ML20207S491

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Revised Monthly Operating Rept for Nov 1986
ML20207S491
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 11/30/1986
From: Bregni L
DETROIT EDISON CO.
To:
Shared Package
ML20207S480 List:
References
NUDOCS 8703190544
Download: ML20207S491 (3)


Text

.

4 OPERATING DATA REPORT

-+'

I DOCKET NO. 50-341 COMPLETED BY L.P.Bregni

~~'

DATE March 13, 1987 TELEPHONE (313)586-1617 OPERATING STATUS 1.

UNIT NAME:'

Fermi 2 INotes l

2.

REPORTING PERIOD: November l

l 3

LICENSED THERMAL POWER (MWt):' 3292 l

l 4.

NAMEPLATE RATING (GROSS MWe):

1215 l

l 5.

DESIGN ELECT RATING (Net MWe): 1093 I

I 6.

MAX DEPENDABLE CAP (GROSS MWe):

l l

7 MAX DEPENDABLE CAP (Net MWE):

l l

8.

IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:

None 9

POWER LEVEL TO WHICH RESTRICTED, IF ANY (MWe Net):

218.6

10. REASONS FOR RESTRICTION, IF ANY: Fermi 2 is in the startup test phase and is currently authorized to operate not in excess of 20% of rated

!~

thermal power.

(Ref. J. G. Keppler letter of September 12, 1986)

THIS MONTH YR TO DATE CUMULATIVE

11. HRS IN REPORTING PERIOD 720 1690.9 1690.9
12. HRS REACTOR WAS CRITICAL 159 1 560.9 560.9
13. REACTOR RESERVE SHUTDOWN HRS 0

0 0

14. HOURS GENERATOR ON-LINE 26.0 95.8 95.8
15. UNIT RESERVE SHUTDOWN HOURS 0

0 0

l.

16. GROSS THERMAL ENERGY GEN (MWH) 36,096 167,568 167,568
17. GROSS ELECT ENERGY GEN (MWH) 2,020 7,640 7,640
18. NET ELECT ENERGY GEN (MWH)

-6,723

-17,266

-17,266

19. UNIT SERVICE FAC10R N/A N/A N/A
20. UNIT AVAILABILITY FACTOR N/A N/A N/A
21. UNIT CAP FACTOR (USING MDC NET)

N/A N/A N/A i

22. UNIT CAP FACTOR (USING DER NET)

N/A N/A N/A

23. UNIT FORCED OUTAGE RATE N/A N/A N/A
24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, DURATION OF EACH): NONE
25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: 12/16/86 3
26. UNITS IN TEST STATUS (PRIOR TO COMERCIAL OPERATION):

FORECAST ACHIEVED INITIAL CRITICALITY 06/20/85 06/21/85 l

INITIAL ELECTRICITY 10/01/86 09/21/86 CO MERCIAL OPERATION 05/01/87 "To Be determined 8703190544 870313 PDR ADOCK 05000341 i

R PDR

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-341 UNIT FERMI 2 DATE March 13, 1987 COMPLETED BY L. P. Bregni TELEPHONE (313) 586-1617 HONTH November DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1 75 17 0

2 75 18 0

'3 0

19 0

4 0

20 0

5 0

21 0

6 0

22 0

7 0

23 0

8 0

24 0

9 0

25 0

10 0

26 0

11 0

27 0

12 0

28 0

13 0

29 0

14 0

30 0

15 0

31 N/A 16 0

~

7

~

i s

' UNIT SHUTDOWNS AND POWER E EDUCTIONS '.

DOCKET NO.

50-341 DATE

' March 13.'1987 UNIT NAME Fermi 2 COMPLETED SY L.

P.

Brooni TELEPHONE (313)586-1617-REPORT MONTH November METHOD OF

' LER SYS COMP CAUSE & CORRECTIVE NO.

DATE TYPE DUR REASON SHUTTING DOWN NO.

CODE CODE ACTION TO PREVENT (1)

(HRS)

(2)

THE REACTOR (4)

(5)

RECURRENCE (3) i 86-04 861102 F

694.0 A

2 N/A.

HC HTEXCHO Shutdown to repair the cause'of excessive air..in-leakage into the condenser. Outage scope haw been expanded to include installation of new relief valves to prevent future overpressurization of the condensate return line.

On November 17 1986-'

overpressurization of this.line

-caused an expansion joint to. rupture and damaged a penetration in the Condensate Storage Tank.

Reported in LER 86-045 dated January 12, 1987.

(1) F: FORCED (2) REASON:

(3) METHOD:

(4) EXHIBIT G - INSTRUCTIONS S SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA-B - MAINTENANCE OR TEST 2 - MANUAL SCRAM ENTRY SHEETS'FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM.

-EVENT REPORT (LER) FILE D - REGULATORY RESTRICTION 4 - CONTINUED (NUREG-0161)-

E - OPERATOR TRAINING & LICENSE EXAMINATION 5 - REDUCED LOAD, F - ADMINISTRATIVE 9 - OTHER G.- OPERATIONAL ERROR (EXPLAIN)

SAME SOURCE H - OTHER (EXPLAIN)

(5) EXHIBIT I -

h

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