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| number = ML16355A293 | | number = ML16355A293 | ||
| issue date = 12/20/2016 | | issue date = 12/20/2016 | ||
| title = | | title = Evaluation of Changes, Tests, and Experiments and Permanent Modifications Team Inspection Report 05000336/2016007 and 05000423/2016007 | ||
| author name = Dentel G | | author name = Dentel G | ||
| author affiliation = NRC/RGN-I/DRS/EB2 | | author affiliation = NRC/RGN-I/DRS/EB2 | ||
| addressee name = Stoddard D | | addressee name = Stoddard D | ||
| addressee affiliation = Dominion Resources, Inc | | addressee affiliation = Dominion Resources, Inc | ||
| docket = 05000336, 05000423 | | docket = 05000336, 05000423 | ||
| license number = DPR-065, NPF-049 | | license number = DPR-065, NPF-049 | ||
| contact person = Dentel G | | contact person = Dentel G | ||
| document report number = IR 2016007 | | document report number = IR 2016007 | ||
| document type = Inspection Report, Letter | | document type = Inspection Report, Letter | ||
| page count = 21 | | page count = 21 | ||
}} | }} | ||
See also: [[ | See also: [[see also::IR 05000336/2016007]] | ||
=Text= | =Text= | ||
{{#Wiki_filter: UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 2100 RENAISSANCE BLVD., SUITE 100 KING OF PRUSSIA, PA | {{#Wiki_filter:UNITED STATES | ||
NUCLEAR REGULATORY COMMISSION | |||
Senior Vice President and Chief Nuclear Officer | REGION I | ||
Innsbrook Technical Center | 2100 RENAISSANCE BLVD., SUITE 100 | ||
5000 Dominion Blvd. Glen Allen, VA | KING OF PRUSSIA, PA 19406-2713 | ||
SUBJECT: MILLSTONE POWER STATION - EVALUATION OF CHANGES, TESTS, AND EXPERIMENTS AND PERMANENT MODIFICATIONS TEAM INSPECTION | December 20, 2016 | ||
REPORT 05000336/2016007 AND 05000423/2016007 | Mr. Daniel G. Stoddard | ||
On November 17, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an | Senior Vice President and Chief Nuclear Officer | ||
inspection at your Millstone Power Station (Millstone), Units 2 and 3. | Innsbrook Technical Center | ||
the NRC inspectors discussed the results of this inspection with Mr. John Daugherty, Site Vice President, and other members of your staff. | 5000 Dominion Blvd. | ||
Glen Allen, VA 23060-6711 | |||
The inspection examined activities conducted under your license as they relate to safety and compliance with the | SUBJECT: MILLSTONE POWER STATION - EVALUATION OF CHANGES, TESTS, AND | ||
EXPERIMENTS AND PERMANENT MODIFICATIONS TEAM INSPECTION | |||
No NRC-identified or self-revealing findings were identified during this inspection. | REPORT 05000336/2016007 AND 05000423/2016007 | ||
Dear Mr. Stoddard: | |||
On November 17, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an | |||
inspection at your Millstone Power Station (Millstone), Units 2 and 3. On November 17, 2016, | |||
the NRC inspectors discussed the results of this inspection with Mr. John Daugherty, Site Vice | |||
President, and other members of your staff. The results of this inspection are documented in | |||
the enclosed report. | |||
The inspection examined activities conducted under your license as they relate to safety and | |||
compliance with the Commissions rules and regulations and with the conditions of your license. | |||
In conducting the inspection, the team reviewed selected procedures, calculations, and records; | |||
observed activities; and interviewed station personnel. | |||
No NRC-identified or self-revealing findings were identified during this inspection. | |||
D. Stoddard -2- | |||
This letter, its enclosure, and your response (if any) will be made available for public inspection | |||
and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document | |||
Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for | |||
Withholding. | |||
Sincerely, | |||
/RA/ | |||
Glenn T. Dentel, Chief | |||
Engineering Branch 2 | |||
Division of Reactor Safety | |||
Docket Nos. 50-336 and 50-423 | |||
License Nos. DPR-65 and NPF-49 | |||
Enclosure: | |||
This | Inspection Report 05000336/2016007 and 05000423/2016007 | ||
w/Attachment: Supplementary Information | |||
cc w/encl: Distribution via ListServ | |||
ML16355A293 | |||
SUNSI Review Non-Sensitive Publicly Available | |||
OFFICE RI/DRS RI/DRP RI/DRS | |||
NAME SPindale EDiPaolo via email GDentel | |||
DATE 12/15/16 12/15/16 12/20/16 | |||
1 | |||
U.S. NUCLEAR REGULATORY COMMISSION | |||
REGION I | |||
Docket Nos. 50-336 and 50-423 | |||
License Nos. DPR-65 and NPF-49 | |||
Report Nos. 05000336/2016007 and 05000423/2016007 | |||
Licensee: Dominion Nuclear Connecticut, Inc. (Dominion) | |||
Facility: Millstone Power Station, Units 2 and 3 | |||
Location: P.O. Box 128 | |||
Waterford, CT 06385 | |||
Inspection Period: October 31, 2016 through November 17, 2016 | |||
Inspectors: S. Pindale, Senior Reactor Inspector, Division of Reactor Safety (DRS), | |||
Team Leader | |||
K. Mangan, Senior Reactor Inspector, DRS | |||
L. Dumont, Reactor Inspector, DRS | |||
M. Orr, Reactor Inspector, DRS | |||
Approved By: Glenn T. Dentel, Chief | |||
Engineering Branch 2 | |||
Division of Reactor Safety | |||
Enclosure | |||
2 | |||
SUMMARY | |||
IR 05000336/2016007 and 05000423/2016007; 10/31/2016 - 11/17/2016; Millstone Power | |||
Station, Units 2 and 3; Engineering Specialist Plant Modifications Inspection. | |||
This report covers a two week inspection of the evaluations of changes, tests, or experiments | |||
and permanent plant modifications. The inspection was conducted by four region-based | |||
engineering inspectors. No findings were identified. The NRCs program for overseeing the | |||
safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor | |||
Oversight Process, Revision 6, dated July 2016. | |||
3 | |||
REPORT DETAILS | |||
1. REACTOR SAFETY | |||
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity | |||
1R17 Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications | |||
(IP 71111.17) | |||
.1 Evaluations of Changes, Tests, and Experiments (36 samples) | |||
a. Inspection Scope | |||
The team reviewed 13 safety evaluations to evaluate whether the changes to the facility | |||
or procedures, as described in the Updated Final Safety Analysis Report (UFSAR), had | |||
been reviewed and documented in accordance with Title 10 of the Code of Federal | |||
Regulations (10 CFR) 50.59 requirements. In addition, the team evaluated whether | |||
Dominion had been required to obtain U.S. Nuclear Regulatory Commission (NRC) | |||
approval prior to implementing the changes. The team interviewed plant staff and | |||
reviewed supporting information including calculations, analyses, design change | |||
documentation, procedures, the UFSAR, technical specifications, and plant drawings to | |||
assess the adequacy of the safety evaluations. The team compared the safety | |||
evaluations and supporting documents to the guidance and methods provided in Nuclear | |||
Energy Institute (NEI) 96-07, Guidelines for 10 CFR 50.59 Evaluations, Revision 1, as | |||
endorsed by NRC Regulatory Guide 1.187, Guidance for Implementation of 10 CFR | |||
50.59, Changes, Tests, and Experiments, to determine the adequacy of the safety | |||
evaluations. | |||
The team also reviewed 23 samples of 10 CFR 50.59 screenings and applicability | |||
determinations for which Dominion had concluded that no safety evaluation was | |||
required. These reviews were performed to assess whether Dominions threshold for | |||
performing safety evaluations was consistent with 10 CFR 50.59. The samples included | |||
design changes, calculations, procedure changes, and setpoint changes. The | |||
screenings and applicability determinations were selected based on the safety | |||
significance, risk significance, and complexity of the change to the facility. | |||
Finally, the team compared Dominions administrative procedures used to control the | |||
screening, preparation, review, and approval of safety evaluations to the guidance in | |||
NEI 96-07 to determine whether those procedures adequately implemented the | |||
requirements of 10 CFR 50.59. The documents reviewed for each section of this report | |||
are listed in the Attachment. | |||
b. Findings | |||
No findings were identified. | |||
4 | |||
.2 Permanent Plant Modifications (13 samples) | |||
.2.1 MP2-11-01079, Replacement of Pressurizer Spray Manual Isolation Gate Valves 2-RC- | |||
252 and 2-RC-253 | |||
a. Inspection Scope | |||
The team reviewed modification MP2-11-01079, which installed two Class 1 manual | |||
isolation valves, replacing the existing valves. The valves are used to isolate the | |||
pressurizer spray nozzles. Dominion replaced two valves and a section of piping to | |||
correct bonnet leakage from the installed valves. The new piping and valves were | |||
installed on existing pipe supports in the containment. Dominion evaluated the seismic | |||
qualifications of the valves to verify adequate structural margin existed for design basis | |||
seismic events; and welded the new valves and piping into the system and performed | |||
associated post-maintenance testing to verify the integrity of the valves, piping, and | |||
associated welds. | |||
The team reviewed the modification to determine if the design bases, licensing bases, or | |||
performance capability of the pressurizer spray header had been degraded by the | |||
modification. The team interviewed design engineers and reviewed design drawings | |||
and calculations to determine if the new piping and valves met applicable specifications | |||
and requirements. Additionally, the team reviewed the post-modification test (PMT) | |||
results, welding certifications, and associated maintenance work orders to determine if | |||
the modification was appropriately implemented. | |||
b. Findings | |||
No findings were identified. | |||
.2.2 MP2-14-01009, Replace the Shutdown Cooling Isolation Valve 2-SI-652 Motor | |||
a. Inspection Scope | |||
The team reviewed modification MP2-14-01009, which replaced the motor for motor- | |||
operated valve 2-SI-652 with a new style motor. The motor was replaced to address | |||
industry operating experience related to corrosion issues identified with magnesium | |||
rotors. Dominion replaced the original motor with a motor of similar electrical and torque | |||
characteristics and an aluminum rotor. As part of the modification, Dominion verified the | |||
motors locked rotor amps, full load amps, and torque capability of the motor would meet | |||
valve and electrical system design requirements. Dominion also verified that the motor | |||
met seismic and environmental qualifications requirements; and motor weight and | |||
dimensions did not impact the seismic qualifications of the safety injection system. | |||
Following installation of the motor, Dominion performed a PMT to ensure design, | |||
licensing, and American Society of Mechanical Engineers (ASME) Code requirements | |||
were met. | |||
The team reviewed the modification to determine if the design bases, licensing bases, or | |||
performance capability of the motor-operated valve, safety injection system, or electrical | |||
system had been degraded by the modification. The team interviewed design engineers | |||
and reviewed design drawings, vendor documentation, and calculations to determine if | |||
the motor met the applicable specifications and requirements for the shutdown cooling | |||
5 | |||
system. Additionally, the team reviewed PMT results and associated maintenance work | |||
orders to determine if the changes were appropriately implemented and the valve test | |||
results were within the required ASME Code and licensing specifications. Finally, the | |||
team reviewed environmental qualification testing results to determine if the testing | |||
bounded the design basis post-accident containment atmosphere. | |||
b. Findings | |||
No findings were identified. | |||
.2.3 MP3-14-01187, Reactor Plant Closed Loop Cooling Water Heat Exchanger 3CCP*E1B | |||
Replacement | |||
a. Inspection Scope | |||
The team reviewed modification MP3-14-01187, which replaced one of three reactor | |||
plant closed loop cooling water (RPCCW) heat exchangers. Dominion replaced the heat | |||
exchanger to restore heat removal capacity and provide additional operating flow margin | |||
to the RPCCW system. Dominion also upgraded the heat exchanger with a more | |||
corrosion/erosion resistant Monel material. As part of the modification, Dominion | |||
redesigned the structural supports for the new heat exchanger to ensure the heat | |||
exchanger and associated RPCCW piping maintained the required Seismic I capability | |||
as required by the licensing basis. Finally, Dominion performed a PMT to assess the | |||
cooling capacity, flow velocity though the heat exchanger tubes, and the integrity of the | |||
RPCCW system. | |||
The team reviewed the modification to determine if the design bases, licensing bases, or | |||
performance capability of the RPCCW heat exchanger had been degraded by the | |||
modification. The team interviewed design engineers and reviewed design drawings, | |||
vendor documentation, and calculations to determine if the heat exchanger met the | |||
specifications and requirements for the RPCCW system. Additionally, the team | |||
reviewed the PMT results and associated maintenance work orders to determine if the | |||
changes were appropriately implemented; the heat removal capability of the heat | |||
exchanger met design requirements; and post-modification leakage results were within | |||
the required ASME Code and licensing specification. The team performed a walkdown | |||
of the heat exchanger to determine if the modification was installed in accordance with | |||
the design, and to assess the overall material conditions of the systems following the | |||
modification work. Finally, the team reviewed the 10 CFR 50.59 screening associated | |||
with this modification as described in Section 1R17.1 of this report. | |||
b. Findings | |||
No findings were identified. | |||
.2.4 MP3-12-01028, Reactor Vessel Head Vent Valve Replacements | |||
a. Inspection Scope | |||
The team reviewed modification MP3-12-01028, which replaced the reactor vessel head | |||
vent valves and associated electrical connections. The valves provide the capability to | |||
vent non-condensable gasses from the reactor vessel following a design basis event. | |||
6 | |||
Dominion performed the modification to correct degraded performance of the previously | |||
installed valves. Dominion performed pre-installation testing on the valves to ensure the | |||
valves met ASME Code leak requirements and post-installation testing to verify the | |||
integrity of the valve flange connections and the correct operation of the valves. | |||
The team reviewed the modification to determine if the design bases, licensing bases, or | |||
performance capability of the valves and associated piping had been degraded by the | |||
modification. The team interviewed design engineers and reviewed design drawings, | |||
calculations, and vendor specifications to determine if the valves met the applicable | |||
specifications and requirements of the reactor head vent system. Additionally, the team | |||
reviewed PMT results, associated maintenance work orders, and leakage test results to | |||
determine if the changes were appropriately implemented. The team reviewed | |||
environmental qualification testing results to determine if the testing bounded the | |||
projected design basis post-accident containment atmosphere. Finally, the team | |||
reviewed the 10 CFR 50.59 screening associated with this modification as described in | |||
Section 1R17.1 of this report. | |||
b. Findings | |||
No findings were identified. | |||
.2.5 MP3-13-01127, Replacement of Service Water Valves 3SWP*AOV39A&B due to | |||
Material Change | |||
a. Inspection Scope | |||
The team reviewed modification MP3-13-01127, which replaced service water air- | |||
operated butterfly isolation valves. The valves operation provided service water to the | |||
emergency diesel generator (EDG) heat exchangers. Dominion performed the | |||
modification to address identified valve degradation due to de-alloying of the cast | |||
aluminum-bronze alloy valve material. Dominion installed the same style valves with | |||
improved metallurgical properties to minimize this salt water degradation mechanism. | |||
Following installation, Dominion performed testing to verify the valves were properly | |||
installed and the ASME Code requirements were met. | |||
The team reviewed the modification to determine if the design bases, licensing bases, or | |||
performance capability of the valve and associated service water and/or air systems had | |||
been degraded by the modification. The team interviewed design engineers and | |||
reviewed design drawings, calculations, and vendor specifications to determine if the | |||
valves met the design and licensing requirements of the system. Additionally, the team | |||
reviewed PMT results and associated maintenance work orders to determine if the | |||
changes were appropriately implemented. Finally, the team performed a walkdown of | |||
the valves to determine if the modification was installed in accordance with the design, | |||
and to assess the overall material conditions of the systems following the modification | |||
work. | |||
b. Findings | |||
No findings were identified. | |||
7 | |||
.2.6 MP3-14-01156, 3HVK CHL 1B Relay Module Replacement | |||
a. Inspection Scope | |||
The team reviewed modification MP3-14-01157, which replaced an existing time delay | |||
relay module in the 19FA control building chiller with a time delay relay module | |||
conversion kit. The new installed time delay relay module conversion kit was a complete | |||
upgrade from the old relay module. However, the automatic chiller re-start feature after | |||
a loss of power, which was built-in in the original relay, was not incorporated in the new | |||
relay module design. Therefore, in order to maintain this operational feature, Dominion | |||
added an additional timing relay to the 19FA control building chiller circuitry. | |||
The team reviewed the modification to verify that the design bases, licensing bases, and | |||
performance capability of the control building chiller had not been degraded by the | |||
modification and had been adequately implemented. The team reviewed the purchase | |||
order and the certification of conformance associated with the relay module kit to verify | |||
that quality requirements, including technical, administrative, regulatory, and reporting | |||
requirements (e.g., specifications, codes, standards, tests, inspections) were specified in | |||
procurement documents. The team interviewed engineering staff to verify that the relay | |||
module design would function in accordance with its design requirements. The team | |||
also reviewed the associated work order instructions and vendor documentation to | |||
ensure that maintenance personnel had implemented the modification as designed. In | |||
addition, the team verified that procedures, design documents, and drawings affected by | |||
the modification had been adequately updated. The team performed a walkdown to | |||
independently assess the performance of the 19FA control building chiller by visually | |||
inspecting the local chiller control panel. The team reviewed the associated PMT results | |||
and the 3HVK CHL1B chiller operational performance to verify that the system | |||
functioned as designed following the modification. Finally, the team reviewed the | |||
10 CFR 50.59 screening associated with this modification as described in Section | |||
1R17.1 of this report. | |||
b. Findings | |||
No findings were identified. | |||
2.7 MP3-14-01148, Replacement of 48/15 Vdc Power Supplies for Solid State Protection | |||
System | |||
a. Inspection Scope | |||
The team reviewed modification MP-14-01149, which installed four 48/15 Vdc power | |||
supplies for the solid state protection system. There are two 48/15 Vdc power supplies | |||
per train, and each power supply provides a 48 Vdc and 15 Vdc output to the solid state | |||
protection system logic and output relays. This change was performed due to preventive | |||
maintenance that required the existing power supplies to be replaced on a ten-year | |||
frequency. The originally installed Basler Electric dual output supply unit was no longer | |||
manufactured, therefore, an equivalent power supply module was procured as a | |||
replacement. | |||
The team reviewed the modification to verify that the design bases and licensing bases | |||
of the power supplies had been adequately implemented. The team reviewed the | |||
8 | |||
equivalency change report to ensure that performance capability of the power supplies | |||
had not been degraded by the modification. The team reviewed the associated work | |||
order instructions and documentation to verify that maintenance personnel had | |||
implemented the modification as designed. The team reviewed the associated PMT | |||
requirements and results of the new power supplies to confirm that the implementation | |||
was properly executed and to verify that the system functioned as designed following the | |||
modification. In addition, the team reviewed procedures, design documents, and | |||
drawings affected by the changes to verify that these documents had been adequately | |||
updated. | |||
b. Findings | |||
No findings were identified. | |||
2.8 10000032204, MP3 Commercial Grade Dedication - Battery Charger Failure Relay | |||
a. Inspection Scope | |||
The team reviewed modification 10000032204, which replaced a relay associated with | |||
Millstone Unit 3 battery charger No. 1. This replacement relay was not designed nor | |||
manufactured as a basic component. The relay was purchased as a commercial grade | |||
item (CGI) and was dedicated by Dominion to be used as a safety-related component. | |||
Dominion characterized this replacement as a like-for-like replacement. The safety | |||
function of the relay was to maintain electrical circuit continuity in the battery charger and | |||
to change states when energized or de-energized by allowing the relay contacts to pick | |||
up or drop out. This change was performed because the original relay failed in service. | |||
The team reviewed the modification to verify that the design bases, licensing bases, and | |||
performance capability of the battery charger relay had not been degraded by the | |||
modification. The team verified that Dominions process for dedicating the CGI provided | |||
reasonable assurance that the commercial grade relay would perform its intended safety | |||
function. Specifically, the team verified that Dominion had established adequate controls | |||
for acceptance of the CGI through its receipt inspection requirements. The team verified | |||
that Dominion properly identified and verified that all critical characteristics associated | |||
with the replacement relay satisfied their respective acceptance criteria. The team | |||
reviewed the associated work order instructions and documentation to verify that | |||
maintenance personnel had implemented the modification as designed. The team | |||
reviewed the associated acceptance criteria and PMT requirements of the new relay to | |||
confirm that the implementation was properly executed and to verify that the battery | |||
charger would function as designed following the modification. Finally, the team | |||
reviewed procedures, design documents, and drawings affected by the changes to verify | |||
that these documents had been adequately updated. | |||
b. Findings | |||
No findings were identified. | |||
9 | |||
.2.9 MP2-15-01097, Reactor Protection System Bistable Trip Unit, Auxiliary Trip Units, and | |||
Trip Test Cable Assemblies Replacement | |||
a. Inspection Scope | |||
The team reviewed design change package MP2-15-01097 for a planned modification | |||
that will replace the reactor protection system (RPS) bistable trip units (BTU), the | |||
auxiliary trip units (ATU), and the trip test cable assemblies (TTCA). This design change | |||
is required to replace the obsolete BTUs, ATUs, and TTCAs for the Millstone Unit 2 | |||
RPS. This design change will replace eight BTUs, two ATUs, and a TTCA in RPS | |||
channel B during the next Unit 2 outage (2R24), and the remaining three channels (A, | |||
C, and D) will be replaced during 2R25. | |||
The team reviewed the design work package to evaluate whether the design bases, | |||
licensing bases, and performance capability of the RPS can be degraded by the | |||
modification. The team reviewed Dominions technical evaluation, design specifications, | |||
calculations, analysis, drawings, and logic control sheets to verify that design | |||
assumptions were valid. The team reviewed the procurement specification to verify that | |||
quality requirements, including technical, administrative, regulatory, and reporting | |||
requirements (e.g., specifications, codes, standards, tests, inspections) were specified in | |||
procurement documents. The team interviewed system engineers and technical staff to | |||
evaluate the adequacy of the modification. Additionally, the team reviewed the 10 CFR | |||
50.59 screening associated with this modification as described in Section 1R17.1 of this | |||
report. | |||
b. Findings | |||
No findings were identified. | |||
2.10 Calculation 96-067, Auxiliary Feedwater System Comprehensive Flow Analysis, and | |||
Modification MP3-14-01107, MP3 TDAFW Pump Overspeed Margin Change | |||
a. Inspection Scope | |||
The team reviewed Millstone Unit 3 Calculation 96-067, which was revised in support of | |||
lowering the operating speed (from 4500 to 4400 rpm) of the turbine-driven auxiliary | |||
feedwater (TDAFW) pump to gain margin to the relief valve setpoint and to increase | |||
pump reliability. This change was implemented due to prior operating experience events | |||
at Millstone Unit 3 involving TDAFW pump/turbine overspeed trips and challenging the | |||
discharge relief valve. The change involved a reduction in auxiliary feedwater (AFW) | |||
flow due to the speed reduction. In the calculation revision, Dominion evaluated the | |||
lower AFW flow on postulated events in the safety analysis. The team also reviewed the | |||
associated modification, MP3-14-01107, TDAFW Pump Overspeed Margin Change, for | |||
which the above calculation supported. | |||
The team reviewed the calculation change to determine if the design bases, licensing | |||
bases, or performance capability of the AFW system had been degraded by reduction in | |||
TDAFW pump operating speed. The team interviewed design engineers and reviewed | |||
the revised calculation and associated design basis events to determine whether the | |||
change met design and licensing requirements. Surveillance procedures, including test | |||
results, were reviewed by the team to determine whether the results were bounded by | |||
10 | |||
the modification and existing analyses. The 10 CFR 50.59 safety evaluation associated | |||
with this change was also reviewed as described in Section 1R17.1 of this report. | |||
b. Findings | |||
No findings were identified. | |||
2.11 MP3-14-01070, Replace Emergency Diesel Generator Air Cooler Service Water Relief | |||
Valves M33SWP*RV90A/RV90B | |||
a. Inspection Scope | |||
The team reviewed modification MP3-14-01070 that Dominion implemented to replace | |||
the service water system thermal protection relief valves to the Unit 3 EDG air coolers. | |||
The function of the relief valves is to provide overpressure protection to the service water | |||
side of the safety-related EDG combustion air heat exchangers in the event of an | |||
unintentional equipment isolation or a thermal transient during component lay-up | |||
conditions. The original relief valves were configured with a metal-to-metal seat design | |||
that was susceptible to the effects of corrosion and debris, resulting in failure to lift within | |||
the specified tolerance of the set pressure. The modification allowed for a soft seat | |||
configuration for both of the system relief valves. | |||
The team reviewed the modification to determine if the design and licensing bases, and | |||
performance capability of the EDG system had been degraded by any of the associated | |||
equipment, process, and/or procedure changes. The team interviewed design | |||
engineers, and reviewed evaluations, surveillance results, technical data sheets, and | |||
associated maintenance activities to verify that Dominion appropriately implemented the | |||
design change in accordance with their design process and assumptions. The team | |||
performed walkdowns of accessible portions of the EDG and service water systems to | |||
assess configuration control and the material condition of the associated components. | |||
The team also reviewed condition reports, completed preventive maintenance activities, | |||
and the EDG system operating logs to determine if there were reliability or performance | |||
issues that may have resulted from the modification. | |||
b. Findings | |||
No findings were identified. | |||
.2.12 MP3-14-01027, Motor-Driven Auxiliary Feed Pump Lube Oil Pump 3FWL*P6A | |||
Replacement | |||
a. Inspection Scope | |||
The team reviewed modification MP3-14-01027 that Dominion implemented to replace | |||
the direct drive (shaft-driven) lube oil pump 3FWL*P6A for AFW pump 3FWA*P1A, due | |||
to unrepairable minor seal leakage and component obsolescence. The AFW pumps | |||
lube oil pump is designed to provide the necessary lubricating oil to the motor-driven | |||
AFW pump. The replacement lube oil pump has slightly different suction and discharge | |||
piping connections, as well as different orientation, which required some minor piping | |||
replacement and rerouting. The replacement lube oil pump was determined to be an | |||
acceptable equivalent replacement pump for the existing 3FWL*P6A. | |||
11 | |||
The team reviewed the modification to determine if the design bases, licensing bases, or | |||
performance capability of the motor-driven AFW pump had been degraded by the | |||
modification. The team interviewed design and system engineers and reviewed | |||
installation procedures, surveillance results, and associated maintenance activities to | |||
determine if the new lube oil pump, piping, and configuration met design specifications | |||
and requirements of the system. The team performed a walkdown of both motor-driven | |||
AFW pumps and the TDAFW pump rooms to assess configuration comparisons and | |||
material conditions. | |||
b. Findings | |||
No findings were identified. | |||
2.13 MP2-14-01001, Replace Emergency Diesel Generator M-7A Service Water Coolers | |||
Supply and Discharge Lines with AL-6XN Material | |||
a. Inspection Scope | |||
The team reviewed modification MP2-14-01001 that replaced 6-inch and 8-inch lined | |||
carbon steel flanged pipe spools on the A train service water supply header to the | |||
Unit 2 A EDG jacket water cooling, lube oil cooling, and air cooler heat exchangers. | |||
The modification also included the replacing previously-installed AL6XN material pipe | |||
spools to correct flange alignment issues, replacing check valve 2-SW-13A with an | |||
AL6XN pipe spool, and replacing stainless steel flow restricting orifices. The | |||
modifications were necessary to eliminate dissimilar metal galvanic interactions and | |||
corrosion issues. | |||
The review was performed to determine if the design bases, licensing bases, or | |||
performance capability of the A EDG had been degraded by the modifications. Design | |||
assumptions were reviewed to evaluate whether they were technically appropriate and | |||
consistent with the UFSAR. The team discussed the impact of the modification on the | |||
EDG operation with responsible engineers. Additionally, the team reviewed | |||
maintenance work orders to confirm that the modifications were appropriately | |||
implemented. The team performed walkdowns of the EDG to assess the quality of the | |||
modification work and the overall material condition of the equipment. The adequacy of | |||
the PMT was verified, and affected design documents and drawings were reviewed to | |||
ensure they had been properly updated. Additionally, the equivalent 10 CFR 50.59 | |||
screen associated with this modification was reviewed as described in Section 1R17.1 of | |||
this report. | |||
b. Findings | |||
No findings were identified. | |||
12 | |||
4. OTHER ACTIVITIES | |||
4OA2 Identification and Resolution of Problems (IP 71152) | |||
a. Inspection Scope | |||
The team reviewed a sample of problems that Dominion had previously identified and | |||
entered into the corrective action program. The team reviewed these issues to verify an | |||
appropriate threshold for identifying issues and to evaluate the effectiveness of | |||
corrective actions. In addition, the team reviewed corrective action condition reports | |||
written on issues identified during the inspection to verify adequate problem identification | |||
and incorporation of the problem into the corrective action system. | |||
b. Findings | |||
No findings were identified. | |||
4OA6 Meetings, including Exit | |||
The team presented the inspection results to Mr. John Daugherty, Site Vice President, | |||
and other members of Dominion staff at an exit meeting on November 17, 2016. The | |||
team returned the proprietary information reviewed during the inspection to Dominion | |||
staff and verified that this report does not contain proprietary information. | |||
ATTACHMENT: SUPPLEMENTARY INFORMATION | |||
A-1 | |||
SUPPLEMENTARY INFORMATION | |||
KEY POINTS OF CONTACT | |||
Dominion Personnel | |||
D. Coleman, Nuclear Technical Specialist | |||
E. Dundon, System Engineer | |||
J. Farley, System Engineer | |||
T. Fecteau, Design Contractor | |||
J. Gardner, System Engineer | |||
Z. Hoagland, System Engineer | |||
R. Kasuga, Design Engineer | |||
M. Legg, Nuclear Engineer | |||
S. OHearn, Nuclear Engineer | |||
F. Perkins, System Engineer | |||
R. Perry, System Engineer | |||
T. Raetz, Design Engineer | |||
T. Ryan, System Engineer | |||
J. Scheeler, Electrical Engineer | |||
C. Thomas, System Engineering | |||
R. Wells, Nuclear Engineer | |||
P. Wynn, Procurement Engineer | |||
NRC Personnel | |||
J. Ambrosini, Senior Resident Inspector | |||
ITEMS OPENED, CLOSED AND DISCUSSED | |||
None | |||
LIST OF DOCUMENTS REVIEWED | |||
10 CFR 50.59 Evaluations | |||
E-14-00075-000, Retire-in-Place of MP2 De-icing Line for the Intake Structure, Revision 0 | |||
MP-EVAL-SAF-S2-EV-15-0001, OP 230J, Changes to Procedure for Boron Injection, Revision 0 | |||
MP-EVAL-SAF-SG-EV-15-0004, Time to Restore Offsite Power to a Good Element, | |||
Revision 0 | |||
S2-EV-13-0001, Reanalysis of the MP2 LOCA and MSL Break Containment Analysis, | |||
Revision 0 | |||
S2-EV-14-0002, Procedure Change, Upender Vertical Input to Fuel Transfer System, 4/13/14 | |||
S3-EV-13-0002, MP3 Rod Withdrawal from Subcritical Analysis, 4/9/13 | |||
S3-EV-13-0003, Analytical Basis of MP3 LBLOCA Containment Response, 4/29/13 | |||
S3-EV-14-0001, SP 3622.9 (TDAFW Pump Full Flow Test) in Mode 1, Revision 1 | |||
S3-EV-14-0004, MP3 TDAFW Pump Operating Speed Change from 4500 to 4400 RPM, | |||
12/2/15 | |||
Attachment | |||
A-2 | |||
S3-EV-14-0005, MP3 Compensatory Action to Control Rate of Opening and Closing TDAFW | |||
Pump Discharge Flow Control Valves, 10/15/14 | |||
SG-EV-15-0002, 345 kV Protective Relay Digital Upgrade, Revision 0 | |||
SG-EV-15-0002, 345 kV Switchyard Breaker Revised Close/Open Cycles, Revision 1 | |||
SG-EV-15-0005, 345 kV Switchyard Breaker-and-Half Configuration, 6/17/15 | |||
10 CFR 50.59 Screened-out Evaluations | |||
MPS2-SCRN-2016-0065-0, C Service Water Discharge Strainer Motor Full Load Amps Greater | |||
than Nameplate, 4/22/16 | |||
MPS2-SCRN-2016-0087-0, Belzona Repair of MP2 Primary Water Transfer Pump Shaft, 5/3/16 | |||
MPS2-SCRN-2016-0124-0, Helecoil Installed in Bonnet Stud Hole of Valve 2-CN-52 to Repair | |||
Damaged Thread per ETE-MP-2011-0067, 7/19/16 | |||
MPS2-SCRN-2016-0143-1, Adjust Packing Load on 2-FW-51B to Eliminate Packing Leakage | |||
without Invalidating Stroke Time Results, 8/7/16 | |||
MPS2-SCRN-2016-0166-0, Replace Valve 2-SW-3.1B with AL-6XN Material, 12/30/15 | |||
MPS2-SCRN-2016-0190-0, Replace Hart Monitor LY-5030A-1 with Firmware Version, 10/19/16 | |||
MPS3-SCRN-2015-0006-0, TDAFW Governor Speed Control Switch Logic Change, 4/22/16 | |||
MPS3-SCRN-2016-0072-0, Change Trip Setpoint for MP3 Pressurizer Safety Valves Flow | |||
Monitoring Switches, 5/2/16 | |||
MPS3-SCRN-2016-0078-1, SLCRS Damper 3HVV*MOD51D Repair, 4/29/16 | |||
MPS3-SCRN-2016-0123-0, MP3 Diesel Instrument Air System, 7/28/16 | |||
MPS3-SCRN-2016-0161-0, SBO DG Vibration-Powered Hour Meter Installation, 10/4/16 | |||
MPS3-SCRN-2016-0164-0, Installation of Oversized Motor Termination Box, 9/6/16 | |||
Screen for AOP 3562, Loss of Instrument Air, 8/14/14 | |||
Screen for Changing MOV 2-SI-652 from Torque Switch to Limit Switch Control, 4/26/14 | |||
Screen for Construction of Permanent Scaffold Frames in MP2 Containment, 4/1/15 | |||
Screen for ETE-MP-2016-1097, Insulation around Yoke of Feedwater Control Valves, 6/14/16 | |||
Screen for IC 2418B/012-00, Revised TI-114 Alarm Setpoint for TCC-MP-2014-018, 8/13/14 | |||
Screen for Implementing Automatic Start Feature for the SBO Diesel Generator, 12/8/15 | |||
Screen for Installation of a Non-Safety-Related Positive Displacement Pump for Refill of the | |||
Safety Injection Accumulator, 8/17/15 | |||
Screen for OP 2204/025-10, Revise OP 2204 to Restore Functionality of RM-4296A/B, 7/11/14 | |||
Screen for Opening RHR Suction MOV breakers, 10/23/13 | |||
Screen for Rerate of MS3 Service Water Strainers to 100 psig at 100 degrees F, 5/9/14 | |||
Screen for Retire-in-Place of Millstone Unit 2 De-icing Line for the Intake Structure, 3/9/15 | |||
Modifications | |||
10000032204, MP3 GDC Battery Charger Failure Relay, Revision, 00 | |||
Calculation 96-067, MP3 Auxiliary Feedwater System Comprehensive Flow Analysis, 10/22/14 | |||
MP2-11-01079, Replacement of Pressurizer Spray Manual Isolation Gate Valves 2-RC-252 and | |||
2-RC-253, Revision 1 | |||
MP2-14-01001, EDG M-7A SW Coolers Supply/Discharge Lines with AL-6XN Material, 3/4/15 | |||
MP2-14-01009, Replace Shutdown Cooling Isolation Valve 2-SI-652 Motor, Revision 0 | |||
MP2-15-01097, MP2 RPS Bistable Trip Unit, Auxiliary Trip Units, and Trip Test Cable | |||
Assemblies Replacement, 9/14/16 | |||
MP3-12-01028, MP3 Reactor Vessel Head Vent Valve Replacements, Revision 1 | |||
MP3-13-01127, MP3 Replacement of Service Water Valves 3SWP*AOV39A&B due to Material | |||
Change, Revision 0 | |||
MP3-14-01027, Motor-Driven AFW Pump Lube Oil Pump 3FWL*P6A Replacement, 4/9/14 | |||
MP3-14-01070, Replace EDG Air Cooler SW Relief Valves M33SWP*RV90A/RV90B, 6/11/14 | |||
MP3-14-01107, MP3 TDAFW Pump Overspeed Margin Change, 12/2/15 | |||
A-3 | |||
MP3-14-01149, Replacement of 48/15 Vdc Power Supplies for SSPS, 10/8/14 | |||
MP3-14-01156, 3HVK CHL 1B Relay Module Replacement, 2/24/15 | |||
MP3-14-01187, MP3 RPCCW Heat Exchanger 3CCP*E1B Replacement, Revision 010 | |||
Calculations and Evaluations | |||
12-001, MP2 SW Model and Design Basis Analysis, Revision 2 | |||
12-350, MP3 Required SW Flow Rate to the CCP Heat Exchangers at 80 degrees F during | |||
LOOP and during an SIS, Revision 1 | |||
527012-189-EM, MP2 Pipe Support Calculation SW System Support No. 527012, Revision 4 | |||
90-069-01065M3, MP3 SW System, GL 89-13, Item IV, Design Basis Summary, Revision 2 | |||
95-052, Safety Grade Cold Shutdown Design Basis Analysis, Revision 6 | |||
96-001, Empirical Adjustment of the MP3 SW Model to 1995 Flow Test Data and Incorporation | |||
of the Latest SW System Design Change Notices, Revision 3 | |||
96-ENG-01279M3, MP3 - Thermal Performance Evaluation of Designated In-Service and | |||
Discretionary Components Subject to Elevated CCP Temperatures during SGCS, | |||
Revision 0 | |||
97-014, MP3 AFW System Determination of AFW Turbine and Pump Speed and AFW System | |||
Flows for Reduced Steam Generator Pressures, 10/6/14 | |||
97-129, CCP System Heat Exchangers - Process Side Temperatures Resulting from CCP | |||
System Operation at 33 F, Revision 1A | |||
CM-AA-CLC-301, SBO Calculation for NUMARC 87-00, Power Uprate to 3650 MW, 10/9/14 | |||
CR- M2-98-1764, Qualified Life of Agastat ETR/EGP/EML and E7000 Timer Delay and Control | |||
Relays, 6/18/98 | |||
DON-NAF-3-0.0-P-A, GOTHIC Methodology for Analyzing the Response to Postulated Pipe | |||
Ruptures Inside Containment, September 2006 | |||
EEQ-TRA-146.0, Qualification Extension Analysis Report for the Environmental Qualification of | |||
the Target Rock Solenoid Operated Globe Valves Model 12E-001, Revision 3 | |||
ETE-MP-2016-1066, Restore Sealing Capability of Damper 3HVV*MOD51D, Revision 1 | |||
ETE-MP-2016-1071, Repair of B Primary MU Water Transfer Pump Shaft (P22B), Revision 0 | |||
ETE-MP-2016-1096, MP2 Steam Generator Feedwater Regulating Valve (2-FW-51B) On-Line | |||
Packing Adjustment, Revision 2 | |||
ETE-MP-2016-1122, Oversize Motor Termination Box for 3CND-P11B, 9/6/16 | |||
ETE-NAF-2012-0152, Implementation of Revised MP2 Containment Analysis Results Required | |||
to Close OD000281 and to Support an Increase in the Ultimate Heat Sink to 80 F, | |||
Revision 0 | |||
ETE-NAF-2013-0002, Implementation of LOCA Containment Analysis with Corrected LOCA | |||
Mass and Energy Releases for MP3, Revision 0 | |||
ETE-NAF-2013-0008, Implementation of the ABB-NV Rod Withdrawal from Subcritical Analysis | |||
for MP 3, Revision 0 | |||
ETE-NAF-3013-0106, Assessment of Operator Vital Area Actions Dose for Powering Residual | |||
Heat Removal System Motor-Operated Valves, Revision 0 | |||
Condition Reports | |||
04-03344 235877 316440 346853 446496 451173 456066 | |||
467710 503721 506095 507788 524412 538015 542278 | |||
544616 549055 549422 551353 553558 555213 563418 | |||
563418 565191 575918 577364 578905 1030128 | |||
1030852 1035794 1036047 1037622 1053463* 1053479* | |||
* Generated as result of this inspection | |||
A-4 | |||
Design & Licensing Bases | |||
Safety Evaluation by the Office of Nuclear Reactor Regulation, in the Matter of Combustion | |||
Engineering, Incorporated CESSAR System 80 Docket No. STN 50-470, December 1975 | |||
Safety Evaluation by the Office of Nuclear Reactor Regulation, Related to Amendment No. 139 | |||
the Facility Operating License No. DPR-65, 3/20/89 | |||
MP2 UFSAR, Revision 34.1 | |||
MP3 UFSAR, Revision 29.1 | |||
Drawings | |||
103225, Shts. 1 - 6, PC ASSY Bistable Trip Module, RPS, Revision B | |||
1501042-M-25203-26008, Sht. 2, MP2 Service Water, Revision 0 | |||
25203-20182, Sht. 1, M-7A Cooling Heat Exchangers SW Supply/Discharge Piping, Revision 10 | |||
25203-26017, Sht. 1, Charging System, Revision 64 | |||
25203-26017, Sht. 2, Deborating and Purification System, Revision 38 | |||
25203-26017, Sht. 3, Boric Acid System, Revision 45 | |||
25212-23018, Sht. 207, Service Water Piping Diesel Generator Building, Revision 6 | |||
25212-23018, Sht. 208, Service Water Piping Diesel Generator Building, Revision 7 | |||
25212-26904, Sht. 1, Chemical and Volume Control, Revision 54 | |||
25212-26913, Sht. 1, High Pressure Safety Injection, Revision 32 | |||
25212-26933, Sht. 4, Service Water, Revision 48 | |||
25212-29041, Sht. 16, Lube Oil Piping - Motor Driven AFW Pump, Revision G | |||
25212-29061, Sht. 15, Control Bldg Water Chill Electrical Diagram [3HVK*CHL1B], Revision 15 | |||
25212-29186, Sht. 10, Pressure Relief Valve, Revision A | |||
25212-29186, Sht. 2, Pressure Relief Valve, Revision 2 | |||
25212-32001, Sht. 7KJ, 120 Vac Control Building Chiller Auxiliary Circuits, Revision 12 | |||
6822-34868A, Shts. 1 and 2, Reactor Protective System, Bistable Trip Unit Schematic, 4/8/79 | |||
D-18767-411-301, Auxiliary Trip Unit Schematic, Revision 2 | |||
NCB-1486-E, ARR130K200F, Summary Relay and ET-6 Alarm Light, 11/9/79 | |||
Miscellaneous | |||
25203-29016, Sht. 23, Certified Test Curve for B&W Pump V2660-40, 11/7/72 | |||
45895745, Purchase Order for Module, Relay, Assembly, Conversion kit, 1/2/12 | |||
ANF-87-161, MP2 Plant Transient Analysis Report - Chapter 15 Events, September 1988 | |||
ANF-87-161, Supplement 1, MP2 Plant Transient Analysis Report - Chapter 15, October 1988 | |||
DCN DM3-00-0166-09, Change Alpha Service Water Relief Valves to Soft Seats, 11/15/09 | |||
DCN DM3-00-0167-09, Change Bravo Service Water Relief Valves to Soft Seats, 11/15/09 | |||
DCN MP2-15-01161, Replace Valve 2-SW-3.1B with AL-6XN Material, Revision 0 | |||
DCN MP3-16-01071, Install Non-Resettable Hour Meter on Station Blackout Diesel Generator | |||
Engine 3BGS-BG-A, Revision 0 | |||
DNES-AA-GN-1002, Document Impact Summary, Revision 13 | |||
DR-2994, Velan Design/Seismic Report for 3 1500 Special Class Bolted Bonnet Gate Valve with | |||
Handwheel - Nuclear Class 1, Revision A | |||
MP2-13-01204, MP2 De-icing Line Retirement, Revision 1 | |||
MP3-13-01034, Ultimate Heat Sink Temperature, LCO Increase from 75 to 80 °F, 7/26/13 | |||
NEI 01-0, Guideline on Licensing Digital Upgrade, Revision 1 | |||
OP 3346A-14, EDG A Operating Logs, 1/19/16 through 9/27/16 | |||
OP 3346A-15, EDG B Operating Logs, 2/2/16 through 10/12/16 | |||
PO-MAT-0045938321, Curtiss Wright Flow Control Co, Supporting Documents for Receipt | |||
Inspection Report Package, 4/8/13 | |||
Receipt Inspection Report Package for the Battery Charger relay, 11/1/14 | |||
SO-14-017, Standing Order, Throttling TDAFW Pump Flow, Revision 1 | |||
Specification for Mechanical Refrigeration Unit, Control Building Water Chiller Cat. 1, 11/13/73 | |||
A-5 | |||
TCC-MP-2014-012, Manual Switch to Replace Fuel Transfer System Upender Vertical Position | |||
Proximity Switch, Reactor Side, Revision 0 | |||
Wyle Seismic Qualification Test Report on Two Battery Charger, 4/26/83 | |||
Procedures | |||
CEN 110, Post Repair/Replacement Leakage Test, Revision 4 | |||
CM-AA-400, 10 CFR 50.59 and 10 CFR 72.48 - Changes, Tests, and Experiments, Revision 8 | |||
CM-AA-DDC-201, Design Change, Revision 17 | |||
CM-AA-RSK-1001, Engineering Risk Assessment, Revision 14 | |||
DNES-AA-GN-1005, Failure Modes and Effects Analysis (FMEA), Revision 3 | |||
IC 2418B, RCS Temperature Instrument Calibration, Revision 015-00 | |||
MP 2703C3, I. R. Chemliner Pump, Revision 8 | |||
MP 3710AA-149E, Lubrication Maintenance Technique, Auxiliary Feedwater Pump Oil and | |||
Strainer Change, Revision 2 | |||
MP 3762WB, Generic Relief Valve Maintenance, Revision 8 | |||
MP-02-NO-GDL405, Determination of Inspection Requirements for Quality Activities, Revision 7 | |||
MP-20-WP-GDL40, Pre and Post Maintenance Testing, Revision 14 | |||
NC 1900.3B, Application of Belzona Products, Revision 1 | |||
OP 2204, Load Changes, Revision 034 | |||
OP 2304J, Boric Acid Addition to CVCS from a Temporary Borated Water Source, Revision 1 | |||
OP 3310B, Accumulator Low Pressure Safety Injection, Revision 17 | |||
OP 3314F, Control Building HVAC and Chill Water, Revision 033-00 | |||
OP 3322, Auxiliary Feedwater System, Revision 026 | |||
OP 3353.VP1C, Main Ventilation and AC Panel VP1C Annunciator Response, Revision 007-00 | |||
OPS-FH 202, Transfer Carriage and Upender Operations, Revision 4 | |||
PI-AA-200, Corrective Action, Revision 32 | |||
PT 31459A, MP# Timing Device Calibration Program, Revision 009 | |||
SP 2613A, Diesel Generator Operability Tests, Facility 1, Revision 25 | |||
SP 2613B, Diesel Generator Operability Tests, Facility 2, Revision 26 | |||
SP 3622.8, Auxiliary Feedwater Valve Operability Test, Revision 010-06 | |||
SP 3622.8-005, 3FWA*P2 Discharge Isolation Valves Stroke Time Test, Revision 000-06 | |||
SP 3622.8-012, TDAFW Pump Control Valves Stroke Time, Revision 02 | |||
SP 3626.13, Service Water Heat Exchangers Fouling Determination, Revision 22 | |||
SP 3626.14, RSS Heat Exchanger SW Supply Piping Flush, Revision 4 | |||
SP 3646A.1, Emergency Diesel Generator A Operability Test, Revision 20 | |||
SP 3646A.2, Emergency Diesel Generator B Operability Test, Revision 22 | |||
WM-AA-301, Operational Risk Assessment, Revision 13 | |||
Surveillance, Functional, and Modifications Acceptance Tests | |||
CBM 104, Vibration Data Acquisition and Overall Vibration Analysis, performed 11/13/14 | |||
CMP 715E, General Practices Flanges and Threaded Fasteners, performed 5/29/15 and 2/15/16 | |||
CMP 727A, Testing and Setting Pressure Relief Valves, performed 9/11/14 and 2/14/16 | |||
CMP 799D, Cutting of Installed Plant Piping, performed 10/28/14 | |||
MP 3762WB, Generic Relief Valve Maintenance, performed 2/15/16 | |||
MP-VE-9, Visual Weld Acceptance Criteria, Weldments and Brazed Joints, performed 10/28/14 | |||
OP 3346A, Emergency Diesel Generator, performed 1/19/16, 2/20/16, 6/7/16 and 9/27/16 | |||
SP 2613K, DG Slow Start Operability Test, Facility 1, performed 9/19/15 and 10/19/16 | |||
SP 2613L-001, Periodic DG Slow Start Operability Test, Facility 2 (Loaded Run), performed | |||
10/07/15 and 10/02/16 | |||
SP 2670-007, Diesel Generator B Heat Exchanger D/P Determination, performed 10/02/16 | |||
SP 3446F31-001, SSPS Refueling Tests, performed 4/22/16 | |||
SP 3622.1, AFW Pump 3FWA*P1A Operational Readiness Test, performed 11/13/14 | |||
SP 3622.3-001, TDAFW Pump Operational Readiness and Quarterly IST Group B Pump Tests, | |||
performed 5/11/16 and 8/8/16 | |||
A-6 | |||
SP 3622.8-001, Auxiliary Feedwater Train A Valve Stroke Time, performed 10/17/16 | |||
SP 3622.8-001, TDAFW Pump Control Valves Stroke Time, performed 8/8/16 | |||
SP 3622.8-005, 3FWA*P2 Discharge Isolation Valves Stroke Time Test, performed 5/18/16 | |||
SP 3622.8-009, Auxiliary Feedwater Train B Valve Stroke Time, performed 9/5/16 | |||
SP 3622.9-001, TDAFW Pump Full Flow Test in Mode 1, performed 1/27/14 | |||
SP 3626.3, 3SWP*AOV39B, EDG B Service Water HX Outlet, Stroke Test, performed 4/17/16 | |||
Vendor Manuals, Standards, and Specifications | |||
25212-041-001, Sulzer Bingham Pump - Installation, Operation and Maintenance of Motor- | |||
Driven Auxiliary Feedwater Pumps, Revision 9 | |||
25212-260-002, Installation, Operation & Maintenance of 200 AMP Battery Charger, Revision 1 | |||
Agastat Nuclear Qualified Time Delay Relays, Revision 1 | |||
Tyco Electronics GP/ML/TR Series 10 Amp Control Relay Non-lathing, Latching & Timing | |||
Versions, Revision 3-13 | |||
Work Orders | |||
53102428795 53102785317 53102737935 | |||
53102437234 53102849166 53102737943 | |||
53102443647 53102351580 53102885049 | |||
53102633524 53102539957 | |||
53102783755 53102618701 | |||
LIST OF ACRONYMS | |||
10 CFR Title 10 of the Code of Federal Regulations | |||
AFW auxiliary feedwater | |||
ASME American Society of Mechanical Engineers | |||
ATU auxiliary trip unit | |||
BTU bistable trip unit | |||
CGI commercial grade item | |||
DRS Division of Reactor Safety | |||
EDG emergency diesel generator | |||
NEI Nuclear Energy Institute | |||
NRC Nuclear Regulatory Commission | |||
PMT post-modification test | |||
RPCCW reactor plant closed cooling water | |||
RPS reactor protection system | |||
TDAFW turbine-driven auxiliary feedwater | |||
TTCA trip test cable assembly | |||
UFSAR Updated Final Safety Analysis Report | |||
}} | }} |
Latest revision as of 10:07, 30 October 2019
ML16355A293 | |
Person / Time | |
---|---|
Site: | Millstone |
Issue date: | 12/20/2016 |
From: | Glenn Dentel Engineering Region 1 Branch 2 |
To: | Stoddard D Dominion Resources |
Dentel G | |
References | |
IR 2016007 | |
Download: ML16355A293 (21) | |
See also: IR 05000336/2016007
Text
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION I
2100 RENAISSANCE BLVD., SUITE 100
KING OF PRUSSIA, PA 19406-2713
December 20, 2016
Mr. Daniel G. Stoddard
Senior Vice President and Chief Nuclear Officer
Innsbrook Technical Center
5000 Dominion Blvd.
Glen Allen, VA 23060-6711
SUBJECT: MILLSTONE POWER STATION - EVALUATION OF CHANGES, TESTS, AND
EXPERIMENTS AND PERMANENT MODIFICATIONS TEAM INSPECTION
REPORT 05000336/2016007 AND 05000423/2016007
Dear Mr. Stoddard:
On November 17, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an
inspection at your Millstone Power Station (Millstone), Units 2 and 3. On November 17, 2016,
the NRC inspectors discussed the results of this inspection with Mr. John Daugherty, Site Vice
President, and other members of your staff. The results of this inspection are documented in
the enclosed report.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
In conducting the inspection, the team reviewed selected procedures, calculations, and records;
observed activities; and interviewed station personnel.
No NRC-identified or self-revealing findings were identified during this inspection.
D. Stoddard -2-
This letter, its enclosure, and your response (if any) will be made available for public inspection
and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document
Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for
Withholding.
Sincerely,
/RA/
Glenn T. Dentel, Chief
Engineering Branch 2
Division of Reactor Safety
Docket Nos. 50-336 and 50-423
License Nos. DPR-65 and NPF-49
Enclosure:
Inspection Report 05000336/2016007 and 05000423/2016007
w/Attachment: Supplementary Information
cc w/encl: Distribution via ListServ
SUNSI Review Non-Sensitive Publicly Available
OFFICE RI/DRS RI/DRP RI/DRS
NAME SPindale EDiPaolo via email GDentel
DATE 12/15/16 12/15/16 12/20/16
1
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Docket Nos. 50-336 and 50-423
License Nos. DPR-65 and NPF-49
Report Nos. 05000336/2016007 and 05000423/2016007
Licensee: Dominion Nuclear Connecticut, Inc. (Dominion)
Facility: Millstone Power Station, Units 2 and 3
Location: P.O. Box 128
Waterford, CT 06385
Inspection Period: October 31, 2016 through November 17, 2016
Inspectors: S. Pindale, Senior Reactor Inspector, Division of Reactor Safety (DRS),
Team Leader
K. Mangan, Senior Reactor Inspector, DRS
L. Dumont, Reactor Inspector, DRS
M. Orr, Reactor Inspector, DRS
Approved By: Glenn T. Dentel, Chief
Engineering Branch 2
Division of Reactor Safety
Enclosure
2
SUMMARY
IR 05000336/2016007 and 05000423/2016007; 10/31/2016 - 11/17/2016; Millstone Power
Station, Units 2 and 3; Engineering Specialist Plant Modifications Inspection.
This report covers a two week inspection of the evaluations of changes, tests, or experiments
and permanent plant modifications. The inspection was conducted by four region-based
engineering inspectors. No findings were identified. The NRCs program for overseeing the
safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor
Oversight Process, Revision 6, dated July 2016.
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REPORT DETAILS
1. REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R17 Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications
.1 Evaluations of Changes, Tests, and Experiments (36 samples)
a. Inspection Scope
The team reviewed 13 safety evaluations to evaluate whether the changes to the facility
or procedures, as described in the Updated Final Safety Analysis Report (UFSAR), had
been reviewed and documented in accordance with Title 10 of the Code of Federal
Regulations (10 CFR) 50.59 requirements. In addition, the team evaluated whether
Dominion had been required to obtain U.S. Nuclear Regulatory Commission (NRC)
approval prior to implementing the changes. The team interviewed plant staff and
reviewed supporting information including calculations, analyses, design change
documentation, procedures, the UFSAR, technical specifications, and plant drawings to
assess the adequacy of the safety evaluations. The team compared the safety
evaluations and supporting documents to the guidance and methods provided in Nuclear
Energy Institute (NEI) 96-07, Guidelines for 10 CFR 50.59 Evaluations, Revision 1, as
endorsed by NRC Regulatory Guide 1.187, Guidance for Implementation of 10 CFR
50.59, Changes, Tests, and Experiments, to determine the adequacy of the safety
evaluations.
The team also reviewed 23 samples of 10 CFR 50.59 screenings and applicability
determinations for which Dominion had concluded that no safety evaluation was
required. These reviews were performed to assess whether Dominions threshold for
performing safety evaluations was consistent with 10 CFR 50.59. The samples included
design changes, calculations, procedure changes, and setpoint changes. The
screenings and applicability determinations were selected based on the safety
significance, risk significance, and complexity of the change to the facility.
Finally, the team compared Dominions administrative procedures used to control the
screening, preparation, review, and approval of safety evaluations to the guidance in
NEI 96-07 to determine whether those procedures adequately implemented the
requirements of 10 CFR 50.59. The documents reviewed for each section of this report
are listed in the Attachment.
b. Findings
No findings were identified.
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.2 Permanent Plant Modifications (13 samples)
.2.1 MP2-11-01079, Replacement of Pressurizer Spray Manual Isolation Gate Valves 2-RC-
252 and 2-RC-253
a. Inspection Scope
The team reviewed modification MP2-11-01079, which installed two Class 1 manual
isolation valves, replacing the existing valves. The valves are used to isolate the
pressurizer spray nozzles. Dominion replaced two valves and a section of piping to
correct bonnet leakage from the installed valves. The new piping and valves were
installed on existing pipe supports in the containment. Dominion evaluated the seismic
qualifications of the valves to verify adequate structural margin existed for design basis
seismic events; and welded the new valves and piping into the system and performed
associated post-maintenance testing to verify the integrity of the valves, piping, and
associated welds.
The team reviewed the modification to determine if the design bases, licensing bases, or
performance capability of the pressurizer spray header had been degraded by the
modification. The team interviewed design engineers and reviewed design drawings
and calculations to determine if the new piping and valves met applicable specifications
and requirements. Additionally, the team reviewed the post-modification test (PMT)
results, welding certifications, and associated maintenance work orders to determine if
the modification was appropriately implemented.
b. Findings
No findings were identified.
.2.2 MP2-14-01009, Replace the Shutdown Cooling Isolation Valve 2-SI-652 Motor
a. Inspection Scope
The team reviewed modification MP2-14-01009, which replaced the motor for motor-
operated valve 2-SI-652 with a new style motor. The motor was replaced to address
industry operating experience related to corrosion issues identified with magnesium
rotors. Dominion replaced the original motor with a motor of similar electrical and torque
characteristics and an aluminum rotor. As part of the modification, Dominion verified the
motors locked rotor amps, full load amps, and torque capability of the motor would meet
valve and electrical system design requirements. Dominion also verified that the motor
met seismic and environmental qualifications requirements; and motor weight and
dimensions did not impact the seismic qualifications of the safety injection system.
Following installation of the motor, Dominion performed a PMT to ensure design,
licensing, and American Society of Mechanical Engineers (ASME) Code requirements
were met.
The team reviewed the modification to determine if the design bases, licensing bases, or
performance capability of the motor-operated valve, safety injection system, or electrical
system had been degraded by the modification. The team interviewed design engineers
and reviewed design drawings, vendor documentation, and calculations to determine if
the motor met the applicable specifications and requirements for the shutdown cooling
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system. Additionally, the team reviewed PMT results and associated maintenance work
orders to determine if the changes were appropriately implemented and the valve test
results were within the required ASME Code and licensing specifications. Finally, the
team reviewed environmental qualification testing results to determine if the testing
bounded the design basis post-accident containment atmosphere.
b. Findings
No findings were identified.
.2.3 MP3-14-01187, Reactor Plant Closed Loop Cooling Water Heat Exchanger 3CCP*E1B
Replacement
a. Inspection Scope
The team reviewed modification MP3-14-01187, which replaced one of three reactor
plant closed loop cooling water (RPCCW) heat exchangers. Dominion replaced the heat
exchanger to restore heat removal capacity and provide additional operating flow margin
to the RPCCW system. Dominion also upgraded the heat exchanger with a more
corrosion/erosion resistant Monel material. As part of the modification, Dominion
redesigned the structural supports for the new heat exchanger to ensure the heat
exchanger and associated RPCCW piping maintained the required Seismic I capability
as required by the licensing basis. Finally, Dominion performed a PMT to assess the
cooling capacity, flow velocity though the heat exchanger tubes, and the integrity of the
RPCCW system.
The team reviewed the modification to determine if the design bases, licensing bases, or
performance capability of the RPCCW heat exchanger had been degraded by the
modification. The team interviewed design engineers and reviewed design drawings,
vendor documentation, and calculations to determine if the heat exchanger met the
specifications and requirements for the RPCCW system. Additionally, the team
reviewed the PMT results and associated maintenance work orders to determine if the
changes were appropriately implemented; the heat removal capability of the heat
exchanger met design requirements; and post-modification leakage results were within
the required ASME Code and licensing specification. The team performed a walkdown
of the heat exchanger to determine if the modification was installed in accordance with
the design, and to assess the overall material conditions of the systems following the
modification work. Finally, the team reviewed the 10 CFR 50.59 screening associated
with this modification as described in Section 1R17.1 of this report.
b. Findings
No findings were identified.
.2.4 MP3-12-01028, Reactor Vessel Head Vent Valve Replacements
a. Inspection Scope
The team reviewed modification MP3-12-01028, which replaced the reactor vessel head
vent valves and associated electrical connections. The valves provide the capability to
vent non-condensable gasses from the reactor vessel following a design basis event.
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Dominion performed the modification to correct degraded performance of the previously
installed valves. Dominion performed pre-installation testing on the valves to ensure the
valves met ASME Code leak requirements and post-installation testing to verify the
integrity of the valve flange connections and the correct operation of the valves.
The team reviewed the modification to determine if the design bases, licensing bases, or
performance capability of the valves and associated piping had been degraded by the
modification. The team interviewed design engineers and reviewed design drawings,
calculations, and vendor specifications to determine if the valves met the applicable
specifications and requirements of the reactor head vent system. Additionally, the team
reviewed PMT results, associated maintenance work orders, and leakage test results to
determine if the changes were appropriately implemented. The team reviewed
environmental qualification testing results to determine if the testing bounded the
projected design basis post-accident containment atmosphere. Finally, the team
reviewed the 10 CFR 50.59 screening associated with this modification as described in
Section 1R17.1 of this report.
b. Findings
No findings were identified.
.2.5 MP3-13-01127, Replacement of Service Water Valves 3SWP*AOV39A&B due to
Material Change
a. Inspection Scope
The team reviewed modification MP3-13-01127, which replaced service water air-
operated butterfly isolation valves. The valves operation provided service water to the
emergency diesel generator (EDG) heat exchangers. Dominion performed the
modification to address identified valve degradation due to de-alloying of the cast
aluminum-bronze alloy valve material. Dominion installed the same style valves with
improved metallurgical properties to minimize this salt water degradation mechanism.
Following installation, Dominion performed testing to verify the valves were properly
installed and the ASME Code requirements were met.
The team reviewed the modification to determine if the design bases, licensing bases, or
performance capability of the valve and associated service water and/or air systems had
been degraded by the modification. The team interviewed design engineers and
reviewed design drawings, calculations, and vendor specifications to determine if the
valves met the design and licensing requirements of the system. Additionally, the team
reviewed PMT results and associated maintenance work orders to determine if the
changes were appropriately implemented. Finally, the team performed a walkdown of
the valves to determine if the modification was installed in accordance with the design,
and to assess the overall material conditions of the systems following the modification
work.
b. Findings
No findings were identified.
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.2.6 MP3-14-01156, 3HVK CHL 1B Relay Module Replacement
a. Inspection Scope
The team reviewed modification MP3-14-01157, which replaced an existing time delay
relay module in the 19FA control building chiller with a time delay relay module
conversion kit. The new installed time delay relay module conversion kit was a complete
upgrade from the old relay module. However, the automatic chiller re-start feature after
a loss of power, which was built-in in the original relay, was not incorporated in the new
relay module design. Therefore, in order to maintain this operational feature, Dominion
added an additional timing relay to the 19FA control building chiller circuitry.
The team reviewed the modification to verify that the design bases, licensing bases, and
performance capability of the control building chiller had not been degraded by the
modification and had been adequately implemented. The team reviewed the purchase
order and the certification of conformance associated with the relay module kit to verify
that quality requirements, including technical, administrative, regulatory, and reporting
requirements (e.g., specifications, codes, standards, tests, inspections) were specified in
procurement documents. The team interviewed engineering staff to verify that the relay
module design would function in accordance with its design requirements. The team
also reviewed the associated work order instructions and vendor documentation to
ensure that maintenance personnel had implemented the modification as designed. In
addition, the team verified that procedures, design documents, and drawings affected by
the modification had been adequately updated. The team performed a walkdown to
independently assess the performance of the 19FA control building chiller by visually
inspecting the local chiller control panel. The team reviewed the associated PMT results
and the 3HVK CHL1B chiller operational performance to verify that the system
functioned as designed following the modification. Finally, the team reviewed the
10 CFR 50.59 screening associated with this modification as described in Section
1R17.1 of this report.
b. Findings
No findings were identified.
2.7 MP3-14-01148, Replacement of 48/15 Vdc Power Supplies for Solid State Protection
System
a. Inspection Scope
The team reviewed modification MP-14-01149, which installed four 48/15 Vdc power
supplies for the solid state protection system. There are two 48/15 Vdc power supplies
per train, and each power supply provides a 48 Vdc and 15 Vdc output to the solid state
protection system logic and output relays. This change was performed due to preventive
maintenance that required the existing power supplies to be replaced on a ten-year
frequency. The originally installed Basler Electric dual output supply unit was no longer
manufactured, therefore, an equivalent power supply module was procured as a
replacement.
The team reviewed the modification to verify that the design bases and licensing bases
of the power supplies had been adequately implemented. The team reviewed the
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equivalency change report to ensure that performance capability of the power supplies
had not been degraded by the modification. The team reviewed the associated work
order instructions and documentation to verify that maintenance personnel had
implemented the modification as designed. The team reviewed the associated PMT
requirements and results of the new power supplies to confirm that the implementation
was properly executed and to verify that the system functioned as designed following the
modification. In addition, the team reviewed procedures, design documents, and
drawings affected by the changes to verify that these documents had been adequately
updated.
b. Findings
No findings were identified.
2.8 10000032204, MP3 Commercial Grade Dedication - Battery Charger Failure Relay
a. Inspection Scope
The team reviewed modification 10000032204, which replaced a relay associated with
Millstone Unit 3 battery charger No. 1. This replacement relay was not designed nor
manufactured as a basic component. The relay was purchased as a commercial grade
item (CGI) and was dedicated by Dominion to be used as a safety-related component.
Dominion characterized this replacement as a like-for-like replacement. The safety
function of the relay was to maintain electrical circuit continuity in the battery charger and
to change states when energized or de-energized by allowing the relay contacts to pick
up or drop out. This change was performed because the original relay failed in service.
The team reviewed the modification to verify that the design bases, licensing bases, and
performance capability of the battery charger relay had not been degraded by the
modification. The team verified that Dominions process for dedicating the CGI provided
reasonable assurance that the commercial grade relay would perform its intended safety
function. Specifically, the team verified that Dominion had established adequate controls
for acceptance of the CGI through its receipt inspection requirements. The team verified
that Dominion properly identified and verified that all critical characteristics associated
with the replacement relay satisfied their respective acceptance criteria. The team
reviewed the associated work order instructions and documentation to verify that
maintenance personnel had implemented the modification as designed. The team
reviewed the associated acceptance criteria and PMT requirements of the new relay to
confirm that the implementation was properly executed and to verify that the battery
charger would function as designed following the modification. Finally, the team
reviewed procedures, design documents, and drawings affected by the changes to verify
that these documents had been adequately updated.
b. Findings
No findings were identified.
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.2.9 MP2-15-01097, Reactor Protection System Bistable Trip Unit, Auxiliary Trip Units, and
Trip Test Cable Assemblies Replacement
a. Inspection Scope
The team reviewed design change package MP2-15-01097 for a planned modification
that will replace the reactor protection system (RPS) bistable trip units (BTU), the
auxiliary trip units (ATU), and the trip test cable assemblies (TTCA). This design change
is required to replace the obsolete BTUs, ATUs, and TTCAs for the Millstone Unit 2
RPS. This design change will replace eight BTUs, two ATUs, and a TTCA in RPS
channel B during the next Unit 2 outage (2R24), and the remaining three channels (A,
C, and D) will be replaced during 2R25.
The team reviewed the design work package to evaluate whether the design bases,
licensing bases, and performance capability of the RPS can be degraded by the
modification. The team reviewed Dominions technical evaluation, design specifications,
calculations, analysis, drawings, and logic control sheets to verify that design
assumptions were valid. The team reviewed the procurement specification to verify that
quality requirements, including technical, administrative, regulatory, and reporting
requirements (e.g., specifications, codes, standards, tests, inspections) were specified in
procurement documents. The team interviewed system engineers and technical staff to
evaluate the adequacy of the modification. Additionally, the team reviewed the 10 CFR
50.59 screening associated with this modification as described in Section 1R17.1 of this
report.
b. Findings
No findings were identified.
2.10 Calculation 96-067, Auxiliary Feedwater System Comprehensive Flow Analysis, and
Modification MP3-14-01107, MP3 TDAFW Pump Overspeed Margin Change
a. Inspection Scope
The team reviewed Millstone Unit 3 Calculation 96-067, which was revised in support of
lowering the operating speed (from 4500 to 4400 rpm) of the turbine-driven auxiliary
feedwater (TDAFW) pump to gain margin to the relief valve setpoint and to increase
pump reliability. This change was implemented due to prior operating experience events
at Millstone Unit 3 involving TDAFW pump/turbine overspeed trips and challenging the
discharge relief valve. The change involved a reduction in auxiliary feedwater (AFW)
flow due to the speed reduction. In the calculation revision, Dominion evaluated the
lower AFW flow on postulated events in the safety analysis. The team also reviewed the
associated modification, MP3-14-01107, TDAFW Pump Overspeed Margin Change, for
which the above calculation supported.
The team reviewed the calculation change to determine if the design bases, licensing
bases, or performance capability of the AFW system had been degraded by reduction in
TDAFW pump operating speed. The team interviewed design engineers and reviewed
the revised calculation and associated design basis events to determine whether the
change met design and licensing requirements. Surveillance procedures, including test
results, were reviewed by the team to determine whether the results were bounded by
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the modification and existing analyses. The 10 CFR 50.59 safety evaluation associated
with this change was also reviewed as described in Section 1R17.1 of this report.
b. Findings
No findings were identified.
2.11 MP3-14-01070, Replace Emergency Diesel Generator Air Cooler Service Water Relief
Valves M33SWP*RV90A/RV90B
a. Inspection Scope
The team reviewed modification MP3-14-01070 that Dominion implemented to replace
the service water system thermal protection relief valves to the Unit 3 EDG air coolers.
The function of the relief valves is to provide overpressure protection to the service water
side of the safety-related EDG combustion air heat exchangers in the event of an
unintentional equipment isolation or a thermal transient during component lay-up
conditions. The original relief valves were configured with a metal-to-metal seat design
that was susceptible to the effects of corrosion and debris, resulting in failure to lift within
the specified tolerance of the set pressure. The modification allowed for a soft seat
configuration for both of the system relief valves.
The team reviewed the modification to determine if the design and licensing bases, and
performance capability of the EDG system had been degraded by any of the associated
equipment, process, and/or procedure changes. The team interviewed design
engineers, and reviewed evaluations, surveillance results, technical data sheets, and
associated maintenance activities to verify that Dominion appropriately implemented the
design change in accordance with their design process and assumptions. The team
performed walkdowns of accessible portions of the EDG and service water systems to
assess configuration control and the material condition of the associated components.
The team also reviewed condition reports, completed preventive maintenance activities,
and the EDG system operating logs to determine if there were reliability or performance
issues that may have resulted from the modification.
b. Findings
No findings were identified.
.2.12 MP3-14-01027, Motor-Driven Auxiliary Feed Pump Lube Oil Pump 3FWL*P6A
Replacement
a. Inspection Scope
The team reviewed modification MP3-14-01027 that Dominion implemented to replace
the direct drive (shaft-driven) lube oil pump 3FWL*P6A for AFW pump 3FWA*P1A, due
to unrepairable minor seal leakage and component obsolescence. The AFW pumps
lube oil pump is designed to provide the necessary lubricating oil to the motor-driven
AFW pump. The replacement lube oil pump has slightly different suction and discharge
piping connections, as well as different orientation, which required some minor piping
replacement and rerouting. The replacement lube oil pump was determined to be an
acceptable equivalent replacement pump for the existing 3FWL*P6A.
11
The team reviewed the modification to determine if the design bases, licensing bases, or
performance capability of the motor-driven AFW pump had been degraded by the
modification. The team interviewed design and system engineers and reviewed
installation procedures, surveillance results, and associated maintenance activities to
determine if the new lube oil pump, piping, and configuration met design specifications
and requirements of the system. The team performed a walkdown of both motor-driven
AFW pumps and the TDAFW pump rooms to assess configuration comparisons and
material conditions.
b. Findings
No findings were identified.
2.13 MP2-14-01001, Replace Emergency Diesel Generator M-7A Service Water Coolers
Supply and Discharge Lines with AL-6XN Material
a. Inspection Scope
The team reviewed modification MP2-14-01001 that replaced 6-inch and 8-inch lined
carbon steel flanged pipe spools on the A train service water supply header to the
Unit 2 A EDG jacket water cooling, lube oil cooling, and air cooler heat exchangers.
The modification also included the replacing previously-installed AL6XN material pipe
spools to correct flange alignment issues, replacing check valve 2-SW-13A with an
AL6XN pipe spool, and replacing stainless steel flow restricting orifices. The
modifications were necessary to eliminate dissimilar metal galvanic interactions and
corrosion issues.
The review was performed to determine if the design bases, licensing bases, or
performance capability of the A EDG had been degraded by the modifications. Design
assumptions were reviewed to evaluate whether they were technically appropriate and
consistent with the UFSAR. The team discussed the impact of the modification on the
EDG operation with responsible engineers. Additionally, the team reviewed
maintenance work orders to confirm that the modifications were appropriately
implemented. The team performed walkdowns of the EDG to assess the quality of the
modification work and the overall material condition of the equipment. The adequacy of
the PMT was verified, and affected design documents and drawings were reviewed to
ensure they had been properly updated. Additionally, the equivalent 10 CFR 50.59
screen associated with this modification was reviewed as described in Section 1R17.1 of
this report.
b. Findings
No findings were identified.
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4. OTHER ACTIVITIES
4OA2 Identification and Resolution of Problems (IP 71152)
a. Inspection Scope
The team reviewed a sample of problems that Dominion had previously identified and
entered into the corrective action program. The team reviewed these issues to verify an
appropriate threshold for identifying issues and to evaluate the effectiveness of
corrective actions. In addition, the team reviewed corrective action condition reports
written on issues identified during the inspection to verify adequate problem identification
and incorporation of the problem into the corrective action system.
b. Findings
No findings were identified.
4OA6 Meetings, including Exit
The team presented the inspection results to Mr. John Daugherty, Site Vice President,
and other members of Dominion staff at an exit meeting on November 17, 2016. The
team returned the proprietary information reviewed during the inspection to Dominion
staff and verified that this report does not contain proprietary information.
ATTACHMENT: SUPPLEMENTARY INFORMATION
A-1
SUPPLEMENTARY INFORMATION
KEY POINTS OF CONTACT
Dominion Personnel
D. Coleman, Nuclear Technical Specialist
E. Dundon, System Engineer
J. Farley, System Engineer
T. Fecteau, Design Contractor
J. Gardner, System Engineer
Z. Hoagland, System Engineer
R. Kasuga, Design Engineer
M. Legg, Nuclear Engineer
S. OHearn, Nuclear Engineer
F. Perkins, System Engineer
R. Perry, System Engineer
T. Raetz, Design Engineer
T. Ryan, System Engineer
J. Scheeler, Electrical Engineer
C. Thomas, System Engineering
R. Wells, Nuclear Engineer
P. Wynn, Procurement Engineer
NRC Personnel
J. Ambrosini, Senior Resident Inspector
ITEMS OPENED, CLOSED AND DISCUSSED
None
LIST OF DOCUMENTS REVIEWED
10 CFR 50.59 Evaluations
E-14-00075-000, Retire-in-Place of MP2 De-icing Line for the Intake Structure, Revision 0
MP-EVAL-SAF-S2-EV-15-0001, OP 230J, Changes to Procedure for Boron Injection, Revision 0
MP-EVAL-SAF-SG-EV-15-0004, Time to Restore Offsite Power to a Good Element,
Revision 0
S2-EV-13-0001, Reanalysis of the MP2 LOCA and MSL Break Containment Analysis,
Revision 0
S2-EV-14-0002, Procedure Change, Upender Vertical Input to Fuel Transfer System, 4/13/14
S3-EV-13-0002, MP3 Rod Withdrawal from Subcritical Analysis, 4/9/13
S3-EV-13-0003, Analytical Basis of MP3 LBLOCA Containment Response, 4/29/13
S3-EV-14-0001, SP 3622.9 (TDAFW Pump Full Flow Test) in Mode 1, Revision 1
S3-EV-14-0004, MP3 TDAFW Pump Operating Speed Change from 4500 to 4400 RPM,
12/2/15
Attachment
A-2
S3-EV-14-0005, MP3 Compensatory Action to Control Rate of Opening and Closing TDAFW
Pump Discharge Flow Control Valves, 10/15/14
SG-EV-15-0002, 345 kV Protective Relay Digital Upgrade, Revision 0
SG-EV-15-0002, 345 kV Switchyard Breaker Revised Close/Open Cycles, Revision 1
SG-EV-15-0005, 345 kV Switchyard Breaker-and-Half Configuration, 6/17/15
10 CFR 50.59 Screened-out Evaluations
MPS2-SCRN-2016-0065-0, C Service Water Discharge Strainer Motor Full Load Amps Greater
than Nameplate, 4/22/16
MPS2-SCRN-2016-0087-0, Belzona Repair of MP2 Primary Water Transfer Pump Shaft, 5/3/16
MPS2-SCRN-2016-0124-0, Helecoil Installed in Bonnet Stud Hole of Valve 2-CN-52 to Repair
Damaged Thread per ETE-MP-2011-0067, 7/19/16
MPS2-SCRN-2016-0143-1, Adjust Packing Load on 2-FW-51B to Eliminate Packing Leakage
without Invalidating Stroke Time Results, 8/7/16
MPS2-SCRN-2016-0166-0, Replace Valve 2-SW-3.1B with AL-6XN Material, 12/30/15
MPS2-SCRN-2016-0190-0, Replace Hart Monitor LY-5030A-1 with Firmware Version, 10/19/16
MPS3-SCRN-2015-0006-0, TDAFW Governor Speed Control Switch Logic Change, 4/22/16
MPS3-SCRN-2016-0072-0, Change Trip Setpoint for MP3 Pressurizer Safety Valves Flow
Monitoring Switches, 5/2/16
MPS3-SCRN-2016-0078-1, SLCRS Damper 3HVV*MOD51D Repair, 4/29/16
MPS3-SCRN-2016-0123-0, MP3 Diesel Instrument Air System, 7/28/16
MPS3-SCRN-2016-0161-0, SBO DG Vibration-Powered Hour Meter Installation, 10/4/16
MPS3-SCRN-2016-0164-0, Installation of Oversized Motor Termination Box, 9/6/16
Screen for AOP 3562, Loss of Instrument Air, 8/14/14
Screen for Changing MOV 2-SI-652 from Torque Switch to Limit Switch Control, 4/26/14
Screen for Construction of Permanent Scaffold Frames in MP2 Containment, 4/1/15
Screen for ETE-MP-2016-1097, Insulation around Yoke of Feedwater Control Valves, 6/14/16
Screen for IC 2418B/012-00, Revised TI-114 Alarm Setpoint for TCC-MP-2014-018, 8/13/14
Screen for Implementing Automatic Start Feature for the SBO Diesel Generator, 12/8/15
Screen for Installation of a Non-Safety-Related Positive Displacement Pump for Refill of the
Safety Injection Accumulator, 8/17/15
Screen for OP 2204/025-10, Revise OP 2204 to Restore Functionality of RM-4296A/B, 7/11/14
Screen for Opening RHR Suction MOV breakers, 10/23/13
Screen for Rerate of MS3 Service Water Strainers to 100 psig at 100 degrees F, 5/9/14
Screen for Retire-in-Place of Millstone Unit 2 De-icing Line for the Intake Structure, 3/9/15
Modifications
10000032204, MP3 GDC Battery Charger Failure Relay, Revision, 00
Calculation 96-067, MP3 Auxiliary Feedwater System Comprehensive Flow Analysis, 10/22/14
MP2-11-01079, Replacement of Pressurizer Spray Manual Isolation Gate Valves 2-RC-252 and
2-RC-253, Revision 1
MP2-14-01001, EDG M-7A SW Coolers Supply/Discharge Lines with AL-6XN Material, 3/4/15
MP2-14-01009, Replace Shutdown Cooling Isolation Valve 2-SI-652 Motor, Revision 0
MP2-15-01097, MP2 RPS Bistable Trip Unit, Auxiliary Trip Units, and Trip Test Cable
Assemblies Replacement, 9/14/16
MP3-12-01028, MP3 Reactor Vessel Head Vent Valve Replacements, Revision 1
MP3-13-01127, MP3 Replacement of Service Water Valves 3SWP*AOV39A&B due to Material
Change, Revision 0
MP3-14-01027, Motor-Driven AFW Pump Lube Oil Pump 3FWL*P6A Replacement, 4/9/14
MP3-14-01070, Replace EDG Air Cooler SW Relief Valves M33SWP*RV90A/RV90B, 6/11/14
MP3-14-01107, MP3 TDAFW Pump Overspeed Margin Change, 12/2/15
A-3
MP3-14-01149, Replacement of 48/15 Vdc Power Supplies for SSPS, 10/8/14
MP3-14-01156, 3HVK CHL 1B Relay Module Replacement, 2/24/15
MP3-14-01187, MP3 RPCCW Heat Exchanger 3CCP*E1B Replacement, Revision 010
Calculations and Evaluations12-001, MP2 SW Model and Design Basis Analysis, Revision 2
12-350, MP3 Required SW Flow Rate to the CCP Heat Exchangers at 80 degrees F during
LOOP and during an SIS, Revision 1
527012-189-EM, MP2 Pipe Support Calculation SW System Support No. 527012, Revision 4
90-069-01065M3, MP3 SW System, GL 89-13, Item IV, Design Basis Summary, Revision 2
95-052, Safety Grade Cold Shutdown Design Basis Analysis, Revision 6
96-001, Empirical Adjustment of the MP3 SW Model to 1995 Flow Test Data and Incorporation
of the Latest SW System Design Change Notices, Revision 3
96-ENG-01279M3, MP3 - Thermal Performance Evaluation of Designated In-Service and
Discretionary Components Subject to Elevated CCP Temperatures during SGCS,
Revision 0
97-014, MP3 AFW System Determination of AFW Turbine and Pump Speed and AFW System
Flows for Reduced Steam Generator Pressures, 10/6/14
97-129, CCP System Heat Exchangers - Process Side Temperatures Resulting from CCP
System Operation at 33 F, Revision 1A
CM-AA-CLC-301, SBO Calculation for NUMARC 87-00, Power Uprate to 3650 MW, 10/9/14
CR- M2-98-1764, Qualified Life of Agastat ETR/EGP/EML and E7000 Timer Delay and Control
Relays, 6/18/98
DON-NAF-3-0.0-P-A, GOTHIC Methodology for Analyzing the Response to Postulated Pipe
Ruptures Inside Containment, September 2006
EEQ-TRA-146.0, Qualification Extension Analysis Report for the Environmental Qualification of
the Target Rock Solenoid Operated Globe Valves Model 12E-001, Revision 3
ETE-MP-2016-1066, Restore Sealing Capability of Damper 3HVV*MOD51D, Revision 1
ETE-MP-2016-1071, Repair of B Primary MU Water Transfer Pump Shaft (P22B), Revision 0
ETE-MP-2016-1096, MP2 Steam Generator Feedwater Regulating Valve (2-FW-51B) On-Line
Packing Adjustment, Revision 2
ETE-MP-2016-1122, Oversize Motor Termination Box for 3CND-P11B, 9/6/16
ETE-NAF-2012-0152, Implementation of Revised MP2 Containment Analysis Results Required
to Close OD000281 and to Support an Increase in the Ultimate Heat Sink to 80 F,
Revision 0
ETE-NAF-2013-0002, Implementation of LOCA Containment Analysis with Corrected LOCA
Mass and Energy Releases for MP3, Revision 0
ETE-NAF-2013-0008, Implementation of the ABB-NV Rod Withdrawal from Subcritical Analysis
for MP 3, Revision 0
ETE-NAF-3013-0106, Assessment of Operator Vital Area Actions Dose for Powering Residual
Heat Removal System Motor-Operated Valves, Revision 0
Condition Reports
04-03344 235877 316440 346853 446496 451173 456066
467710 503721 506095 507788 524412 538015 542278
544616 549055 549422 551353 553558 555213 563418
563418 565191 575918 577364 578905 1030128
1030852 1035794 1036047 1037622 1053463* 1053479*
- Generated as result of this inspection
A-4
Design & Licensing Bases
Safety Evaluation by the Office of Nuclear Reactor Regulation, in the Matter of Combustion
Engineering, Incorporated CESSAR System 80 Docket No. STN 50-470, December 1975
Safety Evaluation by the Office of Nuclear Reactor Regulation, Related to Amendment No. 139
the Facility Operating License No. DPR-65, 3/20/89
MP2 UFSAR, Revision 34.1
MP3 UFSAR, Revision 29.1
Drawings
103225, Shts. 1 - 6, PC ASSY Bistable Trip Module, RPS, Revision B
1501042-M-25203-26008, Sht. 2, MP2 Service Water, Revision 0
25203-20182, Sht. 1, M-7A Cooling Heat Exchangers SW Supply/Discharge Piping, Revision 10
25203-26017, Sht. 1, Charging System, Revision 64
25203-26017, Sht. 2, Deborating and Purification System, Revision 38
25203-26017, Sht. 3, Boric Acid System, Revision 45
25212-23018, Sht. 207, Service Water Piping Diesel Generator Building, Revision 6
25212-23018, Sht. 208, Service Water Piping Diesel Generator Building, Revision 7
25212-26904, Sht. 1, Chemical and Volume Control, Revision 54
25212-26913, Sht. 1, High Pressure Safety Injection, Revision 32
25212-26933, Sht. 4, Service Water, Revision 48
25212-29041, Sht. 16, Lube Oil Piping - Motor Driven AFW Pump, Revision G
25212-29061, Sht. 15, Control Bldg Water Chill Electrical Diagram [3HVK*CHL1B], Revision 15
25212-29186, Sht. 10, Pressure Relief Valve, Revision A
25212-29186, Sht. 2, Pressure Relief Valve, Revision 2
25212-32001, Sht. 7KJ, 120 Vac Control Building Chiller Auxiliary Circuits, Revision 12
6822-34868A, Shts. 1 and 2, Reactor Protective System, Bistable Trip Unit Schematic, 4/8/79
D-18767-411-301, Auxiliary Trip Unit Schematic, Revision 2
NCB-1486-E, ARR130K200F, Summary Relay and ET-6 Alarm Light, 11/9/79
Miscellaneous
25203-29016, Sht. 23, Certified Test Curve for B&W Pump V2660-40, 11/7/72
45895745, Purchase Order for Module, Relay, Assembly, Conversion kit, 1/2/12
ANF-87-161, MP2 Plant Transient Analysis Report - Chapter 15 Events, September 1988
ANF-87-161, Supplement 1, MP2 Plant Transient Analysis Report - Chapter 15, October 1988
DCN DM3-00-0166-09, Change Alpha Service Water Relief Valves to Soft Seats, 11/15/09
DCN DM3-00-0167-09, Change Bravo Service Water Relief Valves to Soft Seats, 11/15/09
DCN MP2-15-01161, Replace Valve 2-SW-3.1B with AL-6XN Material, Revision 0
DCN MP3-16-01071, Install Non-Resettable Hour Meter on Station Blackout Diesel Generator
Engine 3BGS-BG-A, Revision 0
DNES-AA-GN-1002, Document Impact Summary, Revision 13
DR-2994, Velan Design/Seismic Report for 3 1500 Special Class Bolted Bonnet Gate Valve with
Handwheel - Nuclear Class 1, Revision A
MP2-13-01204, MP2 De-icing Line Retirement, Revision 1
MP3-13-01034, Ultimate Heat Sink Temperature, LCO Increase from 75 to 80 °F, 7/26/13
NEI 01-0, Guideline on Licensing Digital Upgrade, Revision 1
OP 3346A-14, EDG A Operating Logs, 1/19/16 through 9/27/16
OP 3346A-15, EDG B Operating Logs, 2/2/16 through 10/12/16
PO-MAT-0045938321, Curtiss Wright Flow Control Co, Supporting Documents for Receipt
Inspection Report Package, 4/8/13
Receipt Inspection Report Package for the Battery Charger relay, 11/1/14
SO-14-017, Standing Order, Throttling TDAFW Pump Flow, Revision 1
Specification for Mechanical Refrigeration Unit, Control Building Water Chiller Cat. 1, 11/13/73
A-5
TCC-MP-2014-012, Manual Switch to Replace Fuel Transfer System Upender Vertical Position
Proximity Switch, Reactor Side, Revision 0
Wyle Seismic Qualification Test Report on Two Battery Charger, 4/26/83
Procedures
CEN 110, Post Repair/Replacement Leakage Test, Revision 4
CM-AA-400, 10 CFR 50.59 and 10 CFR 72.48 - Changes, Tests, and Experiments, Revision 8
CM-AA-DDC-201, Design Change, Revision 17
CM-AA-RSK-1001, Engineering Risk Assessment, Revision 14
DNES-AA-GN-1005, Failure Modes and Effects Analysis (FMEA), Revision 3
IC 2418B, RCS Temperature Instrument Calibration, Revision 015-00
MP 2703C3, I. R. Chemliner Pump, Revision 8
MP 3710AA-149E, Lubrication Maintenance Technique, Auxiliary Feedwater Pump Oil and
Strainer Change, Revision 2
MP 3762WB, Generic Relief Valve Maintenance, Revision 8
MP-02-NO-GDL405, Determination of Inspection Requirements for Quality Activities, Revision 7
MP-20-WP-GDL40, Pre and Post Maintenance Testing, Revision 14
NC 1900.3B, Application of Belzona Products, Revision 1
OP 2204, Load Changes, Revision 034
OP 2304J, Boric Acid Addition to CVCS from a Temporary Borated Water Source, Revision 1
OP 3310B, Accumulator Low Pressure Safety Injection, Revision 17
OP 3314F, Control Building HVAC and Chill Water, Revision 033-00
OP 3322, Auxiliary Feedwater System, Revision 026
OP 3353.VP1C, Main Ventilation and AC Panel VP1C Annunciator Response, Revision 007-00
OPS-FH 202, Transfer Carriage and Upender Operations, Revision 4
PI-AA-200, Corrective Action, Revision 32
PT 31459A, MP# Timing Device Calibration Program, Revision 009
SP 2613A, Diesel Generator Operability Tests, Facility 1, Revision 25
SP 2613B, Diesel Generator Operability Tests, Facility 2, Revision 26
SP 3622.8, Auxiliary Feedwater Valve Operability Test, Revision 010-06
SP 3622.8-005, 3FWA*P2 Discharge Isolation Valves Stroke Time Test, Revision 000-06
SP 3622.8-012, TDAFW Pump Control Valves Stroke Time, Revision 02
SP 3626.13, Service Water Heat Exchangers Fouling Determination, Revision 22
SP 3626.14, RSS Heat Exchanger SW Supply Piping Flush, Revision 4
SP 3646A.1, Emergency Diesel Generator A Operability Test, Revision 20
SP 3646A.2, Emergency Diesel Generator B Operability Test, Revision 22
WM-AA-301, Operational Risk Assessment, Revision 13
Surveillance, Functional, and Modifications Acceptance Tests
CBM 104, Vibration Data Acquisition and Overall Vibration Analysis, performed 11/13/14
CMP 715E, General Practices Flanges and Threaded Fasteners, performed 5/29/15 and 2/15/16
CMP 727A, Testing and Setting Pressure Relief Valves, performed 9/11/14 and 2/14/16
CMP 799D, Cutting of Installed Plant Piping, performed 10/28/14
MP 3762WB, Generic Relief Valve Maintenance, performed 2/15/16
MP-VE-9, Visual Weld Acceptance Criteria, Weldments and Brazed Joints, performed 10/28/14
OP 3346A, Emergency Diesel Generator, performed 1/19/16, 2/20/16, 6/7/16 and 9/27/16
SP 2613K, DG Slow Start Operability Test, Facility 1, performed 9/19/15 and 10/19/16
SP 2613L-001, Periodic DG Slow Start Operability Test, Facility 2 (Loaded Run), performed
10/07/15 and 10/02/16
SP 2670-007, Diesel Generator B Heat Exchanger D/P Determination, performed 10/02/16
SP 3446F31-001, SSPS Refueling Tests, performed 4/22/16
SP 3622.1, AFW Pump 3FWA*P1A Operational Readiness Test, performed 11/13/14
SP 3622.3-001, TDAFW Pump Operational Readiness and Quarterly IST Group B Pump Tests,
performed 5/11/16 and 8/8/16
A-6
SP 3622.8-001, Auxiliary Feedwater Train A Valve Stroke Time, performed 10/17/16
SP 3622.8-001, TDAFW Pump Control Valves Stroke Time, performed 8/8/16
SP 3622.8-005, 3FWA*P2 Discharge Isolation Valves Stroke Time Test, performed 5/18/16
SP 3622.8-009, Auxiliary Feedwater Train B Valve Stroke Time, performed 9/5/16
SP 3622.9-001, TDAFW Pump Full Flow Test in Mode 1, performed 1/27/14
SP 3626.3, 3SWP*AOV39B, EDG B Service Water HX Outlet, Stroke Test, performed 4/17/16
Vendor Manuals, Standards, and Specifications
25212-041-001, Sulzer Bingham Pump - Installation, Operation and Maintenance of Motor-
Driven Auxiliary Feedwater Pumps, Revision 9
25212-260-002, Installation, Operation & Maintenance of 200 AMP Battery Charger, Revision 1
Agastat Nuclear Qualified Time Delay Relays, Revision 1
Tyco Electronics GP/ML/TR Series 10 Amp Control Relay Non-lathing, Latching & Timing
Versions, Revision 3-13
Work Orders
53102428795 53102785317 53102737935
53102437234 53102849166 53102737943
53102443647 53102351580 53102885049
53102633524 53102539957
53102783755 53102618701
LIST OF ACRONYMS
10 CFR Title 10 of the Code of Federal Regulations
ASME American Society of Mechanical Engineers
ATU auxiliary trip unit
BTU bistable trip unit
CGI commercial grade item
DRS Division of Reactor Safety
EDG emergency diesel generator
NEI Nuclear Energy Institute
NRC Nuclear Regulatory Commission
PMT post-modification test
RPCCW reactor plant closed cooling water
TDAFW turbine-driven auxiliary feedwater
TTCA trip test cable assembly