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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2481994-10-0707 October 1994 LER 94-012-00:on 940907,discovered Failure to Perform TS Surveillance Requirements.Caused by Misunderstanding & Inadequate Technical Reviews.Ts Bases for 3/4.8.1 Will Be revised.W/941007 Ltr ML20029D9941994-05-11011 May 1994 LER 94-006-00:on 940415,determined That on 921103, Unidentified RCS Leak Rate of Greater than 1 Gpm Occurred. Caused by Error in RCS Mass Balance Equation.Approved Temporary Change to Procedure OP-903-024.W/940511 Ltr ML20045H4731993-07-15015 July 1993 LER 93-002-00:on 930615,reactor Tripped Due to High SG Level Caused by Failure of Feedwater Control Sys.Caused by Failure of Square Root Extractor in Feedwater Flow Circuit.Failed Components Replaced & Alarm Setpoints reviewed.W/930715 Ltr ML20042F7501990-05-0707 May 1990 LER 90-004-00:on 900408,partial Actuation of Emergency Feedwater Sys Occurred During Scheduled Test of Plant Protection Sys.Caused by Test Circuit Malfunction.Relay Hold Pushbutton Assembly replaced.W/900507 Ltr ML19332C5781989-11-20020 November 1989 LER 89-020-00:on 891031,containment Fan Cooler C Motor Ran in Reverse Direction Reducing Air Flow & Cooling Capacity. Caused by Personnel Not Performing Surveillance Testing. Motor Rewired for Correct Slow Speed operation.W/891120 Ltr ML19324C4611989-11-13013 November 1989 LER 89-019-00:on 891012,4.16-kV Bus 3A2 Metering Potential Transformer Fuse Door Inadvertently Opened,Causing Feeder Breaker & Supply Breaker to Open & Load Sequencer to Reset. Caused by Personnel Error.Drawers relabeled.W/891113 Ltr ML19327C1111989-11-13013 November 1989 LER 89-002-01:on 890125,discovered That Safety Classification of Instrument Air Tubing That Supplies Outlet Isolation Valves Installed as non-nuclear Safety.Caused by Use of Weld Filler Matl.Tech Spec Change Sent ML19327B3511989-10-23023 October 1989 LER 89-018-00:on 890921,while Testing Main Steam Safety Valve,Lift Pressure Found to Be Below Tech Spec Allowable Value.Caused by Error in Judgement by Plant Supervisors. Event Will Be Discussed by superintendent.W/891023 Ltr 1994-05-11
[Table view] Category:RO)
MONTHYEARML20024J2481994-10-0707 October 1994 LER 94-012-00:on 940907,discovered Failure to Perform TS Surveillance Requirements.Caused by Misunderstanding & Inadequate Technical Reviews.Ts Bases for 3/4.8.1 Will Be revised.W/941007 Ltr ML20029D9941994-05-11011 May 1994 LER 94-006-00:on 940415,determined That on 921103, Unidentified RCS Leak Rate of Greater than 1 Gpm Occurred. Caused by Error in RCS Mass Balance Equation.Approved Temporary Change to Procedure OP-903-024.W/940511 Ltr ML20045H4731993-07-15015 July 1993 LER 93-002-00:on 930615,reactor Tripped Due to High SG Level Caused by Failure of Feedwater Control Sys.Caused by Failure of Square Root Extractor in Feedwater Flow Circuit.Failed Components Replaced & Alarm Setpoints reviewed.W/930715 Ltr ML20042F7501990-05-0707 May 1990 LER 90-004-00:on 900408,partial Actuation of Emergency Feedwater Sys Occurred During Scheduled Test of Plant Protection Sys.Caused by Test Circuit Malfunction.Relay Hold Pushbutton Assembly replaced.W/900507 Ltr ML19332C5781989-11-20020 November 1989 LER 89-020-00:on 891031,containment Fan Cooler C Motor Ran in Reverse Direction Reducing Air Flow & Cooling Capacity. Caused by Personnel Not Performing Surveillance Testing. Motor Rewired for Correct Slow Speed operation.W/891120 Ltr ML19324C4611989-11-13013 November 1989 LER 89-019-00:on 891012,4.16-kV Bus 3A2 Metering Potential Transformer Fuse Door Inadvertently Opened,Causing Feeder Breaker & Supply Breaker to Open & Load Sequencer to Reset. Caused by Personnel Error.Drawers relabeled.W/891113 Ltr ML19327C1111989-11-13013 November 1989 LER 89-002-01:on 890125,discovered That Safety Classification of Instrument Air Tubing That Supplies Outlet Isolation Valves Installed as non-nuclear Safety.Caused by Use of Weld Filler Matl.Tech Spec Change Sent ML19327B3511989-10-23023 October 1989 LER 89-018-00:on 890921,while Testing Main Steam Safety Valve,Lift Pressure Found to Be Below Tech Spec Allowable Value.Caused by Error in Judgement by Plant Supervisors. Event Will Be Discussed by superintendent.W/891023 Ltr 1994-05-11
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F2891999-10-13013 October 1999 Drill 99-08 Emergency Preparedness Exercise on 991013 05000382/LER-1999-014, :on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B1999-10-12012 October 1999
- on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B
ML20217G7211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Waterford 3 Ses. with 05000382/LER-1999-013, :on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included1999-09-23023 September 1999
- on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included
05000382/LER-1999-012-01, :on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With1999-09-13013 September 1999
- on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With
ML20211Q2141999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Waterord 3 Ses.With 05000382/LER-1999-011-01, :on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B1999-08-31031 August 1999
- on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B
05000382/LER-1999-010-01, :on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity1999-08-26026 August 1999
- on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity
05000382/LER-1999-009-01, :on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established1999-08-26026 August 1999
- on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established
ML20210Q6361999-07-31031 July 1999 Corrected Monthly Operating Rept for July 1999 for Waterford 3 ML20210S0581999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Waterford 3.With 05000382/LER-1999-008-01, :on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-021999-07-29029 July 1999
- on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-02
05000382/LER-1999-007-01, :on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff1999-07-23023 July 1999
- on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff
ML20210D8951999-07-23023 July 1999 Safety Evaluation Accepting First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 - ISI-020 05000382/LER-1999-006-01, :on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With1999-07-14014 July 1999
- on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With
ML20209H3781999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Waterford 3 Ses. with 05000382/LER-1999-005-01, :on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested1999-06-24024 June 1999
- on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested
ML20195J8951999-06-17017 June 1999 Safety Evaluation Granting Relief for Listed ISI Parts for Current Interval,Per 10CFR50.55a(g)(5)(iii) ML20195J9741999-06-16016 June 1999 Safety Evaluation Supporting Amend 152 to License NPF-38 ML20207E8631999-06-0303 June 1999 Safety Evaluation Accepting Licensee 990114 Submittal of one-time Request for Relief from ASME B&PV Code IST Requirements for Pressure Safety Valves at Plant,Unit 3 ML20195D5491999-06-0303 June 1999 Safety Evaluation Supporting Amend 151 to License NPF-38 ML20195K3391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Waterford 3 Ses.With ML20195C3041999-05-28028 May 1999 Annual Rept on ABB CE ECCS Performance Evaluation Models 05000382/LER-1999-004-02, :on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing1999-05-14014 May 1999
- on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing
ML20206S7401999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Waterford 3.With ML20205T2621999-04-22022 April 1999 LER 99-S02-00:on 990216,contract Employee Inappropriately Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Security Personnel Performed Review of Work & Work Area That Individual Was Involved with ML20206A9641999-04-21021 April 1999 Safety Evaluation Supporting Amend 150 to License NPF-38 05000382/LER-1999-003-02, :on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With1999-04-0909 April 1999
- on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With
ML20205N9671999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Waterford 3 Ses.With ML20205E8531999-03-30030 March 1999 Corrected Pages COLR 3/4 1-4 & COLR 3/4 2-6 to Rev 1, Cycle 10, Colr ML20205A6331999-03-25025 March 1999 SER Accepting Request to Use Mechanical Nozzle Seal Assemblies as an Alternative Repair Method,Per 10CFR50.55a(a)(3)(i) for Reactor Coolant Sys Applications at Plant,Unit 3 05000382/LER-1999-002-03, :on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired1999-03-25025 March 1999
- on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired
ML20204H1401999-03-23023 March 1999 Rev 1 to Engineering Rept C-NOME-ER-0120, Design Evaluation of Various Applications at Waterford Unit 3 ML20204H1231999-03-22022 March 1999 Rev 1 to Design Rept C-PENG-DR-006, Addendum to Cenc Rept 1444 Analytical Rept for Waterford Unit 3 Piping ML20204H2451999-03-22022 March 1999 Rev 2 to C-NOME-SP-0067, Design Specification for Mechanical Nozzle Seal Assembly (Mnsa) Waterford Unit 3 ML20204F0791999-03-17017 March 1999 Rev 1 to Waterford 3 COLR for Cycle 10 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207F3491999-03-0505 March 1999 LER 99-S01-00:on 990203,contraband Was Discovered in Plant Protected Area.Bottle Was Determined to Have Been There Since Original Plant Construction.Bottle Was Removed & Security Personnel Performed Search of Area.With ML20204B5141999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Waterford 3.With ML20203H8151999-02-17017 February 1999 Safety Evaluation Supporting Amend 149 to License NPF-38 ML20203H8591999-02-17017 February 1999 Safety Evaluation Accepting Licensee Second Ten Year ISI Program & Associated Relief Requests for Plant,Unit 3 05000382/LER-1999-001, :on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With1999-02-0404 February 1999
- on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With
ML20202H9161999-02-0202 February 1999 Safety Evaluation Supporting Amend 148 to License NPF-38 ML20199H6261999-01-21021 January 1999 Safety Evaluation Accepting Classification of Instrument Air Tubing & Components for Safety Related Valve Top Works.Staff Recommends That EOI Revise Licensing Basis to Permit Incorporation of Change 05000382/LER-1998-020, :on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With1998-12-31031 December 1998
- on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With
ML20199C9101998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Waterford 3.With ML20198F4691998-12-21021 December 1998 Safety Evaluation Supporting Amend 147 to License NPF-38 ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20206N4131998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Waterford 3.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program 1999-09-30
[Table view] |
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Ref: 10CFR50.73(a)(2)(1)
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October. 23, 1989 U.S., Nuclear Regulatory Commission ATTENTION: Docu'nent Control Desk Washington, D.C, 20555
Subject:
Waterford 3 SES Docket No. 50-382
' License No. NPF-38 Reporting of Licensee Event Report Centlement Attached is Licensee Event Report Number LER-89-018-00 for Waterford Steam Electric Station Unit 3. This Licensee Event Report is submitted pursuant to 10CFR50.73(a)(2)(i).
Very truly yours,
\ g J.R. McGaha 4 Plant Manager - Nuclear JRM/PTG/rk (w/ Attachment) cci Messrs. R.D. Martin J.T. Wheelock - INPO Records Center E.L. Blake W.M. Stevenson D.L. Wigginton NRC Resident Inspectors Office G910300230 891023 ADOCK0500gj2
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On September 21, 1989 Waterford Steam Electric Stntion Unit 3 was operating at 100% reactor power. At 1241 hours0.0144 days <br />0.345 hours <br />0.00205 weeks <br />4.722005e-4 months <br />, while testing a Main Steam Safety Valve, the lift pressure was found to be below the Technical Specification (TS) allowable value. Because of aberrations in indicated main steam pressure when repositioning a gauge that was improperly installed, the surveillance was invalidated. Test equipment (pressure gauge and chart recorder) were checked for proper calibration and operation by 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br />. The surveillance test was performed again at 2037 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.750785e-4 months <br />. The valve was found to lift at a higher pressure but still below the TS limit. The valve setpoint was out of tolerance low in l excess of the four hour TS action requirement. This event is therefore reportable as a condition prohibited by TS.
Although event has identified areas that require improvements, there was a good
' faith effort by all involved personnel to meet the TS requirement by completing the test promptly while insuring accurate test results. The design basis for l
main steam safety valves (overpressure protection) was maintained throughout this event. Therefore, this event did not result in an increased risk to the health and safety of the public or plant personnel.
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0l1l8 - 0j0 0l2 or 0 j6 vom . = mic w.mmim On September 21, 1989. Waterford Steam Electric Station Unit 3 was operating ,
't at 100% power when Main Steam Safety Valve (MSSV) (Ells identifier - RV) testing was being conducted in accordance with mechanical maintenance (MM) proc'edure MN-07-015. "Trevitest of Main Steam Safoty Valves." This procedure involves a minimum of 3 lift tests per safety valve Test #1 - To verify the valve vill open and close properly; Test #2 - To measure valve operating ;
pressure; and Test #3 - To verify test #2 results.
At approximately 1239, maintenance personnel completed Test #1 on valve MS-106A with the valve opening and reseating satisfactorily. Test #2 was then performed I
at 1241. Both of these tests indicated a lift pressure of 1030 psig which is below minimum acceptable (setpoint: 1070 psig i 1%). Several aberrations in l the performance of the in-use Trevitest Heise gauge caused the Mechanical l- Maintenance Supervisor (MMS) and the Operations Shift Supervisor (SS) to question.the test results and invalidate the surveillance test. These [
aberrations included: The Heise gauge indication (Main Steam pressure) changed ;
10 psi vhen the gage was re-oriented from a horizontal to a vertical configuration (90 degree rotation); when depressurized and vented. the gauge indicated less than zero gauge pressure (-10 psig); the valve lif t pressure for the horizontal gauge configuration appeared inordinately low based on the ,
1 previous experience of the MMS. The Heise gauge was delivered to the site L. Metrology Lab for a calibration check. The safety valve was not declared inoperable by the SS at this time because of the questionable p u formance of the gauge.
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[ At approximately 1450, an NRC resident inspector raised the question of
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operability for valve MS-106A with the Trevitest unit still connected to the ,
valve. The SS decided to remove the test unit from MS-106A until he could provide the inspector with a response. At 1535, the inspector questioned the SS on his intentions for dealing with the lov lif t pressure ou test #2 for j MS-106A. The SS informed the inspector that the calibration of the gauge was being verified. The inspector responded by informing the SS that he had just i left the Main Steam Valve area and was told by the HMS that the gauge calibration checked satisfactorily. The SS and Operations Superintendent -
l Nuclear conferred on the issue and deelded to proceed with testing as soon as possible. At approximately 1540, the MMS was contacted to have the Trevitest unit (including the Heise gauge) reinstalled and proceed with testing on MS-106A. j At 1605, the SS was informed : hat testing was ready to commence however, !
approximately 30 minutes later, the SS was notified that the chart recorder [
being used on the Trevitest unit was not operating correctly (the printing arm was skipping on the paper) and would have to be checked.
In conjunction with the continuing plant maintenance activities to resolve the
. problems with MS-106A, plant management became involved via telephone f conference calls with NRC Region IV personnel and the NRC resident inspector.
The Plant Manager and the Chief of Project Section A of Region IV conversed at j approximately 1700. During this conversation, it was discussed whether or not Waterford 3 should commence reducing power to comply with TS 3.7.1.1 (four hour action requirement). The response was not however, Waterford 3 should pursue an enforcement discretion evaluation and inform the NRC of the results within several hours. With this guidance, plant personnel developed an evaluation for presentation to Region IV.
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0 l0 0l4 0F 0 l6 I rart -. = w a =ac wamm nn In a follovup telephone conference at approximately 2000. Waterford 3 management recommended enforcement discretion until the surveillance could be performed. ,
This recommendation was based on an engineering evaluation of current valve status. If the valve did not meet the acceptance criteria when retested TS
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3.7.1.1.a action requirement vould be entered. The NRC initially discussed granting enforcement discretion until the next scheduled plant shutdown :
(approximately 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> away). The NRC requested a chort recess so that Region IV personnel could review the engineering evaluation as well as the scope of the request.
During this period of deliberation, af ter repairing, calibrating, and installing ,
the chart recorder, testing of MS-106A recommenced at 2037. Test #2 (record [
test) was performed with a lift pressure of 1038 peig. MS-106A was declared ,
inoperable and TS 3.7.1.1.a entered.
In a final telephone conversation, Region IV was prepared to grant enforcement I discretion as requested by plant management. However, the valve had already failed the surveillance retest and TS 3.7.1.1.a action requirement had been entered. After the valvo lift setpoint was adjusted, the valve was tested i satisfactorily at 1080 psig (Final Test for Record) and 1072 psig (Final Test for Verification), and was declared operable. TS 3.7.1.1.a was exited at 2100.
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- The root cause of this event was an error in judgement b
- plant staff supervisors. When the questionable test results were first identified, the indeterminate status should have been discussed with higher levels of plant management. As a minimum, the safety valve should have been declared inoperable when the calibration check indicated that the gauge was in calibration; i.e.,
enough information was available to support valve inoperability as a good conservative decision. Enforcement discretion should have been pursued in parallel with these actions within the TS time constraints (four hour action requirement). The design basis for the valve (overpressure protection, which the valve was still capable of providing) and the uncertaiuty of the test equipment are believed to have significantly influenced the decision by the SS for the valve to remain operable. Contributing to this event was some procedure inadequacies, mostly in the areas of human factors, and-specific guidance on how to install the test gauge. The procedure was also nine months past its biennial review date and was written in a format that deviated from that of other Waterford 3 surveillance tests.
To prevent recurrence of this event, this report will be provided to all senior reactor operator license holders at Waterford 3 and will be specifically discussed by the Operations Superintendent - Nuclear with each SS. The above actions should be completed by November 7, 1989. This information has been promulgated in meetings held with maintenance personnel to discuss this event.
Additionally, procedure MM-07-015 is being revised to include: test equipment set-up criteria which will maintain valve operability while testing; notifying the SS on indeterminate conditions found during testing; recording as-f ound test data; and specifying complete calibration requirements for test equipment.
This revision should be completed by March 30, 1990. Additional guidance will be provided by plant management on how to handle test instrumentation malfunctions or indcterminance. A review of other surveillance procedures will be conducted to identify and resolve similar procedure problems. This review and the associated revision of any identified procedures will be completed by March 30, 1990, or before the procedure is used.
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,c . . 4 UCENSEE EVENT REPORT ILER) TEXT CONTINUATION
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Electric Station Unit 3
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0l0 0l6 0F 0 l6 wc w an wim j Preliminary reviews of the Final Safety Analysis. ASME Section 111 article NC7000, and the TS bases indicate that the -l% lift setpoint limit is a standard ASME tolerance value and does not correlate to valve operability as defined in the TS bases. Following further evaluation, a TS change may be initiated to request relief from the lov side limit setpoint or establish a larger allowable variance consistent with industry experience and good engineering practices.
Although this event has identified areas which require improvements, there was a good faith effort by all involved personnel to satisfy TS requirements by completing the testing promptly while inouring accurate test resultr. The design basis for main steam safety valves (overpressure protection) was maintained throughout this event. Therefore, this event did not result in an increased risk to the health and safety of the public or plant personnel.
gMILAR EVDITS None PLANT CONTACT l D.F. Packer, Assistant Plant Manager - Operations & Maintenance. 504/464-3134.
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