ML20207S491

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Revised Monthly Operating Rept for Nov 1986
ML20207S491
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 11/30/1986
From: Bregni L
DETROIT EDISON CO.
To:
Shared Package
ML20207S480 List:
References
NUDOCS 8703190544
Download: ML20207S491 (3)


Text

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4

-+' OPERATING DATA REPORT

~~'

I DOCKET NO. 50-341 COMPLETED BY L.P.Bregni DATE March 13, 1987 TELEPHONE (313)586-1617 OPERATING STATUS

1. UNIT NAME:' Fermi 2 INotes l
2. REPORTING PERIOD: November l l 3 LICENSED THERMAL POWER (MWt):' 3292 l l

., 4. NAMEPLATE RATING (GROSS MWe): 1215 l l

5. DESIGN ELECT RATING (Net MWe): 1093 I I
6. MAX DEPENDABLE CAP (GROSS MWe): # l l MAX DEPENDABLE CAP (Net MWE): # l l 7
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS: None 9 POWER LEVEL TO WHICH RESTRICTED, IF ANY (MWe Net): 218.6
10. REASONS FOR RESTRICTION, IF ANY
Fermi 2 is in the startup test phase and is currently authorized to operate not in excess of 20% of rated

!~ thermal power. (Ref. J. G. Keppler letter of September 12, 1986)

THIS MONTH YR TO DATE CUMULATIVE

11. HRS IN REPORTING PERIOD 720 1690.9 1690.9

! 12. HRS REACTOR WAS CRITICAL 159 1 560.9 560.9

13. REACTOR RESERVE SHUTDOWN HRS 0 0 0
14. HOURS GENERATOR ON-LINE 26.0 95.8 95.8

, 15. UNIT RESERVE SHUTDOWN HOURS 0 0 0

16. GROSS THERMAL ENERGY GEN (MWH) 36,096 167,568 167,568 l.

! 17. GROSS ELECT ENERGY GEN (MWH) 2,020 7,640 7,640

18. NET ELECT ENERGY GEN (MWH) -6,723 -17,266 -17,266
19. UNIT SERVICE FAC10R N/A N/A N/A
20. UNIT AVAILABILITY FACTOR N/A N/A N/A i 21. UNIT CAP FACTOR (USING MDC NET) N/A N/A N/A
22. UNIT CAP FACTOR (USING DER NET) N/A N/A N/A
23. UNIT FORCED OUTAGE RATE N/A N/A N/A
24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, DURATION OF EACH): NONE 3
25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: 12/16/86
26. UNITS IN TEST STATUS (PRIOR TO COMERCIAL OPERATION):

FORECAST ACHIEVED INITIAL CRITICALITY 06/20/85 06/21/85 INITIAL ELECTRICITY 10/01/86 09/21/86 l

CO MERCIAL OPERATION 05/01/87 "To Be determined 8703190544 870313

PDR ADOCK 05000341 R PDR i

. AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-341 UNIT FERMI 2 DATE March 13, 1987 COMPLETED BY L. P. Bregni TELEPHONE (313) 586-1617 HONTH November DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 75 17 0 2 75 18 0

'3 0 19 0 4 0 20 0 5 0 21 0 6 0 22 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 11 0 27 0 12 0 28 0 13 0 29 0 14 0 30 0 15 0 31 N/A 16 0

~ '

, 7

~ i s

' UNIT SHUTDOWNS AND POWER E EDUCTIONS '. -

DOCKET NO. 50-341 DATE ' March 13.'1987 UNIT NAME Fermi 2 COMPLETED SY L. P. Brooni TELEPHONE (313)586-1617-REPORT MONTH November ,

METHOD OF ' LER SYS COMP CAUSE & CORRECTIVE NO. DATE TYPE DUR REASON SHUTTING DOWN NO. CODE CODE ACTION TO PREVENT (1) (HRS) (2) THE REACTOR (4) (5) RECURRENCE (3) i 86-04 861102 F 694.0 A 2 N/A. HC HTEXCHO Shutdown to repair the cause'of excessive air..in-leakage into the condenser. Outage scope haw been expanded to include installation of new relief valves to prevent future overpressurization of the condensate return line. On November 17 1986-'

overpressurization of this.line

-caused an expansion joint to. rupture and damaged a penetration in the Condensate Storage Tank. Reported in LER 86-045 dated January 12, 1987.

(1) F: FORCED (2) REASON: (3) METHOD: (4) EXHIBIT G - INSTRUCTIONS S SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA-B - MAINTENANCE OR TEST 2 - MANUAL SCRAM ENTRY SHEETS'FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM. -EVENT REPORT (LER) FILE D - REGULATORY RESTRICTION 4 - CONTINUED (NUREG-0161)-

E - OPERATOR TRAINING & LICENSE EXAMINATION 5 - REDUCED LOAD, F - ADMINISTRATIVE 9 - OTHER G.- OPERATIONAL ERROR (EXPLAIN) .;

H - OTHER (EXPLAIN) (5) EXHIBIT I - SAME SOURCE h

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