manner using the best information
      available in response to NRC Information Notice 2010-04. The licensee
      completed an evaluation of the information notice that indicated that Waterford 3
      was vulnerable and susceptible to the issue, but the licensee failed to issue a
      condition report as required by their procedure. The failure to initiate a condition
      report resulted in the licensees failure to perform an operability determination of
      the emergency diesel generators as required by, EN-OP-104, Operability
      Determination Process, Revision 6. In the evaluation, the licensee considered
      the fact that they had an Action Request in their system to add routine
      thermography inspections within the voltage regulator cabinets to their
      preventative maintenance program as being adequate. The action request was
      not completed when the inspection team reviewed the issue. The inspectors
      questioned whether there was an operability concern for the emergency diesel
      generators. The licensee recognized their failure to perform an operability
      determination. They performed a prompt operability determination based on no
                                      -4-                              Enclosure 2
 
  observed degradation in performance and declared the emergency diesel
  generators operable. In addition, they plan to conduct the thermography
  inspections during the next scheduled emergency diesel generator surveillance.
  This finding was entered into the licensees corrective action program as
  Condition Report CR-WF3-2012-03761.
  The failure to promptly perform an operability determination of the emergency
  diesel generators in response to NRC Information Notice 2010-04 was a
  performance deficiency. The performance deficiency was more than minor
  because it was associated with the equipment performance attribute of the
  Mitigating Systems Cornerstone and affected the cornerstone objective to ensure
  the availability, reliability, and capability of systems that respond to initiating
  events to prevent undesirable consequences. Specifically, the licensee failed to
  promptly determine the operability of the diesel generators after obtaining
  information of a potential condition adverse to quality. In accordance with NRC
  Inspection Manual Chapter 0609, Attachment 4, "Initial Characterization of
  Findings," the issue was determined to affect the Mitigating Systems
  Cornerstone. In accordance with NRC Inspection Manual Chapter 0609,
  Appendix A, The Significance Determination Process (SDP) for Findings at
  Power, the issue was determined to have very low safety significance (Green)
  because it was not a deficiency affecting the design or qualification of the
  system, it did not represent a loss of system or function, and it was a Technical
  Specification system, but did not represent an actual loss of function of a single
  train for greater than it allowed outage time. Specifically, the licensee performed
  an operability determination in response to the inspectors questions and
  determined the emergency diesel generators were operable based on a review of
  surveillance data and maintenance records. This finding had a cross-cutting
  aspect in the problem identification and resolution area, operating experience
  component, in that the licensee failed to systematically collect, evaluate, and
  communicate to affected internal stakeholders in a timely manner relevant
  internal and external operating experience [P.2.a] (Section 4OA2.5.a).
* Green. The team identified a non-cited violation of 10 CFR Part 50, Appendix B,
  Criterion XVI, Corrective Action, for the failure to take timely corrective action
  for a condition adverse to quality. Specifically, from May 2011, through
  August 2012, the licensee failed to restore a degraded condition, which included
  a corrective action to perform a new design analysis for the emergency
  feedwater pump AB after the removal of heat trace circuit 1-8C, despite having a
  reasonable amount of time to complete it. Currently, plant operators are required
  once per shift to perform temperature verifications of the heat trace to ensure
  condensation does not form in the steam supply pipe to the turbine driven pump
  and to maintain emergency feedwater pump AB in an operable but degraded
  status until the design analysis is complete. This finding was entered into the
  licensees corrective action program as Condition Report CR-WF3-2012-03754.
  The team determined that the failure to complete the corrective action of
  performing a new design analysis to determine if emergency feedwater pump AB
                                    -5-                              Enclosure 2
 
  required a design modification based on the analysis in a timely manner was a
  performance deficiency. The performance deficiency was more than minor
  because it affected the equipment performance attribute of the Mitigating
  Systems Cornerstone objective to ensure the availability, reliability, and capability
  of systems that respond to initiating events to prevent undesirable
  consequences. Specifically, failure to implement this corrective action could
  result in reduced reliability of the emergency feedwater pump AB. In accordance
  with NRC Inspection Manual Chapter 0609, Attachment 4, "Initial
  Characterization of Findings," the issue was determined to affect the Mitigating
  Systems Cornerstone. In accordance with NRC Inspection Manual Chapter
  0609, Appendix A, The Significance Determination Process (SDP) for Findings
  at Power, the issue was determined to have very low safety significance (Green)
  because it affected the design or qualification of mitigating systems, structures,
  and components; however, the systems, structures, and components maintained
  operability. This finding had a cross-cutting aspect in the human performance
  area, resources component, in that the licensee failed to minimize a long-
  standing equipment issue adequately to assure nuclear safety [H.2(a)] (Section
  4OA2.5.b).
* Green. The team identified a cited violation of 10 CFR Part 50, Appendix B,
  Criterion III, Design Control, for the failure to establish measures to assure that
  applicable regulatory requirements and the design basis as defined in
  10 CFR 50.2 are correctly translated into procedures. Specifically, the licensee
  has not determined a basis for the level at which flood control measures are
  initiated, two years after receiving a non-cited violation for the same deficiency.
  As an interim compensatory measure for a previous violation of inadequate
  technical specifications, the licensee modified their flooding procedure to include
  an action to start shutting flood control doors at a river level of 24 feet instead of
  27 feet. The licensee recognized the need to establish a basis for initiating these
  actions at 24 feet, and issued a corrective action to track completion. The
  licensee extended the due date several times and had not completed it by the
  arrival of the inspection team. The inspection team questioned why the licensee
  had not completed the calculation to justify their basis for their compensatory
  measures, noting that it had been over two years since the original violation was
  identified. The inspectors verified through walk-downs, procedure reviews, and
  historical data that the licensees use of 24 feet did not represent an immediate
  operability concern, and that the current river level was sufficiently low to allow
  time for the licensee to correct the deficiency. This finding was entered into the
  licensees corrective action program as condition report CR-WF3-2012-03752.
  The failure to complete the corrective action to establish a basis for flood control
  measures in a timely manner was a performance deficiency. The performance
  deficiency was more than minor because it was associated with the protection
  from external events attribute of the Mitigating Systems Cornerstone and affected
  the cornerstone objective to ensure the availability, reliability, and capability of
  systems that respond to initiating events to prevent undesirable consequences.
  Specifically, the licensee failed to verify through calculations or analysis that the
                                    -6-                              Enclosure 2
 
          actions taken to secure flood doors could be completed in time to protect safety-
          related equipment from flooding due to a levee failure. In accordance with
          NRC Inspection Manual Chapter 0609, Attachment 4, "Initial Characterization
          of Findings," the issue was determined to affect the Mitigating Systems
          Cornerstone. In accordance with NRC Inspection Manual Chapter 0609,
          Appendix A, The Significance Determination Process (SDP) for Findings at
          Power, the issue was determined to have very low safety significance (Green)
          because it did not involve the loss or degradation of equipment or function
          specifically designed to mitigate a seismic, flooding, or severe weather initiating
          event. Specifically, the inspectors confirmed that the licensee could reasonably
          ensure the flood control doors could perform their safety function. This finding
          had a cross-cutting aspect in the human performance area, resources
          component in that the licensee failed to maintain long term plant safety by
          maintenance of design margins and ensuring engineering backlogs low enough
          to support safety. [H.2.a] (Section 4OA2.5.c).
B. Licensee-Identified Violations
  A violation of very low safety significance, which was identified by the licensee, has been
  reviewed by the inspectors. Corrective actions taken by the licensee have been entered
  into the licensees corrective action program. This violation and associated corrective
  action tracking numbers are listed in Section 4OA7 of this report.
                                          -7-                              Enclosure 2
 
                                        REPORT DETAILS
4.  OTHER ACTIVITIES (OA)
4OA2 Problem Identification and Resolution (71152)
    The team based the following conclusions on the sample of corrective action documents
    that were initiated in the assessment period, which ranged from May 1, 2010, to the end
    of the on-site portion of this inspection on August 2, 2012.
.1  Assessment of the Corrective Action Program Effectiveness
    a.      Inspection Scope
            The team reviewed approximately 350 corrective action documents, including
            associated root cause, apparent cause, and direct cause evaluations, out of
            approximately 17,000 corrective action documents that were issued between
            May 1, 2010, and August 2, 2012, to determine if problems were being properly
            identified, characterized, and entered into the corrective action program for
            evaluation and resolution. The team reviewed a sample of system health
            reports, operability determinations, self-assessments, trending reports and
            metrics, and various other documents related to the corrective action program.
            The team evaluated the licensees efforts in establishing the scope of problems
            by reviewing selected logs, work requests, self-assessments results, audits,
            system health reports, action plans, and results from surveillance tests and
            preventive maintenance tasks. The team reviewed work requests and attended
            the licensees daily Condition Review Group, (which is the management review
            committee meeting to assess the reporting threshold, prioritization efforts, and
            significance determination process), as well as observing the interfaces with the
            operability assessment and work control processes when applicable. The teams
            review included verifying the licensee considered the full extent of cause and
            extent of condition for problems, as well as how the licensee assessed generic
            implications and previous occurrences. The team assessed the timeliness and
            effectiveness of corrective actions, completed or planned, and looked for
            additional examples of similar problems. The team conducted interviews with
            plant personnel to identify other processes that may exist where problems may
            be identified and addressed outside the corrective action program.
            The team also reviewed corrective action documents that addressed past
            NRC-identified violations to ensure that the corrective action addressed the
            issues as described in the inspection reports. The inspectors reviewed a sample
            of corrective actions closed to other corrective action documents to ensure that
            corrective actions were still appropriate and timely.
            The team considered risk insights from both the NRCs and Waterford Steam
            Electric Station, Unit 3s risk assessments to focus the sample selection and
            plant tours on risk significant systems and components. The team selected the
                                              -8-                            Enclosure 2
 
  component cooling water and auxiliary component cooling water systems as risk
  significant systems to review. The samples reviewed by the team focused on,
  but were not limited to, these systems. The team also expanded their review to
  include five years of evaluations involving the emergency feedwater system to
  determine whether problems were being effectively addressed. The team
  conducted a walk-down of these systems to assess whether problems were
  identified and entered into the corrective action program.
b. Assessments
  1. Assessment - Effectiveness of Problem Identification
  The team concluded in most cases that the licensee identified issues and
  adverse conditions and entered them into the corrective action program in
  accordance with the licensees corrective action program guidance and NRC
  requirements. The team determined that the licensee generally was identifying
  problems at a low threshold and entering them into the corrective action program.
  The team identified one condition adverse to quality that was not placed in the
  corrective action program. The licensee wrote approximately 17,000 condition
  reports during the two-year period of review. The team noted that this high rate
  of condition report generation is generally a sign of a healthy corrective action
  program. The following issues were noted by the team:
      *    Through the review of NRC information notices over the assessment
            period, the team identified that the licensee failed to enter one information
            notice applicable to Waterford Steam Electric Station, Unit 3s emergency
            diesel generator voltage regulators into their corrective action program.
            The team documented this as a Green non-cited violation in
            Section 4OA2.5.a of this report.
      *    The team identified that some main control room deficiencies, although
            identified by white identification tags, had not been entered into the
            licensees corrective action program. The team documented this as a
            Green non-cited violation in Section 4OA2.5.d of this report.
      *    The licensee self-identified a failure to initiate condition reports that
            resulted in missed operability assessments on two occasions when the
            emergency feedwater pump AB heat trace fell below the required
            temperature per the operating instruction. The team documented this as
            a licensee identified violation in Section 4OA7 of this report.
  2. Assessment - Effectiveness of Prioritization and Evaluation of Issues
  The team concluded that generally the licensee effectively prioritized and
  evaluated conditions adverse to quality. The team found that even with the high
  number of condition reports initiated on a daily basis, the licensees daily action
  review committee pre-screening and the management review committees
                                    -9-                                Enclosure 2
 
effectively assessed each condition adverse to quality. The following are issues
the team identified or reviewed during the inspection:
    *  The licensees extent of condition review for an incorrect preventive
        maintenance classification of a limit switch identified additional incorrect
        classifications. However, the team identified that the licensee failed to
        initiate a separate condition report to document these additional errors
        and, therefore, failed to ensure the testing requirements for each of the
        newly identified components were met until challenged by the team. This
        was documented in Condition Report CR-WF3-2012-03557.
    *  The team identified that the licensee performed an inadequate apparent
        cause evaluation of a failure of the security diesel generator. The
        evaluation identified one cause as being an incorrect maintenance
        classification. When the licensee found the component was properly
        classified in its preventative maintenance optimization program, the
        licensee did not revise their apparent cause. Instead, they determined
        other corrective actions to address security equipment issues.
    *  The team identified that the apparent cause evaluation for inservice
        testing failures of the main feed isolation valves was determined to be
        incorrect. The licensee first determined that the failure was the result of
        moisture intrusion in the hydraulic fluid. However, additional failures and
        a subsequent root cause analysis showed that the failure mechanism
        was actually interior varnishing. This was identified by review of external
        operating experience that was available, but missed during the initial
        apparent cause evaluation.
    *  The team identified a minor violation of 10 CFR Part 50, Appendix B,
        Criterion V, that is not subject to enforcement action in accordance with
        the NRCs Enforcement Policy. The licensee downgraded a Category A
        condition report to Category B without obtaining approval of the condition
        review group as required by Procedure EN-L1-102, Corrective Action
        Program. This was documented in Condition Report CR-WF3-2012-
        03325.
    *  The team reviewed roll up Condition Report CR-WF3-2011-07610, which
        identified that the quality of six previous causal analyses was inadequate.
    *  The team identified that the licensee categorized many conditions
        adverse to quality on the diesel fire pump as Category D. Although their
        process allowed this, they could have identified and corrected non-
        conforming trends in the diesel fire pumps more effectively with a higher
        prioritization. This was documented in Condition Report CR-WF3-2012-
        03747.
                                - 10 -                          Enclosure 2
 
    *  The team determined that the licensee categorized a problem with the
        steam generator feedwater pump B requiring manual operation as an
        Operator Burden when it could have met the definition of an Operator
        Workaround, which carried a higher level of prioritization in the licensee
        work planning process.
    *  The team reviewed a licensee failure to frequently and regularly review a
        degraded and nonconforming condition associated with the reactor
        coolant pump N-9000 stage seals as required by Procedure EN-OP-104,
        Operability Determination Process. This is an example of the licensee
        not thoroughly evaluating problems, such that the resolutions address
        causes and extent of conditions, as necessary. This was documented in
        NRC Inspection Report 05000382/2011002 as a Green non-cited
        violation.
The team reviewed a number of condition reports that involved operability
reviews to assess the quality, timeliness, and prioritization of operability
assessments. In general, both immediate and prompt operability assessments
reviewed were adequately completed in a timely manner.
3. Assessment - Effectiveness of Corrective Actions
Overall, the team concluded that the licensee generally developed appropriate
corrective actions to address problems. However, the team identified a number
of corrective actions associated with conditions adverse to quality that were not
completed in a timely manner:
    *  The team identified that the licensee failed to take timely corrective
        actions to correct a design basis analysis for the emergency feedwater
        pump AB after the removal of required heat trace on the steam supply
        piping. The team documented this as a Green non-cited violation in
        Section 4OA2.5.b of this report.
    *  The team identified that the licensee failed to take timely corrective
        actions to establish a basis through analysis for the initiation of flood
        control measures at a river level of 24 feet. The team documented this as
        a Green cited violation in Section 4OA2.5.c of this report.
    *  The team identified that the licensee failed to have a GMPO/Director
        approve a due date extension on a long-term corrective action from
        CR-WF3-2011-00887 (Corrective Action 13), which is not permitted by
        Procedure EN-LI-102, Corrective Action Program. This resulted in a
        minor violation of 10 CFR Part 50, Appendix B, Criterion V, that is not
        subject to enforcement action in accordance with NRCs Enforcement
        Policy. The corrective action was to complete an engineering analysis to
        determine the scope of modifications needed for the steam driven
                              - 11 -                            Enclosure 2
 
                emergency feedwater turbine steam supply piping. This was documented
                in Condition Report CR-WF3-2012-03461.
              *  The team identified a failure to complete a corrective action to validate
                data for work hours for security personnel. This resulted in a minor
                violation of 10 CFR 26.205.e that is not subject to enforcement action in
                accordance with the NRCs Enforcement Policy. This was documented in
                Condition Report CR-WF3-2012-03729.
              *  The team reviewed a licensee failure to take or perform effective
                corrective actions for boric acid leaks for the past seven years. This is an
                example of the licensees failure to effectively correct identified boric acid
                leaks in a timely manner. This was documented in NRC Inspection
                Report 05000382/2010006 as a Green non-cited violation.
.2 Assessment of the Use of Operating Experience
  a.    Inspection Scope
        The team examined the licensee's program for reviewing industry operating
        experience, including reviewing the governing procedure and self-assessments.
        The team reviewed a sample of 10 condition reports examining operating
        experience documents that had been issued during the assessment period to
        determine whether the licensee had appropriately evaluated the notification for
        relevance to the facility. The team then examined whether the licensee had
        entered those items into their corrective action program and assigned actions to
        address the issues. The team reviewed a sample of root cause evaluations and
        corrective action documents to verify whether the licensee had appropriately
        included industry-operating experience.
  b.    Assessment
        Overall, the team determined that the licensee was adequately evaluating
        industry operating experience for relevance to the facility, based on reviewing a
        sample of 10 condition reports examining industry operating experience. The
        licensee entered all but one applicable item in the corrective action program in
        accordance with station procedures. The team concluded that the licensee was
        evaluating industry operating experience when performing root cause and
        apparent cause evaluations. Both internal and external operating experiences
        were being incorporated into lessons learned for training and pre-job briefs. The
        following are issues the team identified or reviewed during the inspection:
              *  The team identified through the review of NRC information notices over
                the assessment period that the licensee had failed to enter one
                information notice applicable to Waterford 3 emergency diesel generator
                voltage regulators into their corrective action program. In response, the
                licensee did a complete audit of all NRC information notices issued during
                                        - 12 -                            Enclosure 2
 
                  the assessment period and found no other discrepancies. The team
                  documented this as a Green non-cited violation in Section 4OA2.5.a
                  of this report.
              *  The team reviewed three examples from this assessment period of the
                  licensees failure in the use of operating experience, resulting in the
                  licensee not implementing and institutionalizing operating experience
                  through changes to station processes, procedures, equipment, and
                  training programs.
                      o    The team reviewed a licensee failure to implement a preventative
                          maintenance activity to replace dry cooling tower process analog
                          control cards based on internal and industry-wide operating
                          experience that documented previous failures of process analog
                          control cards due to age-related degradation after 15 years. This
                          was documented in NRC Inspection Report 05000382/2011004 as
                          a Green non-cited violation.
                      o    The team reviewed a licensee failure to identify that varnish
                          deposits were causing the main feedwater isolation valve to fail its
                          inservice testing. This resulted from the licensees failure to use
                          relevant external operating experience to identify that other sites
                          experienced similar failures of feedwater isolation valves due to
                          varnish deposits on the interior surfaces. This was documented in
                          NRC Inspection Report 05000382/2011005 as a Green non-cited
                          violation.
                      o    The team reviewed a licensee failure to evaluate the internal
                          condition of the condensate and refueling water storage pool
                          structures through performance of appropriate preventative
                          maintenance after previous documented industry-wide operating
                          experience of concrete degradation due to boric acid. This was
                          documented in Inspection Report 05000382/2011003 as a Green
                          non-cited violation.
.3 Assessment of Self-Assessments and Audits
  a.    Inspection Scope
        The team reviewed a sample size of 22 licensee self-assessments, surveillances,
        and audits to assess whether the licensee was regularly identifying performance
        trends and effectively addressing them. The team reviewed audit reports to
        assess the effectiveness of assessments in specific areas. The team evaluated
        the use of self- and third party assessments, the role of the quality assurance
        department, and the role of the performance improvement group related to
        licensee performance. The specific self-assessment documents reviewed are
        listed in the Attachment.
                                          - 13 -                          Enclosure 2
 
  b.    Assessment
        The team concluded that the licensee had an effective self-assessment process.
        Licensee management was involved with developing tactical self-assessments.
        The team determined that self-assessments were self-critical and thorough
        enough to identify deficiencies. The following are issues the team reviewed
        during the inspection:
            *  The team reviewed a licensee self-assessment of plant status and
                configuration control performed in March 2012. This self-assessment
                was an opportunity for the site to identify and address the issues
                associated with control room deficiencies documented in
                Section 4OA2.5.d of this report, but the assessment did not discuss them.
            *  The team reviewed the licensees failure to perform an adequate risk
                assessment associated with the maintenance window for the turbine
                driven emergency feedwater pump. This is an example of the licensees
                failure to use independent and self-assessments because the licensee
                performed a probabilistic risk assessment model update in April 2009, but
                failed to identify an assumption crediting operator actions that were not in
                procedures. This was documented in NRC Inspection
                Report 05000382/2011007 as a Green non-cited violation.
.4 Assessment of Safety-Conscious Work Environment
  a.    Inspection Scope
        The inspection team conducted individual interviews with over 30 individuals from
        a cross-section of functional organizations: engineering, operations,
        maintenance, quality assurance, radiation protection, chemistry, security officers,
        and contract personnel. Both supervisory and non-supervisory personnel were
        included in these interviews. The team conducted these interviews to assess
        whether conditions existed that would challenge the establishment of a safety-
        conscious work environment (SCWE) at Waterford 3. The team also interviewed
        the Waterford 3 employee concerns program manager and reviewed the last two
        safety culture self-assessment documents.
  b.    Assessment
        Overall, the team concluded that a safety-conscious work environment exists at
        Waterford Steam Electric Station, Unit 3. Employees demonstrated familiarity
        with the various avenues available to raise safety concerns. They appeared
        comfortable with submitting all nuclear safety issues.
        The team noted a potential vulnerability in the licensees safety-conscious work
        environment from discussions with plant personnel. There was a perception
        among some members of the plant staff that management may use the condition
                                        - 14 -                          Enclosure 2
 
              report process to discipline workers when personnel errors were documented in
              the condition reports. Additionally, some personnel stated that they did not write
              condition reports, but rather they passed the comments along to supervisors who
              would enter them into the corrective action program.
              Overall, most individuals were familiar with the employee concerns program and
              its location on site. There was visibility of the program throughout the site. Many
              of the individuals interviewed had knowledge of the employee concerns
              manager; however, no one interviewed indicated having direct interactions with
              the employee concerns manger during the inspection period. Personnel
              understood and were confident in the confidentiality of the program.
              Site personnel have received initial and annual refresher training, which provided
              instruction on safety-conscious work environment policies. Many of the
              individuals interviewed were familiar with this training and with the overall
              message in the training. However, not everyone was familiar with the details of
              the policy. None of the individuals interviewed cited any examples of
              harassment, intimidation, retaliation or discrimination, or any negative reactions
              from management when individuals raised nuclear safety concerns. Finally,
              individuals indicated that if they were to believe unsafe conditions existed, they
              would feel comfortable stopping work without fear of retaliation, even if such
              actions would prolong an outage or extend a planned schedule.
.5    Specific Issues Identified During This Inspection
  a. Failure to Promptly Determine the Operability of the Emergency Diesel Generators
      Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,
      Appendix B, Criterion V, Instructions, Procedures, and Drawings, for a failure to follow
      Procedure EN-OP-104, Operability Determination Process. Specifically, the licensee
      failed to determine the operability of the emergency diesel generators immediately upon
      discovery without delay and in a controlled manner using the best information available
      in response to NRC Information Notice 2010-04.
      Description. The team reviewed the licensees corrective actions taken in response to
      an NRC Information Notice. On February 26, 2010, the NRC issued Information
      Notice 2010-04, Diesel Generator Voltage Regulation System Component [Failure] Due
      to Latent Manufacturing Defect. This information notice describes the failure of a linear
      power reactor in an emergency diesel generator voltage regulation system at a plant
      where the licensees preventive maintenance program did not address the emergency
      diesel generator excitation system magnetic components.
      The licensee completed an evaluation of the information notice per Procedure EN-
      OE-100, Operating Experience Program, on July 1, 2010. This evaluation indicated
      that Waterford 3 was vulnerable and susceptible to the issue, but the licensee failed to
      issue a condition report as required by their procedure. The failure to initiate a condition
      report resulted in the licensees failure to perform an operability determination of the
                                                - 15 -                          Enclosure 2
 
emergency diesel generators as required by Procedure EN-OP-104, Operability
Determination Process, Revision 6.
In the evaluation, the licensee considered the fact that they had an Action Request in
their system that addressed a similar concern to be an acceptable response to this
information notice. Action Request 079684 was initiated on December 10, 2009, to
address recommendations from an INPO assistance visit in 2007 and it included an
action to add routine thermography inspections within the voltage regulator cabinets to
their preventative maintenance program. The Entergy Nuclear Corporate Operating
Experience group also reviewed this information notice on March 4, 2010. In response,
they issued a specific action through their operating experience database to evaluate the
information notice to each Entergy site. However, they failed to issue one to
Waterford 3.
The licensee started routing Action Request 079684 for approval, but they stopped on
March 15, 2010. The licensee attributed this to an incomplete turnover by departing
personnel. No other approval actions were taken until April 16, 2012, when the request
was routed to the next person in the approval process. Again, no further action was
taken, and the action request was not completed when the inspection team reviewed the
issue.
The inspectors questioned why there was no condition report generated and why the
action request had not been completed more than two years after issuance. In
particular, the inspectors questioned whether there was an operability concern for the
emergency diesel generators. The licensee recognized their failure to issue a condition
report and perform an operability determination. They performed a prompt operability
determination based on operating data, work history, and no observed degradation in
performance, and declared the emergency diesel generators operable. In addition, they
plan to conduct the thermography during the next scheduled emergency diesel
generator surveillance.
The licensee initiated CR-WF3-2012-00596 and CR-WF3-2012-03761 to address the
issue. They also initiated CR-HQN-2012-00857 to address the failure of the corporate
organization to include Waterford 3 in their site-specific requests.
Analysis. The failure to promptly perform an operability determination of the emergency
diesel generators in response to NRC Information Notice 2010-04 was a performance
deficiency. The performance deficiency was more than minor because it was associated
with the equipment performance attribute of the Mitigating Systems Cornerstone and
affected the cornerstone objective to ensure the availability, reliability, and capability of
systems that respond to initiating events to prevent undesirable consequences.
Specifically, the licensee failed to promptly determine the operability of the diesel
generators after obtaining information of a potential condition adverse to quality. In
accordance with NRC Inspection Manual Chapter 0609, Attachment 4, "Initial
Characterization of Findings," the issue was determined to affect the Mitigating Systems
Cornerstone. In accordance with NRC Inspection Manual Chapter 0609, Appendix A,
The Significance Determination Process (SDP) for Findings at Power, the issue was
                                        - 16 -                            Enclosure 2
 
  determined to have very low safety significance (Green) because it was not a deficiency
  affecting the design or qualification of the system, it did not represent a loss of system or
  function, and it was a Technical Specification system but did not represent an actual loss
  of function of a single train for greater than it allowed outage time. Specifically, the
  licensee performed an operability determination in response to the inspectors questions
  and determined the emergency diesel generators were operable based on a review of
  surveillance data and maintenance records. This finding had a cross-cutting aspect in
  the problem identification and resolution area, operating experience component, in that
  the licensee failed to systematically collect, evaluate, and communicate to affected
  internal stakeholders in a timely manner relevant internal and external operating
  experience [P.2.a].
  Enforcement. Title 10 of the Code of Federal Regulations Part 50, Appendix B,
  Criterion V, Instructions, Procedures, and Drawings, states, in part, that activities
  affecting quality shall be prescribed by documented instructions, procedures, or
  drawings of a type appropriate to the circumstances and shall be accomplished in
  accordance with these instructions, procedures, or drawings. Licensee Procedure
  EN-OP-104, Operability Determination Process, Revision 6, Section 5.1 step 13
  required that an operability should be determined immediately upon discovery without
  delay and in a controlled manner using the best information available. Contrary to this
  requirement, from July 1, 2010, to July 25, 2012, the licensee failed to accomplish an
  activity affecting quality prescribed by documented instructions. Specifically, the
  licensee failed to determine the operability of the emergency diesel generators as
  required by Licensee Procedure EN-OP-104 in response to NRC Information
  Notice 2010-04. The licensee immediately determined the operability of the emergency
  diesel generators based on operating data and work history, and they established a
  reasonable basis for operability. This violation is being treated as an NCV, consistent
  with Section 2.3.2 of the Enforcement Policy, because it was of very low safety
  significance (Green) with no actual or potential safety consequences and was entered
  into the licensees corrective action program as Condition Report CR-WF3-2012-03761
  to address recurrence. (NCV 05000382/2012008-01, Failure to Promptly Determine the
  Operability of the Emergency Diesel Generators)
b. Failure to Take Corrective Action Associated with the Emergency Feedwater Pump AB
  Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,
  Appendix B, Criterion XVI, Corrective Action, for the failure to take timely corrective
  action for a condition adverse to quality. Specifically, the licensee failed to restore a
  degraded condition, which included a corrective action to perform a new design analysis
  for the emergency feedwater pump AB after the removal of heat trace circuit 1-8C
  despite having a reasonable amount of time to complete it.
  Description. The team performed an in-depth review of corrective actions associated
  with the emergency feedwater system. The turbine driven emergency feedwater pump
  AB has steam piping that is maintained at a high temperature with a heat trace to
  prevent excessive condensation from developing, which could reduce the reliability of
  the pump to perform its design function. The licensee removed heat trace circuit 1-8C
                                          - 17 -                            Enclosure 2
 
from a horizontal section of steam piping because the heat trace was not maintaining the
piping above the required setpoint. In May 2011, the licensee determined that
emergency feedwater pump AB was operable but degraded. A corrective action was
initiated to perform a design analysis using RELAP to determine what modifications
needed to be performed on the system to return the system to a fully operable status.
The team identified that the licensee extended the due date twice for the corrective
action, first from February 23 to June 15, 2012, and then from June 15 until
October 12, 2012. The last extension was approved due to lack of engineering
resources resulting from other activities placed at a higher priority by Waterford 3
management. The team determined that from May 2011 to August 2012, a corrective
action to perform a design analysis for the long-standing equipment issue of determining
whether or not a plant modification is needed to maintain the system operable had not
been performed in a timely manner. Currently, plant operators are required once per
shift to perform temperature verifications of the heat trace to ensure condensation does
not form in the steam supply pipe to the turbine driven pump and maintain emergency
feedwater pump AB in an operable, but degraded, status until the design analysis is
complete. The licensee has entered the concern into their corrective action program as
Condition Report CR-WF3-2012-03754.
Analysis. The team determined that the failure to complete the corrective action of
performing a new design analysis to determine if emergency feedwater pump AB
required a design modification based on the analysis in a timely manner was a
performance deficiency. The performance deficiency was more than minor because it
affected the equipment performance attribute of the Mitigating Systems Cornerstone
objective to ensure the availability, reliability, and capability of systems that respond to
initiating events to prevent undesirable consequences. Specifically, failure to implement
this corrective action could result in reduced reliability of the emergency feedwater pump
AB. In accordance with NRC Inspection Manual Chapter 0609, Attachment 4, "Initial
Characterization of Findings," the issue was determined to affect the Mitigating Systems
Cornerstone. In accordance with NRC Inspection Manual Chapter 0609, Appendix A,
The Significance Determination Process (SDP) for Findings at Power, the issue was
determined to have very low safety significance (Green) because it affected the design
or qualification of mitigating systems, structures, and components; however, the
systems, structures, and components maintained operability. This finding had a cross-
cutting aspect in the human performance area, resources component, in that the
licensee failed to minimize a long-standing equipment issue adequately to assure
nuclear safety [H.2(a)].
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,
states, in part, that measures be established to assure that conditions adverse to quality,
such as failures, malfunction, deficiencies, deviations and non-conformances are
promptly identified and corrected. Contrary to this requirement, from May 2011 through
August 2012, the licensee failed to assure that measures were established to assure
that a condition adverse to quality was promptly corrected. Specifically, the licensee
failed to take prompt corrective action to restore a degraded condition by not performing
                                        - 18 -                            Enclosure 2
 
  a design analysis for emergency feedwater pump AB after heat trace circuit 1-8C was
  removed. Consequently, plant operators are required once per shift to perform
  temperature verifications of the heat trace to ensure condensation does not form in the
  steam supply pipe to the turbine driven pump and maintain emergency feedwater pump
  AB in an operable, but degraded, status until the design analysis is complete. This
  violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement
  Policy because it was of very low safety significance (Green) with no actual or potential
  safety consequence and was entered into the licensees corrective action program as
  CR-WF3-2012-03754 to address recurrence. (NCV 05000382/2012008-02, Failure to
  Take Corrective Action Associated with Emergency Feedwater Pump AB)
c. Failure to Take Timely Corrective Action to Establish a Basis for Flood Control Measures
  Introduction. The team identified a Green cited violation of 10 CFR Part 50, Appendix B,
  Criterion III, Design Control, for the failure to establish measures to assure that
  applicable regulatory requirements and the design basis as defined in 10 CFR 50.2 are
  correctly translated into procedures. Specifically, the licensee has not determined a
  basis for the level at which flood control measures are initiated, two years after receiving
  a non-cited violation for the same deficiency.
  Description. The team reviewed the licensees corrective actions taken in response to a
  non-cited violation from 2010 documented as NCV 2010006-02, Non-conservative
  Technical Specification 3.7.5 Action Statement. The licensee entered this violation into
  their corrective action program under CR-WF3-2010-03232 on May 24, 2010. The
  licensee determined that Technical Specification 3.7.5 Flood Protection was not
  required to be included in their technical specifications and submitted an amendment to
  move it to the Technical Requirements Manual. As an interim compensatory measure,
  the licensee modified their Procedure OP-901-521, Severe Weather and Flooding to
  include an action to start shutting flood control doors at a river level of 24 feet instead of
  27 feet.
  The required actions included verifying that all flood control penetrations below a level of
  30 feet were shut within 12 hours before the river was projected to reach 27 feet. There
  are seven flood control doors of varying sizes that are required to be shut and two valves
  that are required to be locked shut. Five of these doors and both valves are normally
  shut during power operations, but may be open during outages. Most of them require
  entry into the Radiologically Controlled Area and one requires entry into a locked room
  for access.
  The licensee recognized the need to establish a basis for initiating these actions at
  24 feet, and issued Corrective Action 18 (CA-18) in CR-WF3-2010-03232 on
  March 10, 2011, to formally evaluate and document whether 24 feet was an acceptable
  river level elevation at which to initiate flood control measures. The CA-18 due date was
  extended twice and on February 24, 2012, they determined that the methodology they
  intended to use was not acceptable. CA-18 was closed to Corrective Action 23 (CA-23)
  which directed the licensee to issue an engineering change using the methodology used
                                            - 19 -                            Enclosure 2
 
in Waterford 3 UFSAR Section 2.4.3.7. The due date for CA-23 was itself extended to
September 30, 2012.
The inspection team questioned why the licensee had not completed the calculation
to justify their basis for their compensatory measures, noting that it had been over
two years since the original violation was identified. The licensee initiated
CR-WF3-2012-03752 to address this concern. The inspectors verified through
walk-downs, procedure reviews, and historical data that the licensees use of 24 feet
did not represent an immediate operability concern and that the current river level was
sufficiently low to allow time for the licensee to correct the deficiency.
Analysis. The failure to complete the corrective action to establish a basis for flood
control measures in a timely manner was a performance deficiency. The performance
deficiency was more than minor because it was associated with the protection from
external events attribute of the Mitigating Systems Cornerstone and affected the
cornerstone objective to ensure the availability, reliability, and capability of systems that
respond to initiating events to prevent undesirable consequences. Specifically, the
licensee failed to verify through calculations or analysis that the actions taken to secure
flood doors could be completed in time to protect safety-related equipment from flooding
due to a levee failure. In accordance with NRC Inspection Manual Chapter 0609,
Attachment 4, "Initial Characterization of Findings," the issue was determined to affect
the Mitigating Systems Cornerstone. In accordance with NRC Inspection Manual
Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings
at Power, the issue was determined to have very low safety significance (Green)
because it did not involve the loss or degradation of equipment or function specifically
designed to mitigate a seismic, flooding, or severe weather initiating event. Specifically,
the inspectors confirmed that the licensee could reasonably ensure the flood control
doors could perform their safety function. This finding had a cross-cutting aspect in the
human performance area, resources component in that the licensee failed to maintain
long term plant safety by maintenance of design margins and ensuring engineering
backlogs low enough to support safety [H.2.a].
Enforcement. Title 10 of the Code of Federal Regulations Part 50, Appendix B,
Criterion III, Design Control, states, in part, that measures shall be established to
assure that applicable regulatory requirements and the design basis, as defined in
10 CFR 50.2, are correctly translated into specifications, procedures and instructions.
Contrary to the above, from March 10, 2011, to August 2, 2012, the licensee failed to
establish measures to assure that applicable regulatory requirements and the design
basis, as defined in 10 CFR 50.2, were correctly translated into specifications,
procedures and instructions. Specifically, the licensee had not established a design
basis to determine the river level at which flood control measures were to be initiated for
closing the water tight doors, as required in Procedure OP-901-521, Severe Weather
and Flooding. The licensee demonstrated sufficient safety margin based on historical
data and current river levels to provide assurance that this is not an immediate safety
concern. Due to the licensees failure to restore compliance within a reasonable time
                                        - 20 -                            Enclosure 2
 
  following previous NCV 05000382/2010006-02, this violation is being cited as a Notice of
  Violation consistent with Section 2.3.2 of the NRC Enforcement Policy. This is a
  violation of 10 CFR 50, Appendix B, Criterion III. A Notice of Violation is attached.
  (VIO 05000382/2012008-03, Failure to Take Timely Corrective Action to Establish a
  Basis for Flood Control Measures)
d. Failure to Ensure Operator Knowledge of Equipment Status
  Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,
  Appendix B, Criterion V, Instructions, Procedures, and Drawings, for a failure to follow
  Procedure EN-OP-115, Conduct of Operations. Specifically, the licensee failed to
  ensure that control room operators knew the status of equipment at all times.
  Description. The team reviewed how the licensee was addressing deficiencies in plant
  instrumentation, controls, and equipment that impacted the ability of operators to
  properly operate the plant. This included a review of the licensees program to identify,
  compensate for, and correct these plant deficiencies and a walk-down of the control
  room.
  While interviewing the person responsible for tracking plant deficiencies, the inspectors
  discovered that the licensee had two separate governing procedures. The licensee used
  the Entergy Fleet Administrative Procedure EN-FAP-OP-006, Operator Aggregate
  Impact Index Performance Indicator, to track several categories of plant deficiencies in
  a standardized spreadsheet. The licensee also had the local departmental Operating
  Instruction OI-002-000, Annunciator, Control Room Instrumentation and Workarounds
  Status Control. This instruction had different definitions for categories of plant
  deficiencies and directed the use of a different database.
  The inspectors then interviewed the on shift operators in the control room and reviewed
  both databases. The inspectors identified several issues:
          *  The person responsible for tracking plant deficiencies was only using the fleet
              administrative procedure and was unaware of the operating instruction.
          *  On one shift, the shift technical advisor believed the fleet administrative
              procedure was being used and was not aware of the operating instruction,
              while the control room supervisor believed the operating instruction was
              being used and was not aware of the fleet administrative procedure.
          *  The database required by the operating instruction had not been maintained
              for two years.
          *  The operating instruction did not have a category for Operator Burdens;
              however, the shift crew differentiated between Operator Workarounds and
              Operator Burdens. In most cases, they chose the less conservative
              designation of Operator Burden.
                                          - 21 -                            Enclosure 2
 
        *  The fleet administrative procedure was intended for fleet performance
            reporting, not plant deficiency control. It does not direct any actions to
            address and correct plant deficiencies.
        *  The operating instruction subcategorizes Workarounds by scheduling of
            resources rather than by risk significance or impact to operators. The fleet
            administrative procedure does not subcategorize Operator Workarounds or
            Operator Burdens, but the licensee carried over this practice to the fleet
            administrative procedure spreadsheet. This could lead to improper
            prioritization of corrective actions.
        *  The operating instruction directs identification of plant deficiencies through a
            review of work requests, but it does not require a review of condition reports.
        *  Some plant deficiencies were not entered into either database.
        *  Operators were using the same tags for Control Room Deficiencies and
            informal operator notes. These notes are not controlled by either procedure.
        *  A list of plant deficiencies was not immediately available to control room
            operators.
The inspectors determined that when the fleet administrative procedure was issued in
March 2010, the licensee changed their process for tracking deficiencies. The licensee
Procedure W2.109, Procedure Development, Review & Approval, is safety-related and
requires implementation and maintenance of procedures and departmental instructions.
This procedure prescribes a process for approving and revising procedures and
instructions and conducting necessary training. When the licensee began tracking plant
deficiencies per the fleet administrative procedure, the licensee did not revise the
operating instruction to conform to the new process, and the licensee did not train all
affected personnel on the new process. As a result, the operators did not maintain a
consistent accurate list and were not aware of all plant deficiencies, and therefore were
not aware of the status of all plant equipment. This was not in accordance with
Procedure EN-OP-115, Conduct of Operations, Revision 9, Section 5.13 step 1, which
states that the status of plant equipment is known at all times by plant operators.
The licensee initiated CR-WF3-2012-03732 to address the issue. The licensee will
revise the operating instruction to address the process issues and make the intended
changes.
Analysis. The failure to ensure that operators were aware of the status of all plant
equipment was a performance deficiency. The performance deficiency was more than
minor because it was associated with the procedure quality attribute of the Initiating
Events Cornerstone and affected the cornerstone objective to limit the likelihood of those
events that upset plant stability and challenge critical safety functions during shutdown
as well as power operations. Specifically, the licensee failed to implement a procedure
designed to ensure operators were aware of deficiencies in the instrumentation, controls,
                                        - 22 -                            Enclosure 2
 
  and operation of nuclear plant systems. In accordance with NRC Inspection Manual
  Chapter 0609, Attachment 4, "Initial Characterization of Findings," the issue was
  determined to affect the Initiating Events Cornerstone. In accordance with NRC
  Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process
  (SDP) for Findings at Power, the issue was determined to have very low safety
  significance (Green) because it did not cause a reactor trip and the loss of mitigation
  equipment relied upon to transition the plant from the onset of the trip to a stable
  shutdown condition. This finding had a cross-cutting aspect in the human performance
  area, work practices component, in that the licensee failed to define and effectively
  communicate expectations regarding procedural compliance, and personnel did not
  follow procedures [H.4.b].
  Enforcement. Title 10 of the Code of Federal Regulations Part 50, Appendix B,
  Criterion V, Instructions, Procedures, and Drawings, states, in part, that activities
  affecting quality shall be prescribed by documented instructions, procedures, or
  drawings of a type appropriate to the circumstance and shall be accomplished in
  accordance with these instructions, procedures, or drawings. Procedure EN-OP-115,
  Conduct of Operations, Revision 9, Section 5.13, step 1, states that the status of plant
  equipment is known at all times by plant operators. Contrary to this requirement, from
  March 2, 2010, to August 1, 2012, the licensee failed to accomplish an activity affecting
  quality in accordance with the documented instructions appropriate to the circumstance.
  Specifically, the licensee failed to ensure operators knew the status of plant equipment
  at all times in accordance with Licensee Procedure EN-OP-115, Conduct of
  Operations. The licensee has a corrective action to revise their operating instruction for
  tracking plant deficiencies, and none of the current plant deficiencies represents an
  immediate safety concern. This violation is being treated as an NCV, consistent with
  Section 2.3.2 of the Enforcement Policy, because it was of very low safety significance
  (Green) with no actual or potential safety consequences and was entered into the
  licensees corrective action program as CR-WF3-2012-03732 to address recurrence.
  (NCV 05000382/2012008-04, Failure to Ensure Operator Knowledge of Equipment
  Status)
e. Failure to Develop Effective Corrective Actions to Preclude Repetition
  Introduction. The inspectors identified a non-cited violation of 10 CFR Part 50,
  Appendix B, Criterion XVI, Corrective Actions, because the licensee failed to determine
  the cause of a significant condition adverse to quality and take corrective actions to
  prevent recurrence. Specifically, the licensee failed to assure that the cause of the
  condition was determined and corrective action taken to preclude repetition associated
  with a contractors non-compliance with site procedural requirements.
  Description. During refuel outage 16 in 2009, contract instrumentation and control
  technicians performed a functional test on a feedwater heater level switch according to
  work order instructions. Following restoration, a plant transient occurred because a
  valve was out of position (CR-WF3-2009-7420). The licensee determined that the event
  constituted a significant condition adverse to quality in accordance with guidance from
  Procedure EN-LI-102, Corrective Action Process. During the valve manipulation, the
                                          - 23 -                          Enclosure 2
 
work instructions called for concurrent verification. However the licensees root cause
analysis determined that the contract workers failed to perform concurrent verification as
required by the procedure (NCV 2011003-04). The contract workers knew the
procedural requirement, but they behaved inappropriately when they chose not to follow
the instructions. The licensees root cause analysis did not determine why the contract
workers chose not to follow the procedure. The licensees corrective action to preclude
repetition (CAPR) of this significant condition adverse to quality (SCAQ) was to release
the contract workers for not following the procedure and prohibit them from future work
at Entergy sites. No actions to preclude repetition that addressed the underlying cause
of the failure to perform concurrent verification were taken. The team identified that
despite guidance provided in Procedure EN-LI-118, Attachment 9.9, Root Cause
Evaluation Process, which states that discipline of individuals is not an appropriate
CAPR, disciplinary action was the only CAPR identified in the root cause for
CR-WF3-2009-07420 performed on January 7, 2010.
The failure to determine the cause of a significant condition adverse to quality and take
corrective action to preclude repetition had no actual consequences on nuclear plant
safety. However, the failure to determine the cause of the condition adverse to quality
and take corrective action to preclude repetition from an ineffective CAPR has the ability
to lead to more significant safety consequences. The licensee documented this violation
in Condition Reports CR-WF3-2012-03769 and CR-WF3-2012-03772. The corrective
actions include developing additional training and provisions to provide additional
contractor oversight.
Analysis. The failure to determine the cause of a significant condition adverse to quality
and take corrective action to preclude repetition was a performance deficiency. The
performance deficiency was more than minor because if left uncorrected, it could lead to
more significant consequences, therefore it is a finding. Specifically, failure to determine
the cause of a significant condition adverse to qualify and take corrective action to
prevent recurrence can result in recurrence of the condition. In accordance with NRC
Inspection Manual Chapter 0609, Attachment 4, "Initial Characterization of Findings," the
issue was determined to affect the Initiating Events Cornerstone. In accordance with
NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination
Process (SDP) for Findings at Power, the issue was determined to have very low safety
significance (Green) because the finding did not cause a reactor trip and the loss of
mitigation equipment relied upon to transition the plant from the onset of the trip to a
stable shutdown condition. This finding had a cross-cutting aspect in the human
performance, work practice component, in that the licensee failed to follow guidance in
the root cause evaluation procedure when developing appropriate corrective actions to
prevent repetition [H.4(b)].
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,
states, in part, in the case of significant conditions adverse to quality, the measures shall
assure that the cause of the condition is determined and corrective action taken to
preclude repetition. Contrary to this requirement, on January 7, 2010, for a significant
condition adverse to quality, the licensee failed to take measures to assure that the
cause of the condition was determined and corrective actions taken to preclude
                                        - 24 -                            Enclosure 2
 
        repetition. Specifically, the licensee did not determine the underlying cause of the failure
        of the site contract workers to comply with licensees procedural requirements nor were
        corrective actions taken to preclude repetition of the condition. The licensees corrective
        actions to address this problem include developing additional training and provisions to
        provide additional contractor oversight. This violation is being treated as an NCV,
        consistent with Section 2.3.2 of the Enforcement Policy because it was of very low safety
        significance (Green) with no actual or potential safety consequence and was entered
        into the licensees corrective action program as CR-WF3-2012-03769 and
        CR-WF3-2012-03772 to address recurrence. (NCV 05000382/2012008-05, Failure to
        Develop Effective Corrective Actions to Preclude Repetition)
4OA6 Meetings
Exit Meeting Summary
On August 2, 2012, the team presented the inspection results to Keith Nichols, Director of
Engineering, and other members of the licensee staff. The licensee acknowledged the issues
presented. The inspector asked the licensee whether any materials examined during the
inspection should be considered proprietary. No proprietary information was identified.
On August 23, 2012, the team exited with the revised characterization of the inspection results
to William McKinney, Acting Director Nuclear Safety and Assurance, and other members of the
licensee staff. The licensee acknowledged the issues presented.
On September 24, 2012, the team exited with the revised characterization of the inspection
results to Keith Nichols, Director of Engineering, and other members of the licensee staff. The
licensee acknowledged the issues presented.
4OA7 Licensee-Identified Violations
The following violation of very low safety significance (Green) was identified by the licensee
and is a violation of NRC requirements, which meets the criteria of Section VI of the
NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.
    *    Title 10 of the Code of Federal Regulations Part 50, Appendix B, Criterion V,
        Instructions, Procedures, and Drawings, states, in part, that activities affecting quality
        shall be prescribed by documented instructions, procedures, or drawings and shall be
        accomplished in accordance with these instructions, procedures, or drawings. Contrary
        to this requirement, on May 10 and May 12, 2011, the licensee failed to accomplish an
        activity affecting quality as prescribed by the documented procedure. Specifically, the
        licensee failed to perform operability reviews when heat trace circuit 1-8C fell below the
        operating instruction temperature on the steam supply piping to the emergency
        feedwater pump in accordance with Procedure EN-OP-104, Operability Determination
        Process. The team determined that this finding was of very low safety significance
        (Green) because it affected the design or qualification of a mitigating system structure
        component; however, the system structure component maintained its operability.
                                                - 25 -                          Enclosure 2
 
    The emergency feed water pump AB was declared inoperable on May 14, 2011;
    however, subsequent evaluation declared the pump operable but degraded.
    This was documented in the licensees corrective action program as Condition
    Reports CR-WF3-2011-03599 and CR-WF3-2011-03600.
ATTACHMENTS:      SUPPLEMENTAL INFORMATION
                  INFORMATION REQUEST
                                        - 26 -                          Enclosure 2
 
                                SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
S. Adams, Planning Scheduling and Outage Manger
J. Bourgeois, Acting Chemistry Manager
E. Brauner, Supervision of System Engineering
K. Cook, General Manager, Plant Operations
G. Fey, Emergency Planning Manager
S. Fontenot, Acting Corrective Actions and Assessment Manager
R. Gilmore, Engineering and Components Manager
J. Gumnick, Radiation Protection Manager
D. Jacobs, Site Vice President, Operations
J. Jarrell, Assistant Operations Shift Manager
B. Lanka, Manager, System Engineering Manager
B. Lindsey, Maintenance Manager
M. Mason, Acting Licensing Manager
W. McKinney, Acting Director Nuclear Safety and Assurance
K. Nichols, Director of Engineering
R. Porter, Design Engineering Manager
D. Rieder, Quality Assurance Supervisor
K. Rockwood, Acting Technical Training Supervisor
T. Sanders, Security Superintendant
P. Stanton, Design Engineering Supervisor
NRC Personnel
R. Kumana, Project Engineer
R. Smith, Team Leader/Senior Resident Inspector
D. Overland, Resident Inspector
M. Young, Reactor Inspector
                                            A1-1            Attachment 1
 
                LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
05000382/2012008-03 VIO    Failure to Take Timely Corrective Action to Establish a Basis for
                          Flood Control Measures (Section 4OA2.5.c)
Opened and Closed
05000382/2012008-01 NCV Failure to Promptly Determine the Operability of the Emergency
                          Diesel Generators (Section 4OA2.5.a)
05000382/2012008-02 NCV Failure to Take Corrective Action Associated with Emergency
                          Feedwater Pump AB (Section 4OA2.5.b)
05000382/2012008-04 NCV Failure to Ensure Operator Knowledge of Equipment Status
                          (Section 4OA2.5.d)
05000382/2012008-05 NCV Failure to Develop Effective Corrective Actions to Preclude
                          Repetition (Section 4OA2.5.e)
                                        A1-2                            Attachment 1
 
                LIST OF DOCUMENTS REVIEWED
PROCEDURES
NUMBER                                TITLE                          REVISION
EN-LI-104  Self-Assessment and Benchmark Process                          8
EN-LI-102  Corrective Action Process                                      19
EN-LI-118  Root Cause Evaluation Process                                  17
EN-LI-119  Apparent Cause Evaluation (ACE) Process                        15
EN-OP-104  Operability Determination Process                              6
EN-QV-100  Conduct of Nuclear Oversight                                    7
EN-QV-102  Quality Control Inspection Program                              1
EN-QV-108  QA Surveillance Process                                        9
EN-MA-101  Fundamentals of Maintenance                                    10
OP-901-310 Loss of Train A Safety Bus                                    308
OP-903-115 Train A Integrated Emergency Diesel Generator /                21
          Engineering Safety Features Test
ME-007-005 Time Delay Relay Setting Check, Adjustment and                  16
          Functional Test
EN-TQ-201  Systematic Approach to Training Process                        12
EN-TQ-201  Systematic Approach to Training Process                        13
TM-OP-100  Operations Training Manual                                      16
EN-TQ-114  Licensed Operator Requalification Training Program              3
          Description
EN-TQ-126  Inprocessing Training Program                                  6
                              A1-3                          Attachment 1
 
NUMBER                                  TITLE                        REVISION
EN-TQ-126    Inprocessing Training Program                                8
EN-TQ-107    General Employee Training                                    7
EN-EC-100    Guidelines For Implementation Of The Employee                6
              Concerns Program
EN-MA-133    Control of Scaffolding                                        8
OP-002-007    Freeze Protection and Temperature Maintenance                18
EN-IS-102    Confined Space Program                                        8
OP-903-046    Emergency Feed Pump Operability Check                        309
EN-NE-G-013  Human Reliability Analysis for PSA Models                    1
OP-009-003    Emergency Feedwater                                          304
EN-FAP-OP-006 Operator Aggregate Impact Index Performance Indicator        0
OI-002-000    Operator Instruction Annunciator, Control Room              304
              Instrumentation and Workarounds Status Control
EN-OP-137    Licensed Operator Candidate Selection Process                2
EN-LI-125    NRC Cross-Cutting Analysis and Trending                        1
EN-OE-100    Operating Experience Program                                  14
EN-LI-118-06  Common Cause Analysis (CCA)                                  3
OP-002-007    Freeze Protection and Temperature Maintenance                18
OP-903-053    Fire Protection System Pump Operability Test                  17
UNT-005-013  Fire Protection Program                                      12
EN-FAP-LI-001 Condition Review Group (CRG)                                  3
                                  A1-4                      Attachment 1
 
NUMBER                                  TITLE                          REVISION
EN-FAP-LI-003 Corrective Action Review Board (CARB) Process                    8
EN-HU-103    Human Performance Error Reviews                                  7
EN-HU-106    Procedure and Work Instruction Use and Adherence                  0
EN-PL-202    Personnel Expectations Related to Fatigue Management            0
EN-TQ-113    Initial Licensed Operator Training Program Description          7
OP-100-014    Technical Specification and Technical Requirements              317
              Compliance
OP-901-521    Severe Weather and Flooding                                    305
EN-OE-100    Operating Experience Program                                    14
EN-FAP-AD-001 Fleet Administrative Procedure (FAP) Process                    0
EN-AD-101-01  NMM Procedure Writer Manual                                      9
EN-AD-101    Procedure Process                                              14
EN-PL-155    Entergy Nuclear Change Management                                4
W2.109        Procedure Development, Review & Approval                        13
EN-NS-102    Fitness For Duty Program                                          9
EN-NS-117    Fitness For Duty Processes                                      6
EN-OM-123-02  Working Hour Limits eSOMS Users Guide                            1
EN-OM-123    Fatigue Management Program                                      4
EN-PL-202    Personnel Expectations Related to Fatigue Management            0
EN-OP-115    Conduct of Operations                                            9
                                  A1-5                          Attachment 1
 
CALCULATIONS
NUMBER                                          TITLE                              REVISION
EC-C97-003          Probabilistic Evaluation of Tornado Missile Strike for        0, Change 1
                    Waterford 3 Nuclear Station
EC-M00-004          Thermal-Hydraulic Calculation for the EFW Steam Supply              0
                    Valves (MS-401A(B)) and Lines
Calculation No.    Flooding Analysis Outside Containment                                4
MNQ3-5
EC-M99-010          Minimum Flow for DCT Sump Pump                                      0-2
134669-G-07        Scour Analysis and Scour Protection Design from a                    1
                    Hypothetical Levee Break
DRAWINGS
NUMBER                                          TITLE                              REVISION
G-153              Feedwater, Condensate & Air Evacuation Systems
G-151              Flow Diagram Main & Extraction Steam System                        43
G-924              HVAC - Water Treatment Bldg. & Fire Pump House                      6
G1370              Fire Protection Turbine Bldg.                                        2
OTHER DOCUMENTS
NUMBER                                  TITLE                                REVISION/
                                                                                DATE
QS-2012-W3-008  QA Follow-up Surveillance of Category A Condition                  1
                Reports initiated during April 2012
QS-2012-W3-007  QA Follow-up review of EN-QV-126 required issues                  1
                initiated January, February, and March 2012
QS-2011-W3-015  QA Follow-up Surveillance of Category A Condition            July 26, 2011
                Reports initiated during September, 2011
QS-2011-W3-012  QA Follow-up Surveillance of the 2011 Corrective            September 12,
                Action Program (CAP) Audit                                      2011
                                        A1-6                            Attachment 1
 
NUMBER                                  TITLE                          REVISION/
                                                                          DATE
QS-2011-W3-009  QA Follow-up Surveillance of Quality Assurance              1
                Finding CR-WF3-2011-3084
QS-2011-W3-008  QA Follow-up Surveillance of Category A Condition    June 13, 2011
                Reports Initiated During May 2011
QS-2011-W3-007  QA Follow-up Surveillance of Category A Condition          1
                Reports Initiated During April 2011
QS-2011-W3-006  QA Follow-up to Category A Condition Reports for            1
                January and February 2011
LO-WLO-2011-    Quality of Causal Analysis Focused Assessment      October 13, 2011
0007
LO-WLO-2011-    Maintenance Training Focused Self-Assessment          July 29, 2011
0053            (I&C, Mechanical, Electrical)
LO-WLO-2011-    Quality Assurance Self-Assessment Report          December 9, 2011
0124
LO-WLO-2012-    Snapshot Assessment / Benchmark On: PME              May 23, 2012
0015            Performance
LO-WLO-2012-    Snapshot Assessment / Benchmark On:                February 6, 2012
0030            Maintenance - Advanced Qualifications
OE34343-        Seismic Monitoring Systems Failed to Actuate      September 1, 2011
20111008        During a Seismic Event
OE35212-        Extraction Steam System Carbon Steel Reducer      November 3, 2011
20120211        found Below Design Minimum Wall due to
                Unpredicted Flow-Accelerated Corrosion
OE34934-        Nuclear Regulatory Commission Red Finding Root    December 9, 2011
20120107        Cause Analysis Results
LO-WLO-2010-    Licensed Operator Requal 71111.11 Pre-Inspection      March 3, 2011
00143            Assessment
WLO-2011-00018  Evaluate the Effectiveness of Waterford 3 Shift    November 3, 2011
                Manager/STA Training Program
LOR/STAR        Examination # WWEX-LOR-11046R/S                          2011
Biennial Written Examination # WEX-LOR-11043R/S
Exam Worksheet
                                        A1-7                      Attachment 1
 
NUMBER                                TITLE                            REVISION/
                                                                          DATE
Site Broadcast RCA Drain Limitations                                February 16, 2012
              Waterford 3 - 2010 Employee Concerns Data
              Analysis
              Waterford 3 - 2011 Employee Concerns Data
              Analysis
FCBT-GET-      Entergy Fleet Specific Plant Access Training                  17
PATSS
              Training Review Group Meeting Minutes                    June 9, 2010
WLP-TRNC-SATR  Focused SAT Review                                            2
              2nd QTR 2010 Instructor Continuing Training Kickoff
LO-WLO-2010-  Waterford 3 Equipment Reliability and Core            May 27-29, 2010
0059          Business Focused Self Assessment
LO-WLO-2010-  WF3 IST Program Focused Self Assessment              August 20-24, 2010
0091
LO-WLO-2011-  Snapshot Assessment/Benchmark on: Relief Valve        October 26, 2011
0041          Program
WH-TB-11-5-A2  Evaluation Summary: Evaluation of Downstream            June 14, 2011
              Sump Debris Effects in Support of GSI-191
TB-11-5        Assessment of WCAP-16406-P-A Abrasive Wear              March 1, 2011
              Model and Recommendations
WH-TB-10-4-A2  Evaluation Summary: CEDM Upper Pressure              August 17, 2010
              Housing Venting
TB-10-4        Potential for Stress Corrosion Cracking in Control      April 12, 2010
              Element Drive Mechanism Upper Pressure Housing
SD-EFW        Emergency Feedwater                                          11
DCP-3506      Auxiliary Steam Test Connection for EFW Pump          March 12, 1997
              A/B
                                      A1-8                        Attachment 1
 
NUMBER                                TITLE                            REVISION/
                                                                          DATE
DCP-3506      Auxiliary Steam Test Connection for EFW Pump            July 24, 1998
              A/B
DCP-3506      Auxiliary Steam Test Connection for EFW Pump          February 25, 1999
              A/B
DCP-3506      Auxiliary Steam Test Connection for EFW Pump            May 26, 1999
              A/B
DC-3526      EFW Heat Trace Reliability Improvements              September 3, 1999
EC 37263      Replacement of MCC DCT Cubicle Compartments                    0
              Operability Assistance Tool
STI-WO-275977 CS117A, Shutdown Cooling Heat Exchanger                        0
              Discharge Stop Check Valve Leakage Test
EC 31375      Clarify Safety Function and Leakage Criteria for CS-          Draft
              111A(B) and CS-117A(B)
W3-DBD-003    Emergency Feedwater System                                    301
              CRG Report for Tuesday                                  July 31, 2012
              CRG Report for Thursday                                August 2, 2012
              Operational Focus                                        July 31, 2012
              Operational Focus                                      August 2, 2012
LO-WLO-2010-  Status of the Safety Conscious Work Environment          July 6, 2010
00061        in Security
LO-WLO-2012-  Operations Assessment of Plant Status and                March 1, 2012
006          Configuration Control
                                    A1-9                          Attachment 1
 
NUMBER                                    TITLE                          REVISION/
                                                                            DATE
LPL-EQA-4.2B      Environmental Qualification Assessment on Allis-            2
                  Chalmers Form Wound Motors Used in the
                  Waterford SES Unit No. 3
NRC IN 2010-04    Diesel Generator Voltage Regulation System        February 26, 2010
                  Component Due to Latent Manufacturing Defect
NRC-IN-2010-04-  Entergy OE A2 Evaluation Summary                      July 1, 2010
A2-WF3-0002-001
OP-903-053 V134  Fire Protection System Pump Operability Test        January 9, 2008
OP-903-053 V135  Fire Protection System Pump Operability Test          June 18, 2009
ER-W3-2002-      Diesel Fire Pump Louvers                                    0
0429-000
WSES-FSAR-        Updated Final Safety Analysis Report
UNIT-3
OP-903-053 V136  Fire Protection System Pump Operability Test        August 25, 2011
W3-DBD-018        Fire Protection                                              0
NPF-38            Waterford Operating License
W3-DBD-037        Nuclear Island and Building Design - RCB                    1
Ltr from A H Wern Waterford SES Unit No. 3 Levee Stability Analysis  December 7, 1972
TS 3.7.5          Flood Protection                                            NA
W3F1-2011-0018    License Amendment Request to Relocate Technical  November 21, 2011
                  Specifications to the Technical Requirements
                  Manual Waterford Steam Electric Station Unit 3
AR079684          Scope Revision to PMID 6718 incorporate EPRI      December 12, 2009
                  Recommend Pdm
                                          A1-10                    Attachment 1
 
NUMBER                                  TITLE                          REVISION/
                                                                        DATE
                Annual Work Hour Review & Fatigue Assessment            2010
                Summary
                Annual Work Hour Review & Fatigue Assessment            2011
                Summary
ODMI            SI MTRP0001 Auto Vent                                    0
ODMI            LPSI A Gas Accumulation                                  14
Entergy System  Workplace Violence and Weapons                            1
Policies &
Procedures
EN-IS-111        General Industrial Safety Requirements                    11
PS-011-102      Personnel Access Control                                308
PS-011-103      Vehicle Access Control                                  303
PS-011-110      Security Owner Controlled Area Vehicle and              010
                Personnel Access Control
                Waterford 3 Accreditation Board Report            September 2010
CONDITION REPORTS
CR-WF3-2012-03424          CR-WF3-2012-03461              CR-WF3-2012-03479
CR-WF3-2012-03495          CR-WF3-2012-03557              CR-WF3-2012-03596
CR-WF3-2012-03701          CR-WF3-2012-03729              CR-WF3-2012-03732
CR-WF3-2012-03736          CR-WF3-2012-03744              CR-WF3-2012-03745
CR-WF3-2012-03747          CR-WF3-2012-03752              CR-WF3-2012-03754
CR-WF3-2012-03761          CR-WF3-2012-03657              CR-WF3-2012-03658
CR-WF3-2012-03659          CR-WF3-2012-03660              CR-WF3-2012-03661
CR-WF3-2012-03662          CR-WF3-2012-03663              CR-WF3-2012-03664
CR-WF3-2012-03665          CR-WF3-2012-03666              CR-WF3-2012-03667
CR-WF3-2012-03668          CR-WF3-2012-03669              CR-WF3-2012-03670
CR-WF3-2012-03671          CR-WF3-2012-03672              CR-WF3-2012-03736
CR-WF3-2012-03709          CR-WF3-2012-03710              CR-WF3-2012-03711
CR-WF3-2012-03712          CR-WF3-2012-03713              CR-WF3-2012-03714
                                        A1-11                    Attachment 1
 
CONDITION REPORTS
CR-WF3-2012-03715 CR-WF3-2012-03716 CR-WF3-2012-03717
CR-WF3-2012-03718 CR-WF3-2012-03719 CR-WF3-2012-03720
CR-WF3-2012-03721 CR-WF3-2012-03722 CR-WF3-2012-03723
CR-WF3-2012-03724 CR-WF3-2012-03725 CR-WF3-2012-03726
CR-WF3-2012-03727 CR-WF3-2012-03728 CR-WF3-2012-03729
CR-WF3-2012-03730 CR-WF3-2012-03731 CR-WF3-2012-03732
CR-WF3-2012-03733 CR-WF3-2012-03734 CR-WF3-2012-03735
CR-WF3-2012-03736 CR-WF3-2012-03737 CR-WF3-2012-03738
CR-WF3-2012-03739 CR-WF3-2012-03740 CR-WF3-2012-03741
CR-WF3-2012-03742 CR-WF3-2010-03235 CR-WF3-2011-07469
CR-WF3-2009-07420 CR-WF3-2010-01166 CR-WF3-2010-03660
CR-WF3-2010-07223 CR-WF3-2010-06219 CR-WF3-2010-02721
CR-WF3-2011-06832 CR-WF3-2011-00679 CR-WF3-2011-01927
CR-WF3-2011-03163 CR-WF3-2011-07602 CR-WF3-2011-03636
CR-WF3-2011-03190 CR-WF3-2011-06205 CR-WF3-2011-04481
CR-WF3-2011-01356 CR-WF3-2011-07605 CR-WF3-2011-02005
CR-WF3-2011-07606 CR-WF3-2011-06254 CR-WF3-2011-07610
CR-WF3-2011-02927 CR-WF3-2011-03084 CR-WF3-2011-00458
CR-WF3-2011-01737 CR-WF3-2012-01048 CR-WF3-2012-00015
CR-WF3-2012-00351 CR-WF3-2012-06832 CR-WF3-2012-01419
CR-WF3-2012-03496 CR-WF3-2010-02940 CR-HQN-2006-00605
CR-WF3-2011-07845 CR-WF3-2011-03522 CR-WF3-2011-03523
CR-WF3-2011-03525 CR-WF3-2011-03526 CR-WF3-2011-03527
CR-WF3-2011-08044 CR-WF3-2011-08045 CR-WF3-2011-08046
CR-WF3-2011-08048 CR-WF3-2011-08049 CR-WF3-2011-08050
CR-WF3-2010-07466 CR-WF3-2011-00553 CR-WF3-2011-06203
CR-WF3-2011-07610 CR-WF3-2011-06204 CR-WF3-2011-08150
CR-WF3-2011-03550 CR-WF3-2011-05841 CR-WF3-2011-07603
CR-WF3-2011-06852 CR-WF3-2011-03350 CR-WF3-2011-05841
CR-WF3-2011-06850 CR-WF3-2012-00013 CR-WF3-2012-00021
CR-WF3-2012-00014 CR-WF3-2012-00818 CR-WF3-2012-01477
CR-WF3-2007-01955 CR-WF3-2012-00837 CR-WF3-2012-01476
CR-WF3-2010-06760 CR-WF3-2011-00217 CR-WF3-2010-02278
CR-WF3-2011-06653 CR-WF3-2012-00024 CR-WF3-2010-01330
CR-WF3-2010-03660 CR-WF3-2010-03050 CR-WF3-2011-03636
CR-WF3-2009-00655 CR-WF3-2009-1276  CR-WF3-2008-04000
CR-WF3-2011-00415 CR-WF3-2011-04935 CR-WF3-2012-00530
CR-WF3-2000-01334 CR-WF3-2012-01334 CR-WF3-2012-03495
CR-WF3-2012-00632 CR-WF3-2011-01737 CR-WF3-2010-07223
CR-WF3-2010-06219 CR-WF3-2011-00458 CR-WF3-2011-00836
CR-WF3-2012-02902 CR-WF3-2012-03190 CR-WF3-2010-04364
CR-WF3-2012-03736 CR-WF3-2012-03461 CR-WF3-2010-03235
CR-WF3-2010-03564 CR-WF3-2010-00686 CR-WF3-2010-02857
CR-WF3-2009-00802 CR-WF3-2010-00341 CR-WF3-2010-02584
CR-WF3-2012-01576 CR-WF3-2012-01581 CR-WF3-2012-00569
                          A1-12            Attachment 1
 
CONDITION REPORTS
CR-WF3-2012-02314 CR-WF3-2011-03807 CR-WF3-2012-03424
CR-WF3-2011-00544 CR-WF3-2011-08043 CR-WF3-2010-04199
CR-WF3-2011-00934 CR-WF3-2011-08047 CR-WF3-2011-01168
CR-WF3-2011-04562 CR-WF3-2011-01965 CR-WF3-2011-00987
CR-WF3-2011-08140 CR-WF3-2011-02546 CR-WF3-2010-05595
CR-WF3-2011-03811 CR-WF3-2012-01044 CR-WF3-1999-00708
CR-WF3-2011-00836 CR-WF3-2011-07603 CR-WF3-2012-00659
CR-WF3-2012-01045 CR-WF3-2011-06573 CR-WF3-2011-06254
CR-WF3-2010-02672 CR-WF3-2011-06870 CR-WF3-2012-01380
CR-HQN-2010-00503 CR-WF3-2012-00507 CR-WF3-2012-03067
CR-WF3-2011-03524 CR-WF3-2012-00507 CR-WF3-2009-04155
CR-WF3-2010-02135 CR-WF3-2010-00213 CR-WF3-2010-00036
CR-HQN-2012-00857 CR-WF3-2006-03416 CR-WF3-2007-04464
CR-WF3-2009-02487 CR-WF3-2009-03499 CR-WF3-2009-04155
CR-WF3-2010-00812 CR-WF3-2010-00890 CR-WF3-2010-02302
CR-WF3-2010-02721 CR-WF3-2010-02927 CR-WF3-2010-03099
CR-WF3-2010-03565 CR-WF3-2010-03588 CR-WF3-2010-03595
CR-WF3-2010-04344 CR-WF3-2010-04352 CR-WF3-2010-04634
CR-WF3-2010-04641 CR-WF3-2010-04659 CR-WF3-2010-04785
CR-WF3-2010-05141 CR-WF3-2010-05927 CR-WF3-2010-05929
CR-WF3-2010-07232 CR-WF3-2010-07276 CR-WF3-2010-07362
CR-WF3-2010-07552 CR-WF3-2011-00030 CR-WF3-2011-00553
CR-WF3-2011-00786 CR-WF3-2011-01897 CR-WF3-2011-01965
CR-WF3-2011-02546 CR-WF3-2011-03350 CR-WF3-2011-03465
CR-WF3-2011-03618 CR-WF3-2011-04230 CR-WF3-2011-05320
CR-WF3-2011-05779 CR-WF3-2011-05840 CR-WF3-2011-06166
CR-WF3-2011-06303 CR-WF3-2011-06573 CR-WF3-2011-06701
CR-WF3-2011-07443 CR-WF3-2011-07462 CR-WF3-2011-08055
CR-WF3-2011-08060 CR-WF3-2011-08081 CR-WF3-2011-08150
CR-WF3-2012-00315 CR-WF3-2012-00632 CR-WF3-2012-00659
CR-WF3-2012-00772 CR-WF3-2012-00797 CR-WF3-2012-00891
CR-WF3-2012-01139 CR-WF3-2012-01173 CR-WF3-2012-01503
CR-WF3-2012-01581 CR-WF3-2012-01605 CR-WF3-2012-01660
CR-WF3-2012-02046 CR-WF3-2012-02315 CR-WF3-2012-03232
CR-WF3-2012-03479 CR-WF3-2012-03596 CR-WF3-2012-03701
CR-WF3-2012-03732 CR-WF3-2012-03747 CR-WF3-2012-03752
CR-WF3-2012-03764 CR-WF3-2011-02519 CR-WF3-2012-01956
CR-WF3-2009-02172 CR-WF3-2011-03582 CR-WF3-2012-03325
CR-WF3-2009-05353 CR-WF3-2011-05625 CR-WF3-2012-03729
CR-WF3-2010-02672 CR-WF3-2011-06203 CR-WF3-2012-03761
CR-WF3-2010-03232 CR-WF3-2011-07415 CR-ANO-C-2011-00441
CR-WF3-2010-03809 CR-WF3-2011-08059 CR-WF3-2010-07466
CR-WF3-2010-04638 CR-WF3-2011-08308 CR-WF3-2011-00594
CR-WF3-2010-05046 CR-WF3-2012-00746 CR-WF3-2012-01507
CR-WF3-2010-06531 CR-WF3-2012-01014
                          A1-13            Attachment 1
 
WORK ORDERS
248856      52230980      289449
275977      196828        262164
283919      256250        64753
205779      296253        303342
296271      305641        52340992
52356683    52371026      52376231
52389001    254348        257755
246482      254493        263585
286950      261413        279127
298743      28810          287883
245561      52382399      52351187
254203
                    A1-14          Attachment 1
 
                                      Information Request
                                          June 11, 2012
    Biennial Problem Identification and Resolution Inspection - Waterford 3 Nuclear
                                        Generating Station
                                    Inspection Report 2012008
This inspection will cover the period from May 1, 2010, to June 1, 2012. All requested
information should be limited to this period unless otherwise specified. To the extent possible,
the requested information should be provided electronically in Adobe PDF or Microsoft Office
format. Lists of documents should be provided in Microsoft Excel or a similar sortable format.
A supplemental information request will likely be sent during the week of July 9, 2012.
Please provide the following no later than June 30, 2012:
1.      Document Lists
        Note: for these summary lists, please include the document/reference number, the
        document title or a description of the issue, initiation date, and current status. Please
        include long text descriptions of the issues.
        a.    Summary list of all corrective action documents related to significant conditions
              adverse to quality that were opened, closed, or evaluated during the period
        b.    Summary list of all corrective action documents related to conditions adverse to
              quality that were opened or closed during the period
        c.    Summary lists of all corrective action documents which were upgraded or
              downgraded in priority/significance during the period
        d.    Summary list of all corrective action documents that subsume or roll up one or
              more smaller issues for the period
        e.    Summary lists of operator workarounds, engineering review requests and/or
              operability evaluations, temporary modifications, and control room and safety
              system deficiencies opened, closed, or evaluated during the period
        f.    Summary list of plant safety issues raised or addressed by the Employee
              Concerns Program (or equivalent)
        g.    Summary list of all Apparent Cause Evaluations completed during the period
        h.    Summary list of all Root Cause Evaluations planned or in progress, but not
              complete at the end of the period
2.      Full Documents, with Attachments
        a.    Root Cause Evaluations completed during the period
                                              A2-1                            Attachment 2
 
b. Quality assurance audits performed during the period
c. All audits/surveillances performed during the period of the Corrective Action
  Program, of individual corrective actions, and of cause evaluations
d. Corrective action activity reports, functional area self-assessments, and non-
  NRC third party assessments completed during the period (do not include INPO
  assessments)
e. Corrective action documents generated during the period for the following:
  i.      NCVs and Violations issued to Waterford 3
  ii.    LERs issued by Waterford 3
f. Corrective action documents generated for the following, if they were determined
  to be applicable to Waterford 3 (for those that were evaluated, but determined
  not to be applicable, provide a summary list):
  i.      NRC Information Notices, Bulletins, and Generic Letters issued or
          evaluated during the period
  ii.    Part 21 reports issued or evaluated during the period
  iii.    Vendor safet
  iv.    y information letters (or equivalent) issued or evaluated during the period
  v.      Other external events and/or Operating Experience evaluated for
          applicability during the period
g. Corrective action documents generated for the following:
  i.      Emergency planning drills and tabletop exercises performed during the
          period
  ii.    Maintenance preventable functional failures which occurred or were
          evaluated during the period
  iii.    Adverse trends in equipment, processes, procedures, or programs which
          were evaluated during the period
  iv.    Action items generated or addressed by plant safety review committees
          during the period
                                  A2-2                            Attachment 2
 
3. Logs and Reports
  a.    Corrective action performance trending/tracking information generated during the
        period and broken down by functional organization
  b.    Corrective action effectiveness review reports generated during the period
  c.    Current system health reports or similar information
  d.    Radiation protection event logs during the period
  e.    Security event logs and security incidents during the period (sensitive information
        can be provided by hard copy during first week on site)
  f.    Employee Concern Program (or equivalent) logs (sensitive information can be
        provided by hard copy during first week on site)
  g.    List of training deficiencies, requests for training improvements, and simulator
        deficiencies for the period
4. Procedures
  a.    Corrective action program procedures, to include initiation and evaluation
        procedures, operability determination procedures, apparent and root cause
        evaluation/determination procedures, and any other procedures which implement
        the corrective action program at Waterford 3
  b.    Quality Assurance program procedures
  c.    Employee Concerns Program (or equivalent) procedures
  d.    Procedures which implement/maintain a Safety-Conscious Work Environment
5. Other
  a.    List of risk significant components and systems
  b.    Organization charts for plant staff and long-term/permanent contractors
                                          A2-3                          Attachment 2
 
Note: Corrective action documents refers to condition reports, notifications, action requests,
cause evaluations, and/or other similar documents, as applicable to Waterford 3.
As it becomes available, but no later than June 30, 2012, this information should be uploaded
on the Certrec IMS website. When these documents have been compiled (and by June 30,
2012), please download these documents onto a CD or DVD and sent it via overnight carrier to:
Richard L. Smith
U.S. NRC Resident Inspector Office
7003 Bald Hill Road
Port Gibson, MS 39150
Please note that the NRC is not able to accept electronic documents on thumb drives or other
similar digital media. However, CDs and DVDs are acceptable.
                                            A2-4                            Attachment 2
}}

Latest revision as of 21:30, 11 November 2019

IR 05000382-12-008, July 16, 2012 - September 24, 2012, Waterford 3 Biennial Baseline Inspection of the Identification and Resolution of Problems.
ML12310A497
Person / Time
Site: Waterford Entergy icon.png
Issue date: 11/05/2012
From: Ray Kellar
Division of Reactor Safety IV
To: Jacobs D
Entergy Operations
References
EA-12-198 IR-12-008
Download: ML12310A497 (50)


See also: IR 05000382/2012008

Text

UNITED STATES

NUC LEAR REGULATOR Y COMMI SSI ON

RE G IO N I V

1600 EAST LAMAR BLVD

ARL INGTON, TEXAS 76011- 4511

November 5, 2012

EA-12-198

Donna Jacobs, Site Vice President, Operations

Entergy Operations, Inc.

Waterford Steam Electric Station, Unit 3

17265 River Road

Killona, LA 70057-0751

SUBJECT: WATERFORD STEAM ELECTRIC STATION, UNIT 3 -

NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION

REPORT 05000382/2012008 AND NOTICE OF VIOLATION

Dear Ms. Jacobs:

On August 2, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem

Identification and Resolution biennial inspection at your Waterford Steam Electric Station,

Unit 3. The enclosed inspection report documents the inspection results that were discussed on

August 2, 2012, with Keith Nichols, Director of Engineering, and other members of your staff.

After additional in-office inspection, a final telephonic exit meeting was conducted on September

24, 2012 with Keith Nichols, Director of Engineering, and other members of your staff.

This inspection was an examination of activities conducted under your license as they relate to

problem identification and resolution and compliance with the Commissions rules and

regulations and the conditions of your license. Within these areas, the inspection involved

examination of selected procedures and representative records, observations of activities, and

interviews with personnel.

Based on the inspection sample, the inspection team concluded that the implementation of the

corrective action program and overall performance related to identifying, evaluating, and

resolving problems at Waterford Steam Electric Station, Unit 3, were adequate. Licensee

identified problems were entered into the corrective action program at a low threshold.

Problems were generally prioritized and evaluated commensurate with the safety significance of

the problems. Corrective actions were generally implemented in a timely manner

commensurate with their importance to safety and addressed the identified causes of problems.

Lessons learned from industry operating experience were generally reviewed and applied when

appropriate. Audits and self-assessments were effectively used to identify problems and

appropriate actions. Finally, the team determined that the station maintains a safety-conscious

work environment where employees feel free to raise nuclear safety concerns without fear of

retaliation.

Five NRC identified findings of very low safety significance (Green) were identified during this

inspection and are documented in the enclosed report. All five of these findings were

determined to involve a violation of NRC requirements. The NRC is treating four of the five

D. Jacobs -2-

violations as non-cited violations (NCVs), consistent with Section 2.3.2 of the Enforcement

Policy. Additionally, a licensee-identified violation, which was determined to be of very low

safety significance, is listed in this report.

One of the findings that the NRC evaluated under the risk significance determination process as

having very low safety significance (Green) did not meet the criteria to be treated as a non-cited

violation. The violation associated with this issue was evaluated in accordance with the NRC

Enforcement Policy. The current version of this Policy is available on the NRC website at

(http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html). This violation is cited in

the enclosed Notice of Violation (Notice), and the circumstances surrounding it are described in

detail in the subject inspection report. The violation is being cited in the Notice in accordance

with Section 2.3.2 of the Enforcement Policy because you failed to restore compliance in a

reasonable period of time after the violation was previously identified as a non-cited violation.

You are required to respond to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response. This reply should be clearly marked as a

"Reply to a Notice of Violation; EA-12-198" and should specifically include a firm commitment as

to when you will establish a design basis to determine the river level at which flood control

measures were to be initiated for closing the water tight doors as required in

Procedure OP-901-521, Severe Weather and Flooding. If you have additional information that

you believe the NRC should consider, you may provide it in your response to the Notice. The

NRC review of your response to the Notice will also determine whether further enforcement

action is necessary to ensure compliance with regulatory requirements.

If you contest these non-cited violations, you should provide a response within 30 days of the

date of this inspection report, with the basis for your denial, to the Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington DC 20555-0001, with copies to:

(1) the Regional Administrator, Region IV; (2) the Director, Office of Enforcement, United States

Nuclear Regulatory Commission, Washington, DC 20555-0001; and (3) NRC Resident

Inspector Office at Waterford Steam Electric Station, Unit 3.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV; and the NRC Resident Inspector at

Waterford Steam Electric Station, Unit 3.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response will be available electronically for public inspection in the NRC

Public Document Room or from the Publicly Available Records (PARS) component of NRC's

Agency wide Document Access and Management System (ADAMS). ADAMS is accessible

from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic

Reading Room).

Sincerely,

/RA/

Ray Kellar, P.E., Chief

Technical Support Branch

Division of Reactor Safety

D. Jacobs -3-

Docket No.: 50-382

License No: NPF-38

Enclosures:

1. Notice of Violation EA-12-198

2. Inspection Report 05000382/2012008

w/Attachments:

1. Supplemental Information

2. Information Request

cc w/enclosures: Electronic Distribution for Waterford 3

ML12310A497

SUNSI Rev Compl. Yes No ADAMS Yes No Reviewer Initials RLS

Publicly Avail. Yes No Sensitive Yes No Sens. Type Initials

TL/SRI:DRP/C RI:DRP/E PE:DRP/C RI:DRS/EB1 ACES BC:DRP/E

RSmith DOverland RKumana MYoung HGepford DAllen

-e- -e- /RA/ /RA/ /RA/ /RA/

10/23/2012 10/23/2012 10/13/2012 10/23/2012 10/26/2012 10/30/12

BC:DRS/TSB

RKellar

/RA/

11/5/2012

NOTICE OF VIOLATION

Entergy Operations, Inc. Docket No. 50-382

Waterford Steam Electric Station, Unit 2 License No. NPF-38

EA-12-198

During an NRC inspection conducted on July 16 through September 24, 2012, a violation of

NRC requirements was identified. In accordance with the NRC Enforcement Policy, the

violation is listed below:

Title 10 of the Code of Federal Regulations Part 50, Appendix B, Criterion III, Design

Control, states, in part, that measures shall be established to assure that applicable

regulatory requirements and the design basis, as defined in 10 CFR 50.2, are correctly

translated into specifications, procedures, and instructions.

Contrary to the above, from March 10, 2011, to August 2, 2012, the licensee failed to

establish measures to assure that applicable regulatory requirements and the design

basis, as defined in 10 CFR 50.2, were correctly translated into specifications,

procedures and instructions. Specifically, the licensee had not established a design

basis to determine the river level at which flood control measures were to be initiated for

closing the water tight doors as required in Procedure OP-901-521, Severe Weather

and Flooding.

This violation is associated with a Green Significance Determination Process finding.

Pursuant to the provisions of 10 CFR 2.201, Entergy Operations is hereby required to submit a

written statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document

Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator,

Region IV, and a copy to the NRC Resident Inspector at the facility that is the subject of this

Notice, within 30 days of the date of the letter transmitting this Notice of Violation (Notice). This

reply should be clearly marked as a "Reply to a Notice of Violation; EA-12-198" and should

include for each violation: (1) the reason for the violation or, if contested, the basis for disputing

the violation or severity level, (2) the corrective steps that have been taken and the results

achieved, (3) the corrective steps that will be taken, and (4) the date when full compliance will

be achieved. Your response may reference or include previous docketed correspondence if the

correspondence adequately addresses the required response. If an adequate reply is not

received within the time specified in this Notice, an Order or a Demand for Information may be

issued as to why the license should not be modified, suspended, or revoked, or why such other

action as may be proper should not be taken. Where good cause is shown, consideration will

be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001.

-1- Enclosure 1

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs document system (ADAMS), accessible from the

NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not

include any personal privacy, proprietary, or safeguards information so that it can be made

available to the public without redaction. If personal privacy or proprietary information is

necessary to provide an acceptable response, then please provide a bracketed copy of your

response that identifies the information that should be protected and a redacted copy of your

response that deletes such information. If you request withholding of such material, you must

specifically identify the portions of your response that you seek to have withheld and provide in

detail the bases for your claim of withholding (e.g., explain why the disclosure of information will

create an unwarranted invasion of personal privacy or provide the information required by

10 CFR 2.390(b) to support a request for withholding confidential commercial or financial

information). If safeguards information is necessary to provide an acceptable response, please

provide the level of protection described in 10 CFR 73.21.

In accordance with 10 CFR 19.11, you may be required to post this Notice within two working

days of receipt.

Dated this 5th day of November, 2012

-2- Enclosure 1

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 50-382

License: NPF-38

Report: 05000382/2012008

Licensee: Entergy Operations, Inc.

Facility: Waterford Steam Electric Station, Unit 3

Location: 17265 River Road

Killona, LA 70057-0751

Dates: July 16 through September 24, 2012

Team Leader: R. Smith, Senior Resident Inspector, Grand Gulf

Inspectors: D. Overland, Resident Inspector, Waterford 3

R. Kumana, Project Engineer

M. Young, Reactor Inspector

Approved By: Ray Kellar, P.E., Chief

Technical Support Branch

Division of Reactor Safety

-1- Enclosure 2

SUMMARY OF FINDINGS

IR 05000382/2012008; July 16, 2012 -September 24, 2012; Waterford 3 "Biennial Baseline

Inspection of the Identification and Resolution of Problems."

The team inspection was performed by one senior resident inspector, one resident inspector,

one reactor inspector, and one project engineer. One cited violation and four non-cited

violations of very low safety significance (Green) were identified during this inspection. The

significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter 0609, "Significance Determination Process". Findings for which the

significance determination process does not apply may be Green or be assigned a severity level

after NRC management review. The NRC's program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG 1649, "Reactor Oversight Process,"

Revision 4, dated December 2006.

Identification and Resolution of Problems

The team reviewed approximately 350 condition reports, work orders, engineering evaluations,

root and apparent cause evaluations, and other supporting documentation to determine if

problems were being properly identified, characterized, and entered into the corrective action

program for evaluation and resolution. The team reviewed a sample of system health reports,

self-assessments, audits, trending reports and metrics, and various other documents related to

the corrective action program.

Based on these reviews, the team concluded that the licensees corrective action program and

its other processes to identify and correct nuclear safety problems were adequate to support

nuclear safety. However, the team noted at times the licensee staff did not always use the

corrective action program for problems that were perceived as minor. The team also noted

several challenges in correcting adverse conditions in a timely manner. Further, the licensee

had several long-standing issues, which had been in the corrective action process for over a

year without resolution.

The licensee appropriately evaluated industry operating experience for relevance to the facility

and entered applicable items in the corrective action program. However, there was one

example where the licensee failed to enter an information notice into their corrective action

program for evaluation of a condition adverse to quality. The licensee used industry operating

experience when performing root cause and apparent cause evaluations. The licensee

performed effective quality assurance audits and self-assessments, as demonstrated by self-

identification of poor corrective action program performance and identification of ineffective

corrective actions.

Finally, the team determined that the station continued to maintain a safety-conscious work

environment. Employees felt free to raise nuclear safety concerns to the attention of

management without fear of retaliation.

-2- Enclosure 2

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Criterion V, Instructions, Procedures, and Drawings, for a failure to follow

Procedure EN-OP-115, Conduct of Operations. Specifically, the licensee failed

to ensure that control room operators knew the status of equipment at all times.

While interviewing the person responsible for tracking plant deficiencies, the

inspectors discovered that the licensee had two separate governing procedures.

These two instructions had different definitions for categories of plant deficiencies

and different databases for tracking them. The inspectors then interviewed the

on-shift operators in the control room and reviewed both databases. The

inspectors identified several issues, including lack of knowledge by the control

room operators about which procedure to use, failure to track deficiencies in both

databases, and inadequate classification of deficiencies. The inspectors

determined that in March 2010, the licensee changed their process for tracking

deficiencies to be consistent with their fleet reporting process. However, the

licensee did not revise the procedure and did not train all affected personnel on

the new process. As a result, control room operators did not have a complete

and accurate knowledge of all plant deficiencies. This finding was entered into

the licensees corrective action program as Condition Report CR-WF3-2012-

03732.

The failure to ensure that operators were aware of the status of all plant

equipment was a performance deficiency. The performance deficiency was more

than minor because it was associated with the procedure quality attribute of the

Initiating Events Cornerstone and affected the cornerstone objective to limit the

likelihood of those events that upset plant stability and challenge critical safety

functions during shutdown as well as power operations. Specifically, the licensee

failed to implement a procedure designed to ensure operators were aware of

deficiencies in the instrumentation, controls, and operation of nuclear plant

systems. In accordance with NRC Inspection Manual Chapter 0609,

Attachment 4, "Initial Characterization of Findings," the issue was determined to

affect the Initiating Events Cornerstone. In accordance with NRC Inspection

Manual Chapter 0609, Appendix A, The Significance Determination Process

(SDP) for Findings at Power, the issue was determined to have very low safety

significance (Green) because it did not cause a reactor trip and did not cause the

loss of mitigation equipment relied upon to transition the plant from the onset of

the trip to a stable shutdown condition. This finding had a cross-cutting aspect in

the human performance area, work practices component, in that the licensee

failed to define and effectively communicate expectations regarding procedural

compliance, and personnel did not follow procedures H.4.b] (Section 4OA2.5.d).

Appendix B, Criterion XVI, Corrective Actions, because the licensee failed to

determine the cause of a significant condition adverse to quality and take

-3- Enclosure 2

corrective actions to preclude repetition. Specifically, the licensee failed to

assure that the cause of the condition was determined and corrective action

taken to preclude repetition related to a contractors non-compliance with site

procedural requirements. The corrective actions include developing additional

training and provisions to provide additional contractor oversight. This finding

was entered into the licensees corrective action program as Condition Reports

CR-WF3-2012-03769 and CR-WF3-2012-03772.

The failure to determine the cause of a significant condition adverse to quality

and take corrective action to preclude repetition was a performance deficiency.

The performance deficiency was more than minor because if left uncorrected, it

could lead to more significant consequences; therefore, it is a finding.

Specifically, failure to determine the cause of a significant condition adverse to

quality and take corrective action to prevent recurrence can result in recurrence

of the condition. In accordance with NRC Inspection Manual Chapter 0609,

Attachment 4, "Initial Characterization of Findings," the issue was determined to

affect the Initiating Events Cornerstone. In accordance with NRC Inspection

Manual Chapter 0609, Appendix A, The Significance Determination Process

(SDP) for Findings at Power, the issue was determined to have very low safety

significance (Green) because the finding did not cause a reactor trip and the loss

of mitigation equipment relied upon to transition the plant from the onset of the

trip to a stable shutdown condition. This finding had a cross-cutting aspect in the

human performance, work practice component, in that the licensee failed to

follow guidance in the root cause evaluation procedure when developing

appropriate corrective actions to prevent repetition H.4(b) (Section 4OA2.5.e).

Cornerstone: Mitigating Systems

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for a failure to

follow the Operability Determination Process. Specifically, the licensee failed to

determine the operability of the emergency diesel generators immediately upon

discovery without delay and in a controlled manner using the best information

available in response to NRC Information Notice 2010-04. The licensee

completed an evaluation of the information notice that indicated that Waterford 3

was vulnerable and susceptible to the issue, but the licensee failed to issue a

condition report as required by their procedure. The failure to initiate a condition

report resulted in the licensees failure to perform an operability determination of

the emergency diesel generators as required by, EN-OP-104, Operability

Determination Process, Revision 6. In the evaluation, the licensee considered

the fact that they had an Action Request in their system to add routine

thermography inspections within the voltage regulator cabinets to their

preventative maintenance program as being adequate. The action request was

not completed when the inspection team reviewed the issue. The inspectors

questioned whether there was an operability concern for the emergency diesel

generators. The licensee recognized their failure to perform an operability

determination. They performed a prompt operability determination based on no

-4- Enclosure 2

observed degradation in performance and declared the emergency diesel

generators operable. In addition, they plan to conduct the thermography

inspections during the next scheduled emergency diesel generator surveillance.

This finding was entered into the licensees corrective action program as

Condition Report CR-WF3-2012-03761.

The failure to promptly perform an operability determination of the emergency

diesel generators in response to NRC Information Notice 2010-04 was a

performance deficiency. The performance deficiency was more than minor

because it was associated with the equipment performance attribute of the

Mitigating Systems Cornerstone and affected the cornerstone objective to ensure

the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Specifically, the licensee failed to

promptly determine the operability of the diesel generators after obtaining

information of a potential condition adverse to quality. In accordance with NRC

Inspection Manual Chapter 0609, Attachment 4, "Initial Characterization of

Findings," the issue was determined to affect the Mitigating Systems

Cornerstone. In accordance with NRC Inspection Manual Chapter 0609,

Appendix A, The Significance Determination Process (SDP) for Findings at

Power, the issue was determined to have very low safety significance (Green)

because it was not a deficiency affecting the design or qualification of the

system, it did not represent a loss of system or function, and it was a Technical

Specification system, but did not represent an actual loss of function of a single

train for greater than it allowed outage time. Specifically, the licensee performed

an operability determination in response to the inspectors questions and

determined the emergency diesel generators were operable based on a review of

surveillance data and maintenance records. This finding had a cross-cutting

aspect in the problem identification and resolution area, operating experience

component, in that the licensee failed to systematically collect, evaluate, and

communicate to affected internal stakeholders in a timely manner relevant

internal and external operating experience P.2.a] (Section 4OA2.5.a).

Criterion XVI, Corrective Action, for the failure to take timely corrective action

for a condition adverse to quality. Specifically, from May 2011, through

August 2012, the licensee failed to restore a degraded condition, which included

a corrective action to perform a new design analysis for the emergency

feedwater pump AB after the removal of heat trace circuit 1-8C, despite having a

reasonable amount of time to complete it. Currently, plant operators are required

once per shift to perform temperature verifications of the heat trace to ensure

condensation does not form in the steam supply pipe to the turbine driven pump

and to maintain emergency feedwater pump AB in an operable but degraded

status until the design analysis is complete. This finding was entered into the

licensees corrective action program as Condition Report CR-WF3-2012-03754.

The team determined that the failure to complete the corrective action of

performing a new design analysis to determine if emergency feedwater pump AB

-5- Enclosure 2

required a design modification based on the analysis in a timely manner was a

performance deficiency. The performance deficiency was more than minor

because it affected the equipment performance attribute of the Mitigating

Systems Cornerstone objective to ensure the availability, reliability, and capability

of systems that respond to initiating events to prevent undesirable

consequences. Specifically, failure to implement this corrective action could

result in reduced reliability of the emergency feedwater pump AB. In accordance

with NRC Inspection Manual Chapter 0609, Attachment 4, "Initial

Characterization of Findings," the issue was determined to affect the Mitigating

Systems Cornerstone. In accordance with NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings

at Power, the issue was determined to have very low safety significance (Green)

because it affected the design or qualification of mitigating systems, structures,

and components; however, the systems, structures, and components maintained

operability. This finding had a cross-cutting aspect in the human performance

area, resources component, in that the licensee failed to minimize a long-

standing equipment issue adequately to assure nuclear safety H.2(a) (Section

4OA2.5.b).

Criterion III, Design Control, for the failure to establish measures to assure that

applicable regulatory requirements and the design basis as defined in

10 CFR 50.2 are correctly translated into procedures. Specifically, the licensee

has not determined a basis for the level at which flood control measures are

initiated, two years after receiving a non-cited violation for the same deficiency.

As an interim compensatory measure for a previous violation of inadequate

technical specifications, the licensee modified their flooding procedure to include

an action to start shutting flood control doors at a river level of 24 feet instead of

27 feet. The licensee recognized the need to establish a basis for initiating these

actions at 24 feet, and issued a corrective action to track completion. The

licensee extended the due date several times and had not completed it by the

arrival of the inspection team. The inspection team questioned why the licensee

had not completed the calculation to justify their basis for their compensatory

measures, noting that it had been over two years since the original violation was

identified. The inspectors verified through walk-downs, procedure reviews, and

historical data that the licensees use of 24 feet did not represent an immediate

operability concern, and that the current river level was sufficiently low to allow

time for the licensee to correct the deficiency. This finding was entered into the

licensees corrective action program as condition report CR-WF3-2012-03752.

The failure to complete the corrective action to establish a basis for flood control

measures in a timely manner was a performance deficiency. The performance

deficiency was more than minor because it was associated with the protection

from external events attribute of the Mitigating Systems Cornerstone and affected

the cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Specifically, the licensee failed to verify through calculations or analysis that the

-6- Enclosure 2

actions taken to secure flood doors could be completed in time to protect safety-

related equipment from flooding due to a levee failure. In accordance with

NRC Inspection Manual Chapter 0609, Attachment 4, "Initial Characterization

of Findings," the issue was determined to affect the Mitigating Systems

Cornerstone. In accordance with NRC Inspection Manual Chapter 0609,

Appendix A, The Significance Determination Process (SDP) for Findings at

Power, the issue was determined to have very low safety significance (Green)

because it did not involve the loss or degradation of equipment or function

specifically designed to mitigate a seismic, flooding, or severe weather initiating

event. Specifically, the inspectors confirmed that the licensee could reasonably

ensure the flood control doors could perform their safety function. This finding

had a cross-cutting aspect in the human performance area, resources

component in that the licensee failed to maintain long term plant safety by

maintenance of design margins and ensuring engineering backlogs low enough

to support safety. H.2.a] (Section 4OA2.5.c).

B. Licensee-Identified Violations

A violation of very low safety significance, which was identified by the licensee, has been

reviewed by the inspectors. Corrective actions taken by the licensee have been entered

into the licensees corrective action program. This violation and associated corrective

action tracking numbers are listed in Section 4OA7 of this report.

-7- Enclosure 2

REPORT DETAILS

4. OTHER ACTIVITIES (OA)

4OA2 Problem Identification and Resolution (71152)

The team based the following conclusions on the sample of corrective action documents

that were initiated in the assessment period, which ranged from May 1, 2010, to the end

of the on-site portion of this inspection on August 2, 2012.

.1 Assessment of the Corrective Action Program Effectiveness

a. Inspection Scope

The team reviewed approximately 350 corrective action documents, including

associated root cause, apparent cause, and direct cause evaluations, out of

approximately 17,000 corrective action documents that were issued between

May 1, 2010, and August 2, 2012, to determine if problems were being properly

identified, characterized, and entered into the corrective action program for

evaluation and resolution. The team reviewed a sample of system health

reports, operability determinations, self-assessments, trending reports and

metrics, and various other documents related to the corrective action program.

The team evaluated the licensees efforts in establishing the scope of problems

by reviewing selected logs, work requests, self-assessments results, audits,

system health reports, action plans, and results from surveillance tests and

preventive maintenance tasks. The team reviewed work requests and attended

the licensees daily Condition Review Group, (which is the management review

committee meeting to assess the reporting threshold, prioritization efforts, and

significance determination process), as well as observing the interfaces with the

operability assessment and work control processes when applicable. The teams

review included verifying the licensee considered the full extent of cause and

extent of condition for problems, as well as how the licensee assessed generic

implications and previous occurrences. The team assessed the timeliness and

effectiveness of corrective actions, completed or planned, and looked for

additional examples of similar problems. The team conducted interviews with

plant personnel to identify other processes that may exist where problems may

be identified and addressed outside the corrective action program.

The team also reviewed corrective action documents that addressed past

NRC-identified violations to ensure that the corrective action addressed the

issues as described in the inspection reports. The inspectors reviewed a sample

of corrective actions closed to other corrective action documents to ensure that

corrective actions were still appropriate and timely.

The team considered risk insights from both the NRCs and Waterford Steam

Electric Station, Unit 3s risk assessments to focus the sample selection and

plant tours on risk significant systems and components. The team selected the

-8- Enclosure 2

component cooling water and auxiliary component cooling water systems as risk

significant systems to review. The samples reviewed by the team focused on,

but were not limited to, these systems. The team also expanded their review to

include five years of evaluations involving the emergency feedwater system to

determine whether problems were being effectively addressed. The team

conducted a walk-down of these systems to assess whether problems were

identified and entered into the corrective action program.

b. Assessments

1. Assessment - Effectiveness of Problem Identification

The team concluded in most cases that the licensee identified issues and

adverse conditions and entered them into the corrective action program in

accordance with the licensees corrective action program guidance and NRC

requirements. The team determined that the licensee generally was identifying

problems at a low threshold and entering them into the corrective action program.

The team identified one condition adverse to quality that was not placed in the

corrective action program. The licensee wrote approximately 17,000 condition

reports during the two-year period of review. The team noted that this high rate

of condition report generation is generally a sign of a healthy corrective action

program. The following issues were noted by the team:

  • Through the review of NRC information notices over the assessment

period, the team identified that the licensee failed to enter one information

notice applicable to Waterford Steam Electric Station, Unit 3s emergency

diesel generator voltage regulators into their corrective action program.

The team documented this as a Green non-cited violation in

Section 4OA2.5.a of this report.

  • The team identified that some main control room deficiencies, although

identified by white identification tags, had not been entered into the

licensees corrective action program. The team documented this as a

Green non-cited violation in Section 4OA2.5.d of this report.

  • The licensee self-identified a failure to initiate condition reports that

resulted in missed operability assessments on two occasions when the

emergency feedwater pump AB heat trace fell below the required

temperature per the operating instruction. The team documented this as

a licensee identified violation in Section 4OA7 of this report.

2. Assessment - Effectiveness of Prioritization and Evaluation of Issues

The team concluded that generally the licensee effectively prioritized and

evaluated conditions adverse to quality. The team found that even with the high

number of condition reports initiated on a daily basis, the licensees daily action

review committee pre-screening and the management review committees

-9- Enclosure 2

effectively assessed each condition adverse to quality. The following are issues

the team identified or reviewed during the inspection:

  • The licensees extent of condition review for an incorrect preventive

maintenance classification of a limit switch identified additional incorrect

classifications. However, the team identified that the licensee failed to

initiate a separate condition report to document these additional errors

and, therefore, failed to ensure the testing requirements for each of the

newly identified components were met until challenged by the team. This

was documented in Condition Report CR-WF3-2012-03557.

  • The team identified that the licensee performed an inadequate apparent

cause evaluation of a failure of the security diesel generator. The

evaluation identified one cause as being an incorrect maintenance

classification. When the licensee found the component was properly

classified in its preventative maintenance optimization program, the

licensee did not revise their apparent cause. Instead, they determined

other corrective actions to address security equipment issues.

  • The team identified that the apparent cause evaluation for inservice

testing failures of the main feed isolation valves was determined to be

incorrect. The licensee first determined that the failure was the result of

moisture intrusion in the hydraulic fluid. However, additional failures and

a subsequent root cause analysis showed that the failure mechanism

was actually interior varnishing. This was identified by review of external

operating experience that was available, but missed during the initial

apparent cause evaluation.

Criterion V, that is not subject to enforcement action in accordance with

the NRCs Enforcement Policy. The licensee downgraded a Category A

condition report to Category B without obtaining approval of the condition

review group as required by Procedure EN-L1-102, Corrective Action

Program. This was documented in Condition Report CR-WF3-2012-

03325.

identified that the quality of six previous causal analyses was inadequate.

  • The team identified that the licensee categorized many conditions

adverse to quality on the diesel fire pump as Category D. Although their

process allowed this, they could have identified and corrected non-

conforming trends in the diesel fire pumps more effectively with a higher

prioritization. This was documented in Condition Report CR-WF3-2012-

03747.

- 10 - Enclosure 2

  • The team determined that the licensee categorized a problem with the

steam generator feedwater pump B requiring manual operation as an

Operator Burden when it could have met the definition of an Operator

Workaround, which carried a higher level of prioritization in the licensee

work planning process.

  • The team reviewed a licensee failure to frequently and regularly review a

degraded and nonconforming condition associated with the reactor

coolant pump N-9000 stage seals as required by Procedure EN-OP-104,

Operability Determination Process. This is an example of the licensee

not thoroughly evaluating problems, such that the resolutions address

causes and extent of conditions, as necessary. This was documented in

NRC Inspection Report 05000382/2011002 as a Green non-cited

violation.

The team reviewed a number of condition reports that involved operability

reviews to assess the quality, timeliness, and prioritization of operability

assessments. In general, both immediate and prompt operability assessments

reviewed were adequately completed in a timely manner.

3. Assessment - Effectiveness of Corrective Actions

Overall, the team concluded that the licensee generally developed appropriate

corrective actions to address problems. However, the team identified a number

of corrective actions associated with conditions adverse to quality that were not

completed in a timely manner:

  • The team identified that the licensee failed to take timely corrective

actions to correct a design basis analysis for the emergency feedwater

pump AB after the removal of required heat trace on the steam supply

piping. The team documented this as a Green non-cited violation in

Section 4OA2.5.b of this report.

  • The team identified that the licensee failed to take timely corrective

actions to establish a basis through analysis for the initiation of flood

control measures at a river level of 24 feet. The team documented this as

a Green cited violation in Section 4OA2.5.c of this report.

  • The team identified that the licensee failed to have a GMPO/Director

approve a due date extension on a long-term corrective action from

CR-WF3-2011-00887 (Corrective Action 13), which is not permitted by

Procedure EN-LI-102, Corrective Action Program. This resulted in a

minor violation of 10 CFR Part 50, Appendix B, Criterion V, that is not

subject to enforcement action in accordance with NRCs Enforcement

Policy. The corrective action was to complete an engineering analysis to

determine the scope of modifications needed for the steam driven

- 11 - Enclosure 2

emergency feedwater turbine steam supply piping. This was documented

in Condition Report CR-WF3-2012-03461.

  • The team identified a failure to complete a corrective action to validate

data for work hours for security personnel. This resulted in a minor

violation of 10 CFR 26.205.e that is not subject to enforcement action in

accordance with the NRCs Enforcement Policy. This was documented in

Condition Report CR-WF3-2012-03729.

  • The team reviewed a licensee failure to take or perform effective

corrective actions for boric acid leaks for the past seven years. This is an

example of the licensees failure to effectively correct identified boric acid

leaks in a timely manner. This was documented in NRC Inspection

Report 05000382/2010006 as a Green non-cited violation.

.2 Assessment of the Use of Operating Experience

a. Inspection Scope

The team examined the licensee's program for reviewing industry operating

experience, including reviewing the governing procedure and self-assessments.

The team reviewed a sample of 10 condition reports examining operating

experience documents that had been issued during the assessment period to

determine whether the licensee had appropriately evaluated the notification for

relevance to the facility. The team then examined whether the licensee had

entered those items into their corrective action program and assigned actions to

address the issues. The team reviewed a sample of root cause evaluations and

corrective action documents to verify whether the licensee had appropriately

included industry-operating experience.

b. Assessment

Overall, the team determined that the licensee was adequately evaluating

industry operating experience for relevance to the facility, based on reviewing a

sample of 10 condition reports examining industry operating experience. The

licensee entered all but one applicable item in the corrective action program in

accordance with station procedures. The team concluded that the licensee was

evaluating industry operating experience when performing root cause and

apparent cause evaluations. Both internal and external operating experiences

were being incorporated into lessons learned for training and pre-job briefs. The

following are issues the team identified or reviewed during the inspection:

  • The team identified through the review of NRC information notices over

the assessment period that the licensee had failed to enter one

information notice applicable to Waterford 3 emergency diesel generator

voltage regulators into their corrective action program. In response, the

licensee did a complete audit of all NRC information notices issued during

- 12 - Enclosure 2

the assessment period and found no other discrepancies. The team

documented this as a Green non-cited violation in Section 4OA2.5.a

of this report.

  • The team reviewed three examples from this assessment period of the

licensees failure in the use of operating experience, resulting in the

licensee not implementing and institutionalizing operating experience

through changes to station processes, procedures, equipment, and

training programs.

o The team reviewed a licensee failure to implement a preventative

maintenance activity to replace dry cooling tower process analog

control cards based on internal and industry-wide operating

experience that documented previous failures of process analog

control cards due to age-related degradation after 15 years. This

was documented in NRC Inspection Report 05000382/2011004 as

a Green non-cited violation.

o The team reviewed a licensee failure to identify that varnish

deposits were causing the main feedwater isolation valve to fail its

inservice testing. This resulted from the licensees failure to use

relevant external operating experience to identify that other sites

experienced similar failures of feedwater isolation valves due to

varnish deposits on the interior surfaces. This was documented in

NRC Inspection Report 05000382/2011005 as a Green non-cited

violation.

o The team reviewed a licensee failure to evaluate the internal

condition of the condensate and refueling water storage pool

structures through performance of appropriate preventative

maintenance after previous documented industry-wide operating

experience of concrete degradation due to boric acid. This was

documented in Inspection Report 05000382/2011003 as a Green

non-cited violation.

.3 Assessment of Self-Assessments and Audits

a. Inspection Scope

The team reviewed a sample size of 22 licensee self-assessments, surveillances,

and audits to assess whether the licensee was regularly identifying performance

trends and effectively addressing them. The team reviewed audit reports to

assess the effectiveness of assessments in specific areas. The team evaluated

the use of self- and third party assessments, the role of the quality assurance

department, and the role of the performance improvement group related to

licensee performance. The specific self-assessment documents reviewed are

listed in the Attachment.

- 13 - Enclosure 2

b. Assessment

The team concluded that the licensee had an effective self-assessment process.

Licensee management was involved with developing tactical self-assessments.

The team determined that self-assessments were self-critical and thorough

enough to identify deficiencies. The following are issues the team reviewed

during the inspection:

  • The team reviewed a licensee self-assessment of plant status and

configuration control performed in March 2012. This self-assessment

was an opportunity for the site to identify and address the issues

associated with control room deficiencies documented in

Section 4OA2.5.d of this report, but the assessment did not discuss them.

  • The team reviewed the licensees failure to perform an adequate risk

assessment associated with the maintenance window for the turbine

driven emergency feedwater pump. This is an example of the licensees

failure to use independent and self-assessments because the licensee

performed a probabilistic risk assessment model update in April 2009, but

failed to identify an assumption crediting operator actions that were not in

procedures. This was documented in NRC Inspection

Report 05000382/2011007 as a Green non-cited violation.

.4 Assessment of Safety-Conscious Work Environment

a. Inspection Scope

The inspection team conducted individual interviews with over 30 individuals from

a cross-section of functional organizations: engineering, operations,

maintenance, quality assurance, radiation protection, chemistry, security officers,

and contract personnel. Both supervisory and non-supervisory personnel were

included in these interviews. The team conducted these interviews to assess

whether conditions existed that would challenge the establishment of a safety-

conscious work environment (SCWE) at Waterford 3. The team also interviewed

the Waterford 3 employee concerns program manager and reviewed the last two

safety culture self-assessment documents.

b. Assessment

Overall, the team concluded that a safety-conscious work environment exists at

Waterford Steam Electric Station, Unit 3. Employees demonstrated familiarity

with the various avenues available to raise safety concerns. They appeared

comfortable with submitting all nuclear safety issues.

The team noted a potential vulnerability in the licensees safety-conscious work

environment from discussions with plant personnel. There was a perception

among some members of the plant staff that management may use the condition

- 14 - Enclosure 2

report process to discipline workers when personnel errors were documented in

the condition reports. Additionally, some personnel stated that they did not write

condition reports, but rather they passed the comments along to supervisors who

would enter them into the corrective action program.

Overall, most individuals were familiar with the employee concerns program and

its location on site. There was visibility of the program throughout the site. Many

of the individuals interviewed had knowledge of the employee concerns

manager; however, no one interviewed indicated having direct interactions with

the employee concerns manger during the inspection period. Personnel

understood and were confident in the confidentiality of the program.

Site personnel have received initial and annual refresher training, which provided

instruction on safety-conscious work environment policies. Many of the

individuals interviewed were familiar with this training and with the overall

message in the training. However, not everyone was familiar with the details of

the policy. None of the individuals interviewed cited any examples of

harassment, intimidation, retaliation or discrimination, or any negative reactions

from management when individuals raised nuclear safety concerns. Finally,

individuals indicated that if they were to believe unsafe conditions existed, they

would feel comfortable stopping work without fear of retaliation, even if such

actions would prolong an outage or extend a planned schedule.

.5 Specific Issues Identified During This Inspection

a. Failure to Promptly Determine the Operability of the Emergency Diesel Generators

Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for a failure to follow

Procedure EN-OP-104, Operability Determination Process. Specifically, the licensee

failed to determine the operability of the emergency diesel generators immediately upon

discovery without delay and in a controlled manner using the best information available

in response to NRC Information Notice 2010-04.

Description. The team reviewed the licensees corrective actions taken in response to

an NRC Information Notice. On February 26, 2010, the NRC issued Information

Notice 2010-04, Diesel Generator Voltage Regulation System Component [Failure] Due

to Latent Manufacturing Defect. This information notice describes the failure of a linear

power reactor in an emergency diesel generator voltage regulation system at a plant

where the licensees preventive maintenance program did not address the emergency

diesel generator excitation system magnetic components.

The licensee completed an evaluation of the information notice per Procedure EN-

OE-100, Operating Experience Program, on July 1, 2010. This evaluation indicated

that Waterford 3 was vulnerable and susceptible to the issue, but the licensee failed to

issue a condition report as required by their procedure. The failure to initiate a condition

report resulted in the licensees failure to perform an operability determination of the

- 15 - Enclosure 2

emergency diesel generators as required by Procedure EN-OP-104, Operability

Determination Process, Revision 6.

In the evaluation, the licensee considered the fact that they had an Action Request in

their system that addressed a similar concern to be an acceptable response to this

information notice. Action Request 079684 was initiated on December 10, 2009, to

address recommendations from an INPO assistance visit in 2007 and it included an

action to add routine thermography inspections within the voltage regulator cabinets to

their preventative maintenance program. The Entergy Nuclear Corporate Operating

Experience group also reviewed this information notice on March 4, 2010. In response,

they issued a specific action through their operating experience database to evaluate the

information notice to each Entergy site. However, they failed to issue one to

Waterford 3.

The licensee started routing Action Request 079684 for approval, but they stopped on

March 15, 2010. The licensee attributed this to an incomplete turnover by departing

personnel. No other approval actions were taken until April 16, 2012, when the request

was routed to the next person in the approval process. Again, no further action was

taken, and the action request was not completed when the inspection team reviewed the

issue.

The inspectors questioned why there was no condition report generated and why the

action request had not been completed more than two years after issuance. In

particular, the inspectors questioned whether there was an operability concern for the

emergency diesel generators. The licensee recognized their failure to issue a condition

report and perform an operability determination. They performed a prompt operability

determination based on operating data, work history, and no observed degradation in

performance, and declared the emergency diesel generators operable. In addition, they

plan to conduct the thermography during the next scheduled emergency diesel

generator surveillance.

The licensee initiated CR-WF3-2012-00596 and CR-WF3-2012-03761 to address the

issue. They also initiated CR-HQN-2012-00857 to address the failure of the corporate

organization to include Waterford 3 in their site-specific requests.

Analysis. The failure to promptly perform an operability determination of the emergency

diesel generators in response to NRC Information Notice 2010-04 was a performance

deficiency. The performance deficiency was more than minor because it was associated

with the equipment performance attribute of the Mitigating Systems Cornerstone and

affected the cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Specifically, the licensee failed to promptly determine the operability of the diesel

generators after obtaining information of a potential condition adverse to quality. In

accordance with NRC Inspection Manual Chapter 0609, Attachment 4, "Initial

Characterization of Findings," the issue was determined to affect the Mitigating Systems

Cornerstone. In accordance with NRC Inspection Manual Chapter 0609, Appendix A,

The Significance Determination Process (SDP) for Findings at Power, the issue was

- 16 - Enclosure 2

determined to have very low safety significance (Green) because it was not a deficiency

affecting the design or qualification of the system, it did not represent a loss of system or

function, and it was a Technical Specification system but did not represent an actual loss

of function of a single train for greater than it allowed outage time. Specifically, the

licensee performed an operability determination in response to the inspectors questions

and determined the emergency diesel generators were operable based on a review of

surveillance data and maintenance records. This finding had a cross-cutting aspect in

the problem identification and resolution area, operating experience component, in that

the licensee failed to systematically collect, evaluate, and communicate to affected

internal stakeholders in a timely manner relevant internal and external operating

experience P.2.a].

Enforcement. Title 10 of the Code of Federal Regulations Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, states, in part, that activities

affecting quality shall be prescribed by documented instructions, procedures, or

drawings of a type appropriate to the circumstances and shall be accomplished in

accordance with these instructions, procedures, or drawings. Licensee Procedure

EN-OP-104, Operability Determination Process, Revision 6, Section 5.1 step 13

required that an operability should be determined immediately upon discovery without

delay and in a controlled manner using the best information available. Contrary to this

requirement, from July 1, 2010, to July 25, 2012, the licensee failed to accomplish an

activity affecting quality prescribed by documented instructions. Specifically, the

licensee failed to determine the operability of the emergency diesel generators as

required by Licensee Procedure EN-OP-104 in response to NRC Information

Notice 2010-04. The licensee immediately determined the operability of the emergency

diesel generators based on operating data and work history, and they established a

reasonable basis for operability. This violation is being treated as an NCV, consistent

with Section 2.3.2 of the Enforcement Policy, because it was of very low safety

significance (Green) with no actual or potential safety consequences and was entered

into the licensees corrective action program as Condition Report CR-WF3-2012-03761

to address recurrence. (NCV 05000382/2012008-01, Failure to Promptly Determine the

Operability of the Emergency Diesel Generators)

b. Failure to Take Corrective Action Associated with the Emergency Feedwater Pump AB

Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, for the failure to take timely corrective

action for a condition adverse to quality. Specifically, the licensee failed to restore a

degraded condition, which included a corrective action to perform a new design analysis

for the emergency feedwater pump AB after the removal of heat trace circuit 1-8C

despite having a reasonable amount of time to complete it.

Description. The team performed an in-depth review of corrective actions associated

with the emergency feedwater system. The turbine driven emergency feedwater pump

AB has steam piping that is maintained at a high temperature with a heat trace to

prevent excessive condensation from developing, which could reduce the reliability of

the pump to perform its design function. The licensee removed heat trace circuit 1-8C

- 17 - Enclosure 2

from a horizontal section of steam piping because the heat trace was not maintaining the

piping above the required setpoint. In May 2011, the licensee determined that

emergency feedwater pump AB was operable but degraded. A corrective action was

initiated to perform a design analysis using RELAP to determine what modifications

needed to be performed on the system to return the system to a fully operable status.

The team identified that the licensee extended the due date twice for the corrective

action, first from February 23 to June 15, 2012, and then from June 15 until

October 12, 2012. The last extension was approved due to lack of engineering

resources resulting from other activities placed at a higher priority by Waterford 3

management. The team determined that from May 2011 to August 2012, a corrective

action to perform a design analysis for the long-standing equipment issue of determining

whether or not a plant modification is needed to maintain the system operable had not

been performed in a timely manner. Currently, plant operators are required once per

shift to perform temperature verifications of the heat trace to ensure condensation does

not form in the steam supply pipe to the turbine driven pump and maintain emergency

feedwater pump AB in an operable, but degraded, status until the design analysis is

complete. The licensee has entered the concern into their corrective action program as

Condition Report CR-WF3-2012-03754.

Analysis. The team determined that the failure to complete the corrective action of

performing a new design analysis to determine if emergency feedwater pump AB

required a design modification based on the analysis in a timely manner was a

performance deficiency. The performance deficiency was more than minor because it

affected the equipment performance attribute of the Mitigating Systems Cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, failure to implement

this corrective action could result in reduced reliability of the emergency feedwater pump

AB. In accordance with NRC Inspection Manual Chapter 0609, Attachment 4, "Initial

Characterization of Findings," the issue was determined to affect the Mitigating Systems

Cornerstone. In accordance with NRC Inspection Manual Chapter 0609, Appendix A,

The Significance Determination Process (SDP) for Findings at Power, the issue was

determined to have very low safety significance (Green) because it affected the design

or qualification of mitigating systems, structures, and components; however, the

systems, structures, and components maintained operability. This finding had a cross-

cutting aspect in the human performance area, resources component, in that the

licensee failed to minimize a long-standing equipment issue adequately to assure

nuclear safety H.2(a).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

states, in part, that measures be established to assure that conditions adverse to quality,

such as failures, malfunction, deficiencies, deviations and non-conformances are

promptly identified and corrected. Contrary to this requirement, from May 2011 through

August 2012, the licensee failed to assure that measures were established to assure

that a condition adverse to quality was promptly corrected. Specifically, the licensee

failed to take prompt corrective action to restore a degraded condition by not performing

- 18 - Enclosure 2

a design analysis for emergency feedwater pump AB after heat trace circuit 1-8C was

removed. Consequently, plant operators are required once per shift to perform

temperature verifications of the heat trace to ensure condensation does not form in the

steam supply pipe to the turbine driven pump and maintain emergency feedwater pump

AB in an operable, but degraded, status until the design analysis is complete. This

violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement

Policy because it was of very low safety significance (Green) with no actual or potential

safety consequence and was entered into the licensees corrective action program as

CR-WF3-2012-03754 to address recurrence. (NCV 05000382/2012008-02, Failure to

Take Corrective Action Associated with Emergency Feedwater Pump AB)

c. Failure to Take Timely Corrective Action to Establish a Basis for Flood Control Measures

Introduction. The team identified a Green cited violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, for the failure to establish measures to assure that

applicable regulatory requirements and the design basis as defined in 10 CFR 50.2 are

correctly translated into procedures. Specifically, the licensee has not determined a

basis for the level at which flood control measures are initiated, two years after receiving

a non-cited violation for the same deficiency.

Description. The team reviewed the licensees corrective actions taken in response to a

non-cited violation from 2010 documented as NCV 2010006-02, Non-conservative

Technical Specification 3.7.5 Action Statement. The licensee entered this violation into

their corrective action program under CR-WF3-2010-03232 on May 24, 2010. The

licensee determined that Technical Specification 3.7.5 Flood Protection was not

required to be included in their technical specifications and submitted an amendment to

move it to the Technical Requirements Manual. As an interim compensatory measure,

the licensee modified their Procedure OP-901-521, Severe Weather and Flooding to

include an action to start shutting flood control doors at a river level of 24 feet instead of

27 feet.

The required actions included verifying that all flood control penetrations below a level of

30 feet were shut within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> before the river was projected to reach 27 feet. There

are seven flood control doors of varying sizes that are required to be shut and two valves

that are required to be locked shut. Five of these doors and both valves are normally

shut during power operations, but may be open during outages. Most of them require

entry into the Radiologically Controlled Area and one requires entry into a locked room

for access.

The licensee recognized the need to establish a basis for initiating these actions at

24 feet, and issued Corrective Action 18 (CA-18) in CR-WF3-2010-03232 on

March 10, 2011, to formally evaluate and document whether 24 feet was an acceptable

river level elevation at which to initiate flood control measures. The CA-18 due date was

extended twice and on February 24, 2012, they determined that the methodology they

intended to use was not acceptable. CA-18 was closed to Corrective Action 23 (CA-23)

which directed the licensee to issue an engineering change using the methodology used

- 19 - Enclosure 2

in Waterford 3 UFSAR Section 2.4.3.7. The due date for CA-23 was itself extended to

September 30, 2012.

The inspection team questioned why the licensee had not completed the calculation

to justify their basis for their compensatory measures, noting that it had been over

two years since the original violation was identified. The licensee initiated

CR-WF3-2012-03752 to address this concern. The inspectors verified through

walk-downs, procedure reviews, and historical data that the licensees use of 24 feet

did not represent an immediate operability concern and that the current river level was

sufficiently low to allow time for the licensee to correct the deficiency.

Analysis. The failure to complete the corrective action to establish a basis for flood

control measures in a timely manner was a performance deficiency. The performance

deficiency was more than minor because it was associated with the protection from

external events attribute of the Mitigating Systems Cornerstone and affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences. Specifically, the

licensee failed to verify through calculations or analysis that the actions taken to secure

flood doors could be completed in time to protect safety-related equipment from flooding

due to a levee failure. In accordance with NRC Inspection Manual Chapter 0609,

Attachment 4, "Initial Characterization of Findings," the issue was determined to affect

the Mitigating Systems Cornerstone. In accordance with NRC Inspection Manual

Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings

at Power, the issue was determined to have very low safety significance (Green)

because it did not involve the loss or degradation of equipment or function specifically

designed to mitigate a seismic, flooding, or severe weather initiating event. Specifically,

the inspectors confirmed that the licensee could reasonably ensure the flood control

doors could perform their safety function. This finding had a cross-cutting aspect in the

human performance area, resources component in that the licensee failed to maintain

long term plant safety by maintenance of design margins and ensuring engineering

backlogs low enough to support safety H.2.a].

Enforcement. Title 10 of the Code of Federal Regulations Part 50, Appendix B,

Criterion III, Design Control, states, in part, that measures shall be established to

assure that applicable regulatory requirements and the design basis, as defined in

10 CFR 50.2, are correctly translated into specifications, procedures and instructions.

Contrary to the above, from March 10, 2011, to August 2, 2012, the licensee failed to

establish measures to assure that applicable regulatory requirements and the design

basis, as defined in 10 CFR 50.2, were correctly translated into specifications,

procedures and instructions. Specifically, the licensee had not established a design

basis to determine the river level at which flood control measures were to be initiated for

closing the water tight doors, as required in Procedure OP-901-521, Severe Weather

and Flooding. The licensee demonstrated sufficient safety margin based on historical

data and current river levels to provide assurance that this is not an immediate safety

concern. Due to the licensees failure to restore compliance within a reasonable time

- 20 - Enclosure 2

following previous NCV 05000382/2010006-02, this violation is being cited as a Notice of

Violation consistent with Section 2.3.2 of the NRC Enforcement Policy. This is a

violation of 10 CFR 50, Appendix B, Criterion III. A Notice of Violation is attached.

(VIO 05000382/2012008-03, Failure to Take Timely Corrective Action to Establish a

Basis for Flood Control Measures)

d. Failure to Ensure Operator Knowledge of Equipment Status

Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for a failure to follow

Procedure EN-OP-115, Conduct of Operations. Specifically, the licensee failed to

ensure that control room operators knew the status of equipment at all times.

Description. The team reviewed how the licensee was addressing deficiencies in plant

instrumentation, controls, and equipment that impacted the ability of operators to

properly operate the plant. This included a review of the licensees program to identify,

compensate for, and correct these plant deficiencies and a walk-down of the control

room.

While interviewing the person responsible for tracking plant deficiencies, the inspectors

discovered that the licensee had two separate governing procedures. The licensee used

the Entergy Fleet Administrative Procedure EN-FAP-OP-006, Operator Aggregate

Impact Index Performance Indicator, to track several categories of plant deficiencies in

a standardized spreadsheet. The licensee also had the local departmental Operating

Instruction OI-002-000, Annunciator, Control Room Instrumentation and Workarounds

Status Control. This instruction had different definitions for categories of plant

deficiencies and directed the use of a different database.

The inspectors then interviewed the on shift operators in the control room and reviewed

both databases. The inspectors identified several issues:

  • The person responsible for tracking plant deficiencies was only using the fleet

administrative procedure and was unaware of the operating instruction.

  • On one shift, the shift technical advisor believed the fleet administrative

procedure was being used and was not aware of the operating instruction,

while the control room supervisor believed the operating instruction was

being used and was not aware of the fleet administrative procedure.

  • The database required by the operating instruction had not been maintained

for two years.

  • The operating instruction did not have a category for Operator Burdens;

however, the shift crew differentiated between Operator Workarounds and

Operator Burdens. In most cases, they chose the less conservative

designation of Operator Burden.

- 21 - Enclosure 2

  • The fleet administrative procedure was intended for fleet performance

reporting, not plant deficiency control. It does not direct any actions to

address and correct plant deficiencies.

  • The operating instruction subcategorizes Workarounds by scheduling of

resources rather than by risk significance or impact to operators. The fleet

administrative procedure does not subcategorize Operator Workarounds or

Operator Burdens, but the licensee carried over this practice to the fleet

administrative procedure spreadsheet. This could lead to improper

prioritization of corrective actions.

  • The operating instruction directs identification of plant deficiencies through a

review of work requests, but it does not require a review of condition reports.

  • Some plant deficiencies were not entered into either database.
  • Operators were using the same tags for Control Room Deficiencies and

informal operator notes. These notes are not controlled by either procedure.

  • A list of plant deficiencies was not immediately available to control room

operators.

The inspectors determined that when the fleet administrative procedure was issued in

March 2010, the licensee changed their process for tracking deficiencies. The licensee

Procedure W2.109, Procedure Development, Review & Approval, is safety-related and

requires implementation and maintenance of procedures and departmental instructions.

This procedure prescribes a process for approving and revising procedures and

instructions and conducting necessary training. When the licensee began tracking plant

deficiencies per the fleet administrative procedure, the licensee did not revise the

operating instruction to conform to the new process, and the licensee did not train all

affected personnel on the new process. As a result, the operators did not maintain a

consistent accurate list and were not aware of all plant deficiencies, and therefore were

not aware of the status of all plant equipment. This was not in accordance with

Procedure EN-OP-115, Conduct of Operations, Revision 9, Section 5.13 step 1, which

states that the status of plant equipment is known at all times by plant operators.

The licensee initiated CR-WF3-2012-03732 to address the issue. The licensee will

revise the operating instruction to address the process issues and make the intended

changes.

Analysis. The failure to ensure that operators were aware of the status of all plant

equipment was a performance deficiency. The performance deficiency was more than

minor because it was associated with the procedure quality attribute of the Initiating

Events Cornerstone and affected the cornerstone objective to limit the likelihood of those

events that upset plant stability and challenge critical safety functions during shutdown

as well as power operations. Specifically, the licensee failed to implement a procedure

designed to ensure operators were aware of deficiencies in the instrumentation, controls,

- 22 - Enclosure 2

and operation of nuclear plant systems. In accordance with NRC Inspection Manual

Chapter 0609, Attachment 4, "Initial Characterization of Findings," the issue was

determined to affect the Initiating Events Cornerstone. In accordance with NRC

Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process

(SDP) for Findings at Power, the issue was determined to have very low safety

significance (Green) because it did not cause a reactor trip and the loss of mitigation

equipment relied upon to transition the plant from the onset of the trip to a stable

shutdown condition. This finding had a cross-cutting aspect in the human performance

area, work practices component, in that the licensee failed to define and effectively

communicate expectations regarding procedural compliance, and personnel did not

follow procedures H.4.b].

Enforcement. Title 10 of the Code of Federal Regulations Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, states, in part, that activities

affecting quality shall be prescribed by documented instructions, procedures, or

drawings of a type appropriate to the circumstance and shall be accomplished in

accordance with these instructions, procedures, or drawings. Procedure EN-OP-115,

Conduct of Operations, Revision 9, Section 5.13, step 1, states that the status of plant

equipment is known at all times by plant operators. Contrary to this requirement, from

March 2, 2010, to August 1, 2012, the licensee failed to accomplish an activity affecting

quality in accordance with the documented instructions appropriate to the circumstance.

Specifically, the licensee failed to ensure operators knew the status of plant equipment

at all times in accordance with Licensee Procedure EN-OP-115, Conduct of

Operations. The licensee has a corrective action to revise their operating instruction for

tracking plant deficiencies, and none of the current plant deficiencies represents an

immediate safety concern. This violation is being treated as an NCV, consistent with

Section 2.3.2 of the Enforcement Policy, because it was of very low safety significance

(Green) with no actual or potential safety consequences and was entered into the

licensees corrective action program as CR-WF3-2012-03732 to address recurrence.

(NCV 05000382/2012008-04, Failure to Ensure Operator Knowledge of Equipment

Status)

e. Failure to Develop Effective Corrective Actions to Preclude Repetition

Introduction. The inspectors identified a non-cited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Actions, because the licensee failed to determine

the cause of a significant condition adverse to quality and take corrective actions to

prevent recurrence. Specifically, the licensee failed to assure that the cause of the

condition was determined and corrective action taken to preclude repetition associated

with a contractors non-compliance with site procedural requirements.

Description. During refuel outage 16 in 2009, contract instrumentation and control

technicians performed a functional test on a feedwater heater level switch according to

work order instructions. Following restoration, a plant transient occurred because a

valve was out of position (CR-WF3-2009-7420). The licensee determined that the event

constituted a significant condition adverse to quality in accordance with guidance from

Procedure EN-LI-102, Corrective Action Process. During the valve manipulation, the

- 23 - Enclosure 2

work instructions called for concurrent verification. However the licensees root cause

analysis determined that the contract workers failed to perform concurrent verification as

required by the procedure (NCV 2011003-04). The contract workers knew the

procedural requirement, but they behaved inappropriately when they chose not to follow

the instructions. The licensees root cause analysis did not determine why the contract

workers chose not to follow the procedure. The licensees corrective action to preclude

repetition (CAPR) of this significant condition adverse to quality (SCAQ) was to release

the contract workers for not following the procedure and prohibit them from future work

at Entergy sites. No actions to preclude repetition that addressed the underlying cause

of the failure to perform concurrent verification were taken. The team identified that

despite guidance provided in Procedure EN-LI-118, Attachment 9.9, Root Cause

Evaluation Process, which states that discipline of individuals is not an appropriate

CAPR, disciplinary action was the only CAPR identified in the root cause for

CR-WF3-2009-07420 performed on January 7, 2010.

The failure to determine the cause of a significant condition adverse to quality and take

corrective action to preclude repetition had no actual consequences on nuclear plant

safety. However, the failure to determine the cause of the condition adverse to quality

and take corrective action to preclude repetition from an ineffective CAPR has the ability

to lead to more significant safety consequences. The licensee documented this violation

in Condition Reports CR-WF3-2012-03769 and CR-WF3-2012-03772. The corrective

actions include developing additional training and provisions to provide additional

contractor oversight.

Analysis. The failure to determine the cause of a significant condition adverse to quality

and take corrective action to preclude repetition was a performance deficiency. The

performance deficiency was more than minor because if left uncorrected, it could lead to

more significant consequences, therefore it is a finding. Specifically, failure to determine

the cause of a significant condition adverse to qualify and take corrective action to

prevent recurrence can result in recurrence of the condition. In accordance with NRC

Inspection Manual Chapter 0609, Attachment 4, "Initial Characterization of Findings," the

issue was determined to affect the Initiating Events Cornerstone. In accordance with

NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination

Process (SDP) for Findings at Power, the issue was determined to have very low safety

significance (Green) because the finding did not cause a reactor trip and the loss of

mitigation equipment relied upon to transition the plant from the onset of the trip to a

stable shutdown condition. This finding had a cross-cutting aspect in the human

performance, work practice component, in that the licensee failed to follow guidance in

the root cause evaluation procedure when developing appropriate corrective actions to

prevent repetition H.4(b).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

states, in part, in the case of significant conditions adverse to quality, the measures shall

assure that the cause of the condition is determined and corrective action taken to

preclude repetition. Contrary to this requirement, on January 7, 2010, for a significant

condition adverse to quality, the licensee failed to take measures to assure that the

cause of the condition was determined and corrective actions taken to preclude

- 24 - Enclosure 2

repetition. Specifically, the licensee did not determine the underlying cause of the failure

of the site contract workers to comply with licensees procedural requirements nor were

corrective actions taken to preclude repetition of the condition. The licensees corrective

actions to address this problem include developing additional training and provisions to

provide additional contractor oversight. This violation is being treated as an NCV,

consistent with Section 2.3.2 of the Enforcement Policy because it was of very low safety

significance (Green) with no actual or potential safety consequence and was entered

into the licensees corrective action program as CR-WF3-2012-03769 and

CR-WF3-2012-03772 to address recurrence. (NCV 05000382/2012008-05, Failure to

Develop Effective Corrective Actions to Preclude Repetition)

4OA6 Meetings

Exit Meeting Summary

On August 2, 2012, the team presented the inspection results to Keith Nichols, Director of

Engineering, and other members of the licensee staff. The licensee acknowledged the issues

presented. The inspector asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was identified.

On August 23, 2012, the team exited with the revised characterization of the inspection results

to William McKinney, Acting Director Nuclear Safety and Assurance, and other members of the

licensee staff. The licensee acknowledged the issues presented.

On September 24, 2012, the team exited with the revised characterization of the inspection

results to Keith Nichols, Director of Engineering, and other members of the licensee staff. The

licensee acknowledged the issues presented.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee

and is a violation of NRC requirements, which meets the criteria of Section VI of the

NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

  • Title 10 of the Code of Federal Regulations Part 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, states, in part, that activities affecting quality

shall be prescribed by documented instructions, procedures, or drawings and shall be

accomplished in accordance with these instructions, procedures, or drawings. Contrary

to this requirement, on May 10 and May 12, 2011, the licensee failed to accomplish an

activity affecting quality as prescribed by the documented procedure. Specifically, the

licensee failed to perform operability reviews when heat trace circuit 1-8C fell below the

operating instruction temperature on the steam supply piping to the emergency

feedwater pump in accordance with Procedure EN-OP-104, Operability Determination

Process. The team determined that this finding was of very low safety significance

(Green) because it affected the design or qualification of a mitigating system structure

component; however, the system structure component maintained its operability.

- 25 - Enclosure 2

The emergency feed water pump AB was declared inoperable on May 14, 2011;

however, subsequent evaluation declared the pump operable but degraded.

This was documented in the licensees corrective action program as Condition

Reports CR-WF3-2011-03599 and CR-WF3-2011-03600.

ATTACHMENTS: SUPPLEMENTAL INFORMATION

INFORMATION REQUEST

- 26 - Enclosure 2

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

S. Adams, Planning Scheduling and Outage Manger

J. Bourgeois, Acting Chemistry Manager

E. Brauner, Supervision of System Engineering

K. Cook, General Manager, Plant Operations

G. Fey, Emergency Planning Manager

S. Fontenot, Acting Corrective Actions and Assessment Manager

R. Gilmore, Engineering and Components Manager

J. Gumnick, Radiation Protection Manager

D. Jacobs, Site Vice President, Operations

J. Jarrell, Assistant Operations Shift Manager

B. Lanka, Manager, System Engineering Manager

B. Lindsey, Maintenance Manager

M. Mason, Acting Licensing Manager

W. McKinney, Acting Director Nuclear Safety and Assurance

K. Nichols, Director of Engineering

R. Porter, Design Engineering Manager

D. Rieder, Quality Assurance Supervisor

K. Rockwood, Acting Technical Training Supervisor

T. Sanders, Security Superintendant

P. Stanton, Design Engineering Supervisor

NRC Personnel

R. Kumana, Project Engineer

R. Smith, Team Leader/Senior Resident Inspector

D. Overland, Resident Inspector

M. Young, Reactor Inspector

A1-1 Attachment 1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000382/2012008-03 VIO Failure to Take Timely Corrective Action to Establish a Basis for

Flood Control Measures (Section 4OA2.5.c)

Opened and Closed

05000382/2012008-01 NCV Failure to Promptly Determine the Operability of the Emergency

Diesel Generators (Section 4OA2.5.a)05000382/2012008-02 NCV Failure to Take Corrective Action Associated with Emergency

Feedwater Pump AB (Section 4OA2.5.b)05000382/2012008-04 NCV Failure to Ensure Operator Knowledge of Equipment Status

(Section 4OA2.5.d)05000382/2012008-05 NCV Failure to Develop Effective Corrective Actions to Preclude

Repetition (Section 4OA2.5.e)

A1-2 Attachment 1

LIST OF DOCUMENTS REVIEWED

PROCEDURES

NUMBER TITLE REVISION

EN-LI-104 Self-Assessment and Benchmark Process 8

EN-LI-102 Corrective Action Process 19

EN-LI-118 Root Cause Evaluation Process 17

EN-LI-119 Apparent Cause Evaluation (ACE) Process 15

EN-OP-104 Operability Determination Process 6

EN-QV-100 Conduct of Nuclear Oversight 7

EN-QV-102 Quality Control Inspection Program 1

EN-QV-108 QA Surveillance Process 9

EN-MA-101 Fundamentals of Maintenance 10

OP-901-310 Loss of Train A Safety Bus 308

OP-903-115 Train A Integrated Emergency Diesel Generator / 21

Engineering Safety Features Test

ME-007-005 Time Delay Relay Setting Check, Adjustment and 16

Functional Test

EN-TQ-201 Systematic Approach to Training Process 12

EN-TQ-201 Systematic Approach to Training Process 13

TM-OP-100 Operations Training Manual 16

EN-TQ-114 Licensed Operator Requalification Training Program 3

Description

EN-TQ-126 Inprocessing Training Program 6

A1-3 Attachment 1

NUMBER TITLE REVISION

EN-TQ-126 Inprocessing Training Program 8

EN-TQ-107 General Employee Training 7

EN-EC-100 Guidelines For Implementation Of The Employee 6

Concerns Program

EN-MA-133 Control of Scaffolding 8

OP-002-007 Freeze Protection and Temperature Maintenance 18

EN-IS-102 Confined Space Program 8

OP-903-046 Emergency Feed Pump Operability Check 309

EN-NE-G-013 Human Reliability Analysis for PSA Models 1

OP-009-003 Emergency Feedwater 304

EN-FAP-OP-006 Operator Aggregate Impact Index Performance Indicator 0

OI-002-000 Operator Instruction Annunciator, Control Room 304

Instrumentation and Workarounds Status Control

EN-OP-137 Licensed Operator Candidate Selection Process 2

EN-LI-125 NRC Cross-Cutting Analysis and Trending 1

EN-OE-100 Operating Experience Program 14

EN-LI-118-06 Common Cause Analysis (CCA) 3

OP-002-007 Freeze Protection and Temperature Maintenance 18

OP-903-053 Fire Protection System Pump Operability Test 17

UNT-005-013 Fire Protection Program 12

EN-FAP-LI-001 Condition Review Group (CRG) 3

A1-4 Attachment 1

NUMBER TITLE REVISION

EN-FAP-LI-003 Corrective Action Review Board (CARB) Process 8

EN-HU-103 Human Performance Error Reviews 7

EN-HU-106 Procedure and Work Instruction Use and Adherence 0

EN-PL-202 Personnel Expectations Related to Fatigue Management 0

EN-TQ-113 Initial Licensed Operator Training Program Description 7

OP-100-014 Technical Specification and Technical Requirements 317

Compliance

OP-901-521 Severe Weather and Flooding 305

EN-OE-100 Operating Experience Program 14

EN-FAP-AD-001 Fleet Administrative Procedure (FAP) Process 0

EN-AD-101-01 NMM Procedure Writer Manual 9

EN-AD-101 Procedure Process 14

EN-PL-155 Entergy Nuclear Change Management 4

W2.109 Procedure Development, Review & Approval 13

EN-NS-102 Fitness For Duty Program 9

EN-NS-117 Fitness For Duty Processes 6

EN-OM-123-02 Working Hour Limits eSOMS Users Guide 1

EN-OM-123 Fatigue Management Program 4

EN-PL-202 Personnel Expectations Related to Fatigue Management 0

EN-OP-115 Conduct of Operations 9

A1-5 Attachment 1

CALCULATIONS

NUMBER TITLE REVISION

EC-C97-003 Probabilistic Evaluation of Tornado Missile Strike for 0, Change 1

Waterford 3 Nuclear Station

EC-M00-004 Thermal-Hydraulic Calculation for the EFW Steam Supply 0

Valves (MS-401A(B)) and Lines

Calculation No. Flooding Analysis Outside Containment 4

MNQ3-5

EC-M99-010 Minimum Flow for DCT Sump Pump 0-2

134669-G-07 Scour Analysis and Scour Protection Design from a 1

Hypothetical Levee Break

DRAWINGS

NUMBER TITLE REVISION

G-153 Feedwater, Condensate & Air Evacuation Systems

G-151 Flow Diagram Main & Extraction Steam System 43

G-924 HVAC - Water Treatment Bldg. & Fire Pump House 6

G1370 Fire Protection Turbine Bldg. 2

OTHER DOCUMENTS

NUMBER TITLE REVISION/

DATE

QS-2012-W3-008 QA Follow-up Surveillance of Category A Condition 1

Reports initiated during April 2012

QS-2012-W3-007 QA Follow-up review of EN-QV-126 required issues 1

initiated January, February, and March 2012

QS-2011-W3-015 QA Follow-up Surveillance of Category A Condition July 26, 2011

Reports initiated during September, 2011

QS-2011-W3-012 QA Follow-up Surveillance of the 2011 Corrective September 12,

Action Program (CAP) Audit 2011

A1-6 Attachment 1

NUMBER TITLE REVISION/

DATE

QS-2011-W3-009 QA Follow-up Surveillance of Quality Assurance 1

Finding CR-WF3-2011-3084

QS-2011-W3-008 QA Follow-up Surveillance of Category A Condition June 13, 2011

Reports Initiated During May 2011

QS-2011-W3-007 QA Follow-up Surveillance of Category A Condition 1

Reports Initiated During April 2011

QS-2011-W3-006 QA Follow-up to Category A Condition Reports for 1

January and February 2011

LO-WLO-2011- Quality of Causal Analysis Focused Assessment October 13, 2011

0007

LO-WLO-2011- Maintenance Training Focused Self-Assessment July 29, 2011

0053 (I&C, Mechanical, Electrical)

LO-WLO-2011- Quality Assurance Self-Assessment Report December 9, 2011

0124

LO-WLO-2012- Snapshot Assessment / Benchmark On: PME May 23, 2012

0015 Performance

LO-WLO-2012- Snapshot Assessment / Benchmark On: February 6, 2012

0030 Maintenance - Advanced Qualifications

OE34343- Seismic Monitoring Systems Failed to Actuate September 1, 2011

20111008 During a Seismic Event

OE35212- Extraction Steam System Carbon Steel Reducer November 3, 2011

20120211 found Below Design Minimum Wall due to

Unpredicted Flow-Accelerated Corrosion

OE34934- Nuclear Regulatory Commission Red Finding Root December 9, 2011

20120107 Cause Analysis Results

LO-WLO-2010- Licensed Operator Requal 71111.11 Pre-Inspection March 3, 2011

00143 Assessment

WLO-2011-00018 Evaluate the Effectiveness of Waterford 3 Shift November 3, 2011

Manager/STA Training Program

LOR/STAR Examination # WWEX-LOR-11046R/S 2011

Biennial Written Examination # WEX-LOR-11043R/S

Exam Worksheet

A1-7 Attachment 1

NUMBER TITLE REVISION/

DATE

Site Broadcast RCA Drain Limitations February 16, 2012

Waterford 3 - 2010 Employee Concerns Data

Analysis

Waterford 3 - 2011 Employee Concerns Data

Analysis

FCBT-GET- Entergy Fleet Specific Plant Access Training 17

PATSS

Training Review Group Meeting Minutes June 9, 2010

WLP-TRNC-SATR Focused SAT Review 2

2nd QTR 2010 Instructor Continuing Training Kickoff

LO-WLO-2010- Waterford 3 Equipment Reliability and Core May 27-29, 2010

0059 Business Focused Self Assessment

LO-WLO-2010- WF3 IST Program Focused Self Assessment August 20-24, 2010

0091

LO-WLO-2011- Snapshot Assessment/Benchmark on: Relief Valve October 26, 2011

0041 Program

WH-TB-11-5-A2 Evaluation Summary: Evaluation of Downstream June 14, 2011

Sump Debris Effects in Support of GSI-191

TB-11-5 Assessment of WCAP-16406-P-A Abrasive Wear March 1, 2011

Model and Recommendations

WH-TB-10-4-A2 Evaluation Summary: CEDM Upper Pressure August 17, 2010

Housing Venting

TB-10-4 Potential for Stress Corrosion Cracking in Control April 12, 2010

Element Drive Mechanism Upper Pressure Housing

SD-EFW Emergency Feedwater 11

DCP-3506 Auxiliary Steam Test Connection for EFW Pump March 12, 1997

A/B

A1-8 Attachment 1

NUMBER TITLE REVISION/

DATE

DCP-3506 Auxiliary Steam Test Connection for EFW Pump July 24, 1998

A/B

DCP-3506 Auxiliary Steam Test Connection for EFW Pump February 25, 1999

A/B

DCP-3506 Auxiliary Steam Test Connection for EFW Pump May 26, 1999

A/B

DC-3526 EFW Heat Trace Reliability Improvements September 3, 1999

EC 37263 Replacement of MCC DCT Cubicle Compartments 0

Operability Assistance Tool

STI-WO-275977 CS117A, Shutdown Cooling Heat Exchanger 0

Discharge Stop Check Valve Leakage Test

EC 31375 Clarify Safety Function and Leakage Criteria for CS- Draft

111A(B) and CS-117A(B)

W3-DBD-003 Emergency Feedwater System 301

CRG Report for Tuesday July 31, 2012

CRG Report for Thursday August 2, 2012

Operational Focus July 31, 2012

Operational Focus August 2, 2012

LO-WLO-2010- Status of the Safety Conscious Work Environment July 6, 2010

00061 in Security

LO-WLO-2012- Operations Assessment of Plant Status and March 1, 2012

006 Configuration Control

A1-9 Attachment 1

NUMBER TITLE REVISION/

DATE

LPL-EQA-4.2B Environmental Qualification Assessment on Allis- 2

Chalmers Form Wound Motors Used in the

Waterford SES Unit No. 3

NRC IN 2010-04 Diesel Generator Voltage Regulation System February 26, 2010

Component Due to Latent Manufacturing Defect

NRC-IN-2010-04- Entergy OE A2 Evaluation Summary July 1, 2010

A2-WF3-0002-001

OP-903-053 V134 Fire Protection System Pump Operability Test January 9, 2008

OP-903-053 V135 Fire Protection System Pump Operability Test June 18, 2009

ER-W3-2002- Diesel Fire Pump Louvers 0

0429-000

WSES-FSAR- Updated Final Safety Analysis Report

UNIT-3

OP-903-053 V136 Fire Protection System Pump Operability Test August 25, 2011

W3-DBD-018 Fire Protection 0

NPF-38 Waterford Operating License

W3-DBD-037 Nuclear Island and Building Design - RCB 1

Ltr from A H Wern Waterford SES Unit No. 3 Levee Stability Analysis December 7, 1972

TS 3.7.5 Flood Protection NA

W3F1-2011-0018 License Amendment Request to Relocate Technical November 21, 2011

Specifications to the Technical Requirements

Manual Waterford Steam Electric Station Unit 3

AR079684 Scope Revision to PMID 6718 incorporate EPRI December 12, 2009

Recommend Pdm

A1-10 Attachment 1

NUMBER TITLE REVISION/

DATE

Annual Work Hour Review & Fatigue Assessment 2010

Summary

Annual Work Hour Review & Fatigue Assessment 2011

Summary

ODMI SI MTRP0001 Auto Vent 0

ODMI LPSI A Gas Accumulation 14

Entergy System Workplace Violence and Weapons 1

Policies &

Procedures

EN-IS-111 General Industrial Safety Requirements 11

PS-011-102 Personnel Access Control 308

PS-011-103 Vehicle Access Control 303

PS-011-110 Security Owner Controlled Area Vehicle and 010

Personnel Access Control

Waterford 3 Accreditation Board Report September 2010

CONDITION REPORTS

CR-WF3-2012-03424 CR-WF3-2012-03461 CR-WF3-2012-03479

CR-WF3-2012-03495 CR-WF3-2012-03557 CR-WF3-2012-03596

CR-WF3-2012-03701 CR-WF3-2012-03729 CR-WF3-2012-03732

CR-WF3-2012-03736 CR-WF3-2012-03744 CR-WF3-2012-03745

CR-WF3-2012-03747 CR-WF3-2012-03752 CR-WF3-2012-03754

CR-WF3-2012-03761 CR-WF3-2012-03657 CR-WF3-2012-03658

CR-WF3-2012-03659 CR-WF3-2012-03660 CR-WF3-2012-03661

CR-WF3-2012-03662 CR-WF3-2012-03663 CR-WF3-2012-03664

CR-WF3-2012-03665 CR-WF3-2012-03666 CR-WF3-2012-03667

CR-WF3-2012-03668 CR-WF3-2012-03669 CR-WF3-2012-03670

CR-WF3-2012-03671 CR-WF3-2012-03672 CR-WF3-2012-03736

CR-WF3-2012-03709 CR-WF3-2012-03710 CR-WF3-2012-03711

CR-WF3-2012-03712 CR-WF3-2012-03713 CR-WF3-2012-03714

A1-11 Attachment 1

CONDITION REPORTS

CR-WF3-2012-03715 CR-WF3-2012-03716 CR-WF3-2012-03717

CR-WF3-2012-03718 CR-WF3-2012-03719 CR-WF3-2012-03720

CR-WF3-2012-03721 CR-WF3-2012-03722 CR-WF3-2012-03723

CR-WF3-2012-03724 CR-WF3-2012-03725 CR-WF3-2012-03726

CR-WF3-2012-03727 CR-WF3-2012-03728 CR-WF3-2012-03729

CR-WF3-2012-03730 CR-WF3-2012-03731 CR-WF3-2012-03732

CR-WF3-2012-03733 CR-WF3-2012-03734 CR-WF3-2012-03735

CR-WF3-2012-03736 CR-WF3-2012-03737 CR-WF3-2012-03738

CR-WF3-2012-03739 CR-WF3-2012-03740 CR-WF3-2012-03741

CR-WF3-2012-03742 CR-WF3-2010-03235 CR-WF3-2011-07469

CR-WF3-2009-07420 CR-WF3-2010-01166 CR-WF3-2010-03660

CR-WF3-2010-07223 CR-WF3-2010-06219 CR-WF3-2010-02721

CR-WF3-2011-06832 CR-WF3-2011-00679 CR-WF3-2011-01927

CR-WF3-2011-03163 CR-WF3-2011-07602 CR-WF3-2011-03636

CR-WF3-2011-03190 CR-WF3-2011-06205 CR-WF3-2011-04481

CR-WF3-2011-01356 CR-WF3-2011-07605 CR-WF3-2011-02005

CR-WF3-2011-07606 CR-WF3-2011-06254 CR-WF3-2011-07610

CR-WF3-2011-02927 CR-WF3-2011-03084 CR-WF3-2011-00458

CR-WF3-2011-01737 CR-WF3-2012-01048 CR-WF3-2012-00015

CR-WF3-2012-00351 CR-WF3-2012-06832 CR-WF3-2012-01419

CR-WF3-2012-03496 CR-WF3-2010-02940 CR-HQN-2006-00605

CR-WF3-2011-07845 CR-WF3-2011-03522 CR-WF3-2011-03523

CR-WF3-2011-03525 CR-WF3-2011-03526 CR-WF3-2011-03527

CR-WF3-2011-08044 CR-WF3-2011-08045 CR-WF3-2011-08046

CR-WF3-2011-08048 CR-WF3-2011-08049 CR-WF3-2011-08050

CR-WF3-2010-07466 CR-WF3-2011-00553 CR-WF3-2011-06203

CR-WF3-2011-07610 CR-WF3-2011-06204 CR-WF3-2011-08150

CR-WF3-2011-03550 CR-WF3-2011-05841 CR-WF3-2011-07603

CR-WF3-2011-06852 CR-WF3-2011-03350 CR-WF3-2011-05841

CR-WF3-2011-06850 CR-WF3-2012-00013 CR-WF3-2012-00021

CR-WF3-2012-00014 CR-WF3-2012-00818 CR-WF3-2012-01477

CR-WF3-2007-01955 CR-WF3-2012-00837 CR-WF3-2012-01476

CR-WF3-2010-06760 CR-WF3-2011-00217 CR-WF3-2010-02278

CR-WF3-2011-06653 CR-WF3-2012-00024 CR-WF3-2010-01330

CR-WF3-2010-03660 CR-WF3-2010-03050 CR-WF3-2011-03636

CR-WF3-2009-00655 CR-WF3-2009-1276 CR-WF3-2008-04000

CR-WF3-2011-00415 CR-WF3-2011-04935 CR-WF3-2012-00530

CR-WF3-2000-01334 CR-WF3-2012-01334 CR-WF3-2012-03495

CR-WF3-2012-00632 CR-WF3-2011-01737 CR-WF3-2010-07223

CR-WF3-2010-06219 CR-WF3-2011-00458 CR-WF3-2011-00836

CR-WF3-2012-02902 CR-WF3-2012-03190 CR-WF3-2010-04364

CR-WF3-2012-03736 CR-WF3-2012-03461 CR-WF3-2010-03235

CR-WF3-2010-03564 CR-WF3-2010-00686 CR-WF3-2010-02857

CR-WF3-2009-00802 CR-WF3-2010-00341 CR-WF3-2010-02584

CR-WF3-2012-01576 CR-WF3-2012-01581 CR-WF3-2012-00569

A1-12 Attachment 1

CONDITION REPORTS

CR-WF3-2012-02314 CR-WF3-2011-03807 CR-WF3-2012-03424

CR-WF3-2011-00544 CR-WF3-2011-08043 CR-WF3-2010-04199

CR-WF3-2011-00934 CR-WF3-2011-08047 CR-WF3-2011-01168

CR-WF3-2011-04562 CR-WF3-2011-01965 CR-WF3-2011-00987

CR-WF3-2011-08140 CR-WF3-2011-02546 CR-WF3-2010-05595

CR-WF3-2011-03811 CR-WF3-2012-01044 CR-WF3-1999-00708

CR-WF3-2011-00836 CR-WF3-2011-07603 CR-WF3-2012-00659

CR-WF3-2012-01045 CR-WF3-2011-06573 CR-WF3-2011-06254

CR-WF3-2010-02672 CR-WF3-2011-06870 CR-WF3-2012-01380

CR-HQN-2010-00503 CR-WF3-2012-00507 CR-WF3-2012-03067

CR-WF3-2011-03524 CR-WF3-2012-00507 CR-WF3-2009-04155

CR-WF3-2010-02135 CR-WF3-2010-00213 CR-WF3-2010-00036

CR-HQN-2012-00857 CR-WF3-2006-03416 CR-WF3-2007-04464

CR-WF3-2009-02487 CR-WF3-2009-03499 CR-WF3-2009-04155

CR-WF3-2010-00812 CR-WF3-2010-00890 CR-WF3-2010-02302

CR-WF3-2010-02721 CR-WF3-2010-02927 CR-WF3-2010-03099

CR-WF3-2010-03565 CR-WF3-2010-03588 CR-WF3-2010-03595

CR-WF3-2010-04344 CR-WF3-2010-04352 CR-WF3-2010-04634

CR-WF3-2010-04641 CR-WF3-2010-04659 CR-WF3-2010-04785

CR-WF3-2010-05141 CR-WF3-2010-05927 CR-WF3-2010-05929

CR-WF3-2010-07232 CR-WF3-2010-07276 CR-WF3-2010-07362

CR-WF3-2010-07552 CR-WF3-2011-00030 CR-WF3-2011-00553

CR-WF3-2011-00786 CR-WF3-2011-01897 CR-WF3-2011-01965

CR-WF3-2011-02546 CR-WF3-2011-03350 CR-WF3-2011-03465

CR-WF3-2011-03618 CR-WF3-2011-04230 CR-WF3-2011-05320

CR-WF3-2011-05779 CR-WF3-2011-05840 CR-WF3-2011-06166

CR-WF3-2011-06303 CR-WF3-2011-06573 CR-WF3-2011-06701

CR-WF3-2011-07443 CR-WF3-2011-07462 CR-WF3-2011-08055

CR-WF3-2011-08060 CR-WF3-2011-08081 CR-WF3-2011-08150

CR-WF3-2012-00315 CR-WF3-2012-00632 CR-WF3-2012-00659

CR-WF3-2012-00772 CR-WF3-2012-00797 CR-WF3-2012-00891

CR-WF3-2012-01139 CR-WF3-2012-01173 CR-WF3-2012-01503

CR-WF3-2012-01581 CR-WF3-2012-01605 CR-WF3-2012-01660

CR-WF3-2012-02046 CR-WF3-2012-02315 CR-WF3-2012-03232

CR-WF3-2012-03479 CR-WF3-2012-03596 CR-WF3-2012-03701

CR-WF3-2012-03732 CR-WF3-2012-03747 CR-WF3-2012-03752

CR-WF3-2012-03764 CR-WF3-2011-02519 CR-WF3-2012-01956

CR-WF3-2009-02172 CR-WF3-2011-03582 CR-WF3-2012-03325

CR-WF3-2009-05353 CR-WF3-2011-05625 CR-WF3-2012-03729

CR-WF3-2010-02672 CR-WF3-2011-06203 CR-WF3-2012-03761

CR-WF3-2010-03232 CR-WF3-2011-07415 CR-ANO-C-2011-00441

CR-WF3-2010-03809 CR-WF3-2011-08059 CR-WF3-2010-07466

CR-WF3-2010-04638 CR-WF3-2011-08308 CR-WF3-2011-00594

CR-WF3-2010-05046 CR-WF3-2012-00746 CR-WF3-2012-01507

CR-WF3-2010-06531 CR-WF3-2012-01014

A1-13 Attachment 1

WORK ORDERS

248856 52230980 289449

275977 196828 262164

283919 256250 64753

205779 296253 303342

296271 305641 52340992

52356683 52371026 52376231

52389001 254348 257755

246482 254493 263585

286950 261413 279127

298743 28810 287883

245561 52382399 52351187

254203

A1-14 Attachment 1

Information Request

June 11, 2012

Biennial Problem Identification and Resolution Inspection - Waterford 3 Nuclear

Generating Station

Inspection Report 2012008

This inspection will cover the period from May 1, 2010, to June 1, 2012. All requested

information should be limited to this period unless otherwise specified. To the extent possible,

the requested information should be provided electronically in Adobe PDF or Microsoft Office

format. Lists of documents should be provided in Microsoft Excel or a similar sortable format.

A supplemental information request will likely be sent during the week of July 9, 2012.

Please provide the following no later than June 30, 2012:

1. Document Lists

Note: for these summary lists, please include the document/reference number, the

document title or a description of the issue, initiation date, and current status. Please

include long text descriptions of the issues.

a. Summary list of all corrective action documents related to significant conditions

adverse to quality that were opened, closed, or evaluated during the period

b. Summary list of all corrective action documents related to conditions adverse to

quality that were opened or closed during the period

c. Summary lists of all corrective action documents which were upgraded or

downgraded in priority/significance during the period

d. Summary list of all corrective action documents that subsume or roll up one or

more smaller issues for the period

e. Summary lists of operator workarounds, engineering review requests and/or

operability evaluations, temporary modifications, and control room and safety

system deficiencies opened, closed, or evaluated during the period

f. Summary list of plant safety issues raised or addressed by the Employee

Concerns Program (or equivalent)

g. Summary list of all Apparent Cause Evaluations completed during the period

h. Summary list of all Root Cause Evaluations planned or in progress, but not

complete at the end of the period

2. Full Documents, with Attachments

a. Root Cause Evaluations completed during the period

A2-1 Attachment 2

b. Quality assurance audits performed during the period

c. All audits/surveillances performed during the period of the Corrective Action

Program, of individual corrective actions, and of cause evaluations

d. Corrective action activity reports, functional area self-assessments, and non-

NRC third party assessments completed during the period (do not include INPO

assessments)

e. Corrective action documents generated during the period for the following:

i. NCVs and Violations issued to Waterford 3

ii. LERs issued by Waterford 3

f. Corrective action documents generated for the following, if they were determined

to be applicable to Waterford 3 (for those that were evaluated, but determined

not to be applicable, provide a summary list):

i. NRC Information Notices, Bulletins, and Generic Letters issued or

evaluated during the period

ii. Part 21 reports issued or evaluated during the period

iii. Vendor safet

iv. y information letters (or equivalent) issued or evaluated during the period

v. Other external events and/or Operating Experience evaluated for

applicability during the period

g. Corrective action documents generated for the following:

i. Emergency planning drills and tabletop exercises performed during the

period

ii. Maintenance preventable functional failures which occurred or were

evaluated during the period

iii. Adverse trends in equipment, processes, procedures, or programs which

were evaluated during the period

iv. Action items generated or addressed by plant safety review committees

during the period

A2-2 Attachment 2

3. Logs and Reports

a. Corrective action performance trending/tracking information generated during the

period and broken down by functional organization

b. Corrective action effectiveness review reports generated during the period

c. Current system health reports or similar information

d. Radiation protection event logs during the period

e. Security event logs and security incidents during the period (sensitive information

can be provided by hard copy during first week on site)

f. Employee Concern Program (or equivalent) logs (sensitive information can be

provided by hard copy during first week on site)

g. List of training deficiencies, requests for training improvements, and simulator

deficiencies for the period

4. Procedures

a. Corrective action program procedures, to include initiation and evaluation

procedures, operability determination procedures, apparent and root cause

evaluation/determination procedures, and any other procedures which implement

the corrective action program at Waterford 3

b. Quality Assurance program procedures

c. Employee Concerns Program (or equivalent) procedures

d. Procedures which implement/maintain a Safety-Conscious Work Environment

5. Other

a. List of risk significant components and systems

b. Organization charts for plant staff and long-term/permanent contractors

A2-3 Attachment 2

Note: Corrective action documents refers to condition reports, notifications, action requests,

cause evaluations, and/or other similar documents, as applicable to Waterford 3.

As it becomes available, but no later than June 30, 2012, this information should be uploaded

on the Certrec IMS website. When these documents have been compiled (and by June 30,

2012), please download these documents onto a CD or DVD and sent it via overnight carrier to:

Richard L. Smith

U.S. NRC Resident Inspector Office

7003 Bald Hill Road

Port Gibson, MS 39150

Please note that the NRC is not able to accept electronic documents on thumb drives or other

similar digital media. However, CDs and DVDs are acceptable.

A2-4 Attachment 2