ML20199A394

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Insp Rept 50-461/97-22 on 971007-1124.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20199A394
Person / Time
Site: Clinton Constellation icon.png
Issue date: 12/22/1997
From: Kozak T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20199A378 List:
References
50-461-97-22, NUDOCS 9801270205
Download: ML20199A394 (27)


See also: IR 05000461/1997022

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION lli

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Docket Nos:

50 461

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License flos:

NPF-62

Report No:

50 461/97022 (DRP)

Licensee:

lilinois Power Company

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Facility:

Clinton Power Gtation

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Location:

Route 54 West

Clinton, IL 61727

Dates:

October 7 - November 24,1997

Inspectors:

T.W. Pruett, Senior Resident inspector

K. K. Stoedter, Resident inspector

D. E. Zemel, Illinois Department of Nuclear

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Safety

Approved by:

Thomas J. Kozak, Chief

Reactor Projects Branch 4

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EXECUTIVE SUMMARY

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Clinton Pow:r St: tion

NRC Inspect'on Report No. 50-461/g7022 (DRP)

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This inspection included a review of aspects of licensee operations, engineering,

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maintenance, and plant support. The report covers a 7 week period of resident inspection.

Operations

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One example of nonconservative decision making was identified for not assessing

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the impact of shutdown risk due to reduced onsite electrical power availability.

Specifically, the Division ll Emergency Diesel Generator (EDG) was removed from

service for maintenance while the Division i EDG was inoperable due to silting of the

service water system (Section 01.1).

One example of a violation of Technical Specification (TS) 3.0.2 was identified due to

the failure to implement a TS Required Action. Specifically, between July 28 and

October 26,1997, an alternate method of decay heat removal was not verified within

one hour and every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> thereafter following the declaration of an inoperable

train of residual heat removal. Consequently, component cooling water remained

aligned to the "B" Reactor Water Cleanup Heat Exchanger even though the A"

Reactor Water Cleanup Heat Exchanger was being credited as the heat sink for the

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alternate decay heat removal source (Section 01.2).

NRC involvement was required for licensing personnel to recognize c 10 CFR Part

50.73 reportable condition involving the failure to verify an alternate method of decay

heat removal, an operation or condition prohibited by the plant's Technical

Specifications (Section 01.2).

Two weakness in the implementation of the corrective action program were

identified. The weaknesses involved downqrading the significance of a condition

report without supervisory review and operations, licensing, and corrective action

review board personnel not being familiar with significance criteria associated with

condition reports (Section 01.2).

Improvements were made in sampling of the Diesel Fuel Oil System following the

inspectors' identification that the fuel oil day tanks were inspected for water after

recirculating the day tank to the fuel oil stviage tank (Section 02.1).

The inspectors identified that the low level alarm setpoint for both the Division I and

til fuel oil day tanks were incorrectly stated in the corresponding annunciator

response procedures (Section O2.1).

Quality assurance identified several weaknesses in the adequacy and

implementation of the self assessment and maintenance ru!e programs. The audits

represented an improvement in the quality assurance organization's ability to perform

thorough and probing evaluations (Sections 07.1 and M7.1).-

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Ona cx:mpla of a vi l: tion of TS 3.0.2 was id:ntif. d du] to the f:ilur] to implement

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TS R:quir:d Action. Specific lly, cetions w;re not pursu:d to r:stora tho Division I

and ll electrical subsystems to an operable status, immediately on two separate

occasions. Corrective actions for the first occasion were narrow in focus in that they

failed to prevent recurrence (Section 08.1).

Operations personnel did not ensure that information needed to perform an

operability determination for over-greasing of 480V motors was provided in a timely

manner This demonstrated a lack of plant ownership and leadership by the

operations department and was inoicative of a weakness in the operability

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determination program (Section M8.1).

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Training provided to operations personnel did not include

systems which are

available to reduce containment pressure. Additionally, tho ... ~ s Mcy operating

procedures did not include all systems which may be beneficial in reducing

containment pressure. These omissions contributed to operations personnelin the

simulator main control room not taking ernergency operating procedure actiuns to

reduce cuntainment pressure using available plant systems (Section P1.1).

Maintenance

Work control procedures for outages did not provide guidance on evaluating risk

associated with the daily implementation of the outage schedule. This item will be

reviewed as part cf the NRC 0350 Panel oversight of licensee improvement

programs (Section 01.1).

One violation was identified due to the failure to provide controlled copies of vendor

manuals and instructions for measuring and test equipment. Operations personnel

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were not trained in the use of portable tachometers prior to using the tachometers in

the field (Section M1.2).

inconsistent guidance was provided in Procedure CPS 8170.06, " Maintenance

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Troubleshooting." Section 2.1.2 stated that the procedure may be used as guidance

when troubleshooting under a job stepped maintenance work request (MWR) while

Section 1.0 stated that the procedure should not replace or be used in addition to a

job stepped MWR (Section M1.3).

One violation was identified due to the failure to provide maintenance work

instructions for repairing safety related hydramotors as required by procedures.

Additionally, the use of a MWR with broad instructions instead of a procedure with

specific hydramotor repair and overhaul guidance was considered a weakness

(Section M1.4).

While problems were noted with the procedure for hydramotor work, it was

considered a positive step thu work was stopped on two occasions so that

procedural instructions could be modified.

The licensee's corrective actions in responso to a previously identified motor over

greasing issue were narrowly focused and untimely in that multiple departments

failed to recognize the potential generic implicat ons of the over greasing issue until

seven ueeks after the initial concem was identified (Section M8.1).

ErLoineerino

Although trending of equipment deficiencies was not actively performed in the past,

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the Cngineering dep;rtment was taking cction to identify cdv rse trends in cquipment

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perform:nce (S ction E1.1).

Plant Suppm1

A number of problems were identified with operator performance during the off hours

emergency exercise. Simulator main control room personnel failed to recognize a

loss of al! DC control power, did not attempt to restore the reactor core isolation

cooling system, did not initiate the standby gas treatment system as required by the

emergency operating procedures, did not effectively communicate priorities, and did

not perform periodic site wide announcements (Section P1.1).

During the drill, the shift supervisor / command authority did not consult with security

personnel to determine if an alternate response location should be established for

personnel in the emergency response organization. This was considered significant

in that the effectiveness of the emergency response organization could have been

signif;cantly compromised during an actual security threat event (Section P1.1).

1he shift supervisor's efforts to provide auditional supervisory oversight during the

exercise were prudent in that he recognized degrading command and control of

activities in the simulator control room and inserted himself in the decision making

processes (Section P1.1).

Performance in the technical support center during the off hours exercise was poor

in that personnel did not recognize when minimum manning reqtsirements were met,

did not ensure priorities for restorstion of plant equipment were communicated, did

not ensure field teams were accounted for, did not update status boards with

information regarding field teams and degraded equipment, did not adequately

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reference emergency operating procedt:res, and transmitted inaccurate information

concerning system availabiiity due to the use ofinformal communications (Section

P1.1).

Licensee drill observers did not critically assess performance during the off hours

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exercise in that several problems were either not recognized or were inappropriately

classified as positive attributes by evaluators (Saction P1.1).

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Report Details

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Summary of Plant SMigg,

The plant remained shut down throughout the inspection period. Significant work completed

included the removal of silt from the shutdown service water portion of the intake structure

and the refurbishment of Division 1 Westinghouse 4160V breakers,

i. Operations

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Conduct of Operations

01.1 Shutdown Risk Assessment

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IDIAcction Scope (71707)

The inspectors reviewed the licensee's assessment of shutdown risk for removing

the Division II Emergency Diesel Generator (EDG) from service on October 13,

1997, to parform maintenance. The inspectors also reviewed procedures related to

planning and scheduling of maintenance while shutdown including: Procedures CPS

1131.01, " Work Control Program;" CPS 1151.01, " Outage Management;" CPS

1151.02, ' Maintenance and Forced Outages;' CPS 1151.04, * Planned Outage

Scheduling;" CPS 1151.08, "Plannhg and Scheduling Department Organization and

Responsibilities;" and

CPS 1151.09. * Methodology for Outage Safety Reviews."

b.

Observations and Findinas

On October 3,1997, an independent evaluator identified that acceptance criteria did

not exist for sitt levels in the service water intake structure and that portions of the

intake structure had not been inspected for sitt. On October 10, the licensee

determined that the acceptance criteria for the maximum acceptable level of sitt in

the area of the shutdown service water system (SX) intake was four inches and that

the exact impact of excess silt on the SX system was unknown.

On October 13, the licensee determined that the area surrounding the Division 11 SX

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pump suction had silt levels from 412 inches deep. The area surrounding the

Division l SX pump suction was not inspected due to diver safety concems; however,

the licensee assumed the sitt levels were similar. The resolution of issues involving

the reliability of the SX system will be reviewed as part of the NRC Manual Chapter

(MC) 0350 Panel oversight of licensee improvement initiatives.

On October 13, the licensee removed the Division 11 EDG from service to perform

breaker maintenance even though they were aware of the degraded condition of the

SX system. -The planned duration of the maintenance interval was 4 5 days.

On October 14, the licensee declared both Division I and ll EDGs inoperablo but

available due to the inability to asses. the impact that sitting near the Division I and

ll SX pump suctions had on SX system performance and on continued EDG

operation.

On October 14, the inspectors questioned the Assistant Vice President / Interim Plant

Manager, the Planning and Scheduling Director, and the Assistant Plant Manager -

Operations to determine whether or not a shutdown risk assessment had been

performed prior to physically disabling the Division 11 EDG. The inspectors were

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concern d that th3 licens:e had not oveluat:d or d:v: loped a conting:ncy pl:n

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which would assure th:t d:f nse in d:pth was maintain:d for onsit3 slectrical power

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distribution giv:n tho d: grad:d condition of the SX syst:m, th) Division ll circuit

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breakers, and the Division I, ll, and IV battery chargers.

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The inspectors noted that the Assistant Vice President / Interim Plant Manager was

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unaware of the circumstances involving the removal of the Division ll EDG from

service and that the decision had been made by his direct reports. After becoming

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aware of the maintenance activity, the Assistant Vice President / Interim Plant

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Manager directed that the Division ll EDG be restored to service since adoquate

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defense in depta for maintaining an onsite electrical distribution division was not

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maintained

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The inspectors were informed by the Assistant Plant Manager - Operations and the

Planning and Scheduling Director that the decision to remove the Division ll EDG

was based on a desire to increase the reliability of the onsite electrical distribution

system oy completing breaker repair activities and to meet the intent of the TS

regarding immediate restoration of plant equipment. In addition, they believed that

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the Division I EDG remained available since it could be started if needed,

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The inspectors questioned operatio_ns and planning personnel to determine why the

Division i EDG could be considered available if the extent of the silting problem in

the SX system was unknown. Operations and planning personnel acknowledged

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that they had not fully evaluated the impact of sitting on long term operation of the

SX system and continued availability of the EDGs. The inspectors determined that

not assessing the impact of decreased onsite electrical power availability on

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shutdown risk prior to the removal of the Division 11 EDG from service was an

example of nonconservative decision making by operations and planning personnel.

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The inspectors reviewed several procedures regarding outage planning and

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scheduling, Of the six procedures reviewed, only one, Procedure CPS 1151.09,

provided substantial guHance on shutdown risk assessment and maintaining

dafense in depth. However, this procedure was intended to only be used during the

development of initial outage schedules and was not utilized during the day to day

iraplementation of maintenance activities. Planning and scheduling personnel stated

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that they had been narrowly focused during the developmont of outage procedures

and thN a review was in progress to improve the work control process.

Improvements in work control processes will be reviewed as part of the NRC MC 0350 Panel oversight of licensee improvement initiatives.

c.

Conclusions

One example of nonconservative decision making was identified for not assessing

the impact of reduced onsite electrical power availability on shutdown risk. Work

control procedures for outages did not provide guidance on evaluating risk

associated with the daily implementation of the outage schedule.

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-01 2 Loss of Confiouration Control for Altemate Shut Down Coolina

a.

Inspection Scope (71707)

- The inspectors reviewed the circumstances involving the October 26,1997, self

disclosing event regarding the alignment of the component cooling water (CCW)

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system to the "B" reactor water cleanup (RT) heat exchanger instead of the "A" RT

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heat exchanger Because the immediate operability of maintaining TS required

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alternate decay heat removal was addressed by the licensee, the inspectors waited

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until

Nov;mber 14, to revbw th3 issue in ord:r to asecrtain th3 cff;ctiv:nsss of rec:nt

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cheng:s in th3 license 3's cortcetivo action proccss.

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Observations and Findinos

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Misaligned CCW For Alternate Decay Heat Removal

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Between July 1 22,1997, alternate decay heat removal was maintained with CCW

aligned to the "B" RT heat exchanger. On July 22, the RT system was shutdown

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and isolated for an emergent reserve auxiliary transformer outage. On July 28, as

part of the RT system restoration, alternate decay heat removal was aligned to the

"A" RT heat exchanger. However, PCW was unknowingly maintained in service to

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the "B" RT heat exchanger.

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On October 26, operations personnel attempted to use the RT system for decay heat

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removal. However, its was identified that the reactor coolant flow was aligned to the

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"A" RT heat exchanger and the component cooling water flow was aligned to the "B"

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RT heat exchanger, Prior to the event, operations personnel believed that the CCW

system was aligned to the "A" RT heat exchanger. Operations ' ersonnel aligned

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CCW to the "A" RT heat exchanger and initlated condition re 'oc (CR) 1-97-10-495.

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The inspectors noted that between August 3, and October 2t,,1997, the "A" RT

system had been credited as an alternate method of decay heat removal pursuant to

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TS 3.4.10 which requires that with one or two residual heat removal (RHR) shutdown

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cooling subsystems inoperable, venfy an alternate method of decay heat removal for

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each inoperable RHR shutdown cooling subsystem within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and once per 24

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hours thereafter. TS 3.0.2 requires that upon discovery of a failure to meet a limiting

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condition for operation (LCO), the Required Actior6 of the associated Conditions

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shall be met. The inspectors determined "1at the required actions for verifying an

alternate decay heat removal method were not performed in that the licensee did not

vNfy the alignment of the CCW system to the "W RT heat exchanger. The failure to

implement the Required Actions of the associated Condition is a violation of TS 3.0.2

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VIO (50-461/97022 01).

Licensee Evaluation of the Event

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The shift supervisor initially classified CR 1 97 10-495 as 'other." Procedure

CPS 1016.01, " Condition Reports," defines "other" as an item which is not significant

but merits trending, investigation, and/or corrective action. On October 30, the

corrective action review board (CARB) reviewed the CR and raised the classification

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to *potentially significant," pending a review by licensing personncI for reportability

and operations personnel for potential programmatic deficiencies with valve lineups.

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"Potentially significant" is defined in Procedure CPS 1016.01 as an interim

classification used when additional information is required to clarify the significance

of the occurrence.

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- On November 3,liconsing personnel responded on the CR generic comment sheet

that,"the misalignment of CCW was not reportable because, while CCW was not

properly lined up to the "A" RT heat exchanger, the condition was recognizable by

operations and could have been corrected before TS limits were exceeded.

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Because this condition could have been recognized and corrected, this condition

alone could not have prevented the fulfillment of the RT system's safety function.

-Therefore the event was not reportable by the requirement of 10 CFR 50.73."

Because licensing personnel did not believe the item was reportable, they

recommended _ that the CR be downgraded to other,

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On Nov:mber 14, the inspect:rs questioned licensing personn:1 on the r: port bility

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of th3 failurq to v rify cn alt: mate d: cay h::t r:mov:1 method pursu:nt to 10 CFR

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Part 60.73(a)(2)(1)(B), an operction or co,,dition prohtait:d by tha pl:nt's TS. The

Director . Licensing stated that the reportability evaluation had been based on

whether or not there was a loss of safety function and not if a condition prohtbited by

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TS had occuned. Following the discussion with the inspectors, the Director -

Licensing stated that a licensee event report should have been submitted for the

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failure to provide an alternate method of decay heat removal for an inoperable RHR

subsystem. The inspectors noted that the required report to the NRC would likely

have not been made within 30 days without NRC involvement.

On November 12, operations personnel responded on the CR generic comment

sheet that,"the misalignment of CCW was an error in proper implementation of the

lineup for restoration of the system following the clearance of a tagout, not a

programmatic issue with valve lineups. The frequency of discovery of mispositioned

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valves versus the valve lineups has remained relatively constant sin':e 1994."

Operations personnel deterrnined that a generic problem did not exist with valve

lineups and recommended that the CR be downgraded to other.

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On November 18, the inspectors reviewed the licensee's investigation report

regarding the CCW system misalignment and noted that the investigator determined

that the misalignment occurred due to inadequate guidance in the system operating

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procedures. Based on discussions with operations personnel, the inspectors

- determined that the individual who provided the comments specified on the CR

generic comment sheet had not reviewed the investigation report. Additionally, the

CCW valves involved in the event had never been tagged as part of a clearance.

The inspectors also noted that the response to the potentially significant CR did not

receive a review by operations management. The inspectors considered not

providing a departmental supervisory review of recommendations to downgrade the

potentially significant CR to other a weakness in impleme-tation of the corrective

action program.

Procedurt CPS 1016.01, Appendix B, " Significance Criteria," provides criteria for

when a ',R is to be censidered "significant." The inspectors noted that the CCW

misangnment met two of the significance criteria which included: alignment errors

(such as valve mispositioning) that result in a failure or potential failure of equipment

to perform its intended function and conditions which result in a non routine report to

the NRC per

10 CFR Part 50.73. Significant CRs require that a root cause analysis and

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corrective action plan be developed and approved by the CARB The failure to

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identify the CCW misalignmut as a significant condition is an additional example of

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- a weakness in implementation of the corrective action program in that operations,

licensing, and CARB personnel were not aware of factors effecting the significance

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determination for CRs.

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Conclusions

One violation was identified for the failure to implement the Required Actions of the

associated Condition in that an alternate method of decay heat removal was not

verified within one hour and every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> thereafter following the declaration that a

train of RHR was inoperable. Two weakness in the implementation of the corrective

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action program were identified which involved the downgrading of the significance of

a condition report without supervisory review and operations, licensing, and

corrective action review board persontv not being familiar with significance criteria

associated with condition reports.

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NRC inv:lv: ment w:s r;quir:d f:r licensing personnel to rect,,

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50.73 r: portable conditi:n inv:lving th3 failuro to v:rify alt: mate acay neat r:mov 1,

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cn operation or condition prohibit:d by the plant's TS.

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Operational Status of Facilities and Equipment

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02.1

Inspection of Diesel Fuel Oil (DO) System (71707)

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The inspectors reviewed applicable documents related to the DO system and

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performed a system walkdown. The inspectors questioned the system engineer

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concerning checking for accumulated water in the day tanks following diesel

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ope % tion instead of before since the water in the day tank would not have time to

settle out of solution prior to performing the check. The system enginent agreed that

a more accurate assessment could be made if the check was performed prior to

starting the diesel and initiated comment control fomis to ensure that future checks

for accumulated water in the fuel oil day tank were perforrr.ed prior to starting the

diesel generator. The inspectors also identified that the low level setpoints for both

the Division I and lll DO storage tanks were incorrectly stated in annunciator

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response procedures CPS 5060.08, " Alarm Panel 5060 Annunciators Row 8," and

CPS 5064.05, ." Alarm Panel 5064 Annuncistors Row 5." Engineering personnel

documented the discrepancy in CR 1 97 11-062 and the procedures group was

notified of the error. No other concems were identified.

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Quality Assurance in Operations

07.1

Review of Self Assessment Proaram by Quality Assurance

a.

{ nip _getion Scope (7170D

The inspectors reviewed the audit results of a quality assurance evaluation of the

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self assessment program performed between September 29 and October 22,1997.

b.

Observations and Findinas

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Quality assurance (QA) determined that the CPS self assessment program was

ineffective in identifying and correcting deficiencies, that implementing procedures

were inadequate, and that the program had not been adequately implemented.

Based on the findings, the inspectors determined that the audit represented an

improvement in the QA organization's ability to perform thorough and probing

evaluations. Additional reviews to determine the effectiveness of the licensu's self

assessment program will be performed as part of the NRC MC 0350 Panel oversight

of licensee improvement initiatives.

c.

Conclusions

OA aantified several weaknesses in the adequacy and implementation of the self

assessment program. The audit represented an improvement in the QA

organization's ability % perform thorough and probing evaluations.

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Miscellaneous Operations issues (92901)

08.1

(Closed) LER 50-461/97-024: Improper implementation of immediate TS Action

Statements. On September 12,1997, a member of the independent safety

engineering group initiated CR 1-97-09-159 to document a potential TS

noncompliance because work associated with an immediate TS action statement

was stopped as part of a plant wide stand down.

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Tcchnical Specification S:ction 1.3 d; fin:s immediat:ly cs 'th] requir:d cetion

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should bc pursu:d without d: lay cnd in a controlled m:nn:r." Bas d upon this

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definition, the lic:nsco d:t:rmir.:d that tne work stopp:ge during the stand down did

not constitute a vhlation of TS since the stand down was initiated due to the staff's

inability to perform work in a controlled manner.

On October 1, the licensee determined that work to restore Westinghouse 4160V

breakers and the Division I and II AC bus electrical power distribution subsystems to

an operable status was not pursued immediately as required by TS 3.8.10,

" Distribution Systems Shutdown," Action A.2.4. Specifically, breaker work was

stopped from

August 30 through September 1,1997, in order for workers to observe a ho'iday

weekend. Members i plant management, operations, and work control failed to

recognize that the breaker work was bcing performed to comply with an immediate

action statement. CR 1 97 10-025 and LER 50 461/97-024 were generated to

document this event.

Corrective actions for this event included ensuring that site personnel were aware of

how to properly implement a lor g term immediate TS action statement,

communicating to plant schedulers and the work control team that activities

associated with immediate action statements should proceed without interruption,

and irnproving communications to ensure that both management and staff personnel

were aware of work that was being performed to comply with immediate action

statements. Only one corrective action, placing an article in the site wide newsletter,

remained to be completed after October 10,1997.

On October 27, the operations department initiated CR 1 97 10-481 when licensee

personnel identified that work on Westinghouse 4160V breakers was interrupted on

October 1213 due to improper priority being placed on work activities. Specifically,

the task manager for the breaker work al' owed maintenance personnel to stop

working on the breakers in order to provide additional time off even though there was

breaker work remaining to be performed. The task manager did not consult witri

operations personnel prior to making the decir.lon to stop the work, in addition, the

task manager did not understand that the breaker work was required to be pursued

without delay in order to comply with TSs 3.0.10 and 3.0.2.

On November 13, operations initiated CR 1 97-11 264 to document that work on the

Division i SX Room Cooling Coi! Cabinet was interrupted inadvertently due to the

failure to recognize that this work was being performed to comply with a TS

immediate action statement. Although 6 weeks had elapsed since the first example

of a failure to comp'y with an immediate action statement, some maintenance

personnel were unaware that actions related to immediate TS action statements

were required to be pursued without delay, When operations personnel identified

that work on the cooling coil cabinet had been stopped, they initiated actions to bring

additional workers in such that the work could be completed.

On November 17, licensee personnelinitiated CR 1 97 11-351 to document an

adverse trend regarding proper implementation of TS immediate action statements.

At the conclusion of the inspection period, the licensee was planning to perform a

detailed root cause analysis to determine the cause for the improper implementation

and to develop effective corrective actions.

TS 3.0.2 requires that upon discovery of a failure to meet an LCO, the Required

Actions of the associated Conditions shall be met. The immediate corrective actions

for the first event were narrow in scope in that they were unable to prevent

recurrence. Due to the repetitiveness of this issue, the failure to implement the

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Required Actions of the associ:ted Condition f;r TS 3.8.10 is the second cxample of

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o violation of TS 3.0.2.

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c.

Conclusions

One violation was identified for the failure to implement a TS Required Action in that

the licensee did not pursue a.tions to rettore the Division I and ll electrical

distribution subsystems to an operable status immediately. The actions taken in

response to an event identified on October 1 were narrow in scope in that they were

unable to prevent recurrence.

Il Maintenarig.g

M1

Conduct of Maintenance

M1.1 General Comments (61726 and 62707)

The inspectors observed or reviewed the following maintenance and surveillance

activities:

MWR D78136

Perform Repairs to Hydramotor

OFZVG104

MWR D81120

Tube Plugging on Main Control Room

Chiller 'A'

MWR D81501

Troubleshooting Main Contro! Room

Chiller "A"

Procedure CPS 6423.04

Determination of Diesel Fuel Oil Contamination

Procedure CPS 9071.01C001

Diesel Driven Fire Pump Weekly Op. Checklist

Procedure CPS 9080.12

Diesel Fuel Oil Transfer Pump Operability

Procedure CPS 9333.40

Division 1114610V Bus Undervoltage Relay Test

Procedure CPS 9431.12

APRM Channel Calibration

Procedure CPS 9981.01

Diesel Fuel Oil Samplirg and Analysis

M1.2 Performance of Diesel Driven Fire Pumo Testina

a.

Inip_fction_Sggpe (61726)

The inspectors observed the performance of Procedure CPS 9071,01C001, " Diesel

Driven Fire Pumps Weekly Operability Test Checklist."

b.

Observations and Findinas

Step 8.1.4.4 of Procedure CPS 9071.01 required the operator to ensure the engine

was idling at a pre-determined speed using a hand held tachometer. The operator

reviewed the vendor documentation provided with the hand held tachometer prior to

its use. When the inspectors asked why the operator needed to refer to the

documentation, the operator responded that he had not received formal training in

use of the device. Not training personnel on equipment used during the performance

of surveillan J testing was considered a weakness in the operator training program.

The inspectors questioned why a hand held tachometer had to be used instead of

the tachometer installed on the diesel engine. The operator stated that the installed

tachometer was known to be inaccurate so a hand-held device was always used.

The inspectors reviewed the MWR database to determine !f the inaccurate

tachometer had been identified on an MWR and determined that a corrective

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m: int:n:nce document for th3 installed tachomet:r did not cxist. Aft:r furth:r

discussions with operations personn:1, the inspectors learn:d that tho installed

t:chom:t:r was curr:ntly functioning properly. Howev:r, since th] install:d

tachometer had exhibited problems in the past, a decision was made to use a hand

held tachometer during the performance of this surveillance. The decision to use an

alternate tachometer instead of the tachometer installed on the engine demonstrated

operation's lack of confidence that this piece of equipment would properly perform.

10 CFR Part 50, Appendix B, Criterion VI, requires that measures be established to

control the issuance of documents, such as instructions, procedures, or drawings,

which prescribe all activities affecting quality. The inspectors noticed that the vendor

manual provided with the tachometer when it was issued from the measurement and

testing equipment (M&TE) check out area was not a controlled document. A review

of all other vendor manuals in the M&TE check out area determined that they

likewise were not controlled. The failure to ensure that vendor information is

controlled apprt,priately prior to distributing the information for use in the field is a

violation of 10 CFR Pad

Appendix B, L ..

n VI (VIO 50-461/97022-02).

c.

Conclusions

One violation was identifit. due to the fail'Jre to provide controlled copies of vendor

manuals and instructions for measuring and test . quipment. Operations personnel

were

not trained in the use of portable tachometers prior to using the tachometers in the

field and exhibited a hck of confidence in the installed tachometer due to previous

problems with the device.

M1.3 Troubleshootino of Safety Related Eauipment

a.

Inspection Scope (62707)

The inspectors observed electrical maintenance (EM) technicians during the

performance of troubleshooting on the oil pump for the "A" Main Control Room

HVAC Chiller. The procedures and MWR utilized by the EM technicians were

reviewed for adequacy and compliance with upper tier documents.

b.

Observations and Findinag

Through a review of the MWRk, the inspectors determined that it contained generic

steps such as " Troubleshoot control circuitry to determine cause for oil pump start..."

and " Troubleshoot oil pump and related system components ;o determine reason for

excess pump noise." No references to specific procedures for performing the

troubleshooting were noted and directions in the work package stated that the

package was to be returned to maintenance planning following identification of the

problem.

The inspectors were concemed about the lack of specific guidance provided to the

EM technicians in the work package. In d' ~1ssions with maintenance planning

personnel, the planners informed the inspectors that the appropriate way to perform

troubleshooting was with a job stepped MWR.

Procedure CPS 1029.01, " Preparation and Routing of Maintenance Work

Documents," Section 2.2.30, states that " Guidance on troubleshooting is found in

(Procedure)

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CPS 8170.06, ' Maintenance Troubleshooting'." The inspectors r;vhwed Procedure

CPS 8170.06 cnd found that th3 guidance on how to perform troubleshooting was

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inconsist:nt. For example, S:ction 2.1.2 of Proceduro CPS 8170.06 stst:d, "This

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procedure may be used as guidance when troubleshooting under a job stepped

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MWR. However, an MWR is not required...." Conversely, Section 1.0 stated, "It is

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not the intent of this procedure to replace or be used in addition to a job stepped

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MWR."

When the conflicting requirements found in Procedurs CPS 8170.06 were shown to

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maintenance planning personnel, the planners were no longer sure of the

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appropriate mechanism to use to develop and implement troubleshooting plans. ' The

maintenance planning supervisor stated that similar observations were recently made

and that corrective actions for this item were being formulated,

c.

Conclusions

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Procedure CPS 8170/.6 contained conflicting guidance on the use of MWRs to

perform troubleshcoting in that one section stated that the procedure was to be used

as guidance e w'er a jo' stepped MWR while another section stated that Procedure

CPS 8170.06 st suld n .t replace or be used in addition to a job stepped MWR.

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M1.4 P_qdormance of Maintenance on Hydramotor OFZVG104 - MWR D78136

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a.

Inspection Scope (62707)

1

The inspectors observed preventive and corrective maintenance on safety related

hydramotor OFZVG104 for the standby gas treatment system.

b.

Observations and Findinos

On October 21,1997, the inspectors reviewed MWR D78136 for repairing an oilleak

on Standby Gas Treatment System "B" Inlet Damper Hydramotor OFZVG104 and

procedure CPS 8452.04, "NH91 Hydramotor Actuator Maintenance," and determined

that the guidance provided in these documents was inconsistent. For example, the

MWR was job stepped to rework the hydramotor as needed. The job plan was

general and allowed the electricians to do steps they thought were necessary to

effect repairs to the hydramotor. Many job steps included phrasing such as "as

necessary" and "as required" to allow as much flexibility as possible. The inspectors

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noted that Procedure CPS 8452.04 contained specific repair and overhaul

instructions for hydramotors but was only included in the work package for reference.

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The inspectors were concemed that the use of broad statements such as "as

necessary" or "as required" could result in maintenance work being uncontrolled and

undocumented. The inspectors questioned maintenance planning personnel why the

MWR Job steps were broadly written when a current procedure contained specific

instructions for repairing the hydramotor. Maintenance planning personnel explained

that a broad approach was provided within MWRs whenever the planner was unable

to determine the exact repairs that needed to be performed. Procedure CPS

1029.01, " Preparation and Routing of Maintenance Work Documents," Section

8.2.6.5, stated "When partial performance of a procedure is required and the scope

of work is aqi known up front, the planner shall add a signature space for

maintenance supcrvision to specify and document in the MWR package the

section(s)/ steps of the procedure to be performed. - The signature space shall be

prior to the job' step whicn requires a partial procedure to be performed." The

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inspect:rs n:t:d that th3 signatura sp:ce w:s ngt previded on the MWR. Also, no

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partial proceduro or section st ps w:re stipulat:d to cff:ct repairs to th3 hydramotor.

The f:llur3 to prepare m:lat:nznce work documents as r quir:d by Procedura CPS

102g.01 is considered a violation of TS 5.4.1 (VIO 50-461/g7022-03).

Procedural instructions provided in procedure CPS 8452.04 were also weak causing

work to be stopped on two separate occasions. On the first occasion, the procedure

was revised to include instructions related to performing field calibrations for

hydramotors connected to ventilation dampers and to ensure propar hydramotor

position for coupling / uncoupling. Work was stopped a second time to add

axeptable tolerances to acceptance criteria because repeatable performance could

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not be obtained using the information provided in the procedure. Although the

procedural Instructions were not clear, it was considered a positive step that work

was stopped to have the procedure modified.

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c.

Conclusions

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On3 vhl: tion was identifi:d du3 to th3 fa' va to provida maint: nance work

instructions as required by procedure. The use of a maintenance work request with

broad instructions in9h]d of a procedure with specific repair and overhaul guidance

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was considered r rMkness.

M7

Quality Assurance 'n Maintenance Activitieu

M7.1 Review of Maintenance Rule Audit by Quality Assurance

QA performed a review between October 13 and 24,1997 of the implementation of

the maintenance rule program. The QA rev:ew identified that the maintenance rule

program was inadequate and that the implementation of the program was ineff6ctM

The ir.3pectors concluded that QA performed a thorough and probing evaluahn of

the maintenance rule program.

M8

Miscellaneous Maintenance lasues (92903)

M8.1 (Open) Notice of Violation 50-461/97019-04: Over-gressing of Division ill SX Pump

Lower Motor Bearing. The inspectors determined that the licensee's correct;ve

actions for this issue were narrowly focused and untimely. Following the September

18,1997, Identification of the over-greasing issue, engineering and maintenance

personnel developed immediate corrective actions to escertain the material condition

of the

Division lli SX pump motor. During the week of September 29,11 days after initial

discovery, additional meetings were held to develop a plan to address other

potentially over greased motors. However, the corrective action plan to address this

concern was not approved and the issue was not resolved in a timely manner.

Between October 25 and 27,4 weeks following the initial discovery, engineering

personnel evaluated the material condition of th6 Division I and ll SX pump motors

and determined that the motors should be inspected. However, no one identified the

need to consider the impact on additional motors greased in a similar manner until 6

weeks after initial discovery. The failure to identify and evaluate potential generic

impacts on safety related equipment demonstmted a lack of safety focus and a

significant deficiency in the implementation of the corrective action program,

improvements in tne corrective action program will be reviewed by the NRC MC 0350 Panel oversight of licensee improvement initiatives.

(,1 early November, licensee management placed an increased focus on restoring

Division I equipment to an operable status. On November 3, the inspectors noticed

that approximately 26 MWRs had been written and placed on the emergent work list.

The MWRs were to meggar several Division I motors to identify any winding

degradation due to over greasing. When the inspectors asked management why the

work was suddenly emergent when the condition was identified seven weeks earlier,

the inspectors were told that the work needed to be performed to restore Divisior I

operability.

The inspectors reviewed the November 4 work schedule and found that the 26

MWRs had been taken off the emergent work list. When the inspectors asked why

the work was no longer emergent, the Assistant Plant Manager - Operations and the

Director .- Planning and Scheduling stated that tha work no longer needed to be

completed on an emergent basis since determining the conditica of Division i 480V

motors was no longer a restraint to declaring Division I operable. The inspectors

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disagreed with this position since it appeared that the Division I motors were

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assumed ta be oper:ble without an cv:lu tion to support th] cpernbility d:cisi:n.

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B;tw::n Novemb:r 4 - 6 s v:ral lic:ns:3 meetings wera h:Id to d:t:rmhe th3

proper way to resolve the over greasing issue. On November 6, operations

personnel declared all 480V motors inoperable when they determined that the

motors could bc .'egraded due to potential over-gressing. Although operations

personnel were aware that the over gressing issue existed, they had not considered

the potential generic implications of the over-gressing and had waited to receive

additional information from the engineering staff prior to making an operability

decision. Due to ineffective communications engineeling and maintenance

personnel the information was not received until November 6. The failure to ensure

that information needed to pctform operability decisions is provided in a timely

manner demonstrated a lack of plant ownership and leadership by the operations

department.

On November 8, the Assistant Vice President / Interim Plant Manager decided that

numerous 480V motors on all safety related divisions would be opened and

inspected for signs of over-greasing. Although the licensee's current corrective

actions appeared appropriate, the initial untimely resolution of this issue and the

failure to fully communicate and understand the scope of work prior to beginning

work activities was considered a weakness in work control oversight.

111. Enaineerina

E1

Conduct of Engineering

E1.1

Trendino of Hydramotors

a.

Lnspection Scope (37551)

The inspectors reviewed the CR database and the equipment history list to

determine if hydramotor deficiencies were being appropriately tracked by

engineering. The inspectors also reviewed applicable procedures, preventive

maintenance tasks, vendor manuals, preventive maintenance history, and corrective

action requirements,

b.

Obseryptions and Findinas

On October 27,1997, the inspectors reviewed the CR database and determined that

six hydramotor deficiencies had been documented using the CR process in the past

2 years. In addition, the inspectors review of the equipment history list determined

that

53 hydramotor deficiencies had been identified in the last two years ouring the

performance of preventive maintenance tasks. When deficiencies were identified

during preventive maintenance, both maintenance and maintenance planning

personnel implemented a work document authorization (WDA) to complete the

necessary repairs and return the equipment to service.

The inspectors questioned the plant engineering group in an effort to determine why

the hydramotor deficiencies hSd not been classified as an adverse trend.

Engineering personnel explained that a trending organization had existed however,

the organization was disbanded due to re engineering and trending activities were

reassigned as a system engineer activity. Due to the work load of the system

engineers, trending was not being actively performed to determine if adverse trends

existed such that corrective actions could be determined,

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On S:pt:mber 19,1996, cngineering personn:I initiated CR 1 96 09 126 13

d:cument th:t th] cngin:: ring department w:s n:t activ:ly performing tr:nding

cctivitts d: scribed in Nuclear St: tion Engin:: ring Dep rtment Procedur] R.0,

" Equipment Failure Trending and Evaluation." Actions to resolve the CR were

delayed due to the need to complete higher priority work activities associated with

refueling outage - 6 and the need to create a position within the engineering

organization to begin trending equipment problems.

On May 27,1997, the engineering department began gathering MWRs, WDAs, and

surveillance failure histories from the last three years to perform an MWR failure

trend analysis. The results of the failure trend analysis were then used to detemline

if any equipment was exhibiting an adverse performance trend. On November 3,

1997, engineering completed the failure trend analysis and identified 40 potential

adverse trends including an adverse trend for hydramotors (see CR 1 97 11-481).

The inspectors reviewed the hydramotor items identified through the MWR failure

trend analysis and were concemed that hyrdamotor deficiencies were not included

when determining if an adverse trend existed. The inspectors discussed their

concern with engineering personnel and learned that plans were being considered to

trend equipment deficiencies after all the equipment failures were appropriately

identified and trended. At the conclusion of the inspection period, the remaining 39

potential adverse trends were being evaluated by the corresponding cognizant

engineer. Engineering personnel planned to documont any kjentified adverse trends

through the condition reporting process to ensure that the trends were appropriately

identified and corrected,

c.

Conclusions

Although trending of equipment deficiencies was not actively performed in the past,

the engineering department was taking action to idt niify adverse trends in equipment

performance such that the trends were appropriate,y identified and corrected.

IV. Plant Support

P1

Conduct of EP Activities

P1.1

Evaluq1lon of Off Hours Exercise

a.

Inspection Scope (71750)

The inspectors observed portions of an off hours emergency exercise in the

simulator and Technical Support Center (TSC) on October 15,1997. The response

of t'.: eecurity organization was not evaluated.

b.

Observations and Findinas

The event progression involved a loss of condensate resulting in a reactor trip.

Following the trip, saboteurs caused a loss of the Reactor Core Isolation Cooling

(RCIC) pump, a loss of the Division I and 11 DC buses, and a loss of service water,

No radiological consequences were includea in the drill scenario.

Simulator Control Room

Eight operations personnel were observed in the at the controls area of the simulator

within 5 minutes following the initiation of the drill. Because of the increase in

staffing, the line assistant supervisor (LASS) had difficulty maintaining effective

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comm:nd cnd contr:1 cf oper;t:r cetions. Specifically, discussions between

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oper; tors involving restor; tion cf cquipment cecurred without the kn:wledge of th]

LASS cnnunci: tor ccknowledgments were n:t altt:ys clearly communicat:d or

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acknowledged by the LASS, and the use of 3 way communicaticns and repeat backs

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were inconsistent.

The LASS performed frequent crew briefings which included a summary of the event

progression and current degraded plant equipment. However, the LASS did not

priontize the restoration of degraded equipment.

The Shift Supervisor appropriately classified the Unusual Event, Alert. and Site Area

Emergency, and ensured timely off site notifications were made. In addition, the

Shift Supervisor's additional guidance and mentoring to the LASS during the event

was good in that it aided in identification and assignment of personnel oarly in the

event.

As the Alert was declared due to a security comprise and the Site Area Emergency

was declared due to occupation of vital areas, the 'oectors questioned the Shift

Supervisor and emergency planning personnel as W vhy the Emergency Response

Organization (ERO) was dispatched to the site instead of an alternate location. The

Shift Supervisor stated that he had not considered an altemate response location nor

had he discussed the issue with the security organization. Emergency planning

personnel stated that had this been a real event, local authorities would have

responded and established road blocks to control access to the facility. The

inspectors noted that discussion of establishing road blocks was not performed

during the exercise. The failure to consider an alternate response location for ERO

personnel was considered significant in that the ability to maintain the emergancy

response functions could have been compromised if personnel were put in danger

during an escalating security event.

Operators demonstrated a lack of awareness olsystem failures and restoration.

Specifically, the simulator control room did not investigate the cause for he loss of

the RCIC system. The lack of a RCIC pump failure investigation was considered

significant in that only one safety related injection source (high pressure core spray)

remained available for maintaining reactor vessellevel.

Operators did not recognize a totalloss of Division I and 11 DC power for

approximately

20 minutes. The loss of DC power remained unrecognized even after operators

were unsuccessful in opening safety relief valves to maintain reactor pressure

control. The failure to recognize the loss of DC power was considered significant in

that indications and annunciators clearly signified that DC power had been lost. The

operators did not note that the inability to operate the safety relief valves was directly

related to a loss of control power.

Two unplanned actuations of plant components occurred when field teams restored

Division I and 11 DC power. During the restoration of Division i DC powcr, the

Division i EDG automatically staited when control power was re-energize 1 The

crew promptly secured the EDG because no cooling water was available due to the

loss of the service water systems fol lowing the explosion in the screen house. Even

though the crew knew DC power was being restored, they failed to recognize that

the EDG would automatically start, This failure was significant in that it

demonstrated a lack of awareness by the operators on the impact of system

restorations on plant operation.

Approximately 25 minutes later, the Division ll EDG automatically started when

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Division ll DC power w s restored. One) ag:in th3 simulator control room was

r;quir:d 13 securo th] EDG due to tha loss of s.trvice wat:r. The shift supervisor

st:t2d thet h3 was un:w ra that Division ll DC power w:s in th] process of being

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restored. This failure was significant in that operations personnel failed to take

compensatory actions to prevent the automatic statt of the Division ll EDG even after

they had recently been required to take mitigating actions for Division 1.

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Due to a loss of cooling water, containment temperature and pressure slowly

increased until the crew manually initiated containment spray at 2.2 psig in

containment. On October 18, the inspectors questioned the licensee to determine if

a mitigating action could have been taken prior to spraying down containment since

the operators had several indications to verify a radiological event was not in

progress. Operations personnelinitially responded that they were unaware of other

mitigating actions which could be taken.

The inspectors reviewed Emergency Operating Procedure (EOP) 6," Primary

Containment Control," and noted that for containment pressure, a requirement

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existed to " hold drywell and containment pressure to below 1.68 psig using the

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standby gas treatment system (SGTS)." The inspectors discussed the EOP

requirement with the Shift Supervisor and a licensed reacter operator and

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determined that the SGTS had not been initiated.

The inspectors discussed the usage of EOP 6 with emergency planning personnel

and two senior reactor operator instructors from the operations training group on

Octooer 23,1997. The instructors did not view the failure to initiate the SGTS as a

significant concern for the following reasons:

First, the crew tried to mitigate the pressure rise by attempting to restore

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chilled water to containment. This was viewed as acceptable by the

instructors since the loss of chilled water caused the temperature / pressure

rise and the initiation of SGTS only addressed the increased containment

pressure symptom. The inspectors noted that symptomatic based ECH are

intended to be worked concurrently and that while restoring chilled water was

a success path for contalnnient temperature, it did not alleviate the

responsibility of the operators to perform other tasks associated with pressure

reduction.

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S:cond, the instruct:rs stat:d th:t the Cffect the SGTS h:d en lowering

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cont:inment pressure b cimost useless wh;n you hav] cther pri:ritts.

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Specifically, the SGTS is a r;lativ:ly low flow system (apprcxim:t:ly 500 cfm)

on a large volume containment. Therefore, any pressure reduction achieved

would be minimal. The inspectors noted that the instructors did not have an

evaluation to support this position, and, if the impact was minimal, ad'iitional

guidance should be provided to the operators in the EOP.

The inspectors reviewed the EOP Technical Bases, Section 10, " Primary

Containment Control," and determined that the initial action taken to controi

drywell and containment pressure is thu used during normal plant operation-

burping the drywell and venting through SGTS. The first step in tne

drywell/ containment pressure branch thus provides a smocth transition from

general plant operating procedures to EOPs and ensures that normal

methods of primary containment pressure control are tried before more

complex actions. The inspectors determined that the instructors' opinions

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were inconsistent with the bases for the EOPs.

Third, the instructors stated that insufficient resources sere availab!e in the

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control room to initiate the SGTS and recover important BOP systems such

as station air and cocMg water. Additionally, their position was that initiating

the SGTS was a poor resource allocation since something else would have

suffered. The insWuctors believed that SGTS initiation was a time consuming

evolution which did not provide substantial benefit and therefore was not

worthy of allocating licensed operator resources. One of the instructors

stated that in the past 8 years of training operators he had not observed a

crew attempt to initiate the SGTS to decrease containment pressure.

The inspectors. were later informed by operations personnel that alignment of

the SGTS to containment requires approximately 6-10 minutes. Therefore,

the inspectom determined that the control room misapplied an additional

licensed RO resource by assigning him phone communications with the

operational support center (OSC) instead of EOP mitigating actions.

Additionally, the crew did not seek assistance of licensed ooerators which

were readily available in the OSC. The failure of the operating crew to seek

additional Isensed operator resources was considered significant in that it

hampered implementation of the EOPs. Training on seeking and use of

additional operator resources is an inspection Followup Item (IFI) 50-

461/97022-04.

On October 24,1997, the inspectors discussed the use of EOPs with senior licensee

management. Their preliminary review determined that the operator actions were

acceptable; however, an independent review would be performed to determine if the

EOPs were properly implemented. The licensee believed that the crew effectively

prioritized actions by attempting to restore containment pressure by pursuing

activities to reduce containment temperature w.d thd they ran out of resources to

align the SGTS. Additionally, the licensee stated that operations training may have

cciitributed to a mind set where operators believed that the SGTS was not effective

on pressure reduction.

On October 30,1997, the inspectors again discussed the staff's performance during

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the exercise with the Assistant Vice President. He acknowledged that the facility had

done a poor job training on the expectations for utilizing the SGTS, that problems

may exist with EOP 6 in that it does not specify all normal plant systems which could

be used to decrease containment pressure, and that his staff should have discovered

the issue prior to NRC involvement. The Assistant Vice President also stated that a

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t:chnical justific tion for not using th; SGTS could in provid:d; howev:r, it would

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not m ka up for tr;ining, confusion on tha usa of th] SGTS or othsr syst:ms, or

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poor pl:nning of cxp:ctations for drills.

The inspectors determined that the '9ilure to implement the EOPs for primary

containment control a significant cc1cem. Negative training was provided to

operators in that they were not exp.cted to implement the reqaired EOP actions for

initiating the SGTS, Additionally, EOP 6 was not adequate in that additional systems

were not specified for containment pressure reduction. The licensee's actions to

correct training on EOP 6 is an inspection Followup ltem IFl (50-461/97022-05).

Technical Support Center (TSC)

The inspectors observed activities in the TSC Oom prior to the arrival of the

emergency response organization until completion of the drill critique. The TSC met

the minimum staff manning requirements 59 minutes following the declaration of an

Alert. However, the TSC Director did not recognize that minimum staff manning

requirements were met until 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 22 minutes. At that time, a decision was

made to delay transfer of command authority from the simulator to the TSC until the

shift supervisor completed notifications for the upgrade to a Site Area Emergency.

The TSC assumed command authority at 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 29 minutes. The decision to

delay transfer of command authority was considered prudent by the licensee.

However, the transfer could have occurred prior to the upgrade to the Site Area

Emergency if the TSC had recognized minimum staffing had been achieved.

Three TSC briefs were performed during the drill. The briefing interval was based on

a 30-minute period without consideration for changing plant conditions or event

progression. The briefs summarized degraded conditions in the plant but did not

establish priorities for the restoration of plant equipment. Input from the various TSC

program areas was not obtained during the briefs. Consequently, various responses

to the event were developed without a coo dinated plan. For example, Division i DC

power was restored without the TSC kncwing a field team had been dispatched,

service water system status was improperly communicated, and the availability of

service water to RHR was incorrect.

Emergency Plan Implementing Procedures (EPIP) EC-03, "Notificatian of Unusual

Event," EC 04, " Alert, " and EC-05, " Site Area Emergency," each required periodic

status updates over the public address system until the emergency is terminated.

The inspectors noted that periodic site wide announcements informing personnel of

the event progression were not performed by either the simulator or the TSC.

EPIP EC-12. " Emergency Teams," required the OSC supervisor keep the station

emergency director advised of emergency teams status and progress. The simulator

dispatched non-licensed operators on several occasions without consulting with

either the TSC or the OSC. Therefore, the OSC supervisor and the site emergency

director were

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un::wara of the loc;ti:n of th3 non-licensed oper: tors, although non-lic:nsed

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operctors ara consid; rid fi;ld terms which r;quira tracking by tha OSC supervisor.

9

CPS Emergency Plan, Section 2.3.2.5, requhes eat the TSC emergency operations

supervisor assess and evaluate emergency conditions. The inspectors noted that

the EOPs were not referenced by TSC personnel until 51 minutes following

activation of the TSC. Evun then, the EOPs were only reviewed after prompting on

several occasions by the Illinois Department of Nuclear Safety representative. The

inspectors consideced the failure of TSC personnel to review EOPs a significant

concern in that assessment of plant status with regards to the EOPs was not

performed to support the operating crew.

EPIP FE-01, "TSC Operations," Section 4.5.2, requires that the TSC Administrative

Supervisor is responsible for displaying infon% tion on the key events and problem

board and ensuring the data remains accurate. The inspectors noted that status

boards were not updated in the TSC in a timely manner. Specifically, service water

status was added 44 minutes after the explosion in the screen house, secondary

containment data was not specified, field teams restored Division i DC power even

though they were listed as 'Torming," and RCIC was not listed on the major problem

board.

Drill Observer Comments

The inspectors reviewed post exercise entiques, logs, and written comments

provided by the drill observers in the TSC and simulator. One observer was

assigned to monitor control room activities. Positive attributes noted by the observer

in the simulator included: (1) the shift supervisor's oversight of the operating crew;

(2) quick classification of the emergency events; and (3) evacuation of non essantial

personnel. Negative attributes included: (1) recognition of the loss of DC power; (2)

not providing a reason for the NOUE and ALERT classifications when making

gatronics announcements;

(3) communications between the simulator and TSC/OSC; (4) receipt of a phone call

regarding the status of RCIC; (5) and not being prepared for automatic actuations.

No unsatisfactory grades were ass!gned to the crew performance in the simulator.

The inspectors noted that the simulator drill observers did not assess 3 way

communications, annunciator response, establishment of priorities by the LASS, the

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use of an attemate ERO location, the lack of RCIC restoration, or EOP 6 usage.

Given the number of unidentified issues, the inspectors determined that the observer

was either not sufficiently critical or that insufficient resources were used to provide a

meaningful assessment.

The TSC observers noted the following positive attributes: (1) delaying the transfer

of command and contiol from the simulator to the TSC; (2) control of emergency

repair teams; (3) three part communication; (4) communications between security

and the TSC; (5) brainstorming of ideas by engineering; and (6) following EOP

usage by the simulator. Negative attributes included: (1) response _to the TSC; (2)

use of logs; and (3) TSC staff briefings.

The inspectors noted that the TSC observeia did not assess a lack of prioritization of

issues, periodic announcements of event progression, and updating of status boards.

Additionally, the inspectors noted that the observers incorrectly viewed

communications, control of emergency repair teams, and EOP usage as positive

attributes.' Given the number of unidernified or misrepresented issues, the inspectors

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determined that the observers were not sufficiently critical to provide a meaningful

assessment.

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Ex:rci o Critiqu] R: port

.

"

On October 30,1997 th? licens73 issu:d tha final r: port for th] cft:r hours ex:rciso.

The report did not address the failure to attempt to restore RCIC or consider an

alternate location for the ERO. The report also did not assess the ability of the

evaluators to provide a critical evaluation of the exercise even though several

observations were missed (use of available licensed operator resources, EOP 6

usage, establishmant of priorities, site wide announcements, selection of an alternate

ERO location, RCIC restoration, EOP usage in the TSC, and updating of status

boards).

The report considered TSC usage of EOPs and control of repair teams as positive

even though members of ths TSC were prompted on several occasions to review the

EOPs and tracking of non-licensed operator field teams was inadequate.

c.

Conclusions

. Operator performance during the off hoss exercise was poor in that they failed to

recognize or attempt to restore degraded equipment, did not initiate the SGTS as

required by the EOPs, did not effectively communicate priorities, and did not perform

periodic site wide anrouncements. The Shift Supervisor's efforts to provide

additional supervisory oversight during the exercise were prudent.

Training provided to operations personnel and the failure to includ3 in training

systems which rnay be beneficial in reducing containment pressure in the EOPs

contributed to the operators not implementing EOP req" ired actions to control

containment pressure using available plant systems.

Performance in the TSC was rcarginal in that the TSC director did not recognize

minimum manning require. ants, priorities were not effectively communicated, field

teams were not controlled, status boards were not updated, EOPs were not

adequately referenced, and communications resulted in the transmission of

inaccurate information.

The licensee did not critically assess performance during the exercise in that several

observations were either not recognized or inappropriately classified as positive

attributes by evaluators.

V. Manaaement Meetinos

X1

Exit Meeting Summary

The inspectors presenteo the inspection results to members of licensee management at the

conclusion of the inspection period on November 25,1997. The licensee acknowledged the

findings presented. The inspectors asked the licensee whether any materials examined

during the inspection should be considered proprietary. No proprietary information was

identified.

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X3-

Management Meeting summary -

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On N:v:mber 14, members of tha NRC Clinton Ov;rsight Penel met with lilinils Power

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management to discuss the curre

status of several programmatic deficiencies. .The

_ program areas included; preventive maintenance, corrective actions, work control, quality -

assurance, and the development of the Plan for Excellence.-

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PERSONS CONTACTED

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Licenaee -

J. Cook, Senior Vice President

W. Romberg, Assistant Vice President

L. Wigley, Manager - Nuclear Station Engineering Department

R. Phares, Manager - Nunlear Safety and Performance Improvement

J. Palchak, Manager - Nuclear Training and Support

- G. Baker, Manager - Quality 6,:surance

.

'J Gruber Director - Corrective Action

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J. Place, Director - Plant Radiation and Chemistry

R. Joyce, Assistant Plant Manager - Maintenance

- M 1Lyon, Assistant P, ant Manager - Operations

~ J. Hale, Director - Planning & Scheduling

W. Bousquet, Director - Plant Support and Services

- J. Sipek, Director - Licensing

INSPECTION PROCEDURES USED

IP 37551:

Engineering Observations

IP 61728:

Surveillance Observation

IP 62707: -

Maintenance Observation

IP 71707:

Plant Operations

IP 71750:

Plant Support and Observations

a

IP 92901:

Followup - Operations

2

IP 92903:

Followup - Maintenance

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ITEMS OPENED, CLOSED, AND DISCUSSED.

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Ooened

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50-461/97022-01a,b VIO ' Failure to it,.slement required actions of the associated

condition as required t,y Technical Specification 3.0.2.

50-461/97022-02

VIO

Failure to control copies of M&TE vendor manuals used in

performance of work activities.

_ 50-461/97022-03

VIO . Failure to prepare maintenance work documents as required by

' procedure.

504 61/97022-04

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Training on seeking and use of additional operator resources.

50-461/97022-05

IFl

Correction of training on EOP 6.

Closed

50-461/97 024

LER -Improper Implementation of immediate Technical Specification

Action Statements.

Discussed

50-461/97019-04

VIO

Over greasing of Division lli SX Pump tower Motor Bearing.

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LIST OF ACRONYMS

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CARB Corrective Action Review Board

CCW Component Cooling Water

- CR

. Condition Report =

DO

' Diesel Generator Fuel Oil System

DRP ' Division of Reactor Projects

. EDG Emergency Diesel Generator

,

- EM

Electrical Maintenance -

' EOP Emergency Operating Procedure .

EPIP Emergency Plan implementing Procedure

.

ERO: Emergency Response Organization

~' LASS' Line Assistant Shift Supervisor

LCO Limiting Condition for Operation

- M&TE Measurement and Test Equipment

- MWR . Maintenance Work Request

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NRC ' Nuclear Regulatory Commission-

'OSC? Operations Support Center

. PDR Public Document Room

QA

- Quality Assurance .

RCIC Reactor Core Isolation Cooling System

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RHR Ret.idual Heat Removal System

<

RT

Reactor Water Cleanup

SGTS Standby Gas Treatment System

SSC . Structure, System, or Component -

SX.

- Shutdown Service Water System

TSC ~ ~ Technical Support Center

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WDA ' Work Document Authorization

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