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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2481994-10-0707 October 1994 LER 94-012-00:on 940907,discovered Failure to Perform TS Surveillance Requirements.Caused by Misunderstanding & Inadequate Technical Reviews.Ts Bases for 3/4.8.1 Will Be revised.W/941007 Ltr ML20029E5581994-05-13013 May 1994 LER 94-005-00:on 940415,dicovered That Several Valves Were Not Being Tested Per Requirements of ASME Section Xi.Caused by Inappropriate Action.Corrective Action:Pump & Valve Team Has Been Formed to Perform in Depth reviews.W/940513 Ltr ML20029D9941994-05-11011 May 1994 LER 94-006-00:on 940415,determined That on 921103, Unidentified RCS Leak Rate of Greater than 1 Gpm Occurred. Caused by Error in RCS Mass Balance Equation.Approved Temporary Change to Procedure OP-903-024.W/940511 Ltr ML20045H4731993-07-15015 July 1993 LER 93-002-00:on 930615,reactor Tripped Due to High SG Level Caused by Failure of Feedwater Control Sys.Caused by Failure of Square Root Extractor in Feedwater Flow Circuit.Failed Components Replaced & Alarm Setpoints reviewed.W/930715 Ltr ML20029B6381991-03-0808 March 1991 LER 89-007-01:on 890331,inadequate Design of Air Accumulators Due to Inadequate Review of Design Requirements Implemented as Part of post-TMI Action Plan.Design Change 3195 Phase I implemented.W/910308 Ltr ML20029A8471991-02-28028 February 1991 LER 90-019-01:on 901212,both Trains of Control Room Heating Ventilation & Air Conditioning Sys Inoperable Due to Breach in Control Room Envelope.Caused by Air Flow Past Retaining Angle.Leakage Paths repaired.W/910228 Ltr ML20028G9631990-10-0202 October 1990 LER 90-013-00:on 900903,unsampled Gas Released from Gaseous Waste Mgt Sys.Caused by Internal Leakage Past Discharge Isolation Valves.Administrative Controls in Place to Ensure That Gas Decay Tanks Sampled Prior to release.W/901002 Ltr ML20028G9211990-09-24024 September 1990 LER 90-012-00:on 900825,reactor Tripped Due to Lightning Strike.Station Mod Request Issued to Provide Uninterruptable Power Source for Steam Bypass Control sys.W/900924 Ltr ML20044A6661990-06-27027 June 1990 LER 90-006-00:on 841218.determined That Shutdown Cooling Sys Relief Valve Setpoint Not Set,Per Tech Spec Requirement. Caused by Procedural Inadequacy.Procedure MM-007-006 revised.W/900627 Ltr ML20043G1961990-06-15015 June 1990 LER 90-001-01:on 900223,discovered Controlled Ventilation Area Sys Airlock Doors D-170 & D-171 Open.Caused by Inadequate Administrative Controls.Procedural Instructions Developed to Govern Control of Air Lock doors.W/900615 Ltr ML20043G2041990-06-14014 June 1990 LER 89-006-01:on 870105,safety Class Break Requirements Not Met.Caused by Programmatic Breakdown in Administrative Controls.Valves Closed & Design Drawings & Procedures revised.W/900614 Ltr ML20043B1121990-05-21021 May 1990 LER 90-005-00:on 900420,condenser Vacuum Pump Discharge Wide Range Gas Monitor Setpoint Discovered to Be Incorrect.Caused by Inadequate Change Procedure for Data Base Manual. Administrative Procedures revised.W/900521 Ltr ML20042F7501990-05-0707 May 1990 LER 90-004-00:on 900408,partial Actuation of Emergency Feedwater Sys Occurred During Scheduled Test of Plant Protection Sys.Caused by Test Circuit Malfunction.Relay Hold Pushbutton Assembly replaced.W/900507 Ltr ML20012D6671990-03-23023 March 1990 LER 90-001-00:on 900223,discovered Controlled Ventilation Area Sys Airlock Doors D-170 & D-171 Open.Caused by Inadequate Administrative Controls.Procedural Instructions Will Be developed.W/900323 Ltr ML19354E0181990-01-22022 January 1990 LER 89-024-00:on 891223,manual Trip of Plant Initiated in Response to Decreasing Level in Steam Generator.Caused Probably by Anomaly in Main Feed Regulating Valve Pneumatic Control Sys.Tent Erected Around valve.W/900122 Ltr ML19354E0171990-01-19019 January 1990 LER 89-023-00:on 890927,MSIV 2MS-124B,determined to Have Broken Stem.Caused by MSIV Hydraulic Control Unit Thermal Valve Leakage.Replacement MSIV Stems W/Increased Blend Radius Designed to Decrease Stress installed.W/900119 Ltr ML20005E0971989-12-29029 December 1989 LER 89-017-01:on 890819,automatic Reactor Trip Initiated by Plant Protection Sys Response to Variations in Core Axial Shape Index.Caused by Failure of Pulldown & Lower Gripper Coil Current Sensors.Equipment replaced.W/891229 Ltr ML20011D2541989-12-20020 December 1989 LER 89-022-00:on 891128,plant Operated in Condition Prohibited by Tech Specs When Emergency Diesel Generator a Inoperable More than 24 H.Caused by Personnel Error.Ltr Issued to All Shift supervisors.W/891220 Ltr ML20011F4591989-12-18018 December 1989 LER 89-021-00:on 891116,emergency Diesel Generator a Declared Inoperable When Essential Svcs Chiller a Declared Inoperable W/O Verifying Availability of Offsite Ac Power. Caused by Personnel Error.Supervisor counseled.W/891218 Ltr ML19332C5781989-11-20020 November 1989 LER 89-020-00:on 891031,containment Fan Cooler C Motor Ran in Reverse Direction Reducing Air Flow & Cooling Capacity. Caused by Personnel Not Performing Surveillance Testing. Motor Rewired for Correct Slow Speed operation.W/891120 Ltr ML19327C1111989-11-13013 November 1989 LER 89-002-01:on 890125,discovered That Safety Classification of Instrument Air Tubing That Supplies Outlet Isolation Valves Installed as non-nuclear Safety.Caused by Use of Weld Filler Matl.Tech Spec Change Sent ML19324C4611989-11-13013 November 1989 LER 89-019-00:on 891012,4.16-kV Bus 3A2 Metering Potential Transformer Fuse Door Inadvertently Opened,Causing Feeder Breaker & Supply Breaker to Open & Load Sequencer to Reset. Caused by Personnel Error.Drawers relabeled.W/891113 Ltr ML19327B3511989-10-23023 October 1989 LER 89-018-00:on 890921,while Testing Main Steam Safety Valve,Lift Pressure Found to Be Below Tech Spec Allowable Value.Caused by Error in Judgement by Plant Supervisors. Event Will Be Discussed by superintendent.W/891023 Ltr 1994-05-13
[Table view] Category:RO)
MONTHYEARML20024J2481994-10-0707 October 1994 LER 94-012-00:on 940907,discovered Failure to Perform TS Surveillance Requirements.Caused by Misunderstanding & Inadequate Technical Reviews.Ts Bases for 3/4.8.1 Will Be revised.W/941007 Ltr ML20029E5581994-05-13013 May 1994 LER 94-005-00:on 940415,dicovered That Several Valves Were Not Being Tested Per Requirements of ASME Section Xi.Caused by Inappropriate Action.Corrective Action:Pump & Valve Team Has Been Formed to Perform in Depth reviews.W/940513 Ltr ML20029D9941994-05-11011 May 1994 LER 94-006-00:on 940415,determined That on 921103, Unidentified RCS Leak Rate of Greater than 1 Gpm Occurred. Caused by Error in RCS Mass Balance Equation.Approved Temporary Change to Procedure OP-903-024.W/940511 Ltr ML20045H4731993-07-15015 July 1993 LER 93-002-00:on 930615,reactor Tripped Due to High SG Level Caused by Failure of Feedwater Control Sys.Caused by Failure of Square Root Extractor in Feedwater Flow Circuit.Failed Components Replaced & Alarm Setpoints reviewed.W/930715 Ltr ML20029B6381991-03-0808 March 1991 LER 89-007-01:on 890331,inadequate Design of Air Accumulators Due to Inadequate Review of Design Requirements Implemented as Part of post-TMI Action Plan.Design Change 3195 Phase I implemented.W/910308 Ltr ML20029A8471991-02-28028 February 1991 LER 90-019-01:on 901212,both Trains of Control Room Heating Ventilation & Air Conditioning Sys Inoperable Due to Breach in Control Room Envelope.Caused by Air Flow Past Retaining Angle.Leakage Paths repaired.W/910228 Ltr ML20028G9631990-10-0202 October 1990 LER 90-013-00:on 900903,unsampled Gas Released from Gaseous Waste Mgt Sys.Caused by Internal Leakage Past Discharge Isolation Valves.Administrative Controls in Place to Ensure That Gas Decay Tanks Sampled Prior to release.W/901002 Ltr ML20028G9211990-09-24024 September 1990 LER 90-012-00:on 900825,reactor Tripped Due to Lightning Strike.Station Mod Request Issued to Provide Uninterruptable Power Source for Steam Bypass Control sys.W/900924 Ltr ML20044A6661990-06-27027 June 1990 LER 90-006-00:on 841218.determined That Shutdown Cooling Sys Relief Valve Setpoint Not Set,Per Tech Spec Requirement. Caused by Procedural Inadequacy.Procedure MM-007-006 revised.W/900627 Ltr ML20043G1961990-06-15015 June 1990 LER 90-001-01:on 900223,discovered Controlled Ventilation Area Sys Airlock Doors D-170 & D-171 Open.Caused by Inadequate Administrative Controls.Procedural Instructions Developed to Govern Control of Air Lock doors.W/900615 Ltr ML20043G2041990-06-14014 June 1990 LER 89-006-01:on 870105,safety Class Break Requirements Not Met.Caused by Programmatic Breakdown in Administrative Controls.Valves Closed & Design Drawings & Procedures revised.W/900614 Ltr ML20043B1121990-05-21021 May 1990 LER 90-005-00:on 900420,condenser Vacuum Pump Discharge Wide Range Gas Monitor Setpoint Discovered to Be Incorrect.Caused by Inadequate Change Procedure for Data Base Manual. Administrative Procedures revised.W/900521 Ltr ML20042F7501990-05-0707 May 1990 LER 90-004-00:on 900408,partial Actuation of Emergency Feedwater Sys Occurred During Scheduled Test of Plant Protection Sys.Caused by Test Circuit Malfunction.Relay Hold Pushbutton Assembly replaced.W/900507 Ltr ML20012D6671990-03-23023 March 1990 LER 90-001-00:on 900223,discovered Controlled Ventilation Area Sys Airlock Doors D-170 & D-171 Open.Caused by Inadequate Administrative Controls.Procedural Instructions Will Be developed.W/900323 Ltr ML19354E0181990-01-22022 January 1990 LER 89-024-00:on 891223,manual Trip of Plant Initiated in Response to Decreasing Level in Steam Generator.Caused Probably by Anomaly in Main Feed Regulating Valve Pneumatic Control Sys.Tent Erected Around valve.W/900122 Ltr ML19354E0171990-01-19019 January 1990 LER 89-023-00:on 890927,MSIV 2MS-124B,determined to Have Broken Stem.Caused by MSIV Hydraulic Control Unit Thermal Valve Leakage.Replacement MSIV Stems W/Increased Blend Radius Designed to Decrease Stress installed.W/900119 Ltr ML20005E0971989-12-29029 December 1989 LER 89-017-01:on 890819,automatic Reactor Trip Initiated by Plant Protection Sys Response to Variations in Core Axial Shape Index.Caused by Failure of Pulldown & Lower Gripper Coil Current Sensors.Equipment replaced.W/891229 Ltr ML20011D2541989-12-20020 December 1989 LER 89-022-00:on 891128,plant Operated in Condition Prohibited by Tech Specs When Emergency Diesel Generator a Inoperable More than 24 H.Caused by Personnel Error.Ltr Issued to All Shift supervisors.W/891220 Ltr ML20011F4591989-12-18018 December 1989 LER 89-021-00:on 891116,emergency Diesel Generator a Declared Inoperable When Essential Svcs Chiller a Declared Inoperable W/O Verifying Availability of Offsite Ac Power. Caused by Personnel Error.Supervisor counseled.W/891218 Ltr ML19332C5781989-11-20020 November 1989 LER 89-020-00:on 891031,containment Fan Cooler C Motor Ran in Reverse Direction Reducing Air Flow & Cooling Capacity. Caused by Personnel Not Performing Surveillance Testing. Motor Rewired for Correct Slow Speed operation.W/891120 Ltr ML19327C1111989-11-13013 November 1989 LER 89-002-01:on 890125,discovered That Safety Classification of Instrument Air Tubing That Supplies Outlet Isolation Valves Installed as non-nuclear Safety.Caused by Use of Weld Filler Matl.Tech Spec Change Sent ML19324C4611989-11-13013 November 1989 LER 89-019-00:on 891012,4.16-kV Bus 3A2 Metering Potential Transformer Fuse Door Inadvertently Opened,Causing Feeder Breaker & Supply Breaker to Open & Load Sequencer to Reset. Caused by Personnel Error.Drawers relabeled.W/891113 Ltr ML19327B3511989-10-23023 October 1989 LER 89-018-00:on 890921,while Testing Main Steam Safety Valve,Lift Pressure Found to Be Below Tech Spec Allowable Value.Caused by Error in Judgement by Plant Supervisors. Event Will Be Discussed by superintendent.W/891023 Ltr 1994-05-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F2891999-10-13013 October 1999 Drill 99-08 Emergency Preparedness Exercise on 991013 ML20217G7211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Waterford 3 Ses. with ML20211Q2141999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Waterord 3 Ses.With ML20210Q6361999-07-31031 July 1999 Corrected Monthly Operating Rept for July 1999 for Waterford 3 ML20210S0581999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Waterford 3.With ML20210D8951999-07-23023 July 1999 Safety Evaluation Accepting First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 - ISI-020 ML20209H3781999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Waterford 3 Ses. with ML20195J8951999-06-17017 June 1999 Safety Evaluation Granting Relief for Listed ISI Parts for Current Interval,Per 10CFR50.55a(g)(5)(iii) ML20207E8631999-06-0303 June 1999 Safety Evaluation Accepting Licensee 990114 Submittal of one-time Request for Relief from ASME B&PV Code IST Requirements for Pressure Safety Valves at Plant,Unit 3 ML20195K3391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Waterford 3 Ses.With ML20195C3041999-05-28028 May 1999 Annual Rept on Abb CE ECCS Performance Evaluation Models ML20206S7401999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Waterford 3.With ML20205T2621999-04-22022 April 1999 LER 99-S02-00:on 990216,contract Employee Inappropriately Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Security Personnel Performed Review of Work & Work Area That Individual Was Involved with ML20205N9671999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Waterford 3 Ses.With ML20205E8531999-03-30030 March 1999 Corrected Pages COLR 3/4 1-4 & COLR 3/4 2-6 to Rev 1, Cycle 10, Colr ML20205A6331999-03-25025 March 1999 SER Accepting Request to Use Mechanical Nozzle Seal Assemblies as an Alternative Repair Method,Per 10CFR50.55a(a)(3)(i) for Reactor Coolant Sys Applications at Plant,Unit 3 ML20204H1401999-03-23023 March 1999 Rev 1 to Engineering Rept C-NOME-ER-0120, Design Evaluation of Various Applications at Waterford Unit 3 ML20204H1231999-03-22022 March 1999 Rev 1 to Design Rept C-PENG-DR-006, Addendum to Cenc Rept 1444 Analytical Rept for Waterford Unit 3 Piping ML20204H2451999-03-22022 March 1999 Rev 2 to C-NOME-SP-0067, Design Specification for Mechanical Nozzle Seal Assembly (Mnsa) Waterford Unit 3 ML20204F0791999-03-17017 March 1999 Rev 1 to Waterford 3 COLR for Cycle 10 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207F3491999-03-0505 March 1999 LER 99-S01-00:on 990203,contraband Was Discovered in Plant Protected Area.Bottle Was Determined to Have Been There Since Original Plant Construction.Bottle Was Removed & Security Personnel Performed Search of Area.With ML20204B5141999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Waterford 3.With ML20203H8591999-02-17017 February 1999 Safety Evaluation Accepting Licensee Second Ten Year ISI Program & Associated Relief Requests for Plant,Unit 3 ML20199H6261999-01-21021 January 1999 Safety Evaluation Accepting Classification of Instrument Air Tubing & Components for Safety Related Valve Top Works.Staff Recommends That EOI Revise Licensing Basis to Permit Incorporation of Change ML20199C9101998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Waterford 3.With ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20206N4131998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Waterford 3.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program ML20195E5161998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Waterford 3.With ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual ML20154K0801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Waterford 3 Ses. with ML20151W8331998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Waterford,Unit 3. with ML20237B6831998-08-17017 August 1998 LER 98-S01-00:on 980723,discovered That Waterford 3 Physical Security Plan,Safeguards Document Was Not Under Positive Control of Authorized Person at All Times.Caused by Human Error/Inappropriate Action.Counseled Employee Involved ML20237C5661998-08-17017 August 1998 Safety Evaluation Accepting Licensee Request for Exemption from Section Iii.O of Appendix R to 10CFR50 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237B5261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Waterford 3 ML20236S9031998-07-22022 July 1998 SER Accepting Rev 19 to Quality Assurance Program for Waterford Steam Electric Station,Unit 3 ML20198H3911998-07-14014 July 1998 Non-proprietary Rev 5 to HI-961586, Thermal-Hydraulic Analysis of Waterford-3 Spent Fuel Pool ML20236N4181998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Waterford,Unit 3 ML20248E7781998-06-0101 June 1998 Annual Rept on Abb CE ECCS Performance Evaluation Models ML20249A4711998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Waterford 3 Ses ML20196A4051998-05-31031 May 1998 Rept of Facility Changes,Tests & Experiments,Per 10CFR50.59 for 970601-980531. with ML20198H4681998-05-20020 May 1998 Non-proprietary Rev 1 to HI-981942, Independent Review of Waterford Unit 3 Spent Fuel Pool Cfd Model ML20247A3891998-05-0101 May 1998 SG Eddy Current Examination (8th Refueling Outage) ML20247F6761998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Waterford,Unit 3.W/ ML20217M8951998-04-30030 April 1998 QA Program Manual ML20217P8281998-04-0707 April 1998 Safety Evaluation Accepting Relief Authorization for Alternative to Requirements of ASME Section Xi,Subarticle IWA-5250 Bolting Exam for Plants,Per 10CFR50.55a(a)(3)(i) ML20216B1751998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Waterford 3 Ses ML20217M1411998-03-0303 March 1998 Rev 2 of Waterford 3 Cycle 9 Colr 1999-09-30
[Table view] |
Text
. . . _ - . . . .
t Entegy saierar on ><iaa PO Box B iac-Operations xcioca.t^ 700cc Tel 004-464 3120 D.F. Packer i
Geowa:Mmaur nam onem j W*ertyd 3 W3F1-94-0050 i
A4.05 PR May 13, 1994 U.S. Nuclear Regulatory Commission
. Attn: Document Control Desk Washington, D.C. 20555 i
Subject:
Waterford 3 SES 1
Docket No. 50-382 License No. NPF-38 Reporting of Licensee Event Report i
Gentlemen: ,
I Attached is Licensee Event Report Number LER-94-005-00 for Waterford Steam Electric' Station Unit 3. This Licensee Event Report is submitted in accordance with 10CFR50.73(a)(2)(i). ,
l )
Very truly yours, iQ D.F. Packer General Manager Plant Operations l DFP/GCS/tjs Attachment 2 cc: L.J. Callan, NRC Region IV 4
G.L. Florreich J.T. Wheelock - INP0 Records Center R.B. McGehee N.S. Reynolds NRC Resident Inspectors Office (WADM526)
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Administrator - LRPD 9405190094 940513
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NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED 3Y OMB NO. 3150-0104 (5 *2) l .
EXPIRES 5/31/95 l
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' LICENSEE EVENT REPORT (LER) M.!?S$u'5sCnEZ TSUJiaO ,Nrst @l:"C AND RECORDS MANAGEME NT eMNcs !MNgg 7714L U S NUCiE AR HL SULATOm COMM LEN. A A.cnNLiON, DC 2 %$ 0001, AND 70 THE PAPEHWDRK REDUCh0N PROJECT (3150 0104t. OF FiCE OF '
I (See reverse for reouired number of digits / characters for each block) MANAGEMENT AND BUDGET, WASHING'ON, DC 2203 '
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Waterford Steam Electric Station Unit 3 05000 PAGE 10F p)5 Tif LE (4) ,
Valves in the Inservice Test Plan - Pump and Valve, not Tested '
, EVENT DATE (5) LER NUMBER (6i REPORT NUMBER (7) OTHER FACILITIES INVOLVED (8)
MONT H DAY YEAR YEAR MONTH DAY YEAR f AQUIY NAME DOCFIT NUMHC H
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04 15 94 94 - 005 00 05 13 94 n/a 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 6: (Check one or more) (11)
MODE (9) 5 l 20 402(b) 20.405(c) 50.73(a>(2)(iv) 73 71(bi l POWER ' 20 405(a)(1)(i) 50.36(c)(1) 5013(a)(2)(v) 73.71(c) ,
LEVEL (10) 0 20 405(a)U)(n) 50.36(c)(2) 50 73(a)(2)(vii) OTHER l 20.405(a)(1)(ni) A 50.73sa )(2)(il 50 73(a)(2)(vui)(A) W'W '" At*ac' 20.405ta)(1)(tv) 50.73(a)(2)(ii) 50.73(a)(2)(vui)(B) r, A[
20.405(a)(1)(v) 5013(a)(2)(ni) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
- h. A Mt i TELEPHONE NuYULH pr.clude A'ea Gocel John Houghtaling, Mgr. Tech. Services 504/464-3131 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTE M COMPONENT MANUFACTURER CAUSE SYSTEM COMOONENT MANUFACTURER y SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED WJN'" uv vt Aa f es, compie?e EXPECTED SUBMtSS:ON CATE No X
ABSTRACT (Limit to 1400 spaces. i.e , approximately 15 single-spaced typewritten knes) (16)
On April 15, 1994, a Shift Technical Advisor discovered that several valves were not being tested per the requirements of ASME section XI. Specifically valves SI-6011, SI-6012, CVR-401A and CVR-401B remote position indicators were not being observed at least once every two years to verify that valve position matched remote indication. Also identified was that power operated valves SBV-ll3A, SBV-1138, SBV-114A and SBV-ll4B were not being timed in their closed stroke direction. Technical Specification 4.0.5(a) requires that inservice testing of ASME Code Class 1, 2, and 3 pumps and valves be performed in accordance with Section XI of the ASME Boiler and Pressure Vessel Code.
The root cause of this event is inappropriate action resulting in a failure to properly incorporate IST Plmn requirements into the appropriate operating procedures during initial IST Plan implementation. A Pump & Valve Review Team has been established to perform an in depth review of the Plan and the associated implementing documents. This event did not compromise the health and safety of the public.
NRC F ORM 366 (5 90
REQUIRED NUMBER OF DIGITS / CHARACTERS
- FOR EACH BLOCK BLOCK NUMBER OF TIRE NUMBER DIGITS / CHARACTERS 1 UP TO 46 FACILITY NAME !
2 DOCKET NUMBER 3 IN ADDITIO TO 05000 3 VARIES PAGE NUMBER 4 UP TO 76 TITLE 5 ^
2 PER BLOCK 7 TOTAL 6 LER NUMBER 3 FOR SEQUENTIAL NUMBER 2 FOR REVISION NUMBER 7 ^
2 PER BLOCK UP TO 18 - FACILITY NAME OTHE FACILUIES MOND 8 TOTAL - DOCKET NUMBER 3 IN ADDITION TO 05000 9 1 OPERATING MODE 10 3 POWER LEVEL I' REQUIREMENTS OF 10 CFR CHECK BOX THAT APPLIES 0 50 FOR NME 12 LICENSEE CONTACT 14 FOR TELEPHONE l CAUSE VARIES I 2 FOR SYSTEM 13 4 FOR COMPONENT EACH COMPONENT FAILURE 4 FOR MANUFACTURER NPRDS VARIES l 14 CHECK BOX THAT APPLIES
"^ j 15 2 PER BLOCK I l l
l l
1 i
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l REQUIRED NUMBER OF DIGITS / CHARACTERS FOR EACH BLOCK I NUMBER OF BLOCK I
NUMBER DIGITS / CHARACTERS l 1 UP TO 46 FACILITY NAME l DOCKET NWBER 3 IN ADDITION TO 05000 3 VARIES PAGE NUMBER l
l 4 UP TO 76 TITLE 5 NT DATE 2 PER BLOCK 7 TOT AL 2 M YEAR LER NUMBER 6
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'# ECE D CHECK BOX THAT APPLIES 15 EXPECTED SUBMISSION DATE 2 PER BLOCK
l i
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMisslON APPROVED BY OMB NO. 3150-0104 l Iset ,
EXPIRES $/31/95 l fN O CT R ; O HRS A LICENSEE EVENT REPORT (LER) COMusN1s ReaARosa sanots tsrum To THc iNrORMues TEXT CONTINUATION E"$a" 8c S7%$$'5*178d'S'A$$"$$
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Waterford Steam Electric Station Unit 3 05000 382 2 OF 5 94 - 005 -
00 l r ~ ~. ,,-. . n,.a .. . ._,.., -= F - n o r, REPORTABLE OCCURRENCE j On April 15, 1994, a Shift Technical Advisor discovered that valves were )
not being tested per the requirements of ASME section XI. Specifically valves SI-6011 (EIIS Identifier BP-FSV), SI-6012 (EIIS Identifier BP-FSV),
CVR-401A (EIIS Identifier BF-FSV) and CVR-401B (EIIS Identifier BF-FSV) remote position indicators were not being observed at least once every two years to verify that their valve operators were accurately indicated as per the requirements of ASME Section XI Article IWV-3300. Also power operated valves SBV-113A (EIIS Identifier VC-20), SBV-1138 (EIIS Identifier VC-20),
SBV-114A (EIIS Identifier VC-20) and SBV-114B (EIIS Identifier VC-20) were not being timed in their closed stroke direction as per the requirements of ASME Section XI Article IWV-3413(b). Technical Specification 4.0.5(a) requires that inservice testing of ASME Code Class 1, 2, and 3 pumps and
, valves be performed in accordance with Section XI of the ASME Boiler and Pressure Vessel Code. The failure to test these valves per A3ME section XI requirements is a violation of Waterford 3 Technical Specification 4.0.5(a) which requires testing of ASME code class 1, 2, and 3 pumps and valves. Per 10CFR50.73(a)(2)(i)(B) any operation or condition prohibited by the plant's Technical Specification is reportable as an LER.
INITIAL CONDITIONS Plant Power 0%
Plant Operating Mode: Mode 5; Cold Shutdcwn Procedures Being Performed Specific to This Event: None Technical Specification LC0's in Effect Specific to this Event: None Major Equipment Out of Service Specific to this Event: None NRO FORM 366A (5 94
b 3 FORM 366A U.S. NUCLEAR REGULATORY COMMISSIOII APPROVEo BY OMB NO. 3150-0104 sn EXPIRES 5/31/95 ESTIMATED BUROEN PER RESPONSE TO COMPLY WITH TH:s LICENSEE EVENT REPORT (LER) E " E s"REf E E nif fs*'u d b E M fv" %2l TEXT CONTINUATION g u"5 $***v"v's i E *$11"r$"E**'$'A N "$$^$
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F ACILITY NAME (1) DOCH ET NUMBER (2) LER NUMBER 14) PAGE (3)
SEQvE TA REv;SiON I YUR NUVSER NUMBER Waterford Steam Electric Station Unit 3 05000 382 3 oF 5 94 - 005 -
00 1 EXT pt more space is revea, use edwtionai comes o! kRC Form 3664 (17) l EVENT SEQUENCE l
On April 15, 1994 a Shift Technical Advisor (STA) discovered during a review of the Waterford 3 Pump and Valve Inservice Test Plan (IST) that valves SI-60ll, SI-6012, CVR-401A, CVR-401B, SBV-113A, SBV-1138, SBV-ll4A and SBV-ll48 were in the IST plan as required but their testing requirements were only partially addressed in the plant's implementing procedures.
I Valves SI-6011, SI-6012, CVR-401A and CVR-401B have been in the IST Plan since revision 1 dated April 4, 1984. The ASME Section XI requirement to verify that valve position indicators are accurately indicating has never been proceduralized and consequently never verified. Valves SBV-Il3A, SBV-113B, SBV-114A and SBV-1148 have been in the IST Plan since revision 0 dated August 16, 1982. The ASME Section XI requirement to time these valves ;
in the closed stroke direction has also never been proceduralized and consequently never verified. l l
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CAUSAL FACTORS The root cause of this event is inappropriate action resulting in a failure !
I to properly incorporate IST Plan requirements into the appropriate -
operating procedures during initial IST Plan implementation. Although past corrective actions associated with the IST problems appeared to be adequate, it is believed that due to the accumulation of unrelated concerns identified with the Plan, a full review of it and its implementing documents is warranted.
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NRC FORM 366A (S 921 I
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSloN APPROVED BY OMB No. 3150-0104 (s e2) EXPlRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THis
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SEQUENTIAL REVIS60N YEAR Waterford Steam Electric Station Unit 3 05000 382 3 oF 5 94 - 005 00 Tw vi n. ,o.c. , n,.a. . .-- ..n. a wc r.<,, xm o n EVENT SE0VENCE On April 15, 1994 a Shift Technical Advisor (STA) discovered during a review of the Waterford 3 Pump and Valve Inservice Test Plan (IST) that valves SI-60ll, SI-601'2, CVR-401 A, CVR-401B, SBV-ll?A, SBV-ll3B, SBV-ll4A and SBV-ll4B were in the IST plan as required but their testing requirements were only partially addressed in the plant's implementing procedures.
Valves SI-60ll, SI-6012, CVR-401A and CVR-4018 have been in the IST Plan since revision 1 dated April 4, 1984. The ASME Section XI requirement to verify that valve position indicators are accurately indicating has never
, been proceduralized and consequently never verified. Valves SBV-113A, SBV-Il3B, SBV-Il4A and SBV-ll4B have been in the IST Plan since revision 0 l dated August 16, 1982. The ASME Section XI requirement to time these valves l in the closed stroke direction has also never been proceduralized and consequently never verified.
CAUSAL FACTORS
- The root cause of this event is inappropriate action resulting in a failure to properly incorporate IST Plan requirements into the appropriate operating procedures during initial IST Plan implementation. Although past corrective actions associated with the IST problems appeared to be adequate, it is believed that due to the accumulation of unrelated concerns identified with the Plan, a full review of it and its implementing documents is warranted.
NRC FORM 366A {5 92)
1 .
J NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (s 02 ,
EXPIRES 5/31/95
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DOCKET NUMBER (2) LER NUMBER (s) PAGE (3)
FACILITY NAME (1)
SEQVENTaAL REVISION mR ""**'" ""**'"
Waterford Steam Electric Station Unit 3 05000 382 i op 5 94 - 005 -
00 TEXT (it inore space es reewes, use ea:nonal copies of NAC Form J66Aj (17)
IMMEDIATE CORRECTIVE MEASURES i
j lhe required IST testing of valves SI-6011, SI-6012, CVR-401A, and CVR-4018 was performed on April 17, 1994 per work authorization WA 01123100. A l
2 procedure change for OP-903-043 was initiated to t%e the closure of valves SBV-113A, SBV-113B, SBV-114A and SBV-114B per the requirement of the IST plan.
l ACTIONS TO PREVENT RECURREi4CE j
I A Pump & Valve Review Team has been established to perform an in depth review of the IST Plan to ensure all current IST requirements are procedurally implemented.
A periodic test method will be implemented for valves SI-6011, SI-6012, CVR-401A and CVR-401B to verify valve position indications.
SAFETY SIGNIFICANCE 4
The purpose of the inservice testing of the valves identified in this LER i was to determine the amount of valve degradation. Upon the discovery that
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valves SI-6011, SI-6012, CVR-401A, and CVR-401B position indicators were
- not being verified they were immediately tested and proven to be operational.
Although plant procedures have no time requirement associated with stroking these valves closed, valves SBV-113A, SBV-1138, SBV-114A, and SBV-114B were stroked in both the open and close position per plant procedure OP-903-043 NRC FOAV 366A (5 92)
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SEQUENTA REVtSiON WR NUMBER NUMBER
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Waterford Steam Electric Station Unit 3 382 5 op 5 05000 !
l 94 -
005 - 00 l Tw w -. w.c. a r.w.s . .xw.a.e.. .r uaC m ass e n
" Shield Building Ventilation System Operability Check" . As such, the
! operability of the valves was demonstrated.
i Based on the above, this event did not compromise the health and safety of the general public or plant personnel. ;
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SIMILAR EVENTS 2
j Problems with the IST Plan were identified in LER 89-014 and LER 90-010. In LER 89-014 the Auxiliary Component Cooling Water-valves (EIIS Identifier l BI-V) ACC-116A and ACC-116B were not included in the Pump & Valve IST g
program. The root cause of this event was misinterpretation of the ASME
, Section XI definition of ' active ' valves. Because ACC-116A and ACC-1168 i
were judged to be ' passive' in relation to the ASME XI definition ,- they i were never included in the IST program. In LER 90-010 feedwater check l valves, FW-181A and FW-181B, and both Emergency Diesel Generator fuel oil transfer pumps had been excluded from the Pump & Valve IST program. The
! root cause of this event was an inadequate review of ASME Section XI IST l requirements during the development of the Pump & Valve IST Plan program.
- Although these events are related to the events described in this LER, the I
significant difference is that for the events of this LER there were no ,
k discrepancies identified with the Pump and Valve IST plan but with the
! procedural implementation of the plan.
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d NRC FORM 366A $ 92)
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