ML20204F795

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Monthly Operating Rept for Feb 1999 for Hope Creek Generating Station,Unit 1.With
ML20204F795
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 02/28/1999
From: Bezilla M, Hassler D, Todd F
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LR-N99118, NUDOCS 9903250370
Download: ML20204F795 (9)


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OPSEG Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit MAR 151999 LR-N99118 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

MONTHLY OPERATING REPORT I HOPE CREEK GENERATING STATION UNIT 1 DOCKET NO. 50-354 In compliance with Section 6.9, Reporting Requirements for the Hope Creek Technical  ;

Specifications, the operating statistics for February 1999 are being forwarded. Also being forwarded to you, pursuant to the requirements of 10CFR50.59(b), is the summary of changes, tests, and experiments that were implemented during February 1999.

Sincerely, s

Mark B. Bezilla General Manager -

Hope Creek Operations [

l DVH k Attachments C Distribution T

9903250370 990228 ~

PDR ADOCK 05000354 R PDR-- J

.au-Thepmerisin prh:nk 95 2168 REV 694

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NUMBER

I SECTION OF PAGES '

Operating Data Report.. .. . .. . . . . . . .......................................1 I Monthly Operating Summary.......... .... .... . ..... ... .......... . . ... ,, ,, . 1 Summary of Changes, Tests, and Experiments... ..... ................2 i

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i DATE: 03/09/99

,- COMPLETED BY: F.Todd TELEPHONE: (609) 339-1316 Reporting Period February 1999 OPERATING DATA REPORT I Design Electrical Rating (MWe-Net)

Maximum Dependable Capacity (MWe-Net) 1031 Month Year-to-date Cumulative I No. of hours reactor was critical 289 l1033 l 90162 l No. of hours generator was on line (service 288 l1032 88641 .

I hours) l Unit reserve shutdown hours 0 l0 l0 l Net Electrical Energy (MWH) 297543 l 1074548 l 89672069 l UNIT SHUTDOWNS NO. DATE TYPE DURATION REASON METHOD OF CORRECTIVE ACTIONI F= FORCED (HOURS) (1) SHUTTING COMMENT S= SCHEDULED DOWN THE REACTOR (2) 1 2/13/99 S 360 C 1 Refuel Outage 2/28/99 (1) Reason (2) Method I

A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip / Scram C - Refueling 3 - Automatic TripiScram D - Regulatory Restriction 4 - Continuation E - Operator Training / License Examination 5 - Other (Explain)

F - Administrative '

G - Operational Error (Explain)

H - Other

DOCKET NO.; 50-354

, UNIT: Hope Cree _k DATE: 03/09/99 COMPLETED BY: D. Hassler TELEPHONE: {609) 339-1445 Summary Of Monthly Operating Experience

. Hope Creek entered the month of January at approximately 100% reactor l power.

. Restart from RF08 is expected on March 30,1999.

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DOCKET NO.:50-354 UNIT: Hope Creek DATE:03/09/99 COMPLETED BY:D. Hassler TELEPHONE: (609) 339-1989

SUMMARY

OF CHANGES. TESTS. AND EXPERIMENTS

.FOR THE HOPE CREEK GENERATING STATION MONTH February 1999 The following items completed during February 1999 have been evaluated to determine:

1. If the prcbability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the safety analysis report may be increased; or
2. If a possibility for an accident or malfunction of a different type than any evaluated previously in the safety analysis report may be crested; or
3. If the margin of safety as defined in the basis for any technical specification is reduced.

The 10CFR50.59 Safety Evaluations showed that these items did not create a new safety hazard to the plant nor did they affect the safe shutdown of the reactor. These items did not change the plant effluent releases and did not alter the existing environmental impact. The 10CFR50.59 Safety Evaluations determined that no unreviewed safety or environmental questions are involved.

Desian Chanaes Summary of Safety Evaluations 4EC-3203, Package 3, Iron Reduction Test Skid Removal. This design change removed the iron filter and ion exchange test skid. When in operation the test skid took a draw off of the discharge side of Primary Condensate Pumps and returned it to the suction side.

The design basis, system descriptions, system classifications, etc of the Condensate l and Condensate Demineralizer systems, as described in the UFSAR, will not be  !

affected. This design change does not increase the possibility or consequences of any accident or malfunction, does not reduce the margin of safety, and therefore, does not involve an Unreviewed Safety Question. ,

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SUMMARY

OF CHANGES. TESTS AND EXPERIMENTS l FOR THE HOPE CREEK GENERATING STATION - Cont'd t

4EC-3538, Packages 3 and 4, RHR and CORE Spray Suction Strainers. This design change installs Emergency Core Coosng System suction strainers in the suppression pool with new strainers for the Residual Heat Removal (RHR) and Core Spray (CS) pumps.

This design change replaces the existing bolt-on Zurn strainers with larger Performance Contracting, Inc. (PCI) stacked disk strainers. The new larger PCI suction strainer provides increased surface area and thus increases the flow area of the ,

strainer. The new strainers meet the same function and flow capacity of the plant systems. This design change does not increase the possibility or consequences of any accident or malfunction, does not reduce the margin of safety, and therefore, does not involve an Unreviewed Safety Question.

4EC-3658, Package 1, Hope Creek Plant Historian. This design change installed the Plant Historian System (PHS) which will collect data frorn CRIDS and store the data for historical information.

1 The PHS system consists of a digital equipment computer server, computer  !

workstations, color printers and an interface card to the CRIDS computer. The functions of the plant process computers were not changed by this design change and this design change does not increase the possibility or consequences of any accident j or malfunction, does not reduce the margin of safety, and therefore, does not involve l an Unreviewed Safety Question.

Temporary Modifications Summary of Safety Evaluations i

There were no reportable changes in this category implemented during January 1999.

Procedures Summary of Safety Evaluations NC.NA-AP.ZZ-0024(Q) Revision 9, Radiation Protection Program. This procedure revision addressed minor organizaaon changes as well as changes to conform to 10 CFR 20.

The organizational changes reflect the current organization structure. The revision also changed the doses to minors and pregnant members of the public making them consistent with 10 CFR 20 that was effective October 24,1998. This procedure revision does not increase the possibi'ity or consequences of any accident or malfunction, does not reduce the margin of safety, and therefore, does not involve an Unreviewed Safety Question.

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3.UMMARY OF CHANGES. TESTS AND EXPERIMENTS FOR THE HOPE CREEK GENERATING STATION - Cont'd HC.OP-SO.SB-0001(Q) Revision 15, Reactor Protection System Operation. This procedure revisicn addresses a change that affects the Reactor Protection System (RPS) scram signa! generated when the mode switch is placed in the shutdown position. This signal is addressed in the UFSAR and is not a Technical Specifications requirement. l During the course of a refueling outage, it is necessary to move the mode switch between the refueling and shutdown positions for testing and surveillance purposes and to conduct core alterations. The procedure revision facilitates bypassing of the RPS scram signal generated when the mode switch is placed in the shutdown position. l All other scram signals remain unaffected and the rod block generated when the mode switch is in the shutdown position remains in effect. This change will allow the signal to be bypassed and therefore inoperable in Mode 5. I accordance with the prerequisites of the procedure, the evolution will not be performed unless permission has been l obtained from the Operations Superintendent, all control rods have been inserted (or the core is off-loaded) and no core alterations are in progress. This procedure revision does not increase the possibility or consequences of any accident or malfunction, does not reduce the margin of safety, and therefore, does not involve an Unreviewed Safety Question.

UFSAR Chanae Notices Summarv of Sciety Evaluations Change Notice HCN 98-037, NBU Reorganization- Maintenance / Engineering.

This UFSAR change shifted selected programmatic responsibilities between the Nuclear Maintenance and Nuclear Engineering Departments.

This UFSAR change does not increase the possibility or consequences of any accident or malfunction, does not reduce the margin of safety, and therefore, does not involve an Unreviewed Safety Question. .

J Change Notice HCN 98-039, FRVS Testing Compliance with Reg Guide 1.52. This )

UFSAR change was made to address issues related to testing of the Hope Creek Filtration, Recirculation and Ventilation System (FRVS). l The change clarify the testing requirements to state that the FRVS ventilation and recirculation heaters will be dissipating heat during the 10 hour1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> monthly test required by the Technical Specifications. The changes restore conformance between the UFSAR descriptions and Hope Creek's licensing basis. This UFSAR change does not increase the possibility or consequences of any accident or malfunction, does not reduce the margin of safety, and therefore, does not involve an Unreviewed Safety Question.

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SUMMARY

OF CHANGES. TESTS. AND EXPERIMENTS FOR THE HOPE CREEK GENERATING STATION - Cont'd Change Notice HCN 99-002, Allow Use of Combined CRB/FSB Grapple. This UFSAR change was to allow use of the General E!ectric Combined Control Rod / Fuel Support Piece (CRB/FSP) Grapple and associated Grid Guide.

The combined CRB/FSP Grapple is used for the same purposes as the Control Rod Grapple and Fuel Support Piece Grapple. The combined CRB/FSP Grapple will grapple both items effectively simultaneously and as such is considered a change to a

. 1 procedure described in the SAR. This UFSAR change does not increase the possibility i or consequences of any accident or malfunction, does not reduce the margin of safety, and therefore, does not involve an Unreviewed Safety Question.

Change Notice HCN 99-003, Editing of Nonessential Fuel Handling Tools and

  • Servicing Equipment. This UFSAR change was to delete reference to certain fuel handling system tools and equipment that are no longer used.

The information relating to nonescential (not essential to safety) fuel handling tools and servicing equipment was simplified in order to improve focus, clarity and maintenance.

This UFSAR change does not increase the possibility or consequences of any accident or malfunction, does not reduce the margin of safety, and therefore, does not involve an Unreviewed Safety Question.

Deficiency Reports Summary of Safety Evaluations 1 i

There were no reportable changes in this category implemented during January 1999.

Other Summary of Safety Evaluation Safety Evaluation H99-008, Hope Creek Reload Safety Evaluation for Cycle 8 Extension. This safety evaluation was to permit the Hope Creek Generating Station to continue operation beyond its previously reviewed and approved reload design basis.

Operation beyond the original end of cycle condition to February 13,1999 can be accomplished with either continued full power operation or power coast down. A power coast down does not involve the reduction of feedwater temperature for the purposes of cycle extension which is prohibited by the License Condition No.11. Cycle extension by means of a power coast down is within the existing current capabilities and design of the plant. ThP safety evaluation does not increase the possibility or consequences of any accident or malfunction, does not reduce the margin of safety, and therefore, does not involve an Unreviewed Safety Question.

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SUMMARY

OF CHANGES. TESTS AND EXPERIMENTS FOR THE HOPE CREEK GENERATING STATION - Cont'd Safety Evaluation H99-009, Hope Creek Cycle 9/Relaod 8 Core Operation. This safety evaluation was to review the Hope Creek Generating Station (HCGS) Cycle 9 core and fuel designs.

I The core design is different from that previously evaluated against SAR design basis via 10 CFR 50.59 and approved for HCGS cycle 8. Operation of cycle 9 will be accomplished within the existing power-flow map utilizing existing operating controls.

Operation during cycle 9 will not require any new or different functions from structures, systems or components or the need for new procedures. No new operating practices are required due to the cycle 9 reload core design. This safety evaluation does not increase the possibil;ty or consequences of any accident or malfunction, does not i reduce the margin of safety, and therefore, does not involve an Unreviewed Safety Question. l Safety Evaluation H99-012, processing of Chemical Waste Tank Effluents Through the Radwaste Floor Drain System. Thic safety evaluation reviewed the operation of three of five Liquid Waste Management System (LWMS) and evaluates an af ternate disposal method.

The change allows liquid wastes collected in the Chemical Waste Processing subsystem to be drained to and neutralized within the Regenerant Waste Processing (RWP) subsystem. The liquid waste would then be transferred from the RWP to the Floor Drain system via a temporary hose. Once treated in the floor drain system, the liquid effluent could then be discharged to the Condensate Storage Tank for reuse in  !

the plant or could be discharged from the plant to the Delaware River after mixing with the cooling tower blowdown as stated in section 11.2.2.1.2 of the UFSAR. This method will be scceptable as an alternste method if the normal prccessing path is not available. This safety evaluation does not increase the possibility or consequences of any accident or malfunction, does not reduce the margin of safety, and therefore, does not involve an Unreviewed Safety Question.

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