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| issue date = 11/06/1996
| issue date = 11/06/1996
| title = Part 21 Rept Re Defective 350 HP,1800 RPM,460 VAC,3 Phase, 5006P Frame,1.15 Sf,Vertical Hollow Shaft Motor Used as Service Water Pump motor.Safety-Relayed Cgiee Revised to Enhance Steps for Exam of Windings & Workmanship
| title = Part 21 Rept Re Defective 350 HP,1800 RPM,460 VAC,3 Phase, 5006P Frame,1.15 Sf,Vertical Hollow Shaft Motor Used as Service Water Pump motor.Safety-Relayed Cgiee Revised to Enhance Steps for Exam of Windings & Workmanship
| author name = MECREDY R C
| author name = Mecredy R
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| addressee name = VISSING G S
| addressee name = Vissing G
| addressee affiliation = NRC (Affiliation Not Assigned)
| addressee affiliation = NRC (Affiliation Not Assigned)
| docket = 05000244
| docket = 05000244
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:CATEGORY1REGULAT~.INFORMATION DISTRIBUTION STEM(RIDS)ACCESSION NBR:9611150001 DOC.DATE:
{{#Wiki_filter:CATEGORY 1 REGULAT~   . INFORMATION DISTRIBUTION             STEM (RIDS)
96/11/06NOTARIZED:
ACCESSION NBR:9611150001             DOC.DATE: 96/11/06 FAOIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester NOTARIZED: NO          DOCKET  I G 05000244 Alp H.NAME            AUTHOR AFFILIATION MECREDY,R.C.         Rochester Gas 6    Electric    Corp.
NOFAOIL:50-244 RobertEmmetGinnaNuclearPlant,Unit1,Rochester GAlpH.NAMEAUTHORAFFILIATION MECREDY,R.C.
RECIP.NAME           RECIPIENT AFFILIATION VISSING,G.S.
Rochester Gas6ElectricCorp.RECIP.NAME RECIPIENT AFFILIATION VISSING,G.S.


==SUBJECT:==
==SUBJECT:==
Part21reptredefective 350HP,1800RPM,460VAC,3phase,5006PFrame,l.15 SF,vertical hollowshaftmotorusedasservicewaterpumpmotor.Safety-Relayed CGIEErevisedtoenhancestepsforexamofwindings&workmanship.
Part  21  rept re defective 350 HP,1800 RPM,460 VAC,3 phase, 5006P  Frame,l.15 SF,vertical hollow shaft motor used as service water pump motor. Safety-Relayed CGIEE revised to enhance steps for exam of windings & workmanship.
DISTRIBUTION CODE:IE19TCOPIESRECEIVED:LTR 1ENCL(SIZE:TITLE:,Part 21Rept(50DKT)NOTES:License Expdateinaccordance with10CFR2,2.109(9/19/72).
DISTRIBUTION CODE: IE19T          COPIES RECEIVED:LTR         1  ENCL  ( SIZE:
DOCKETI0500024405000244GRECIPIENT IDCODE/NAME PD1-INTERNAILECENTENRRDRMPECBRES/DSIR/EIB RGN2RGN4COPIESLTTRENCL111111111111RECIPIENT IDCODE/NAME VISSING,G.
TITLE:,Part     21 Rept  (50 DKT)
NRR/DISP/PSIB/B PDRWARD,M.RGN1RGN3COPIESLTTRENCL11111111110EXTERNAL:
NOTES:License Exp date        in accordance with 10CFR2,2.109(9/19/72).                 05000244 G
INPORECORDCTRNRCPDR1111NOACSILVER,ENUDOCSFULLTXT1111~>"tt~Jyg ENNOTETOALL"RIDS"RECIPIENTS:
RECIPIENT            COPIES            RECIPIENT              COPIES ID CODE/NAME         LTTR ENCL        ID CODE/NAME            LTTR ENCL              0 PD1-                       1    1      VISSING,G.                 1    1 INTERNA      ILE  CENTE              1    1      NRR/DISP/PSIB/B             1    1 NRR DR M PECB              1    1      PDR WARD, M.               1    1 RES/DSIR/EIB              1    1      RGN1                        1    1 RGN2                      1    1      RGN3                        1    1 RGN4                      1    1 EXTERNAL: INPO RECORD CTR              1    1      NOAC SILVER,E              1    1 NRC PDR                    1    1      NUDOCS FULL TXT            1    1 E
PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATION REMOVEDFROMDISTRIBUTION LISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION, CONTACTTHEDOCUMENTCONTROLDESK(DCD)ONEXTENSION 415-2083FULLTEXTCONVERSION REQUIREDTOTALNUMBFROFCOPIESREQUIRED:
                                                          ~>"tt~Jyg N
LTTR15ENCL15 Cr ANDROCHESTER GASANDEIECTRICCORPORATION
NOTE TO  ALL "RIDS" RECIPIENTS:
~89EASTAVEMIJE, ROCHESTER, N.Y146d9-0001 AREACODE7I65'-2700ROBERTC.MECREDYVicePresident NuclearOperations November6,1996U.S.NuclearRegulatory Commission DocumentControlDeskAttn:GuyS.VissingProjectDirectorate I-1Washington, D.C.20555
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBFR OF COPIES REQUIRED: LTTR              15    ENCL      15
 
C r
 
AND ROCHESTER GAS AND EIECTRIC CORPORATION ~   89 EASTAVEMIJE, ROCHESTER, N. Y 146d9-0001   AREA CODE7I6 5'-2700 ROBERT C. MECREDY Vice President Nuclear Operations November 6, 1996 U.S. Nuclear Regulatory Commission Document Control Desk Attn: Guy S. Vissing Project Directorate I-1 Washington, D.C. 20555


==Subject:==
==Subject:==
10CFRPart2130DayReportR.E.GinnaNuclearPowerPlantDocketNo.50-244
10 CFR Part 21 30 Day Report R.E. Ginna Nuclear Power Plant Docket No. 50-244
 
==Dear Mr. Vissing:==
 
In accordance with 10 CFR Part 21, Rep'orting of Defects and Noncompliance, Section 21 (d)
(3) (ii), which requires "Written notification to the NRC ... on the identification of a defect or failure to comply", the attached 10 CFR 21 report is hereby submitted.
Ve          ly yours Robert C. Me edy xc:          Mr. Guy S. Vissing (Mail Stop 14C7)
Project Directorate I-1 Washington, D.C. 20555 Regional Administrator U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna Senior Resident Inspector
~Con qiXS<5000i            VS,XX06 PDR        ADOCK      05000244 8                          PDR
 
Page 2 10CFR21 30  DAY WRITTEN REPORT I. NAME AND ADDRESS OF THE INDIVIDUALINFORMING THE COMMISSION:
NAME:          Robert C. Mecredy Vice President Nuclear Operations ADDRESS:      Rochester Gas & Electric Corporation 89 East Avenue Rochester, New York 14649 II. IDENTIFICATION OF THE FACILITY, THE ACTIVITY, OR THE BASIC COMPONENT SUPPLIED FOR SUCH FACILITYWHICH FAILS TO COMPLY OR CONTAINS A DEFECT:
The facility is the R.E. Ginna Nuclear Power Plant. The basic component is a 350 HP, 1800 RPM, 460 VAC, 3 phase, 5006P Frame, 1.15 SF, vertical hollow shaft motor for use as a Service Water (SW) pump motor. This component was installed at the R.E.
Ginna Nuclear Power Plant to upgrade the motor for the "A" SW pump from a 300 HP to a 350 HP motor. (The "A" SW pump was never declared operable with this defective motor installed.)
III. IDENTIFICATION OF THE FIRM CONSTRUCTING THE FACILITY OR SUPPLYING THE BASIC COMPONENT WHICH FAILS TO COMPLY OR CONTAINS A DEFECT:
The motor was a commercial-grade motor manufactured by:
U.S. Electrical Motors Division of Emerson Electric Co.
8100 W. Florissant Ave.
PO Box 3946 St. Louis, MO 63136 The motor was procured from:
Auburn Armature, Inc.
48 Canoga St.
Auburn, NY 13021 Note: This motor was purchased commercial-grade, was commercially-dedicated by Rochester Gas & Electric, and satisfied all testing requirements included in the procurement documents.
 
Page 3
~
IV. NATURE OF THE DEFECT OR FAILURE TO COMPLY AND THE SAFETY HAZARD WHICH IS CREATED OR COULD BE CREATED BY SUCH DEFECT OR FAILURE TO COMPLY:
A 350 HP motor      was installed on the "A" SW pump in July, 1996. Post-modification functional testing revealed unacceptable megger readings. The motor was removed from the "A" SW pump, disassembled and inspected. The inspection revealed degradation of motor insulation integrity due to damaged motor leads, which could result in the failure of the motor in service. The overall quality of the motor was below that normally expected for a commercial grade motor.
The safety hazard which could be created by such a defect is the complete loss of Service Water. In the scenario of the "C" SW pump out of service and a concurrent loss of power to Bus 17 (which supplies power to the "B" and "D" SW pumps), a loss of all SW would occur if the "A" SW pump failed to operate due to the identified defect.
V. THE DATE ON WHICH THE INFORMATION OF SUCH DEFECT OR FAILURE TO COMPLY WAS OBTAINED:
The information was obtained on August 5, 1996.
VI. IN THE CASE OF A BASIC COMPONENT WHICH CONTAINS A DEFECT OR FAILS TO COMPLY, THE NUMBER AND LOCATION OF 'ALL SUCH COMPONENTS IN USE AT, SUPPLIED FOR, OR BEING SUPPLIED FOR GINNA STATION:
There are four (4) SW pumps located in the Screenhouse Building at Ginna Station.
A 350 HP motor had previously been procured separately. This motor was installed to upgrade the existing 300 HP motor on the "D" SW pump in August, 1995. This 350 motor is of similar design to the 3 motors discussed below, and was also manufactured by U.S. Electrical Motors. This motor was tested satisfactorily and placed in service in August, 1995, and operated trouble-free. As discussed below, this motor did not contain a defect.
Three (3) 350 HP motors, manufactured by U.S. Electrical Motors, were purchased at a later date (as a group) for upgrade of the existing 300 HP motors on the "A", "B", and "C" SW pumps. As discussed below, two of these three motors were discovered to be defective.
 
Page 4 VI~~. THE CORRECTIVE ACTION WHICH HAS BEEN, IS BEING, OR WILL BE TAKEN; THE NAME OF THE INDIVIDUALOR ORGANIZATIONRESPONSIBLE FOR THE ACTION; AND THE LENGTH OF TIME THAT HAS BEEN OR WILL BE TAKEN TO COMPLETE THE ACTION:
The following corrective actions have been completed:
: 1. Ginna Station Maintenance personnel removed the defective 350 HP motor from the "A" SW pump, and shipped this motor and one uninstalled 350 HP motor to an Appendix B motor facility. These two motors both exhibited degradation of motor insulation integrity. The motors were tested, inspected, and confirmed to be defective. They were refurbished by the motor facility, and returned to Ginna Station.
: 2. The "A" SW pump remained inoperable until one of the above refurbished motors was reinstalled and satisfactorily tested in August, 1996.
: 3. The similar 350 HP motor, installed on the "D" SW pump in August, 1995, had shown no signs of motor degradation. However, this motor was removed from the "D" SW pump in October, 1996, and was replaced by the other refurbished spare motor.
: 4. Thus, corrective action was completed for these two defective motors in August, 1996, and these two refurbished motors were subsequently installed on the "A" and "D" SW pumps, and have fulfilled operability test requirements.
5 ~    Electrical testing on the other two 350 HP motors did not indicate any degradation of the motor insulation integrity. Nevertheless, as a conservative measure, they were shipped to an Appendix B motor facility in October, 1996, for diagnostics and troubleshooting.
These remaining two 350 HP motors have been disassembled, inspected, and tested at an Appendix B motor facility. Electrical testing, performed at the motor facility, achieved satisfactory performance results, confirming that the motor (previously installed on the "D" SW pump) was operable while in service.
However, some minor deficient conditions were noted on both motors. These motors were also refurbished.        These refurbishments are considered to be conservative corrective measures which involved motor releading, insulation redip and bearing rework.
The following corrective actions are scheduled for completion by March, 1997:
Safety-related motor Commercial Grade Item Engineering Evaluations (CGIEE's) will be revised to enhance steps for the examination of windings and overall workmanship to ensure motors are constructed with acceptable quality.
CGIEE preparation guidelines willbe enhanced to incorporate the lessons learned from these defective motors.
 
F 4s


==DearMr.Vissing:==
Page 5
Inaccordance with10CFRPart21,Rep'orting ofDefectsandNoncompliance, Section21(d)(3)(ii),whichrequires"Writtennotification totheNRC...ontheidentification ofadefectorfailuretocomply",theattached10CFR21reportisherebysubmitted.
~ VIII. ANY ADVICE RELATED TO THE DEFECT OR FAILURE TO COMPLY ABOUT THE FACILITY, ACTIVITY, OR BASIC COMPONENT THAT HAS BEEN, IS BEING, OR WILLBE GIVEN TO PURCHASERS OR LICENSEES:
VelyyoursRobertC.Meedyxc:Mr.GuyS.Vissing(MailStop14C7)ProjectDirectorate I-1Washington, D.C.20555RegionalAdministrator U.S.NuclearRegulatory Commission RegionI475Allendale RoadKingofPrussia,PA19406GinnaSeniorResidentInspector
: 1. Source surveillance during motor assembly may have detected this defect.
~ConqiXS<5000i VS,XX06PDRADOCK050002448PDR 10CFR2130DAYWRITTENREPORTPage2I.NAMEANDADDRESSOFTHEINDIVIDUAL INFORMING THECOMMISSION:
: 2. A detailed physical inspection (or disassembly) upon receipt may have detected this defect.
NAME:RobertC.MecredyVicePresident NuclearOperations ADDRESS:Rochester Gas&ElectricCorporation 89EastAvenueRochester, NewYork14649II.IDENTIFICATION OFTHEFACILITY, THEACTIVITY, ORTHEBASICCOMPONENT SUPPLIEDFORSUCHFACILITYWHICHFAILSTOCOMPLYORCONTAINSADEFECT:ThefacilityistheR.E.GinnaNuclearPowerPlant.Thebasiccomponent isa350HP,1800RPM,460VAC,3phase,5006PFrame,1.15SF,verticalhollowshaftmotorforuseasaServiceWater(SW)pumpmotor.Thiscomponent wasinstalled attheR.E.GinnaNuclearPowerPlanttoupgradethemotorforthe"A"SWpumpfroma300HPtoa350HPmotor.(The"A"SWpumpwasneverdeclaredoperablewiththisdefective motorinstalled.)
: 3. Completion of commercial dedication could be dependent upon satisfactory completion of post-modification functional testing.}}
III.IDENTIFICATION OFTHEFIRMCONSTRUCTING THEFACILITYORSUPPLYING THEBASICCOMPONENT WHICHFAILSTOCOMPLYORCONTAINSADEFECT:Themotorwasacommercial-grade motormanufactured by:U.S.Electrical MotorsDivisionofEmersonElectricCo.8100W.Florissant Ave.POBox3946St.Louis,MO63136Themotorwasprocuredfrom:AuburnArmature, Inc.48CanogaSt.Auburn,NY13021Note:Thismotorwaspurchased commercial-grade, wascommercially-dedicated byRochester Gas&Electric, andsatisfied alltestingrequirements includedintheprocurement documents.
Page3~IV.NATUREOFTHEDEFECTORFAILURETOCOMPLYANDTHESAFETYHAZARDWHICHISCREATEDORCOULDBECREATEDBYSUCHDEFECTORFAILURETOCOMPLY:A350HPmotorwasinstalled onthe"A"SWpumpinJuly,1996.Post-modification functional testingrevealedunacceptable meggerreadings.
Themotorwasremovedfromthe"A"SWpump,disassembled andinspected.
Theinspection revealeddegradation ofmotorinsulation integrity duetodamagedmotorleads,whichcouldresultinthefailureofthemotorinservice.Theoverallqualityofthemotorwasbelowthatnormallyexpectedforacommercial grademotor.ThesafetyhazardwhichcouldbecreatedbysuchadefectisthecompletelossofServiceWater.Inthescenarioofthe"C"SWpumpoutofserviceandaconcurrent lossofpowertoBus17(whichsuppliespowertothe"B"and"D"SWpumps),alossofallSWwouldoccurifthe"A"SWpumpfailedtooperateduetotheidentified defect.V.THEDATEONWHICHTHEINFORMATION OFSUCHDEFECTORFAILURETOCOMPLYWASOBTAINED:
Theinformation wasobtainedonAugust5,1996.VI.INTHECASEOFABASICCOMPONENT WHICHCONTAINSADEFECTORFAILSTOCOMPLY,THENUMBERANDLOCATIONOF'ALLSUCHCOMPONENTS INUSEAT,SUPPLIEDFOR,ORBEINGSUPPLIEDFORGINNASTATION:Therearefour(4)SWpumpslocatedintheScreenhouse BuildingatGinnaStation.A350HPmotorhadpreviously beenprocuredseparately.
Thismotorwasinstalled toupgradetheexisting300HPmotoronthe"D"SWpumpinAugust,1995.This350motorisofsimilardesigntothe3motorsdiscussed below,andwasalsomanufactured byU.S.Electrical Motors.Thismotorwastestedsatisfactorily andplacedinserviceinAugust,1995,andoperatedtrouble-free.
Asdiscussed below,thismotordidnotcontainadefect.Three(3)350HPmotors,manufactured byU.S.Electrical Motors,werepurchased atalaterdate(asagroup)forupgradeoftheexisting300HPmotorsonthe"A","B",and"C"SWpumps.Asdiscussed below,twoofthesethreemotorswerediscovered tobedefective.
Page4VI~~.THECORRECTIVE ACTIONWHICHHASBEEN,ISBEING,ORWILLBETAKEN;THENAMEOFTHEINDIVIDUAL ORORGANIZATION RESPONSIBLE FORTHEACTION;ANDTHELENGTHOFTIMETHATHASBEENORWILLBETAKENTOCOMPLETETHEACTION:Thefollowing corrective actionshavebeencompleted:
1.GinnaStationMaintenance personnel removedthedefective 350HPmotorfromthe"A"SWpump,andshippedthismotorandoneuninstalled 350HPmotortoanAppendixBmotorfacility.
Thesetwomotorsbothexhibited degradation ofmotorinsulation integrity.
Themotorsweretested,inspected, andconfirmed tobedefective.
Theywererefurbished bythemotorfacility, andreturnedtoGinnaStation.2.The"A"SWpumpremainedinoperable untiloneoftheaboverefurbished motorswasreinstalled andsatisfactorily testedinAugust,1996.3.Thesimilar350HPmotor,installed onthe"D"SWpumpinAugust,1995,hadshownnosignsofmotordegradation.
However,thismotorwasremovedfromthe"D"SWpumpinOctober,1996,andwasreplacedbytheotherrefurbished sparemotor.4.Thus,corrective actionwascompleted forthesetwodefective motorsinAugust,1996,andthesetworefurbished motorsweresubsequently installed onthe"A"and"D"SWpumps,andhavefulfilled operability testrequirements.
5~Electrical testingontheothertwo350HPmotorsdidnotindicateanydegradation ofthemotorinsulation integrity.
Nevertheless, asaconservative measure,theywereshippedtoanAppendixBmotorfacilityinOctober,1996,fordiagnostics andtroubleshooting.
Theseremaining two350HPmotorshavebeendisassembled, inspected, andtestedatanAppendixBmotorfacility.
Electrical testing,performed atthemotorfacility, achievedsatisfactory performance results,confirming thatthemotor(previously installed onthe"D"SWpump)wasoperablewhileinservice.However,someminordeficient conditions werenotedonbothmotors.Thesemotorswerealsorefurbished.
Theserefurbishments areconsidered tobeconservative corrective measureswhichinvolvedmotorreleading, insulation redipandbearingrework.Thefollowing corrective actionsarescheduled forcompletion byMarch,1997:Safety-related motorCommercial GradeItemEngineering Evaluations (CGIEE's) willberevisedtoenhancestepsfortheexamination ofwindingsandoverallworkmanship toensuremotorsareconstructed withacceptable quality.CGIEEpreparation guidelines willbeenhancedtoincorporate thelessonslearnedfromthesedefective motors.
F4s Page5~VIII.ANYADVICERELATEDTOTHEDEFECTORFAILURETOCOMPLYABOUTTHEFACILITY,
: ACTIVITY, ORBASICCOMPONENT THATHASBEEN,ISBEING,ORWILLBEGIVENTOPURCHASERS ORLICENSEES:
1.Sourcesurveillance duringmotorassemblymayhavedetectedthisdefect.2.Adetailedphysicalinspection (ordisassembly) uponreceiptmayhavedetectedthisdefect.3.Completion ofcommercial dedication couldbedependent uponsatisfactory completion ofpost-modification functional testing.}}

Latest revision as of 18:01, 29 October 2019

Part 21 Rept Re Defective 350 HP,1800 RPM,460 VAC,3 Phase, 5006P Frame,1.15 Sf,Vertical Hollow Shaft Motor Used as Service Water Pump motor.Safety-Relayed Cgiee Revised to Enhance Steps for Exam of Windings & Workmanship
ML17264A730
Person / Time
Site: Ginna Constellation icon.png
Issue date: 11/06/1996
From: Mecredy R
ROCHESTER GAS & ELECTRIC CORP.
To: Vissing G
NRC (Affiliation Not Assigned)
References
REF-PT21-96 NUDOCS 9611150001
Download: ML17264A730 (8)


Text

CATEGORY 1 REGULAT~ . INFORMATION DISTRIBUTION STEM (RIDS)

ACCESSION NBR:9611150001 DOC.DATE: 96/11/06 FAOIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester NOTARIZED: NO DOCKET I G 05000244 Alp H.NAME AUTHOR AFFILIATION MECREDY,R.C. Rochester Gas 6 Electric Corp.

RECIP.NAME RECIPIENT AFFILIATION VISSING,G.S.

SUBJECT:

Part 21 rept re defective 350 HP,1800 RPM,460 VAC,3 phase, 5006P Frame,l.15 SF,vertical hollow shaft motor used as service water pump motor. Safety-Relayed CGIEE revised to enhance steps for exam of windings & workmanship.

DISTRIBUTION CODE: IE19T COPIES RECEIVED:LTR 1 ENCL ( SIZE:

TITLE:,Part 21 Rept (50 DKT)

NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 G

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL 0 PD1- 1 1 VISSING,G. 1 1 INTERNA ILE CENTE 1 1 NRR/DISP/PSIB/B 1 1 NRR DR M PECB 1 1 PDR WARD, M. 1 1 RES/DSIR/EIB 1 1 RGN1 1 1 RGN2 1 1 RGN3 1 1 RGN4 1 1 EXTERNAL: INPO RECORD CTR 1 1 NOAC SILVER,E 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 E

~>"tt~Jyg N

NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBFR OF COPIES REQUIRED: LTTR 15 ENCL 15

C r

AND ROCHESTER GAS AND EIECTRIC CORPORATION ~ 89 EASTAVEMIJE, ROCHESTER, N. Y 146d9-0001 AREA CODE7I6 5'-2700 ROBERT C. MECREDY Vice President Nuclear Operations November 6, 1996 U.S. Nuclear Regulatory Commission Document Control Desk Attn: Guy S. Vissing Project Directorate I-1 Washington, D.C. 20555

Subject:

10 CFR Part 21 30 Day Report R.E. Ginna Nuclear Power Plant Docket No. 50-244

Dear Mr. Vissing:

In accordance with 10 CFR Part 21, Rep'orting of Defects and Noncompliance, Section 21 (d)

(3) (ii), which requires "Written notification to the NRC ... on the identification of a defect or failure to comply", the attached 10 CFR 21 report is hereby submitted.

Ve ly yours Robert C. Me edy xc: Mr. Guy S. Vissing (Mail Stop 14C7)

Project Directorate I-1 Washington, D.C. 20555 Regional Administrator U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna Senior Resident Inspector

~Con qiXS<5000i VS,XX06 PDR ADOCK 05000244 8 PDR

Page 2 10CFR21 30 DAY WRITTEN REPORT I. NAME AND ADDRESS OF THE INDIVIDUALINFORMING THE COMMISSION:

NAME: Robert C. Mecredy Vice President Nuclear Operations ADDRESS: Rochester Gas & Electric Corporation 89 East Avenue Rochester, New York 14649 II. IDENTIFICATION OF THE FACILITY, THE ACTIVITY, OR THE BASIC COMPONENT SUPPLIED FOR SUCH FACILITYWHICH FAILS TO COMPLY OR CONTAINS A DEFECT:

The facility is the R.E. Ginna Nuclear Power Plant. The basic component is a 350 HP, 1800 RPM, 460 VAC, 3 phase, 5006P Frame, 1.15 SF, vertical hollow shaft motor for use as a Service Water (SW) pump motor. This component was installed at the R.E.

Ginna Nuclear Power Plant to upgrade the motor for the "A" SW pump from a 300 HP to a 350 HP motor. (The "A" SW pump was never declared operable with this defective motor installed.)

III. IDENTIFICATION OF THE FIRM CONSTRUCTING THE FACILITY OR SUPPLYING THE BASIC COMPONENT WHICH FAILS TO COMPLY OR CONTAINS A DEFECT:

The motor was a commercial-grade motor manufactured by:

U.S. Electrical Motors Division of Emerson Electric Co.

8100 W. Florissant Ave.

PO Box 3946 St. Louis, MO 63136 The motor was procured from:

Auburn Armature, Inc.

48 Canoga St.

Auburn, NY 13021 Note: This motor was purchased commercial-grade, was commercially-dedicated by Rochester Gas & Electric, and satisfied all testing requirements included in the procurement documents.

Page 3

~

IV. NATURE OF THE DEFECT OR FAILURE TO COMPLY AND THE SAFETY HAZARD WHICH IS CREATED OR COULD BE CREATED BY SUCH DEFECT OR FAILURE TO COMPLY:

A 350 HP motor was installed on the "A" SW pump in July, 1996. Post-modification functional testing revealed unacceptable megger readings. The motor was removed from the "A" SW pump, disassembled and inspected. The inspection revealed degradation of motor insulation integrity due to damaged motor leads, which could result in the failure of the motor in service. The overall quality of the motor was below that normally expected for a commercial grade motor.

The safety hazard which could be created by such a defect is the complete loss of Service Water. In the scenario of the "C" SW pump out of service and a concurrent loss of power to Bus 17 (which supplies power to the "B" and "D" SW pumps), a loss of all SW would occur if the "A" SW pump failed to operate due to the identified defect.

V. THE DATE ON WHICH THE INFORMATION OF SUCH DEFECT OR FAILURE TO COMPLY WAS OBTAINED:

The information was obtained on August 5, 1996.

VI. IN THE CASE OF A BASIC COMPONENT WHICH CONTAINS A DEFECT OR FAILS TO COMPLY, THE NUMBER AND LOCATION OF 'ALL SUCH COMPONENTS IN USE AT, SUPPLIED FOR, OR BEING SUPPLIED FOR GINNA STATION:

There are four (4) SW pumps located in the Screenhouse Building at Ginna Station.

A 350 HP motor had previously been procured separately. This motor was installed to upgrade the existing 300 HP motor on the "D" SW pump in August, 1995. This 350 motor is of similar design to the 3 motors discussed below, and was also manufactured by U.S. Electrical Motors. This motor was tested satisfactorily and placed in service in August, 1995, and operated trouble-free. As discussed below, this motor did not contain a defect.

Three (3) 350 HP motors, manufactured by U.S. Electrical Motors, were purchased at a later date (as a group) for upgrade of the existing 300 HP motors on the "A", "B", and "C" SW pumps. As discussed below, two of these three motors were discovered to be defective.

Page 4 VI~~. THE CORRECTIVE ACTION WHICH HAS BEEN, IS BEING, OR WILL BE TAKEN; THE NAME OF THE INDIVIDUALOR ORGANIZATIONRESPONSIBLE FOR THE ACTION; AND THE LENGTH OF TIME THAT HAS BEEN OR WILL BE TAKEN TO COMPLETE THE ACTION:

The following corrective actions have been completed:

1. Ginna Station Maintenance personnel removed the defective 350 HP motor from the "A" SW pump, and shipped this motor and one uninstalled 350 HP motor to an Appendix B motor facility. These two motors both exhibited degradation of motor insulation integrity. The motors were tested, inspected, and confirmed to be defective. They were refurbished by the motor facility, and returned to Ginna Station.
2. The "A" SW pump remained inoperable until one of the above refurbished motors was reinstalled and satisfactorily tested in August, 1996.
3. The similar 350 HP motor, installed on the "D" SW pump in August, 1995, had shown no signs of motor degradation. However, this motor was removed from the "D" SW pump in October, 1996, and was replaced by the other refurbished spare motor.
4. Thus, corrective action was completed for these two defective motors in August, 1996, and these two refurbished motors were subsequently installed on the "A" and "D" SW pumps, and have fulfilled operability test requirements.

5 ~ Electrical testing on the other two 350 HP motors did not indicate any degradation of the motor insulation integrity. Nevertheless, as a conservative measure, they were shipped to an Appendix B motor facility in October, 1996, for diagnostics and troubleshooting.

These remaining two 350 HP motors have been disassembled, inspected, and tested at an Appendix B motor facility. Electrical testing, performed at the motor facility, achieved satisfactory performance results, confirming that the motor (previously installed on the "D" SW pump) was operable while in service.

However, some minor deficient conditions were noted on both motors. These motors were also refurbished. These refurbishments are considered to be conservative corrective measures which involved motor releading, insulation redip and bearing rework.

The following corrective actions are scheduled for completion by March, 1997:

Safety-related motor Commercial Grade Item Engineering Evaluations (CGIEE's) will be revised to enhance steps for the examination of windings and overall workmanship to ensure motors are constructed with acceptable quality.

CGIEE preparation guidelines willbe enhanced to incorporate the lessons learned from these defective motors.

F 4s

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~ VIII. ANY ADVICE RELATED TO THE DEFECT OR FAILURE TO COMPLY ABOUT THE FACILITY, ACTIVITY, OR BASIC COMPONENT THAT HAS BEEN, IS BEING, OR WILLBE GIVEN TO PURCHASERS OR LICENSEES:

1. Source surveillance during motor assembly may have detected this defect.
2. A detailed physical inspection (or disassembly) upon receipt may have detected this defect.
3. Completion of commercial dedication could be dependent upon satisfactory completion of post-modification functional testing.