ML20057A420

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Insp Repts 50-327/93-33 & 50-328/93-33 on 930711-0807. Violations & Deviations Noted.Major Areas Inspected:Plant Operations,Maint,Surveillance,Evaluation of Licensee self- Assessment Capability & LER Closeout
ML20057A420
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 09/03/1993
From: Holland W, Kellog P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20057A412 List:
References
50-327-93-33, 50-328-93-33, NUDOCS 9309140178
Download: ML20057A420 (41)


See also: IR 05000327/1993033

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S UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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" REGION 11

101 MARIETTA STREET, N.W., SUITE 290U

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p ATLANTA, GEORGIA 303234199

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Report Nos.: 50-327/93-33 and 50-328/93-33

Licensee: Tennessee Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga, TN 37402-2801

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Docket Nos.: 50-327 and 50-328 License Nos.: DPR-77 and DPR-79  ;

Facility Name: Sequoyah Units 1 and 2

Inspection Conducted: July 11 through August 7, 1993 '

Lead Inspector:

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Date' Signed

Inspectors: S. M. Shae fer, Resident Inspector '

A. R. Long, Resident Inspector

S. E. Sparks, Project Engineer

C. R. Ogle, Resident Inspector, H. B. Robinson

M. T. Widmann, Reactor Engineer, RII

B. R. Bonser, Senior Resident Inspector, Vogtle

S. G. Tingen, Resident Inspector, Surry

J. Zeiler, Resident Inspector, Catawba

Approved by: I ~~/ ./ 6793

Datt Signed

Pai// 'O .' ( tn1 tion 4A

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SUMMARY

Scope:

Routine resident inspection was conducted on site in the areas of plant '

operations, plant maintenance, plant surveillance, evaluation of licensee

self-assessment capability, licensee event report closecut, followup on

previous inspection findings, and engineered safety function system walkdowns. <

During the performance of this inspection, the resident inspectors conducted

several reviews of the licensee's backshift or weekend operations.

This report also addresses special inspections conducted in the areas of

backlog and operations. These two areas were identified by the licensee as

needing attention in their subt'+tal of the Sequoyah Restart Plan to the NRC.

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Results:

In the area of Operations, two examples of weaknesses were identified

regarding the adequacy of operation's procedures. One en .mple related to the

utilization of a System Operating Instruction (SOI) outside of its intended

purpose and a second example involved an S0I that was difficult to perform as

written. In addition, a lack of attention to detail was identified regarding

the completion of procedure documentation (paragraphs 3.a.2 and 3.a.3).

In the area of Operations, a violation was identified regarding inadequate

configuration controls for a temporary system important to safety (paragraph

4.a).

In the area of Engineering, a violation was identified regarding an inaccurate

Catege y 1 drawing which resulted in a control air system isolation event.

Two additional examples of Category 1 drawing discrepancies were also

identified (paragraph 4.b).

In the area of Maintenance, an Unresolved Item was identified

regarding potential inoperability of both Control Room Emergency Ventilation

System trains. This issue is unresolved pending the completion of the

licensee's incident investigation to resolve when the B train Control Room

Isolation was made inoperable (paragraph 4.d).

In the area of Maintenance, a violation was identified for failure to perform

Technical Specification required boron sampling of the water in the Unit 1 '

refueling cavity (paragraph 5.b).

In the area of Maintenance, a violation was identified for failure to perform

timely reviews of completed surveillance instructinos as required by Site

Standard Practice 8.2 (paragraph 5.d).

In the area of Plant Support, strengths were identified regarding licensee

internal and external assessments. The senior management oversight group's

continuing frank and honest perception of Sequoyah's progress allowed

management to sharpen their focus on problem areas. The Nuclear Assurance

Department continued to provide good feedback to plant management on

continuing problem areas during their ongoing assessment processes i

(paragraph 6).

In the area of Operations, an Inspector Followup Item was identified regarding

the inspector's identification of unevaluated boric acid conditions on the

inside of the Unit 1 containment steel liner and the intended design of liner

flashing (paragraph 9.b).

In the area of Plant Support, a concern was identified regarding management's

decision on Unit I to remain flooded at refueling water levels with known

refueling cavity liner leakage while concentrating on Unit 2 restart work.

Specifically, at the flooded condition, leakage through the refueling cavity i

liner resulted in NRC identification of wetting of safety-related components

in the Unit I lower containment (paragraph 9.b).

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In the area of Engineering, a violation was identified for failure to control  ;

the design / modification of heat trace on a safety system (paragraph 10.b).

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In the area of Maintenance, a weakness was identified regarding the acceptance

of degraded performance from heat trace stripchart recorders (paragraph 10.b).

In the area of Operations, a non-cited violation was identified for failure to  ;

identify a disabled annunciator in accordance with administrative requirements l

(paragraph 10.b).  !

In the area of Engineering, a Deviation was identified for failure to maintain

the FSAR current with actual plant configuration or processes (paragraph

10.c).

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REPORT DETAILS

1. Perrr w Contacted

Licensee Employees

  • R. Eytchison, Vice President Nuclear Operations
  • R. Fenechs Site Vice President
  • K. Powers, Plant Manager
  • J. Baumstark, Operations Manager
  • L. Bryant, Maintenance Manager
  • H. Burzynski, Nuclear Engineering Manager
  • D. Driscoll, Site Quality Assurance Manager
  • J. Gates, Outage Manager

C. Kent, Chemistry and Radiological Controls Manager

  • D. Lundy, Technical Support Manager
  • R. Rausch, Planning and Schedule Manager
  • R. Shell, Site Licensing Manager

J. Smith, Regulatory Licensing Manager

  • R. Thompson, Compliance Licensing Manager
  • J. Ward, Engineering and Modifications Manager
  • N. Welch, Operations Superintendent

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NRC Employees

R. Crlenjak, Chief, DRP Branch 4

P. Kellogg, Chief, DRP Section 4A

  • Attended exit interview.

Other licensee employees contacted included control room operators,

shift technical advisors, shift supervisors and other plant personnel.

Acronyms and initialisms used in this report are listed in the last

paragraph.

On July 22 and 23, Mr. A. F. Gibson, Director, Division of Reactor

Safety, Region II, visited the Sequoyah site. Mr. Gibson reviewed

restart activities with NRC inspectors onsite regarding NRC inspections-

in progress, had discussions with licensee management, and attended NRC

inspector exit meetings.

On July 22 and 23, Mr. Paul Kellogg, Section Chief, Division of Reactor

Projects, RII, visited the Sequoyah site. Mr. Kellogg toured portions

of the facility with the inspectors, met with TVA management, and

attended NRC inspector exit meetings.

On July 23, 1993-the licensee announced corporate management changes.

The changes were in the Technical Support organization. Effective

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July 26, Mr. J. P. Maciejewski moved from General Manager of Nuclear

Assurance to General Manager of Operations Services. Mr. Paul Baron,

Browns Ferry Manager of Nuclear Assurance and Licensing was selected as

the new General Manager of Nuclear Assurance. Both positions report to

Dr. Mark Medford, Vice President of Technical Support.

On July 27, the licensee issued Revision I to the Sequoyah Nuclear Plant

Restart Plan. The revision generally incorporated additional or updated

processes issued since Revision 0; reflected additional BRC task l

assignments, and incorporated senior management oversight group

comments.  ;

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On August 4, 1993 the NRC Sequoyah Restart Panel met onsite to review )

the progress of NRC activities being accomplished at Sequoyah Nuclear

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Plant prior to restart of a unit.

On August 5,1993 the NRC restart panel met with licensee management on  ;

site in a public meeting to discuss restart activities with licensee

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senior management. The licensee presented the status of restart

activities to date including ongoing licensee assessments of progress

and post restart plans. NRC management and staff members in attendance -

included:

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S. Ebneter, Region II Administrator  ;

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E. Herschoff, Director, DRP, RII i

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A. Gibson, Director, DRS, RII (NRC Restart Panel Chairman) .

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F. Hebdon, Project Director, NRR (NRC Restart Panel Member)  ;

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R. Crienjak, Chief, Branch 4, DRP, RII (NRC Restart Panel Member)

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P. Kellogg, Chief, Section 4A, DRP, RII i

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D. LaBarge, Senior Project Manager, NRR (NRC Restart Panel Member) ]

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2. Plant Status

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Unit I began the inspection period in day 95 the Cycle 6 refueling ,

outage in MODE 6 (fuel onload in progress). The licensee completed fuel l

onload on July 12. On July 16, the refueling cavity was lowered to  !

facilitate repairs to an air leak which developed on the supply line to i

the inflatable refuelii.g cavity seal. After repairs were completed on l

July 17, the refueling cavity was filled to elevation 726 and the Unit 1  ;

cavity was covered with a tarp as an FME measure. Unit I remained in  :

this condition (MODE 6) through the remainder of the period while work j

effort focused on Unit 2.  ;

Unit 2 began the inspection period in MODE 5 (Day 132 of a forced I

outage). During the period activities were completed in accordance with j

the licensee's restart plan and forced outage schedule. At the end of  ;

the inspection period, Unit 2 remained in MODE 5 with activities ongoing i

in accordance with the licensee's restart plan.

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3. Operational Safety Verification (71707)

a. Daily Inspections

The inspectors conducted daily inspections is the following areas:

control room staffing, access, and operator behavior; operator

adherence to approved procedures, TS, and LCOs; examination of

panels containing instrumentation and other reactor protection

system elements to determine that required channels are operable;

and review of control room operator logs, operating orders, plant

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deviation reports, tagout logs, temporary modification logs, and

tags on components to verify compliance with approved procedures.

The inspectors also routinely accompanied plant management on

plant tours and observed the effectiveness of management's

influence on activities being performed by plant personnel.

1) On July 17, 1993, the inspectors reviewed Unit I activities

associated with refueling cavity draindown. The draindown

was to support repairs on the air supply line to the reactor

cavity inflatable sesl (as discussed in paragraph 4.a). The

inspectors reviewed selected portions of 0-S0-68-4, DRAINING

THE REACTOR COOLANT SYSTEM, Revision 9. The inspectors

concluded that the draindown was accomplished in accordance

with c.he 50.

During the review, the inspectors were informed by the unit

operator that the final draindown was delayed. This was due

to step 6.2.20 of the instruction limiting the number of

turns which HCV-74-34, RHR to RWST return isolation valve,

was opened. Step 6.2.20 instructed the operators to

throttle HCV-74-34 to achieve less than or equal to 500 gpm

and not to exceed 2 turns open. However, during the

draindown, operators noted that the two turns allowed by the

procedure only corresponded to a 45 gpm flowrate. In

addition, the operators recalled that during prior

performances of the procedure, the flowrate may have been

much closer to the 500 gpm limit at two turns.

- Given this information, the inspectors questioned the

licensee if the reduced flow rate could be a result of

, previous inconsistencies involving operators failing to ,

appropriately account for slack in the valve operator during

the throttling of some valves.

The licensee reviewed the valve maintenance history. This

indicated that the valve had been worked on during the

current outage. This work involved tightening of the valve

internals. The licensee concluded that this accounted for

the variance in the flowrates which were observed by the

operators. The inspectors agreed with the licensee's '

determination;-however, considering the work

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performed on the valve, the change in flowrate for the

draindown could have been better anticipated. The licensee

stated that a re-baseline of the desired flowrate for a

given number of valve operator turns would be performed.

Once completed, the procedure would also be revised to

reflect the expected flowrate. The inspector did not have

any further concerns.  !

2) During a review of activities in progress concerning valve

lineup checklist, System Operating Instruction, S01-88.1, '

" Containment Iso',ation System," Revision 34, an inspector

identified a number of concerns with the sign-offs and the

use of the procedure. Four valve positions indicated on

S01-88.1 were identified by the operator as not being in the

position listed on the instruction. However, a sign-off was

made by the operator and a yellow " post-it" was placed on

the instruction to indicate the position found in the field.

During review of 501-88.1,Section V, the inspector noted

that an operator should fill out a CDS, attach it to the

instruction and circle on the procedure the mispositioned

valve (s) when identified; howaver, during the review of 501-

88.1 no valves were circled and no CDS sheet was attached to

the procedure. ,

The inspector discussed the inconsistencies with operations

personnel. 501-88.1 was developed to verify containment

isolation during reduced inventory or mid-loop. Plant

Operations was using the instruction to determine open

penetrations in containment during MODE 6 work. The

checklist was being used for recording openings in '

containment to provide information to the SR0 to enable

quick closure of the containment openings in the event it

was necessary. The inspector concluded that the checklist

procedure in use was weak in providing guidance for the .

containment closure function. However, the inspector also

concluded that the licensee did maintain configuration

control of the components during the activities. The

licensee agreed with the inspector's conclusions and

initiated the development of a new check list designed for

the specific purpose of tracking openings in the containment

during MODE 6 operations. The inspector considered the

utilization of 501-88.1 for use outside of its intended

purpose as a first example of a weakness with regard to the

adequacy of operations procedures.

In addition to the above, during the inspector's review of

SSP-12.3, EQUIPMENT CLEARANCE PROCEDURE, Revision 1, a lack

of attention to detail was identified in a operations

tag-out process. During the tagging out of the steam

generator blowdown sample isolation valves, Tag-out Number

1-92-1381, the operator did not properly fill out the valve

location or number description as part the clearance

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procedure. Two valve listings were incomplete. Valves 821

and 823 had no prefix identifier associated with the listing  ;

(e.g. 1-VLV-1-820). The licensee recognized the inattention l

during the performance of the procedure.

3) On July 29, with Unit 2 in Mode 5, the inspectors witnessed

operations personnel add borated water to the RWST from the

Boric Acid Blender using procedure 501-62.2, Boron

Concentration Control, Rev. 40. This procedure contains

multiple (12) sections for configuring the Boron

Concentration Control System in various modes of operation.

The instructions for configuring the system in its normal

mode of operation, automatic makeup, are prescribed in

Section VI.A of this procedure. In order to refill the

- RWST, the operators were using Section VI.I, Blending to  !

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RWST Using Boric Acid Blender. The refill activity was

initirted successfully and without incident. However, during l

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review of the procedure, the inspectors noted that Section i

4 VI.I was not a self-complete or stand-alone instruction in t

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that it required that the operators refer to Section VI.A to

perform critical steps and then return to Section VI.I. '

This in and of itself was not a problem, but the procedure  ;

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failed to specify which steps in Section VI.A were necessary

to be performed. The operators indicated that they knew  ;

which steps were necessary based on their knowledge of the  !

, system and from repeated performance of the procedure. The  !

l operators performed steps 1-5 in Section VI.A which included i

! verifying that valve and power availability checklists were j

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completed, as well as starting the Primary Makeup and Boric  :

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Acid Pumps, and placing the blender outlet valve to its Auto i

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! During discussions with the operators concerning the

procedure, the inspectors learned that an operations i

procedure upgrade program had been ongoing and one of the l

areas identified was the need to revise procedures with  !

multiple sections to be more self-complete or stand-alone.

The inspectors questioned the procedure writers about the  :

i status of this upgrade program and learned that it had been i

initiated in late 1987 as a result of identified weaknesses 1

in the technical quality and format of operation procedures. 1

However, the licensee reported that this project had not

been completed due to the redirection of plant resources,

and there were currently 64 procedures that had not been

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revised. The licensee reported that revisions to all

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procedures that were categorized as critical to operations

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were' completed. The inspectors concluded that without prior

knowledge or experience with the subject procedure, it would  ;

, be difficult to perform as written. This is considered a

- second example of a weakness with regard to the adequacy of 1

operations procedures. The inspectors considered that the i

upgrade project needs additional management attention.

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In addition, the inspectors, at the exit interview, ,

questioned how the remainder of the procedures to be ,

upgraded were being tracked for completion; or if the

procedures needed to be added as an additional backlog area.

The licensee indicated they would review the procedure

revision process status. The inspectors will monitor this

issue in future inspections.

b. Weekly Inspections ,

The inspectors conducted weekly inspections in the following

areas: operability verification of selected ESF systems by valve '

alignment, breaker positions, condition of equipment or component,

and operability of instrumentation and support items essential to '

system actuation or performance. Plant tours were conducted which ,

included observation of general plant / equipment conditions, fire

protection and preventative measures, control of activities in

progress, radiation protection controls, missile hazards, and ,

plant housekeeping conditions / cleanliness.

On July 17, the inspectors were in the control room to monitor

maintenance activities to repair an air leak on the Unit I reactor

cavity seal air supply line and to monitor operators control of

the draindown for the repair. A video monitor in the Unit I area  ;

of the control room had been allowing the operators to view the  :

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leaking supply line and closely monitor the actual water level

(near the vessel flange). The video camera position was being ,

controlled by Health Physics personnel (Rad Con) in the refueling

deck health physics office. However, once the maintenance

activity began, the inspectors noted that the camera was moved

from the activity to another area. The inspectors questioned the

operator as to why the camera was moved off the activity. The

operator indicated that Rad Con frequently moved the cameras off

of work in progress.

The inspectors questioned the operator if he needed to watch the

repair to the cavity seal air supply. The operator stated that he

could still adequately monitor the water level with the camera in '

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the current position. The operator also indicated that he was

reluctant to request Rad Con to move the camera back to the  ;

activity because he did not want to interfere with the work '

activity. The inspector agreed that the operator could adequately

monitor the water level with the camera in the new position;

however, the inspectors also considered that operator monitoring ,

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of the seal airline repair activity may have been appropriate due

to the importance of the evolution. i

The inspectors discussed the above practices with Operations and l

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Rad Con management. They indicated to the inspectors that the use '

of the available cameras would be better defined between *

Operations and Rad Con personnel. This included guidance for

Operations use of cameras for monitoring of evolutions in -

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progress. The inspectors considered that management actions taken

to correct the subject practices were appropriate; however, the i

inspectors also concluded that the above activity demonstrated

poor interaction between Operations and Rad Con personnel due, in

part, to inadequate communication of management expectations in

this area. i

c. Biweekly Inspections {

The inspectors conducted biweekly inspections in the following

areas: verification review and walkdown of safety-related tagouts

in effect; review of the sampling program (e.g., primary and

secondary coolant samples, boric acid tank samples, plant liquid

and gaseous samples); observation of control room shift turnover;

review of implementation and use of the plant corrective action

program; verification of selected portions of containment I

isolation lineups; and verification that notices to workers are

posted as required by 10 CFR 19.

d. Other Inspection Activities

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Inspection areas included the turbine building, diesel generator

building, ERCW pumphouse, protected area yard, control room, Unit ,

I and 2 containments, vital 6.9 KV shutdown board rooms, 480 V .

breaker and battery rooms, and auxiliary building areas including

all accessible safety-related pump and heat exchanger rooms. RCS  ;

leak rates were reviewed to ensure that detected or suspected *

leakage from the system was recorded, investigated, and evaluated; l

and that appropriate actions were taken, if required. RWPs were  ;

reviewed, and specific work activities were monitored to assure i

they were being accomplished per the RWPs. Selected radiation  ;

protection instruments were periodically checked, and equipment l

operability and calibration frequencies were verified. t

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e. Physical Security Program Inspections

In the course of the monthly activities, the inspectors included a l

review of the licensee's physical security program. The  ;

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performance of various sh:fts of the security force was observed

in the conduct of daily activities to include: protected and vital i

area access controls; searching of personnel and packages;  !

escorting of visitors; badge issuance and retrieval; and patrols t

and compensatory posts. In addition, the inspectors observed i

protected area lighting, and protected and vital areas barrier  ;

integrity.

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f. Licensee NRC Notifications

(1) On July 13, 1993 the licensee made a four hour notification

to the NRC as required by 10 CFR 50.72 regarding an

inadvertent closing of containment isolation valves during

tagout on a non-essential control air header. The closing

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of the valves constituted an ESF actuation. The event i

occurred while operators were establishing a clearance  ;

boundary for modifications to the control air system. All  !

safety systems functioned as required, with the exception ,

that the B auxiliary air compressor failed to load. The

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licensee initiated an Incidant Investigation to determine l

the root cause and develon - arrective actions for the cient.

This event is further dis u sed in paragraph 4.b.  ;

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(2) On July 15, 1993 the licensee made a special report in  ;

accordance with TS 3.7.11.1, Action b. due to the removal of  ;

portions of the auxiliary building high pressure fire *

protection system from service. The applicable system  ;

4 piping was removed to facilitate repairs to system leakage.  ;

Compensatory measures were taken to provide adequate backup .

fire protection and monitoring during the evolutions. The  !

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estimated time for the repairs was two weeks.

1 (3) On July 19, 1993 the licensee made a four hour notification  !

to the NRC as required by 10 CFR 50.72 regarding a manual

ESF actuation of the B ABGTS. A Unit 2 steam generator

1 rccirculation pump motor in the auxiliary building general ,

supply fan room caught fire necessitating stopping of the i

i auxiliary building supply fans. The stopping of the supply  :

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fans prompted the licensee to start the ABGTS to provide 4

ventilation to the affected areas. The motor fire was j

, contained in approximately six minutes. No other equipment

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was affected. The licensee initiated an incident

investigation to determine the cause of the motor fire. )

(4) On August 1, 1993 the licensee made a four hour notification  !

to the NRC as required by *.0 CFR 50.72 regarding a condition  ;

which could potentially fail to control a radiological  !

release and/or mitigate the consequences of an accident. A l

potential for both of the Control Room Ventilation trains to '

have been inoperable was discovered. The licensee

discovered that the B train MCR isolation signal was

inoperable due to a lifted lead on scal-in circuitry. The B

train CRI capability was last proved operable during testing

performed on July 15, 1993. Subsequent testing of the B

train revealed that it was inoperable. At various instances

during the period July 15 through July 29, 1993, the A train

operability was affected due to work or outages on A train

components. Corrective actions for the event involved a

field design change which installed the misplaced wire and

tested the circuitry to prove operability of the B train

CRI. This event is further discussed in paragraph 4.c as an

Unresolved Item.

(5) On August 5, 1993, the licensee made a four hour l

notification to the NRC as required by 10 CFR 50.72 l

regarding the identification of a non-1E qualified control i

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circuitry on the auxiliary building general supply and l

exhaust, and fuel handling exhaust fans. The non-lE

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qualified control circuitry on the fans could result in

their failure to trip on an auxiliary building isolation i

signal. Failure to trip would not allow adequate filtering ,

and control of radiation releases from the auxiliary  :

building. This condition was identified by licensing ,

engineering personnel as a result of a generic review of a  !

Watts Bar CAQR. The inspectors will followup on the ,

licensee's corrective actions for this issue. )

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Within the areas inspected, no violations were identified.

4. Maintenance Inspections (62703 & 42700)

During the reporting period, the inspectors reviewed maintenance i'

activities to assure compliance with the appropriate procedures and

requirements. Inspection areas included the folicwing:

a. On July 17, the inspectors monitored activities associated with ,

leaks on the Unit I cavity seal ring air supply. The leaks were  !

identified on July 14, after refueling was complete. The repairs j

were made in accordance with WR C075932 and WO 93-04454-00. The

work involved the replacement of a l\4 inch flexible tube from the 1

reactor cavity seal air supply manifold to the cavity seal. The

seal is put in place during floodup of the refueling canal and is

pressurized by air (normal) or nitrogen (backup) supplies.

The inspectors reviewed the work order package and observed the

replacement of the tube. In general, the activity was controlled

in an adequate manner. However, the inspectors observed that once

the new tube was installed, the worker stepped on the air supply  !

several times during cleanup of the job site. Also, the worker l

repeatedly stepped on the cavity seal ring (with the supply air

secured) during the beginning of the activity.

After the repairs were completed, a small leak still remained at

one of the mechanical fittings. The licensee evaluated the leak

and determined that the amount of leakage was negligible and

decided that reflooding of the refueling cavity was acceptable.

The inspectors concluded that although the repairs to the supply

line did not. fully eliminate the leakage, the repairs did

substantially reduce the leakage such that the air supply pressure

to the seal could be maintained.

During the review of the completed work package after the repairs

were performed and during discussions with plant personnel -

involved in the activity, the inspectors identified the following

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The work plan indicated that the normal and backup air I

supply to the seal were isolated; however, the return of the I

backup supply was annotated as "not applicable." j

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All of the normal and backup supply valve manipulations were ,

performed without the use of second party or independent l'

verification.

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None of the _ configuration changes to the air supply valves

were annotated on Appendix A of SSP-6.24, MAINTENANCE

MANAGEMENT SYSTEM CONFIGURATION CONTROL LOG, Revision 3.

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Although the workplan required the maintenance actirity to  ;

be performed with the vessel level at 702 feet (at f.'enge), l

the work was actually performed at several inches abow this  ;

level.  ;

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The inspectors discussed these discrepancies with licensee j

management. The most significant concern was that the normal and  :

' backup supply valves were being operated, in part, by work plan i

instructions, and not part of a configuration control program or  :

process. In addition, several of the above examples indicated  :

that valve operations were either accomplished or not accomplished l

e at the will of the craft. The inspectors considered that the j

valves associated with maintaining the reactor cavity seal j

pressurized during core alterations should be in the licensee's i

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configuration control program. j

f The inspectors reviewed the licensee's configuration control l

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program administrative requirements. The program is_ implemented l

via SSP-12.2, SYSTEM AND EQUIPMENT STATUS CONTROL, Revision 4. l

The inspectors determined that the temporary pressurization system

for +,he reactor cavity seal was not being controlled by SSP-12.2 i

during core alterations. The inspectors concluded that adequate l

controls had not been in place for the reactor cavity air supply i

to support previously performed refueling evolutions. The-  !

inspectors considered that SSP 12.2 was inadequate in that the  ;

procedure did not require configuration control for valves in this  ;

important to safety temporary system. Failure to provide for i

configuration controls for a temporary system important to safety j

is identified as a Violation (327, 328/93-33-01) Inadequate i

Configuration Control for a Temporary System Supporting fuel  !

Handling Evolutions. l

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b. On July 13, 1993, while establishing a clearance for DCN M-9507 in  !

the control air system for work involving a moisture element, both~  !

control air headers in the auxiliary building were inadvertently i

isolated. The isolation resulted in the closing of containment  ;

isolation valves associated with the ice condenser and radiation -

monitor systems.

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The inspectors responded to the plant and control room when

notified of the event. They concluded that operations response '

and immediate corrective actions for the event was good. All

safety systems functioned as required, with the exception that the i

B auxiliary air compressor was reported as to have failed to load -

as required. The licensee initiated an incident investigation to

determine the root cause and develop correctivo actions for the '

event. The cause of the isolation of both the A and B air headers

was determined to be an inaccurate category I drawing which was

used to establish the clearance boundary. Specifically, drawing ,

transition flags on the control air flow diagrams mislabeled '

headers A and B on drawing 47W848-2. This drawing error was

determined to have occurred during a 1977 revision.

WR C223971 was initiated to investigate the control air compressor

B problem. The licensee identified that the B auxiliary control

air compressor actually did load; however, valve 0-FCV-32-94, '

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Dryer Purge Valve, failed open allowing air to bypass to the vent

muffler. Repair to the failed valve was initiated and completed.

Corrective actions for the drawing problem involved a walkdown of

all the drawing transition flags on the control air drawings. No

additional problems were identified. Additional walkdowns were ,

performed on other systems such as high pressure fire protection,

service air, and raw cooling water. These systems were chosen, in i

part, due to the drawing for these systems having multiple sheets

and thus more transition flags. No additional problems were

identified. The licensee concluded that other systems that were t

previously walked down during the design baseline verification '

program were acceptable without further walkdown.

Additional corrective actions for the event, according to the t

licensee, will include a functional evaluation of the drawing .

program by Nuclear Engineering. This evaluation will utilize  !

questionnaires, drawing deviation searches, and other means to *

identify the potential extent of condition for other drawings.

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The inspectors reviewed the s@ ject event in regard to regulatory

significance. 10 CFR 50, Appeacix B, Criterion III, requires, in

part, that drawing changes be adequately reviewed for accuracy.

The failure to maintain the subject category I control air system ,

drawing in an accurate configuration is identified as a Violation [

(327,328/93-33-02).  ;

During the licensee's review of the event, they determined that '

one recent transition discrepancy was found on the service air  !

system and actions had been initiated to correct the problem prior  !

to the event of July 13. This discrepancy was also on a Category i

1 drawing. In addition, a third Category 1 drawing discrepancy

was identified by the licensee on July 29. This example involved j

logic diagram 47W611-88-1. The problem was identified during an  !

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unrelated work activity. Corrective actions for this problem were ,

initiated by the licensee.

c. On July 30, 1993, the inspectors observed the maintenance

activities associated with the 18-month calibration of

differential pressure switch FS-311-8 which controls the operation

of the Control Building Emergency Air Clean-Up Fan A-A. This

activity was accomplished according to procedure SI-197, Periodic

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Calibration of Control Building Heating Ventilation, and Air

Conditioning System, Rev. 2. The inspector verified that the

activity was properly coordinated through operations, ensuring t

that TS LCO 3.7.7 was entered for rendering Control Building

Emergency Air Cleanup Fan A-A inoperable during the activity.

Instrument technicians determined that the "as-found" setpoints

for the switch were within acceptable limits. The inspector

reviewed the work package, completed procedures, and test

equipment calibration data. No discrepancies were identified. l

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d. On August 1, 1993, an event was discovered regarding a condition

which could potentially have made inoperable both of the Control

Room Ventilation trains. The licensee discovered that the B train i

MCR isolation signal was inoperable due to a lifted lead on the i

seal-in circuitry. The B train CRI capability was last proved

operable during testing performed on July 15. Subsequent testing

of the B train on August I revealed that it was inoperable. At  !

various instances during the period July 15 through July 29, 1993,

the A train MCR ventilation system operability was affected due to

work or outages on A train components.

wediate corrective

actions for the event involved a field design change which

properly installed the misplaced wire and performed testing to

prove operability of the B train CRI capability.

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The inspector interviewed licensee personnel involved in the event

investigation process. Preliminary information indicated that

work had been performed on B train ventilation system components

shortly before the train was di covered to be inoperable on August

1. However, by the end of the inspection period, the licensee

could not determine when the lifted seal-in lead was disconnected.

The inspectors will monitor the licensee's incident investigation ,

in this area in future inspections. The event could have

potentially made inoperable both trains of the control room

isolation capability. This issue will be identified as URI 327,

328/93-33-03, pending the completion of the licensee's incident

investigation to resolve when the B train CRI was made inoperable.

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Within the areas inspected, two violations were identified. ,

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5. Surveillance Inspections (61726 & 42700)

During the reporting period, the inspectors reviewed various

surveillance activities to assure compliance with the appropriate

procedures and requirements. The inspection included a review of the

following procedures and observation of surveillance:

a. On July 20, the inspectors observed the performance of a portion

of 2-SI-SXP-074-128. A, RESIDUAL HEAT REMOVAL PUMP 2A-A QUARTERLY

OPERABILITY TEST, Revision 1. The steps observed were performed

to verify check valves 2-74-555 and 2-74-515 were closed and

sealing. The inspector observed good test control and ,

communications during the conduct of the surveillance. The

inspector also reviewed the completed surveillance package after

reviews were completed by the operating crew. No deficiencies

were noted.

b. On July 20, 1993, with Unit 1 in Mode 6 and the refueling cavity

flooded, the licensee determined that a required TS surveillance

to measure boron concentration in the Unit I refueling canal had

not been performed at the required frequency. Surveillance

requirement 4.9.1.2 states that the boron concentration of the

reactor coolant system and the refueling canal shall be determined

by chemical analysis at least once per 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The licensee has

interpreted this requirement to mean that boron samples of the RCS

and refueling canal are required at least every 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in MODE

6. The purpose of this requirement is to maintain and verify a

uniform boron concentration in the water having direct access to

the reactor vessel. This surveillance is normally performed by  ;

the chemistry department on Monday, Wednesday and Friday.

According to the licensee, chemistry technicians contacted the  :

control room on July 13,14,16 and 19 and asked if the refueling

canal was full of water. The technicians received a response that

the refueling canal was drained and concluded that a boron sample i

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was not necessary. Apparently the control room misunderstood the

technicians question and thought the question referred to the fuel

handling building transfer canal. This apparent breakdown in ,

clear communication resulted in a failure to sample the shield

building refueling canal by July 17, 1993 as required.

When cavity samples were taken the boron concentration was in ,

specification. The inspector concluded from the preliminary

information that this was an example of poor control during the

conduct of special condition surveillance. Another illustration '

of this is that the licensee identified the subject missed TS

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surveillance as a result of identifying that they had missed an '

ODCM surveillance to take tritium grab samples with the refueling '

canal flooded and the shield building exhaust in operation.

The inspectors reviewed the subject event for regulatory

significance. The failure to perform TS surveillance 4.9.1.2 is j

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identified as a Violation (327/93-33-04). In addition, the

inspectors were specifically concerned with the frequency of

missed surveillance's at Sequoyah. This was particularly evident

during the closecut of LERs in paragraph 7 of this report. This

concern was discussed with the licensee. The inspectors will r

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continue to monitor the licensee's activities in this area during

future inspections.

c. The inspectors reviewed the July 14, 1993 results of surveillance

1-SI-SFT-074-001.0, RHR Injection Flow Rate Measurement, Pump

Performance and Check Valve Test, Revision 3. One of the purposes

of this surveillance is to verify a minimum RHR pump flow rate in

accordance with TS 4.5.2.h.3. TS 4.5.2.h.3 specifies a minimum

flow rate of 3931 gpm; however,1-SI-SFT-001.0 is more ,

conservative in that it specifies a minimum flow rate of 4227 gpm.

During the test, the B RHR pump flow rate was 4100 gpm which

failed to meet the procedure's minimum acceptance criteria of 4277 i

gpm.

The B RHR pump was declared inoperable for Modes 1 through 4.  ;

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During the test of the B RHR pump, RWST level was 30%. The

licensee concluded that the cause of the low B RHR pump flow rate

was due to a low HPSH attributed to low level in the RWST. At the y

end of the inspection period, the licensee was in the process of i

revising the RHR pump flow rate acceptance criteria in 1-SI-SFT- 3

001.1 to account for the effect of RWST level on pump discharge  !

flow rate. The inspector considered the licensee's actions

adequate to resolve the concern.

d. During this inspection period, the inspectors reviewed recently

completed SI packages to determine if they were beiag reviewed  ;

within the timeframe required by the licensee's procedures. Over  ;

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the past two years, several events have occurred where, as a

result of routine engineering review of completed sis, operability  ;

problems were identified.  ;

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The inspectors reviewed procedure SSP-3.2, Surveillance Test  !

Program, Rev.1, which controls the implementation of the

licensee's surveillance program. Section ?.5.3 of this procedure i

describes the licensee's process for reviewing completed SI  ;

packages. Item 3.5.3.H requires that TS related packages be  ;

returned to the SI Scheduling Group within 10 calendar days  :

following completion of the surveillance. The inspectors reviewed l

a small sample of recently completed surveillance packages to

determine if this 10 day review period was being adhered to. As a

result, several examples were identified where this requirement

was not being met. Among these included the following:

Surveillance Procedure /Sub.iect Performance Review l

Date Time

SI-45.1 (service water pump J-A test) 05/07/93 16 days  ;

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51-45.2 (service water pump K-A test) 05/07/93 15 days

SI-45.3 (service water pump L-B test) 05/08/93 15 days

SI-45.4 (service water pump H-B test) 05/08/93 24 days

SI-46.5 (CCS pump C-S test) 06/02/93 17 days

SI-100 (vital battery channel I test) 05/28/93 18 days

SI-100 (vital battery channel II test) 05/04/93 30 days

SI-102 (diesel generator inspections) 08/06/93 12 days

The inspectors discussed these discrepancies with the SI

Scheduling Group and learned that a process existed for tracking

TS related sis that have not been returned within 10 days. The

inspectors reviewed a current (July 29) listing of delinquent sis,

noting that the total of 45 for both units was a high number. The

licensee indicated that this number had increased significantly

since the outage began, and that the number had been as high as

60. The licensee reported that prior to the outage, the i.tsber of

delinquent sis ranged between 5 and 15, which was still considered

by the inspectors to be higher than what could be reasonably

maintained during non-outage conditions. The inspectors noted

that as part of the restart program for the current dual Unit

outage, the status of delinquent sis is one of 50 backlog items

that is being tracked and is currently receiving increased

management attention. The failure to perform SI reviews in

accordance with the timeframe specified in SSP 8.2 is identified

as a Violation. This violation will be identified as VIO 327,

328/93-33-05, Failure to Follow the Requirements of SSP-8.2 for

Timely Surveillance Instruction Reviews.

Within the areas inspected, two violations were identified.

6. Evaluation of Licensee Self-Assessment Capability (40500)

During this inspection period, selected reviews were conducted of the

licensee's ongoing self-assessment programs in order to evaluate the

effectiveness of these programs.

a. On July 23, 1993 the inspectors attended the exit meeting for a

SMOG which had been established for the purpose of providing

senior TVA management with independent assessments of the Sequoyah

Restart Program and other selected areas of interest. The initial

SMOG exit meeting was discussed in inspection report 327, 328/93-

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The SM0G concluded that several of the issues identified in their ,

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initial reviews were now being addressed by Sequoyah management.

However, the SM0G considered additional management attention was

needed in insisting that programs were proactive, thorough, well ,

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individual accountability for personnel performance problems t

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a. (Closed) LER 50-327/91-01, Electrical Board Room and Main Control

Room Air Handling Unit Sequence Timers not Calibrated Within the

Required Fregrency Because of Nontechnical Specification

Classification. This issue involved the failure to test a plant

modification in accordance with TS 4.8.1.1.2.d.10 which requires

that EDG load sequence timers be calibrated every 18 months. The

plant modification involved installation of sequence timers for

the MCR and electrical board room AHUs. These sequence timers

were not calibrated in 18 month intervals after installation. The

root cause of these sequence timers not being calibrated within

the TS required frequency was the failure to recognize that the

timers were required to be calibrated by TSs. Also, the WP for

the installation of these t'; m was not expeditiously closed

which contributed to the probit ' losing the WP would have

required review of the modificat wo and identify required

surveillance procedures. As corrective action the licensee

reviewed all open WPs and made the appropriate procedural

revisions. The licensee also placed the electrical board room and

MCR air handling unit sequence timers into their SI program. The

inspectors reviewed procedures 1/2-SI-EDC-202-220.A&B, Setpoint

Verification and Calibration For Time Delay Relays Associated With

Automatic Load Sequence Timers, Revision I and verified that the

procedures contained instructions for calibrating the MCR and

electric board room AHU sequence timers. The inspectors also

reviewed the current status of open WPs and DCNs. There were

approximately 22 open WPs. Nine of the open WPs were scheduled to

be completed prior to startup of the respective unit and the

remaining dealt with security which would be closed when the

security entrance is complete. There were approximately ten open

DCNs. Seven were recently initiated and the remaining three were

approximately six to eight months old. The inspectors verified

that the three older open DCNs where either startup items or were

modifications tn non-safety related systems. The inspectors

concluded that plant modifications were being closed in a timely

manner.

b. (Closed) LER 50-327/93-06, Inadequate TS Surveillance Performance

for Four Fire Protection Valves. This issue involved a

surveillance procedure that was rewritten to incorporate the new

procedure format. During the rewrite, verification that four

containment isolation valves in the fire protection system

repositioned during the test was inadvertently omitted from the

procedure. As a result the October 7, 1991 performance of 1-SI-

OPS-82-26.A, Loss of Offsite Power With SI-D/G 1A-A Containment

Isolation Test, failed to verify that these containment isolation

valves repositioned in accordance with TSs 3.7.11.2 and 4.6.3.2.

The inspectors reviewed 1-SI-0PS-82-26. A, Revision 4 and verified

that it was revised to properly test the four valves. The

inspectors also reviewed the March 29, 1993 performance copy of 1-

SI-0PS-82-26. A, Revision 4 and verified that the four valves were

tested. As corrective action the licensee reviewed procedures

prepared or reviewed by the individuals involved with the

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The inspectors concluded that the continuing frank and honest

perception of Sequoyah's progress allowed for management to focus

on problem areas. The inspectors consider that the SMOG

assessments are a strength regarding the licensee's internal

commitment to change the way that they will do business at i

Sequoyah.  ;

b. During this inspection period, selected reviews were conducted of

the licensee's on-going self-assessment programs in order to

evaluate the effectiveness of these programs. The inspectors

continued to receive weekly debriefs from the onsite nuclear ,

assurance group. The latest debriefs indicated that progress was '

being made in all program areas. In addition, the latest SMOG

review considered the nuclear assurance restart readiness reviews

to be very positive and provide sound performance indicators that

should facilitate early identification and resolution of problems.

The inspectors consider that the Nuclear Assurance Department

continues to provide good feedback to plant management on

continuing problem areas. The inspectors consider this area to be  ;

a strength. '

c. On' July 22, 1993, the inspector monitored an incident

investigation meeting to determine the causes and corrective r

action for a missed TS surveillance. The lead investigator had

prepared a package of material on the event for each of the

meeting participants. During the meeting the lead investigator

covered the details of the event and assigned individuals follow-

up items. The inspector concluded that the meeting was productive -

for the participants; however, overall the meeting did not reach ,

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its full potential and did not appear to receive the priority one  :

would expect for an event that has occurred previously and of this

significance. One participant was distracted by having to leave

for another meeting and there was no operations representative

present to follow that important area. The inspectors will review

the results of the licensee's investigation when the LER is issued

to assess the licensee's investigation of the event. ,

Within the areas inspected, no violations were identified.

7. Licensee Event Report Review (92700)

The inspectors reviewed the LERs listed below to ascertain whether NRC

reporting requirements were being met and to evaluate initial adequacy

of the corrective actions. The inspector's review also included

followup on implementation of corrective action and/or review of

licensee documentation that all required corrective action (s) were

either complete or identified in the licensee's program for tracking of

outstanding actions.

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inadequate procedure for technical adequacy and no discrepancies

were identified. The licensee also enhanced training of ,

independent qualified reviewers to include this issue. The .

inspectors reviewed lesson plan EGT224.102, Independent Qualified  ;

Review, dated July 2, 1993 and verified that the course was

enhanced. While discussing this issue with the operations ,

procedure gnup, a procedure writer identified an error in logic

drawing 1, C/-611-88-1. The drawing did not show valves26-241 -

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and 26-242 as having a phase A containment isolation signal input.

The procedure writer processed a Design Change Notice Drawing

Deviation to get the drawing revised. This drawing problem and -

other drawing issues were also discussed in paragraph 4.b of this

report.

c. (Closed) LER 50-327/93-08, EGTS Decay Cooling Valve failed to Open l

as Required During a Surveillance Requirement Test Because of

Miscalibrated Flow Switches. This issued involved an incorrect

procedure revision that resulted in a flow switch being calibrated

to the wrong setpoints. The revision was incorrect in that a

previous revision that specified the desired flow switch setpoints

was inadvertently omitted during a subsequent revision. As a

result, the two decay cooling valves in the A EGTS train would not

automatically open if the system was placed into operation. TS 3.6.1.8 requires these valves to be operable in Modes 1, 2, 3 and

4. This condition existed from April 1992 to March 1993. The

licensee evaluated the operability of the EGTS in this condition

and concluded that the design temperature would not be exceeded.

Therefore, the system was operable. As corrective action the flow

switch was recalibrated and valves tested in accordance with 0-SI-

OPS-065-136.0, EGTS Cleanup Subsystem Functional Test, Revision 0.

The inspectors reviewed the performance copy of 0-SI-0PS-065-136.0

that was performed on April 27, 1993 and verified that the EGTS

Train A decay cooling valves properly operated. Personnel that

are qualified reviewers or preparers were retrained on how to

properly incorporate procedure revisions. The inspectors reviewed

the training letter that provided this training. Also as

corrective action the licensee sampled procedures to verify that

all procedure revisions were being properly incorporated. The QA

Department performed this review and identified another example

where procedure revisions were not properly incorporated into a

procedure. As a result the procedure group sampled additional  :

procedures and did not identify any similar findings. The QA

Department has scheduled a followup assessment in this area to

begin August 20, 1993.

d. (Closed) LER 327/93-10, Westinghouse Electric Corporation Error '

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Results in Nonconservative COMS Setpoints. This issue involved an

error in the development of the calculation for the COMS setpoints

and was generic to all Westinghouse plants that had COMS setpoints

generated by Westinghouse. The error resulted in COMS setpoints

that did not conform to the standards of 10 CFR 50.60, Acceptance

Criteria for fracture Prevention Measures for Lightwater Nuclear

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Power Reactors for Normal operation. In a letter dated June 5,

1993, the licensee requested and exemption from the requirements

of 10 CFR 50.60 and on June 18, 1993 this exemption was approved

by the NRC. This exemption allowed the licensee to operate with

the existing COMS setpoints.  ;

Within the areas inspected, no violations were identified.

8. Action on Previous Inspection Findings (92701,92702)

a. (Closed) VIO 328/92-22-02: Failure to follow the Requirements of

SSP-12.5 and Maintenance Procedure 03027-2002. This event

involved an instrument technician failing to properly re-terminate

a wire in flow switch 2-FS-74-24 associated with the miniflow

valve for RHR pump 28-B. This miswiring occurred during

performance of maintenance procedure 03027-2002 for calibrating >

the flow switch and resulted in the malfunctioning of the RHR

miniflow valve when the pump was later operated as part of routine i

testing.

The violation involved the failure to follow both the maintenance

procedure 03027-2002 and the independent verification requirements

of procedure SSP-12.6. The licensee determined the wiring error

was caused by personnel inattention to detail, inadequate self-

checking work practices, and the failure to conduct proper second '

party verification. In addition, post-maintenance test

requirements were not accomplished to ensure the proper operation

of the miniflow valve following repairs.

The inspectors reviewed the licensee's response to the violation

and verified that the licensee's corrective actions to prevent

recurrence had been satisfactorily completed. These corrc-ctive

actions included: 1) verifying the correct flow switch wiring in

all other RHR miniflow valves, 2) briefing maintenance craftsmen,

planners, and procedure writers on this event with emphasis on the

need for adequate post-maintenance testing and independent l

verification, 3) revising the RHR miniflow valve switch i

maintenance procedures to require independent verification for >

wiring connections, and 4) training planners on the proper way to

specify acceptance criteria for verifying that components can .

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perform their intended functions.

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The inspectors noted that the commitment to revise only the l

instrument calibration procedure for the RHR flow switch to be  !

limited in scope, but, during the conduct of this review, it was

found that all other instrument calibration procedures have also

been enhanced to include independent verification of lifted wires,

jumper removals, and instrument tubing connections. The

inspectors also noted that the licensee had recently revised the

verification program procedure, SSP-12.6, Equipment Status

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Verification and Checking Program, Rev. 4. This procedure was ,

effective on June 15, 1993, and resulted in fundamental changes in .

the verification process. These included: 1) deleting the 2nd f

party verification technique, 2) redefining independent .

verification as being conducted physically separate and it a  !

different time from when the activity was initially performed, and

3) adding a " Concurrent Verification" technique which requires

agreement between the performer and the verifier prior to

performing a given act. The inspectors consider these chsnges to

be enhancements to the verification process and should help reduce

the occurrence of component mispositionings due to personnel ,

error. The inspectors considered the licensee's actions in

response to this violation to be satisfactory.

b. (Closed) VIO 50-327,328/93-02-01, Violation of TS 6.8.1 for .

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Failure to follow and/or Inadequate Procedures with Multiple

Examples. In a letter dated March 25, 1993 the licznsee responded

to this violation and identified the corrective actions to be ,

implemented in response to the violation. The first example of

this violation involved operators performing switching evolutions

out of sequence. As corrective action the licensee issued SSP- ,

12.8, Switchyard Switching Order Execution, dated June 1, 1993. ,

The inspectors reviewed SSP-12.18 and verified that switching  !

orders were required to be accomplished in the given order. The

second example of this violation involved a system engineer and

non-licensed operator performing maintenance on Unit 2, number 3

heater drain tank level controller without a WR or procedure. As

corrective action the licensee issued memorandums dated April 9  ;

and 26, 1993 to Operations, Maintenance and Technical Support '

personnel explaining the station policy on adjustment of level

indication controllers and use of metering orifice clean-out

plugs. The inspectors reviewed the memorandums and considered the

policy acceptable. The inspectors also discussed the policy with

a licensed operator and concluded that the operator w&s

knowledgeable of the policy. The third example of this violation

involved delaying a PM for calibration of the Unit 2 6.9 KV

shutdown board delay relays without providing a technical

justification. As corrective action the station increased

sensitivity to delinquent PM by requiring the Maintenance Manager

to review the delinquent PM list on a weekly basis and the Site VP

review delinquent PMs on a monthly basis. The inspectors reviewed

the current delinquent PM backlog and concluded that technical

justifications were being provided for PMs that were delinquent.

However, the inspectors also noted that there were a large number,

approximately 242, of delinquent PMs with technical

justifications. The inspectors were informed that a large number

of scheduled PMs were postponed during the Cycle 5 RFOs.

c. (Closed) VIO 50-327,328/93-05-03, Failure to Comply With the ,

Requirements of TS 3.6.11, 3.6.1.2.c and 3.6.1.3.b. This issue

involved a loss of primary containment integrity due to an

improperly assembled flange on the Unit I upper containment outer

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airlock bulkhead. In a letter dated April 20, 1993, the licensec l

responded to this violation. The letter stated that as long term l

corrective action the SI that tests the containment personnel i

airlocks would be revised to include testing the back side of the  !

subject blank flange and blind flanges, with similar application,

would be evaluated to determine whether alternate testing methods

are appropriate. The inspectors reviewed SI-159.1.2, Personnel  !

Airlock Pen-X2B operability and Overall Leakage Test, Revision 3

and verified that it contained instructions to test the upper

containment outer airlock bulkhead blank flange from the back

side. The licensee's evaluation to determine if similar types of

flanges should be tested from the back side concluded that it was

not feasible. The inspectors concluded that the licensee's

corrective actions were adequate.

Within the areas inspected, no violations were identified.

9. ESF SYSTEM WALKDOWNS (71710)

During the inspection period, walkdowns were performed on portions of

the Unit 1 Reactor Coolant System (RCS), the Emergency Gas Treatment *

System (EGTS), and the Unit 1 Ice Condenser System were conducted.

Inspector findings and conclusions are discussed below.

a. EMERGENCY GAS TREATMENT SYSTEM

Areas inspected included the EGTS room, Unit 2 annulus, and the  ;

main control room EGIS panel. The following material condition

deficiencies were identified in the EGTS room:

There was an air leak located upstream of the pressure

regulator to the SOV for valve 2-FCV-65-9. '

There was tape covering a small hole in the ductwork between

valves 2-FCV-65-50 and 1-FCV-65-51. ,

The patches on the flexible ductwork downstream of EGTS fan l

B-B were not fully secured. i

The following material condition deficiencies were identified in

the Unit 2 annulus: ,

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Lubricant was leaking from the actuators on Valves 2-PSV-65= l

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87 and 2-PSV-65-81.

The annulus door was not properly aligned and the top latch

was broken.

The inspectors discussed these deficiencies with the system

engineer and walked the system down a second time with the system

engineer. During this walkdown WRs were initiated for the above

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deficiencies that had not been previously identified. Most of the  !

l deficiencies were also identified by the licensee during their .

recent walkdown of the' system. None of these deficiencies

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rendered the EGTS inoperable.

Housekeeping was considered adequate in the EGTS room and poor in

the annulus. There was debris on the floor of the annulus. The

debris included broken light bulbs, broken telephone, tape and ,

paper. There was plastic tubing, rope, cable, and electrical

extension cords hanging from the railings or walls. ,

b. UNIT 1 REACTOR COOLANT SYSTEM

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l Areas inspected included portions of the Unit I lower containment,

l raceway, seal table area, and other safety-related areas.

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Housekeeping in the general areas was adequate for an outage  ;

period. The following significant material condition deficiencies i

were identified:

(1) In the Ur. "vay, the inspectors identified remnants of

previous bot.- _.d leakage on the containment vessel steel

liner. The leakage was from various accumulator and/or fan

rooms above the raceway compartment. The inspectors noted

that the leakage had been accumulating behind a stainless

steel flashing barrier, approximately 5 feet tall, which

I runs the full circumference of the r.cceway attached to the  !

inside of the containment liner. The leakage had been

flowing behind the flashing due to deteriorated sealant

along the top of the flashing. The inspectors were ,

concerned that the boric acid behind the flashing could 1

cause corrosion on the containment liner. Based on the

appearance of the sealant, the inspectors also concluded

that the condition existed for a long period of time.

l The inspectors identified the concern to the licensee. At

the end of the inspection period, the licensee was preparing

to remove flashing from the suspect areas to inspect the

containment liner for corrosion.

In addition to the above concern, the inspectors questioned

whether the licensee had been maintaining the design basis

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for the stainless steel flashing. Preliminary reviews

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identified that the flashing design was for post-LOCA

containment liner thermal shock considerations. The

inspectors questioned whether this design function was

dependent on a water tight seal from the flashing to the

containment liner. With questionable sealing due to the

i deteriorated sealant, the inspectors considered that the

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flashing barrier was not waterproof.

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The above issues were identified as an IFI with regard to

the inspectors identification of unevaluated boric acid

conditions on the inside of the Unit I containment vessel

steel liner and design of liner flashing (IFI 327, 328\93-

33-06).

(2) Water or similar liquid was found on raceway floor near

accumulator room number 3. The inspectors' concern was that

the liquid may have been coming from behind the stainless ,

steel flashing barrier as described in previous paragraph. >

(3) During tours of the lower containment, the inspectors

reevaluated previously identified reactor cavity liner

leakage. Specifically, significant leakage from the

refueling cavity was identified as flowing down the outside

of the vessel biological shield / support concrete wall. Most

of the leakage was being collected via plastic tarps and  ;

funnels; however, some was not. Additional leakage was

identified on one of the reactor cavity drain plugs which

are installed during the outage for cavity floodup. The

liner leakage issue and potential pathways of this leakage

were previously discussed in Inspection Report 327, 328/93-

13.

Tours made by the inspectors this inspection period were

conducted with the refueling cavity at approximately 23 feet

above the vessel flange; whereas previous inspections were

performed at lower water levels. At the current level, the

liner leakage was more pronounced and estimated at

approximately 3,000 gpd by the licensee. Due to previous

concerns raised by the inspectors, increased monitoring of

the leakage quantity had been occurring; however, the

inspectors concluded that the licensee was not aggressively

monitsring current leakage paths or aware of changes in

these paths. This resulted in the inspectors identification

that safety-related components such as seismic supports,

junction boxes for both trains of control rod drive

equipment, pipe and conduit supports, etc. were being wetted

with borated water. Due to the broad area of leakage, it

was difficult for the inspectors to determine the extent of

the condition, in that, flowpaths along ventilation,

conduit, supports, and the floor of th9 containment could

have deposited the leakage in other areas.

The inspectors discussed these concerns with licensee

management. As a result, the licensee reevaluated the

priority of an existing action plan to identify the leakage

sources. The ac.tions include both wet and dry cavity

detection techniques. In addition, a preliminary evaluation

of the effect of the leakage on safety components was

initiated. The inspectors will continue to monitor the

licensee actions in this area during future inspections.

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The inspectors discussed the development of the current

situation with licensee management. Shortly after refueling

was completed, a Unit I schedule decision was made not to

install the reactor head and complete evolutions which would

include reducing the refueling cavity levels and  ;

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subsequently reduce or eliminate the subject leakage. This

decision was made, in part, to allow more work resource  ;

focus on Unit 2 restart issues. The inspectors concluded

that the decision not to complete Mode 6 evolutions was made i

without fully considering the excessive leakage through the i

Unit I cavity liner into lower containment. The inspectors

were soecifically concerned that safety-related components

and support equipment were being exposed to boric acid

envirtiments for an extended period of time.

A concern was identified regarding management's decision on

Unit 1 to remain flooded at refueling water levels with

known refueling cavity liner leakage while concentrating on

Unit 2 restart work. Specifically, at the flooded I

condition, leakaae through the refueling cavity liner i

resulted in NRC identification of wetting of safety-related

components in the Unit I lower containment.

) c. UNIT I LOWER ICE CONDENSER l

4 Areas inspected included the ice bays, visible portions of the ice  ;

buckets, and electrical and glycol conduit / piping. In addition,  :

the inspectors also reviewed the implementation of a recent q

modification to the Unit 1 ice condenser. The modification i

installed sealant to cracks which were previously identified in

the wear slab (floor) of the condenser. The following

observations and/or material condition deficiencies were

identified:

$ -

Housekeeping during modifications in progress was mixed;

however, the inspectors considered that completed areas were

adequately addressed regarding cleanliness. The inspectors

recognized that final inspections had not been performed.

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Several ice door blast bags were torn which could allow the

j shock absorber material to be released and possibly impact

the containment sump (post-LOCA).

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Several differences were identified regarding the

performance and as-left conditions of condenser floor

l sealing modifications between portions of the condenser.  ;

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The inspectors verified that the applicable work plan for  !

the modification provided the latitude for these

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4 differences. The overall adequacy of the floor sealing 4

modification will be reviewed during closeout of Violation

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327, 328/92-06-02, Failure to Meet the Requirements of TS l

3.6.5.3 for Ice Condenser Door Operability.

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During discussions with Modifications personnel, the

inspector was informed that several of the ice doors had a

potential interference fit with the door frame as a result

of the above modifications. The inspector noted that

testing (door pull test) was scheduled to be performed which

would identify any potential operability problem in this

area prior to unit restart. The licensee was informed of

this potential problem at the exit interview.

Within the areas inspected, no violations were identified.

10. RESTART REVIEW ACTIVITIES

During this period, inspection activities continued regarding review of

the licensee's restart plan. These inspections included verifications

that the licensee was following their plan in the backlog and operations

areas. Initial inspections of the licensee's restart plan were

addressed in Inspection Reports 327, 328/93-16 and 327, 328/93-23.

a. Review of Backlog Evaluation Process (71707)

During this inspection period, the inspectors reviewed the

licensee's backlog evaluation process. The inspectors verified

that open items which were evaluated by the licensee as restart

items met the criteria established. Items which were not restart

items were verified by the inspectors to have an acceptable

justification to defer until post restart. The inspectors

reviewed the system backlog notebooks which the licensee developed

to document these evaluations. The system notebooks contained

maintenance work request listings, CAQR corrective actions, DCNs,

Major Issues List items, obsolete equipment items, and other open

issues. The inspectors verified that items recommended by the BRC

as restart items were listed on the most current Restart Evalu-

ation for Sequoyah Nuclear Plant printout or were scheduled to be  :

presented to the MRRC. Items identified as non restart items were l

reviewed and discussed as necessary with the accountable system

engineer to ensure that adequate justification existed to defer l

until post restart. In addition, portions of the associated i

sections of the FSAR, TSs, and Sequoyah's Restart Plan were also

evaluated.

The systems reviewed during this inspection period are identified

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below:

System 43 -

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Sampling

System 55 -

Annunciators

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System 61 -

Ice Condenser

System 92 -

Nuclear Instrumentation

System 234 - Heat Tracing

The results of this period's review of the licensee's backlog

evaluation process indicated that, in general the process was

acceptable. However, the inspectors identified several

deficiencies in the licensee's review process. As part of the

backlog review process, the System Engineer, Department Manager,

BRC, and MRRC, review the backlog item against the restart

evaluation criteria and concur on the item being restart or post ,

restart. (MRRC only reviews backlog items considered to be

restart items.) A number of the Backlog Review Item Forms were

identified by the inspector as deficient in the following ways:  ;

. Missing signatures from either the System Engineer or

Department Manager.

  • No restart evaluation criteria xmpleted on the form during ~

the review process.

~ Restart criteria checked-off as applicable while 1

concurrently the backlog item being checked-off as having no

restart criteria applicable.

In addition, during review of a modification package provided by e

the licensee on one of the backlog items, the inspector identified  ;

missing signatures by the Nuclear Engineering Coordinator on the i

transmittal forms of primary drawings for Work Package 1516-02,

SQN AI-19 Form, Part VI Revision 10, Attachment 18.

At the time of the inspection, the missing signatures and

uncompleted restart backlog item evaluations identified by the

inspector were forwarded to the system engineer and site licensing

to be addressed. The inspectors considered these discrepancies as

an example of a lack of attention to detail.

Based on these reviews, the inspectors concluded that the backlog

review process, although not totally without error, was considered

adequate to accomplish its objective. In addition, the system ,

engineers for the systems reviewed were generally knowledgeable of

their systems functions. The engineers were cognizant of the

associated restart and post restart work scheduled on their

systems, with some exceptions as discussed in following

paragraphs.

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b. System Walkdowns (71707)

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The results of the inspectors system walkdowns were as follows:

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System 43 - Sampling

Several minor issues were identified on the sampling system to the

systems engineer and chemistry laboratory supervisor during the

wal kdown. The issues identified included: abandoned pressure,

temperature and flow equipment not tagged in the plant, pressure

gauges not properly maintained, tools (e.g. vice grips,

screwdriver, open end wrench and crescent wrench) were left inside

contaminated cabinets on small tubing, and water spillage on the

work bench at the liquid sampling panel, in a clean area, was

noted by the inspector two consecutive days during the system

wal kdowns. At the end of the inspection period, the licensee

indicated that the issues identified by the inspector would be

addressed appropriately. '

Sequoyah has a plant modification and design change control

program in place, SSP 9.3, Revision 6, that addresses abandoning

equipment. However, SSP 9.3 does not address older equipment

abandoned previous to the program being implemented. Sampling

system equipment that was abandoned in 1982 has not been tagged in

the plant. The systems engineer was aware of this discrepancy,

but the issue had not been resolved. Chemistry laboratory

technicians, users of the system, are not aware of equipment out

of service.

Upon further discussions with the system engineer and operations

personnel, the licensee was aware of other systems that have old

equipment abandoned in place and are currently not tagged in

accordance with their plant modification program SSP-9.3.  :

There was currently no mechanism in place to review old equipment

taken out of service to place it in the current abandonment

program. These concerns were brought up to the licensea at the

exit briefing. In response to the discussions, the licensee plans

to review all equipment abandoned in place and develop a complete '

listing of abandoned equipment for both units in accordance with

SSP-9.3.

During walkdowns and discussions with the systems engineer and

chemistry laboratory supervisors, the inspector was made aware

that the sampling system was functioning, but not as designed.

Compensatory measures (i.e. grab sampling) were being implemented

to ensure that sampling requirements were being met. Proper

analysis and trending of data could not be performed by the

technicians when their time was spent manually collecting grab

samples from the system. Instrument availability was identified

as a concern. Fifty percent of the sampling system instruments

were routinely inoperable, and as high as 80% at any one time.

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Numerous work requests had been written by the licensee to upgrade

the operation of the sampling system. At the time of this ,

inspection, the field work required to improve the operation and t

performance of the sampling system had begun. The inspectors

concluded that this system had not received adequate attention

during previous operation. *

System 55 - Annunciators i

The inspectors reviewed the system engineer's notebook for the

annunciator system. With the system engineer, the inspectors

reviewed the status of all items identified in the notebook. For

those items identified as non-restart the inspectors interviewed

the system engineer and other necessary tech support personnel to

understand the logic used to categorize the item as a non-restart

item. The inspectors concluded from these reviews that the

licensee had appropriately categorized backlog for the annunciator

system. The inspectors also concluded that the items identified

as post-restart had an appropriate justification to delay repairs.

The inspectors also performed a partial system walkdown. This

included an inspection of the interiors of approximately 8

cabinets containing the annunciator hardware, as well as, the

inside of two control room panels. The inspectors also witnessed

diagnostic tests performed by the system engineer on the

annunciator system.

During the walkdown, the inspectors noted minor material

deficiencies in the cabinets inspected. These included items such '

as tie wraps clippings, a wire remnant, and a disconnected clamp

for a sound powered phone conduit. The inspectors were' advised

that some of the cabinets in which the debris was found had been  ;

the subject of recent modification work and that the final

closecuts of the cabinets were not complete. These items were

identified to the system engineer for resolution. The inspectors

also noted sunflower seeds in the bottom of two annunciator

cabinets. This was identified to licensee management during the

weekly debrief on July 16, 1993. Prior to their departure from

the site, the inspectors were adviced by the system engineer that

WRs had been written to address these observations. The

inspectors concluded that none of the identified represented a  :

restart item. No other items were identified during the walkdown.

Overall, the inspectors concluded that the review of the

annunciator system backlog had appropriately categorized the

backlog work. Further, the inspectors did not note any new  ;

material deficiencies that impacted the annunciator system

readiness for restart.

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System 61 - Ice Condenser

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The inspectors reviewed the system engineer's notebook for the ice

condenser system. The inspectors discussed with system  ;

engineering personnel the status of items identified in the

notebook. For items identified as non-restart which did not have '

a clear justification, the inspectors interviewed technical

support personnel to ascertain the rationalization used to

categorize the item as a non-restart item. The inspectors

concluded from these reviews that the licensee had appropriately ,

categorized backlog for the ice condenser system. The inspectors '

also concluded that the items identified as post-restart had

appropriate jrstification for not incorporating the item into the

restart work. The inspectors also noted that the system engineer '

was reviewing the aggregate affect of all the ice condenser system

WRs on system performance.  ;

The inspector also performed partial system walkdowns in the Unit i

1 ice condenser and on associated equipment for both unit's

condensers. The results of this walkdown were previously

identified in paragraph 9.c.

System 92 - Nuclear Instrumentation

The inspector did not identify any discrepancies on the nuclear

instrumentation system. A concern was raised to the system

engineer on the cleaning of the NIS instruments. A preventive

maintenance (PM) procedure was written to require cleaning of the

NIS equipment on a routine basis. Over the last several years

that PM was eliminated. The inspector raised a concern on how the

licensee would clean the NIS instruments and what would ensure

that the equipment would not short circuit because of accumulated '

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dirt and dust. As a result of the concern identified, the

licensee is reconsidering implementing the cleaning PM for the NIS

instruments.

System 234 - Heat Tracing

The inspectors reviewed the status of all items identified in the l

system engineer's notebook. For each item, the inspectors

examined the logic used to categorize items as restart or non-  ;

restart. Special emphasis was placed by the inspectors on  :

understanding the suitability of delaying repairs for those items  !

classified as non-restart. Finally, the inspectors performed a i

partial walkdown of the system. The results and conclusions of

this inspection are discussed below:

Heat Trace Stripchart Recorders

During the system walkdown, the inspectors observed the  !

performance of the stripchart recorders installed to monitor heat  ;

trace equipped piping. Of the 8 recorders surveyed by the l

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inspectors, 7 had performance or material problems that rendered

the stripchart recorders potentially inoperable. Five of the

stripchart recorders that were potentially inoperable monitored

some TS related circuits. Four of these stripcharts had active,

high priority WRs but none were coded as restart items. (The ,

inspectors were informed that the remaining stripchart recorder

was to be repaired under a PM.)

The inspectors reviewed a listing of previous WRs associated with

the heat trace stripchart recorders. This listing indicated

previous problems similar to those observed by the inspectors as ,

well as repetitive failures.

The inspectors discussed the issue of degraded stripchart

performance with the system engineer and licensee management. The

inspectors were presented with similar arguments from several

licensee personnel to minimize the significance of the stripchart

recorders. The arguments are summarized as follows: 1) the flow

path from the boric acid tanks is not routinely designated as one

of the TS required boron injection flowpath(s) (hence, monitoring '

its temperature on a constant basis is of reduced consequence); 2)

the stripchart recorders are nbsolete and difficult to maintain;

3) the weekly TS required surveillance can be accomplished by the

use of measuring and test equipment; 4) the stripchart recorders

will be replaced during the U2C6 outage coincident with the

licensee's implementation of a reduction in boric acid

concentration; and 5) when the boric acid concentration is

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reduced, the heat tracing will be abandoned and the need to

monitor CVCS piping temperatures to prevent crystallization will

be eliminated.

The inspectors concluded that the licensee has and continues to

accept degraded performance from its heat trace stripchart

recorders. While the ISs do not require the stripchart recorders,

they are the devices used to ensure proper daily performance of a

safety-related system. If a need arises to rely on the BA system

for a TS boration flowpath, the ability to monitor and trend

temperatures of heat traced piping will be severely hampered. The

licensee's willingness to accept this degraded performance is a

weakness.

Disabled Centrol Room Annunciators

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The inspectors reviewed the status of the control room

annunciators associated with the boric acid heat trace system.

Annunciators 1-XA-55-60-21 and 1-XA-55-6C-28, SI/CVC Trouble

System A Heat Trace and SI/CVC Trouble System B Heat Trace,

respective.y, were provided in the control room to alarm on

abnormal heat trace performance. This alarm feature is discussed

Section 6.3.2.2 of the FSAR. Both alarms were disabled on March

6, 1992 in accordance with Sequoyah Nuclear Plant Periodic  ;

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Instruction 0-PI-0PS-301-001.0, Annunciator Alarm and/or P-250

Computer Point Disablement.  ;

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The inspectors independently reviewed the safety l

Assessment / Evaluation performed in accordance with site Standard  !

Practice, SSP-12.13,10 CFR 50.59 Evaluations of- Changes, Tests, i

And Experiments, to support the annunciator disablements. While j

the inspectors agreed with the conclusions of the Safety i

Assessment / Evaluation, the inspectors did note two minor errors.  ;

First, Safety Assessment Item C stated that the heat trace system '

is not required by Tech Specs. Section 3/4 1.2 of the TS Basis

states that associated heat tracing systems are required

components for the boron injection system. Thus, the statement in

the safety assessment is technically incorrect. This error was ,

not noted in the reviews of the safety assessment. However, this

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point was not central to the conclusions arrived at in the

evaluation. Furthermore, the discussion in the safety evaluation  !

correctly categorized the need for heat trace. Second, Appendix ,

C, Safety Assessment / Evaluation Cover Sheet QA Record for the {

evaluation, incorrectly states that FSAR change is not required as  :

a result of the analyzed disablements. These errors were

identified to the licensee. l

The inspectors noted on July 15, 1993, that the annunciator i

windows were not annotated to reflect the fact that the alarms  ;

were disabled. Step 6.4 [6] of Stquoyah Nuclear Plant Periodic  !

Instruction, 0-PI-0PS-301-001.0, Annunciator Alarm and/or P-250 .

Computer Point Disablement requires that a blue dot be attached to  !

the annunciator window when it is disabled. No blue dots were

affixed to the disabled annunciator windows. However, the

disabled annunciators were appropriately annotated in the 1

Disabled / Nonfunctional Annunciator Sequential Log and the points  ;

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were properly listed in the computer generated Disable Report. '

Therefore, the failure to place blue dots on the disabled

annunciator has minimal safety significance. ,

On July 21, 1993, the inspectors observed blue dots affixed to the l

disabled annunciators. The licensee also discussed with the  !

inspector a proposed change to 0-PI-0PS-301-001.0 to reduce the ,

potential for errors when disabling annunciators in the future. .

The failure to properly mark a disabled annunciator is identified  !

as a Violation (NCV 327/93-33-07), Failure to Properly Annotate ,

Disabled Control Room Annunciators. This violation will not be j

subject to enforcement action because the licensee's effort in  :

identifying and correcting the violation meet the criteria j

specified in Section VII.B of the Enforcement Policy. j

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Inoperabla Unit 1 Emergency Boration Flowpath

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Heat trace circuits 61 P/S were originally provided to maintain

the temperature of a significant portion of the boric acid-  !

flowpath to Unit I above the 145" F minimum of TS 4.1.2.1. and

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4.1.2.2.. Specifically, the circuit was originally installed

between the filter bypass line and the emergency boration line.

Hence, the circuit provided heat trace protection for the Unit I

emergency boration flowpath.

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The inspectors reviewed documentation that indicated the licensee

had experienced problems with the performance of this circuit

prior to 1992. However, repair efforts had failed to affect a

long term solution to the problem. In January 1992, a portion of

the CVCS piping in the vicinity of the emergency boration line

connection dropped in temperature. The resultant boric acid

precipitation caused a blockage in the emergency boration

flowpath. The emergency boration flowpath was subsequently

declared inoperable. The licensee's corrective actions included

clearing the blockage, installing temporary heat trace on a

portion of the emergency boration flowpath, and implementing a

TACF to resolve circuit 61 performance.

The temporary heat trace was installed on the last 6 - 8 feet of

piping in the BA flowpath just upstream of the emergency boration

line connec+'on. This 120v heat trace was powered from a plug in

a wall outlet. The installation of this heat trace was

accomplished by WR C125530. This installation resulted in a

change to the design of the heat trace circuit as described in

Section 6.3.2.2 of the FSAR. Specifically, the FSAR requires 100

percent redundant and separate heat tracing each supplied from a

separate bus capable of being connected to the redundant emergency

diesel generators.

Criterion III, Design Control of Appendix B to 10 CFR 50 requires

that design changes be subject to design control measures. Site

Standard Practice, SSP-6.1, Conduct of Maintenance, requires that

deviations from design configuration be accomplished in accordance

with AI-19 (Part VI) Modifications: Permanent Design Change

Control Program or SSP-12.4 Temporary Alterations Control Form.

Despite these requirements, the design of the heat trace circuitry

on the Ur.it 1 emergency boration flowpath was modified by a work

request on January 25, 1992. Failure to implement the design

control proce;s for modification of heat trace circuitry on CVCS

is identified as a violation (327, 328/VIO 93-33-08), Design

Change To Heat Trace Circuitry For Unit 1 Emergency Boration

Flowpath Outside Of Plant Procedures.

Temporary Alteration, TACF 0-92-0005-234 was started to

reconfigure circuits 61 P/S. The TACF divided the existing

circuit into two separate circuits. The terminal 200 feet of the .

original 61 P/S circuits was designated as 115 P/S. These new

circuits were powered through temporary cables from spare circuits

in the SIS heat trace panels. The first 60 feet of the original

circuits 61 P/S remained powered from the original power supply

and retained the original circuit designations of 61 P/S.

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Following the circuit reconfiguration, the licensee determined

that circuits 115 P/S would still not maintain satisfactory

temperatures in the CVCS piping. Therefore, the temporary heat ,

trace powered from the wall outlet was left installed and the Unit '

I emergency boration flowpath remained inoperable. It was

recognized by the licensee that additional efforts would be

required to ensure adequate heat trace circuits 115 P/S

performance. However, the TACF was not completed and no MOD /TACF

was accomplished to restore the system. ,

Throughout the inspection effort, the licensee asserted that

despite the technical inoperability of the Unit 1 emergency

boration flowpath, the flowpath remained functional. The  !

inspectors independently reviewed a Boration Flow Path

Verification Test performed in accordance with 0-SI-0PS-000-009.R

on March 19, 1993, that indicated satisfactory Unit 1 emergency

boration flows. Thus, the inspectors agreed that boric acid could  ;

be injected into Unit I along this flowpath.

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In summary, at the time of the inspector's walkdown of the boric

acid heat trace system during the week of July 12, 1993 the Unit 1

boric acid flowpath was inoperable, but available; circuits lib .

P/S were powered from temporary cables; and temporary heat trace

powered from a wall outlet was installed in the emergency boration

flowpath. This configuration had existed for approximately 18

months.

The inspectors also noted that the restoration of the Unit 1

emergency flowpath was not classified as a restart issue. The

inspectors reviewed documentation that indicated that contrary to

the system engineer's recommendation the item was categorized by

the BRC and MRRC as a non-restart issue.

Based on discussions with various licensee personnel, the

inspectors concluded that the licensee's decision not to restore

the Unit 1 emergency boratioa flowpath for the previous 18 months

or prior to restart was based on the following: the TS

requirements for boration flowpaths could be satisfied with

flowpaths from the RWST, and a modification to implement reduced

boric acid concentration, currently scheduled for the U2C6 outage

would eliminate the need for this heat tracing.

During the inspection period, the licensee decided to implement a .

modification to restore proper performance and configuration of

'

heat trace circuits 115 P/S. This modification will also remove  ;

the temporary heat trace. The inspectors were informed that this i

modification would be accomplished prior to U1 restart. Further, ,

the licensee has committed to have the MRRC revisit all '

outstanding heat trace issues.

Overall, the inspectors determined that the backlog review process ,

for the heat trace system had failed to appropriately categorize  :

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all issues. Based on arguments presented by several licensee

personnel, the' inspectors concluded that this failure was due to a

willingness by the licensee to accept degraded performance from

the heat trace system,

c. FSAR Review: (71707)  !

!

The inspector compared the current FSAR to the existing system i

configurations installed at Sequoyah Units 1 & 2. The inspectors i

identified that the licensee currently does not meet the license  !'

commitment of.FSAR Section 7.7.1.3.1, " Monitoring Functions

Provided by the Nuclear Instrumentation System," for power range i

channels. .The power range channel recorders installed in the  !

control rooms of units 1 and 2 are not, and have not, been

functioning since early 1991. At the time of the inspection, the i

licensee was not able to exactly determine when the recorders were  ;

considered inoperable. Power range channels recorders monitor  ;

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power distribution in the core within specified safe limits. The  :

recorders are used to measure reactor power level, axial- power  !

imbalance, and radial power imbalance. The power channels, as  ;

delineated in the FSAR, are to be capable of recording overpower

excursions up to 200 percent of full power. Sequoyah currently i

has that capability through the Intermediate Range recorders. ,

Based on this information, the inspectors concluded that the lack  !

of operable power range channel recorders was a Deviation from j

what was described in the FSAR.  ;

In evaluating the FSAR for the Sampling System, the inspector  :

identified a number of discrepancies between FSAR Section 9.3.2.2, t

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" System Description," and the existing system configuration

installed in the plant. Most notably were various system  :

components either abandoned, incorrect system function or type- .

component described in the FSAR for the sampling system. The  !

following examples illustrate the type of discrepancies identified  :

in the FSAR:  !

  • Not all sample lines originating within containment have

air-operated valves installed. Work Package, WP-1515 and i

WP-1516, were completed in 1990 to install solenoid operated i

valves in the steam generator blowdown sampling system.

.

  • No portable sample analyzer equipment .s available to j

measure boron concentration in the reactor coolant system as '

described in the FSAR. ,

  • Boron concentration monitors are abandoned in place, but l

their function is described in the FSAR.

  • Hot sample room primary samples are not analyzed for pH.

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. Automatic analyzers and/or recorders do not analyze silica

or sodium. The equipment associated with these variables

are abandoned or out of service. ,

FSAR discrepancies in Table 9.3.2-1, Sheets 1 - 10, describe

equipment abandoned or out of service by the licensee;

  • Specific components of the ccudensate demineralizer, System I

062, are abandoned or out of iervice.

  • Specific components of the Waste and Auxiliary Waste "

Evaporator systems are abandoned or out of service.

  • Specific components of the Waste Treatment, System 028, are

abandoned or out of service.

Revisions 6 and 8 to Table 9.3.2-1, were issued by the licensee,

on equipment which are abandoned or not in service. In addition,

sampling points currently being used by the chemistry laboratory

technicians are absent from the itemized list in the table.

Based on this review the inspector has concluded that the

licensee's current FSAR deviates from license commitments

describing the function and type of equipment in service at t

Sequoyah. The systems affected were the NIS and Sampling systems.

The identified FSAR discrepancies will be identified as a

Deviation from the FSAR (327, 328/93-33-09). ,

d. Plant Operations (71707) ,

During this period, reviews continued in the operations department +

area in accordance with the NRC restart issues plan. The

inspectors specifically focused on corrective actions for past

regulatory issues relating to conduct of operations and

configuration controls. Regulatory issues closecut is addressed

in paragraph 8.

The inspectors also reviewed the following specific items:

-

The inspectors continued to hold weekly meetings with

operations management to discuss progress being made in thre

area of operator preparation for return of Unit 2 to

operation. Conduct of operation and configuration control

areas were specifically reviewed.

-

The inspectors continued to monitor the operations

department standdown meetings which were held during this

period. Plant tours and control room observations allowed

for a determination that operator attention to detail and

accountability for actions were improving. l

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Detailed reviews on Nuclear Assurance observations in the

operations areas were reviewed.

Based on the issues addressed in this report, the inspectors

consider that sensitivity to the way business is being

accomplished at Sequoyah needs further management attention. ,

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In the areas inspected, one violation, one non-cited violation, and one

deviation were identified. ,

11. Exit Interview

The inspection scope and results were summarized on August 9,1993 with

those individuals identified by an asterisk in paragraph I above. The  ;

inspectors described the areas inspected and discussed in detail the -

inspection findings listed below. Proprietary information is not

contained in this report. Dissenting comments were not received from

the licensee.

Item Number Descrintion and Reference

VIO 327, 328/93-33-01 Inadequate Configuration Control for

a Temporary System Supporting Fuel

Handling Evolutions (paragraph 4.a).

VIO 327, 328/93-33-02 10 CFR 50, Appendix B, Criterion III

violation for failure to maintain

the subject category I control air

system drawing in an accurate

configuration (paragraph 4.b).

URI 327, 328/93-33-03 Unresolved Item pending the

completion of the licensee's

incident investigation to resolve

when the B train CRI was made

inoperable (paragraph 4.c).

VIO 327, 328/93-33-04 Failure to perform TS surveillance

4.9.1.2 concerning refueling cavity

boron concentrations (paragraph

5.b).

VIO 327, 323/93-33-05 Failure to follow the Requirements

of SSP-8.2 for Timely Surveillance

Instruction Reviews (paragraph 5.d).

IFI 327, 328/93-33-06 NRC identification of unevaluated

boric acid conditions on the inside

of the Unit I containment vessel

steel liner and the design of liner

flashing (aaragraph 9.b).

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NCV 327/93-33-07 Failure to Properly Annotate )

Disabled Control Room Annunciators  !

(paragraph 10.b). l

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VIO 327/93-33-08 Design Change To Heat Trace

Circuitry For Unit 1 Emergency

Boration Flowpath Outside Of Plant  :

Procedures (paragraph 10.b).  :

DEV 327, 328/93-33-09 Deviations from the licensee's

current FSAR and plant

configuration affecting the Nuclear

Instrumentation and Sampling systems

(paragraph 10.c).

Strengths and weaknesses summarized in the results paragraph were

discussed in detail.

Licensee management was informed of the items closed in paragraphs 7

and 8.

12. List of Acronyms and Initialisms

,

ABGTS - Auxiliary Building Gas Treatment System

AHU -

Air Handling Unit  !

AI -

Administrative Instruction

BRC -

Backlog Review Committee '

CAQR - Condition Adverse to Quality Report

CCS -

Component Cooling Water System

CDS -

Configuration Determination Sheet

CFR -

Code of Federal Regulations i

COMS - Cold Over Pressure Mitigation System

CRI -

Control Room Isolation

CVCS - Chemical Volume Control System

'

DCN -

Design Change Notice

DRP -

Division of Reactor Projects

EDG -

Emergency Diesel Generator -

EGTS - Emergency Gas Treatment System

ERCW - Essential Raw Cooling Water

ESF -

Engineered Safety Feature

FCV -

Flow Control Valve

FME -

Foreign Material Exclusion i

FSAR - Final Safety Analysis Report ,

GPD -

Gallons per Day

GPM -

Gallons per Minute

IFI -

Inspector Follow-Up

KV -

Kilovolt

LC0 -

Limiting Condition for Operation [

LER -

Licensee Event Report

LOCA - Loss of Coolant Accident

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MCR -

Control Room

NCV -

Non-cited Violation

MRRC - Management. Restart Review Committee

NIS - Nuclear Instrumentation System

NPSH - Net Positive Suction Head

NRC -

Nuclear Regulatory Commission

NRR - Nuclear Reactor Regulation

ODCM -

Offsite Dose Calculation Manual

OPS -

Operations

PMs -

Preventative Maintenance

PMT -

Post-maintenance Test

QA -

Quality Assurance

RCS - Reactor Coolant Sy, tem

RF0 -

Refueling Outage

RHR -

Residual Heat Removal i

RII -

NRC Region II

RWP -

Radiation Work Permit

RWST - Refueling Water Storage Tank

SI -

Surveillance Instruction

SMOG - Senior Management Oversight Group

50 -

System Operations

501 -

System Operating Instruction

SOS -

Shift Operating Supervisor -

S0V -

Solenoid Operated Valve

SQN -

Sequoyah

SR0 -

Senior Reactor Operator

SSP -

Site Standard Practice

TACF - Temporary Alteration Control Form

TS -

Technical Specifications

URI -

Unresolved Item

VIO -

Violation

VLV -

Valve

WO -

Work Order

WPs -

Work Plans

WR -

Work Request

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