ML20207S492
| ML20207S492 | |
| Person / Time | |
|---|---|
| Site: | Fermi |
| Issue date: | 12/31/1986 |
| From: | Bregni L DETROIT EDISON CO. |
| To: | |
| Shared Package | |
| ML20207S480 | List: |
| References | |
| NUDOCS 8703190546 | |
| Download: ML20207S492 (3) | |
Text
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
DOCKET NO. 50-341 COMPLETED BY L.P.Bregni DATE March 13, 1987 TELEPHONE (313)586-1617 OPERATING STATUS 1.
UNIT NAME:
Fermi 2 l Notes l
2.
REPORTING PERIOD: December l
l 3
LICENSED THERMAL POWER (MWt): 3292 l
l 4.
NAMEPLATE RATING (GROSS MWe):
1215 l
l 5.
DESIGN ELECT RATING (Net MWe): 1093 l
l 6.
MAX DEPENDABLE CAP (GROSS MWe):
l l
7 MAX DEPENDABLE CAP (Net MWe):
l l
8.
IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS: None 9.
POWER LEVEL TO WHICH RESTRICTED, IF ANY (MWe Net):
218.6
- 10. REASONS FOR RESTRICTION, IF ANY: Fermi 2 is in the startup test phase and is currently authorized to operate not in excess of 20% of rated thermal power.
(Ref. J. G. Keppler letter of September 12, 1986)
THIS MONTH YR TO DATE CUMULATIVE
- 11. HRS IN REPORTING PERIOD 744 2434.9 2434.9
- 12. HRS REACTOR WAS CRITICAL 308.9 869.8 869.8
- 13. REACTOR RESERVE SHUTDOWN HRS 0
0 0
- 14. HOURS GENERATOR ON-LINE 33 7 129.5 129.5
- 15. UNIT RESERVE SHUTDOWN HOURS 0
0 0
- 16. GROSS THERMAL ENERGY GEN (MWH) 55,680 223,248 223,248
- 17. GROSS ELECT ENERGY GEN (MWH) 2,810 10,450 10,450
- 18. NET ELECT ENERGY GEN (MWH)
-8,693
-25,959
-25,959
- 19. UNIT SERVICE FACTOR N/A N/A N/A
- 20. UNIT AVAILABILITY FACTOR N/A N/A N/A
N/A N/A N/A
- 22. UNIT CAP FACTOR (USING DER NET)
N/A N/A N/A
- 23. UNIT FORCED OUTAGE RATE N/A N/A N/A
- 24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, DURATION OF EACH)
None
- 25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: N/A
- 26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
FORECAST ACHIEVED INITIAL CRITICALITY 06/20/85 06/21/85 INITIAL ELECTRICITY 10/01/86 09/21/86 COMMERCIAL OPERATION 05/01/87
- To Be determined h IM h 05000341 870313 R
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-341 UNIT FERMI 2 DATE March 13, 1987 COMPLETED BY L. P. Bregni TELEPHONE (313) 586-1617 MONTH December DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 0
17 0
2 0
18 0
3 0
19 0
4 0
20 0
5 0
21 0
6-0 22 0
7 0
23 0
8 0
24 0
9 0
25 0
10 0
26 0
11 0
27 0
12 0
28 0
13 0
29 0
14 0
30 68 15 0
31 55 16 0
UNIT SHUTDOWNS AND POWER.EEDUCTIONS :
DOCKET NO.
50-341 DATE March 13. 1987 j
UNIT NAME Fermt 2 COMPLETED BY L.
P.
Bregni
.i TELEPHONE.
(313)585-1617 r
REPORT MONTH December METHOD OF LER SYS COMP CAUSE'& CORRECTIVE NO.
DATE TYPE DUR REASON SHUTTING DOWN NO.
CODE CODE ACTION TO PREVENT (1)
(HRS)
(2)
THE REACTOR (4)
(5)
RECURRENCE (3) 86-04 861102 F
710.7 A
4 N/A HC HTEXCHO Shutdown continued from last month to repair the cause of excessive air in-leakage into the condenser and to install new relief valves to prevent future overpressuriza-tion of the condensate return line.
(1) F: FORCED (2) REASON:
(3) METHOD:
(4) EXHIBIT G - INSTRUCTIONS S: SCHEDULED A - EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - MANUAL SCRAM ENTRY SHEETS FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM EVENT REPORT (LER) FILE D-REGULATORY RESTRICTION 4 - CONTINUED (NUREG-0161)
E - OPERATOR TRAINING & LICENSE EXAMINATION 5 - REDUCED LOAD F - ADMINISTRATIVE 9 - OTHER G.- OPERATIONAL ERROR (EXPLAIN)
H - OTHER (EXPLAIN)
(5) EXHIBIT I - SAME SOURCE I
...