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{{#Wiki_filter:May 13, 2019
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PILGRIM NUCLEAR POWER STATION
PILGRIM NUCLEAR POWER STATION
  - INTEGRATED INSPECTION REPORT 05000293/2019001
  - INTEGRATED INSPECTION REPORT 05000293/2019001

Revision as of 23:13, 11 July 2019

Integrated Inspection Report 05000293/2019001
ML19133A225
Person / Time
Site: Pilgrim
Issue date: 05/13/2019
From: Anthony Dimitriadis
NRC/RGN-I/DRP/PB5
To: Brian Sullivan
Entergy Nuclear Operations
Dimitriadis A
References
IR 2019001
Download: ML19133A225 (18)


Text

SUBJECT:

PILGRIM NUCLEAR POWER STATION

- INTEGRATED INSPECTION REPORT 05000293/2019001

Dear Mr. Sullivan:

On March 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Pilgrim Nuclear Power Station (Pilgrim).

On April 18, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented one self-revealing Severity Level IV violation with no associated finding. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC resident inspector at Pilgrim. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding."

Sincerely,

/RA/ Anthony Dimitriadis, Chief Reactor Projects Branch 5

Division of Reactor Projects Docket Number: 50-293 License Number: DPR-35

Enclosure:

Inspection Report 05000293/2019001

Inspection Report

Docket Number: 50-293

License Number: DPR-35

Report Number: 05000293/2019001

Enterprise Identifier: I-2019-001-0042

Licensee: Entergy Nuclear Operations, Inc. (Entergy)

Facility: Pilgrim Nuclear Power Station (Pilgrim)

Location: Plymouth, Massachusetts

Inspection Dates: January 1, 2019 to March 31, 2019

Inspectors: E. Burket, Senior Resident Inspector B. Pinson, Resident Inspector P. Boguszewski, Resident Inspector S. Pindale, Senior Reactor Inspector J. Schoppy, Senior Reactor Inspector J. Vazquez, Resident Inspector S. Wilson, Health Physicist A. Ziedonis, Senior Resident Inspector Approved By: Anthony Dimitriadis, Chief Reactor Projects Branch 5

Division of Reactor Projects

2

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Entergy's performance at Pilgrim by conducting the baseline inspections described in this report in accordance with the

Reactor Oversight Process (ROP). The ROP is the NRC's program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and violations being considered in the NRC's assessment are summarized in the table below.

List of Findings and Violations Target Rock Relief Valve Pilot Assembly Fa iled As-Found Lift Test, A Condition Prohibited by Plant Technical Specifications Cornerstone Significance Cross-cutting Aspect Report Section Not Applicable NCV 05000293/2019001-01 Open/Closed Not Applicable 71153 A self-revealed, Severity Level IV, NCV of TS 4.6.D.1, Safety and Relief Valves, was identified when Entergy was notified that the as-found lift setpoint of a safety relief valve (SRV) exceeded the technical specification (TS) tolerance limit of 1155 +/- 34.6 psig (+/- 3 percent) during routine testing at an offsite vendor's test facility. Specifically, the as-found lift setpoint of SRV, pilot serial number 1025, exceeded the maximum allowable TS value of 1189.6 psig by 7.4 psig.

Additional Tracking Items Type Issue number Title Report Section Status LER 05000293/2018-003-00 Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, a Condition Prohibited by Plant Technical Specifications 71153 Closed LER 05000293/2019-001-00 Reactor Core Isolation Cooling System Declared Inoperable During Surveillance Testing 71153 Closed LER 05000293/2019-002-00 Failure of Main Steam Isolation Valve Limit Switch Results in a Condition Prohibited by Technical Specifications 71153 Closed

3

PLANT STATUS

===The unit began the inspection period at rated thermal power. On January 3, 2019, the station reduced power to 25 percent to troubleshoot and repair 'A' feedwater regulating valve. On January 6, 2019, operations personnel returned the unit to rated thermal power. On January 16, 2019, the station reduced power to 25 percent to repair a leaking primary containment isolation system valve. On January 17, 2019, operations personnel returned the unit to rated thermal power. On March 20, 2019, the station reduced power to 35 percent to repair a leaking feedwater heater valve in the condenser bay. On March 21, 2019, operations personnel returned the unit to rated thermal power and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, "Light-Water Reactor Inspection Program - Operations Phase." The inspectors performed plant status activities described in IMC 2515, Appendix D, "Plant Status," and conducted routine reviews using IP 71152, "Problem Identification and Resolution." The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.03)

(1) The inspectors evaluated readiness for impending adverse weather conditions for extreme cold temperatures on January 31, 2019.

71111.04 - Equipment Alignment

Partial Walkdown (IP Section 03.01)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) 'B' emergency diesel generator on February 5, 2019
(2) High pressure coolant injection system on February 9, 2019
(3) Reactor building closed cooling water on February 25-26, 2019
(4) 'A' and 'B' salt service water before and after 'B' salt service water testing on March 18-20, 2019

4 71111.04S - Equipment Alignment Complete Walkdown (IP Section 03.02) (1 Sample)===

===The inspectors evaluated system configurations during complete walkdowns of the following system:

(1) 'A' emergency diesel generator following maintenance and testing on March 27, 2019

71111.05A - Fire Protection (Annual)

Annual Inspection (IP Section 03.02)

(1) The inspectors evaluated fire brigade performance on January 30, 2019.

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) 'B' switchgear (fire zone 2.1) on February 24, 2019
(2) Cable spreading room (fire zone 3.2) on February 24, 2019
(3) Radwaste corridor area (fire zone 3.1) on February 26, 2019
(4) 'B' reactor building closed cooling water (fire zone 1.22) on March 9, 2019
(5) Machine shop (fire zone 3.8) on March 19, 2019

71111.07T - Heat Sink Performance Triennial Review (IP Section 02.02)

The inspectors evaluated heat exchanger/sink performance on the following:

(1) 'B' spent fuel pool cooling heat exchanger
(2) 'B' reactor building closed cooling water heat exchanger
(3) Ultimate heat sink associated with service water system operation and intake structure condition

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

The inspectors observed and evaluated licensed operator performance in the control room during down power to 25 percent and isolation of 'C' main steam line on January 3, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)===

The inspectors observed and evaluated licensed operator requalification training in the

===simulator on March 13, 2019.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Rod worth minimizer troubleshooting and repairs on February 20, 2019
(2) Main stack high range effluent monitors following return to (a)(2) status on February 20, 2019
(3) Neutron monitoring instrumentation following return to (a)(2) status completed March 12, 2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01)

The inspectors evaluated the risk assessments for the following planned and emergent work

activities:

(1) Emergent work to troubleshoot and replace recirculation motor generator set B1 speed limiter on January 5, 2019
(2) Elevated risk during reactor core isolation cooling testing and inoperability on January 8, 2019
(3) Elevated risk during emergency diesel generator maintenance on February 4, 2019
(4) Elevated risk during reactor core isolation cooling maintenance and testing on March 27, 2019

71111.15 - Operability Determinations and Functionality Assessments

Sample Selection (IP Section 02.02)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Reactor core isolation cooling operability evaluation after quarterly surveillance and replacement of flow controller (CR-2019-0145) on January 8, 2019
(2) Reactor core isolation cooling operability following flow oscillations (CR-2019-0802)on February 6, 2019
(3) Main steam isolation valve AO-203-1C input to reactor protection system past operability (CR-2019-0090) on February 20, 2019
(4) Control rod drive operability following scram pilot valve air header alarms (CR-2019-1783) on March 29, 2019

71111.18 - Plant Modifications

===Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Feedwater check valve, 6-CK-62B, clamp installation
(2) Main steam isolation valve 1C reactor protection system relay K3F

71111.19 - Post Maintenance Testing

Post Maintenance Test Sample (IP Section 03.01)===

The inspectors evaluated the following post maintenance tests:

(1) 'B' emergency diesel generator turbo air assist relay replacement post work testing on February 4, 2019
(2) Drywell to torus vacuum breaker AO-5045D relay replacement post work testing on March 14, 2019
(3) 'B' fuel pool pump, P210B, post work testing on March 18, 2019

71111.22 - Surveillance Testing

===The inspectors evaluated the following surveillance tests:

In Service Testing (IST) (IP Section 03.01)===

(1) 8.5.4.1 High pressure coolant injection operability and flow rate test on February 5, 2019 Surveillance Testing (IP Section 03.01) (4 Samples)===
(1) 8.5.5.1 Reactor core isolation cooling operability run on January 10, 2019

===(2) 8.M.2-1.5.10 High pressure coolant injection vacuum breaker isolation valve testing on February 5, 2019

(3) 8.5.1.1 Core spray operability surveillance on March 5, 2019
(4) 8.3.3 Scram discharge isolation volume vent and drain valve operability surveillance on March 21, 2019

71114.06 - Drill Evaluation

Emergency Preparedness (EP) Drill (IP Section 02.01)

The inspectors evaluated the conduct of a routine emergency planning drill on Wednesday, February 13, 2019.

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Contamination and Radioactive Material Control (IP Section 02.03)

The inspectors observed the monitoring of potentially contaminated material leaving the radiological controlled area and inspected the methods and radiation monitoring instrumentation used for control, survey, and release of that material. The inspectors selected several sealed sources from inventory records and assessed whether the sources were accounted for and were tested for loose surface contamination. The inspectors evaluated whether any recent transactions involving nationally tracked sources were reported in accordance with requirements.

High Radiation Area and Very High Radiation Area Controls (IP Section 02.05) (1 Sample)===

The inspectors reviewed the procedures and controls for high radiation areas, very high

===radiation areas, and radiological transient areas in the plant.

Instructions to Workers (IP Section 02.02) (1 Sample)===

The inspectors reviewed high radiation area work permit controls and use, reviewed

===electronic alarming dosimeter alarms and set points, observed worker briefings on radiological conditions, and observed containers of radioactive materials and assessed whether the containers were labeled and controlled in accordance with requirements.

Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section 02.06) (1 Sample)===

===The inspectors evaluated radiation worker performance with respect to radiation protection work permit requirements. The inspectors evaluated radiation protection technicians in performance of radiation surveys and in providing radiological job coverage.

Radiological Hazard Assessment (IP Section 02.01) (1 Sample)===

===The inspectors conducted independent radiation measurements during walkdowns of the facility and evaluated:

(1) The radiological survey program
(2) Changes to plant operations since the last inspection
(3) Recent plant radiation surveys for radiological work activities
(4) Air sampling and analysis
(5) Continuous air monitor use Radiological Hazards Control and Work Coverage (IP Section 02.04) (1 Sample)===

===The inspectors evaluated in-plant radiological conditions and performed independent radiation measurements during facility walkdowns and observation of radiological work activities. The inspectors assessed whether posted surveys; radiation work permits; worker radiological briefings and radiation protection job coverage; the use of continuous air monitoring, air sampling and engineering controls; and dosimetry monitoring were consistent 8 with the present conditions. The inspectors examined the control of highly activated or contaminated materials stored within the spent fuel pool and the posting and physical controls for selected high radiation areas, locked high radiation areas, and very high radiation areas.

71124.04 - Occupational Dose Assessment

External Dosimetry (IP Section 02.02)

The inspectors reviewed the current annual collective dose estimate; basis methodology; and measures to track, trend, and reduce occupational doses for ongoing work activities.

The inspectors evaluated the adjustment of exposure estimates, or re-planning of work. The

inspectors reviewed post-job ALARA evaluations.

Source Term Categorization (IP Section 02.01) (2 Samples)===

(1) The inspectors evaluated radiological work planning by reviewing significant work activities to verify that ALARA planning was integrated into work procedures and

===radiation work permit documents.

(2) The inspectors evaluated the licensee's characterization of the source term and use of scaling factors for the use of hard-to-detect radionuclide activity.

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) ===

For the period January 1, 2018 through December 31, 2018 BI02: RCS Leak Rate Sample (IP Section 02.11) (1 Sample)===

For the period January 1, 2018 through December 31, 2018 MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (1 Sample)

For the period January 1, 2018 through December 31, 2018

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03)

The inspectors reviewed the licensee's implementation of its corrective action program related to the following issues:

(1) Condition reports 2018-9566, 2019-0021, 2019-0078 and 2019-0302, Rod worth minimizer block action outside of design and subsequent inoperability
(2) Condition report 2016-2205, Boraflex neutron-absorbing panel degradation in the spent fuel pool 9
(3) Condition report 2018-0820, Target rock safety relief valve pilot assembly failed as-found lift test
(4) Condition report 2007-4079 and 2016-3672, Part 21 automatic voltage regulator for emergency diesel generators

71153 - Follow-up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following Licensee Event Reports (LERs) which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx

(1) LER 05000293/2018-003-00, Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, a Condition Prohibited by Plant Technical Specifications (ADAMS Accession No. ML18093A388). The circum stances surrounding this LER are documented in the Inspection Results section of the report.
(2) LER 05000293/2019-001-00, Reactor Core Isolation Cooling System Declared Inoperable During Surveillance Testing on March 5, 2019 (ADAMS Accession No.

ML19064A593). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. The inspectors also concluded that no violation of NRC requirements occurred.

(3) LER 05000293/2019-002-00, Failure of Main Steam Isolation Valve Limit Switch Results in a Condition Prohibited by Technical Specifications (ADAMS Accession No. ML19065A050). The circumstances surrounding this LER are documented in the Inspection Results section of the report.

INSPECTION RESULTS

Observation 71152 The inspectors performed a review of Entergy's evaluation and corrective actions associated with LER 05000293/2018-003-00, "Target Rock Relief Valve Pilot Assembly Failed As-Found Lift Test, A Condition Prohibited by Plant Techni cal Specifications." This LER, and the associated condition report, CR-PNP-2018-00820, evaluated and documented a main steam safety relief valve as-found lift setpoint test failure. Specifically, one of the four safety relief valves exceeded the technical specification tolerance limit of 1155 +/- 34.6 psig (+/- 3 percent) during routine testing at an offsite vendor's test facility. The setpoint drift has been attributed to "corrosion bonding" which involves bridging oxide buildup between the Stellite 21 pilot disc surface and Stellite 6 pilot valve body seating surface.

As documented in NRC Regulatory Issue Summary 2000-12, corrosion bonding is a known phenomenon in the nuclear industry that affects the 2-stage target rock safety relief valves. It characteristically results in the valve lifting at a higher pressure, failing to meet its setpoint criteria during the first lift attempt; but the affected safety relief valve typically lifts satisfactorily at its nominal setpoint during consecutive tests (after the corrosion bond is broken during the initial lift).

The inspectors evaluated Entergy's prioritization and timeliness of corrective actions to determine whether they were appropriately identifying, characterizing, and correcting problems associated with this issue, and whether the planned or completed corrective actions were commensurate with the safety significance. The inspectors determined Entergy staff 10 implemented corrective actions intended to impr ove safety relief valve performance, which included changing the pilot disc material to Stellite 6B with a platinum coating. This material is expected to reduce the likelihood of corrosion bonding. Previously (circa 2011), Entergy staff replaced the 2-stage safety relief valves with 3-stage target rock safety relief valves, in part, to address the corrosion bonding issue. However, operating experience with the 3-stage target rock safety relief valve at Pilgrim as well as other boiling water reactors, revealed an unrelated problem with the 3-stage safety relief valve design. In response, Entergy staff installed the 2-stage design during the Spring 2015 refueling outage pending a final resolution of the 3-stage safety relief valve design issue.

Relative to the one safety relief valve that did not meet test acceptance criterion, Entergy staff performed an evaluation of the as-found set pressures for all four safety relief valves and concluded no design or licensing basis limits would have been exceeded had the safety relief valves been required to operate. The inspectors reviewed the evaluation and did not identify deficiencies; the safety impact due to one safety relief valve being slightly out of tolerance was minimal.

During the refueling outage in which the four safety relief valves were removed for testing, Entergy staff replaced all four safety relief valves with those that were refurbished, certified, and tested (to within +/- 1 percent of 1155 psig as per TS 4.6.D.1). As stated above, Entergy provided a less susceptible material with platinum coating in an effort to prevent continued setpoint drift due to corrosion bonding.

The inspectors concluded Entergy staff implemented corrective actions consistent with industry and vendor initiatives to minimize the corrosion bonding issues. These corrective actions implemented industry and vendor recommendations and were commensurate with the safety significance of the issue. The Enforcement aspect of this issue is dispositioned below.

Observation 71152 The inspectors conducted inspection activities to follow up on Entergy's continuing corrective actions taken to address degraded Boraflex neutron absorption panels in the Pilgrim spent fuel pool. The NRC previously reviewed this issue and Entergy's prior corrective actions in 2017, as discussed in NRC Inspection Reports 05000293/2017001 (ADAMS Accession No.

ML17136A015) and 05000293/2017004 (ADAMS Accession No. ML18045A058).

Inspectors reviewed Entergy's logs for fuel moves taking place in 2018, documentation of the current spent fuel pool configuration, and a revised criticality analysis that was implemented by Entergy. Inspectors also discussed actions taken and the details of the criticality analysis with knowledgeable Entergy staff. Inspectors reviewed Entergy's administrative controls for managing criticality in the spent fuel pool to ensure that fuel moves and the current fuel configuration adhered to the established requirements. Additionally, inspector's reviewed Entergy's current plans for the eventual offload of all fuel in the spent fuel pool to dry cask storage.

Based on their review, the inspectors concluded that there is reasonable assurance that the reconfigured spent fuel pool provides sufficient margin to ensure that criticality will be maintained within regulatory limits in the spent fuel pool during and following the offload of the fuel currently in the reactor core into the spent fuel pool. Throughout 2018, Entergy took actions to unload a portion of the fuel from the spent fuel pool into dry-cask storage, and these actions introduced sufficient capacity into the spent fuel pool to safely conduct full 11 offload of the fuel currently in the core. This offload is planned to take place following the planned shutdown and permanent cessation of operations.

Target Rock Relief Valve Pilot Assembly Fa iled As-Found Lift Test, A Condition Prohibited by Plant Technical Specifications Cornerstone Severity Cross-cutting Aspect Report Section Not Applicable Severity Level IV NCV 05000293/2019001-01

Open/Closed

Not Applicable 71153 A self-revealed, Severity Level IV, NCV of TS 4.6.D.1, Safety and Relief Valves, was identified when Entergy was notified that the as-found lift setpoint of a safety relief valve (SRV) exceeded the technical specification (TS) tolerance limit of 1155 +/- 34.6 psig (+/- 3 percent) during routine testing at an offsite vendor's test facility. Specifically, the as-found lift setpoint of SRV, pilot serial number 1025, exceeded the maximum allowable TS value of 1189.6 psig by 7.4 psig.

Description:

On January 26, 2018, Entergy staff received results that an as-found setpoint test for one of the four main steam SRV pilot stage assemblies had exceeded the lift setting tolerance prescribed in TSs. Specifically, one of the four pilot stage assemblies tested experienced drift beyond the +/- 3 percent tolerance permitted by Technical Specification 4.6.D.1. The SRV had been in service the prior operating cycle. Entergy staff concluded that the cause of the setpoint drift was attributed to corrosion bonding between the pilot disc and seating surfaces. This condition was reportable under 10 CFR 50.73(a)(2)(i)(B) as any operation or condition which was prohibited by the plant's technical specifications.

Corrective Actions: Entergy staff replaced all four SRVs with those that were refurbished, certified, and tested (to within +/- 1 percent of 1155 psig as per TS 4.6.D.1). Entergy staff implemented additional corrective actions intended to improve SRV performance. Specifically, they changed the pilot disc material (Stellite 6B with a platinum coating), which is expected to be less susceptible to the corrosion bonding phenomenon.

Corrective Action Reference: CR-PNP-2018-00820

Performance Assessment:

The NRC determined this violation was not reasonably foreseeable and preventable by the licensee and therefore is not a performance deficiency.

The inspectors concluded Entergy staff implemented corrective actions consistent with industry and vendor initiatives to minimize the corrosion bonding issues. These corrective actions implemented industry and vendor recommendations and were commensurate with the safety significance of the issue.

Enforcement:

The ROP's significance determination process does not specifically consider the regulatory process impact in its assessment of licensee performance. Therefore, it is necessary to address this violation, which impedes the NRC's ability to regulate using traditional enforcement. Because there is no performance deficiency, and therefore no finding was identified, it is necessary to address this violation using traditional enforcement to adequately deter non-compliance. The inspectors reviewed the NRC Enforcement Policy, Section 2.2.1, "Factors Affecting Assessment of Violations", issued on May 15, 2018. Section 2.2.1 states, in part, that in determining the appropriate enforcement response to a violation, the NRC considers, whenever possible, risk inform ation in assessing the safety or security significance of violations and assigning severity levels. The inspectors also reviewed IMC 12 0609, Appendix A, "The Significance Determination Process for Findings At-Power," Exhibit 2, "Mitigating Systems Screening Questions," issued on June 19, 2012. The inspectors determined the issue to be of very low safety significance (Green) because it did not represent a loss of system or function because the SRV (pilot valve serial number 1025)remained capable of lifting to protect the reactor coolant system. As a result, the inspectors determined that the issue's significance was Severity Level IV.

Violation: TS 4.6.D.1 requires that all four SRVs shall be operable with a lift setpoint of 1155 psig +/- 34.6.

Contrary to the above, on January 26, 2018, Entergy staff identified that the as-found lift setpoint for one SRV (pilot valve serial number 1025) was measured above the TS 4.6.D.1 maximum allowable value. Because this discovery occurred after the valve was removed from service, Entergy determined that it was reasonable to conclude that while the valve had been installed, the lift setpoint was not within the TS required values, resulting in the valve being inoperable for a period of time in excess of the TS 4.6.D.1 allowed outage time for one SRV.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy. The ROP's significance determination process does not specifically consider violations without findings in its assessment of licensee performance. Therefore, it is necessary to address this violation using traditional enforcement to adequately deter non-compliance.

The disposition of this violation closes Licensee Event Report 05000293/2018-003-00.

Minor Violation 71153 Minor Violation: The failure to take actions in accordance with the time constraints required by Technical Specifications Table 3.1.1.

As described in Licensee Event Report 05000293/2019-002-00, Entergy identified that on January 3, 2019, operators did not place the associated reactor protection system logic channel in a tripped position within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> as required per technical specifications after the limit switch LS6 failed to open when main steam isolation valve 1C was closed.

Screening: The inspectors determined the performance deficiency was minor, because there was no impact to the main steam isolation valve closure scram function within the reactor protection system.

Enforcement:

This failure to comply with Technical Specifications Table 3.1.1 constitutes a minor violation that is not subject to enforcement action in accordance with the NRC's Enforcement Policy.

The disposition of this minor violation closes Licensee Event Report 05000293/2019-002-00.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 18, 2019, the inspector presented the quarterly resident inspector inspection results to Brian Sullivan and other members of the licensee staff.

14

DOCUMENTS REVIEWED

Inspection

Procedure Type Designation Description or Title Revision or

Date 71111.04 Drawings M212, Sh.1 Service Water System P & ID Revision 97 Miscellaneous 8.5.3.14 SSW Flow Rate Operability Test performed

3/19/19 Procedures 2.2.32 Salt Service Water System (SSW) Revision 97 71111.05Q Procedures 5.5.2 Special Fire Procedure Revision 59 EN-DC-161 Control of Combustibles Revision 19 71111.07A Engineering

Evaluations

WT-WTPNP-2017-0140 CA 34 Salt Service Water System Maintenance Rule (a)(1)

Evaluation

dated 8/16/17 Procedures 2.2.32 Salt Service Water System (SSW) Revision 98 5.3.3 Loss of All Service Water Revision 30 5.3.37 Loss of Spent Fuel Pool Cooling Event Revision 6 71111.11Q Procedures EN-OP-115 Conduct of Operations Revision 26 71111.12 Procedures EN-DC-205 Maintenance Rule Monitoring Revision 6 71111.13 Procedures EN-WM-104 On-line Risk Assessment Revision 18 71111.15 Procedures 2.2.92 Main Steam Line Isolation and Turbine Bypass Valves Revision 57 EN-OP-104 Operability Determination Process Revision 16 71111.18 Procedures EN- DC-115 Engineering Change Process Revision 26 EN- DC-136 Temporary Modifications Revision 18 71114.06 Procedures EP-AD-601 Emergency Action Level Technical Basis Document Revision 9 71152 Corrective Action Documents CR-PNP-2016-

205 CR-PNP-2018-

00565 CR-PNP-2018-

07519 CR-PNP-2018-

09458 CR-PNP-2018-

09459 CR-PNP-2018-

09461

Inspection

Procedure Type Designation Description or Title Revision or

Date Miscellaneous Engineering

Report ECH-NE-

19-00018 PNPS Fuel Storage Criticality Safety Analysis of Spent Fuel Storage Racks Utilizing Burnup Credit to Remove Boraflex

Credit Revision 0

ICA 2017- 45

through 2017-49

Item Control Area Transfer Forms

ICA 2018-03

through 2018-17

Item Control Area Transfer Forms

ICA 2018-27 Item Control Area Transfer Form

NA Diagram of current spent fuel pool configuration by criticality safety analysis fuel type, Cycle 22

generated

on February

28, 2019 Procedures PNPS 4.3 Fuel Handling Revision 140 71153 Corrective Action Documents

2019-0090

2019-0838