ML20207S494
| ML20207S494 | |
| Person / Time | |
|---|---|
| Site: | Fermi |
| Issue date: | 01/31/1987 |
| From: | Bregni L DETROIT EDISON CO. |
| To: | |
| Shared Package | |
| ML20207S480 | List: |
| References | |
| NUDOCS 8703190549 | |
| Download: ML20207S494 (3) | |
Text
-
OPERATING DATA REPORT 4
DOCKET NO.- 50-341 COMPLETED BY L. P. Bregni
-DATE March 13, 1987 TELEPHONE (313)586-1617 OPERATING STATUS 1.
UNIT NAME:
Fermi 2 l Notes l
2.
REPORTING PERIOD: January l
l 3
LICENSED THERMAL POWER (MWt): 3292 l
l 4.
NAMEPLATE RATING (GROSS MWe):
1215 l
I 5
DESIGN ELECT RATING (Net W e): 1093
_ l I
6.
MAX DEPENDABLE CAP (GROSS MWe):
l l
J 7
MAX DEPENDABLE CAP (Net MWe):
l l
8.
IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS: None 9
POWER LEVEL TO WHICH RESTRICTED, IF ANY (MWe Net):
218.6
- 10. REASONS FOR RESTRICTION, IF ANY: Fermi 2 is in the startup test phase and is currently authorized to operate not in excess of 20% of rated thermal-power.
(Ref. J. G. Keppler letter of September 12, 1986)
THIS MONTH YR '!O DATE CUMULATIVE
- 11. HRS IN REPORTING PERIOD 744 744 3178.9
- 12. HRS REACTOR WAS CRITICAL 361.7 361.7 1,231.5 i
- 13. REACTOR RESERVE SHUTDOWN HRS 0
0 0
i
- 14. HOURS GENERATOR ON-LINE 54.1 54.1 183.6
)
- 15. UNIT RESERVE SHUTDOWN HOURS 0
0 0
- 16. GROSS THERMAL ENERGY GEN (HWH) 124,128 124,128 347,376
- 17. GROSS ELECT ENERGY GEN (MWH) 5,620 5,620 16,070
- 18. NET ELECT ENERGY GEN (MWH)
-7,695
-7,695
-33,654 i
- 19. UNIT SERVICE FACTOR N/A N/A N/A
N/A N/A N/A
- 22. UNIT CAP FACTOR (USING DER NET)
N/A N/A N/A
- 23. UNIT FORCED OUTAGE RATE N/A N/A N/A l
- 24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, DURATION OF EACH) l Maintenance Modification Outage, Completion of Test Condition 2, 14 days l-
- 25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: N/A
- 26. UNITS IN TEST STATUS (PRIGH TO COMMERCIAL OPERATION):
FORECAST ACHIEVED INITIAL CRITICALITY 06/20/85 06/21/85 INITIAL ELECTRICITY 10/01/86 09/21/86 COMERCIAL OPERATION 05/01/87 8703$90 b Y O Sh PDR ADOCK 05000341 R
P5R
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-341 UNIT FERMI 2 DATE March 13, 1987 COMPLETED BY L. P. Bregni TELEPHONE (313) 586-1617 MONTH January DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 95 17 0
2 81 18 0
3 0
19 0
4 0
20-0 5
60 21 0
6 0
22 0
7 0
23 0
8 0
24 0
9 0
25 0
10 0
26 0
11 0
27 0
12 0
28 0
13 0
29 0
14 0
30 0
15 0
31 68 16 0
l I
I 1
UNIT SHUTDONNS AND POWER REDUCTIONS I
DOCKET NO.
50-341 DATE March 13. 1987 l
(
UNIT NAME Fermi 2 COMPLETED BY L.
P.
Brenni l
TELEPHONE (313)S86-1617 REPORT MONTH January I
l l
METHOD OF LER SYS COMP CAUSE & CORRECTIVE NO.
DATE TYPE DUR REASON SHUTTING DOWN NO.
CODE CODE ACTION TO PREVENT (1)
(HRS)
(2)
THE REACTOR (4)
(5)
RECURRENCE (3) 87-01 870102 F
71.3 A
9 N/A CC PIPEXXA Reactor was not shut down.
The l
turDine-generator was shut down I
after three small steam leaks were i
\\
detected. The leaks were from l
broken spare instrument lines located between the turbine l
l control valves and the turbine -
I generator. Steam is being directed to the main condenser.
l j
87-02 ( 870105 F
618.6 A
2 N/A CC PIPEXxA On January 5 testing was completed I
on automatic voltage regulator A while the turbine generator was on line.
Shut down to inspect and repair welds on instrument taps attached to the main steam lines.
Outage scope was expanded to in-c1ude work on the Control Center HVAC Chiller.
1 (1) F: FORCED (2) REASON:
(3) METHOD:
(4) EXHIBIT G - INSTRUCTIONS S: SCHEDULED A - EOUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - MANUAL SCRAM ENTRY SHEETS FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM EVENT REPORT (LER) FILE D - REGULATORY RESTRICTION 4 - CONTINUED (NUREG-0161)
E - OPERATOR TRAINING & LICENSE EXAMINATION 5 - REDUCED LOAD i
F - ADMINISTRATIVE 9 - OTHER i
G.- OPERATIONAL ERROR (EXPLAIN)
H - OTHER (EXPLAIN)
(5) EKH1 BIT I - SAME SOURCE l
,