ML20151K019

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Insp Rept 50-461/97-11 on 970407-0523.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support
ML20151K019
Person / Time
Site: Clinton Constellation icon.png
Issue date: 07/25/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20151J994 List:
References
50-461-97-11, NUDOCS 9708050306
Download: ML20151K019 (38)


See also: IR 05000461/1997011

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. U.S. NUCLEAR REGULATORY COMMISSION

REGION 111

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! Docket Nos: 50-461

License Nos: NPF-62

Report No: 50-461/97011 (DRP)

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Licensee: Illinois Power Company i

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Facility: Clinton Power Station

Location: Route 54 West

Clinton, IL 61727

Dates: April 7 - May 23,1997

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Inspectors: F.D. Brown, Acting Senior Resident

K.K. Stoedter, Resident inspector

R.A. Langstaff, Resident inspector

D.M. Chyu, Electrical Systems inspector

M. Parker, Senior Resident, Palisades

S. Ray, Senior Resident, Prairie Island

Approved by: Christopher G. Miller, Acting Chief, Branch 4

Division of Reactor Projects

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9708050306 970725

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PDR ADOCK 05000461

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EXECUTIVE SUMMARY

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Clinton Power Station

NRC Inspection Report 50-461/97011 (DRP) '

This inspection included aspects of licensee operations, engineering, maintenance, and

plant support. The report covers a 6-week period of supplemented resident inspection.

Ooerations

The NRC closely monitored the implementation of the current procedure adherence

and adequacy policy. Generalimprovement over previous performance was noted.

Prompt changes were made to procedures which could not be implemented as

written. (Section 01)

Operator turnovers usually covered the appropriate information. The inspectors

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observed an on-duty operating crew demonstrate a questioning attitude and

prudently avoid an unnecessary TS LCO entry. However, the inspectors identified

several examples of opportunity for improved performance. (Section 01.1)

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The inspectors identified that a non-licensed operator and a maintenance mechanic

were in the process of violating procedural steps during a surveillance on the

control room ventilation system. A potentially weak independent verification was

also identified by the inspectors. One violation was identified. (Section 01.2) l

The inspectors identified that the system drawing for the safety related diesel

generator ventilation system was incorrect and that breakers in safety MCCs were

mislabeled. This condition had existed since start-up, but had not been identified or

corrected by the licensee. (Section 02.1)

The inspectors identified that valves in the air start systems for all three Emergency

Diesel Generators (EDGs), and a valve in the fuel oil system for the Division lli EDG,

were not locked open as required by the licensee's locked valve program. One

violation was identified. (Section 02.3) l

Maintenance

The failure to adequately document and communicate the status of job conditions

resulted in maintenance induced damage to a containment isolation valve. One

violation was identified. (Section M1.3)

Operations and maintenance failed to establish and verify that plant protective logic

was in the appropriate condition which resulted in an inadvertent engineered safety

features actuation of the standby gas treatment system during performance of a

surveillance. One violation was identified. (Section M1.4)

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A controls and instrumentation techbician lifted leads not covered by the procedure

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and a runback of the "A" reactor recirculation flow control valve resulted. One

violation was identified. (Section M1. 5)

The licensee performed tests to determine the revision (identification) number for

three breakers before performing "as-found" functional tests. This preconditioning

resulted in potentially invalid test data. One violation was identified.

(Section M2.1)

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The inspectors noted apparent material condition problems with PosiSeal butterfly I

valves in service water systems, synch check relays in safety related breakers, and

lubricants in motor operated valves. The licensee focused on repairing the specific

problems, not on identifying repetitive or potential common mode failure

mechanisms, or on preventing reoccurrences. The inspectors were also concerned

that material condition problems identified on maintenance work requests received

limited review for generic implications. (Section M2.4)

The inspectors identified that the licensee procedure for controlling material which

could clog emergency core cooling system strainers in a post lost of coolant

accident environment was inadequate. After a slow initial response to this issue,

the licensee initiated actions to resolve the concem. The issue of degraded . ,

containment coatings had not been resolved at the end of the period. One violation l

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was identified. (Section M2.5)

Enaineerina

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The inspectors identified that the licensee failed to analyze or evaluate the potential

loads on safety related piping induced by temporary scaffolding during a seismic

! event. One violation was identified. (Section E1.1)  ;

The licensee identified a potentially generic concern associated with the seismic

qualification of circuit breaker cabinets when breakers are removed. The inspectors

considered the identification of this issue to have been indicative of a proactive l

safety consciousness. The implementation of a procedure to address this issue

was inadequate. The inspectors identified concerns with the licensee's stated

approach to assessing cabinet operability. (Section E1.2)

Plant Succort

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The inspectors observed an individual reaching into a contamination area without ~

protective clothing. One violation was identified. (Section R1.2)

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Reoort Details

Summarv of Plant Status

The plant remained shutdown throughout this inspection period.

l. Ooerations

01 Conduct of Operations  !

The inspectors noted that the sensitivity to procedural adequacy and adherence within the

Operations Department had, with few exceptions, improved from previous inspection

periods. Only two examples of clear non-compliance with working procedures were

identified; one of these occurred early in the inspection period, and the other was in the

Maintenance area. These examples are discussed in more detail in Sections 01.2 and

M1.5. Procedures were used as written or were changed prior to continuing with work

during all other direct inspector observations. Approximately 200 procedure changes were

processed during this inspection period. Despite these improvements, the inspectors made

several observations that indicated continued opportunities for improvement in the general

conduct of operations.

01.1 Conduct of Ooerations in the Control Room

a. Inspection Scooe (71707)

The inspectors observed Main Control Room (MCR) turnovers to verify that all

i necessary information conceming plant system status was discussed and  ;

understood. The inspectors also performed routine observation of the general

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conduct of operations within the MCR using inspection Procedure 71707. '

b. Observations and Findinas

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The information provided in tumovers was generally adequate to ensure that

oncoming crews were aware of plant status and planned activities.

Good Performance involvino Shutdown Coolino

On April 8,1997, the inspectors entered the MCR and observed the on-duty crew

discussing a procedure change. A reactor operator (RO) informed the inspectors

! that a Residual Heat Pemoval (RHR) "A" heat exchanger inlet valve 1SXO82A, had

  • to be stroked to damonstrate operability. Procedure CPS 9069.02, " Division 1 SX

Valve Operability," was written for performance of this valve stroking with Division

l SX out of service. Existiag plant conditions did not support removing Division l

SX from service, so a temporary procedure change was being processed to stroke

, the valve independent of a full divisional outage. Two alternatives existed. The

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first alternative involved securing shutdown cooling, and entering a Technical

Specification (TS) Limitinc Sondition for Operation (LCO). The shift understood that

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a member of plant management had directed that this alternative be used. The

- second altemative involved more demanding work for the operators in that a ,

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manual valve in a contamination area would have to be closed and then reopened, '

but this alternative would not require that shutdown cooling be secured. The crew

subsequently revised Procedure CPS 9069.02 to require the more labor intensive

alternative, avoiding the otherwise unnecessary TS LCO entry. The inspectors j

considered the crew's decision to change the operating procedure in a way which

avoided an unnecessary TS LCO entry to be indicative of positive performance in

operations.

Ooerator Unfamiliarity with Annunciator Status

During a MCR panel walkdown on April 7,1997 the inspectors noticed that the -

annunciators for the inboard and outboard reactor core isolation cooling system

(RCIC) turbine exhaust vacuum breakers were lit. When the inspectors inquired as

to why these specific annunciators were lit, one RO stated that he was unsure. A

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second RO indicated that the status of RCIC was not important since the system

was out of service due to the plant operating in Mode 4. Neither RO attempted to

determine why the annunciators were lit. Two days later, the inspectors posed the

same question (reason for the RCIC annunciators)'to ancther RO. !n this instance,

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the RO stated that he could not immediately recall the reason why the annunciators

were lit; however, he quickly reached for the annunciator response procedure and l

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informed the inspectors that the annunciators were lit due to a Group 7 isolation on j

low steam pressure.

Although the RCIC system was not operable while in Mode 4, the inspectors were

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concerned by the operators' unfamiliarity with annunciator status and causes for

changes in system configuration. Licensee management told the inspectors that

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they planned to increase annunciator awareness as part of the improvements in

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Weak Communications Durina Surveillance l

On April 28,1997, the inspectors observed a portion of surveillance Procedure CPS

9070.01, " Control Room HVAC Filter Package Operability Test Run," Revision 25.

This surveillance required a 10-hour system run with system data to be recorded

every two hours. The procedure stated that five of the parameters were to be

recorded from local instruments in the field, and the sixth, system flow, was to be  ;

recorded from control room instrumentation. The sheet on which the data was j

recorded was separate from the procedure, and did not identify where the data was '

to be obtained. The inspectors observed that data from the field was recorded in j

the record copy of the surveillance data sheet based on information conveyed over

the phone. The inspectors were concerned that each of the five individual values  ;

was not provided to the operator, rather, the operator was told the data was "the I

same as the readings two hours ago." The inspectors felt that this communication

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technique could result in misrecording one of the five values from the field or the

failure of the control room operator to verify that the sixth value had not changed.

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and verified that they were consistent with the recorded data. The on-duty licensee  ;

  • staff informed the inspectors that this was a routine surveillance with data that did l

not typically change during the test run, and that the observed communication

techniques were within management's expectations. The Operations Manager

subsequently informed the inspectors that this was an example of an opportunity to I

improve communication techniques. l

Trackina Surveillance Dalga

On May 7,1997, operations personnel declared the high pressure core spray l

(HPCS) system inoperable due to exceeding the allowable surveillance frequency,

including the TS extension of 25%. Although operations monitored the surveillance

expiration dates of numerous systems including HPCS, the scheduling of the HPCS

surveillance was overlooked during turnovers and was not scheduled for

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performance. Operations personnel recognized the need to perform the HPCS

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surveillance test approximately ono hour before the system needed to be declared

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inoperable. Since the surveillance test took several hours to perform, operations

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personnel appropriately declared HPCS inoperable and ensured that actions with a

potential to drain the reactor vessel had been suspended in accordance with l

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technical specifications,

c. Conclusion

Operator tumovers usually covered the appropriate information. The inspectors

observed an on-duty operating crew demonstrate a questioning attitude and

prudently avoid an unnecessary TS LCO entry. However, the inspectors identified l

several examples of opportunity for improved performance.

01.2 Weaknesses in Performance of a Surveillance

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a. Insoection Scooe (61726/71707)

The inspectors observed the performance of surveillance CPS 9170.02, " Control

Room HVAC Chilled Water Valve Operability Test," Revision 26, performed on

April 8,1997.

b. Observations and Findinas

On April 1,1997, the licensee's revised procedural adherence policy, which

required procedure steps to be performed in the order written unless otherwise

specified, became effective. During the performance of Procedure CPS 9170.02,

the inspectors observed a non-licensed operator (NLO) give a maintenance

mechanic permission to perform procedural steps out of sequence. The surveillance

procedure required that a flange be installed on line OVC120E, per step 8.1.6, in

order to complete in-service testing on the control room ventilation (VC) chilled

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water shutdown service water makeup check valve. Upon test completion, the

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mechanic inquired if the installed flange could be removed. The NLO briefly

reviewed the procedure and gave the mechanic permission to remove the flange.

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As the mechanic began loosening the flange connection, the inspectors recognized

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!- that the next procedure step instructed the closure of the auto makeup inlet

isolation valve. The procedure step did not reference the removal of the flange.

The inspectors called the mechanic's attention to this fact, and the mechanic

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stopped the flange removal. The pipe behind the flange was pressurized with low

energy chilled water at the time of the inspectors' observation.

The failure to perform procedure steps in the order stated by the procedure was

considered a violation (50-461/97011-01) of TS 5.4.1.

Step 8.1.12 directed that valve OVC016A be closed and independently verified.

The inspectors observed that the independent verifier was in close proximity to the

procedure performer and possibly watched the step' performance. The inspectors

then asked the independent verifier if the independent verification method used met

the time and distance expectations delineated in Procedure CPS 1401.01, " Conduct

of Operations," Revision 22. The independent verifier stated that his presence at

the job site was acceptable as long as he was not directing the actions of the

individual perforrning the surveillance. Procedure CPS 1401.01, stated that '

independent verification was " intended" to have both time and distance between

the act and the verification. The inspectors discussed the apparent inconsistency

between the operator's understanding of the requirements and Procedure CPS

1401.01's stated " intent." Operations Department rnanagers informed the

inspectors that the observed performance did not completely satisfy plant

management's expectations, but did satisfy the plant's procedural requirements.

The inspectors will continue to assess the effectiveness of the plant's independent

verification procedures and practices under inspector Follow-up System item eel

50-461/96015-01 a.

The inspectors also observed the independent verification of Step 8.1.22 which

ensured that instrument vent valve OPC-VC550AV was closed. Upon finding the

instrument, the independent verifier noticed that the vent valve was not labeled

with an equipment identification number (EIN). The procedure performer explained

that since the instrument was labeled, and the instrument had only one vent, he

was confident that the correct valve was manipulated. The independent verifier

was not comfortable signing the procedure step and contacted the control room for

further guidance. It was later determined that the performer manipulated the

correct valve. The inspectors considered the independent verifier's actions to be

appropriate.

c. Conclusions

The inspectors identified that a N1.0 and a maintenance mechanic were in the

process of violating procedural steps during a surveillance on the Control Room

ventilation system. A potentially weak independent verification was eko identified

by the inspectors. One violation was identified.

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.02 Operational Status of Facilities and Equipment

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02.1 Enaineered Safety Feature (ESF) System Walkdowns (71707) l

a. Insoection Scone -

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The inspectors used inspection Procedure 71707 to walkdown portions of the low

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pressure core spray system (LPCS), the diesel generator room ventilation system ,

(VD) and the Division ll safety related switchgear. Although not an ESF system, ,

the inspectors also walked down portions of the component cooling water (CC)

system.

b. Observations and Findinas

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On April 14,1997, while performing a routine walkdown of safety related and ESF

switchgear, the inspectors noted that the 480 VAC breaker at Motor Control Center '

(MCC) 181, cubicle 9D, was in the open, deenergized, position. This breaker was

labeled as."D.G. Roorr 1B Vent Sys. Damper 1VD12YB." The inspectors asked the

Line Assistant Shift Supervisor (LASS) why the breaker was deenergized. The .

LASS reviewed the mechanical system drawing for the system, M05-1103, " Diesel *'

Gen. Room Ventilation (VD)," Revision L, and concluded that 1VD12YB was a '

motor operated valve (MOV) which appeared to be required for system balancing.

The LASS could not immediately determine why the damper breaker was open.

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The licensee subsequently determined that Field Engineering Change Notice (FECN)

14531 had removed power from Dampers 1VD12YA,1VD12YB, and 1VD12YC

during post-construction system testing. The MCC label for 1VD12YC had been

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corrected to read " spare," but the MCC labels for 1VD12YA and 1VD12YB had not '

been updated. The licensee initiated a condition report (CR) and hung caution tags

on the breakers labeled as 1VD12YA and 1VD12YB to indicate that they were

" spares."

The inspectors walked down the VD systems and determined that dampers

1VD12YA, B, and C were installed, and were provided with self contained hydraulic i

actuators. Based upon the licensee's determination that no power was supplied to

these actuators, they were essentially manual valves, contrary to the system '

drawing.

The inspectors reviewed drawing M05-1103 to determine whether it contained

other errors. No other discrepancies were noted.

The inspectors discussed the VD system observations with the cognizant system

l engineer. The system engineer informed the inspectors that an operator had

identified the mislabeling of the 480 VAC beakers for 1VD12YA and B in

j January 1997, but that the breaker labels had not yet been corrected when the

inspectors noted the problem. The M05-1103 discrepancies had not previously

been identified or documented.

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The inspectors considered the incomplete implementation of FECN 14531 and the 1

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discrepancies of M05-1103 to be examples of a problem with design control.

However, this problem was of minor significance and is being treated as a

Non-Cited Violation (50-461/97011-02) consistent with Section IV of the NB;

Enforcement Poliev. The inspectors were concemed that system walkdowns by

operators and system engineers were weak, since a non-energized breaker in a

safety related MCC had not been investigated and dispositioned during nine years 3

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of plant operation. Similar concerns are identified in Section M2.3 of this report.

c. Conclusions

As the result of a system walkdown, the inspectors identified that the system

drawing for the safety related VD system was incorrect and that breakers in safety

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MCCs were mislabeled. These conditions had existed since start-up, but had not

been corrected by the licensee. The conditions did not affect system operability.

No concerns were identified during the LPCS or CC walkdowns.

02.2 Inconsistencies Found Within Eauioment Control Proaram *

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a. Insoection Scone (71707)

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During the course of plant tours, the inspectors verified the position of various

components and that danger and caution tags were placed on the proper

equipment. "

b. Observations and Findinas

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During a make-up water pumphouse (MWPH) walkdown, the inspectors noted that

the EIN on danger tag 57 for tagout 96-1049 did not match the nameplate on the

' breaker cubicle. Specifically, the danger tag stated the EIN as OWM12PA (power

supply for the makeup demineralize pump) while the breaker cubicle ncmeplate

stated " spare."

The licensee told the inspectors that the EIN for the breaker within the cubicle was

previously OWM12PA. However, the breaker was abandoned as part of a upgrade

to the MWPH, and the cubicle nameplate was changed without updating the tagout

information.

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inspection Report 50-461/96009 discussed deficiencies in the safety tagging

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program, including the absence of a feedback mechanism to correct ta0ging .

inconsistencies. The safety tagging supervisor explained to the inspectors that

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feedback to correct changes in the plant due to modifications was provided prior to

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releasing the modification for operations. However, feedback to correct tagging {

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deficiencies which occurred during the installation of a modification, or due to the  ;

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abandonment of equipment, did not normally occur and was not required by the l

] licensee's safety tagging or modification programs. The inspectors were concerned

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by the practice of not updating tagouts during modifications since post modification

~ testing could require energization of mislabeled components prior to the

modification's release for operation. This could reduce the effectiveness of the

personnel safety provided by the tagout. The licensee acknowledged this issue

during discussion with the inspectors.

c. Conclusions

The inspectors identified that the licensee's safety tagging program allowed

inconsistencies between equipment EINs and the EIN listed on safety tags to exist

during the performance of modifications. The inspectors considered this a

weakness since the level of personnel safety during post modification testing could

be affected by the inconsistent nomenclature. ~

02.3 Imolementation of Locked Valve Proaram on Emeraency Diesel GeneratorJEDG)

Sucoort Systems

a. Insoection Scooe

The inspectors performed routine walkdowns of the EDGs and their support

systems and compared the observations to the licensee's program requirements,

b. Observations and Findinas

Procedure CPS 1401.01, " Conduct of Operations," Revision 26, Section 8.5.2,

required that components, the unauthorized manipulation of which could

compromise plant safety or availability, be chained, lockwired, or otherwise suitably

locked. The inspectors observed that six valves in the air start system for the

Division i EDG, and six valves in the air start system for the Division ll EDG were

not locked open. Four valves in the air start system for Division 111 were not locked

open. The valves involved were 1DG150 through 1DG165. One valve, the supply

emergency cutoff valve in the Division 111 fuel oil system, was also not locked open.

The inspectors questioned plant staff as to why the air start and fuel oil valves

were not locked open since the closure of one or more of these valves would

appear to compromise the availability of the EDGs. Plant staff acknowledged that

the valves should have been locked open, and were in the process of locking the

valves open at the end of the inspection period. Plant staff did not know why the

valves had not previously been locked or tagged. The failure to lock open the

Division lli EDG fuel oil supply cutoff Valve and valves 1DG150 through 1DG165 as

required by Procedure CPS 1401.01 was a violation (50-461/97011-03) of TS 5.4.1.

c. Conclusions

The inspectors identified that valves in the air start systems for all three EDGs, and

a valve in the fuel oil system for the Division 111 EDG, were not locked open as

required by the licensee's locked valve program. One violation was identified.

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i 07 Quality Assurance in Operations

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Review of Emeroency Resoonse/Emeroency Ooeratino Procedures (EOPs) Audit

a. Insoection Scoce (71707)

The inspectors reviewed Audit Report 038-97-03, " Emergency

Response / Emergency Operating Procedures," issued April 29,1997.

b. Observations and Findinos

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The inspectors confirmed, through discussions with the lead auditor, that no walk

throughs of EOPs had been conducted during performance of Audit Report Q38-97-

03. The lead auditor stated that procedure walk throughs were more of a

performance review rather than a compliance review. Due to recent chan<;es in

philosophy, Nuclear Assessment management had determined that audits should

focus more on compliance and that surveillances would focus more on

performance. However, the lead auditor was not aware of whether surveillances

had reviewed EOPs from a performance standpoint. Based on discussions with the

surveillance supervisor, the inspectors determined that no surveillance had covered

EOP walk throughs in the previous year. The inspectors considered procedure walk

throughs an important assessment tool for: 1) assessing the adequacy of

procedure validation and verification (V&V),2) scnfirming that changes in the field

since V&V have not adversely affected performance of the procedure, and 3)

assessing operator training and knowledge.

c. Conclusions

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An audit of EOPs lacked depth in that procedures were not verified in the field. Not

I performing procedure walkthroughs of a sample of EOPs, either through audits or

surveillances, was considered a weakness.

II. Maintenance

M1 Conduct of Maintenance

a. insoection Scone (61726/62703)

The inspectors observed or reviewed portions of the following surveillance and

maintenance work requests (MWRs) and other maintenance activities.

-MWR D76266/ CPS 8433.01 Generic Procedure for 125 VDC Battery

j Maintenance

-MWR D71146 Packing Replacement for Reactor Water

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Cleanup Valve 1G33F053

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-MWR D76456 Rotor Work on RCIC Turbine Exhaust

, Vacuum Breaker

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-PCIFWM135 Feedwater Flow Line A Flow Transmitter

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Loop Calibration

-CPS 9053.07 RHR B/C Pumps and RHR B/C Water Leg

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Pump Operability

-CPS 9170.02 Control Room HVAC Chilled Water Valve

Operability Test

-CPS 9382.02 125 VDC Battery ICV and Battery

Charger Checks

l -CPS 9532.61 CRVICS Fuel Building Exhaust Radiation

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t- 1 RIX-PR006A (B,C,D) Channel Functional

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-CPS 9069.02 Div i SX Valve Operability

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-CPS 9070.01 Control Room HVAC Filter Package

Operability Test Run

-CPS 8410.07 Reactor Recirculation 6900 Volt Vacuum

Circuit Breaker Maintenance

b. Observations and Findinas

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The inspectors found the work performed under these activities to be generally

acceptable, with procedures present and in use. Comments for specific work

activities are discussed in further detail below. Due to the operator performance

issues identified during the performance of Procedure CPS 9170.02, all relevant  ;

comments were included in Section 01.2.  !

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l M1.2 Performance of 125VDC Batterv Maintenance

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a. Insoection Scoos (62703) l

The inspectors observed portions of the maintenance performed on the Division 11

125VDC battery under MWR D76266.

b. Observations and Findinas

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While torquing the battery terminals of a Division il battery, the torque wrench

! s.ipped and came into contact with a neighboring battery post, causing a short

i oischarge. Although the torque wrench had been taped to provide electrical

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insulation prior to use, the electrician had not taped the area around the torque

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wrench dial. No personnel were injured and only minor damage to the battery post

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occurred.

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The system engineer performed an as-found inspection and noted no battery ,

abnormalities. However, to ensure that the battery internals were not dam'aged, '

the system engineer requested that specific gravity and cell voltage checks be

performed on both cells in their discharged condition.

The inspectors later learned that the electricians had decided not to perform the

requested cell voltage and specific gravity checks since these actions were not

supported by an approved procedure. Electrical Maintenance (EM) personnel did 1

not communicate their inability to perform the requested checks to the system

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engineer. The cell voltage and specific gravity readings for all cells were obtained

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after the cells were recharged and prior to returning the battery to service. No

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deficiencies were identified with cell voltage or specific gravity. l

The inspectors reviewed the condition report (CR) associated with this event and

questioned the description of the immediate actions taken. Specifically, the

immediate corrective actions stated " stopped work, directed that a set of gravities

be taken on Cells 4 and 5, had NSED evaluate damage." These actions were

signed as complete although, as explained above, the pre-recharge " set of

gravities" requested by the system engineer were not obtained.

Procedure CPS 1016.01, " Condition Reports," Revision 29, Step 8.1.4.2a, states

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" document immediate actions and ensure actions are carried out and/or initiated 1

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as necessary and initial /date when complete in space provided on CPS No.

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1016.01F001." The inspectors considered EM supervision's signoff that the initial

corrective actions were complete when alternate actions were performed to be a

i

violation of Procedure CPS 1016.01. However, this violation is of minor

significance and is being treated as a Non-Cited Violation (50-461/97011-04)

consistent with Section IV of the NRC Enforcement Poliev. See Section M7.1 for

additional discussion of this issue.

c. Conclusions

Poor insulation of a torque wrench resulted in shorting between two 125VDC

safety related batteries. No significant damage occurred to the batteries. EM

,

personnel failed to obtain revision to a corrective action document when the

!

specified actions could not be completed.

M1.3 Damaoe to MOV Motor Overload Heaters Due to inadeouate Tumover

a. Insoection Scoce (62703)

The inspectors reviewed the circumstances surrounding damage to the reactor core

isolation cooling (RCIC) exhaust vacuum breaker outboard isolation valve

(1E51F077) during VOTESm testing.

13

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l

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On April 23,1997, night shift EM personnel suspended VOTES testing of Valve

1E51F077 to correct problems with a limit switch. While testing was suspended.

l~ operations personnel noticed that the associated MOV test prep switch (TPS) was

l not in its usual position, and asked the EM personnel whether it could be retumed

!

l

to " normal." The EM and operations personnel concluded that the TPS no longer

needed to be iri "u. pass" since testing of the MOV was suspended. Following this

discussion, operations personnel retumed the TPS to the normal position.

l On April 24, the day shift ems completed work on the limit switch and resumed

preparations for VOTES testing. While the day shift ems verified the position of

many tags prior to resuming work, verification of all previously performed steps

was not required. The night shift ems had not communicated the repositioning of

l the MOV TPS during tumover with the day shift EM group leader and had not

included this information within the MWR continuation sheets. _ The MOV TPS was

not repositioned prior to performing the VOTES test. This resulted in EM and

engineering personnel performing the test without thermal overload or torque

switch protection (torque switch protection was bypassed due to test set-up). The

MOV motor and breaker sustained damage when the valve was subjected to a

l locked rotor condition.

b. Observations and Findinas

l

The licensee wrote condition report CR 1-97-04-187 describing the event and held

I a critique (EM 97-010). Specific observations conceming the critique are discussed

!

in Section M7.3.

!

Procedure CPS 1501.02, " Conduct of Maintenance," Revision 18, Step 8.1.4.6,-

!

which the inspectors reviewed, stated "if work is performed during more than one

,

shift provide information to succeeding shift personnel to assure work is completed i

in a safe an effective manner." The inspectors considered the failure to provide

information on the status of the MOV TPS to be a violation (50-461/97011-05) of l

l

TS 5.4.1.

c. Conclusions

The failure to adequately document and turnover the status of job conditions

resulted in maintenance induced damage to a containment isolation valve. A

violation of procedure was identified.

M1.4 initiation of Standbv Gas Treatment (VG) System Durina Surveillance Activity

l a. Insoection Scone (61726)

l l

The inspectors reviewed the circumstances surrounding an inadvertent initiation of

the VG system during a channel functional test of process radiation monitor

PR006A.

l

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. . . . . . . . .

.

b.

Observations and Findino_ s

~

\

The inadvertent actuation of the VG system occurred r ng a trip signal

due to inse ti

to Process Radiation Monitor PR006A while monitor PR006D w as inadvertently in a

tripped condition. Monitor PR006D was placed ,

in trip , when

on March 6 1997

' local trip switch. Operations clearedut did tagout

e

not

97-933

place the local trip switch back to the normal position due to inadequat

, ,

e tagout

restoration guidance. Specifically, the caution tagout restoration

e as

erred

position r

to the removal of the caution tag without giving guidance e position of the

to th

local trip

remained switch.

in trip. Because

Procedure CPS of this error, the local trip

or PR006D

switch for monit

Step 8.6.3, required that the proper restoration r ag position be identi

,

,

removal. The failure to include the restoration position wc on for the local trip s i

monitor PR006D was a violation (50-461/97011-06) of TS 5.41 ..

During the critique for the inadvertent VG system actuation lice

,

one procedure noncompliance. Step 8.1.8 of Procedure nsee

CPS staff identified

9532 61 "CRVICS

. ,

Revision 38, directed the controlsan toand onal Test," instrumentat

the components for each division were in the untripped conditi ensure

indicated approximately 0 volts.rmed The

ng that the C&l

Step 8.1.8

DMMtechnician th

and ground as zero volts when it was -

actually 120 vo

s error, the

C&1 technician did not identify that monitor PR006D ped condition.

was in the trip

The licensee determined that the physical constraints s voltage

associated with thi

revising the test process so that accurate ue

e y to be

voltage re

in accordance with Procedure CPS 9532.61obtained. The failu

e

was licensee identifi d and corrective

Violation (50-461/97011-07) consistent with Sect

Enforcement Policy. ..

..

-

e

c. Conclusions

The failure of Operations and Maintenance toy establish at plant

and verif th

protective logic was in the appropriate condition resulted in an inadve t

r ent ESF VG

cited violation were identified. system actuation during one non-

performance of a surv

M1.5

a.

Lifted Lead Results in Reactor Recirculation a ve Runback (RR) Flow Con

Insoection Scone (617261

The inspectors reviewed the details surrounding a runback of the "A" RR

control valve during performance of a preventivefinw maintenance (PM) acti

.

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b. Observations and Findinos

On May 14,1997 C&l personnel performed PM task PCIFWM135, calibration of the

feedwater flow measurement instrument loop. The PM data sheet instructed the

C&l technician to obtain correct contact indication between terminals 13 and 14 on

trip unit 1C34-K618A by measuring the voltage between these two terminals. Due

i

to plant conditions, correct contact indication could not be obtained using the

j

above method because the indication was masked by position of the contacts  :

between Terminals 9 and 10 (Terminals 9,10,13, and 14 are in parallel). To

obtain an accurate contact indication, the technician lifted lead between Terminals

13 and 14. Because wiring from Terminal 14 supplied power to trip units further

downstream, power was lost to other trip units as the lead was lifted. ' This

produced an unexpected runback of the "A" RR flow control valve (the "B" valve

was locked out prior to the evont). The RR flow control valves are a reactivity

control when the unit is operating.

Operations personnelinitiated a CR and held a critique following this event. The

technician involved in the event stated that he did not consult any prints prior to

lifting the lead because he assumed that his actions would have no effect on the

plant. Lifting of leads was not authorized within the work package. C&l

supervision noted that the technician's actions were not covered within the system  ;

impact matrix for the task. The inspectors reviewed the work package and

i

determined that two additionalleads were lifted without an appropriate system

impact matrix.

Procedure CPS 1501.02, " Conduct of Maintenance," Revision 18, Step 4.8, stated

"if the work requires lif ting leads or otherwise interrupting electrical circuit

continuity... complete a system impact matrix and attach it to the work document."

The inspectors considered the failure to complete a system impact matrix to

!

' evaluate the consequences of actions not previously evaluated in accordance witli

Procedure CPS 1501.02 to be a violation (50-461/97011-08) of TS 5.4.1. The

inspectors were concerned by this occurrence because it involved a plant employee

who knowingly performed steps not covered by the work package in use, or by an

approved procedure, a performance issue for which plant management had initiated

substantial corrective actions.

c. Conclusions

A C&l technician lifted leads not covered by the procedure and a runback of the

i

' "A" reactor recirculation flow control valve resulted. One procedural violation was

identified.

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.

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-, . - . - - _ - . - . - - . - - . - _ . . . - . - . ~ . - . . ~ . . - . _ - . . - - . - . . . . .

L

.

.

M2 Maintenance and Material Condition of Facilities and Equipment

M2.1 B_r.gaker Testina

a. Insoection Scone (61726)

,

The inspectors reviewed:

i

l e Job No. PEMAP1012, "8410.04 Testing for 1DC14E4A/15"

e Job No. PEMAP1054, "8410.04 Testing for 1 AP41E2C"

,

e Job No. PEMAP1057, "8410.04 Testing for 1 AP73E13C"

t e CR 1-96-12-124, " Questionable Breaker Not Removed From System"

l e CPS 8410.04, " Molded Case Circuit Breaker Functional Testing and i

L Maintenance," Revision 9

e CPS 8410.05, " Type HE Molded Case Circuit Breaker Revision Level Test,"

Revision 4

L e Licensee responses to information Notices 89-21 and 96-24

! e Calculation Numbers 19-M-3, Revision 1,19AN-4, and 19-AQ-3 -

~

b. Observations and Findinos

On February 27,1989, the NRC issued information Notice (IN) 89-21, " Changes in

Performance Characteristics of Molded-Case Circuit Breakers." This IN discussed

instances in which vendors made revisions to the performance characteristics of

molded-case circuit breakers (MCCBs) without making corresponding revisions to  :

the breaker's part number. In addressing this issue, the licensee re-classified MCCB l

part numbers as 1976/ Revision 3,1986/ Revision 3,1985/ Revision 4,

{

! 1989/ Revision 4, or 1990/ Revision 5 based on individual breaker performance

! characteristics. The licensee then performed reviews to determine whether the

newly classified breakers remained properly coordinated. The mviews determined

that all installed safety related breakers were acceptable. The licensee was still

reviewing the acceptability of the 120V distribution panels. In addition, the

l licensee determined that safety related MCCs could contain breakers having all

l MCCB revisions while non-safety related MCCs could only contain MCCBs having

! i

,

certain revisions.

i

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f

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l The licensee periodically performed Procedure CPS 8410.04 to verify the operability i

of installed MCCBs. This procedure applies a designated current to each tested

breaker to ascertain the proper breaker response. In addition, the licensee developed

Procedure CPS 8410.05 to test MCCBs in the plant's store room to verify or

identify these breakers' part number revisions prior to their use in the plant. The ,

inspectors determined that Step 8.1 of Procedure CPS 8410.05 required exercising l

(manually opening and closing) a tested breaker 5 times to. ensure free operation.

Therefore, the performance of Procedure CPS 8410.05 on an installed breaker prior

to performance of Procedure CPS 8410.04 would constitute breaker

, preconditioning in that test data obtained after manual cycling of the breaker would

j no longer represent the breakers'in service performance. The inspectors reviewed

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. . . .. . - - - _ . - _ - - _ - . .

.

.

'

Procedure CPS 8410.04 and did not identify any preconditioning concerns. The

' licensee stated that Procedure CPS 8410.05 was not intended to be performed on

installed MCCBs.

On December 11,1996, Procedure CPS 8410.05 was partially performed on '

installed breaker 1 AP41E2C, which protects containment penetration 1C11-F003.

The licensee subsequently completed Procedure CPS 8410.04 with satisfactory

results, in response to the inspectors' questions, the licensee identified that on

October 9 and December 30,1996, installed Breakers 1 AP73E13C and

1DC14E4A/15, respectively, were also tested by Procedure CPS 8410.05 prior to

performance of Procedure CPS 8410.04.

!

l

10 CFR Part 50, Appendix B, Criterion V, " Procedures / required in part, that

l activities affecting quality be prescribed by procedures appropriate to the

circumstances. The licensee's procedures for testing Breakers 1 AP41E2C,

t

1 AP73E13C, and 1DC14E4A/15 were not appropriate in that they did not ensure

that as-found data was obtained for comparison with the as-found acceptance

,

' criteria required by 10 CFR Part 50, Appendix B, Criterion XI. These procedures

which were not appropriate to the circumstances were a violation (VIO 50-

461/97011-09) of 10 CFR Part 50, Appendix B, Criterion V.

c. Conclusions

The licensee performed tests to determine the revision number for three breakers

before performing "as-found" functional tests. This precenditioning resulted in

potentially invalid test data. A violation of 10 CFR Part 50, Appendix B, Criterion V

was identified.

M2.2 installation of Temocrary Modifications

'

a. Insoection Scooe (62707)

The inspectors were concerned that some temporary modifications (TMs) were

installed incorrectly with the supply line connected to load terminals and load

connected to line terminals. The ins:nctors redewed the following work packages:

MWR D73749 for TM 97-010, "Aternate Power to 120V distribution panelin

1 AP75E to keep VR/VQ Running," installed on January 26,1997

e

MWR D72424 for TM 96101, " Temporary Power for 1FCO23 During Division 2

Bus Outage," installed on December 30,1996, and removed on January 2,

,

'

1997.

e MWR D62937, for TM 97-014, " Temporary Power to Orarations Radio Base

I Station A, Receiver Cable 3 and 1JB674," installed on f . arch 3,1997

,

,

i

18

I

MWR D73885 for TM 97-004, " Install Temporary Modification to Maintain

  • Power to 1 AP87E," installed on January 17,1997, and removed on

January 20,1997.

. e

MWR D72416 for installing TM to maintain power to 125 VDC MCC 1D during

4160 Bus 1B1 outage, installed on December 27,1996, and removed on

January 6,1997.

MWR D60155 for installing and removing TM to cross-tie non-divisional battery

charger to Division 2 DC bus, installed on December 9,1996, and removed on

December 19,1996.

b. Observations and Findinas '

Step 9 in MWR D62937, stated, " Lift and remove the line side leads from the top

of Breaker 10AL. Using cond 7ctors/ cable of Min 4 AWG, jumper from the load side

of Breaker 10AR to the line side of Breaker 10AL." The licensee connected two

breakers in series to provide breaker protection. The inspectors did not identify any

personnel safety concern with this breaker configuration.

MWRs D72416 and D60155 required installation of cross-ties from the non-

divisional MCC 1F to divisional MCC 1D and 18, respectively, during a bus outage

in accordance with Procedtire CPS 3503.01, " Battery and DC Distribution." Step

8.2.7.3.8 in Procedure CPS 3503.01 required connection of two conductors to the

load side of the spare breaker on MCC 1F. By conventional configuration, the top

of the breaker was designated as the line terminal and the bottom of the breaker as

the load terminal. However, for the spare breaker, the line side was connected to

the bottom of the breaker. The procedure did not clarify that the load side was at

the top of the breaker. Therefore,it would appear that the conductors were

terminated to the line terminals.

Step 8.2.7.2.9 in Procedure CPS 3503.01 required connection of a Class 1E

disconnect switch to the spare breaker at MCC 1F. However, the procedure did

not clarify that the connection should be made to the load terminals which were

located at the top of the breaker. The licensee initiated Comment Control Forms

(CCFs) to clarify that the spare breaker had its line conductors terminated at the

bottom terminals. In addition, the connection of the conductors or the disconnect

switch was to be made to the load terminals located at the top of the spare breaker

for MCC 1F.

In both installations, the conductors and the disconnect switch were connected to

the load terminals located at the top of the spare breaker. This field configuration

was in accordance with Drawing No. E03-1DC17E. The inspectors also reviewed

the drawings for the line and load connections of UPS breakers for MCC 1 A,18,

and 1D. The line terminals were designated at the bottom of the breakers. The

licensee reviewed the vendors manuals and concluded that the in-plant

configurations were consistent with the vendor and design drawings.

19

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1.

c. Conclusions

-

The inspectors did not identify any installation problems associated with the

instructions provided in the above work packages. However, there were minor

procedural deficiencies in Procedure CPS 3503.01 for which the licenseo initiated

l CCFs.

M2.3 Miscellaneous Material Condition Problems

a. Insoection Scoce (71707)

The inspectors toured the facility to assess material condition.

b. Observations and Findinos

The inspectors observed the following undocumented deficiencies on safety-related

equipment:

e

The inspectors noted a number of room and equipment coolers with loose or

broken inspection door handles. None of the problems had been identified with

maintenance request tags. Examples of room coolers with deficient handles

included the reactor core isolation cooling room, "A" RHR heat exchanger room.

"B" shutdown service water room, and several of the safeguards switchgear

rooms. In addition, several non-safety related room coolers had similar

deficiencies.

Although the inspectors did not identify any operability issues with the

deficiencies, they were concerned that certain ventilation lineups might result in

the cooler housing being briefly pressurized, popping open the doors. This could

result in the cooling coils being bypassed during subsequent operation of the

fans. The concern was brought to the attention of the Shift Supervisor. The

inspectors noted that most of the deficient handles on safety-related coolers had

subsequently been identified with maintenance request tags.

The inspectors noted that the Standby Liquid Control common supply line check

valve, Valve 1C41-F006, was missing the cotter pin and lock wire which would

normally hold the manual operating lever in place. Similar valves in other

systems had the cotter pins and wires. Lack of the pin would not affect

operability unless something caused the handle to move from its normal

position. The inspectors informed the LASS of this finding. The LASS

determined that the presence of the pin and lock wire was not checked in the

system valve lineup checklist, was not shown on the piping and instrumentation

drawing, was not included in the locked valve program, and was not required by

TSs. However, the LASS had a maintenance request tag placed on the valve to

initiate action to get the pin and wire installed.

The inspectors later discussed the issue with the system engineer. The

engineer determined that the applicable drawing for the valve (Anchor / Darling

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.

Valve Company drawing W8121407, revision C) showed that the pin and lock

i*

wire should be installed. The inspectors reviewed surveillance Procedure

9015.02, "r tandby Liquid Control injection Operability," Revision 33, which

manually exercised the valve, using the handle, and noted that it did not

L

! mention the pin or lock wire. The inspectors reviewed maintenance procedure

8120,04, " Maintenance of Anchor / Darling Tilting Disc Check Valves,"

Revision 12, and noted that the procedure provided instructions to install the pin

and lock wire when reassembling the valve after maintenance. However, the

inspectors noted that Procedure 8120.04, Appendix C, " List of Anchor / Darling

i

Tilting Disc Check Valves," did not list 1E41-F006 or 1E41-F007. The system

ersgineer agreed that both_ of those valves should have been incli.ded on the list,

and wrote a comment control form to initiate a revision.

e

The inspectors noted that both constant level oiler bulbs on the A fuel pool

cooling pump were missing their locking bolts. The inspectors were concerned

i that a seismic event or significant pump or piping vibration could cause the

bulbs to fall off. Loss of the oiler bulbs would not have an immediate effect on

operability of the pumps, but would prevent the oiler from automatically

compensating for small oil losses. The inspectors informed the LASS of the

j- - concern. The oilers were subsequently corrected.

! c. Conclusions

l

l The inspectors noted minor material condition issues associated with safety related

l

room coolers, a safety related check valve, and oilers on a fuel pool cooling pump.

i

All of these problems should have been readily apparent to plant management,

operators, and system engineers performing tours and system walk downs.

M2.4 Material Condition Deficiency identification and Trackina l

a. Insoection Scooe (62703)

The inspectors performed routine assessments of equipment histories, maintenance

records, and current maintenance requests to identify repetitive failures, indications

of possible common mode failure machanisms, or other adverse performance trends

which might be indicative of ineffective or inadequate maintenance,

b. Observations and Findinas

!

The inspectors observed several material condition issues during this inspection

period which did not appear to be rece!ving adequate attention. While the material

conditions had been identified for repair, the inspectors found that in some cases

prompt operability determinations or evaluations for possible common mode

failures, repetitive failures in components with different unique identifiers (EINs), or

other adverse trends were not being performed. No examples of inoperable

4 aquipment for which appropriate actions were not taken were identified, but the

i

inspectors were concemed by the potential programmatic implications of this issue.  :

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"

i ' PosiSeal Butterfiv Valves in Service Water Systems

.

-

During a plant tour on April 30,1997, the inspectors noted that there were

maintenance request tags on valves 1SXO14A and 1SX0148, the service water

(WS) to SX isolation valves. The tags noted that there was leakage from the SX to

WS systems when the valves were closed. The inspectors were concemed by the

potential effect of flow diversion on SX operability, and investigated the issue.

Both valves were PosiSeal butterfly valves.

i

i

MWR D73235 had been issued on December 19,1996, because the licensee noted

l- that the WS system remained pressurized when the WS pumps were secured and

the 1SXO14A and B valves were closed. The valves are automatic isolation

designed to close whenever the associated SX pump start, thus isolating the non- ~

safety related WS piping from the safety related SX piping. Excessive leakage

through the valves could degrade the availability of SX cooling water to safety- i

related loads. The inspectors noted that the MR was evaluated by the Shift

Supervisor as having no significant effect on operability and was given a priority of

4 with " repair with unit on line" indicated. The inspectors discussed the condition

of the valves with the system engineer in an attempt to evaluate whether the

operability decision and priority were appropriate. ,

!

The system engineer stated that the amount of leakage was small, and that the

isolated WS system had been maintained depressurized by continuously draining )

through a 3/4-inch drain line. The system engineer said that at about the same  !

,

l

time the back leakage was discovered, significant back leakage was identified

through 1SXO14C on Division 111 SX, and the valve had been replaced. The

inspectors asked whether the leakage through any of the three valves had been

,

'

l

quantified, whether the leakage had been formally analyzed for effects on SX 4

system operability, and whether a CR had been issued. The answer to all the

questions was "no." j

The next day the system engineer informed the inspectors that he had thought

about the issue further and decided to recommend that both valves be replaced.

On May 5, ?197, CR 1-97-05-050 was issued documenting the concems, a

conditional s cerability determination, and the need for further evaluation of the

leakage. The conditional operability determination was baseo an the fact that the

unit was shutdown and that the temperature of the ultimate heat sink was 45

degrees below the design maximum.

On May 8,1997, licensee engineering, outage planning, and other personnel met to

.

discuss the plans for resolving the issues with the valves. Engineering personnel I

. stated that the valves should be replaced because once PosiSeal butterfly valves

started leaking, degradation could accelerate. Information was presented regarding

the condition of Valve 1SXO14C which had been replaced, previous replacement of

the Valves 1SXO14A and B, and problems experienced with similar valves which

isolated SX from the fuel pool cooling system. The decision was made to replace

both valves.

! 22

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,

- _ - - - - - - - - _. . - - . - -

.

.

- The inspectors performed a cursory review of the history of PosiSeal butterfly

  • valves in service water applications at Clinton Power Station. The inspectors

l

determined that Valves 1SX014A, B, and C had been replaced in 1991 and 1992

due to excessive leakage, and that similar valves had failed to provide adequate

isolation between the SX and component cooling water systems earlier in the

current outage (Inspection Report 50-461/96015, Section M2.1). 1

The inspectors concluded that PosiSeal butterfly valves had a history of in service

! 1

failure at Clinton, were known to degrade rapidly once seat leakage developed, and

l

were capable of rendering the SX system inoperable due to inter-system leakage.

The inspectors also determined that the licensee had not evaluated whether the

-

maintenance, testing, and planned replacement programs for these valves provided

reasonable assurance of SX system operability during future operating cycles.

Synch Check Relav Failure in Safety Related Breaker

On April 11,1997, the inspectors performed a routine review of MCR logs. During

this review, the insp*ctors noted that 4160 voit breaker 1 AP09EC feeding the

"1B1" safety related bus from the Emergency Reserve Auxiliary Transformer

(ERAT), had failed to close during an attempted bus transfer. This failure had

occurred approximately ten hours earlier. A MWR had been initiated to trouble

shoot and repair the breaker. A CR was not generated until the inspectors asked

whether one was appropriate.

l

The CR which was subsequently written for the breaker failure provided the

I

additionalinformation that the breaker failure had been caused by a faulty synch

i

!

check relay. The CR classified the degraded material condition as a Maintenance

Rule functional failure. The inspectors verified that the synch check relay was not

required for automatic transfer of the bus, but noted that TS surveillance SR- 3.8.1.S required periodic manual operation of the breaker with successful transfer

j of bus 181 as acceptance criteria.

l

she inspectors performed a cursory review of the history of synch check relays at

the Clinton Power Station. The inspectors determined that the failure of synch

check relays had previously been documented in Inspection Report 50-461/96009,

Section M1.2, and that during the course of that inspection period, plant staff had

told the inspectors that synch check relays had a history of failures.

The inspectors were concerned that a safety related breaker failed to meet its TS

surveillance acceptance criteria, as demonstrated by an in service failure to close,

and that this failure was attributed to a component with a known failure history,

but no CR was written until the inspectors intervened, and no investigation of root

cause for prevention of failure repetition was initiated by the licensee.

1.ubricant Dearadation in a Safety Related Motor Ooerated Valve (MOV)

While reviewing MWR D76456 for the RCIC exhaust vacuum breaker outboard

isolation valve, a safety related valve, the inspectors noted that a MWR

.

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continuation sheet entry had been made which identified degraded lubricant on the

  • pinion gear of the MOV actuator. The MOV was being repaired to correct limit

l

'

switch deficiencies. The inspectors noted that this lubricant degradation had not

been identified on any tracking document, so neither the condition or its causes

could be analyzed or trended.

l

The inspectors reviewed the PM tasks for the above valve and determined that the

last PM on the MOV had been performed in 1992. The inspectors determined that

the vonder recommended replacement of the MOV lubricant on an 18 month

frequency, or as appropriate based upon service experience. The inspectors found

that the exhaust vacuum breaker outboard isolation valve had originally been on a

18-month PM frequency, but that the PM frequency had been changed to

54 months after 1992. The inspectors verified that the recommended lubricant had

been used in the current and preceding PMs.

l

The inspectors were concerned that the cause and consequences of this degraded

.

lubricant in a safety related valve was not being evaluated. The inspectors

!

discussed the condition of the MOV lubricant with a maintenance individual who

stated that all MOVs exhibited similar lubricant degradation, and that it "was

^

nothing to be concerned about." The inspectors were concerned that the

information on degraded lubricants was not being adequately tracked, trended, or

analyzed.

Historv of Licensee Assessment of Material Condition Problems

The inspectors reviewed the licensee's history of identifying and assessing material

condition problems relative to repetitive or generic failure mechanisms. The CR

1-89-05-084 had identified inconsistencies between how MWRs and CRs were

used to assess material condition deficiencies. The Notice of Violation attached to

inspection Report 50-461/92016 identified that a material condition deficiency

resolved on a MWR had not been adequately assessed for generic impact on other

components inspection Report 50-461/96009 documented that repetitive failures

of Feedwater System containment isolation check valves had nm been adequately

addressed to prevent reoccurrence. A Severity Level ill violation was issued for the

failure to correct check valve leakage. An apparent violation for inadequate

corrective actions related to maintenance of safety related breakers was identified

in inspection Report 50-461/97003 (EA 97-132). Many of the referenced problems

with breaker maintenance had been identified and addressed in a non-integrated

manner using MWRs.

Indications of Effectiveness

The inspectors reviewed the licensee's Material Condition Management Program

l

" Trend Report" for January 1997. This report documented that trending of

vibration data was being performed and that some repetitive component failures

were being documented and dispositioned. The inspectors' review of CRs initiated

during the inspection period supported the observation that repetitive failures of a

component within a three month period were being documented on CRs.

f

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Proarammatic Concern l

,

The inspectors noted that the licensee's corrective action program did not require

that material condition deficiencies identified on MWRs be reviewed for generic

application or repetitiveness (with the exception that CRs were required to be l

written when MWRs indicated inat a system or component failed twice within a

i

three month period). Degraded material conditions identified on MWRs were also

l

not subject to root cause analysis to prevent reoccurrence. The inspectors were

concerned that the failure to perform adequate assessment of material condition

problems identified on MWRs could lead to future equipment reliability or operability

problems.

Status of issues at the Conclusion of the Period

The inspectors requested that the licensee evaluate whether the failure of PosiSeal

butterfly valves in service water systems, breaker failure due to faulty synch check

relays, and MOV lubricant degradation were generic or repetitive material condition

.

l

problems, and to provide the maintenance history and trending data which

supported the conclusions. The inspectors consider the effectiveness of the

licensee's process for identifying and preventing recurring material condition

problems which were adverse to safety to be an unresolved item (50-461/97011-

10) pending review of the licensee's maintenance history and trending data and the

licensee's corrective actions for degraded safety related breakers (Inspection

Report 50-461/97003).

c. Conclusions

The inspectors noted material condition problems with PosiSeal butterfly valves in

service water systems, synch check relays in safety related breakers, and lubricants

in MOVs. The licensee's response to these issues appeared to be focused on

repairing the specific problems, not on assessing potential repetitive or potential

common mode failure mechanisms, or on preventing recurrcnces. The inspectors

were also concerned that material condition problems identified on MWRs received

limited review for generic implications. An unresolved item was opened pending

review of more detailed material history and trending data and the licensee's

response to a pending enforcement action.

M2.5 Control of Transient Materialin Containment

a. Insoection Scoca (71707)

The inspectors performed reviews of generic correspondence on Emergency Core

Cooling System (ECCS) suction strainer clogging and performed walkdowns of

containment to identify whether the licensee's housekeeping and transient material

programs were adequate and properly implemented.

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. _ _ _ _ _ . _ _ _ . . _ _ _ _ _ _ . _ . _ _ _ . _ _ _ . _ . _ _ . _ _ _ _ _ . _ _ ..

.

b. Observations and Findinos  :

While performing walkdowns of the containment, the inspectors identified several

items of potential concern. These included:

Pealing and degraded coatings on the containment walls

,

' The use of double backed tape and magnets to hold signs and placards in place

within containment

l

The extensive use of caution tape and foam insulation as an occupational safety

and health precaution for permanently installed interferences within containment

,

The extensive use of radiological tape and glued or self-adhesive labels on

systems and structures in containment

The use of paper (fibrous) caution and maintenance request tags in containment

The poor housekeeping control over old wires, tape, and general debris in some

portions of containment.

The inspectors reviewed Procedure CPS 1019.05, " Control of Transient

Equipment / Materials," Revision 3, and found that it did not address many of the

items discussed above. The inspectors also found that while the procedure

specified limits for transient materials in containment, there was no specified

implementation process to ensure that the cumulative amount of transient material

from all sources would be below the licensee identified threshold for proper ECCS

strainer operation in a post loss of coolant accident (LOCA) environment.

l The inspectors discussed the above issues with the Licensing and Engineering

!

staffs. The inspectors requested information on the environmental qualification of

the coatings and rihesives used in containment, and the documented mialysis that

the presence of large amounts of flexible and semi-rigid materialin containment did

not represent an undue potential challenge to the ECCS strainers. The licensee's

initial response referenced strainer design type considerations rather than the

implementation of ongoing controls. At this time, the inspectors reviewed an

Engineering Evaluation associated with CR 1-9610-033, " Foreign Material in

Suppression Pool Area of Drywell," and found that the CR also focused on design

considerations for ECCS strainers rather than on-going operability considerations.

The inspectors identified their concerns to licensee management who, after

,

i

discussion with the inspectors and independent walkdowns of containment,

acknowledged that Procedure CPS 1019.05 was inadequate for the control of

material which could cause clogging of ECCS strainers under post LOCA conditions.

This conclusion was documented in CR 1-97-05-178. The following CRs regarding

ECCS strainer clogging were also written subsequent to the inspectors involvement

with this is. 3vw; 1-97-05-014,1-97-05-184, and 1-97-05-232.

!

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- 10 CFR Part 50, Appendix B, Criterion V, " Procedures," requires, in part, that

  • - activities affecting quality be prescribed by procedures of a type appropriate to the

circumstances. CPS 1019.05, Revision 3, Section 8.8, was not appropriate to the

i

circumstances in that it failed to identify or provide for adequate control for material

which could clog ECCS strainers in a post LOCA environment, a violation (50-

461/97011-11) of 10 CFR Part 50, Appendix B, Criterion V.

I

The licensee informed the inspectors that they had initiated procurement of

environmentally qualified (EO) adhesives and labels for use in containment at the i

i

end of the inspection period. The licensee also initiated revision of Procedure CPS

,

1019.05 to ensure that it adequately identified and controlled material which could

'

cause ECCS strainer clogging. The licensee had not provided the inspectors an

assessment of the impact of degraded containment coatings, or a corrective action

plan, at the end of the inspection period. ,

'

c. Conclusion ,

,

The inspectors identified that the licensee procedure for controlling material which

could clog ECCS strainers in a post LOCA environment was inadequate. After a

slow initial response to this issue, the licensee initiated actions to resolve the

concem. The issue of degraded containment coatings had not been resolved at the

end of the period. One violation of NRC requirements was identified.

M3 Maintenance Procedures and Documentation

M3.1 Documentation Contained Within Maintenance Packaaes

a. insoection Scope (62707)

The inspectors reviewed Job No. PEMAP1054, "8410.04 Testing for 1 AP41E2C," i

MWR D63102, " Install New Control Switches for Bridge," MWR D70531, " Red Pen

,

!

Sticks at 100%," D71601, " Transmitter is Sending a Low Flow Signal to DCS

Computer," and CR 1-96-12-124, " Questionable Breaker Not Removed From

l System."

b. Observations and Findinas

On December 11,1996, the technicians tested MCCB 1 AP41E2C using Job

,

l No. PEMAP1054. The individuals could not find the stamp which contained

i

information concerning the breaker revision; therefore, they used Procedure CPS

8410.05, " Type HE Molded Case Circuit Breaker Revision Level Test," Revision 4,

to determine the breaker revision. When the breaker appeared not to reset within

five seconds, the technicians marked the surveillance as failed and turned over to

the next shift personnel for disposition. The engineering personnel of the next shift

l

i

found the stamp and the breaker revision on the face of the breaker. Therefore,

Procedure CPS 8410.05 was not re-performed. Procedure CPS 8410.04 was then

,

performed satisfactorily. Detailed resolution and evaluation of this breaker's failure

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' to reset within five seconds were documented in the MWR In addition, CR 1-96-

'* 12-124 was initiated on December 13,1996 to document this discrepancy end

resolution.

A note between Steps 8.10 and 8.11 in Procedure CPS 8410.05 stated, "Within -

5 seconds of breaker trip, manually reset breaker by opening then attempt to close

breaker to verify trip was due to instantaneous trip unit. If breaker will not latch

closed, trip was influenced by the thermal trip unit and can not be considered a

valid instantaneous trip." Step 8.11 stated, "If breaker trips, reset breaker and

close if possible within = 5 second after trip." When the technicians observed that

I

the breaker did not reset within 5 seconds on December 11, this condition showed

-

that the trip was due to a thermal and not an instantaneous trip. Therefore, the

breaker trip was not a valid instantaneous trip. The inspectors reviewed the

i

completed Job No. PEMAP1054 and did not find the documentation acsociated

l

with Procedure CPS 8410.05. The licensee stated that the reasons not to include

documentation associatt 4h Procedure CPS 8410.05 were:

  • Procedure CPS 8410.05 was not a required test because the date and revision

of the breaker were subsequently identified.

l *

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The failure of the breaker to reset within 5 seconds was not a valid failure but

showed that further testing was necessary to determine the instantaneous trip i

set point.

The licensee committed to change the procedure to clarify that breaker revision was

determined by a valid instantaneous trip.

!

The inspectors agreed that the documentation of Procodure CPS 8410.05 of

December 11,1996, did not need to be included in the maintenance package.

However, a violation of 10 CFR Part 50, Appendix B, Criterion V was identified

during review of testing associated with MCCB 1 AP41E2C (Section M2.1).

c. Conclusion

The inspectors did not identify any violations during a review of Job No.

PEMAP1054,

M3.2 Environmental Qualification (EQ) Documentation of Material

a. insoection Scone

The inspectors reviewed Procedure CPS 8492.01, " Cable Termination,"

Revision 21. The review included checklists associated with this procedure, and

Nuclear Station Engineering Department Maintenance Standards for Raychem

material.

)

.

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b. Observations and Findinas

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The inspectors reviewed each section of Procedure CPS 8492.01 to verify the type

and qualification of materials specified for Class 1E components. Procedure CPS

8492.01 required the use of Raychem kits for Class 1E cable insulation or i

termination and the use of either Raychem kits or Okonite tape for non-1E

applications. The Raychem materials specified in the procedure were EQ for 40

years except for Raychem NPKX and NPKP kits. These two kits were not included

in the Nuclear Station Engineering Department Maintenance Standards manual. The

licensee determined that these two kits were also EQ, but were not included in the

,

manual. The licensee committed to initiate a CR and revise the manual.

L

l c. Conclusion -

!

The inspectors concluded that for all Class 1E applications, the licensee appeared to

use EQ qualified materials in accordance with CPS 8492.01.

M3.3 Review of Maintenance Work Packaoe for the Reactor Water Cleanuo System

a. Insoection Scone (62703)

l The inspectors reviewed maintenance work request (MWR) D71146 for the reactor

l

'

water cleanup discharge inboard isolation valve for conformance with the

requirements of CPS 1501.02, " Conduct of Maintenance."

,

b. Observations and Findinas

Operations personnel wrote MWR D71146 to replace the packing on valve

1G33F053. While reviewing the work package, the inspectors identified that both

EM and quality verification (OV) had signed MWR Job Step 8 for replacing parts on

the valve's motor operator per Procedure CPS 8451.05. The inspectors reviewed

the work package and determined that the only part replaced was the limit switch

i

cover gasket.

! The inspectors reviewed Procedure CPS 8451.05, " Corrective Maintenance for

l Limitorque SMB-000 and SMB-00 Actuators," and determined that the procedure

i

did not specifically address the replacement of the limit switch cover gasket.

! However, Procedure CPS 8451.50, " Motor Operated Valve Testing with VOTES,"

!

which maintenance used to test the valve after the packing was replaced (Job

Step 12), contained a specific step for replacing the limit switch cover gasket if

necessary.

l

QV personnel explained to the inspectors that the replacement of the limit switch

cover gasket could be performed using either procedure because some activities

were covered within more than one procedure. Further discussions with QV -

supervision determined that signing multiple job steps when the activity performed

l was covered by more than one procedure was not isolated.

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Since EM and OV personnel did not perform work using Procedure CPS 8451.05 as

  • directed by Job Step 8, Procedure CPS 1501.02, " Conduct of Maintenance,"

required that Job Step 8 be noted as "not applicable." Procedure CPS 1501.02

also required that a note be placed in the back of the MWR stating the reason the

job step was not performed. The failure to comply with Procedure CPS 1501.02 '

constituted a violation of minor significance and is being treated as a Non-Cited

Violation (50 461/97011-12) consistent with Section IV of the NRC Enforcement

Policy. See Section M7.1 for additional discussion of this issue.

c. Conclusions

Both maintenance and QV personnel signed that work was completed using

Procedure CPS 8451.05 when it was actually completed using Procedure CPS

8451.50.

M7 Quality Assurance in Maintenance Activities  !

M7.1 Sensitivity to Quality Record Sion-offs

Sections M1.2 and M3.2 of this report document instances where Quality Record

sign-offs were completed for actions slightly different than actually performed.

While each case was individually minor, the generalissue is of regulatory

significance. The inspectors discussed, with plant management, the need to ensure

that Maintenance and Nuclear Assessment personnel were appropriately sensitive

conceming the accuracy of their sign-offs. Plant Management acknowledged the

importance of such sensitivity.

1

M7.2 OV Sion-off Missed

a. insoection Scoce

On September 17,1996, a step requiring notification of Quality Verification (QV)

personnel was added in Procedure CPS 8492.01 C001, " Cable Termination

Checklist," by Procedure Advance Change (PAC) 0496-96. The inspectors were

concerned that necessary QV activities were not specified in Procedure CPS

8492.01, " Cable Termination" and its associated checklist CPS 8492.01 C001.

The inspectors reviewed revisions of Procedures CPS 8492.01, CPS 8492.01C001

and Nuclear Assessment Procedure (NAP) 110.02, " Quality Verification Planning."

b. Observation and Findinos

Step 2.1.3 in Procedure CPS 8492.01, Revision 20, required the use of the cable

termination checklist (Procedure CPS 8492.01C001, Revision 9), when

maintenance was performed on safety and quality related systems. The checklist

contained eight OV signature blocks for various steps in the procedure.

!

On August 26,1996, Procedures CPS 8492.01, Revision 21 and CPS

8492.01C001, Revision 21 (Revisions 10 through 20 were not used) were issued.

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Step 5.4 in Procedure CPS 8492.01 required notification of QV personnel before

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the performance of this procedure on any Class 1E system or component when OV

1*

was called out on the Authorizing Work Document. In addition, this notification

!

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was to be treated as a QV witness allowing for verification deemed appropriate for

the scope of work being performed. This practice was consistent with NAP

110.02. Step 8.1.2.1 of the procedure also required use.of the checklist for all

l work performed by this procedure. However, Revision 21 of the checklist did not

l contain a QV signoff for personnel to denote QV inspection. Therefore, the

! licensee issued PAC 0496-96 to add signoffs for notifications of QV before

! performing this procedure on Class 1E systems or components.

' Although the signoff for OV personnel was not in Procedure CPS 8492.01 C001,

Revision 21, from August 26 to September 17,1996, the inspectors had

reasonable assurance that necessary QV activities were performed on Class 1E

systems or components because Step 5.4 in CPS 8492.01, Revision 21, was stillin

effect. In addition, any QV requirements would be denoted in work packages as

deemed necessary.

c. Conclusions

The inspectors concluded that from August 26 to September 17,1996, QV

l

activities were performed on Class 1E systems even though sign-offs for OV

l inspections were not in Procedure CPS 8492.01C001 checklist.

M7.3 Review of Maintenance Critiaues

l a. Insoection Scooe (40500)

The inspectors reviewed Critiques PS97-009 and EM 97-010 against the

requirements of Procedure CPS 1016.05, " Conduct and Documentation of

Critiques."

b. Observations and Findinas:

Critioue PS97-009

On April 9,1997, the inspectors observed maintenance work on the "C" RHR

pump. The mechanics had started to remove a drain plug from the seal cooler for

the pump and noted that service water to the seal cooler was still pressurized. The

l

mechanics reinstalled the drain plug, stopped work, and notified their supervision of

the problem. The licensee initiated CR 1-97-04-072 to document the problem, and

that a tagout error had occurred. The inspectors attended the critique, held April 9,

1997, and reviewed the critique report, Critique PS97-009, issued April 30,1997.

During the critique, the licensee determined that the tagout performed for the work

failed to consider the work being performed on the service water side of the seal

cooler, and that the mechanics failed ensure that the tagout was adequate as

, required by Procedure CPS 1014.01, " Safety Tagging." These conclusions were

,

,

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appropriately documented in the critique report. The inspectors determined that the

. licensee's conclusion regarding the primary cause of the error was appropriate.

The failure to adequately prepare or implement the tagout for the RHR C seal

cooler, as required by Procedure CPS 1014.01, was considered a violation of minor

significance and is being treated as a Non-Cited Violation (50-461/97011-13)

consistent with Section IV of the NRC Enforcement Policv.

The inspectors noted that relevant facts established during the critique were not

documented in the critique report. Specifically, having multiple tasks on a single

work document contributed to the failure to identify work on the service water side

i

of the seal cooler when the tagout was developed. The failure to document this

could have led to missed opportunities for desirable corrective actions.

Critioue EM 97-010

Critique EM 97-010 reviewed the circumstances of the MOV damage discussed in

Section M1.3.

~

The inspectors noted that the critique report stated that no apparent procedure

noncompliance or non-conservative operations had occurred during the event. The

inspectors discussed this determination with several individuals who attended the

critique. The inspectors found that the determination of no noncompliance and no

non-conservative operations focused heavily on the procedure in use at the time of

the event. Individuals at the critique placed little emphasis on determining if

requirements delineated in administrative procedures such as " Conduct of

Maintenance" should have prevented the event. As discussed in Section M1.3, the

inspectors identified one noncompliance related to " Conduct of Maintenance." The

inspectors were concerned that this narrow focus reflected inadequate sensitivity

to, and familiarity with, administrative maintenance requirements.

c. Conclusions

The inspectors reviewed two Maintenance critiques and noted opportunities for

improvement in each.

l

111. Enaineerina

E1 Conduct of Engineering

E1.1 Attachment of Scaffoldina to Safetv-Related Pioina Not Analyzed

a. Insoection Scooe (37551)

L

The inspectors observed scaffolding attached to safety-related equipment. The

inspectors reviewed the scaffolding attachment for adequacy of analysis and

.

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adequacy of the scaffolding procedure, Procedure CPS 8901.10, "Scaf fold

Erection /Use/ Dismantling," Revision O.

b. Observations and Findinas

During a tour of the RHR "B" pump room, April 28,1997, the inspectors observed

that scaffolding was attached to the minimum flow line for the RHR "B" pump and

one of the pipe supports for the line. The inspectors reviewed Procedure CPS

8901.10 and determined that the procedure permitted the observed scaffolding

attachment. Specifically, Step 8.3.19.6 and Appendix G of Procedure CPS

8901.10 stated that it was acceptable to attach scaffolding to pipes of 4 inches

diameter and greater. However,in response to questions by the inspectors,

engineering personnel stated that no evaluation had been performed which

demonstrated that the attachment of the scaffolding would not cause undue stress

upon safety-related piping during a seismic event. Design engineering initiated CR

1-97-05-035 to document that no evaluation had been performed and to document

the inadequacy of Procedure CPS 8901.10 and Procedure CPS 1019.05, " Control

of Transient Equipment / Materials," Revision 3. In addition, the licensee inspected

other scaffolding in the plant and identified additional examples of scaffolding

attached to safety-related equipment. 10 CFR Part 50, Appendix B, Criterion V,

" Procedures," requires in part that activities affecting quality be prescribed by

procedures appropriate to the circumstances. The failure of the procedure to

require and evaluation of the additional stress upon the RHR "B" pump minimum

flow line piping is a violation (50-461/97011-14) of 10 CFR Part 50, Appendix B,

Criterion V.

c. Conclusions:

The inspectors identified that the licensee failed to analyze or evaluate the loads on

safety related piping induced by temporary scaffolding. One violation of 10 CFR

Part 50, Appendix B, Criterion V, was identified.

E1.2 Seismic Qualification of Circuit Breaker Cabinets

a. insoection Scoce (37551)

The inspectors reviewed the circumstances associated with implementation of a

procedure for controlling the seismic configuration of safety related circuit breaker

cabinets.

b. Observations and Findinas

The licensee identified that the seismic qualification of safety related breaker

cabinets had been based upon having breakers in each bay of the cabinet. Breakers

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were typically removed from their bays for performance of preventive maintenance

or repair. The licensee identified that the removal of the breaker's weight from the

cabinet affected the critical characteristics of the cabinet during a potential seismic

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event, and that this had the potential to place the cabinet's other safety related

breakers in an unanalyzed condition.

4

The licensee reviewed the original seismic qualification process and performed some l

additional analysis to establish criteria for conditions in which the removal of

breakers from their bays would not affect the operability of the other breakers in l

the cabinet. The identified criteria was compiled into Procedure CPS 1014.11,

l

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"6900/4160/480V Switchgear/ Circuit Breaker Operability Program," Revision 0, j

issued May 2,1997. '

!

On May 5,1997, the licensee recognized that the 480V 1 A unit substation had l

been in non-compliance with the requirements of Procedure CPS 1014.11 since the

!

procedure was issued. In addition, a combination of breaker removals performed

~

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prior to May 2 and on May 5,1997, placed the Division 14160V switchgear into a

condition of non-compliance with Procedure CPS 1014.11. Both electrical cabinets

were promptly declared inoperable, and CRs were written to document the

inadequate implementation planning associated with the issuance of Procedure CPS

1014.11. Corrective actions included the commitment to walk down field i

conditions prior to implementation of new procedures and implementation of a  !

method to track the status of individual breakers within the safety related

switchgear. The failure to ensure that the 480V 1 A unit substation and the 4160V l

Division 1 switchgear were in compliance with Procedure CPS 1014.11 was l

licensee identified and corrective actions were considered appropriate, therefore it is

being treated as a Non-Cited Violation (50-461/97011-15) consistent with

Section Vll.B.1 of the NRC Enforcement Policv.

The inspectors concluded that the licensee exhibited a good safety focus in

identifying the breaker , abinet seismic qualification issue. However, the inspectors  ;

were concerned that the licensee appeared to be using probabilistic risk assessment '

in determining operability criteria. Such an approach would be inconsistent with the

definition of operability contained in TS, and discussed in Generic Letter 91-18.

The inspectors were also concerned with the past operability of safety related

switchgear. These concerns were forwarded to the Office of Nuclear Reactor

Regulation for review, and are considered an inspection follow-up item

(50-461/97011-16) pending a NRC review of the licensee's analysis of electrical

cabinet seismic qualifications and the suitability of the operability control program

established in Procedure CPS 1014.11.

c. Conclusions

The licensee identified a potentially generic concern associated with the seismic

qualification of circuit breaker cabinets when breakers are removed. The inspectors

concluded that the licensee exhibited a good safety focus by identification of this

issue. The implementation of a procedure to address this issue was inadequate,

l and a procedure violation resulted. The inspectors identified concerns with the

licensee's stated approach to assessing cabinet operability, and a follow-up item

was opened pending NRC review of this issue.

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IV. Plant Sucoort

R1 Radiological Protection and Chemistry (RP&C) Controls

R1.1 Minor Weakness.in Usina Small Article Monitor (SAM-9) Identified '

a. Insoection Scoce (83750)

The inspectors observed several personnel use the SAM-9 to release personal items

from the radiological controlled area (RCA).

b. Observations and Findinos

!

The inspectors observed a member of the licensee's staff exit the turbine building  !

and then stop to converse with another staff member who was waiting in line to '

use the SAM-9. The inspectors left the area after monitoring several small articles

and continued to exit the RCA by processing through the personnel contamination

monitors (PCMs). Prior to the inspectors successfully processing through the PCM,

the two individuals discussed above exited the SAM-9 area and entered the PCMs.

Because of the short time which had elapsed, the inspectors were confident that

the individual who was not in line to use the SAM-9 had failed to monitor his

personal items.

The inspectors immediately notified a radiation protection (RP) technician who

confronted the individual prior to exiting the RCA. The individual stated that he had  !

forgotten to use the SAM-9 prior to entering the PCM area. The individual then

returned to the SAM-9 area and processed his item through the monitor. No >

!

contamination was found. The RP technician reminded the individual of the

purpose of the SAM-9 and reinforced the need for attention to detail. No violations

occurred since the individual was reminded to use the SAM-9 prior to him exiting

the RCA.

c. Conclusions

!

,

One example of licensee personnel not immediately processing personal items

!

through the SAM-9 was identified.

R1.2 Contamination Controls Not fully lmolemented

a. Insoection Scone

The inspectors observed an individual reach into a contaminated area without

protective clothing. The inspectors assessed the individual's actions and reviewed

applicable procedure requirements.

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b. Observations and Findinos

d

On May 8,1997, the inspectors observed an individual, inside containment, leaning

into a posted contaminated area and reaching out to tum a metal valve label inside

the contaminated area. Although the individual handled the label, the individual

-

was not wearing gloves nor any other protective clothing. The licensee had defined

l

the activities being performed by the individual as being under a "C" radiological '

classification. The licensee subsequently held a fact finding meeting, documented  ;

on CR 1-97-05-100, which confirmed the inspectors observations. ~

Section 6.0 of Procedure CPS 1024.02, " Radiological Work Control," Revision 4,

specified that personnel performing radiological work were not permitted to deviate  :

from established radiological control requirements without specific written or verbal

guidance from responsible radiation protection personnel. Radiation Worker ,

Information Sheet (RWIS) 5.6, " Minor Radiological Risk Work Rules for Mechanical

Maintenance," dated January 14,1997 specified radiological control requirements

activities with a "C" radiological classification. Instruction 7 of RWIS 5.6 specified

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that protective clothing be worn for entry into Contamination Areas. The failure to

wear protective clothing in a contaminated area was contrary to RWIS 5.6 and CPS  :

1024.02, and is considered a violation (50-461/97011-17) of Technical

Specification (TS) 5.4.1. ,

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c. Conclusions

The inspectors observed that radiological controls were not properly implemented

when an individual reached into a contamination area without protective clothing.

One violation of procedures was identified. 5

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V. Manaaement Meetinas

X1 Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on May 23,1997. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

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\s INSPECTION PROCEDURES USED

!' IP 37551: On-site Engineering

IP 40500: Effectiveness of Licensee Controls in identifying, Resolving, and Preventing

Problems -

IP 61726: Surveillances

IP 61703: Maintenance Observation

IP 62707: Maintenance Observation

IP 71707: Plant Operations

l lP 71750: Plant Support

! IP 83750: Occupational Exposure

IP 92700: Onsite Follow up of Written Reports of Nonroutine Events at Power Reactor

Facilities

IP 92902: Followup - Engineering

IP 92903: Followup - Maintenance

IP 93702: Prompt Onsite Response to Events at Operating Power Reactors

ITEMS OPENED, CLOSED, AND DISCUSSED

Ooened

50-461/97011-01 VIO failure to perform steps as written

50-461/97011-02 NCV inaccurate VD system drawings

50-461/97011-03 VIO failure to lock open EDG support system valves

50-461/97011-04 NCV quality record sensitivity

50-461/97011-05 VIO inadequate shift turnover i

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50-461/97011-06 VIO no restoration on caution tag

50-461/97011-07 NCV incorrect performance of t,urveillance actions

50-461/97011-08 VIO failure to complete an impact matrix

50-461/97011-09 VIO breaker preconditioning

50-461/97011-10 URI identifying material condition issues

50-461/97011-11 VIO control of loose material in containment

50-461/97011-12 NCV quality record sensitivity

50-461/97011-13 NCV inadequate tagout

50-461/97011-14 VIO scaffolding loads on safety related piping l

50-461/97011-15 NCV seismic qualification of switchgear 1

50-461/97011-16 IFl assessment of electrical cabinet operability

50-461/97011-17 VIO contamination controls

Closed

50-461/97011-02 NCV inaccurate VD system drawings

50-461/97011-04 NCV quality record sensitivity

50-461/97011-07 NCV incorrect performance of surveillance actions

50-461/97011-12 NCV quality record sensitivity

l 50-461/97011-13 NCV inadequate tagout

l 50-461/97011-15 NCV seismic qualification of switchgear

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PERSONS CONTACTED

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Licensee -

W. Connell, Vice President

W. Romberg, Assistant Vice President

P. Yocum, Manager - Clinton Power Station

D. Thompson, Manager - Nuclear Station Engineering Department

R. Phares, Assistant to the Vice President

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