05000324/LER-1982-123, Forwards Updated LER 82-123/03L-4

From kanterella
(Redirected from ML20081D178)
Jump to navigation Jump to search
Forwards Updated LER 82-123/03L-4
ML20081D178
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 03/07/1984
From: Dietz C
CAROLINA POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
BSEP-84-0493, BSEP-84-493, NUDOCS 8403150179
Download: ML20081D178 (1)


LER-2082-123, Forwards Updated LER 82-123/03L-4
Event date:
Report date:
3242082123R00 - NRC Website

text

_ _ .

l c :=*

CP&L U & Light Ccmpany oMys Brunswick Steam Electric Plant P. O. Box 10429 Southport, NC 28461-0429 March 7, 1984 FILE: B09-13510C SERIAL: BSEP/84-0493 Mr. James P. O'Reilly, Administrator U. S. Nuclisar Regulatory Commission Region II, Suite 3100 101 Marietta Street N.W.

Atlanta, GA 30303 BRUNSWICK STEAM ELECTRIC PLANT, UNIT NO. 2 DOCKET NO. 50-324 LICENSE NO. DPR-62 SUPPLEMENT TO LICENSEE EVENT REPORT 2-82-123

Dear Mr. O'Reilly:

l In accordance with Section 6.9.1.9b of the Technical Specifications for Brunswick Steam Electric Plant, Unit No. 2, the enclosed supplemental Licensee Event Report is submitted. This report was originally distributed on February 22, 1984, Serial BSEP/84-0412; however, portions of the report were inadvertently omitted during the distribution. The report, which is in accordance with the format set forth in NUREG-0161, July 1977, is being redistributed in its entirety.

Very.truly yours, 5

C. R. Dietz, General Manager Brunswick Steam Electric Plant RMP/dgr/LETDR1 Enclosure cc: Mr. R. C. DeYoung NRC Document Control Desk OFl'ICIAL COPY ks k h k OS

}l

(7 77) U P date Report: 1

.. LICENSEE EVENT REPORT Previous Report Date: 2-10-84 I e

CONTROL BLOCK: l 1

l l l l l lh 6

(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) l0 l1l8 9l Nl Cl B l E l Pl 2 l@l 0 l 0 l- l 0LICENSE le 15 l0 l NUMBER 0 l0 l0 l- l0 l 0l@l 25 4l 26 l l LICENSE TvPE JC l l@l57 CA1 l bd l@

7 LICENSEE CODE CON'T lolil 7 8 so)RC l60L @l 0 l 5 lDOCKET 68 0 l- NUMBER l0 l 3 l 2 l4 68 hl 69 1 l EVENT OI 1DATE l Ol 8 l 2 l@l 0REPOHT 74 75 l 2 DATE l 2 12 80l 8 l4 l@

EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h 10121 l During an orderly reactor shutdown. while attemotine to automatically transfer bus 2D 1 l o 13 l l from the unit auxiliary transformer (UAT) to the unit startup transformer (SAT), a l Io l4 l l loss of 4160 V emergency bus E-3 occurred. In addition, No. 3 diesel ,renerator was 1 f7TTll determined to be inoperable. This event did not affect the health and safety of the l I

lo Is l lpublic.

Io I7I I I I O 18 I I Technical Specif' cations 3.8.1.1, 3.8.2.I, 6.9.l.9b l 80 DE CODE SUSC E COMPONENT CODE SUSCOCE S E F5Til 7 8 l E l n l@ W@ M@ l cl xl Tl n l n i K l@ M@ U @

9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION EVENT YE A R R EPORT No. CODE TYPE NO.

LER Ro

@yREg l, 8 l 2 l

_ .c s 22

[.--J 23 ll l 2l 3l26 24

\/l 27 l0 l 3l 28 29 lL l 30 l-l 31 WAJ K N AC O CN NT ME HOURS S8 IT FOR1 8. SUPPL 1, MANUFACT RER l33o l@l34x l@ lA 3b l@ (C_jh M 3l4 0l0l2l6l40 l44Y l@ lYl@ l L l@

42 43 lIl2l0l3l@

44 47 CAUSE DESC' R IPTION AND CORRECTIVE ACTIONS 27 l i j o l l This event occurred because both the SAT output breaker and No. 3 diesel nenerator l li li j l output breaker failed to close when the UAT output breaker was opened. The UAT l l ,,373 gbreaher, Model No. 5HK350, was installed in p?. ace of the SAT breaker and power'to E-3 l g lvas restored. I'rocedural changes were implemented to .ompensate for simultaneous I g,,,,lclose and open signals ta the diesel generator's output breakers under certain l 7 8 9 Conditions, so STA S Y. POWER OTHER STATUS CIS PY DISCOVERY DESCRIPTION Operational Event I1 l5 l l X l@ l0 ll l 7 l@l NA l lAl@l l ACTIVITY CC TENT AMOUNT OF ACTIVITY LOCATION OF RELEASE 1 6 NA l l NA l 7

RELE ASE@D OF RELCASE{@l 8 9 10 11 44 4". 80 PERSONNEL EXPOSURES NUV8ER TYPE C(SCRIPTION l

l t l 7 l { 0 l 0 l 0 l@l Z l@l NA

' ' ' PERSONNEL'imu'd,ES NUv8E R oESCRiPTiO~@

l li t a8l 9l 010101@l 7 11 12 NA 80 LOSS OF OR DAVAGE TO FACILITY h TYPE DESCPIPTICN V NA I l i l o l l Z I@l Pb8Li TV h/* NRC USE ONLY ISSU E D g l N l@DESCRIPTICN l -%WO3OjO2M- PDR NA l ltIil11IIII!!!

7 g 3 :o 68 63 80 3 NAME OS PRED AREA R. M. Poulk. Jr. PHONE: 919-457-9521 E,

l LER ATTACHMENT - R0 (f2-82-123 Facility: Unit No. 2 Event Date: October 10, 1982 While performing an orderly reactor shutdown, an attempt to manually transfer the power source to bus 2D from the unit auxiliary transformer (UAT) to the unit startup transformer (SAT) failed. When an attempt was made to effect an automatic transfer of the power source to bus 2D, a loss of voltage to 2D, and thus emergency bus E-3, occurred. The loss of bus E-3 rendered 2A core spray pump and 1A and 2A RHR pumps inoperable due to lack of their normal and emergency power supplies.

This event occurred when the UAT output breaker was manually opened and the SAT output breaker, ITE Model No. 5HK350, failed to automatically close in to supply bus 2D. Prior to this event, No. 3 diesel generator had been started under Control Room manual control and brought up to operating speed with the diesel generator output breaker open. This was done so that the diesel wculd be up to speed if the transfer failed. Emergency bus E-3 is normally supplied from bus 2D, cnd No. 3 diesel generator is the emergency standby power source to E-3. Immediately following the failure of the SAT output breaker, No. 3 diesel generator failed to close on bus E-3. This rendered bus E-3 dead which assisted in causing a scram and Group I isolation.

Shortly after this event, a quick trouble check of the SAT output breaker determined a problem within the breaker. The UAT output breaker was then installed in the SAT output breaker compartment and power to bus 2D was restored from the SAT within one hour and forty-five minutes of the event. In addition, bus E-3 reenergized. A close inspection and troubleshooting of the failed SAT output breaker revealed the breaker had failed to automatically close as a result of a sheared breaker charging spring motor actuator. The charging spring motor casing mounting screw bad backad out of the motor housing causing the motor actuator to shear and separate from the breaker which prevented charging the breaker charging springs for breaker closing capability. The failed breaker from the SAT output breaker compartment was tuen repaired using a replacement charging motor assembly, tested satisfactorily for operation, and. installed in the UAT output breaker compartment.

The failure ci a breaker in this manner could prevent it from closing following a trip or a normal opening operation, thus causing a potential loss of power to its respective bus. A sufficient number of failures occurring at the same time could affect the operability of safety-related systems. These 4160 V breakers are 1ccated throughout the plant in both safety-related loads and balance-of plant loads.

An investigation into the failure of the ou+put breaker of No. 3 diesel generator to close in to bus E-3 revealed chat simultaneous close and open signals to the breaker prevented automatic closing of the breaker on loss of voltage to bus E-3. The plant emergency buses utilize a high speed undervoltege relay which applies a one-second trip open signal to the applicable diesel generator output breaker on loss of voltage to the bus.

i i

1

LER ATTACHMENT - RO #2-82-123 (Continued)

This relay ensures the diesel generator is separated from an abnormal emergency bus on loss of voltage. In addimion, plant emergency buses utilize an inverse time undervoltage elay (1.5 seconds) which causes loads to be shed from the emergency bus on loss of bus voltage. This permits tying the diesel to its applicable bus after the bus is stripped. While the diesel generator is in Control Room manual or local manual, a loss of voltage to the E-bus will result in a failure of the diesel to close on the E-bus. In reality, a voltage drop on the bus will occur somewhat slower and varies with the loads on the bus.

The bus inverse time undervoltage relay will sense the voltage drop condition when it decreases to approximately 82 percent of normal, and the high speed undervoltage relay senses the voltage drop condition at some percentage less than 40 percent of normal. As a result, bus loads shed and a close signal to the diesel generator output breaker occurs before the high speed undervoltage relay one-second trip signal is removed, thus preventing the output breaker from closing. To close the diesel generator output breaker in this situation, the high speed undervoltage relay c1cse signal must be removed and reapplied.

The investigation determined this can he accomplished by placing the keylock remote shutdown switch on the applicable E-bus switchgear breaker compartment to the local position and then back to normal.

As a result of this event, plant modifications were developed, approved, and implemented to eliminate the problem. As a result of the SAT output breaker failure, applicable plant surveillance procedures have been revised as required to perform a check of plant 4160 V switchgear charging spring mounting attachment bolts during periodic preventive maintenance operability inspections of the breaker mechanisms. Safety-related breakers for both units have been inspected to assure that the breakers are operable. This action was completed during the Unit No. 1 1983 refueling outage.

l w_