Safety Insp Rept 50-461/87-02 on 870518-0629.No Violations or Deviations Noted.Major Areas Inspected:Licensee Action on Previous Insp Findings,Review of Allegations,Ler Review & Followup & Monthly Maint ObservationML20235M853 |
Person / Time |
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Site: |
Clinton |
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Issue date: |
07/08/1987 |
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From: |
Knop R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
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To: |
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Shared Package |
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ML20235M838 |
List: |
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References |
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50-461-87-02-01, 50-461-87-2-1, NUDOCS 8707170350 |
Download: ML20235M853 (13) |
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Category:INSPECTION REPORT
MONTHYEARIR 05000461/19990191999-10-15015 October 1999 Insp Rept 50-461/99-19 on 990913-17.Noncited Violation Noted.Major Areas Inspected:Evaluation of Effectiveness of Aspects of Radiation Protection Program IR 05000461/19990141999-10-0101 October 1999 Insp Repts 50-461/99-14 & 50-461/98-12 on 990729-0908.Two Violations Occurred & Being Treated as Ncvs.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000461/19990131999-08-19019 August 1999 Insp Rept 50-461/99-13 on 990611-0728.Non-cited Violations Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support IR 05000461/19990101999-07-16016 July 1999 Insp Rept 50-461/99-10 on 990422-0610.Noncited Violations Identified.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000461/19990171999-07-0909 July 1999 Insp Rept 50-461/99-17 on 990607-11.No Violations Noted. Major Areas Inspected:Review of Access Authorization Program,Communications,Protected Areas Access Control of Personnel,Packages,Matl & Vehicles & Testing & Maint IR 05000461/19990121999-07-0707 July 1999 Insp Rept 50-461/99-12 on 990607-11.No Violations Noted. Major Areas Inspected:Evaluation of Effectiveness of Aspects of Chemistry & Radiation Protection Programs Including Quality Control of Lab & Inline Instrumentation IR 05000461/19990041999-05-0505 May 1999 Insp Rept 50-461/99-04 on 990301-0407.Non-cited Violations Noted.Major Areas Inspected:Effectiveness of Operators to Safely Operate Facility IR 05000461/19990011999-04-30030 April 1999 Insp Rept 50-461/99-01 on 990208-0325.Noncited Violation Noted.Major Areas Inspected:Operations,Maint & Plant Support IR 05000461/19990111999-04-30030 April 1999 Insp Rept 50-461/99-11 on 990408-21.Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000461/19990031999-04-21021 April 1999 Insp Rept 50-461/99-03 on 990208-0318.Eight Violations Occurred & Being Treated as non-cited Violations.Major Areas Inspected:Engineering Organization Effectiveness & Readiness for Restart Through in-depth Review of Calculations IR 05000461/19990061999-04-21021 April 1999 Insp Rept 50-461/99-06 on 990217-0407.Violations Noted.Major Areas Inspected:Operations,Maint & Engineering IR 05000461/19990081999-04-0909 April 1999 Insp Rept 50-461/99-08 on 990309-12.No Violations Noted. Major Areas Inspected:Licensee Performance During Exercise of Emergency Plan IR 05000461/19990071999-04-0101 April 1999 Insp Rept 50-461/99-07 on 990301-05.No Violations Noted. Major Areas Inspected:Review of Alarm Stations,Protected Area Detection & Assessment Aids IR 05000461/19980291999-03-24024 March 1999 Insp Rept 50-461/98-29 on 981214-990217.No Violations Noted. Major Areas Inspected:Review of Circumstances Surrounding High Number of Licensed Operator Failures That Occurred as Result of 1998 Annual Operator Requalification Exam IR 05000461/19990021999-03-18018 March 1999 Insp Rept 50-461/99-02 on 990107-0216.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering, & Plant Support IR 05000461/19990051999-03-10010 March 1999 Insp Rept 50-461/99-05 on 990208-12.Violation Noted.Major Areas Inspected:Evaluation of Effectiveness of Aspects of RP Program IR 05000461/19980281999-02-0101 February 1999 Insp Rept 50-461/98-28 on 981214-18.No Violations Noted. Major Areas inspected:follow-up Review of Licensee Program for Implementating 10CFR50.65,maint,quality Assurance Program & Engineering IR 05000461/19980201999-01-22022 January 1999 Insp Rept 50-461/98-20 on 981118-990106.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000461/19980271998-12-31031 December 1998 Insp Rept 50-461/98-27 on 981117-20.No Violations Noted. Major Areas Inspected:Licensee Performance During Exercise of Emergency Plan IR 05000461/19980181998-12-17017 December 1998 Insp Rept 50-461/98-18 on 981002-1117.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000461/19980261998-12-13013 December 1998 Insp Rept 50-461/98-26 on 981013-30.Violations Were Identified,But No Notice Was Issued.Major Areas Inspected: Engineering & Plant Support IR 05000461/19980191998-11-25025 November 1998 Insp Rept 50-461/98-19 on 980914-1009.No Violations Noted. Major Areas Inspected:Engineering IR 05000461/19980171998-10-30030 October 1998 Insp Rept 50-461/98-17 on 980819-1001.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000461/19980241998-10-29029 October 1998 Insp Rept 50-461/98-24 on 980921-1001.No Violations Noted. Major Areas Inspected:Review of Licensee Radiological Planning for ECC Suction Strainer Mod IR 05000461/19980251998-10-28028 October 1998 Insp Rept 50-461/98-25 on 981005-09.No Violations Noted. Major Areas Inspected:Portion of EP Program,Review of Documentation,Tours & Observations of Emergency Response Facilities & Equipment & Follow Up on Previous Findings IR 05000461/19980141998-09-17017 September 1998 Insp Rept 50-461/98-14 on 980707-0818.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000461/19980111998-08-0707 August 1998 Insp Rept 50-461/98-11 on 980527-0710.Enforcement Discretion Being Exercised for Six Violations Identified.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000461/19980131998-07-0808 July 1998 Insp Rept 50-461/98-13 on 980622-25.No Violations Noted. Major Areas Inspected:Effectiveness of Aspects of RP Program ML20236L3171998-07-0707 July 1998 Insp Rept 50-461/98-09 on 980504-08.No Violations Noted. Major Areas Inspected:Review of Documentation Re Actual EP Activation,Evaluation of Quality of EP Program Related Audits & Reviews & Effectiveness of Mgt Controls IR 05000461/19980081998-06-25025 June 1998 Insp Rept 50-461/98-08 on 980414-0528.Enforcement Discretion Has Been Authorized for Listed Violations.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000461/19980101998-06-0303 June 1998 Insp Rept 50-461/98-10 on 980511-15.Violations Noted.Major Areas Inspected:Plant Support IR 05000461/19980061998-05-11011 May 1998 Insp Rept 50-461/98-06 on 980304-0414.No Violations Noted. Major Areas Inspected:Aspects of Licensee Operations, Engineering,Maint & Plant Support ML20217F4611998-04-22022 April 1998 Insp Rept 50-461/98-07 on 980323-27.Violations Noted.Major Areas Inspected:Plant Support IR 05000461/19980031998-03-27027 March 1998 Insp Rept 50-461/98-03 on 980123-0303.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000461/19980041998-03-20020 March 1998 Insp Rept 50-461/98-04 on 980213-16.No Violations Noted. Major Areas Inspected:Operations & Maint ML20202H7541998-02-13013 February 1998 Insp Rept 50-461/97-25 on 971125-980122.Violations Noted. Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000461/19980021998-02-0202 February 1998 Insp Rept 50-461/98-02 on 980105-09.No Violations Noted. Major Areas Inspected:Plant Support Performance & Specifically Evaluation of Effectiveness of RP Program IR 05000461/19970241998-01-0202 January 1998 Insp Rept 50-461/97-24 on 971201-05.No Violations Noted. Major Areas Inspected:Plant Support Activities.Selective Elements of Access Authorization Program,Security Communication Sys & Testing Were Reviewed & Evaluated IR 05000461/19970231997-12-23023 December 1997 Insp Rept 50-461/97-23 on 971103-07.No Violations Noted. Major Areas Inspected:Findings & Conclusions from Insp of Licensed RO & SRO Requalification Training Programs ML20199A3941997-12-22022 December 1997 Insp Rept 50-461/97-22 on 971007-1124.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20198L2741997-12-22022 December 1997 Insp Rept for Clinton Power Station on 970923-1003 & 1020-31.Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support IR 05000461/19970181997-11-24024 November 1997 AIT Insp Rept 50-461/97-18 on 970805-18.Violations Noted. Major Areas Inspected:Circumstances Surrounding 970805 & 970722 RHR Pump a Circuit Breaker Failures at CPS IR 05000461/19970151997-11-12012 November 1997 Insp Rept 50-461/97-15 on 970707-0825.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20199A8771997-11-12012 November 1997 Insp Rept 50-461/97-19 on 970826-1006.Violations Noted.Major Areas Inspected:Operations,Maint,Engneering & Plant Support IR 05000461/19970141997-10-14014 October 1997 Insp Rept 50-461/97-14 on 970524-0707.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000461/19970201997-10-11011 October 1997 Insp Rept 50-461/97-20 on 970707-0829.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering & Maint IR 05000461/19970071997-09-29029 September 1997 Insp Rept 50-461/97-07 on 970313-0522.No Violations Noted. Major Areas Inspected:Licensee Operations & Surveillance Testing IR 05000461/19970171997-08-25025 August 1997 Insp Rept 50-461/97-17 on 970714-18 & 27-28.No Violations Noted.Major Areas Inspected:Review of Gaseous & Liquid Radwaste Programs Including Effluent Releases & Monitoring ML20151K0191997-07-25025 July 1997 Insp Rept 50-461/97-11 on 970407-0523.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support ML20149J5211997-07-15015 July 1997 Insp Rept 50-461/97-12 on 961209-970703.No Violations Noted. Major Areas Inspected:Review of Specific Commitments Licensee Made in Response to Confirmatory Action Ltrs Associated w/960905 Reactor Recirculation Pump Seal Failure 1999-08-19
[Table view] Category:NRC-GENERATED
MONTHYEARIR 05000461/19990191999-10-15015 October 1999 Insp Rept 50-461/99-19 on 990913-17.Noncited Violation Noted.Major Areas Inspected:Evaluation of Effectiveness of Aspects of Radiation Protection Program IR 05000461/19990141999-10-0101 October 1999 Insp Repts 50-461/99-14 & 50-461/98-12 on 990729-0908.Two Violations Occurred & Being Treated as Ncvs.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000461/19990131999-08-19019 August 1999 Insp Rept 50-461/99-13 on 990611-0728.Non-cited Violations Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support IR 05000461/19990101999-07-16016 July 1999 Insp Rept 50-461/99-10 on 990422-0610.Noncited Violations Identified.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000461/19990171999-07-0909 July 1999 Insp Rept 50-461/99-17 on 990607-11.No Violations Noted. Major Areas Inspected:Review of Access Authorization Program,Communications,Protected Areas Access Control of Personnel,Packages,Matl & Vehicles & Testing & Maint IR 05000461/19990121999-07-0707 July 1999 Insp Rept 50-461/99-12 on 990607-11.No Violations Noted. Major Areas Inspected:Evaluation of Effectiveness of Aspects of Chemistry & Radiation Protection Programs Including Quality Control of Lab & Inline Instrumentation IR 05000461/19990041999-05-0505 May 1999 Insp Rept 50-461/99-04 on 990301-0407.Non-cited Violations Noted.Major Areas Inspected:Effectiveness of Operators to Safely Operate Facility IR 05000461/19990011999-04-30030 April 1999 Insp Rept 50-461/99-01 on 990208-0325.Noncited Violation Noted.Major Areas Inspected:Operations,Maint & Plant Support IR 05000461/19990111999-04-30030 April 1999 Insp Rept 50-461/99-11 on 990408-21.Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000461/19990031999-04-21021 April 1999 Insp Rept 50-461/99-03 on 990208-0318.Eight Violations Occurred & Being Treated as non-cited Violations.Major Areas Inspected:Engineering Organization Effectiveness & Readiness for Restart Through in-depth Review of Calculations IR 05000461/19990061999-04-21021 April 1999 Insp Rept 50-461/99-06 on 990217-0407.Violations Noted.Major Areas Inspected:Operations,Maint & Engineering IR 05000461/19990081999-04-0909 April 1999 Insp Rept 50-461/99-08 on 990309-12.No Violations Noted. Major Areas Inspected:Licensee Performance During Exercise of Emergency Plan IR 05000461/19990071999-04-0101 April 1999 Insp Rept 50-461/99-07 on 990301-05.No Violations Noted. Major Areas Inspected:Review of Alarm Stations,Protected Area Detection & Assessment Aids IR 05000461/19980291999-03-24024 March 1999 Insp Rept 50-461/98-29 on 981214-990217.No Violations Noted. Major Areas Inspected:Review of Circumstances Surrounding High Number of Licensed Operator Failures That Occurred as Result of 1998 Annual Operator Requalification Exam IR 05000461/19990021999-03-18018 March 1999 Insp Rept 50-461/99-02 on 990107-0216.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering, & Plant Support IR 05000461/19990051999-03-10010 March 1999 Insp Rept 50-461/99-05 on 990208-12.Violation Noted.Major Areas Inspected:Evaluation of Effectiveness of Aspects of RP Program IR 05000461/19980281999-02-0101 February 1999 Insp Rept 50-461/98-28 on 981214-18.No Violations Noted. Major Areas inspected:follow-up Review of Licensee Program for Implementating 10CFR50.65,maint,quality Assurance Program & Engineering IR 05000461/19980201999-01-22022 January 1999 Insp Rept 50-461/98-20 on 981118-990106.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000461/19980271998-12-31031 December 1998 Insp Rept 50-461/98-27 on 981117-20.No Violations Noted. Major Areas Inspected:Licensee Performance During Exercise of Emergency Plan IR 05000461/19980181998-12-17017 December 1998 Insp Rept 50-461/98-18 on 981002-1117.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000461/19980261998-12-13013 December 1998 Insp Rept 50-461/98-26 on 981013-30.Violations Were Identified,But No Notice Was Issued.Major Areas Inspected: Engineering & Plant Support IR 05000461/19980191998-11-25025 November 1998 Insp Rept 50-461/98-19 on 980914-1009.No Violations Noted. Major Areas Inspected:Engineering IR 05000461/19980171998-10-30030 October 1998 Insp Rept 50-461/98-17 on 980819-1001.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000461/19980241998-10-29029 October 1998 Insp Rept 50-461/98-24 on 980921-1001.No Violations Noted. Major Areas Inspected:Review of Licensee Radiological Planning for ECC Suction Strainer Mod IR 05000461/19980251998-10-28028 October 1998 Insp Rept 50-461/98-25 on 981005-09.No Violations Noted. Major Areas Inspected:Portion of EP Program,Review of Documentation,Tours & Observations of Emergency Response Facilities & Equipment & Follow Up on Previous Findings IR 05000461/19980141998-09-17017 September 1998 Insp Rept 50-461/98-14 on 980707-0818.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000461/19980111998-08-0707 August 1998 Insp Rept 50-461/98-11 on 980527-0710.Enforcement Discretion Being Exercised for Six Violations Identified.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000461/19980131998-07-0808 July 1998 Insp Rept 50-461/98-13 on 980622-25.No Violations Noted. Major Areas Inspected:Effectiveness of Aspects of RP Program ML20236L3171998-07-0707 July 1998 Insp Rept 50-461/98-09 on 980504-08.No Violations Noted. Major Areas Inspected:Review of Documentation Re Actual EP Activation,Evaluation of Quality of EP Program Related Audits & Reviews & Effectiveness of Mgt Controls IR 05000461/19980081998-06-25025 June 1998 Insp Rept 50-461/98-08 on 980414-0528.Enforcement Discretion Has Been Authorized for Listed Violations.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000461/19980101998-06-0303 June 1998 Insp Rept 50-461/98-10 on 980511-15.Violations Noted.Major Areas Inspected:Plant Support IR 05000461/19980061998-05-11011 May 1998 Insp Rept 50-461/98-06 on 980304-0414.No Violations Noted. Major Areas Inspected:Aspects of Licensee Operations, Engineering,Maint & Plant Support ML20217F4611998-04-22022 April 1998 Insp Rept 50-461/98-07 on 980323-27.Violations Noted.Major Areas Inspected:Plant Support IR 05000461/19980031998-03-27027 March 1998 Insp Rept 50-461/98-03 on 980123-0303.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000461/19980041998-03-20020 March 1998 Insp Rept 50-461/98-04 on 980213-16.No Violations Noted. Major Areas Inspected:Operations & Maint ML20202H7541998-02-13013 February 1998 Insp Rept 50-461/97-25 on 971125-980122.Violations Noted. Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000461/19980021998-02-0202 February 1998 Insp Rept 50-461/98-02 on 980105-09.No Violations Noted. Major Areas Inspected:Plant Support Performance & Specifically Evaluation of Effectiveness of RP Program IR 05000461/19970241998-01-0202 January 1998 Insp Rept 50-461/97-24 on 971201-05.No Violations Noted. Major Areas Inspected:Plant Support Activities.Selective Elements of Access Authorization Program,Security Communication Sys & Testing Were Reviewed & Evaluated IR 05000461/19970231997-12-23023 December 1997 Insp Rept 50-461/97-23 on 971103-07.No Violations Noted. Major Areas Inspected:Findings & Conclusions from Insp of Licensed RO & SRO Requalification Training Programs ML20199A3941997-12-22022 December 1997 Insp Rept 50-461/97-22 on 971007-1124.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20198L2741997-12-22022 December 1997 Insp Rept for Clinton Power Station on 970923-1003 & 1020-31.Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support IR 05000461/19970181997-11-24024 November 1997 AIT Insp Rept 50-461/97-18 on 970805-18.Violations Noted. Major Areas Inspected:Circumstances Surrounding 970805 & 970722 RHR Pump a Circuit Breaker Failures at CPS IR 05000461/19970151997-11-12012 November 1997 Insp Rept 50-461/97-15 on 970707-0825.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20199A8771997-11-12012 November 1997 Insp Rept 50-461/97-19 on 970826-1006.Violations Noted.Major Areas Inspected:Operations,Maint,Engneering & Plant Support IR 05000461/19970141997-10-14014 October 1997 Insp Rept 50-461/97-14 on 970524-0707.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000461/19970201997-10-11011 October 1997 Insp Rept 50-461/97-20 on 970707-0829.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering & Maint IR 05000461/19970071997-09-29029 September 1997 Insp Rept 50-461/97-07 on 970313-0522.No Violations Noted. Major Areas Inspected:Licensee Operations & Surveillance Testing IR 05000461/19970171997-08-25025 August 1997 Insp Rept 50-461/97-17 on 970714-18 & 27-28.No Violations Noted.Major Areas Inspected:Review of Gaseous & Liquid Radwaste Programs Including Effluent Releases & Monitoring ML20151K0191997-07-25025 July 1997 Insp Rept 50-461/97-11 on 970407-0523.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support ML20149J5211997-07-15015 July 1997 Insp Rept 50-461/97-12 on 961209-970703.No Violations Noted. Major Areas Inspected:Review of Specific Commitments Licensee Made in Response to Confirmatory Action Ltrs Associated w/960905 Reactor Recirculation Pump Seal Failure 1999-08-19
[Table view] Category:INSPECTION REPORT
MONTHYEARIR 05000461/19990191999-10-15015 October 1999 Insp Rept 50-461/99-19 on 990913-17.Noncited Violation Noted.Major Areas Inspected:Evaluation of Effectiveness of Aspects of Radiation Protection Program IR 05000461/19990141999-10-0101 October 1999 Insp Repts 50-461/99-14 & 50-461/98-12 on 990729-0908.Two Violations Occurred & Being Treated as Ncvs.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000461/19990131999-08-19019 August 1999 Insp Rept 50-461/99-13 on 990611-0728.Non-cited Violations Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support IR 05000461/19990101999-07-16016 July 1999 Insp Rept 50-461/99-10 on 990422-0610.Noncited Violations Identified.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000461/19990171999-07-0909 July 1999 Insp Rept 50-461/99-17 on 990607-11.No Violations Noted. Major Areas Inspected:Review of Access Authorization Program,Communications,Protected Areas Access Control of Personnel,Packages,Matl & Vehicles & Testing & Maint IR 05000461/19990121999-07-0707 July 1999 Insp Rept 50-461/99-12 on 990607-11.No Violations Noted. Major Areas Inspected:Evaluation of Effectiveness of Aspects of Chemistry & Radiation Protection Programs Including Quality Control of Lab & Inline Instrumentation IR 05000461/19990041999-05-0505 May 1999 Insp Rept 50-461/99-04 on 990301-0407.Non-cited Violations Noted.Major Areas Inspected:Effectiveness of Operators to Safely Operate Facility IR 05000461/19990011999-04-30030 April 1999 Insp Rept 50-461/99-01 on 990208-0325.Noncited Violation Noted.Major Areas Inspected:Operations,Maint & Plant Support IR 05000461/19990111999-04-30030 April 1999 Insp Rept 50-461/99-11 on 990408-21.Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000461/19990031999-04-21021 April 1999 Insp Rept 50-461/99-03 on 990208-0318.Eight Violations Occurred & Being Treated as non-cited Violations.Major Areas Inspected:Engineering Organization Effectiveness & Readiness for Restart Through in-depth Review of Calculations IR 05000461/19990061999-04-21021 April 1999 Insp Rept 50-461/99-06 on 990217-0407.Violations Noted.Major Areas Inspected:Operations,Maint & Engineering IR 05000461/19990081999-04-0909 April 1999 Insp Rept 50-461/99-08 on 990309-12.No Violations Noted. Major Areas Inspected:Licensee Performance During Exercise of Emergency Plan IR 05000461/19990071999-04-0101 April 1999 Insp Rept 50-461/99-07 on 990301-05.No Violations Noted. Major Areas Inspected:Review of Alarm Stations,Protected Area Detection & Assessment Aids IR 05000461/19980291999-03-24024 March 1999 Insp Rept 50-461/98-29 on 981214-990217.No Violations Noted. Major Areas Inspected:Review of Circumstances Surrounding High Number of Licensed Operator Failures That Occurred as Result of 1998 Annual Operator Requalification Exam IR 05000461/19990021999-03-18018 March 1999 Insp Rept 50-461/99-02 on 990107-0216.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering, & Plant Support IR 05000461/19990051999-03-10010 March 1999 Insp Rept 50-461/99-05 on 990208-12.Violation Noted.Major Areas Inspected:Evaluation of Effectiveness of Aspects of RP Program IR 05000461/19980281999-02-0101 February 1999 Insp Rept 50-461/98-28 on 981214-18.No Violations Noted. Major Areas inspected:follow-up Review of Licensee Program for Implementating 10CFR50.65,maint,quality Assurance Program & Engineering IR 05000461/19980201999-01-22022 January 1999 Insp Rept 50-461/98-20 on 981118-990106.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000461/19980271998-12-31031 December 1998 Insp Rept 50-461/98-27 on 981117-20.No Violations Noted. Major Areas Inspected:Licensee Performance During Exercise of Emergency Plan IR 05000461/19980181998-12-17017 December 1998 Insp Rept 50-461/98-18 on 981002-1117.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000461/19980261998-12-13013 December 1998 Insp Rept 50-461/98-26 on 981013-30.Violations Were Identified,But No Notice Was Issued.Major Areas Inspected: Engineering & Plant Support IR 05000461/19980191998-11-25025 November 1998 Insp Rept 50-461/98-19 on 980914-1009.No Violations Noted. Major Areas Inspected:Engineering IR 05000461/19980171998-10-30030 October 1998 Insp Rept 50-461/98-17 on 980819-1001.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000461/19980241998-10-29029 October 1998 Insp Rept 50-461/98-24 on 980921-1001.No Violations Noted. Major Areas Inspected:Review of Licensee Radiological Planning for ECC Suction Strainer Mod IR 05000461/19980251998-10-28028 October 1998 Insp Rept 50-461/98-25 on 981005-09.No Violations Noted. Major Areas Inspected:Portion of EP Program,Review of Documentation,Tours & Observations of Emergency Response Facilities & Equipment & Follow Up on Previous Findings IR 05000461/19980141998-09-17017 September 1998 Insp Rept 50-461/98-14 on 980707-0818.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000461/19980111998-08-0707 August 1998 Insp Rept 50-461/98-11 on 980527-0710.Enforcement Discretion Being Exercised for Six Violations Identified.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000461/19980131998-07-0808 July 1998 Insp Rept 50-461/98-13 on 980622-25.No Violations Noted. Major Areas Inspected:Effectiveness of Aspects of RP Program ML20236L3171998-07-0707 July 1998 Insp Rept 50-461/98-09 on 980504-08.No Violations Noted. Major Areas Inspected:Review of Documentation Re Actual EP Activation,Evaluation of Quality of EP Program Related Audits & Reviews & Effectiveness of Mgt Controls IR 05000461/19980081998-06-25025 June 1998 Insp Rept 50-461/98-08 on 980414-0528.Enforcement Discretion Has Been Authorized for Listed Violations.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000461/19980101998-06-0303 June 1998 Insp Rept 50-461/98-10 on 980511-15.Violations Noted.Major Areas Inspected:Plant Support IR 05000461/19980061998-05-11011 May 1998 Insp Rept 50-461/98-06 on 980304-0414.No Violations Noted. Major Areas Inspected:Aspects of Licensee Operations, Engineering,Maint & Plant Support ML20217F4611998-04-22022 April 1998 Insp Rept 50-461/98-07 on 980323-27.Violations Noted.Major Areas Inspected:Plant Support IR 05000461/19980031998-03-27027 March 1998 Insp Rept 50-461/98-03 on 980123-0303.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000461/19980041998-03-20020 March 1998 Insp Rept 50-461/98-04 on 980213-16.No Violations Noted. Major Areas Inspected:Operations & Maint ML20202H7541998-02-13013 February 1998 Insp Rept 50-461/97-25 on 971125-980122.Violations Noted. Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000461/19980021998-02-0202 February 1998 Insp Rept 50-461/98-02 on 980105-09.No Violations Noted. Major Areas Inspected:Plant Support Performance & Specifically Evaluation of Effectiveness of RP Program IR 05000461/19970241998-01-0202 January 1998 Insp Rept 50-461/97-24 on 971201-05.No Violations Noted. Major Areas Inspected:Plant Support Activities.Selective Elements of Access Authorization Program,Security Communication Sys & Testing Were Reviewed & Evaluated IR 05000461/19970231997-12-23023 December 1997 Insp Rept 50-461/97-23 on 971103-07.No Violations Noted. Major Areas Inspected:Findings & Conclusions from Insp of Licensed RO & SRO Requalification Training Programs ML20199A3941997-12-22022 December 1997 Insp Rept 50-461/97-22 on 971007-1124.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20198L2741997-12-22022 December 1997 Insp Rept for Clinton Power Station on 970923-1003 & 1020-31.Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support IR 05000461/19970181997-11-24024 November 1997 AIT Insp Rept 50-461/97-18 on 970805-18.Violations Noted. Major Areas Inspected:Circumstances Surrounding 970805 & 970722 RHR Pump a Circuit Breaker Failures at CPS IR 05000461/19970151997-11-12012 November 1997 Insp Rept 50-461/97-15 on 970707-0825.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20199A8771997-11-12012 November 1997 Insp Rept 50-461/97-19 on 970826-1006.Violations Noted.Major Areas Inspected:Operations,Maint,Engneering & Plant Support IR 05000461/19970141997-10-14014 October 1997 Insp Rept 50-461/97-14 on 970524-0707.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000461/19970201997-10-11011 October 1997 Insp Rept 50-461/97-20 on 970707-0829.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering & Maint IR 05000461/19970071997-09-29029 September 1997 Insp Rept 50-461/97-07 on 970313-0522.No Violations Noted. Major Areas Inspected:Licensee Operations & Surveillance Testing IR 05000461/19970171997-08-25025 August 1997 Insp Rept 50-461/97-17 on 970714-18 & 27-28.No Violations Noted.Major Areas Inspected:Review of Gaseous & Liquid Radwaste Programs Including Effluent Releases & Monitoring ML20151K0191997-07-25025 July 1997 Insp Rept 50-461/97-11 on 970407-0523.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support ML20149J5211997-07-15015 July 1997 Insp Rept 50-461/97-12 on 961209-970703.No Violations Noted. Major Areas Inspected:Review of Specific Commitments Licensee Made in Response to Confirmatory Action Ltrs Associated w/960905 Reactor Recirculation Pump Seal Failure 1999-08-19
[Table view] Category:UTILITY
MONTHYEARIR 05000461/19900221990-11-0202 November 1990 Insp Rept 50-461/90-22 on 901015-19.Violation Noted But Not Cited.Major Areas Inspected:Radiation Protection Program During Refueling/Maint Outage ML20058A7541990-10-18018 October 1990 Insp Rept 50-461/90-20 on 900924-28.No Violations Noted. Major Areas Inspected:Chemistry Program,Including Procedures,Organization & Training,Reactor Sys Water QC Programs & QA & QC Programs in Labs IR 05000461/19900151990-08-0303 August 1990 Insp Rept 50-461/90-15 on 900723-27.No Violations Noted. Major Areas Inspected:Annual Emergency Preparedness Exercise Involving Followup on Licensee Actions on Previously Identified Items IR 05000461/19900111990-07-25025 July 1990 Safety Insp Rept 50-461/90-11 on 900512-0703.Violations Noted.Major Areas Inspected:Licensee Action on Previous Insp Findings,Operational Safety,Event Followup,Radiological Controls,Maint/Surveillance,Lers,Tmi Items & Meetings IR 05000461/19890281989-10-0404 October 1989 Insp Rept 50-461/89-28 on 890911-15.Violations Noted.Major Areas Inspected:Fire Protection Program,Including Review of Fire Protection Organization,Administrative Controls & Fire Protection Sys Surveillance Test Program IR 05000461/19890251989-08-18018 August 1989 Partially Withheld Physical Security Insp & Allegation Review Rept 50-461/89-25 on 890717-0802 (Ref 10CFR 73.21). Violations Noted.Major Areas Inspected:Security Program Mgt Effectiveness & Review of Allegations IR 05000461/19890241989-08-17017 August 1989 Insp Repts 50-461/89-24 on 890801-04.No Violations Noted. Major Areas Inspected:Radiological Protecction,Radwaste & Transportation Programs Including,Aspects of Licensee Operational Radiation Protection IR 05000461/19890221989-07-27027 July 1989 Insp Rept 50-461/89-22 on 890619-0721.No Violations or Deviations Noted.Major Areas Inspected:Startup Testing Activities Subsequent to Initial Refueling Outage,Areas of Core Performance & Nuclear Engineering IR 05000461/19890181989-07-18018 July 1989 Safety Insp Rept 50-461/89-18 on 890512-0707.Violations Noted.Major Areas Inspected:Previous Insp Findings,Onsite Followup of Written Repts,Allegation Followup,Operational Safety Verification & Monthly Maint Observation IR 05000461/19890211989-07-14014 July 1989 Insp Rept 50-461/89-21 on 890601-23.Violation Noted.Major Areas Inspected:Failure of Reactor Recirculation Pump B Seals & Subsequent Equipment Problems Which Occurred on 890601.Several Weaknesses Identified IR 05000461/19890201989-07-12012 July 1989 Insp Rept 50-461/89-20 on 890627-29.No Violations Noted. Major Areas Inspected:Annual Emergency Preparedness Exercise & Evaluation of 890601 Emergency Plan Activation IR 05000461/19890191989-06-23023 June 1989 Partially Withheld Safeguards Insp Rept 50-461/89-19 on 890206 & 0522-0607 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected:Mgt Support,Protected & Vital Area Barriers, Access Control - Personnel,Packages & Vehicles & Testing IR 05000461/19890231989-06-21021 June 1989 Enforcement Conference Rept 50-461/89-23 on 890614.Matters Discussed:Apparent Violation of 10CFR50.49,Paragraphs (F) & (G) Re Hydrogen Igniter Field Connections,Instrument Circuits Landed on Terminal Blocks in GE Instrument Racks IR 05000461/19890161989-06-14014 June 1989 Safety Insp Rept 50-461/89-16 on 890227-0303 & 890316-17.No Violations Noted.Major Areas Inspected:Followup on Allegation RIII-87-A-0027,involving Containment Integrity & Inservice Testing Program IR 05000461/19890141989-06-0808 June 1989 Insp Rept 50-461/89-14 on 890316-0530.Violations Noted.Major Areas Inspected:Licensee Action on Previous Insp Findings, Regional Request,Nrc Compliance Bulletin & Generic Ltr Followup & Monthly Maint Observation IR 05000461/19890171989-05-19019 May 1989 Insp Rept 50-461/89-17 on 890403-27.No Violations Noted. Major Areas Inspected:Field Alterations & Plant Mods & Dedication of commercial-grade Equipment for safety-related Applications IR 05000461/19890031989-05-10010 May 1989 Insp Rept 50-461/89-03 on 890123-26,0227-28 & 0313-0407. Violation Noted.Major Areas Inspected:Maint,Support of Maint & Related Mgt Activities IR 05000461/19890121989-04-14014 April 1989 Insp Rept 50-461/89-12 on 890301-03 & 31.No Violations or Deviations Noted.Major Areas Inspected:Verification That SSER6 Required Remote Shutdown Sys Mods Installed Prior to Startup from First Refueling IR 05000461/19890081989-04-0505 April 1989 Insp Rept 50-461/89-08 on 890127-0316.Violations Noted.Major Areas Inspected:Licensee Action on Previous Insp Findings, Followup of Info Notices & Regional Requests,Refueling Activities & Operational Safety Verification IR 05000461/19890131989-04-0404 April 1989 Insp Rept 50-461/89-13 on 890308-21.No Violations Noted. Major Areas Inspected:Allegation & Associated Issue Re Staffing Provisions for Emergency Response Organization at Plant IR 05000461/19890051989-04-0303 April 1989 Insp Rept 50-461/89-05 on 890119-0323.No Violations Noted. Major Areas Inspected:Review of Programs,Procedures, Observation of Work Activities,Data Review,Mod Activities & Licensee Action on Info Notice 88-003 IR 05000461/19890151989-03-28028 March 1989 Enforcement Conference Rept 50-461/89-15 on 890321.Matters Discussed:Apparent Violation Re Inadequate Licensee Action to Correct & Prevent Recurrence of Previously Identified Environ Qualification Deficiencies ML20236D6511989-03-16016 March 1989 Safety Insp Rept 50-461/89-06 on 890206-0303.Violation Noted:Failure to Perform Adquate Corrective Action on Kynar Butt Splices & Junction Boxes.Major Areas Inspected:Lers,Reg Guide 1.97 Commitments & Torque Switches IR 05000461/19890041989-03-10010 March 1989 Insp Rept 50-461/89-04 on 890103-06,10-20 & 0224.No Violations Noted.Major Areas inspected:fitness-for-duty Issue Involving Senior Manager,Including Adherence W/Licensee Procedures in Determining If Employee Fit IR 05000461/19880301989-02-15015 February 1989 Safety Insp Rept 50-461/88-30 on 881206-890127.Violations Noted.Major Areas Inspected:Licensee Action on Previous Insp Findings,Review of Info Notices & Preparation for Refueling & Refueling Activities IR 05000461/19880251988-10-21021 October 1988 Insp Rept 50-461/88-25 on 880926-1014.No Violations or Deviations Noted.Weaknesses Noted Re Training for non-operating Personnel Performing safety-related Activities.Major Areas Inspected:Generic Ltr 83-28 IR 05000461/19880261988-10-19019 October 1988 Insp Rept 50-461/88-26 on 880926-30.Violations Noted. Major Areas Inspected:Radiological Protection & Radwaste Mgt Programs,Including Organization & Mgt Controls,Internal Exposure Controls & Control of Radioactive Matls IR 05000461/19880201988-10-18018 October 1988 Insp Rept 50-461/88-20 on 880727-28 & 1018.Violations Noted. Major Areas Inspected:Followup on Allegation RIII-87-A-0027 IR 05000461/19880241988-10-0606 October 1988 Insp Rept 50-461/88-24 on 880114-16 & 19-20.No Violations Noted.Major Areas Inspected:Chemistry & Environ Radiological Monitoring Programs,Qa Program,Audits & Appraisals & Changes in Organization IR 05000461/19880211988-09-16016 September 1988 Safety Insp Rept 50-461/88-21 on 880810-0906.Violations Noted.Major Areas Inspected:Onsite Followup of Written Repts of Nonroutine Events,Operational Safety Verification,Monthly Maint & Surveillance Observation & Training Effectiveness IR 05000461/19880181988-08-30030 August 1988 Insp Rept 50-461/88-18 on 880707-28 & 0810-17.No Violations Noted.Major Areas Inspected:Allegations Made by Former Employees of Util Contractor,Employed During Const of Plant, Indicating That Certain Requirements of ASME Code Violated IR 05000461/19880171988-08-11011 August 1988 Insp Rept 50-461/88-17 on 880712-15.No Violations Noted. Major Areas Inspected:Radiological Protection Program & Related Allegations,Including Organization,Mgt Controls & Staffing & External Exposure Controls IR 05000461/19880191988-08-11011 August 1988 Partially Withheld Physical Security Insp Rept 50-461/88-19 on 880725-29 (Ref 10CFR73.21).Major Areas Inspected:Mgt Effectiveness Security Organization,Records & Repts,Testing & Maint,Keys & Combination & Safeguards Contingency Plan IR 05000461/19880141988-07-29029 July 1988 Insp Rept 50-461/88-14 on 880518-0706.Violations Noted. Major Areas Inspected:Action on Previous findings,10CFR21 Rept Followup,Info Notice Followup,Compliance Bulletin Followup & Operational Safety Verification IR 05000461/19880081988-06-17017 June 1988 Insp Rept 50-461/88-08 on 880424-28.No Violations, Deficiencies or Deviations Noted.Major Areas Inspected: Emergency Response Facility Appraisal,Reviews of Radioactive Release Assessment & Meteorological Info IR 05000461/19880091988-06-0808 June 1988 Insp Rept 50-461/88-09 on 880404-0518.No Violations Noted. Major Areas Inspected:Licensee Action on Previous Insp Findings & Onsite Followup of Written Repts of Nonroutine Events at Power Reactor Facilities IR 05000461/19880131988-05-31031 May 1988 Insp Rept 50-461/88-13 on 880427-29 & 0511-13.No Violations or Deviations Noted.Major Areas Inspected:To Determine Compliance W/Atws Rule,10CFR50.62,per Temporary Instruction 2500/20 (Module 25020) IR 05000461/19870271988-05-27027 May 1988 Insp Rept 50-461/87-27 on 870810-880429.No Violations or Deviations Noted.Major Areas Inspected:Followup on Allegation RIII-87-A-027 & Licensee Followup Actions to Violations & Unresolved Item Noted in Previous Insps IR 05000461/19880121988-05-18018 May 1988 Insp Rept 50-461/88-12 on 880425-27.No Violations, Deficiencies,Deviations,Exercise Weaknesses or Open Items Noted.Major Areas Inspected:Emergency Preparedness Exercise of Key Functions & Locations During Exercise IR 05000461/19880071988-05-17017 May 1988 Insp Rept 50-461/88-07 on 880321-0415.No Violations or Deviations Noted.Major Areas Inspected:Quality Verification Activities,Qc,Operations Surveillance & Conduct of Control Operations IR 05000461/19880041988-04-28028 April 1988 Insp Rept 50-461/88-04 on 880217-0404.Violations Noted. Major Areas Inspected:Licensee Action on Previous Insp Findings,Nrc Compliance Bulletin Followup,Operational Safety Verification & Training Effectiveness ML20151S9901988-04-21021 April 1988 Partially Withheld Annual Reactive Insp 50-461/88-11 on 880405-08 (Ref 10CFR73.21).Violation Noted.Apparent Noncompliance Noted.Major Areas Inspected:Review of Licensee Reported Security Event on 880404 IR 05000461/19880061988-04-21021 April 1988 Insp Rept 50-461/88-06 on 880314-18,28-31 & 0406.No Violations Noted.Major Areas Inspected:Mod Process & Associated Quality Verification Process & Followup of Previous Inspector Identified Problems IR 05000461/19880021988-04-13013 April 1988 Insp Rept 50-461/88-02 on 880115-0406.No Violations or Deviations Noted.Major Areas Inspected:Actions on Previously Identified Item & Review of Startup Test Results IR 05000461/19880051988-03-31031 March 1988 Safety Insp Rept 50-461/88-05 on 880224-26.No Violations or Deviations Noted.Major Areas Inspected:Solid Radwaste Program Including,Organization & Mgt Controls,Qualifications & Training,Solid Radwaste & Transportation Activities IR 05000461/19880031988-02-26026 February 1988 Safety Insp Rept 50-461/88-03 on 880111-0217.Violation Noted.Major Areas Inspected:Info Notice & Generic Ltr Followup,Onsite Followup of Written Repts of Nonroutine Events at Power Reactor Facilities & Operational Safety IR 05000461/19870391988-01-24024 January 1988 Insp Rept 50-461/87-39 on 871125-880111.Violations Noted. Major Areas Inspected:Licensee Action on Previous Insp Findings,Ie Bulletin Followup,Operational Safety Verification,Monthly Maint & Surveillance Observations IR 05000461/19870401988-01-0505 January 1988 Insp Rept 50-461/87-40 on 871208-09 & 16.No Violations, Deficiencies or Deviations Noted.Major Areas Inspected: Available Facility Space & Layout,Communication & NRC Computer Compatibility IR 05000461/19870351987-12-29029 December 1987 Insp Rept 50-461/87-35 on 871005-1120.Violations Noted.Major Areas Inspected:Qa Program Verification,Maint & Followup of Inspector Identified Problems IR 05000461/19870381987-12-22022 December 1987 Partially Withheld Physical Security Insp Rept 50-461/87-38 on 871130-1204 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected:Security Plan/Implementing Procedures, Security Organization & Program Audit & Physical Barriers 1990-08-03
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000461/19990191999-10-15015 October 1999 Insp Rept 50-461/99-19 on 990913-17.Noncited Violation Noted.Major Areas Inspected:Evaluation of Effectiveness of Aspects of Radiation Protection Program IR 05000461/19990141999-10-0101 October 1999 Insp Repts 50-461/99-14 & 50-461/98-12 on 990729-0908.Two Violations Occurred & Being Treated as Ncvs.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support ML20217J1361999-09-30030 September 1999 Notice of Violation from Investigation on 971028-980921. Violation Noted:During Jan 1997,QV Dept Discriminated Against Qv Inspector,For Having Engaged in Protected Activities ML20217J1481999-09-30030 September 1999 Notice of Violation from Investigation Conducted from 991028-980921.In Jan 1997,CH Tewksbury Engaged in Deliberate Misconduct That Caused Util to Be in Violation of 10CFR50.7 IR 05000461/19990131999-08-19019 August 1999 Insp Rept 50-461/99-13 on 990611-0728.Non-cited Violations Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support IR 05000461/19990101999-07-16016 July 1999 Insp Rept 50-461/99-10 on 990422-0610.Noncited Violations Identified.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000461/19990171999-07-0909 July 1999 Insp Rept 50-461/99-17 on 990607-11.No Violations Noted. Major Areas Inspected:Review of Access Authorization Program,Communications,Protected Areas Access Control of Personnel,Packages,Matl & Vehicles & Testing & Maint IR 05000461/19990121999-07-0707 July 1999 Insp Rept 50-461/99-12 on 990607-11.No Violations Noted. Major Areas Inspected:Evaluation of Effectiveness of Aspects of Chemistry & Radiation Protection Programs Including Quality Control of Lab & Inline Instrumentation PNO-III-99-028, on 990506,reactor Achieved Criticality Starting Up from Sept 1995 Outage.Region III Maintained Continuous Insp Coverage Throughout Restart Period.Info in Preliminary Notification Reviewed1999-05-28028 May 1999 PNO-III-99-028:on 990506,reactor Achieved Criticality Starting Up from Sept 1995 Outage.Region III Maintained Continuous Insp Coverage Throughout Restart Period.Info in Preliminary Notification Reviewed IR 05000461/19990041999-05-0505 May 1999 Insp Rept 50-461/99-04 on 990301-0407.Non-cited Violations Noted.Major Areas Inspected:Effectiveness of Operators to Safely Operate Facility IR 05000461/19990011999-04-30030 April 1999 Insp Rept 50-461/99-01 on 990208-0325.Noncited Violation Noted.Major Areas Inspected:Operations,Maint & Plant Support IR 05000461/19990111999-04-30030 April 1999 Insp Rept 50-461/99-11 on 990408-21.Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support ML20206G9821999-04-30030 April 1999 Notice of Violation from Insp on 990408-21.Violation Noted:Licensee,Despite Having Considered Issue Closed in Corrective Action Program,Failed to Correct Condition Adverse to Quality IR 05000461/19990031999-04-21021 April 1999 Insp Rept 50-461/99-03 on 990208-0318.Eight Violations Occurred & Being Treated as non-cited Violations.Major Areas Inspected:Engineering Organization Effectiveness & Readiness for Restart Through in-depth Review of Calculations IR 05000461/19990061999-04-21021 April 1999 Insp Rept 50-461/99-06 on 990217-0407.Violations Noted.Major Areas Inspected:Operations,Maint & Engineering IR 05000461/19990081999-04-0909 April 1999 Insp Rept 50-461/99-08 on 990309-12.No Violations Noted. Major Areas Inspected:Licensee Performance During Exercise of Emergency Plan IR 05000461/19990071999-04-0101 April 1999 Insp Rept 50-461/99-07 on 990301-05.No Violations Noted. Major Areas Inspected:Review of Alarm Stations,Protected Area Detection & Assessment Aids IR 05000461/19980291999-03-24024 March 1999 Insp Rept 50-461/98-29 on 981214-990217.No Violations Noted. Major Areas Inspected:Review of Circumstances Surrounding High Number of Licensed Operator Failures That Occurred as Result of 1998 Annual Operator Requalification Exam IR 05000461/19990021999-03-18018 March 1999 Insp Rept 50-461/99-02 on 990107-0216.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering, & Plant Support ML20204E6931999-03-10010 March 1999 Notice of Violation from Insp on 990208-12.Violtion Noted: Licensee Did Not Make Adequate Surveys to Assure Compliance with 10CFR20.1902(b) Requiring Posting of Each High Radiation Area with Signs Displaying Listed Words IR 05000461/19990051999-03-10010 March 1999 Insp Rept 50-461/99-05 on 990208-12.Violation Noted.Major Areas Inspected:Evaluation of Effectiveness of Aspects of RP Program IR 05000461/19980281999-02-0101 February 1999 Insp Rept 50-461/98-28 on 981214-18.No Violations Noted. Major Areas inspected:follow-up Review of Licensee Program for Implementating 10CFR50.65,maint,quality Assurance Program & Engineering IR 05000461/19980201999-01-22022 January 1999 Insp Rept 50-461/98-20 on 981118-990106.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support PNO-III-99-002, on 990106,partial Loss of Offsite Power Occurred.Power Lost to Rhrs,Normal Shutdown Cooling Sys & in Svc at Time of Event.Plant Three EDGs Started Automatically & Provided Power to Safety Sys.Power Restored to Rhrs Pump1999-01-0808 January 1999 PNO-III-99-002:on 990106,partial Loss of Offsite Power Occurred.Power Lost to Rhrs,Normal Shutdown Cooling Sys & in Svc at Time of Event.Plant Three EDGs Started Automatically & Provided Power to Safety Sys.Power Restored to Rhrs Pump IR 05000461/19980271998-12-31031 December 1998 Insp Rept 50-461/98-27 on 981117-20.No Violations Noted. Major Areas Inspected:Licensee Performance During Exercise of Emergency Plan IR 05000461/19980181998-12-17017 December 1998 Insp Rept 50-461/98-18 on 981002-1117.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000461/19980261998-12-13013 December 1998 Insp Rept 50-461/98-26 on 981013-30.Violations Were Identified,But No Notice Was Issued.Major Areas Inspected: Engineering & Plant Support IR 05000461/19980191998-11-25025 November 1998 Insp Rept 50-461/98-19 on 980914-1009.No Violations Noted. Major Areas Inspected:Engineering ML20155E7131998-10-30030 October 1998 Notice of Violation from Insp on 980819-1001.Violation Noted:On 980909,operator Responding to Alarming Annunciator on Area Radiation Monitoring Sys Did Not Announce Annunciator to Control Room Supervisor IR 05000461/19980171998-10-30030 October 1998 Insp Rept 50-461/98-17 on 980819-1001.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000461/19980241998-10-29029 October 1998 Insp Rept 50-461/98-24 on 980921-1001.No Violations Noted. Major Areas Inspected:Review of Licensee Radiological Planning for ECC Suction Strainer Mod IR 05000461/19980251998-10-28028 October 1998 Insp Rept 50-461/98-25 on 981005-09.No Violations Noted. Major Areas Inspected:Portion of EP Program,Review of Documentation,Tours & Observations of Emergency Response Facilities & Equipment & Follow Up on Previous Findings IR 05000461/19983011998-10-0909 October 1998 NRC Operator Licensing Retake Exam Rept 50-461/98-301(OL) Administered to One Applicant Requesting SRO License on 980831-0904.Applicant Passed Operating Retake Exam But Not Issued SRO License to Operate Plant IR 05000461/19980141998-09-17017 September 1998 Insp Rept 50-461/98-14 on 980707-0818.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support ML20237B1531998-08-11011 August 1998 Notice of Violation from Insp on 980521.Violation Noted:On 980119,individual Exited RCA Utilizing Point Other than Designated Areas W/O Obtaining Approval from Radiological Operations Supervisor IR 05000461/19980111998-08-0707 August 1998 Insp Rept 50-461/98-11 on 980527-0710.Enforcement Discretion Being Exercised for Six Violations Identified.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000461/19980131998-07-0808 July 1998 Insp Rept 50-461/98-13 on 980622-25.No Violations Noted. Major Areas Inspected:Effectiveness of Aspects of RP Program ML20236L3071998-07-0707 July 1998 Notice of Violation from Insp on 980504-08.Violation Noted: on 980213,ERDS Not Initiated within 1 H of Declaration of Alert & Only One Electrical Maint Personnel on Shift Trained & Assigned as Member of Emergency Response Organization ML20236L3171998-07-0707 July 1998 Insp Rept 50-461/98-09 on 980504-08.No Violations Noted. Major Areas Inspected:Review of Documentation Re Actual EP Activation,Evaluation of Quality of EP Program Related Audits & Reviews & Effectiveness of Mgt Controls IR 05000461/19980081998-06-25025 June 1998 Insp Rept 50-461/98-08 on 980414-0528.Enforcement Discretion Has Been Authorized for Listed Violations.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support ML20237E6641998-06-0505 June 1998 EN-98-044:informs Commission That NRC Intends to Exercise Enforcement Discretion & Not Issue Citation or Propose Civil Penalty for Four Violations of Maint Rule.Ltr Describing Action Will Be Issued on or About 980612 ML20248J8641998-06-0303 June 1998 Notice of Violation from Insp on 980511-15.Violation Noted: Between 980429 & 980513,control Rod Drive Filter Area on 712 Elevation of Turbine Building,Radiation Area W/Radiation Dose of 8 Mrem Per Hour,Was Not Posted W/Warning Sign IR 05000461/19980101998-06-0303 June 1998 Insp Rept 50-461/98-10 on 980511-15.Violations Noted.Major Areas Inspected:Plant Support IR 05000461/19980061998-05-11011 May 1998 Insp Rept 50-461/98-06 on 980304-0414.No Violations Noted. Major Areas Inspected:Aspects of Licensee Operations, Engineering,Maint & Plant Support ML20217F4431998-04-22022 April 1998 Notice of Violation from Insp on 980323-27.Violation Noted: Description of Facility in USAR Not Accurate in All Matl Respects ML20217F4611998-04-22022 April 1998 Insp Rept 50-461/98-07 on 980323-27.Violations Noted.Major Areas Inspected:Plant Support IR 05000461/19980031998-03-27027 March 1998 Insp Rept 50-461/98-03 on 980123-0303.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000461/19973131998-03-24024 March 1998 NRC Operator Licensing Exam Rept 50-461/97-313OL Conducted on 980126-0205.Exam Results:Exam Was Administered to Two RO & Seven SRO Applicants.Five SRO & Two RO Applicants Passed All Portions of Exam & Two SRO Applicants Failed ML20217D8511998-03-20020 March 1998 EN-98-014:informs Commission That NRC Will Exercise Enforcement Discretion Per Section VII.B.2 of Enforcement Policy & Not Issue NOV to Il Power Co for Several Violations Associated W/Loss of Shutdown Cooling Event on 980213 IR 05000461/19980041998-03-20020 March 1998 Insp Rept 50-461/98-04 on 980213-16.No Violations Noted. Major Areas Inspected:Operations & Maint 1999-09-30
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Inspection Report - Clinton - 1987002 |
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U. S. NUCLEAR REGULATORY COMMISSION
REGION III
Report No. 50-461/87020(PRP)
Docket No. 50-461 License No. NPF-62 Licensee: Illinois Power Company 500 South 27th Street Decatur, IL 62525 Facility Name: Clinton Power Station Inspection At: Clinton Site, Clinton, IL Inspection Conducted: May 18 through June 29, 1987 Inspectors: P. Hiland L. McGregor S. Ray J. McCormick-Barger R.C.[nop,ChiafCd /
Approved By:
Projects Section IB 7[I 7 Date j J
Inspection Summary ;
Inspection on May 18 through June 29, 1987 (Report No. 50-461/87020(DRP))
Areas Inspectet: Routine, unannounced safety inspection by the resident inspector and region-based inspector of licensee action on previous inspection findings; review of allegations; licensee event report review and followup; monthly maintenance observation; monthly surveillance observation; operational safety verification; engineered safety feature system walkdown; training effectiveness; onsite followup of events at operating reactors; startup test witnessing; and management meetin Results: Of the 11 areas inspected, no violations or deviations were identifie >
8707170350 070708 PDR ADOOK0500g1
, o DETAILS Personnel Contacted Illinois Power Company (IP)
- K. Baker, Supervisor - I&E Interface, Licensing and Safety (L&S)
- T. Camilleri, Manager - Scheduling Outage and Maintenance
- R. Campbell, Manager - QA
- W.Connell, Manager-NuclearStationEngineeringDepartment(NSED) '
- J. Cook, Assistant Manager - Clinton Power Station (CPS)
- J. Fertic, Director Quality Systems & Audits R. Freeman, Assistant Plant Manager, Maintenance
- W. Gerstner, Executive Vice President
- D. Hall, Vice President, Nuclear
- D. Holesinger, Assistant Manager - Startup E. Kant, Assistant Manager, NSED
- J. Miller, Manager, Scheduling & Outage Management J. Palchak, Supervisor - Plant Support Services
- J. Perry, Manager - Nuclear Program Coordination
- R. Schultz, Director, Planning & Programming
- F. Spangenberg, Manager - L&S P. Telthorst, Licensing and Safety
- E. Till, Director Nuclear Training J. Weaver, Director - Licensing
- J. Wilson, Manager - CPS
- R. Wyatt, Director-Nuclear Program Assessment Soyland/WIPC0
- J. Greenwood, Manager Power Supply Nuclear Regulatory Commission I,
- P. Hiland, Senior Resident Inspector, Clinton
- *#S. Ra,y, Resident Inspector, Clinton i
L. McGregor, Senior Resident Inspector, RIII
- B. Siegel, Licensing Project Manager, NRR
- R. Knop, Chief, Projects Section 1B
- W. Forney, Chief, Projects Branch 1, RIII
- Denotes those attending the management meeting on June 17, 198 * Denotes those attending the monthly exit meeting on June 29, 1987.
The inspector also contacted and interviewed other licensee and contractor personne l
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r 4 2. Licensee Action On Previous Inspection Findings (92701) (Closed)OpenItem(461/86074-01): Surveillance Procedur " Purpose" Section Referenced Incorrect Technical Specificatio l During the initial development of Clinton Power Station (CPS)
surveillance procedures, the referenced technical specification requirement satisfied by the procedure was based on the. draft Technical Specifications. Subsequent. revisions to the CPS Technical Specifications resulted in ' renumbering many surveillance j requirement The licensee established interim controls via a Plant Manager's 1 Standing Order (PMS0-039) that used a " Master" list of surveillance requirements (Technical Specification to procedure cross-reference)
to determine applicable Technical Specification LCOs due to a failed surveillance. During this report period, the licensee completed the necessary revisions to surveillance procedures'that had been identified as having incorrect references in the purpose sectio This item is close ;
No violations or deviations were identifie l I
3. Review of Allegations (99014)
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(Closed) Allegation (RIII-87-A-0063(#215)): Intimidation of Nuclear Station Engineering Department (NSED) Supervisin'g Engineer. .On May 4, i 1987, the inspector was informed by the licensee's Manager - Quality Assurance that an investigation was to be performed on an expressed !
concern of intimidation. On May 5, 1987, the individual alleging ;
intimidation discussed the details of the concern with the inspecto Concern
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l On April 30, 1987, during an engineering meeting.to discuss the disposition of Condition Report (CR) 1-87-03-014,:the concerned
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l individual perceived that a Director within the Nuclear Station j Engineering Department had been intimidating when attempting.to '
persuade the concerned individual to revise the disposition-to i CR 1-87-03-01 The perceived intimidation was verbal comments directed toward the concerned individua Review The inspector noted that the technical issues concerning Condition Report 1-87-03-014 had been initially discussed with the licensee on ,
about April 27, 1987, and are the subject of Unresolved ' Item 461/86015-01 (Reference: Inspection Report 50-461/87015, paragraph 10.b.).
During this report period, the licensee completed.their investigation of the intimidation concern. That investigation concluded that no i intimidation took place; however,.it was also concluded that the conduct
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f 1 of the NSED Director toward the NSED Supervising Engineer was not appropriate. The NSED Director was provided counseling from the Manager-NSED regarding his conduct when interacting with other employee The inspector interviewed eight personnel that had been interviewed by the licensee during the conduct of their investigation. Those interviews were conducted to verify the accuracy of the investigation report that was provided to the inspector. The inspector did not identify any discrepancies between the licensee's investigation report .
interviews and those conducted by the inspector. The consensus of the )
interviewed personnel was that the exchange was a heated argument and i did not intimidate them from performing their work in a quality manne Conclusion ,
The allegation was partially substantiated in that the licensee's investigation concluded that the conduct of the Director-NSED was'not appropriate. The disposition to Condition Report- 1-87-03-014 was not revised by the concerned individual based on the perceived verbal intimidation nor were the interviewed personnel intimidated by the incident. The concerned individual presented this issue to approp-riate licensee management (i.e. QA - Manager) who in turn initiated the investigation described above. This item is close No violations or deviations were identifie . Onsite Followup Of Written Reports Of Nonroutine Events At Power Reactor Facilities (92700)
For the LERs listed below, the inspector performed-an onsite followup j inspection'of the LER to determine whether response to the event was adequate and met regulatory requirements, license conditions, and commitments and to determine whether the licensee had taken corrective i actions as stated in the LE :
, (Closed) LER 87-014-00 (461/87014-LL) [ ENS No. 08050]: Automatic l Actuation of the High Pressure Core Spray System (HPCS) Due to L
Utility Control and Instrumentation Technician Erro :
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This LER was initially reviewed as documented:in Inspection Report 50-461/87015, paragraph 7.a.(8). At the time of that inspection, ;
this LER remained open pending the inspectors verification of training and revision to Clinton Power Station Maintenance Procedure i CPS No. 8801.12. " Local Mounted Instrument Valve Operation".
i l During this report period, the inspector verified through, review of l training records that maintenance department personnel had been ;
I provided training on this LER. In addition, the inspector verified i that CPS No. 8801.12 had been revised in revision 8,' dated April 23, 1987, to provide proper instructions for backfilling transmitters i prior to placing on service. Based on the above verification that l corrective actions as described in LER 87-014-00 had been completed, this item is closed.
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a < (Closed) LER 87-020-00 (461/87020-LL) [ ENS No. 8197]: ' Automatic Isolation of Reactor Water Cleanup System Due to High Differential Flow. Signal as a Result of Operator Erro 'l This LER was initially reviewed as documented in Inspection Report 50-461/87015, paragraph 7.a.(10). At the time of that' inspection, ]
this LER remained open pending the inspectors verification that Operating Procedure CPS No. 3002.01, "Heatup and Pressurization". g was revised and the training described in the LER was complete During this report period, the inspector verified through review of training records that operations department personnel had been provided training on this LER. In. addition, the inspector's review- .
of CPS No. 3002.01, revision 8, dated June 2, 1987, indicated that the changes identified in the LER had been incorporated. Based on the above verifications that corrective actions as described in LER :
87-014-00 had been completed, this item is close No violations or deviations were identifie . Monthly Maintenance Observation (62703)
Selected portions of the plant maintenance activities on safety-relate'd I systems and components were observed or reviewed to ascertain that~the activities were performed in accordance with approved procedures, regulatory guides, industry codes and standards, and that the performance of. the activities conformed to the technical specifications. Th inspection included activities associated.with preventive or corrective maintenance of mechanical equipment and systems. The following items were considered during these inspections: the: limiting conditions forL operation were met while components or systems were removed from service; approvals were obtained prior to initiating the work; activities were accomplished using approved procedures and were inspected as applicable; functional testing and/or calibration was performed prior to returning the components or systems to service; parts and materials that were used were properly certified; and maintenance of appropriate fire prevention, radiological, and housekeeping condition The inspector observed / reviewed the following work activities:
Maintenance Work Request N Activity C-49385 Hydrostatic Test of Reactor. Water Cleanup Train - A C-49863 Corrective Maintenance on Reactor Water Cleanup Train - B No violations or deviations were identifie , .
6. Surveillance (61726)
An inspection of inservice and testing activities was performed to ascertain that the activities were accomplished in accordance with applicable regulatory guides, industry codes and standards, and in conformance with regulatory requirement Items which were considered during the inspection included whether adequate procedures were used to perform the testing, test instruments-tion was calibrated, test results conformed with technical specifications and procedural requirements, and that tests were performed within the required time limit The inspector determined that the test results were reviewed by someone other than the personnel involved with the performance of the test, and that any deficiencies identified during the testing were reviewed and resolved by appropriate management personne The inspectors observed / reviewed the following activitie t Procedure N Surveillance / Test Activig CPS No. 9432.17 RWCU Area High Delta Temperature Channel Functional / Calibration CPS No. 9463.02 Suppression Pool Water Level Channel Calibration No violations or deviations were identifie . Operational Safety Verification (71707)
The inspector observed control room operations, attended selected pre-shift briefings, reviewed applicable logs, and conducted discussions ,
with control room operators during the inspection period. The inspectors !
verified the operability of selected emergency systems and verified tracking of LCOs. Routine tours of the auxiliary, fuel, containment, control, diesel generator, and turbine buildings and the screenhouse were conducted to observe plant equipment conditions including potential for fire hazards, fluid leaks, and operating conditions (i.e., vibration, process parameters, operating temperatures, etc). The inspector verified j that maintenance requests had been initiated for discrepant conditions '
observed. The inspector verified by direct observation and discussion l with plant personnel that security procedures and radiation protection i (RP) controls were being properly implemente During the report period, the licensee completed startup testing through Test Condition 1 (20% Reactor Power). Test Condition 2 with power levels up to 55% commenced on June 9, 1987. The licensee anticipated completion 3 of Test Condition 2 activities in early July followed by an eleven day operator training and/or evaluation period. Test Condition 3 with power levels up to 75% was anticipated to commence in late Jul No violations or deviations were identifie i 6 .
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8. Engineered Safety Feature System Walkdown' (7'1710)
The inspector performed a walkdown of the division'1 Low Pressure Coolant Injection (RHR) system during the report period to verify the system l status. At the time the walkdown was performed, the licensee had identified the division 1-Low Pressure Coolant' Injection rystem as an {
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operable Emergency Core Cooling. system meeting all the requirements of the plant's ' technical specification For the purpose of this walkdown, the inspector utilized the following system drawings and the checklists contained in the system operating procedure: I
! CPS No. 3312.01V0001, revision 5,-RHR Valve Lineup l CPS No. 3312.01E001, revision 5, RHR Electrical Lineup P&ID M05-1075, sheet 1, revision Z j For the inspection performed, the following. attributes were observed:
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System lineup procedures matched the plant drawing Valve and electrical switch / breaker positioning agreed with the lineup checklist Valves were-locked when require Equipment conditions appeared correct with no. evidence of damag Equipment and components were properly identifie Interiors of electrical and instrumentation cabinets were free of debris, loose material, uncontrolled jumpers, with no evidence of rodent Instrumentation was properly installed and functionin Lubrication was provided, where observabl Housekeeping was adequate and appropriate levels of cleanliness were being maintaine Support systems essential to. system actuation (Division I Shutdown Sersice Water and Division I Emergency Diesel) were operationa In conjunction with the above, the inspector reviewed the results of q current surveillance perfonoed on the LPCI-A system to verify technical ;
specification requirements were met. The following surveillance test results were reviewed:
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Surveillance N Title Frequency Test Date l CPS No. 9053.01 LPCI OPERABILITY CHECK Monthly 06/10/87 q (LPCI A/B)
CPS No. 9053.04 RHR (A/B/C) VALVE Quarterly 04/15/87~ j
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(Stroke Time)
OPERABILITY CHECKS 18 Months -
(Position Indication)
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CPS No. 9053.06 CONTAINMENT SPRAY SYSTEM 18 Months 11/12/86 FUNCTIONAL TEST CPS No. 9053.07 RHR PUMPS OPERABILITY Quarterly 04/11/87 The inspector concluded that the LPCI-(division 1) system was operable based on direct field observations of the above lineups and inspection attributes. In addition, the inspector's review of current surveillance tests for the LPCI system indicated the plant's technical specifications were being me No violations or deviations were identifie . Training (41400 & 41701)
The effectiveness of training programs for licensed and nonlicensed personnel were reviewed by the inspectors during the witnessing of the licensee's performance of routine surveillance, startup testing, maintenance, and operational activities and during the review of the licensee's response to events which occurred during the months of May/ June 1987. Personnel appearerj to be knowledgeable of the tasks being performed, and nothing was observed which indicated any ineffectiveness of trainin As discussed below in paragraph 11.b., the inspectors observed simulator training in preparation for a Loss of Offsite Power test (STP-31-1).
The training observed appeared to provide an effective simulation of the ,
expected test senari l i
No violations or deviations were identifie . Onsite Followup of Events at Operating Reactors (93702)
! General The inspector performed onsite followup activities for events which occurred during the inspection period. Followup inspection included one or more of the following: reviews of operating logs, procedures, condition reports; direct observation of licensee actions; and interviews of licensee personnel. For each event, the inspector reviewed one or more of the following: the sequence of actions; the functioning of safety systems required by plant conditions; licensee actions to verify consistency with plant procedures and license conditions; and attempted to verify the nature of the event. Additionally, in some cases, the inspector verified that licensee investigation had identified root causes of equipment malfunctions and/or personnel errors and were taking or had taken appropriate corrective actions. Details of the events and licensee corrective actions noted during the inspector's followup are provided in paragraph b. belo ,
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l b. Details (1) Automatic Scram Due To Feedwater Valve Failure [ ENS No. 08767]
At about 6:15 p.m. CDT on May 24, 1987, the licensee experienced an automatic scram signal when APRM neutron flux level reached the 40% power setpoint (Test Condition 1 l Setpoint). The cause for the increased neutron flux was a l failed open feedwater regulating valve that caused an increased I flow of feedwater to the reactor. This increased flow of '
feedwater resulted in neutron flux increase due to the cooling effect. At the time of this event the reactor plant was in i
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mode 1, operating at about 18% power (25% indicated due to APRM gain adjustment). In accordance with plant procedures, the shift supervisor declared an unusual event at about 6:17 due to the unanticipated reactor scram. -The unusual event was terminated at about 6:55 p.m. The licensee notified the NRC Operations Center of this event via the ENS at about 7:13 i CDT on May 24, 198 This event was similar to a manual !
reactor scram that was initiated on May 6, 1987, due to failure of the same feedwater regulating valve (reference: Event N ). However, the failure mechanism for the May 6 event appeared to be unrelated to the failure mechanism for-this even (2) ESF Actuation Due to Reactor Water Cleanup Isolation [ ENS No. 08887j At about 6:30 p.m. CDT on June 5,1987, the licensee experienced an ESF actuation when the Reactor Water Cleanup System (RT) isolated on high differential flow. At the time of event occurrence, the licensee was establishing feedwater flow to the Reactor Vessel. The pressure changes from the Feedwater System under low flow conditions were sensed by the Reactor Water Cleanup System as a high differential flow. During this event, the reactor plant was in mode 2, operating at less than 1% power. The licensee notified the NRC Operations Center of this event via the ENS at about 9:00 p.m. CDT on June 5, 198 (3) Inoperable Reactor Trip Function [ ENS No. 08889]
l At about 1:30 a.m. CDT on June 7,1987, the licensee identified three "normally open" instrument root valves that were close With these valves in the closed position, turbine first stage pressure signals were isolated from the Rod Control &
Inforniation System (RCIS) and the reactor protective system (RPS) logic. The RCIS system limits the " notch" movement of control rods when turbine first stage pressure is indicating greater than 20% rated thermal power. The RPS inserts an automatic reactor trip function on turbine stop valve closure or turbine control valve fast closure when turbine first stage pressure is indicating greater than 40% rated thermal powe _
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Immediate action of the licensee was to open the three root valves in accordance with the applicable valve lineup. At the time of this event, the licensee was in Test Condition 1 of their startup test program which had limited reactor power levels to a maximum of 20%. During this event, the reactor plant was in mode 1, operating at about 13% power. The licensee notified the NRC Operations Center of this event via the ENS at about 4:15 a.m. CDT on June 7, 198 (4) Reactor Water Cleanup Isolation [ ENS No. 09028]
At about 6:45 p.m. CDT on June 17, 1987, the licensee experienced an automatic isolation of the Reactor Water Cleanup System (RT) due to a spurious high temperature alarm. A RT heat exchanger room high temperature alarm was received in the main control room and the RT system isolated. However, RT temperature recorders did not indicate any abnormai reading In addition, a tour of the RT heat exchanger rooms by plant operators did not identify any abnormal temperatures. The licensee notified the NRC Operations Center of this event via the ENS at about 9:00 p.m. on June 17, 198 (5) Declaration of Unusual Event Due to Earthquake [ENSNo.08937]
At about 6:50 p.m. CDT on June 10, 1987, ground motion due to a seismic event was noted by the licensee. At the time of the event, the reactor plant was in Mode 1 operating at about 17%
powe Initial control room observations did not indicate any effects to plant systems or equipment. One EHC pump on the turbine throttle control skid did auto start at about 6:52 The licensee initially notified the NRC Operations Center of the event at about 7:45 p.m. via the ENS. At the time of initial notification, the event magnitude was unknown but believed to be small. Operations personnel completed an initial inspection of all accessible plant areas including the cooling lake dam by 11:56 p.m.; no abnormalities were identified. The licensee assembled cognizant engineering and quality personnel on site at about 10:00 p.m. to evaluate the magnitude of the event (as recorded on passive seismic plates)
and to conduct additional inspections of plant structure The inspection teams (comprised of engineers and QC) completed their walkdowns of accessible plant areas at about 3:00 a.m. on June 11; no abnormalities were identified. At about 3:30 June 11, the licensee notified the NRC Operations Center via the ENS of activities that had been performed. At about 3:45 a.m., the licensee completed initial analysis of the passive seismic plates and concluded that the acceleration setpoint for declaring an Unusual Event (0.02G) may have been exceeded. At about 4:00 a.m. June 11, the licensee notified the NRC Operations Center via the ENS that an Unusual Event was i
declared at 3:45 a.m. and terminated at 3:55 a.m. Throughout '
the licensee's investigation into the event, the reactor plant was maintained stable and planned testing was suspende .. _ _ _ _ _ _ _ _ _ _ _ _ _ _ .
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(6) Turbine Trip Due to Failure in EHC System At about 8:30 a.m. CDT on June 18, 1987, the licensee experienced a trip of the Main Turbine generator while operating at about 33% reactor power. The turbine trip was due to a failure in the hydraulic line connected to the #4 turbine control valve causing a loss of EHC system fluid and the subsequent turbine trip. At the time of event occurrence, the inspector was in the main control room observing plant operations. Plant operators responded to the event in accordance with operating procedures. Reactor plant systems responded as expected. A reactor trip did not occur for this event since first stage shell pressure was below the 40%
automatic trip setpoint. The licensee reduced reactor power to about 14% while repairs were being made. A previously planned design modification was implemented that installed flexible couplings at the point where the EHC hydraulic lines attach to the turbine control valve No violatio- or deviations were identifie . Startup Test Witnessing and Observation (72302) ; During the inspection period, the inspectors witnessed various portions of STP-19-1, " Core Performance" and STP-22-1, " Pressure Regulation", including establishment of prerequisites, procedure changes, updates to revision 1, and preliminary post performance analysis. The inspectors observed that test procedures of the latest revision were available and in use by all appropriate crew member Test crews were adequately staffed, sufficiently knowledgeable and their actions were properly coordinated. All test prerequisites and initial conditions were met or waived in accordance with test program requirements. Permanent plant ,
equipment and test equipment required by the procedures were in service and where necessary, were calibrated to a common time bas {
Technical Specification LC0 appeared to be adhered to at all time The inspector reviewed and concurred with the licensee's preliminary-evaluation that the level 2 acceptance criteria were satisfied for Section 7.0, " Core Thermal Power Procedures", and Section 8.0,
" Analysis". The performance of this test using the Backup Core Limits Evaluation Program (BUCLE), and in conjunction with data from STP-11-1, "LPRM Calibration" and STP-12-1 "APRM Calibration" was totally satisfactory. The inspector noted that core flow appeared to be lower than expected under present plant conditions. However, the lower flow indication did not affect the core performance
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The inspectors reviewed the " Pressure Regulator" test procedure and witnessed the 2, 7.5 and 10 psig step changes on channel "A" and the 10 psig step changes to channel "B". In all tests there was a l
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e 5 i slight drop in reactor water level and pressure, however, the plant systems returned to normal values within 1.5 to 2.5 minutes. The pressure and level oscillations were small in magnitude and quickly recovered to the setpoint value ,
, The inspectors witnessed the performance of STP-31-1, " Loss of Turbine Generator and Offsite Power". The inspectors verified that the test procedure of the latest revision was available and in use by all appropriate crew members. Technical Specification LCOs l appeared to be adhered to at all times. The inspectors noted that i shift supervisors directed both the test activities and the recovery from Loss of Offsite power in accordance with plant operating procedure In addition to the actual test performance, the inspector observed the pretest training conducted at the t,linton plant specific simulator. The inspectors also attended the pre-shift briefings i provided to the test crews. Both the simulator training and l pre-shift briefings appeared to be thorough and comprehensive.
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Throughout the conduct of this test and recovery, plant operators l responded in accordance with operating procedures and supervisory j l directio Plant systems appeared to respond as expected with only l l minor exception .
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Review of the test results will be conducted during a future inspection, l No violations or deviations were identified, i
12. Management Meeting (30702)
l On June 17, 1987, NRC management met with IP management at the Clinton Power Station to discuss the status of the facility, the licensee's Mon:hly Performance Monitoring Management Report and actions being taken i to enhance the licensee's performance. Key personnel attending this meeting are identified by (#) in paragraph 1 of this repor The licensee discussed plant operations to date and summarized significant events; the licensee discussed the status of their Maintenance Work Request (MWR) backlog; the licensee's response and evaluation of the June 10, 1987 seismic event was discussed; the '
licensee discussed their corrective action and operational monitoring program; and the licensee presented the status of their INP0 training accreditation progra NRC (Region III) management acknowledged the licensee's status and plans.
l 13. Exit Meetings (30703)
The inspector met with licensee representatives (denoted in paragraph 1)
throughout the inspection and at the conclusion of the inspection on June 29, 1987. The inspector summarized the scope and findings of the inspection activities. The licensee acknowledged the inspection findings.
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The inspector also discussed the likely informational content of the inspection report with regard to documents or processes reviewed by the inspectors during the inspection. The licensee did not identify any such documents / processes as proprietary.
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