ML20207S483

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Monthly Operating Rept for Feb 1987
ML20207S483
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 02/28/1987
From: Bregni L
DETROIT EDISON CO.
To:
Shared Package
ML20207S480 List:
References
NUDOCS 8703190527
Download: ML20207S483 (4)


Text

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OPERATING DATA REPORT DOCKET NO. 50-341 COMPLETED BY L.P.Bregni DATE March 13 ,1987 TELEPHONE (313)586-1617 OPERATING STATUS  !

1. UNIT NAME: Fermi 2 l Notes l
2. REPORTING PERIOD: February l l 3 LICENSED THERMAL POWER (MWt): 3292 l l l

! .4. NAMEPLATE RATING (GROSS MWe): 1215 l l

5. DESIGN ELECT RATING (Net MWe): 1093 I I
6.
  • l

( MAX DEPENDABLE CAP (GROSS MWe): l

  1. l 7 MAX DEPENDABLE CAP (Net MWE): l
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS: None l 9 POWER LEVEL TO WHICH RESTRICTED, IF ANY (MWe Net):- 546.5
10. REASONS FOR RESTRICTION, IF ANY: Fermi 2 is in the startup test phase I and is currently authorized to operate not in excess of 50% of rated thermal power. (Ref. A. B. Davis letter of February 16, 1987).

THIS MONTH YR TO DATE CUMULATIVE

11. HRS IN REPORTING PERIOD 672 1416 3850 9
12. HRS REACTOR WAS CRITICAL 625.9 987.6 1857.4
13. REACTOR RESERVE SHUTDOWN HRS 0 0 0
14. HOURS GENERATOR ON-LINE 572.8 626.9 756.4
15. UNIT RESERVE SHUTDOWN HOURS 0 0 0 l
16. GROSS THERMAL ENERGY GEN (MWH) 371,136 495,264 718,512
17. GROSS ELECT ENERGY GEN (MWH) 71,852 77,472 87,922
18. NET ELECT ENERGY GEN (MWH) 55,558 47,863 21,904
19. UNIT SERVICE FACTOR N/A N/A N/A
20. UNIT AVAILABILITY FACTOR N/A N/A N/A
21. UNIT CAP FACTOR (USING MDC NET) N/A N/A N/A
22. UNIT CAP FACTOR (USING DER NET) N/A N/A N/A N/A N/A N/A
23. UNIT FORCED OUTAGE RATE
24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, DURATION OF EACH)

Maintenance Modification Outage, Completion of Test Condition 2, 14 days

25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: N/A
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

FORECAST ACHIEVED INITIAL CRITICALITY 06/20/85 06/21/85 INITIAL ELECTRICITY 10/01/86 09/21/86 COMMERCIAL OPERATION 05/01/87 8703190527 870313 PDR ADOCK 05000341 R PDR l

. AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-341 UNIT FERMI 2 DATE March 13, 1987 COMPLETED BY L. P. Bregni

-TELEPHONE (313) 586-1617 MONTH February DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 98 17 83 2 99 18 78 3 112 19 97 4 111 20 111 5 101 21 105 6 106 22 110 7 85 23 26 8 120 24 118 9 37 25 147 10 72 26 186 11 83 27 0 12 96 28 0 13 104 29 N/A

! N/A 14 75 30 15 100 31 N/A 16 92

= '

UNIT SHUTDOWNS AND POWE"3 CEDUCTIONS DOCKET NO. 50-341 D' ATE March 13. 1987 UNIT NAME Fermi 2 COMPLETED BY- L. P. Bregni .

'SLEPHONE (313)586-1617 REPORT MONTH February METHOD OF LER SYS COMP CAUSE & CORRECTIVE NO. DATE TYPE DUR REASON SHUTTING DOWN NO. CODE CODE ACTION TO PREVENT (1) (HRS) (2) THE REACTOR- (4) (5) RECURRENCE (3) 87-03 870216 F 3.2 A 9 N/A . HA GENERAD Reactor was not shut down. Turbine Generator tripped due to the per-formance of procedure 27.112.04 (Turbine Generator Valves ~ Low VAC on Load Test). The purpose of this procedure is to verify the opera-bility of the Turbine Generator Low Condenser Vacuum Trip Circuitry.

The procedure has been revised to prevent inadvertant turbine trips.

87-04 870217 F 10.3' A 9 N/A HA GENERAD Reactor was not shut down. Gener-ator was shut down to investigate a-possible ground on field. No evidence of a ground fault was

. discovered.

(1) F: FORCED (2) REASON: (3) METHOD: .(4) EXHIBIT G - INSTRUCTIONS S: SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - MANUAL SCRAM ENTRY SHEETS FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM EVENT REPORT (LER) FILE D - REGULATORY RESTRICTION 4 - CONTINUED (NUREG-0161)

E - OPERATOR TRAINING & LICENSE EXAMINATION 5 - REDUCED LOAD F - ADMINISTRATIVE 9 - OTHER G.- OPERATIONAL ERROR (EXPLAIN)

H - OTHER (EXPLAIN) (5) EXHIBIT 1 - SAME SOURCE

IMIT SHUTDOWNS AND POWEJ EEDUCTIONS

?

DOCKET NO. 50-341 DATE March 13. tr87  ;

1 UNIT NAME Farmi 2' COMPLETED CY- L. P. Pr'ani TELEPHONE (313)S86-1617 REPORT MONTH February METHOD OF LER SYS COMP CAUSE & CORRECTIVE-NO. DATE TYPE DUR REASON . SHUTTING DOWN NO. CODE CODE ACTION TO PREVENT (1) (HRS) (2) THE REACTOR (4) (5) RECURRENCE (3) 87-05 870218 F 5.3 A 9 N/A HA GENERAD Reactor was not shut down. Genera-tor was shut down again for addi-tional investigation of a possible ground fault. No evidence of a fault was found.

87-06 870223 F 22.2 A 9 N/A HA GENERAD Reactor was not shut down. Genera-tor automatically shut down. -The cause of the trip is att11 under investigation.

87-07 870226 F 58.4 A 3 87-002 HA .GENERAD Turbine trip and subsequent reac-tor was due to a generator negative ground fault. The most probable cause is that an aluminum strip in the. iso phase bus duct broke free and made contact with the bos which resulted in a ground. fault. During a future outage all other aluminum strips located in the iso phase cooling ducts.will be removed.

(1) F: FORCED (2) REASON: (3) METHOD: (4) EXHIBIT G - INSTRUCTIONS S: SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2'- MANUAL SCRAM . ENTRY SHEETS FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM EVENT REPORT (LER). FILE D - REGULATORY RESTRICTION 4 - CONTINUED (NUREG-0161)

E - OPERATOR TRAINING & LICENSE EXAMINATION 5 - REDUCED LOAD F - ADMINISTRATIVE 9 - OTHER G.- OPERATIONAL ERROR (EXPLAIN)

H - OTHER (EXPLAIN) (5) EXHIBIT 1 - SAME SOURCE