ML17347B316: Difference between revisions

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See also: [[followed by::IR 05000250/1989027]]


=Text=
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{{#Wiki_filter:AC CElZ RATED Dl STPJBUTJ ON DEMON STRATlON SYSTEM REGULATORY
{{#Wiki_filter:AC CElZ RATED Dl STPJBUTJ ON DEMON STRATlON SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)CESSION NBR:8909120388 DOC.DATE: 89/09/01 NOTARIZED:
INFORMATION
NO FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 50-251 Turkey Point Plant, Unit 4, Florida Power and Light C AUTH.NAME AUTHOR AFFILIATION WOODY,C.O.
DISTRIBUTION
Florida Power&Light Co.RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SYSTEM (RIDS)CESSION NBR:8909120388
 
DOC.DATE: 89/09/01 NOTARIZED:
==SUBJECT:==
NO FACIL:50-250
Responds to violations noted in Insp Repts 50-250/89-27
Turkey Point Plant, Unit 3, Florida Power and Light C 50-251 Turkey Point Plant, Unit 4, Florida Power and Light C AUTH.NAME AUTHOR AFFILIATION
WOODY,C.O.
Florida Power&Light Co.RECIP.NAME
RECIPIENT AFFILIATION
Document Control Branch (Document Control Desk)SUBJECT: Responds to violations
noted in Insp Repts 50-250/89-27
&50-251/89-27.
&50-251/89-27.
DISTRIBUTION
DISTRIBUTION CODE: IEOID COPIES RECEIVED:LTR ENCL t SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice of Vio ation Response NOTES: DOCKET 05000250 05000251 RECIPIENT ID CODE/NAME PD2-2 PD INTERNAL: AEOD AEOD/TPAD LOIS, ERASMIA NRR/DEST DIR NRR/DOEA DIR 1 1 NRR/DREP/RPB 10 NUDOCS-ABSTRACT OGC/HDS2 RES MORI SSEAU I D EXTERNAL: LPDR NSIC COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1'1 1 1 1 1 1'1 1 RECIPIENT ID CODE/NAME EDISON,G AEOD/DEIIB DEDRO NRR SHANKMAN,S NRR/DLPQ/PEB NRR/DREP/EPB 10 NRR/PMAS/I LRB12 OE IZ RMAN, J G FIL 02 H2~ILE 01 NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1.1 1 1 1 1 1 1 R h NOIR'IO ALL'RING" RECZEKZÃIS'LEASE HELP US IO REDUCE RASTE.'MIRCT
CODE: IEOID COPIES RECEIVED:LTR
'IHE DOCGMERZ CGNZROL DESK, RXN Pl-37 (EXT.20079)KO iKZMINATR KX3R NAME PKH DISTBIHUTICN LISTS FOR DO(XIMEHIS VXJ MN'T NEEDt TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24-D S Cl P.O.Bc,x 14000, Juno Beach, FL 33408.0420 SEPTEMBER 1 1989 L-89-325 10 CFR 2.201 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Gentlemen:
ENCL t SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice
Re: Turkey Point Units 3 and 4 Docket Nos.50-250 and 50-251 Reply to Notice of Violation Ins ection Re ort 89-27 Florida Power&Light Company (FPL)has reviewed the subject inspection report and pursuant to 10 CFR 2.201 the response is attached.Very truly yours, pe~~~C.O.oody Acti Senior Vice President-Nuclear COW/JRH/cm Attachment cc: Stewart D.Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant 8 F05'1203C<3 (y0y01 PDR ADOCK 0 F0002'50 9 PDC w~gg(I<an FPL Group company  
of Vio ation Response NOTES: DOCKET 05000250 05000251 RECIPIENT ID CODE/NAME PD2-2 PD INTERNAL: AEOD AEOD/TPAD LOIS, ERASMIA NRR/DEST DIR NRR/DOEA DIR 1 1 NRR/DREP/RPB
 
10 NUDOCS-ABSTRACT
ATTACHMENT RE: Turkey Point Units 3 and 4 Docket Numbers 50-250 and 50-251 NRC Inspection Report 89-27 FINDING A TS 6.8.1 requires that written procedures and administrative policies shall be established, implemented and maintained that meet or exceed the requirements and recommendations of Appendix A of USNRC Regulatory Guide 1.33 and Sections 5.1 and 5.3 of ANSI N18.7-1972.
OGC/HDS2 RES MORI SSEAU I D EXTERNAL: LPDR NSIC COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1'1 1 1 1 1 1'1 1 RECIPIENT ID CODE/NAME EDISON,G AEOD/DEIIB
Administrative Procedure O-ADM-209, Equipment Tagging and Labeling, provides the responsibilities, precautions, limitations and instructional guidance for establishing and maintaining an accurate, com-plete and effective plant tagging program.Contrary to the above, engraved label plates were replaced on the Unit 3 Safe-ty In)ection Block Switch without following the requirements of Administrative Procedure O-ADM-209, resulting in two separate safeguard actuations within a 24-hour period.RESPONSE A 1.FPL concurs with the finding.2.The cause for this finding was personnel error by non-licensed utility personnel'he label on the Safety In)ection Block Switch had been re-cently replaced with a label which contained more detailed information.
DEDRO NRR SHANKMAN,S
Both the person responsible for validating the label and the person who installed the label for the Safety Injection Block Switch failed to ade-quately validate all the information contained on the new label.The new label installed had the"Blocked" and"Unblocked" switch positions re-versed.This resulted in the switch being placed unknowingly in the"Unblocked" position instead of the"Blocked" position.With the switch in the"Unblocked" position, when the manual block buttons were released, an SI signal was produced.An unclear drawing was the reason the inaccurate label was not identified following the first SI actuation.
NRR/DLPQ/PEB
The I&C technician was required by the Plant Work Order for this activity to verify that the switch had proper continuity in the block, neutral, and unblock positions.
NRR/DREP/EPB
When he performed this step, confusing information on drawing 5610-M-430-171, Sheet 5,"Units 3 an 4 Safeguards System," lead the technician to believe that the switch was responding correctly.
10 NRR/PMAS/I
This resulted in the inaccurate label not being  
LRB12 OE IZ RMAN, J G FIL 02 H2~ILE 01 NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1.1 1 1 1 1 1 1 R h NOIR'IO ALL'RING" RECZEKZ&#xc3;IS'LEASE
 
HELP US IO REDUCE RASTE.'MIRCT
'IHE DOCGMERZ CGNZROL DESK, RXN Pl-37 (EXT.20079)KO iKZMINATR KX3R NAME PKH DISTBIHUTICN
LISTS FOR DO(XIMEHIS
VXJ MN'T NEEDt TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24-D S  
Cl  
P.O.Bc,x 14000, Juno Beach, FL 33408.0420
SEPTEMBER 1 1989 L-89-325 10 CFR 2.201 U.S.Nuclear Regulatory
Commission
Attn: Document Control Desk Washington, D.C.20555 Gentlemen:
Re: Turkey Point Units 3 and 4 Docket Nos.50-250 and 50-251 Reply to Notice of Violation Ins ection Re ort 89-27 Florida Power&Light Company (FPL)has reviewed the subject inspection
report and pursuant to 10 CFR 2.201 the response is attached.Very truly yours, pe~~~C.O.oody Acti Senior Vice President-Nuclear COW/JRH/cm
Attachment
cc: Stewart D.Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant 8 F05'1203C<3 (y0y01 PDR ADOCK 0 F0002'50 9 PDC w~gg(I<an FPL Group company  
ATTACHMENT
RE: Turkey Point Units 3 and 4 Docket Numbers 50-250 and 50-251 NRC Inspection
Report 89-27 FINDING A TS 6.8.1 requires that written procedures
and administrative
policies shall be established, implemented
and maintained
that meet or exceed the requirements
and recommendations
of Appendix A of USNRC Regulatory
Guide 1.33 and Sections 5.1 and 5.3 of ANSI N18.7-1972.
Administrative
Procedure O-ADM-209, Equipment Tagging and Labeling, provides the responsibilities, precautions, limitations
and instructional
guidance for establishing
and maintaining
an accurate, com-plete and effective plant tagging program.Contrary to the above, engraved label plates were replaced on the Unit 3 Safe-ty In)ection Block Switch without following the requirements
of Administrative
Procedure O-ADM-209, resulting in two separate safeguard actuations
within a 24-hour period.RESPONSE A 1.FPL concurs with the finding.2.The cause for this finding was personnel error by non-licensed
utility personnel'he
label on the Safety In)ection Block Switch had been re-cently replaced with a label which contained more detailed information.
Both the person responsible
for validating
the label and the person who installed the label for the Safety Injection Block Switch failed to ade-quately validate all the information
contained on the new label.The new label installed had the"Blocked" and"Unblocked" switch positions re-versed.This resulted in the switch being placed unknowingly
in the"Unblocked" position instead of the"Blocked" position.With the switch in the"Unblocked" position, when the manual block buttons were released, an SI signal was produced.An unclear drawing was the reason the inaccurate
label was not identified
following the first SI actuation.
The I&C technician
was required by the Plant Work Order for this activity to verify that the switch had proper continuity
in the block, neutral, and unblock positions.
When he performed this step, confusing information
on drawing 5610-M-430-171, Sheet 5,"Units 3 an 4 Safeguards
System," lead the technician
to believe that the switch was responding
correctly.
This resulted in the inaccurate
label not being  
identified.
identified.
Two switch contact blocks which showed signs of physical damage were considered
Two switch contact blocks which showed signs of physical damage were considered to be the cause of the first SI actuation.
to be the cause of the first SI actuation.
Corrective steps which have been taken and the results achieved include: a.b~The Unit 3 Safety In)ection Block Switch has been relabeled to correctly identify switch positions.
Corrective
The Safety In)ection Block Switch labels in the Simulator and in the Unit 4 Control Room have been verified to be correct.4.Corrective steps which will be taken to, avoid further violations include: a~The individual responsible for validating the tag, and the individ-ual responsible for placing the tag were counseled.
steps which have been taken and the results achieved include: a.b~The Unit 3 Safety In)ection Block Switch has been relabeled to correctly identify switch positions.
This counseling stressed the importance of verifying the information contained on tags before they are installed.b.Administrative Procedure 0-ADM-209 has been revised to require in-dependent verification by a Reactor Control Operator of the accuracy of information on new tags being installed in the Control Room.c.Drawing 5610-M-430-171, Sheet 5 has been revised to remove confusion related to the switch nomenclature orientation.
The Safety In)ection Block Switch labels in the Simulator and in the Unit 4 Control Room have been verified to be correct.4.Corrective
5.Date when full compliance will be achieved: a.Action item 3.a,was completed on June 23, 1989.b.Action item 3.b was completed on June 23, 1989.c.Action item 4.a was completed on June 23, 1989.d.Action item 4.b was completed on July 7, 1989.e.Action item 4.c was completed on August 15, 1989.FINDIHG B 10 CFR 50, Appendix B, Criterion III, as implemented by the approved Florida Power and Light Company Topical Quality Assurance Report (FPLTQAR)1-76A, Revision II, Topical Quality Requirement (TQR)3.0, Revision 7, requires that measures be established to assure that applicable regulatory requirements and the design basis are correctly translated into specifications, drawings, pro-cedures, and instructions.
steps which will be taken to, avoid further violations
Contrary to the above, the required 2.0 second opening time specified for the Pressurizer Power Operated Relief Valve (PORV)in the Overpressure Mitigating System (OMS)Safety Evaluation Report dated March 14, 1980, was not incorpor-ated into the licensee s Inservice Testing Program.Instead, a non-conserva-tive acceptance criteria of 15.0 seconds was used.This resulted in the Unit 3 and 4 PORVs being unable to maintain Reactor Coolant System (RCS)pressure  
include: a~The individual
 
responsible
b elow the 10 CFR 50, Appendix G limits, had the most limiting design basis transient occurred.This condition existed on several occasions from May 1984 to June 1988, as exhibited by a review of PORV stroke timing records.RESPONSE B 1.FPL concurs with the finding.2.The cause for this finding was an inadequate design process The process did not verify that the design basis opening time of 2.0 seconds for the PORVs could be met by the PORVs installed at Turkey Point, nor did the process assure that the proper acceptance criteria was incorporated into the Plant s affected documents; 3.Corrective steps which have been taken and the results achieved include: a~Westinghouse has performed an evaluation of the increased PORV stroke times against each of three overpressure events (inadvertent start of two charging pumps with a loss of letdown, spurious start of one safety in)ection pump, and inadvertent starting of a RCP with a temperature differential between the secondary system and the RCS of 50 degrees F).The mass in)ection pressure transient of a spur-ious start of a single safety in)ection pump has been determined to be the most limiting pressure transient event.The final results showed that the PORVs could be tested up to 3.45 seconds and still prevent the most limiting pressure transient from exceeding 10CFR50, Appendix G limits.For the case of two charging pumps starting with a loss of letdown and of inadvertent starting of a RCP with a temperature differential between the secondary system and the RCS of 20 degrees F (Turkey Point operating procedures specify 10 degrees F), the Westinghouse evaluation demonstrated that PORV opening stroke times would have to exceed 10.0 seconds before the limits of 10CFR50, Appendix G would be approached
for validating
.b.Plant Change/Modification (PC/M)88-535 has been issued to increase the size of the Unit 4 PORV instrument air and nitrogen backup supply line tubing.This PC/M has been implemented and was demon-strated to be effective in decreasing the PORV opening time through performance of Preoperational Procedure 0800.216,"Pressurizer PORV Nitrogen Backup and Timing." This procedure requires an opening time of 1.65 to 3.45 seconds and a closing time of 1.0 to 2.0 seconds using both instrument air and nitrogen backup supplies.C~PC/M 88-427 has been issued to increase the size of the Unit 3 PORV instrument air supply line tubing as a temporary measure to decrease the PORV opening stroke time.This PC/M has been implemented and was demonstrated to be effective through.performance of Startup Field Procedure SFP-13,"Startup Test Control-Interim Department-al Testing." Permanent modifications to the PORV instrument air and nitrogen backup supply line tubing will be implemented on the Unit 3 PORVs prior to restart from the next refueling outage.Compensatory measures are in place as a condition of NRC Discretionary Enforcement to allow continued Unit 3 operation with PORV opening stroke times of less than or equal to 10.0 seconds until these permanent modifications are completed.
the tag, and the individ-ual responsible
Operating Procedure OP 0209 F 1,"Valve Exercising Procedure," provides instructions for the periodic exercising of Safety Class 1, 2, and 3 valves for which exercising is required by the Valve Test Program portion of the Turkey Point Inservice Testing Program.This pro-cedure has been revised to ensure the Unit 4 PORVs meet an opening stroke time of 3.45.e.OP 0209.1 has been revised to ensure the Unit 3 PORVs meet an open-ing stroke time of less than or equal to 10.0 seconds.OP 0209.1 will be revised to specify an opening stroke time of 3.45 seconds for the Unit 3 PORVs upon completion of long term corrective modi-fications during the next refueling outage.Operations Surveillance Procedure 4-0SP-041.4,"Overpressure Miti-gating System Nitrogen Backup Leak and Functional Test," has been revised to ensure the Unit 4 PORVs meet an opening stroke time of 3.45 seconds using the nitrogen backup supply.g~Procedure 3-0SP-041.4 has been revised to ensure the Unit 3 PORVs meet an opening stroke time of less than or equal to 10.0 seconds using the nitrogen backup supply.3-0SP-041.4 will be revised to specify an opening stroke time of 3.45 seconds for the Unit 3 PORVs using the nitrogen backup supply upon completion of long term modi-fications during the next refueling outage.4.Corrective steps which will be taken to avoid further violations include: a~Administrative Procedure (AP)0103 18'acility Operating License Amendments and/or Changes," has been revised to require the Nuclear Engineering Department personnel to document the review of proposed license amendments and provide a response to the Regulation and Compliance Group.b~Nuclear Engineering Quality Instruction (QI)3.11,"JPN Review of Technical Specification Amendments," has been issued which requires the review of technical specification amendments for impact on eng-ineering design documents.
for placing the tag were counseled.
5.Date when full compliance will be achieved: a~Action item 3.a was completed on March 2, 1989.b~Action item 3.b was completed on March 2, 1989.c~Action item 3.c will be complete prior to startup from the next Unit 3 refueling outage which is currently scheduled for May 31, 1990.d.Action item 3.d was completed on February 24, 1989~  
This counseling
 
stressed the importance
e.Action item 3.e will be complete prior to startup from the next Unit 3 refueling outage which is currently scheduled for May 31, 1990.f.Action item 3.f was completed on May 2, 1989.g.Action item 3.g will be complete prior to startup from the next Unit 3 refueling outage which is currently scheduled for May 31, 1990.h.Action item 4.a was completed on November 28, 1988.i.Action item 4.b was completed in December 1988.}}
of verifying the information
contained on tags before they are installed.b.Administrative
Procedure 0-ADM-209 has been revised to require in-dependent verification
by a Reactor Control Operator of the accuracy of information
on new tags being installed in the Control Room.c.Drawing 5610-M-430-171, Sheet 5 has been revised to remove confusion related to the switch nomenclature
orientation.
5.Date when full compliance
will be achieved: a.Action item 3.a,was completed on June 23, 1989.b.Action item 3.b was completed on June 23, 1989.c.Action item 4.a was completed on June 23, 1989.d.Action item 4.b was completed on July 7, 1989.e.Action item 4.c was completed on August 15, 1989.FINDIHG B 10 CFR 50, Appendix B, Criterion III, as implemented
by the approved Florida Power and Light Company Topical Quality Assurance Report (FPLTQAR)1-76A, Revision II, Topical Quality Requirement (TQR)3.0, Revision 7, requires that measures be established
to assure that applicable
regulatory
requirements
and the design basis are correctly translated
into specifications, drawings, pro-cedures, and instructions.
Contrary to the above, the required 2.0 second opening time specified for the Pressurizer
Power Operated Relief Valve (PORV)in the Overpressure
Mitigating
System (OMS)Safety Evaluation
Report dated March 14, 1980, was not incorpor-ated into the licensee s Inservice Testing Program.Instead, a non-conserva-
tive acceptance
criteria of 15.0 seconds was used.This resulted in the Unit 3 and 4 PORVs being unable to maintain Reactor Coolant System (RCS)pressure  
b elow the 10 CFR 50, Appendix G limits, had the most limiting design basis transient occurred.This condition existed on several occasions from May 1984 to June 1988, as exhibited by a review of PORV stroke timing records.RESPONSE B 1.FPL concurs with the finding.2.The cause for this finding was an inadequate
design process The process did not verify that the design basis opening time of 2.0 seconds for the PORVs could be met by the PORVs installed at Turkey Point, nor did the process assure that the proper acceptance
criteria was incorporated
into the Plant s affected documents;
3.Corrective
steps which have been taken and the results achieved include: a~Westinghouse
has performed an evaluation
of the increased PORV stroke times against each of three overpressure
events (inadvertent
start of two charging pumps with a loss of letdown, spurious start of one safety in)ection pump, and inadvertent
starting of a RCP with a temperature
differential
between the secondary system and the RCS of 50 degrees F).The mass in)ection pressure transient of a spur-ious start of a single safety in)ection pump has been determined
to be the most limiting pressure transient event.The final results showed that the PORVs could be tested up to 3.45 seconds and still prevent the most limiting pressure transient from exceeding 10CFR50, Appendix G limits.For the case of two charging pumps starting with a loss of letdown and of inadvertent
starting of a RCP with a temperature
differential
between the secondary system and the RCS of 20 degrees F (Turkey Point operating procedures
specify 10 degrees F), the Westinghouse
evaluation
demonstrated
that PORV opening stroke times would have to exceed 10.0 seconds before the limits of 10CFR50, Appendix G would be approached
.b.Plant Change/Modification (PC/M)88-535 has been issued to increase the size of the Unit 4 PORV instrument
air and nitrogen backup supply line tubing.This PC/M has been implemented
and was demon-strated to be effective in decreasing
the PORV opening time through performance
of Preoperational
Procedure 0800.216,"Pressurizer
PORV Nitrogen Backup and Timing." This procedure requires an opening time of 1.65 to 3.45 seconds and a closing time of 1.0 to 2.0 seconds using both instrument
air and nitrogen backup supplies.C~PC/M 88-427 has been issued to increase the size of the Unit 3 PORV instrument
air supply line tubing as a temporary measure to decrease the PORV opening stroke time.This PC/M has been implemented
and was demonstrated
to be effective through.performance
of Startup Field Procedure SFP-13,"Startup Test Control-Interim Department-
al Testing." Permanent modifications
to the PORV instrument
air and nitrogen backup supply line tubing will be implemented
on the Unit 3  
PORVs prior to restart from the next refueling outage.Compensatory
measures are in place as a condition of NRC Discretionary
Enforcement
to allow continued Unit 3 operation with PORV opening stroke times of less than or equal to 10.0 seconds until these permanent modifications
are completed.
Operating Procedure OP 0209 F 1,"Valve Exercising
Procedure," provides instructions
for the periodic exercising
of Safety Class 1, 2, and 3 valves for which exercising
is required by the Valve Test Program portion of the Turkey Point Inservice Testing Program.This pro-cedure has been revised to ensure the Unit 4 PORVs meet an opening stroke time of 3.45.e.OP 0209.1 has been revised to ensure the Unit 3 PORVs meet an open-ing stroke time of less than or equal to 10.0 seconds.OP 0209.1 will be revised to specify an opening stroke time of 3.45 seconds for the Unit 3 PORVs upon completion
of long term corrective
modi-fications during the next refueling outage.Operations
Surveillance
Procedure 4-0SP-041.4,"Overpressure
Miti-gating System Nitrogen Backup Leak and Functional
Test," has been revised to ensure the Unit 4 PORVs meet an opening stroke time of 3.45 seconds using the nitrogen backup supply.g~Procedure 3-0SP-041.4
has been revised to ensure the Unit 3 PORVs meet an opening stroke time of less than or equal to 10.0 seconds using the nitrogen backup supply.3-0SP-041.4
will be revised to specify an opening stroke time of 3.45 seconds for the Unit 3 PORVs using the nitrogen backup supply upon completion
of long term modi-fications during the next refueling outage.4.Corrective
steps which will be taken to avoid further violations
include: a~Administrative
Procedure (AP)0103 18'acility
Operating License Amendments
and/or Changes," has been revised to require the Nuclear Engineering
Department
personnel to document the review of proposed license amendments
and provide a response to the Regulation
and Compliance
Group.b~Nuclear Engineering
Quality Instruction (QI)3.11,"JPN Review of Technical Specification
Amendments," has been issued which requires the review of technical specification
amendments
for impact on eng-ineering design documents.
5.Date when full compliance
will be achieved: a~Action item 3.a was completed on March 2, 1989.b~Action item 3.b was completed on March 2, 1989.c~Action item 3.c will be complete prior to startup from the next Unit 3 refueling outage which is currently scheduled for May 31, 1990.d.Action item 3.d was completed on February 24, 1989~  
e.Action item 3.e will be complete prior to startup from the next Unit 3 refueling outage which is currently scheduled for May 31, 1990.f.Action item 3.f was completed on May 2, 1989.g.Action item 3.g will be complete prior to startup from the next Unit 3 refueling outage which is currently scheduled for May 31, 1990.h.Action item 4.a was completed on November 28, 1988.i.Action item 4.b was completed in December 1988.
}}

Revision as of 07:27, 17 August 2019

Responds to Violations Noted in Insp Repts 50-250/89-27 & 50-251/89-27.Corrective Actions:Administrative Procedure 0-ADM-209 Revised to Require Independent Verification by Reactor Control Operator of Accuracy of Info on New Tags
ML17347B316
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 09/01/1989
From: Woody C
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-89-325, NUDOCS 8909120388
Download: ML17347B316 (13)


Text

AC CElZ RATED Dl STPJBUTJ ON DEMON STRATlON SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)CESSION NBR:8909120388 DOC.DATE: 89/09/01 NOTARIZED:

NO FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 50-251 Turkey Point Plant, Unit 4, Florida Power and Light C AUTH.NAME AUTHOR AFFILIATION WOODY,C.O.

Florida Power&Light Co.RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Responds to violations noted in Insp Repts 50-250/89-27

&50-251/89-27.

DISTRIBUTION CODE: IEOID COPIES RECEIVED:LTR ENCL t SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice of Vio ation Response NOTES: DOCKET 05000250 05000251 RECIPIENT ID CODE/NAME PD2-2 PD INTERNAL: AEOD AEOD/TPAD LOIS, ERASMIA NRR/DEST DIR NRR/DOEA DIR 1 1 NRR/DREP/RPB 10 NUDOCS-ABSTRACT OGC/HDS2 RES MORI SSEAU I D EXTERNAL: LPDR NSIC COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1'1 1 1 1 1 1'1 1 RECIPIENT ID CODE/NAME EDISON,G AEOD/DEIIB DEDRO NRR SHANKMAN,S NRR/DLPQ/PEB NRR/DREP/EPB 10 NRR/PMAS/I LRB12 OE IZ RMAN, J G FIL 02 H2~ILE 01 NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1.1 1 1 1 1 1 1 R h NOIR'IO ALL'RING" RECZEKZÃIS'LEASE HELP US IO REDUCE RASTE.'MIRCT

'IHE DOCGMERZ CGNZROL DESK, RXN Pl-37 (EXT.20079)KO iKZMINATR KX3R NAME PKH DISTBIHUTICN LISTS FOR DO(XIMEHIS VXJ MN'T NEEDt TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24-D S Cl P.O.Bc,x 14000, Juno Beach, FL 33408.0420 SEPTEMBER 1 1989 L-89-325 10 CFR 2.201 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Gentlemen:

Re: Turkey Point Units 3 and 4 Docket Nos.50-250 and 50-251 Reply to Notice of Violation Ins ection Re ort 89-27 Florida Power&Light Company (FPL)has reviewed the subject inspection report and pursuant to 10 CFR 2.201 the response is attached.Very truly yours, pe~~~C.O.oody Acti Senior Vice President-Nuclear COW/JRH/cm Attachment cc: Stewart D.Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant 8 F05'1203C<3 (y0y01 PDR ADOCK 0 F0002'50 9 PDC w~gg(I<an FPL Group company

ATTACHMENT RE: Turkey Point Units 3 and 4 Docket Numbers 50-250 and 50-251 NRC Inspection Report 89-27 FINDING A TS 6.8.1 requires that written procedures and administrative policies shall be established, implemented and maintained that meet or exceed the requirements and recommendations of Appendix A of USNRC Regulatory Guide 1.33 and Sections 5.1 and 5.3 of ANSI N18.7-1972.

Administrative Procedure O-ADM-209, Equipment Tagging and Labeling, provides the responsibilities, precautions, limitations and instructional guidance for establishing and maintaining an accurate, com-plete and effective plant tagging program.Contrary to the above, engraved label plates were replaced on the Unit 3 Safe-ty In)ection Block Switch without following the requirements of Administrative Procedure O-ADM-209, resulting in two separate safeguard actuations within a 24-hour period.RESPONSE A 1.FPL concurs with the finding.2.The cause for this finding was personnel error by non-licensed utility personnel'he label on the Safety In)ection Block Switch had been re-cently replaced with a label which contained more detailed information.

Both the person responsible for validating the label and the person who installed the label for the Safety Injection Block Switch failed to ade-quately validate all the information contained on the new label.The new label installed had the"Blocked" and"Unblocked" switch positions re-versed.This resulted in the switch being placed unknowingly in the"Unblocked" position instead of the"Blocked" position.With the switch in the"Unblocked" position, when the manual block buttons were released, an SI signal was produced.An unclear drawing was the reason the inaccurate label was not identified following the first SI actuation.

The I&C technician was required by the Plant Work Order for this activity to verify that the switch had proper continuity in the block, neutral, and unblock positions.

When he performed this step, confusing information on drawing 5610-M-430-171, Sheet 5,"Units 3 an 4 Safeguards System," lead the technician to believe that the switch was responding correctly.

This resulted in the inaccurate label not being

identified.

Two switch contact blocks which showed signs of physical damage were considered to be the cause of the first SI actuation.

Corrective steps which have been taken and the results achieved include: a.b~The Unit 3 Safety In)ection Block Switch has been relabeled to correctly identify switch positions.

The Safety In)ection Block Switch labels in the Simulator and in the Unit 4 Control Room have been verified to be correct.4.Corrective steps which will be taken to, avoid further violations include: a~The individual responsible for validating the tag, and the individ-ual responsible for placing the tag were counseled.

This counseling stressed the importance of verifying the information contained on tags before they are installed.b.Administrative Procedure 0-ADM-209 has been revised to require in-dependent verification by a Reactor Control Operator of the accuracy of information on new tags being installed in the Control Room.c.Drawing 5610-M-430-171, Sheet 5 has been revised to remove confusion related to the switch nomenclature orientation.

5.Date when full compliance will be achieved: a.Action item 3.a,was completed on June 23, 1989.b.Action item 3.b was completed on June 23, 1989.c.Action item 4.a was completed on June 23, 1989.d.Action item 4.b was completed on July 7, 1989.e.Action item 4.c was completed on August 15, 1989.FINDIHG B 10 CFR 50, Appendix B, Criterion III, as implemented by the approved Florida Power and Light Company Topical Quality Assurance Report (FPLTQAR)1-76A, Revision II, Topical Quality Requirement (TQR)3.0, Revision 7, requires that measures be established to assure that applicable regulatory requirements and the design basis are correctly translated into specifications, drawings, pro-cedures, and instructions.

Contrary to the above, the required 2.0 second opening time specified for the Pressurizer Power Operated Relief Valve (PORV)in the Overpressure Mitigating System (OMS)Safety Evaluation Report dated March 14, 1980, was not incorpor-ated into the licensee s Inservice Testing Program.Instead, a non-conserva-tive acceptance criteria of 15.0 seconds was used.This resulted in the Unit 3 and 4 PORVs being unable to maintain Reactor Coolant System (RCS)pressure

b elow the 10 CFR 50, Appendix G limits, had the most limiting design basis transient occurred.This condition existed on several occasions from May 1984 to June 1988, as exhibited by a review of PORV stroke timing records.RESPONSE B 1.FPL concurs with the finding.2.The cause for this finding was an inadequate design process The process did not verify that the design basis opening time of 2.0 seconds for the PORVs could be met by the PORVs installed at Turkey Point, nor did the process assure that the proper acceptance criteria was incorporated into the Plant s affected documents; 3.Corrective steps which have been taken and the results achieved include: a~Westinghouse has performed an evaluation of the increased PORV stroke times against each of three overpressure events (inadvertent start of two charging pumps with a loss of letdown, spurious start of one safety in)ection pump, and inadvertent starting of a RCP with a temperature differential between the secondary system and the RCS of 50 degrees F).The mass in)ection pressure transient of a spur-ious start of a single safety in)ection pump has been determined to be the most limiting pressure transient event.The final results showed that the PORVs could be tested up to 3.45 seconds and still prevent the most limiting pressure transient from exceeding 10CFR50, Appendix G limits.For the case of two charging pumps starting with a loss of letdown and of inadvertent starting of a RCP with a temperature differential between the secondary system and the RCS of 20 degrees F (Turkey Point operating procedures specify 10 degrees F), the Westinghouse evaluation demonstrated that PORV opening stroke times would have to exceed 10.0 seconds before the limits of 10CFR50, Appendix G would be approached

.b.Plant Change/Modification (PC/M)88-535 has been issued to increase the size of the Unit 4 PORV instrument air and nitrogen backup supply line tubing.This PC/M has been implemented and was demon-strated to be effective in decreasing the PORV opening time through performance of Preoperational Procedure 0800.216,"Pressurizer PORV Nitrogen Backup and Timing." This procedure requires an opening time of 1.65 to 3.45 seconds and a closing time of 1.0 to 2.0 seconds using both instrument air and nitrogen backup supplies.C~PC/M 88-427 has been issued to increase the size of the Unit 3 PORV instrument air supply line tubing as a temporary measure to decrease the PORV opening stroke time.This PC/M has been implemented and was demonstrated to be effective through.performance of Startup Field Procedure SFP-13,"Startup Test Control-Interim Department-al Testing." Permanent modifications to the PORV instrument air and nitrogen backup supply line tubing will be implemented on the Unit 3 PORVs prior to restart from the next refueling outage.Compensatory measures are in place as a condition of NRC Discretionary Enforcement to allow continued Unit 3 operation with PORV opening stroke times of less than or equal to 10.0 seconds until these permanent modifications are completed.

Operating Procedure OP 0209 F 1,"Valve Exercising Procedure," provides instructions for the periodic exercising of Safety Class 1, 2, and 3 valves for which exercising is required by the Valve Test Program portion of the Turkey Point Inservice Testing Program.This pro-cedure has been revised to ensure the Unit 4 PORVs meet an opening stroke time of 3.45.e.OP 0209.1 has been revised to ensure the Unit 3 PORVs meet an open-ing stroke time of less than or equal to 10.0 seconds.OP 0209.1 will be revised to specify an opening stroke time of 3.45 seconds for the Unit 3 PORVs upon completion of long term corrective modi-fications during the next refueling outage.Operations Surveillance Procedure 4-0SP-041.4,"Overpressure Miti-gating System Nitrogen Backup Leak and Functional Test," has been revised to ensure the Unit 4 PORVs meet an opening stroke time of 3.45 seconds using the nitrogen backup supply.g~Procedure 3-0SP-041.4 has been revised to ensure the Unit 3 PORVs meet an opening stroke time of less than or equal to 10.0 seconds using the nitrogen backup supply.3-0SP-041.4 will be revised to specify an opening stroke time of 3.45 seconds for the Unit 3 PORVs using the nitrogen backup supply upon completion of long term modi-fications during the next refueling outage.4.Corrective steps which will be taken to avoid further violations include: a~Administrative Procedure (AP)0103 18'acility Operating License Amendments and/or Changes," has been revised to require the Nuclear Engineering Department personnel to document the review of proposed license amendments and provide a response to the Regulation and Compliance Group.b~Nuclear Engineering Quality Instruction (QI)3.11,"JPN Review of Technical Specification Amendments," has been issued which requires the review of technical specification amendments for impact on eng-ineering design documents.

5.Date when full compliance will be achieved: a~Action item 3.a was completed on March 2, 1989.b~Action item 3.b was completed on March 2, 1989.c~Action item 3.c will be complete prior to startup from the next Unit 3 refueling outage which is currently scheduled for May 31, 1990.d.Action item 3.d was completed on February 24, 1989~

e.Action item 3.e will be complete prior to startup from the next Unit 3 refueling outage which is currently scheduled for May 31, 1990.f.Action item 3.f was completed on May 2, 1989.g.Action item 3.g will be complete prior to startup from the next Unit 3 refueling outage which is currently scheduled for May 31, 1990.h.Action item 4.a was completed on November 28, 1988.i.Action item 4.b was completed in December 1988.