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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P2061999-10-26026 October 1999 Forwards for First Energy Nuclear Operating Co Insp Rept 50-346/99-17 on 990928-1001.Insp Was Exam of Activities Conducted Under License Re Implementation of Physical Security Program.No Violations Identified ML20217N3851999-10-20020 October 1999 Forwards RAI Re Licensee 990521 Request for License Amend to Allow Irradiated Fuel to Be Stored in Cask Pit at Davis-Besse,Unit 1.Response Requested within 60 Days from Receipt of Ltr ML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20217F8371999-10-0808 October 1999 Forwards Insp Rept 50-346/99-10 on 990802-0913.One Violation Occurred Being Treated as NCV ML20217A5641999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Davis-Besse on 990901.Informs That NRC Plans to Conduct Addl Insps to Address Questions Raised by Issues Re Operator Errors & Failure to Commit to JOG Topical Rept on MOV Verification ML20212L0691999-09-30030 September 1999 Forwards,For Review & Comment,Copy of Preliminary ASP Analysis of Operational Condition Discovered at Unit 1 on 981014,as Reported in LER 346/98-011 ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls ML20212D3501999-09-21021 September 1999 Forward Copy of Final Accident Sequence Precursor Analysis of Operational Event at Plant,Unit 1 on 980624,reported in LER 346/98-006 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211P3001999-09-0707 September 1999 Forwards FEMA Transmitting FEMA Evaluation Rept for 990504 Emergency Preparedness Exercise at Davis-Besse Nuclear Power Plant.No Deficiencies Identified.One Area Requiring C/A & Two Planning Issues Identified ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K0951999-08-30030 August 1999 Forwards Request for Addl Info Re Fire & Seismic Analyses of IPEEE for Davis-Besse Nuclear Power Station,Unit 1. Response Requested within 60 Days ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211D1171999-08-20020 August 1999 Forwards Insp Rept 50-346/99-09 on 990623-0802.Violations Identified & Being Treated as Noncited Violations ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20211B0161999-08-13013 August 1999 Forwards SE Accepting Evaluation of Second 10-year Interval Inservice Insp Program Request for Relief Numbers RR-A16, RR-A17 & RR-B9 for Plant,Unit 1 ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps ML20210P8051999-08-0909 August 1999 Forwards Insp Rept 50-346/99-15 on 990712-16.No Violations Noted.However,Several Deficiencies Were Identified with Implementation of Remp,Which Collectively Indicated Need for Improved Oversight of Program IR 05000346/19980211999-08-0606 August 1999 Refers to NRC Insp Rept 50-346/98-21 Conducted on 980901- 990513 & Forwards Nov.Two Violations Identified Involving Failure to Maintain Design of Valve & Inadequate C/A for Degraded Condition Cited in Encl NOV 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210H6101999-07-30030 July 1999 Informs That Region III Received Rev 21 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Revision Was Submitted Under Provisions of 10CFR50.54(q) in Apr 1999 ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete ML20210C4381999-07-20020 July 1999 Forwards Insp Rept 50-346/99-08 on 990513-0622.Unidentified RCS Leak Approached TS Limit of 1 Gallon Per Minute Prior to Recently Completed Maint Outage.Three Violations of NRC Requirements Identified & Being Treated as NCVs ML20209G3681999-07-15015 July 1999 Advises That Info Submitted in & 990519 Affidavit Re Design & Licensing Rept,Davis-Besse,Unit 1 Cask Pit Rack Installation Project,Holtec Intl, HI-981933,marked Proprietary,Will Be Withheld from Public Disclosure ML20207H6401999-07-0909 July 1999 Discusses Closure of TAC MA0540 Re Util Responses to RAI on GL 92-01,rev 1,suppl 1, Rv Structural Integrity. Staff Has Revised Info in Rvid & Releasing It as Rvid Version 2 ML20209D1341999-07-0808 July 1999 Forwards Notice of Withdrawal of Application for Amend to Operating License.Proposed Change Would Have Modified Facility TSs Pertaining to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20195K2751999-06-16016 June 1999 Forwards Safety Evaluation Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207G0751999-06-0707 June 1999 Forwards Insp Rept 50-346/99-04 on 990323-0513.Violations Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207F4231999-06-0202 June 1999 Forwards Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504, IAW 10CFR50.4.NRC Evaluated Exercise Has Been Rescheduled for 991208,since NRC Did Not Evaluate 990504 Exercise ML20207E9561999-05-28028 May 1999 Forwards Update to NRC AL 98-03,re Estimated Info for Licensing Activities Through Sept 30,2000 ML20207E2521999-05-28028 May 1999 Forwards Rev 18,App A,Change 1 to Davis-Besse Nuclear Power Station,Unit 1,industrial Security Plan IAW Provisions of 10CFR50.54(p).Encl Withheld,Per 10CFR73.21 ML20207E7801999-05-21021 May 1999 Forwards Application for Amend to License NPF-3,allowing Use of Expanded Spent Fuel Storage Capacity.Proprietary & non- Proprietary Version of Rev 2 to HI-981933 Re Cask Pit Rack Installation Project,Encl.Proprietary Info Withheld ML20206N0231999-05-0606 May 1999 Forwards License Renewal Applications for Davis-Besse Nuclear Power Station,Unit 1 for ML Klein,Cn Steenbergen & CS Strumsky.Without Encls ML20206D2421999-04-28028 April 1999 Forwards Combined Annual Radiological Environ Operating Rept & Radiological Effluent Release Rept for 1998. Rev 11, Change 1 to ODCM & 1998 Radiological Environ Monitoring Program Sample Analysis Results Also Encl PY-CEI-NRR-2382, Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl1999-04-21021 April 1999 Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl ML20206B8831999-04-17017 April 1999 Forwards 1634 Repts Re Results of Monitoring Provided to Individuals at Davis-Besse Nuclear Power Station During 1998,per 10CFR20.2206.Without Repts ML20205K5641999-04-0707 April 1999 Forwards Response to NRC 980415 RAI Re GL 96-06, Assurance of Equipment Operability & Ci During Design-Basis Accident Conditions. Rept FAI/98-126, Waterhammer Phenomena in Containment Air Cooler Swss, Encl ML20205K3871999-04-0707 April 1999 Forwards Copy of Application of Ceic,Oec,Ppc & Teco to FERC, Proposing to Transfer Jurisdictional Transmission Facilities of Firstenergy Operating Companies to American Transmission Sys,Inc.With One Oversize Drawing ML20205J1171999-03-29029 March 1999 Forwards Rev 1 to BAW-2325, Response to RAI Re RPV Integrity, Per GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity. Rev Includes Corrected Values in Calculations PY-CEI-NRR-2377, Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1)1999-03-29029 March 1999 Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1) ML20205F5961999-03-27027 March 1999 Forwards Comments on Preliminary Accident Sequence Percursor (ASP) Analysis of 980624 Operational Event at Dbnps,Unit 1, as Transmitted by NRC Ltr ML20205D4791999-03-26026 March 1999 Forwards Rept Submitting Results of SG Tube ISI Conducted in Apr 1998.Rept Includes Description of Number & Extent of Tubes Inspected,Location & Percent wall-thickness Penetration for Each Indication of Imperfection ML20205L2031999-03-26026 March 1999 Submits Correction to Dose History of Tj Chambers.Dose Records During 1980-1997 Were Incorrectly Recorded Using Wrong Social Security Number.Nrc Form 5 Not Encl ML20205C7371999-03-25025 March 1999 Certifies That Dbnps,Unit 1,plant-referenced Simulator Continues to Meet Requirements of 10CFR55.45(b) for Simulator Facility Consisting Solely of plant-referenced Simulator.Acceptance Test Program & Test Schedule,Encl ML20205E3551999-03-19019 March 1999 Requests That Proposed Changes to TS 6.8.4.d.2 & TS 6.8.4.d.7 Be Withdrawn from LAR Previously Submitted to NRC ML20204J6361999-03-17017 March 1999 Forwards Firstenergy Corp Annual Rept for 1998 & 1999 Internal Cash Flow Projection as Evidence of Util Guarantee of Retrospective Premiums Which May Be Served Against Facilities PY-CEI-NRR-2375, Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage1999-03-15015 March 1999 Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage ML20204E6821999-03-12012 March 1999 Requests That Listed Changes Be Made to NRC Document Svc List for Davis-Besse Nuclear Power Station,Unit 1 1999-09-09
[Table view] Category:RESEARCH INSTITUTION/LABORATORY TO NRC
MONTHYEARML20209D9751986-10-31031 October 1986 Forwards Technical Evaluation Rept EGG-EA-6941, Conformance to Reg Guide 1.97,Davis-Besse Nuclear Power Station. Licensee Conforms to or Is Justified in Deviating from All Variables in Reg Guide 1.97 ML19302H6161986-04-29029 April 1986 Submits Updated Status of Confirmatory Items Identified in 860319 Technical Evaluation Rept Re Facility Sys Review & Test Program ML20214E1721986-02-25025 February 1986 Ack Receipt of 860210 & 21 Ltrs Accepting Task Orders 3 & 4 Under FIN A-3552 & Task Order 5,respectively.Orders Include Work at Palisades & LaSalle Stations & Mod Review at Davis-Besse.Modified Task Order 4 Under FIN A-3550 Encl ML20154L0871986-02-18018 February 1986 Discusses Util Ltr of Complaint Re Theory Section of 851119 Written Exam.Theory Section Considered Prototypic ML20073S6661983-04-22022 April 1983 Forwards Final Rept of Bnwl Participants at 830413-14 Emergency Preparedness Exercise.Areas Covered Include Technical Support Ctr,Control Room,Operations Support Ctr & Offsite Monitoring Teams ML19332A4471980-09-0808 September 1980 Submits Info Re Status of Evaluation & Mods of Diesel Generator Annunciator Sys.Corrective Actions Required Include Separate Annunciator Sys for Disabling & Nondisabling Conditions & Wording on Annunciators 1986-04-29
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t 2Ba April 22, 1983 0BaHelle I'a " ' " ' "" I * L a l" " """
e o um w, Ra hbful. \\ adonet m I 5 \ 97 G2
""P'"" " 375-6836
- m. . n.za .
Mr. Thomas Ploski ! FalNCIPAL STAFF l Division of Emergency Preparedness u.
I , a; g;p g g and Operations Support i j i U.S. Nuclear Regulatory Commission k ~ y c. g i j .
Region III [ t r, t.n ! .
799 Roosevelt Road jy :. - '
Glen Ellyn, IL 60137 gj/ ,
p 4
1, _j I
Dear Tom,
._ T~T~ f .__J -i i
DAVIS-BESSE NUCLEAR POWER PLANT EMERGENCY EXERCISE REPORT Enclosed is the finalized report of G. W. Bethke, C. D. Corbit, W. F.
McCready, J. G. Myers, and W. V. Thomas, who were Pacific Northwest Laboratory (PNL) participants during the Davis-Besse Nuclear Power Plant Emergency Pre-paredness Exercise, April 13 and 14, 1983. Only minor changes were made from the rough draft supplied to you prior to leaving Davis-Besse. Areas covered by PNL are as follows:
G. W. Bethke Technical Support Center W. F. McCready Control Room C. D. Corbit Operations Support Center J. G. Myers Offsite Monitoring Teams W. V. Thomas Operations Support Center ;
1 If you have any questions regarding the report, please contact W. V. Thomas on FTS (509) 375-2088.
Very truly yours, p Fr$n' h a J. B. Martin W. . Thesay Technical Leader Senior Research Scien ist Health Physics Technology Section Health Physics Technology Section JBM:mae Enclosure cc: FG Pagano, w/ enclosure SA Schwartz, w/o enclosure KE Perkins, w/o enclosure 8305100011 830422 APR 2 91983 PDR ADOCK 05000346 F PDR
[ I'3$
Operational Support Center A. Name: W. V. Thomas B. Assignment: OSC, Health Physics Monitoring Area The Health Physics (HP) Monitoring Office was manned promptly upon declaration of Alert. Accountability in the HP area was completed in less than 10 minutes and relayed to the OSC Supervisor upstairs on the turbine deck. Supervision in the HP office was promptly assumed by the HP Foreman. A head set was hooked up to the Gaitronics and communication was maintained with the OSC Supervisor. Additional communication was maintained by telephone. HP logs were maintained by the HP Foreman and the Communicator.
HP monitoring teams were dispatched by the HP Foreman to assist maintenance and repair teams. All teams were briefed prior to departure as to radiation levels in the plant and plant status conditions. Prior to dispatch accumulated exposures for team members were determined and allowed exposures were assigned. In plant radiation surveys were performed in a professional manner. The RCS activity was observed, the sample was collected and analyzed within three hours.
l l
C. Comments i A number of scenario problems were noted:
l l
I i
(
l _,
- 1. Dose rates and radiological conditions within the plant as evidenced by the RMS should have been given in the scenario.
- 2. Accumulated personnel radiation exposures to the maintenance team and HP team members, while closing the MSL relief valve and obtaining the RCS, should have been included in the scenario.
- 3. An additional controller should have been assigned to the HP monitoring office. Instead, one controller was assigned to the two areas which ccm-pose the OSC.
F. Chronology Time Observation 1415 Call to CR to report RCS resulsts: 65 uCi/gm I-131 equivalent.
1445 Second coolant sample obtained and counted.
1515 Call to CR to report 310 uCi/gm I-131 equivalent.
1520 Assembly in Rad Chem area.
1525 Accountability complete all accounted for.
1530 All rep's pulled, flo entry to RACA permitted.
Time Observation 1536 Dispatch 2 rad /techs to search Rm.100 for 2 UE employees missing during accountability.
1537 UE employees report to RACA.
1550 Request for 2 HP/ testers to ECC. Plant chem. reports.
1610 Sample and letdown area RMS: 5 R/hr, no airborne.
1613 Request to confirm RMS readings; #1 ECCS 1003 A&B.
1617 Dose rates confirmed. Monitoring teams recalled.
1620 OPS requests additional RCS sample.
1620 1003 A&B 60 cpm increased. Decision made to take air sample.
1622 Rad / Chem team dispatched for additional RCS.
1627 Request for check of reactor power level 67%.
1635 Report to CR: 310 uCi/gm I-131 equivalent; 310 pCi/cc noble gas in third RCS.
i
Time Observation 1645 No.1 diesel generator tripped - cannot restart. Problem with overspeed trip.
1655 Request for Rad. Tech. at DBAB to open counting lab.
1703 Announcement: loss of station computer and annunciator in Control Room-Site Area Emergency declared.
1710 TSC requests resurvey of Auxiliary Building. Briefing by OSC i
{ Director, instructed to carry respirator equipment.
i 1715 Proceed with HP monitor and maintenance tean to shut main steam relief valve (MSRV).
1745 Return to HP monitoring room.
1746 OSC Coordinator briefed on MSRV activity; MSRV still open.
1756 Requests for radiation survey and air sample of Turbine Building and 603 ft level of Auxiliary Building.
1815 MS monitors still background.
l 1820 Simulated RCS; same results reported to CR.
Time Observation 1920 Report of tube failure.
1925 General Emergency declared.
1937 13.5 mR/hr at site boundary; normal readings on turbine floor.
End of Day 1 Drill Time 2230 Reassemble in HP monitoring room.
2245 Report to OSC. KI distributed to security force.
j 2250 Check of CAM and RMS. No background increase on CAM. Auxiliary Building monitors read 5 R/hr.
2253 Request survey of main steam relief valve. Still 500 mR/hr at door, 2.5 R/hr door open, 7.5 R/hr at valve.
2254 One man reports iodine allergy; told to leave area.
i 2304 Four 2-man maintenance teams working on valve closure; 2-man HP coverage provided.
Time Observation 2337 Continuing work on steam line valve; s1/2 hr work renaining.
Condenser vaccum started. Area roped off. Will dump polishers, at 150 mR/hr general area, to rad waste holdup tanks.
2349 Recheck of CANS, check polisher general area, reset ARMS to prevent nuisance alarms in Control Room.
I 2402 Main steam line relief valve has been closed. Rad survey requested in area.
2430 Drill terminated.
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TSC A. Name: G. W. Bethke B. Assignment: TSC C. Positive Conments
- 1. Electrical engineering efforts in the TSC were very detailed and well thought out.
- 2. The Chem /HP Manager performed analysis and calculations in a very pro-fessional manner (although it is questionable whether he should be doing this rather than concentrating on management).
D. Negative Comments
- 1. The TSC at Davis-Besse, although operated in accordance with site pro-cedures, is quite different in concept from any perviously observed.
Examples:
- The role of Emergency Director passed directly from the Shift Super-visor to ECC Management.
- The Plant Manager was never the Emergency Director.
- The TSC had no consistent, strong management presence.
- Various people in the TSC (e.g., Chem Manager /HP) are not in the chain of command of the " Operations Assessment Manager" (i.e.,
" Senior" man in TSC).
- 2. General iSC comments:
- It took about an hour after Alert declaration to post the first plant parameters and status.
- No TSC activation checklist was in use.
- No general announcement was made by anyone "in charge" in the TSC.
- Reactor systems analysis in the TSC did not receive the type of detailed effort that electrical problems received (e.g., treatment of analysis of coolant mass balance as an impossible task).
- The Chem /HP manager had to perform the majority of the " accurate" dose calculations personnaly. His primary assistant was in the ECC.
He should have a small team in the TSC. Had there been significant in-plant radiological problems, it is not apparent how he could have dealt with them.
- No consolidated official log was maintained in the TSC.
- The lack of prepared forms (such as offsite dose calculation forms) necessitated people writing in their books. Recommend providing a supply of forms and worksheets.
- 3. Dose asessment calculations received from NRC over the ENS did not con-tain information on assumptions made. Since the calculations did not agree with those made by the licensee, they decided to ignore them. They should have compared results and assumptions over the HPN.
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- 4. It took approximately 45 minutes after the start of the release to perform accurate dose projections.
- 5. The technical personnel in the TSC did not have adequate knowledge of records or personnel to retrieve technical data (e.g., results of latest ILRT).
- 6. No formal plans were made (on day 1) to provide for long term shift man-ning, logistics, etc.
- 7. The return of RCP's to service following the return of offsite power was treated fairly lightly. This in fact would be a closely scrutinized procedure. TSC management verbalized a lack of concern for RCP seal failure.
- 8. The decision to start steaming #1 S/G to the condensor (after drawing a vacuum with steam from #2 S/G) was made with little regard for radiological consequences in the B.0.P. This discussion (with the Chem /HP Manager) took place at a point in time after which they would have started steaming the S/G. This problem was somewhat scenario related.
- 9. The matrix management organization could result in command and control problems during a real emergency.
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Control Room /TSC A. Name: W. F. McCready B. Assignment: Control Room, TSC C. Scenario Problems / Controller Problems
- 1. Containment airborne activity and corresponding radiation level data (due to normal leakage with elevated coolant activity) was ignored - i.e., no data provided.
- 2. Airborne activity and general area radiation levels around letdown system components in the Auxiliary Building were ignored - i.e., data not provided. Note: Control Room Controller created data when necessary.
- 3. MSL radiation monitors on 1-1 steam line (analyze - gross) were not provided. Note: Control Room Controller later created data as necessary.
- 4. Direct gamma dose rates from steam safety tailpipe were not considered in data generation.
- 5. Only one set of Tcand T data h
was provided. (Presumably unaffected loop.) This will present a problem later in the exercise. Note: TSC Controllers were not sure which loop the data applied to.
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- 6. The 1300 briefing of controllers on April 12 was the first training the scenario developers had given the controller team. This may result in problems. Controllers pointed out these scenario problems at the brief-ing but it was too late.
- 7. Confusion was caused (at least at NRC) by the lack of explanation in the scenario for failed fuel (i.e., no transients, no loose parts, monitor readings,etc.). This created a potential security sabotage scenario in parallel .
- 8. The Controllers gave out 7.5 R/hr at MS safety relief valveabout 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> before the tube rupture. This caused great confusion in the CR.
- 9. The scenario did not include off centerline plume data, nor did it include open/ closed window readings.
- 10. The Controllers may not have provided chemists with complete coolant isotopic analysis. This caused great confusion in the TSC and CR since they had only Xe-133 and I-131 equivalent data.
- 12. The Controllers did not explain the clock vs. scenario time convention to the players before the 0830 restart on day 2. This will ultimately cause problems. They did not because they decided later to go to clock time.
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- 13. The Controllers in the TSC did not pay any attention to the participants plan to draw a vacuum in #1 S/G to terminate the release. Therefore, they were not in communication with each other to make data adjustments.
- 14. The scenario did not accurately reflect the time necessary to recover from loss of offsite AC power and the re-initiation of RCP's. It was not clear that that action should even be taken right away due to one idle leg, cold water injection, or boron levels, etc.
- 15. The Control Room needs two Controllers: one to pass out cue cards and data and one to be in overall control of the exercise and to handle scenario problems. The Control Room Controller did an excellent job in this exercise, considering the work overload.
D. Comments on EPIP EI 1300.07, TSC Activation
. Formal logbooks were not distributed (or used) as required per section 5.4.7.
. The Tech. Engineer (or anyone else) did not verbally brief TSC personnel on pla.it or radiological conditions as required "tr section 5.6.5.
. B&W was contacted late (s 2110)
. Bechtel was r.ot contacted.
. NSAL was not contacted (as per section 5.9.5) i l
e No formal record of TSC activities was maintained. One stenographer was keeping a record in a spiral notebook of items passed by the two technical communicators. The more formal looking log was not used as required per section 5.9.6.
Offsite Monitoring A. Name: John Myers B. Assignment: Observe offsite monitoring team (s) activities C. Summary: Radiation monitoring teams were well versed in use of radiation detection and air sampling equipment. Instruments were functionally checked prior to use. All had been calibrated within the prescribed schedule. Teams were able to quickly locate sampling locations assigned by ECC. Air samples were correctly taken and filters were properly field read, bagged, and tagged with results recorded.
Continuous communications were maintained via radio between teams and ECC.
Soil and vegetation samples were properly taken, bagged and tagged. Installed dosimeters were in weather proof containers.
D. Findings:
. Problems with security at the Administration Building (i.e., lack of adequate communications) caused a delay of s15 minutes in delivery of an air sanple to the RTL.
. Air samples were taken during a severe rain storm. If this had been an actual event, most if not all, of the iodine in the plume would have been washed out and the air sample would have been meaningless.
. Maps showing sectors, roads, and sampling / dose rate points were printed on 8 1/2 in. x 11 in. paper. Information (e.g., road designations, sample points, etc.) could not be quickly identified due to the reduced size.
. Teams were recalled to the RTL to deliver air samples resulting in time lost from assigned task (i.e., offsite monitoring). One team could have handled this by picking up samples from other teams.
. Sedans were used and equipment was placed in the trunk. There were no offroad/4 wheel drive vehicles available for use off established roads.
. There was no backup communications (i.e., walkie talkies) available. Had
! the vehicle radio failed, communications with the ECC would have been I
impossible. Note: walkie talkies are stored in the instrument cabinet in the RTL but were apparently out-of-service.
. No observer or controller was assigned directly to the RTL. Tean observers / controllers functioned only when teams came in from the field.
. Teams did not routinely keep track of their exposure (read pencils) or report same to the ECC. Note: ECC asked for this information only once.
Teams kept no exposure log.
. Personnel dosimetry did not include self reading dosimeters with ranges higher than 0-1.0 R/hr.
. At the only permanent sampling station visited, no calibration tag was noted on the continuous air monitor.
. The ECC failed to keep offsite teams appraised of plant conditions in a routine manner.
. Plume centerline data was not transmitted to the offsite teams. Teams were never informed by the ECC where the centerline was in relation to assigned sampling locations or if assigned locations were indeed in the plume. Plume tracking was inadequate.
E. Chronology T'me Observation Day 1 1575 Functional checks of offsite instruments started.
1611 Functional checks completed.
1700 Offsite teams dispatched.
1719 Reported to and held at intersection of Rt. 2 and Russell (entrance to to Administration Building). Took dose rate measurements and an 1939 air sample.
1939 Ordered to return to RTL to deliver air sample.
Time Observation 1958 Delivered sample to RTL.
2040 Arrived at Rt. 19 and Genzman in Sector L. Took dose rate measure-ments and air sample; reported to ECC.
2113 Requested to bring air sample to RTL.
2126 Arrived at RTL and delivered air sample.
2132 Team released. End of day 1.
Day 2 0908 Offsite teams dispatched.
0921 Arrived at Magee Marsh (Rts. 2 and 23). Dose rates taken and reported to ECC.
t 0928 Arrived at Crane Creek State Park. Dose rates taken and reported to ECC.
0936 Arrived at Crane Creek Store (Rt. 2). Dose rates taken and reported to ECC.
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Time Observation 0949 Arrived at Rts. 208 and 579. Dose rates and air sample taken, to Results reported to ECC.
1017 1019 Ordered to report to RTL.
1033 Arrived at RTL. Team released.
1 1110 Tean dispatched to obtain soil and grass sample (simulation) 1131 Arrived at sampling station T8 (Morris Orchard). Simulated soil and grass collection.
1150 Arrived at RTL. Team released.
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OSC, Maintenance A. Name: C. D. Corbit B. Assignment: OSC, Maintenance Team D. Summa ry: The Unusual Event was announced in the OSC at 1421. Just prior to the announcement of the Alert at 1520, the Maintenance Engineer asked the offgoing shift to remain at the plant until further notice because high iodine concentrations had been found in the primary loop. By 1925, the first-aid team, fire brigade, and OSC were fully manned and accounted for. OSC personnel were generally responsive to all support activities requested, and the OSC Manager was clearly in charge at all times. All controllers, observers and participants properly conducted their roles. OSC logs were properly naintained.
The first call to the OSC, from the Diesel Generator Room, had a bad con-nection. The OSC Manager had the caller recall the OSC on another line and that cleaned up the connection problem. The communications system functioned well throughout the remainder of the exercise.
Two communication problems were observed. The first arose during a response
, to gag a steam vent valve (SP 1781). At 1649 it was announced that the OSC could not send a team to gag the valve because the foreman did not know where the steam suits were. Nonetheless, the OSC sent a team to gag the valve and the observer went with them. After picking up a valve gag (and simulating a 1
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screwdriver and crescent wrench), the team found that their security passes did not open door 605. A security guard was called, who arrivea in less than 3 minutes and opened door 605 with a key. The maintenance craftsmen explained that steam suits would not be needed.
The second communications problem related to the station access control point (Guard Station). The OSC was told that the Guard Station had been taken over by outside forces. This turned out to be false. The OSC promptly called the security force and obtained permission to gain access in and out of the plant via the "old" guard station, permission was granted. Miscommunication occurred in spite of the fact that the exercise scenario did not contain any security events.
D. Findings
. Two personnel communications problems were observed, one involving the need for steam suits, the second, a security problem that did not exist.
The licensee should review the methods for rumor control within the plant during emergency simulations and events. At a minimum, the in-plant security control point (CAS) should be contacted for information on security events.
E. Chronology Time Observation Day 1 1420 UE was announced over PA system / alarm. "No assembly is required at this time."
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Time Observation 1515 High primary coolant iodine concentrations (above technical specifi-cations) was announced. OSC Manager requested offshift personnel to remain onsite until further notice.
1520 Alert was called, iodine concentrations in primary coolant increased.
1525 OSC operational. Fire brigade in place and first-aid team in place. OSC Manager had bad phone connection, recall on different line cleaned it up.
Following rapid accounting for personnel by various assigned leaders, cross checking with the computer print-out occurred. This was a lengthy process lasting about one hour. The computer program does not place personnel by organization, whereas the accountability does. Further, only one pre-developed accountability checklist was observed by the inspector.
1604 Contractor personnel were evacuated.
1621 All cross checks of accountability were completed.
1633 Reactor trip announced.
1635 Maintenance team sent to Diesel Generator.
Time' Observation Day 2 0830 Drill resumption announced. OSC manned.
0851 Resurvey of steam valve location requested; the OSC Manager ordered it done.
0856 OSC survey shows no problems.
1100 Downgraded emergency to Alert.
1123 Secured OSC.
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r Time Observation 1649 Cannot send team to repair steam valve. Foreman does not known where steam suits are.
1704 Site Area Emergency declared; Control Room annunciators and computer lost.
1730 Observed maintenance team simulate valve gag. Door 605 would not respond to security cards of team (nor observers). Security was called and they opened the door. At door 602, the Radiation Tester made dose rate measurements. Controller gave information from wrong scenario page: the Tester calculated 45 minutes of stay time was the maximum allowed. Maintenance Craftsmen said they could gag valve in 2 minutes unless the disk was broken. Gagging was not allowed at this time. Five minute delay required to determine which valve required gaging.
1820 General . Emergency announccd.
2006 Radiation readings showed OSC had no habitability problem. Before they left the OSC, the Testers were asked what the airborne readings were--they did not know. The OSC Manager requested readings on dose rates and air samples every 30 minutes.
l 2200 Activities ceased, exercise terminated for the day.
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