ML062420513

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IR 05000382-06-009 on 03/06/2006-08/09/2006 for Waterford Steam Electric Station, Unit 3; Discrepant or Unreported Performance Indicator Data and Notice of Violation
ML062420513
Person / Time
Site: Waterford Entergy icon.png
Issue date: 08/30/2006
From: Howell A
NRC/RGN-IV/DRP
To: Venable J
Entergy Operations
References
EA-06-136 IR-06-009
Download: ML062420513 (33)


See also: IR 05000382/2006009

Text

August 30, 2006

EA-06-136

Joseph E. Venable

Vice President Operations

Waterford 3

Entergy Operations, Inc.

17265 River Road

Killona, LA 70066-0751

SUBJECT: WATERFORD STEAM ELECTRIC STATION, UNIT 3 - NRC INSPECTION

REPORT 05000382/2006009 AND NOTICE OF VIOLATION

Dear Mr. Venable:

On August 9, 2006, the NRC completed an inspection at your Waterford Steam Electric Station,

Unit 3. The enclosed report documents the inspection findings which were preliminarily

discussed on May 11, 2006, with Mr. Kevin Walsh and other members of your staff. A followup

call concerning the disposition of the related enforcement activities was conducted with you and

other members of your staff on June 23, 2006, and a final telephonic exit meeting was

conducted on August 9, 2006.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

Within these areas, the inspection consisted of selected examination of procedures and

representative records, observations of activities, and interviews with personnel.

The report documents one violation of 10 CFR 50.9, with two examples, for reporting inaccurate

information to the NRC associated with the NRCs Safety System Unavailability (High Pressure

Injection and Residual Heat Removal) Performance Indicators. The performance indicator

information was inaccurate because your staff improperly concluded that the Train B high

pressure safety injection and Train B containment spray systems were still available for the full

range of potential accidents during an extended period when the containment safety injection

sump suction valve was partially open during the period of November 11, 2003 to September 9,

2004. If this data had been accurately reported, then the High Pressure Injection Performance

Indicator should have been Red and the Residual Heat Removal Performance Indicator should

have been Yellow up until the point that the safety system unavailability performance indicators

were replaced by the mitigating systems performance index (MSPI) on April 1, 2006.

The Enforcement Policy, Supplement VII, specifies that issues such as reporting inaccurate

performance indicator data that would have caused a performance indicator to change color

from Green to Yellow or Red would be a Severity Level III violation. However, the NRC has

determined that a Severity Level IV violation was more appropriate in this particular

circumstance. This determination was made primarily on the basis that the risk significance

Entergy Operations, Inc.

-2-

associated with the valve being mis-positioned was determined to be very low (Green) as

documented in NRC Inspection Report 05000382/2004005. Additionally, under the NRCs

recently implemented MSPI program, which replaced the safety system unavailability

performance indicator program on April 1, 2006, a similar set of circumstances would have

resulted in a Green outcome because of the differences in the way fault exposure is treated

under the former safety system unavailability performance indicator program and the current

MSPI program. While the overall risk significance of the underlying performance deficiency

was low, the failure to provide accurate information calls into question the ability to effectively

and consistently implement the performance indicator program, particularly for circumstances in

which the performance indicator outcome may result in a degradation of the cornerstone safety

objective.

The Severity Level IV violation is being cited because not all the criteria specified in Section

VI.A.1 of the NRC Enforcement Policy for a noncited violation were satisfied. Specifically,

Entergy failed to restore compliance and report corrected or accurate performance indicator

information, or otherwise notify NRC that the data reported in the past was not accurate, within

a reasonable time after the potential violation was initially identified. For the purposes of this

criterion, you were notified of the violation during the May 11, 2006, exit debrief meeting. Even

though the safety system unavailability performance indicators were superceded by MSPI

before the date of the exit meeting, the failure to accurately report the data was still material

because the NRC used the information to determine its level of oversight of Waterford 3.

Additionally, as stated in the Enforcement Policy, 10 CFR 50.9 violations are not evaluated

under the Significance Determination Process because violations of this nature impact the

ability of the NRC to properly regulate its licensees. You are required to respond to this letter

and should follow the instructions specified in the enclosed Notice when preparing your

response. The NRC will review your response, in part, to determine whether further

enforcement action is necessary to ensure compliance with regulatory requirements.

The NRC Action Matrix is described in NRC Inspection Manual Chapter 0305, Operating

Reactor Assessment Program. In accordance with the Action Matrix, one Red and one Yellow

performance indicator input would have placed your facility in the Multiple/Repetitive Degraded

Cornerstone, column. This would have required the implementation of Inspection Procedure 95003, Supplemental Inspection for Repetitive Degraded Cornerstone, Multiple Degraded

Cornerstones, Multiple Yellow inputs, or One Red Input, at your facility, as well as a number of

additional regulatory actions. For the same reasons as those specified for categorizing the

violation at Severity Level IV, the NRC also determined that a deviation from the NRC Action

Matrix was warranted. In lieu of these actions, we will implement actions as specified in the

Licensee Response column because, in this circumstance, this will provide the appropriate level

of regulatory response. This deviation from the NRC Action Matrix is documented in a

memorandum dated July 25, 2006.

Entergy Operations, Inc.

-3-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosures, the July 25, 2006, Action Matrix Deviation Memorandum, and your response will be

made available electronically for public inspection in the NRC Public Document Room or from

the NRCs document system (ADAMS), accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html. Should you have any questions concerning this

inspection, we will be pleased to discuss them with you.

Sincerely,

/RA/

Authur T. Howell III, Director

Division of Reactor Projects

Docket: 50-382

License: NPF-38

Enclosures:

Notice of Violation

NRC Inspection Report 050000382/2006009

w/Attachment: Supplemental Information

cc w/Enclosure:

Senior Vice President and

Chief Operating Officer

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Vice President, Operations Support

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Wise, Carter, Child & Caraway

P.O. Box 651

Jackson, MS 39205

General Manager, Plant Operations

Waterford 3 SES

Entergy Operations, Inc.

17265 River Road

Killona, LA 70066-0751

Entergy Operations, Inc.

-4-

Manager - Licensing Manager

Waterford 3 SES

Entergy Operations, Inc.

17265 River Road

Killona, LA 70066-0751

Chairman

Louisiana Public Service Commission

P.O. Box 91154

Baton Rouge, LA 70821-9154

Director, Nuclear Safety &

Regulatory Affairs

Waterford 3 SES

Entergy Operations, Inc.

17265 River Road

Killona, LA 70066-0751

Richard Penrod, Senior Environmental

Scientist

Office of Environmental Services

Northwestern State University

Russsell Hall, Room 201

Natchitoches, LA 71497

Parish President

St. Charles Parish

P.O. Box 302

Hahnville, LA 70057

Winston & Strawn LLP

1700 K Street, N.W.

Washington, DC 20006-3817

Entergy Operations, Inc.

-5-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (RJC1)

Senior Resident Inspector (MCH)

Branch Chief, DRP/E (DNG)

Senior Project Engineer, DRP/E (VGG)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

OEMAIL

D. Starkey, OE

D. Solorio, OE

J. Luehman, OE

M. Vasquez

M. Haire

Only inspection reports to the following:

DRS STA (DAP)

J. Lamb, OEDO RIV Coordinator (SCO)

ROPreports

WAT Site Secretary (AHY)

SUNSI Review Completed: __DNG__

ADAMS: / Yes

G No Initials:_DNG____

/ Publicly Available G Non-Publicly Available G Sensitive

/ Non-Sensitive

R:\\REACTORS\\WAT\\2006\\WT2006-09RP-GDR.wpd

RIV:SRI:DRS/EB1

NRR

SPE:DRP/D ACES

C:DRP/E

D:DRP

GDReplogle

MAJunge

MCHay

GMVasquez

DNGraves

ATHowell

/RA/

E-GDR

/RA/

/RA/

/RA/

/RA/

6/16/06 & 6/23/06

6/12/06

6/20/06

8/24/06

8/24/06

8/30/06

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

Enclosure 1

NOTICE OF VIOLATION

Entergy Operations, Inc.

Docket No. 50-382

Waterford Steam Electric Station

License No. NPF-38

EA-06-136

During an NRC inspection conducted on March 6 through May 11, 2006, a violation of NRC

requirements was identified. In accordance with the NRC Enforcement Policy, the violation is

listed below:

10 CFR 50.9 requires, in part; Information provided to the Commission by a licensee

shall be complete and accurate in all material respects.

Contrary to the above, from approximately November 1, 2004, (when the licensee

initially submitted the subject performance indicator information) to May 11, 2006,

information provided to the Commission in the form of system unavailability statistics for

the high pressure safety injection (Train B) and containment spray (Train B) systems

was not complete and accurate in all material respects. The licensee significantly

under-reported the unavailability hours for each train. This was material because the

NRC used the information to determine its response (e.g., inspection) to the data.

This is a Severity Level IV violation (Supplement VII).

Pursuant to the provisions of 10 CFR 2.201, Entergy Operations is hereby required to submit a

written statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document

Control Desk, Washington, DC 20555 with a copy to the Regional Administrator, Region IV, and

a copy to the NRC Resident Inspector at the facility that is the subject of this Notice, within 30

days of the date of the letter transmitting this Notice of Violation (Notice). This reply should be

clearly marked as a "Reply to a Notice of Violation; EA-06-136" and should include: (1) the

reason for the violation, or, if contested, the basis for disputing the violation or severity level,

(2) the corrective steps that have been taken and the results achieved, (3) the corrective steps

that will be taken to avoid further violations, and (4) the date when full compliance will be

achieved. Your response may reference or include previous docketed correspondence, if the

correspondence adequately addresses the required response. If an adequate reply is not

received within the time specified in this Notice, an order or a Demand for Information may be

issued as to why the license should not be modified, suspended, or revoked, or why such other

action as may be proper should not be taken. Where good cause is shown, consideration will

be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001.

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs document system (ADAMS), accessible from the

NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should

not include any personal privacy, proprietary, or safeguards information so that it can be made

available to the public without redaction. If personal privacy or proprietary information is

necessary to provide an acceptable response, then please provide a bracketed copy of your

-2-

Enclosure 1

response that identifies the information that should be protected and a redacted copy of your

response that deletes such information. If you request withholding of such material, you must

specifically identify the portions of your response that you seek to have withheld and provide in

detail the bases for your claim of withholding (e.g., explain why the disclosure of information will

create an unwarranted invasion of personal privacy or provide the information required by

10 CFR 2.390(b) to support a request for withholding confidential commercial or financial

information). If safeguards information is necessary to provide an acceptable response, please

provide the level of protection described in 10 CFR 73.21.

Dated this 30th day of August, 2006

Enclosure 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.:

50-382

License No.:

NPF-38

Report No.:

05000382/2006009

Licensee:

Entergy Operations, Inc.

Facility:

Waterford Steam Electric Station, Unit 3

Location:

Hwy. 18

Killona, Louisiana

Dates:

March 6 through August 9, 2006

Inspectors:

G. D. Replogle, Senior Reactor Inspector, Division of Reactor Safety

M. A. Junge, Mechanical Engineer, Office of Nuclear Reactor Regulation

Approved By:

Arthur T. Howell III, Director, Division of Reactor Projects

ATTACHMENTS:

Supplemental Information

Enclosure 2

-2-

SUMMARY OF FINDINGS

IR05000382/2006-009; 03/06/2006-08/09/2006; Waterford Steam Electric Station, Unit 3;

Discrepant or Unreported Performance Indicator Data

The report covered a 5 month period of inspection by a Region IV senior reactor inspector and

a mechanical engineer from the NRCs Office of Nuclear Reactor Regulation. The inspector

identified one Severity Level IV violation, which is not subject to the Significance Determination

Process. Findings for which the Significance Determination Process does not apply may be

Green or be assigned a severity level after NRC management review. The NRCs program for

overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 3, dated July, 2000.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Severity Level IV. The inspector identified a violation of 10 CFR 50.9, with two

examples, for the failure to provide accurate information to the NRC associated with the

Safety System Unavailably High Pressure Injection and Residual Heat Removal

Performance Indicators. The performance indicator information was inaccurate because

the licensee improperly concluded that the Train B high pressure safety injection and

Train B containment spray systems were still available during an extended period when

the containment safety injection sump suction valve was partially open. The inspector

found that the licensee had underestimated the size of valve (SI 602B) opening when

assessing system availability and failed to address inconsistencies between their field

data, diagnostic test data and their own informal calculations. Further, a second

analysis performed by a contractor (to determine the as-found valve position) was

inadequate, as it contained several errors and inappropriate assumptions. The licensee

also provided inadequate contractor oversight with respect to this effort. The erroneous

valve position determination resulted in the licensee reporting system availability

information that caused the performance indicators to be Green when the High Pressure

Safety Injection System Unavailability Performance Indicator should have been Red and

the Residual Heat Removal System Unavailability Performance Indicator should have

been Yellow.

The failure to provide accurate information to the NRC in accordance with 10 CFR 50.9

requirements was a performance deficiency. The issue had more than minor

significance in that, had the information been accurate, two performance indicators

would have changed color. Per the NRC Enforcement Policy,Section IV.A.3, these

issues are not subject to the Significance Determination Process. The Enforcement

Policy, Supplement VII, specifies that a Severity Level III violation would be appropriate

for these issues. However, considering: 1) the NRCs recently implemented Mitigating

Systems Performance Index program, which would have resulted in the subject

performance indicators returning to the Green threshold; and 2) the risk associated with

Enclosure 2

-3-

the underlying valve performance issue was of very low safety significance (Green), the

NRC determined that a Severity Level IV violation was more appropriate. This finding

had problem identification and resolution crosscutting aspects, in that the

implementation of the licensees Corrective Action Program did not result in a thorough

evaluation of the identified condition such that information reported to the NRC was

verified to be complete and accurate (Section 4OA1).

B.

Licensee-Identified Violations

None.

Enclosure 2

-4-

REPORT DETAILS

4OA1 Discrepant or Unreported Performance Indicator Data (71150)

a. Inspection Scope

The purpose of the inspection was to evaluate the accuracy of performance indicator

information submitted by the licensee for the High Pressure Injection and Residual Heat

Removal Performance Indicators. The accuracy of the performance indicator

information was questioned after an operator found containment safety injection sump

suction Valve SI-602B partially open on September 9, 2004. This condition could have

affected the availability of the Train B high pressure safety injection and Train B

containment spray systems. The licensee determined that the valve had been partially

open since November 11, 2003, when valve technicians incorrectly set one of the

Valve SI-602B limit switches. The partially open valve posed potential challenges to the

availability of the noted trains in response to medium break and large break loss of

coolant accidents. The availability of the high pressure safety injection system affected

the Safety System Unavailability High Pressure Injection Performance Indicator while

availability of the containment spray system affected the Safety System Unavailability

Residual Heat Removal Performance Indicator.

The inspector reviewed the licensees evaluation of the as-found valve position, the root

cause evaluation report and two contractor-furnished analyses. One contractor had

performed an evaluation of system impacts based on different valve positions. The

second contractor performed an analysis to determine the valves as-found position. In

addition, the inspector interviewed plant personnel who were involved with issue

identification and problem evaluation. Finally, the inspector obtained motor-operated

valve drawings and valve test data and performed independent calculations to

determine the valves as-found position.

The underlying valve performance issue was documented as a licensee-identified

violation of very low risk significance (Green) in NRC Inspection

Report 05000382/2004005, Section 4OA7. Therefore, the focus of this inspection dealt

solely with the determination of the accuracy of the data submitted to the NRC regarding

the two subject performance indicators.

b.

Findings

Introduction. The inspector identified a violation of 10 CFR 50.9, with two examples, for

the failure to provide accurate information to the NRC associated with the High Pressure

Safety Injection System Unavailability and Residual Heat Removal System Unavailability

Performance Indicators. The performance indicator information was inaccurate because

the licensee improperly concluded that the Train B high pressure safety injection and

Train B containment spray systems were still available during an extended period when

the containment safety injection sump suction Valve SI-602B, was partially open. The

inspector found that the licensee had underestimated the size of the valve opening when

assessing system availability and failed to address inconsistencies between their field

Enclosure 2

-5-

data, diagnostic test data and their own informal calculations. Furthermore, a second

analysis performed by a contractor to determine the valves position was inadequate, as

it contained several errors and unsupported assumptions. The licensee provided

inadequate contractor oversight with respect to this effort. The erroneous valve position

determination resulted in the licensee reporting system availability information that

caused the two performance indicators to indicate Green when the High Pressure

Injection System Unavailability Performance Indicator should have been Red and the

Residual Heat Removal System Unavailability Performance Indicator should have been

Yellow.

Background: On September 9, 2004, during a system piping integrity test, the test

operator found the containment safety injection sump suction Valve SI-602B partially

open. The valve is a 24 inch Fisher 9200 series butterfly valve driven by an SMB-00

electric actuator through a quarter turn H2BC gear operator. The licensee determined

that the condition had existed since November 11, 2003, when one of the valve limit

switches was set incorrectly and prevented the valve disc from reaching the fully closed

and seated position.

In response to medium and large break loss of coolant accidents that pressurize

containment, the partially open valve posed two potential challenges to system

availability. First, the pressurized containment would force air, steam and water through

the valve and into the system flow streams. Air entrainment can cause excessive pump

vibration and pump air binding which can render the system unavailable. Second, the

system suction lines could be pressurized sufficiently as to force and hold closed the

refueling water storage pool discharge check Valve SI-107B. This would starve the

system pumps of a suction source of water, rendering them unavailable. Depending on

the position of SI-602B, this condition had the potential of rendering the high pressure

safety injection system Train B, low pressure safety injection system Train B, and

containment spray system Train B unavailable. However, in this case, the unavailability

of the Train B low pressure safety injection system would not affect a performance

indicator value.

The licensee performed a detailed analysis to determine the equipments sensitivity to

air entrainment and suction header pressurization. The licensee determined that the

total valve opening could not exceed 0.41 square inches. In addition, the licensee

attempted to replicate the valve position and then took physical gap measurements to

determine the affected valve disc area. The licensee determined that the open area

was 0.25 square inches, which was within the 0.41 square inch acceptance limit. The

licensee then took additional valve measurements and determined that the valves as-

found position was approximately 3.2E open. In response to the NRC questions and

concerns regarding the valves actual as-found position, the licensee contracted with an

industry engineering firm to again determine the as-found valve position.

Summary: The following bullets summarize the inspector observations and findings.

Additional details concerning each identified problem are provided in subsequent

sections of this report.

Enclosure 2

-6-

The licensees evaluation of system impacts, based on different possible valve

positions, was conservative and effective. The evaluation concluded that system

availability could be maintained with a maximum valve opening of 0.41 square

inches. The inspector had no findings of significance related to this evaluation.

The licensees re-creation of the as-found position of Valve SI-602B was

inadequate because it failed to account for direction-dependent differences in

valve performance. Specifically, valve leakage started and stopped at different

handwheel positions depending on whether the valve was being opened or

closed. The licensees re-creation concluded that the valve was 3.2E open.

A subsequent engineering evaluation performed by a contractor was inadequate

because:

The contractors evaluation of the licensees re-creation of the valves as-found

position also failed to account for direction-dependent differences in valve

performance. The licensee had not provided the contractor with the pertinent

test data. This affected one of five contractor valve position assessments.

The contractor inappropriately assumed that the valve was over-traveling past

the 0E position. The contractor provided no objective evidence to support this

assumption and the inspector identified evidence to the contrary. The two

calculations that used this assumption concluded that the valve was 3.4E and

3.5E from the 0E position. However, when the inspector applied correction

factors to these calculations to account for the erroneous assumption, the

calculated valve positions were 5.4E and 5.6E, respectively.

The contractor used an inappropriate value for the Modulus of Rigidity (an

engineering term related to the stiffness of a round bar when torque is applied) in

one calculation. This made two calculations that were based on different values

of handwheel turns (0.55 and 1.0) come to the same final result. This

inappropriate factor was used in one calculation but not the other.

The contractors estimation of valve position based on HBC operator stop nut

measurements was not credible. The data, which was provided by the licensee,

was obtained under informal and uncontrolled conditions, was not specific as to

the conditions under which it was obtained, and was inconsistent with other

information. This affected one contractor calculation.

The licensee reviewed the contractors analysis prior to providing it to the NRC

but they failed to identify the noted problems.

The inspector performed two additional independent calculations and determined

that the valves as-found position was slightly greater than 5E from the zero

position. The licensee had performed similar calculations and had obtained

similar results, but had not formalized these efforts. In addition, the licensee had

Enclosure 2

-7-

not attempted to explain the inconsistencies between these calculations and

other results that they utilized. The licensees evaluation of these issues lacked

sufficient engineering rigor.

A summary of the calculated valve positions, including inspector corrected values and

results from independent NRC calculations, is provided below:

Contractor Calculations and NRC Corrections

Calculation Method/

Referenced Position

Change in Disc

Position from

Referenced Position

Inspector

Corrected

Values

HBC Stop Nut

2.915E

Not Credible,

Inconsistent

Data

Handwheel Closure (one full

handwheel turn)

2.870E

3.9E

Least Accurate

Stroke Time Comparison

3/10/1999 Trace (diagnostic

system traces)

3.363E

5.4E

Reasonable

Approximation

Stroke Time Comparison

11/6/2003 Trace (diagnostic

system traces)

3.549E

5.6E

Reasonable

Approximation

Disc Measurement

3.186E

Inadequate Re-

creation

Average

3.177E

Independent NRC Calculations

Method

Results

Relative

Accuracy

Inservice Stroke Time Tests

5.9E

Reasonable

Approximation

Diagnostic System Test Data

5.5E

Most Accurate

The detailed supporting sections of this report are organized into three main categories:

Assessment of Licensees Initial Evaluation

Assessment of Licensees Contractor Evaluation

Independent NRC Calculations

Enclosure 2

-8-

Assessment of Licensees Initial Evaluation

Licensees First Field Test: The licensee performed field testing to estimate the

valves as-found position.

The first field test was a local leak rate test. The test involved slowly opening the valve

using the manual handwheel in 1/8 turn increments to the 2-1/4 turns open position.

Then an operator closed the valve in 1/8 turn increments until it was fully closed. The

valve operator stated that he did not start counting the handwheel turns until he

obtained resistance. That means that the operator did not count the first part of the

handwheel operation before the handwheel dogs engaged into the drive sleeve slots.

Until the handwheel dogs are engaged, the handwheel would spin freely. The inspector

considered this approach appropriate for counting handwheel turns.

The inspector noted that the apparent positions of the valve when leakage started

(going open) and stopped (going closed) were sensitive to the direction of valve

movement. For example, in the open direction gross leakage initiated between 1-3/8

and 1-1/2 handwheel turns from hard-seat contact. In the closing direction, gross

leakage stopped between 7/8 and 3/4 handwheel turn from hard-seat contact. In

response to inspectors questions, the licensee stated that they had also noticed this

discrepancy but had not attempted to evaluate it.

The inspector reviewed the valves diagnostic testing system torque traces and

determined that the significant difference between the points where leakage started and

stopped was due to gear play. The traces revealed that, when the valve changed

direction, the motor and gears operate for 1.34 seconds before the valve stem started to

move. In the more pertinent part of the trace (from hammer-blow to the initiation of

valve movement) the time delay was 0.8 seconds. This is the more pertinent trace

section because it mimics the valve/actuator response when it is operated with the

handwheel. The delay of 0.8 seconds equates to about 0.6 handwheel turn worth of

motion, which turns out to be the approximate difference in the handwheel positions

noted above.

In reality, for both the opening and closing directions the valve disc was in about the

same position when gross flow initiated and stopped. The indicated position in the open

direction was misleading because the licensee did not account for the gear play

contribution. Accounting for this type of gear play is only necessary when changing the

valves direction and will usually only affect the estimated position (using handwheel

turns) in the open direction.

The table, below, illustrates the affect of gear play on the valve position. In this

example, the valve in question is repositioned from full closed to 1.8 handwheel turns

open. Then the valve is repositioned back to the closed position. For this example, one

full handwheel turn is equal to 5.14E of valve movement.

Enclosure 2

-9-

Opening

Handwheel

turns from

fully

closed,

going open

Actual valve

position in

equivalent

handwheel

turns from

fully closed

Valve

position in

degrees

open

0

0

0E

0.2

0

0E

0.4

0

0E

0.6

0

0E

0.8

0.2

1.0E

1.0

0.4

2.0E

1.2

0.6

3.0E

1.4

0.8

4.1E

1.6

1.0

5.1E

1.8

1.2

6.2E

Closing

Handwheel

turns from

fully closed,

going

closed

Actual valve

position in

equivalent

handwheel

turns from fully

closed

Valve

position in

degrees

open

1.8

1.2

6.2E

1.6

1.2

6.2E

1.4

1.2

6.2E

1.2

1.2

6.2E

1.0

1.0

5.1E

0.8

0.8

4.1E

0.6

0.6

3.0E

0.4

0.4

2.0E

0.2

0.2

1.0E

0

0

0E

As demonstrated above, when the valve is being repositioned in the open direction,

handwheel position is not an accurate indicator of valve position unless the amount of

gear play is known and accounted for. Conversely, moving in the closed direction, once

the valve moves through the gear-play region, the handwheel position is a relatively

accurate indicator of valve position. This fact is important and has direct ramifications

on the licensees evaluation as discussed below.

Licensees Second Field Test: The second field test involved positioning the valve to

the one handwheel turn open position and taking internal gap measurements. The gap

measurements were then used to estimate the approximate valve opening. For clarity,

each major step is discussed separately:

1.

The licensee opened the valve one full handwheel turn, against resistance, and

match-marked the valves position indicator. The indicator is directly aligned with

the valve stem. It is connected to the stem through a splined shaft, which has a

small amount of gear play.

The inspector noted that because of the position error in the opening direction

(due to gear play), the valve was not the equivalent of one full handwheel turn

open (5.12E) but was about 0.4 handwheel turn open (2E).

2.

An operator opened the valve to the 40 percent open position (about 34E).

Enclosure 2

-10-

3.

The operator then closed the valve to align the match-markings that were made

in the first step. The inspector noted that the licensee had not counted the

number of turns back to this position to verify that the valve was actually one

handwheel turn from the seat. Instead, the licensee aligned the valve indicator

to the match marks that corresponded to the 0.4 handwheel (2E) open position.

If there had been no gear play between the indicator and the valve stem, then

the valve would have been only 2E open. This gear play between the indicator

and the valve stem caused the indicator to lead the actual valve position very

slightly. When reversing the valves direction (going in the closed direction) the

gear play would cause the valve to be slightly more open at the match-marked

position than when the match-marks were made. Since this gear play

constituted only a portion of the total gear play in the valve/actuator system, it

was not sufficient to cause the valve to be the equivalent of one full handwheel

turn open (5.12E).

4.

The licensee took gap measurements between the valve disc and body.

5.

The licensee took additional internal measurements and established that the

valve disc was approximately 3.2E open.

6.

The licensee repeated the procedure and calculated the total valve open area at

0.25 square inches (using the larger of the two measurements). The two

measurements were approximately 50% different in magnitude. The licensee

identified small gaps between the Tee-Ring and the seat in one lower quadrant

and in a small section of one upper quadrant, where the Tee-Ring had torn.

The inspector noted that, between the two tests, the licensee had to reposition the valve

to the full closed position in order to start the procedure over for the second set of

measurements. The licensee could have easily verified that the valve was actually one

full handwheel turn from hard-seat contact at this point in their procedure. The licensee

did not perform this verification. If they had done so, then they would have found that

the valve was not one full handwheel turn away from the fully closed position.

Assessment of Licensees Contractor Evaluation

As discussed later in this report, the inspector had performed independent calculations

and determined that the valve was slightly more than 5E open. In response to the

inspector concerns, the licensee hired a contract engineering firm to evaluate the valves

as-found position. The licensee provided the inspectors with the contractors report,

Independent Assessment of Disc Position of SI-602B Between November 3, 2003 and

September 11, 2004, dated May 8, 2006.

The engineering firm determined that the valve was likely at the 3.2E open position,

consistent with the licensees claims. The engineering firm calculated the valves

position using four different methods, five estimations in all. However, the inspector

identified several inappropriate assumptions and errors in the analysis. The following

table summarizes the vendors results as well as the inspector corrected values:

Enclosure 2

-11-

Calculation Method/

Referenced Position

Change in Disc

Position from

Referenced

Position

Inspector

Corrected

Values

HBC Stop Nut

2.915E

Not Credible,

Inconsistent

Data

Handwheel Closure (one

full handwheel turn)

2.870E

3.9E

Stroke Time Comparison

3/10/1999 Trace

(diagnostic system

traces)

3.363E

5.4E

Stroke Time Comparison

11/6/2003 Trace

(diagnostic system

traces)

3.549E

5.6E

Disc Measurement

3.186E

Inadequate

Re-creation

Average

3.177E

The inspector findings are discussed in detail below:

HBC Stop Nut Method: This method is based on gap measurements between one of

the HBC operator stop nuts and the adjacent enclosure wall. The stop nuts are used in

the HBC-2 operator to limit valve travel. While the licensee did not utilize the stop nuts

for this purpose, the gap measurements provided some information with respect to the

as-found valve position. Most importantly, the stop nut is on the same shaft as the

handwheel. Stop nut movement correlates directly with handwheel movement (when

the handwheel is engaged). Since the stop nuts had seven threads per inch, one

handwheel turn equates to 143 mils in stop nut travel.

The licensee had stated that when the valve was checked, after the operator had closed

it, the as-found stop nut gap measurement was 70 mils. After the valve was opened

and closed electrically (with the inappropriate limit switch setting) the gap measurement

was 150 mils. The licensee then adjusted the valve limit switch until the stop nut

measurement was 71 mils. The licensee provided this data to the engineering

contractor.

The contractor calculated that the operator had turned the valve handwheel 0.55 turns

when he found it. Considering stem deflection (based on the torque at the final valve

position being 965 foot-lbs) the contractors calculated as-found valve position was

Enclosure 2

-12-

2.915E open. The contractors report indicated that the 0.55 handwheel turns appeared

inconsistent with the operators statements (that he had closed the valve approximately

one full handwheel turn).

The inspector noted the following problems and inconsistencies with the data and the

contractors assessment.

As noted by the contractor, gap measurements did not correlate with operator

statements. The HBC stop nut movement should correlate exactly with

handwheel movement. The components are on the same shaft. But, the gap

measurements indicated that the operator had only turned the valve 0.55

handwheel turn while the operator had indicated that he had repositioned the

valve approximately 1 full handwheel turn.

The HBC gap measurement taken after the operator closed the valve was

70 mils. The gap measurement taken after the valve limit switch was adjusted

so that the stop nut gap approximated the same position was 71 mils. These

two gap measurements are almost exactly the same. Accordingly, the torque on

the valve stem that coincided with each measurement should have been about

the same. They were not. The torque value after the operator closed the valve

was 965 ft-lbs while the torque value measured after the limit switch was

adjusted was 454 ft-lbs.

The gap measurements were not performed in accordance with procedures and

the existing documentation was unclear with respect to what was measured and

when it was measured. The licensee had stated that they took gap

measurements after each of 15 limit switch adjustments (when they were

attempting to properly adjust the values limit switch on September 11, 2004).

However, no data was apparently recorded for 14 of the gap measurements.

When asked on more that one occasion for any and all documents associated

with these gap measurements, the licensee provided only two documents that

contained gap values. One document, Work Order 51581 stated, in part:

After adjustment 145 mils Desired HW set 70 mils using ETT as AS

switched to sts. gap = 71

The work order contained no steps to take these measurements and the

meaning of some of the terminology was not clear. For example, 145 mils was

obtained after adjustment. The document does not state what adjustment was

made. Additionally, there was no formally controlled record of the 150 mil value

which the contractor used in the calculations (the 145 mil value was not used in

the calculations). The 150 mil value was recorded in the computer system but

not in the hard copy of the work order.

The second document, a print of a computer screen (print date May 5, 2006)

stated, in part:

WO# 51581 150 mils Desired HQ set at 70 mils.

Enclosure 2

-13-

While this document provided some of the same measurement values utilized by

the contractor in their calculations, the 150 mil value was inconsistent with the

value actually documented in the work order (145 mils after adjustment). In

addition, this value was contained in an uncontrolled computer file and was not

subject to any quality controls such that it could have been changed in an

uncontrolled manner.

The results from the stop nut measurements were inconsistent with results that

the inspector obtained from other calculations, such as those based on

diagnostic system torque traces and Inservice Testing stroke times. The time

signature data in the diagnostic system torque traces was of a high quality and

was very accurate with respect to the identification of artifacts and the time they

occurred (provided later in this report).

A representative from Limitorque informed the inspector that the HBC stop nut

threads were 1-1/4 X 7 UNC - coarse. This means, in part, that the stop nut has

7 threads per inch and they are coarse, versus fine or medium grade. The

inspector also noted, while inspecting the threads on a much smaller HBC unit,

that the stop nuts could move slightly from side to side (without any stop nut

rotation). Limitorque had not designed the stop nuts to be used for the purpose

of taking precise measurements for the purpose of estimating valve position.

They were only provided as a means to stop valve movement. Making precise

measurements, to within a few mils, would be very difficult.

Based on the above, the inspector had a low level of confidence in the accuracy of the

HBC stop nut gap measurements and it was not clear that calculations based on these

values provided meaningful results. Compared to the quality of the other available data,

such as the valve torque traces, the HBC stop nut measurements were not credible.

Handwheel Turns: The contractor calculated the as-found valve position based on the

operators statement that he had repositioned the valve approximately one full

handwheel turn. The contractor based this calculation on 1.0 handwheel turn (exactly)

and then deducted the contribution from stem deflection. Stem deflection is the amount

of stem rotation observed without corresponding valve movement (the twisting of the

stem due to torque). This would occur when the operator continued to turn the valves

handwheel after the valve disc had contacted the hard-seat.

The inspector identified that the contractors calculation for stem deflection utilized an

inappropriate factor (torsional stiffness) instead of the standard classical equation that

is used for these purposes. This error affected the calculation sufficiently as to make

the final result (2.9E from the backseat) appear the same as the calculation based on

HBC stop nuts (the contractor had utilized the classical engineering equation in lieu of

the torsional stiffness factor in the HBC stop nut calculation). Getting almost exactly the

same value in the two calculations was unexpected because the stop nut calculation

was based on 0.55 handwheel turn worth of movement while the handwheel turn

calculation was based on 1.0 handwheel turn worth of movement. Since the other

factors should have been the same, the calculations should have produced different

results.

Enclosure 2

-14-

The contractor derived the torsional stiffness factor from a portion of the diagnostic

system torque trace between hard seat contact and motor-cuttoff. The contractor had

performed no validation testing of the torsional stiffness factor to verify that it properly

predicted system deflection. The stem deflection equation used by the contractor was:

Stem Deflection = Torque/Torsional Stiffness

The inspector noted that the torsional stiffness factor included deflection from all of the

actuator/HBC gear trains (including a sliding worm gear in the Limitorque actuator) when

only a much smaller portion of the gear train is in service when operating the valve with

the handwheel. The inspector observed that the use of the torsional stiffness factor, in

lieu of the classical equation, resulted in a higher calculated stem deflection value and a

smaller valve opening for the handwheel calculation.

Calculated as-found position = calculated position - stem deflection

Furthermore, the contractor acknowledged that the torsional stiffness factor was not

linear, as it appeared to change based on the amount of torque applied to the system.

However, the contractor calculated and utilized the value as if it were linear. The

contractor used the one calculated value for all circumstances.

The inspector also observed that the contractor had calculated the torsional stiffness for

three different closing strokes and had obtained three different results, as provided

below:

431 ft-lbs/degree

310 ft-lbs/degree

358 ft-lbs/degree

The relatively large degree of variability in this factor called into question its usefulness

in any of the stem deflection calculations. Any factor used to calculate stem deflection

should demonstrate good repeatability. The contractor chose to use the

310 ft-lbs/degree value, which also provided the most optimistic (lesser degree of valve

opening) results for the handwheel turn calculation. The contractor calculated the

stem deflection to be:

2.273E

The contractor then calculated the amount of valve opening based on this method as:

5.12E - 2.273 E = 2.9E

NOTE: The contractor also used the torsional stiffness term in their stroke time

calculations. The effect of using this term in these calculations makes the

calculated valve position more open, which is conservative. The magnitude of

the adjustment, however, was much smaller, as a much smaller torque

difference was applied. As noted later in this report, the contractor had used a

different inappropriate assumption in these calculations which made the

calculated valve position appear more closed.

Enclosure 2

-15-

Various text and reference books provide a classical equation for calculating the angle

of deflection of a round bar with a given torque (for example, Mechanical Engineering

Design, Fourth Edition, Shigley and Mitchell). Since the stem torque was known (from

a direct measurement on the stem) and the diameter, material and length of the stem

was also known, the contractor should have utilized the standard equation for this

purpose. Considering the configuration of the other components in the affected gear

train, deflection of the other components should be negligible. The equation, along with

applicable values, is provided below:

= Twist Angle in radians = (T*l)/(G*J)

T = Torque (use the torque difference in this case) = 705 ft-lbs

l = Length of Stem = 28 inches

G = Modulus of Rigidity = 11,500,000 psi

J = Polar Moment of Inertia = *d4/32 = 0.92

d = Diameter of Stem = 1.75 inches

The stem deflection based on the above is: 1.27E, compared to the 2.273E used by the

contractor. The difference is:

2.27E - 1.27E = 1.0E

Adjusting the contractors calculation to account for this difference, the valve position

should be:

2.9E + 1.0E = 3.9E position.

In addition to the above, converting this data to the same units as used in the

contractors torsional stiffness factor, the apparent torsional stiffness using the widely

accepted engineering equations would be:

555 ft-lbs/degree, which is substantially greater than the 310 ft-lbs/degree value

used by the contractor.

While the inspector agreed that this calculation provided the valves position based on

the operators recollection, the operator had only estimated the amount of handwheel

movement at approximately, one handwheel turn. The actual amount of travel could

have been a little more or a little less. The inspector considered other calculations,

based on diagnostic system torque traces, for example, to provide a much higher level

of accuracy and confidence.

Stroke Time Measurements: The contractor performed two calculations based on the

timing of artifacts in the diagnostic system torque traces. The contractor referred to

these as stroke time measurements. These were similar to a calculation performed by

the inspector in a later part of this report (Diagnostic System Test Data Method). They

should not be confused, however, with another calculation performed by the inspector

that was based on Inservice Testing stroke time measurements.

Enclosure 2

-16-

The theory behind the position estimation calculation is that by comparing the as-found

(partially open valve) torque trace with a torque trace of the same valve where it did fully

close (to the 0E position), the angle of the valve opening with respect to the 0E degree

position can be calculated. The inspector agreed that this method of analysis should

provide an accurate as-found valve position.

The inspector found that instead of comparing the as-found torque trace to traces where

the valve was at the fully closed position, indicated by the presence of hard seat contact

on the trace, the contractor had compared the as-found torque trace to other valve

traces where the valve did not reach the 0E position. This resulted in significantly under-

estimating the valves position. The contractor used the closing stroke dated March 10,

1999, and the closing stroke dated November 6, 2003, as reference traces.

For the 1999 torque trace, the valve stopped significantly before the 0E position. The

inspector calculated the distance that the 1999 valve stroke was from the hard seat by

utilizing a trace that was known to reach the 0E position, as evidence by a characteristic

shape when the valve reaches the hard seat. Based on this approach, the inspector

determined that the valve in the 1999 trace had stopped at the 1.9E position. The valve

was leaktight but was still not fully seated. The valve vendors drawing indicated that the

valve could be leak tight out to the 3.2E position. To find the actual as-found valve

angle, the inspector added this additional amount of travel to the contractors results.

3.36E + 1.9E = 5.4E

For the November 6, 2003, reference trace, the valve had traveled closer to the valve

seat than in the 1999 reference trace. However, the contractor chose a point

substantially before the valve had stopped moving as the reference point and treated

this point as if it were the 0E position. This reference point was 0.57 seconds short of

hard seat contact. That equates to 2.15E degrees of additional travel. Adding this

amount to the contractors calculation resulted in:

3.549E + 2.15E = 5.6E

NOTE: For the two calculations above, the inspector neglected any additional

adjustment for stem deflection, as the torque in these traces was substantially

smaller than in the handwheel case and any additional adjustment would be very

small. Additionally, the stem deflection would cause the valve to be slightly more

open (making the problem worse, not better).

The inspector determined that the contractor had utilized an inappropriate assumption

when performing these calculations. The contractor had assumed that the valve stop

was not in the correct position, or was absent altogether, and that the valve was over-

traveling past the 0E position. This would make all of the calculated valve opening

angles smaller by the amount of over-travel. The contractors report indicated that the

valve was at the 0E position when it was at the first large torque peak and had further

stated that this information came from the valve vendor. Some torque traces had two

torque peaks (one at the 3.6E position and one at the 2.2E position). The inspector

noted that the contractor had no objective evidence to support this claim. In addition,

the inspector disagreed with this contention for the following reasons:

Enclosure 2

-17-

The inspector called the valve vendor and the vendor did not agree that the 0E

position was at the first large torque peak. In addition, the vendor indicated that

for over-travel to occur, the valve stop set-screw, which is attached to a larger

hard stop, would have to be misadjusted or missing. The vendor stated that the

set-screw was either staked or welded into position at the factory.

The licensee had also informed the inspector that they had measured the gap

between the set-screw stop and the larger hard stop during the past outage and

had verified with the valve vendor that it was the proper size (0.25 inches). This

indicated that the valve stop set-screw was in the correct position.

The inspector reviewed a similar valve trace for the identical valve in Train A,

Valve SI-602A. The inspector noted that the valve displayed the same two

hump-like features as were evident in the Valve SI-602B traces. If

Valve SI-602B was over-traveling past the 0E position, as described by the

contractor, both valves were over-traveling. This was not likely, given the vendor

information regarding set-screw installation.

As a bounding exercise, if the set-screw was totally missing, the valve could only

travel an additional 0.25 inches at the outer edge. That equates to only an

additional 1.2 degrees of valve travel. The inspector calculated the angular

distance between the large hump and the hardseat (without correction for stem

deflection at 3.6E). In other words, the hump was too far from the hard stop for

this theory to be credible.

Independent NRC Calculations

The inspector used the licensees test data and two calculation methods to determine

the as-found position of Safety Injection Valve SI-602B. Based on the calculations, the

inspector determined that the valve was open slightly more than 5E, which was

significantly more than the 3.2E assumed in the licensees analysis. The following table

provides a summary of the results:

Method

Results

Relative Accuracy

Inservice Stroke Time Tests

5.9E

Reasonably Accurate

Diagnostic System Test Data

5.5E

Most Accurate

The calculations are provided below:

NRC Calculation 1: Based on Inservice Stroke Time Tests: Since the

inappropriate limit switch setting also affected the valves stroke time, the

inspector calculated the valve position based on the difference in the recorded

stroke times. The inspector compared the average of the stroke times when the

limit switch was set incorrectly to the average of the stroke times when the limit

switch was set properly.

Enclosure 2

-18-

Stroke Times (Close Direction), Limit Switch set Incorrectly:

11/7/2003

22.2 Seconds

1/6/2004

22.5

3/30/2004

22.5

6/25/2004

22.5

Average = 22.4 Seconds

Stroke Times (Close Direction), Limit Switch set Properly

9/11/2004

23.9

12/7/2004

23.7

3/1/2005

24

5/25/2005

24

6/16/2005

23.9

8/16/2005

23.9

8/17/2005

23.9

11/8/2005

23.8

1/31/2006

24.2

Average = 23.9 Seconds

Calculate Difference in Averages

= 23.9 - 22.4 = 1.5 seconds

Calculate Valve Speed in Degrees per Second (based on 1800 RPM motor

speed)

Given Information:

Limitorque actuator overall ratio (OAR) = 41.0

Limitorque HBC operator ratio = 70

Motor speed = 1800 rpm (based on motor speed curve)

Calculate the time for the valve to rotate 90E:

((41*70) motor rev. per valve rev.)(60 seconds per minute)(90E)

(1800 motor revolutions per min)(360E)

= 23.9 seconds

Determine the valve speed in degrees per second:

= (90E)/(23.9 seconds) = 3.77E/second

Enclosure 2

-19-

Calculate the Difference in Valve Travel (based on valve speed and difference in

stroke times)

= (1.5 seconds) * 3.77E/second = 5.66E open

Calculate Stem Deflection Adjustment (from stem torque traces)

T = Stem Torque Difference, Between As-Found Torque when Partially

Open (285 foot-lbs) and the Torque when Valve Disc Starts to

Move (150 foot-lbs)

= 265 - 150 = 115 foot lbs

l, d, G and J are the same as used in an earlier calculation.

Based on the above,

= (115 foot-lbs * 28 inches * 12 inches/foot)/(11,500,000 psi*.92)

= 0.00365 radians * (180E/ radians) = 0.21E

Calculate Valve Opening Based on the Difference in Inservice Stroke Times

Since stem deflection causes the valve disc to lag slightly, stem deflection affect

causes the valve to be slightly more open.

= 5.66E + 0.21E = 5.87E . 5.9E

The accuracy of this calculation is affected by the method used for measuring

the individual stroke times. When testing the valve, operators used a stop

watch. There is some variability in operator response times when stopping the

watch. This uncertainty is limited to some degree because the calculation uses

the difference in the average stroke times, versus comparing any two points

directly. Considering that the data scatter was very limited, the response times

for the opening and closing tests should approximately cancel each other in the

calculation. Therefore, this calculation should provide a reasonable estimation of

valve position.

Calculation 2: Based on VOTES Torque Traces: This method of

approximation utilizes data taken directly from diagnostic system torque traces.

Diagnostic system torque traces are very accurate when identifying the location

of artifacts in the traces with respect to time. Artifacts such as the start of valve

movement and the point where the valve disc hits the hard seat are easily

identified by commonly known characteristic shapes on the traces. Accordingly,

the timing between artifacts, which is performed in this calculation, is easily

determined and the results are very accurate. When combined with relatively

minor adjustments to account for stem deflection and valve coastdown (the

amount of valve travel after the motor is de-energized), the final calculated valve

position is very accurate when compared to other estimation methods.

Enclosure 2

-20-

The inspector considered this method the most accurate of all of the

approximation methods used in this report.

Given Information:

Limitorque actuator overall ratio (OAR) = 41.0

Limitorque HBC operator ratio = 70

Motor speed = 1800 rpm

Valve Speed = 3.77 degrees/second (calculated earlier)

NOTES:

1.

The calculation assumes that the 1800 rpm motor experiences no

slippage. This is generally a safe assumption considering the applicable

part of the motor curve (torque = less than 1 foot pound). As part of a

sensitivity analysis, however, the inspector also performed a calculation

assuming worst case slippage (the motor rotates at 1775 rpm). This is

considered more than bounding for this problem.

2.

The inspector used data from two motor-operated valve torque traces. In

one trace (2005), the closing limit switch was set properly while in the

other (2003) the limit switch was set short of the target (and is the

genesis of the discrepant PI inspection).

Part A: Determine the size of the valve opening (in degrees) in 2003 when the

limit switch was set incorrectly (based on 1800 revolutions per minute motor

speed).

1.

Determine the valve travel time when the limit switch was set correctly

(information from 2005 MOV torque trace):

Time valve starts moving (from MOV trace) = 1.36 seconds

Time close limit switch opens = 23.55 seconds

Travel time = 23.55 - 1.36 = 22.19 seconds

2.

Calculate the distance traveled (in degrees) when limit switch was set

correctly:

(22.19 sec)(3.77E/second) = 83.7E

Therefore, when the valve was full open, it was 83.7E away from hard

seat contact.

Enclosure 2

-21-

3.

Determine the valve travel time when the limit switches were set

incorrectly (information from 2003 MOV torque trace):

Time valve starts moving (from MOV trace) = 1.34 seconds

Time close limit switch opens = 22.02 seconds

Travel time = 22.02 - 1.34 = 20.7 seconds

4.

Calculate the distance traveled (in degrees) when the limit switch was set

incorrectly:

(20.7 sec)(3.77E/second) = 78.0E

5.

Calculate the valves open angle (in degrees) from the seat when the

closing limit switch opened in 2003:

= total distance traveled in 2005 (from full open to seat) - total distance

traveled in 2003

= 83.7E - 78.0E = 5.7E

6.

Determine the time that the valve continued to move after the closing limit

switch contact opened (2003 trace):

Limit switch opened at 22.02 seconds

Valve stopped moving at 22.22 seconds

Time of additional travel = 22.22-22.02 = 0.2 seconds

The most that the valve could have continued to travel was:

(0.2 seconds)(3.77E) = .75E

Since the valve was not traveling at full speed for the entire time, but was,

instead, slowing to a stop, use 1/2 of the above.

1/2 * .75E = .38E

7.

Determine the 2003 distance from the seat considering additional valve

coasting after the limit switch contact opened:

= 5.7E - .38E = 5.3E

8.

Adjust for Stem Deflection (use same value as in NRC Calculation 1)

5.3E + .21E = 5.5E

Enclosure 2

-22-

Part B (sensitivity case): Determine the size of the valve opening in 2003 when

the valve closing limit switch was set incorrectly (assuming 1775 revolutions per

minute motor speed, maximum slippage).

Part B was completed in exactly the same manner as Part A above, with the

exception that the motor speed was changed from 1800 revolutions per minute

to 1775 revolutions per minute. The resultant valve angle was:

5.3E

The inspector asked the plants engineers if they had performed other calculations

similar to those performed in this report (by the inspector) to determine valve position.

The engineers stated that they had performed similar calculations and that they had

obtained similar results (the valve was approximately 5E open). However, the engineers

did not formalize these calculations or formally address the inconsistencies between

their field data, the diagnostic system data and the calculations.

Performance Indicator Conclusions

During the first 2 years of Reactor Oversight Process implementation, NRC staff and

industry identified problems with the safety system unavailability performance indicators

and worked to implement incremental changes to the indicators. Over the next 4 years,

a working group developed a performance indicator that addressed the identified

problems. This indicator, the Mitigating System Performance Index, was implemented

April 1, 2006, and is addressed in NRC Regulatory Issue Summary 2006-07, Changes

to the Safety System Unavailability Performance Indicators.

Based on a valve opening of approximately 5E, which is a close approxiation of the

degree of valve opening as determined by the NRC, the Train B high pressure safety

injection and both Train B containment spray pumps were unavailable between

November 11, 2003, and September 9, 2004, for a range of medium and large break

loss of coolant accidents. The licensee calculated the maximum tolerable valve opening

area at 0.41 square inches. According to the valve vendor, a valve opening of 5E

corresponded to an opening size of 3.16 square inches, over 7 times the acceptable

opening.

The inspector determined that the High Pressure Injection and Residual Heat Removal

Performance Indicator information provided to the NRC was not accurate. Based on

revised data, the High Pressure Injection Performance Indicator should have been Red

while the Residual Heat Removal Performance Indicator should have been Yellow up

until the point that the safety system unavailability performance indicators were replaced

by MSPI on April 1, 2006. Specifically, revising the reported performance indicator data

to reflect the appropriate system unavailability would have caused the High Pressure

Injection Unavailability Performance Indicator to turn White in the fourth quarter of 2003

with a value of 2.5%, Yellow in the first quarter of 2004 with a value of 6.9%, and Red in

the second quarter of 2004 with a value of 11.2%. The indicator would have remained

Red until the changeover to MSPI on April 1, 2006. The Residual Heat Removal

System Unavailability Performance Indicator, which includes Containment Spray, would

Enclosure 2

-23-

have turned White in the first quarter of 2004 with a value of 3.6%, and Yellow in the

second quarter of 2004 with a value of 5.8%. The Indicator would have remained

Yellow until the changeover to MSPI on April 1, 2006.

Analysis. The failure to provide accurate information to the NRC in accordance with

10 CFR 50.9 requirements was a performance deficiency. The issue had more than

minor significance because, had the information been accurate, two performance

indicators would have changed color. Per the NRC Enforcement Policy,Section IV.A.3,

these issues are not subject to the Significance Determination Process. In determining

the violations severity level, the NRC considered a recent revision to the Mitigating

Systems Performance Indicators. Specifically, under the revised process fault exposure

hours would not be counted and the affected performance indicators would return to the

Green performance level. Additionally, the initial performance deficiency, Valve SI-602B

being left slightly open, had been evaluated under the Significance Determination

Process and found to be of very low safety significance (Green). Following identification

of the mis-positioned valve, the licensee promptly placed the valve in the correct position

which reestablished the functionality of the affected systems. The licensee conducted a

root cause evaluation of the underlying performance deficiency, and took actions to

ensure that the condition was not present on similarly operated valves. Field

verifications were conducted to ensure that similar valves were in fact, fully closed.

Accordingly, the NRC concluded that the concerns are more consistent with a Severity

Level IV violation in lieu of the Severity Level III recommendation made in the

Enforcement Policy (Supplement VII). This finding had problem identification and

resolution crosscutting aspects in that the licensees Corrective Action Program did not

thoroughly evaluate the identified condition such that information reported to NRC was

verified to be complete and accurate.

Enforcement. 10 CFR 50.9 requires, in part, that Information provided to the

Commission... by a licensee... shall be complete and accurate in all material respects.

Contrary to the above, from approximately November 1, 2004 (when the licensee initially

submitted the information) to May 11, 2006, information provided to the Commission in

the form of unavailability statistics, for the Train B high pressure safety injection and

Train B containment spray systems, was not complete and accurate in all material

respects. The licensee significantly under-reported the unavailability hours for each

train. This violation did not qualify for consideration as a noncited violation because the

violation did not meet the Enforcement Policy,Section VI.A.1.a criterion in that the

noncompliance was not corrected within a reasonable time following the identification of

the violation. For the purposes of this criterion, the violation was identified on the

inspection exit debrief date of May 11, 2006. As of the date of this inspection report

issuance, the licensee had not corrected the inaccurate information

(NOV 05000382/2006009-01).

Enclosure 2

-24-

4OA6 Meetings, Including Exit

Exit Meeting Summary

On May 11, 2006, the senior reactor inspector presented the inspection results to

Mr. Kevin Walsh, General Manager, Plant Operations and other members of the

licensees staff, who acknowledged the findings. The inspector updated the licensee by

telephone on June 23, 2006, with respect to proposed enforcement conclusions. A final

telephonic exit meeting was conducted on August 9, 2006, with respect to a subsequent

review of additional information provided by the licensee. The conclusions remained the

same. Some proprietary information was reviewed during the inspection but none of the

information was documented in this report.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment

A-1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

J. Venable, Vice President, Operations

T. Gaudet, Manager, Quality Assurance

A. Harris, Acting Director, Nuclear Safety Assurance

J. Holman, Manager, Nuclear Engineering

B. Lanka, Supervisor, Engineering Design

T. Mitchell, General Manager Plant Operations, Arkansas Nuclear One

R. Murillo, Manager, Licensing

R. Osborn, Manager, Engineering Programs and Components

K. Peter, Manager, Design Engineering

P. Stanton, Supervisor, Engineering Programs and Components

T. Tankersley, Director, Safety Assurance

K. Walsh, General Manager, Plant Operations

B. Williams, Director, Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000382/2006009-01

NOV

Inaccurate Performance Indicator Information

LIST OF DOCUMENTS REVIEWED

Condition Reports

CR-WF3-2000-00048

CR-WF3-2004-02847

CR-WF3-2006-01567

Drawings

52B8124, 24 body, SMB-00-HBC-1 Actuator Limitorque - 9200 Electric Actuated Control

Valve, Revision B

Various piping and instrumentation diagrams for the safety injection and containment spray

systems

K11131, Cross-Section Adjustable Elastomer Tee Ring in Disc Edge, dated February, 1972

Butterfly Valve Information Sheet, Sheet B-3, dated October 10, 1995

Vendor supplied drawing of valve configuration, no date, title or revision number

Attachment

A-2

Work Orders

51581

55621

66541

50686649

Miscellaneous

MPR draft letter report titled Waterford Unit 3 Safety Injection and Containment Spray

System Air Entrainment Reanalysis for Large and Medium Break LOCA, dated

February 21, 2006.

Licensee document No. 2493C, Rev. 1, Appendix D: Response to NRC Comments of

May 11, 2006

MPR-2758, Waterford 3 Safety Injection and Containment Spray Systems Past

Availability Evaluation, Revision 0

Calculation Number ECM05-007, Waterford 3 Safety Injection and Containment Spray

Systems Past Availability Evaluation for Medium Break LOCA, Revision 0

Calculation Number ECM05-006, Waterford 3 Safety Injection and Containment Spray

Systems Past Availability Evaluation, Revision 0

Root Cause Analysis Report, SI-602 B Not Fully Seated, CR-WF3-2004-2847, Dated

September 9, 2004, Report Date: November 10, 2004.

MPR-2469, Appendix J, Verification of Hydraulic Analysis Program, Revision 0

Various safety injection Valve SI-602A and SI-602B motor-operated valve VOTES

traces, dated November 6, 2003; September 11, 2004; May 5, 2005; May 7, 2005; and

May 12, 2005

White Paper, Standard of Proof for Assessing Past Operability, no date

Limitorque AC Motor Curve, 10 Ft-Pound motor

STI-W3-2005-0004-00. Special Test Instructions (STI): Leak Rate Test of SI-602B,

performed on May 25, 2005

Informal calculation to determine as-found backpressure, assuming 0.25 square inch

opening, no date

Table of trended Inservice Test data for Valve SI-602B, no revision or date

Estimated valve opening areas for 4E and 5E open positions, dated April 4, 2006

Independent Assessment of Disc Position of SI 602B between November 3, 2003, and

September 11, 2004, dated May 8, 2006, Kalsi Engineering