LER 89-002-01:on 890125,discovered That Safety Classification of Instrument Air Tubing That Supplies Outlet Isolation Valves Installed as non-nuclear Safety.Caused by Use of Weld Filler Matl.Tech Spec Change SentML19327C111 |
Person / Time |
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Site: |
Waterford |
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Issue date: |
11/13/1989 |
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From: |
Brennan T LOUISIANA POWER & LIGHT CO. |
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To: |
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Shared Package |
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ML19327C110 |
List: |
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References |
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LER-89-002, LER-89-2, NUDOCS 8911200003 |
Download: ML19327C111 (6) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2481994-10-0707 October 1994 LER 94-012-00:on 940907,discovered Failure to Perform TS Surveillance Requirements.Caused by Misunderstanding & Inadequate Technical Reviews.Ts Bases for 3/4.8.1 Will Be revised.W/941007 Ltr ML20029D9941994-05-11011 May 1994 LER 94-006-00:on 940415,determined That on 921103, Unidentified RCS Leak Rate of Greater than 1 Gpm Occurred. Caused by Error in RCS Mass Balance Equation.Approved Temporary Change to Procedure OP-903-024.W/940511 Ltr ML20045H4731993-07-15015 July 1993 LER 93-002-00:on 930615,reactor Tripped Due to High SG Level Caused by Failure of Feedwater Control Sys.Caused by Failure of Square Root Extractor in Feedwater Flow Circuit.Failed Components Replaced & Alarm Setpoints reviewed.W/930715 Ltr ML20042F7501990-05-0707 May 1990 LER 90-004-00:on 900408,partial Actuation of Emergency Feedwater Sys Occurred During Scheduled Test of Plant Protection Sys.Caused by Test Circuit Malfunction.Relay Hold Pushbutton Assembly replaced.W/900507 Ltr ML19332C5781989-11-20020 November 1989 LER 89-020-00:on 891031,containment Fan Cooler C Motor Ran in Reverse Direction Reducing Air Flow & Cooling Capacity. Caused by Personnel Not Performing Surveillance Testing. Motor Rewired for Correct Slow Speed operation.W/891120 Ltr ML19324C4611989-11-13013 November 1989 LER 89-019-00:on 891012,4.16-kV Bus 3A2 Metering Potential Transformer Fuse Door Inadvertently Opened,Causing Feeder Breaker & Supply Breaker to Open & Load Sequencer to Reset. Caused by Personnel Error.Drawers relabeled.W/891113 Ltr ML19327C1111989-11-13013 November 1989 LER 89-002-01:on 890125,discovered That Safety Classification of Instrument Air Tubing That Supplies Outlet Isolation Valves Installed as non-nuclear Safety.Caused by Use of Weld Filler Matl.Tech Spec Change Sent ML19327B3511989-10-23023 October 1989 LER 89-018-00:on 890921,while Testing Main Steam Safety Valve,Lift Pressure Found to Be Below Tech Spec Allowable Value.Caused by Error in Judgement by Plant Supervisors. Event Will Be Discussed by superintendent.W/891023 Ltr 1994-05-11
[Table view] Category:RO)
MONTHYEARML20024J2481994-10-0707 October 1994 LER 94-012-00:on 940907,discovered Failure to Perform TS Surveillance Requirements.Caused by Misunderstanding & Inadequate Technical Reviews.Ts Bases for 3/4.8.1 Will Be revised.W/941007 Ltr ML20029D9941994-05-11011 May 1994 LER 94-006-00:on 940415,determined That on 921103, Unidentified RCS Leak Rate of Greater than 1 Gpm Occurred. Caused by Error in RCS Mass Balance Equation.Approved Temporary Change to Procedure OP-903-024.W/940511 Ltr ML20045H4731993-07-15015 July 1993 LER 93-002-00:on 930615,reactor Tripped Due to High SG Level Caused by Failure of Feedwater Control Sys.Caused by Failure of Square Root Extractor in Feedwater Flow Circuit.Failed Components Replaced & Alarm Setpoints reviewed.W/930715 Ltr ML20042F7501990-05-0707 May 1990 LER 90-004-00:on 900408,partial Actuation of Emergency Feedwater Sys Occurred During Scheduled Test of Plant Protection Sys.Caused by Test Circuit Malfunction.Relay Hold Pushbutton Assembly replaced.W/900507 Ltr ML19332C5781989-11-20020 November 1989 LER 89-020-00:on 891031,containment Fan Cooler C Motor Ran in Reverse Direction Reducing Air Flow & Cooling Capacity. Caused by Personnel Not Performing Surveillance Testing. Motor Rewired for Correct Slow Speed operation.W/891120 Ltr ML19324C4611989-11-13013 November 1989 LER 89-019-00:on 891012,4.16-kV Bus 3A2 Metering Potential Transformer Fuse Door Inadvertently Opened,Causing Feeder Breaker & Supply Breaker to Open & Load Sequencer to Reset. Caused by Personnel Error.Drawers relabeled.W/891113 Ltr ML19327C1111989-11-13013 November 1989 LER 89-002-01:on 890125,discovered That Safety Classification of Instrument Air Tubing That Supplies Outlet Isolation Valves Installed as non-nuclear Safety.Caused by Use of Weld Filler Matl.Tech Spec Change Sent ML19327B3511989-10-23023 October 1989 LER 89-018-00:on 890921,while Testing Main Steam Safety Valve,Lift Pressure Found to Be Below Tech Spec Allowable Value.Caused by Error in Judgement by Plant Supervisors. Event Will Be Discussed by superintendent.W/891023 Ltr 1994-05-11
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F2891999-10-13013 October 1999 Drill 99-08 Emergency Preparedness Exercise on 991013 05000382/LER-1999-014, :on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B1999-10-12012 October 1999
- on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B
ML20217G7211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Waterford 3 Ses. with 05000382/LER-1999-013, :on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included1999-09-23023 September 1999
- on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included
05000382/LER-1999-012-01, :on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With1999-09-13013 September 1999
- on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With
ML20211Q2141999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Waterord 3 Ses.With 05000382/LER-1999-011-01, :on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B1999-08-31031 August 1999
- on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B
05000382/LER-1999-010-01, :on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity1999-08-26026 August 1999
- on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity
05000382/LER-1999-009-01, :on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established1999-08-26026 August 1999
- on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established
ML20210Q6361999-07-31031 July 1999 Corrected Monthly Operating Rept for July 1999 for Waterford 3 ML20210S0581999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Waterford 3.With 05000382/LER-1999-008-01, :on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-021999-07-29029 July 1999
- on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-02
05000382/LER-1999-007-01, :on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff1999-07-23023 July 1999
- on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff
ML20210D8951999-07-23023 July 1999 Safety Evaluation Accepting First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 - ISI-020 05000382/LER-1999-006-01, :on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With1999-07-14014 July 1999
- on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With
ML20209H3781999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Waterford 3 Ses. with 05000382/LER-1999-005-01, :on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested1999-06-24024 June 1999
- on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested
ML20195J8951999-06-17017 June 1999 Safety Evaluation Granting Relief for Listed ISI Parts for Current Interval,Per 10CFR50.55a(g)(5)(iii) ML20195J9741999-06-16016 June 1999 Safety Evaluation Supporting Amend 152 to License NPF-38 ML20207E8631999-06-0303 June 1999 Safety Evaluation Accepting Licensee 990114 Submittal of one-time Request for Relief from ASME B&PV Code IST Requirements for Pressure Safety Valves at Plant,Unit 3 ML20195D5491999-06-0303 June 1999 Safety Evaluation Supporting Amend 151 to License NPF-38 ML20195K3391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Waterford 3 Ses.With ML20195C3041999-05-28028 May 1999 Annual Rept on ABB CE ECCS Performance Evaluation Models 05000382/LER-1999-004-02, :on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing1999-05-14014 May 1999
- on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing
ML20206S7401999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Waterford 3.With ML20205T2621999-04-22022 April 1999 LER 99-S02-00:on 990216,contract Employee Inappropriately Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Security Personnel Performed Review of Work & Work Area That Individual Was Involved with ML20206A9641999-04-21021 April 1999 Safety Evaluation Supporting Amend 150 to License NPF-38 05000382/LER-1999-003-02, :on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With1999-04-0909 April 1999
- on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With
ML20205N9671999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Waterford 3 Ses.With ML20205E8531999-03-30030 March 1999 Corrected Pages COLR 3/4 1-4 & COLR 3/4 2-6 to Rev 1, Cycle 10, Colr ML20205A6331999-03-25025 March 1999 SER Accepting Request to Use Mechanical Nozzle Seal Assemblies as an Alternative Repair Method,Per 10CFR50.55a(a)(3)(i) for Reactor Coolant Sys Applications at Plant,Unit 3 05000382/LER-1999-002-03, :on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired1999-03-25025 March 1999
- on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired
ML20204H1401999-03-23023 March 1999 Rev 1 to Engineering Rept C-NOME-ER-0120, Design Evaluation of Various Applications at Waterford Unit 3 ML20204H1231999-03-22022 March 1999 Rev 1 to Design Rept C-PENG-DR-006, Addendum to Cenc Rept 1444 Analytical Rept for Waterford Unit 3 Piping ML20204H2451999-03-22022 March 1999 Rev 2 to C-NOME-SP-0067, Design Specification for Mechanical Nozzle Seal Assembly (Mnsa) Waterford Unit 3 ML20204F0791999-03-17017 March 1999 Rev 1 to Waterford 3 COLR for Cycle 10 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207F3491999-03-0505 March 1999 LER 99-S01-00:on 990203,contraband Was Discovered in Plant Protected Area.Bottle Was Determined to Have Been There Since Original Plant Construction.Bottle Was Removed & Security Personnel Performed Search of Area.With ML20204B5141999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Waterford 3.With ML20203H8151999-02-17017 February 1999 Safety Evaluation Supporting Amend 149 to License NPF-38 ML20203H8591999-02-17017 February 1999 Safety Evaluation Accepting Licensee Second Ten Year ISI Program & Associated Relief Requests for Plant,Unit 3 05000382/LER-1999-001, :on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With1999-02-0404 February 1999
- on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With
ML20202H9161999-02-0202 February 1999 Safety Evaluation Supporting Amend 148 to License NPF-38 ML20199H6261999-01-21021 January 1999 Safety Evaluation Accepting Classification of Instrument Air Tubing & Components for Safety Related Valve Top Works.Staff Recommends That EOI Revise Licensing Basis to Permit Incorporation of Change 05000382/LER-1998-020, :on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With1998-12-31031 December 1998
- on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With
ML20199C9101998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Waterford 3.With ML20198F4691998-12-21021 December 1998 Safety Evaluation Supporting Amend 147 to License NPF-38 ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20206N4131998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Waterford 3.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program 1999-09-30
[Table view] |
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L . 1 seRC Po,sm 386 U S. NUCLE AJ4 R$1UL ATORY COMMIT $lON 53 s.PP20VE3 OMD NO 31660104 i
. LICENSEE EVENT REPORT (LER) '"a'8"
F Acittiv NAME til DOCKET NUMSEM (26 FAGE G i Waterford Steam Electric Station Unit 3 015 l 0 !a l 0 l 310 l2 1loFl0 l6 l TITLt set Inadequate Qualification of Instrument Air Tubing During Initial Construction l 6vaNT OATS isi tar NuMmER isi RiPORT oATsin OTHR rACiuf.as Nv0Lvio toi MONTH DAY YEAR Yt Aft $ M '4 , fff,$ e0 NTH DAY v t Arq # % ALIT v h AMes DOCEf f NVM6tRt$n N/A 0l6l0l0l0l l l 4
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- TH18 REPORT 88 SUDMITTED PUR$UANT TO THE REOUIREMENTS OF 10 CPR { ICnece one or sne , or the terapw.ng7 till OPE R Af tNG MODE 191 6 20 402tbl to 406tel 50.73ee H2lt.el T3.71106 tR 20 406teH1H4 50 391sHil 50 73teHf. Hut 73.71tel 1101 l l 20 406teH1 Heal 60.38(eH2) 60.736ed2iftel HE $pec se Abst et, 20 406ieH1 Held 50.73teH2Hil 60.7SeeH2Hn4HA) Je6A>
20 406tsHIHevi X 50,73m H2Hiil to 4eH2HetesHel 20 4061elt1Het 60.73te H2Hetil F0 73tel(2Hal LICENSEE CONTACT FOR THIS LER (121 N1ME TE LEPHONE NUMBER ARE A COQ 4 T.P. Brennan, Design Engineering Manager 5 l0 14 4 I 614 l- l 313 l 0l0
- r. COMPLITI' ONE LINE FOR E ACH COMPONENT F AILURE OfECRIBED IN THl3 REPORT 413)
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I I I I ! I I I I I I I I I SUPPLEMENT AL REPORT E XPECTED 1141 MONTH DAY YEAR SUBM r $$ SON Y $ 5 (19,ee. resorete 1MPfCTfD $U0 MISSION DA ff! NC l l l A. T R ACT u -, ,, m0 ue. , e . e ,...,-e-, ,, nee,. .ye .,ue r,,e.mm.o., n .>
At 1954 hours0.0226 days <br />0.543 hours <br />0.00323 weeks <br />7.43497e-4 months <br /> on January 25, 1989, Vaterford Steam Electric Station Unit 3 was operating at 82% power when Design Engineering (DE) personnel discovered a discrepancy with the safety classification of Instrument Air (IA) tubing that supplies the actuators of Safety Injection Sump Outlet Isolation Valves SI-602A&B. Tubing supports were installed seismically qualified, but the tubing as shown in design documents was installed na non-nuclear safety (NNS) during initial construction. Because SI 602A'.' v. ~ squired to open after a LOCA coincident with a Safe Shutdown Earthy nE), this event is reportable as a condition outside the planc's design bat The root cause of this event was the insufficient documentation of code interpretations during initial construction. An investigation revealed that safety class tubing and weld filler material were used. The tubing welds passed penetrant tests, and records were reviewed to ensure the welders were qualified to perform safety related welding. The tubing is considered to be classified as safety class 3 and would perform its design function. Thus, this event did not threaten the health or safety of the public or plant personnel.
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At 1954 hours0.0226 days <br />0.543 hours <br />0.00323 weeks <br />7.43497e-4 months <br /> on January 25, 1989, Waterford Steam Electric Station Unit 3 was operating at 82% power when Design Engineering (DE) personnel discovered a discrepancy with the safety classification of instrument air (EIIS Identifier LD) tubing that supplies the actuators of Safety Injection (SI) Valves SI 602A&B (EIIS Identifier BF-V). The discrepancy was documented in nonconformance condition identification (NCI) 261147. The tubing in question runs from the volume tank (EIIS Identifier LD-TK) to the valve actuator. The tubing was installed as non-nuclear safety (NNS); however, tubing supports and tube I tracks were installed as seismic category one. NNS tubing is not considered to be cperable following a seismic event, but seismic supports and tube tracks would prevent it from damaging other safety-related equipment.
l S1 602A&B are the SI Sump Outlet Isolation Valves. The valves are closed during normal operation and open upon receipt of a Recirculation Actuation Signal (RAS). The RAS is generated upon receipt of two out of four Refueling Water l Sturage Pool (RWSP) (EIIS Identifier BP-TK) lov level alarms with a Safety 1
Injectica Actuation Signal (SIAS) present. This causes the valves to open when RWSP level lovers to 10%. The purpose of the RAS is to n.aintain adequate suction to the Containment Spray Pumps (EIIS Identifier BE-P) and the High Pressure Safety Injection (HPSI) Pumps (EIIS Identifier BQ-P) during a Loss of l Coolant Accident (LOCA),
General Design Criterion 2 as stated in Final Safety Analysis Report (FSAR) section 3.1.2 requires components that are vital to the mitigation and control j of accident conditiens be designed to withstand the effects of a LOCA coincident with the effects of a Safe Shutdown Earthquake (SSE). Because automatic operation of SI 602A&B requires that instrument air be available to the valve
- actuator, the instrument air tubing should be classified as safety class 3.
Credit is not taken for manual operation of these valves because radiation levels in their vicinity during the design large break LOCA would be too high to allow normal access to the valves. Der,ign and installation drawings show l
that this tubing was installed as NNS, so thin event is reportable as a j condition outside the design basis of the plant. The condition has existed l since issuance of the operating license on December 18, 1984.
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Waterford Steam via. ** gggu gyy,y; Electric Station Unit 3 0 l5 l0 l0 [0 l3 l8l 2 8[9 --
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0 l1 0l3 or 0 l6 itXT F more apeso e reembed ame eas,nonsi NAC pome Jm4W (171 The root cause of this event was insufficient documentation of code interpretations by the Architect Engineer (AE) during initial construction.
ANSI N18.2 Section 2.3.1.3 states that the portions of compressed gas systems required to support control or operation of safety systems should be qualified safety class 3. However, the rules of ASME Section III are not intended to be applicable to valve operators, controllers, and position indicators under Article NA-1130, 1971 edition through 1973 addenda, because the valve topworks are not considered part of the pressure retaining boundary. The AE interpreted Article NA-1130 to include instrument air tubing connected to the
( valve. Thus, design and installation drawings show the tubing was installed l
as NNS, seismically supported. Based on information from the AE, the installation
! of the tubing per ANSI B31.1, seismically supported, is aleguate to assure the l
tubing would perform its design function and meet safety class 3 requirements.
l l
l Actions were also taken to confirm that the subject tubing classification meets safety class 3 requirements. On January 26, 1989, maintenance rcretanel performed l a walkdown of the tubing and welds. Construction documentation associated with the tubing was reviewed. Letter LW3-386-82 from Ebasco Services, Inc. , to Louisiana Power and Light (LP&L), dated March 17, 1982, revealed that ANSI B31.1 instrument tubing and fittings used at Waterford 3 were drawn from the same qualified stock as those used for ASME Section III installation. During construction, welding electrodes and filler material were procured in accordance with ASME Section III as code class material. The walkdown of the tubing identified tubing heat numbers and welder identification numbers. The tubing heat numbers corresponded to ASME Section III Code Class 2. The welder identification numbers were checked to verify that the welders were qualified to weld code class tubing. Welders are qualified to ASME Section 'IX for both ANSI B31.1 welding and ASME Section III welding. The welds satisfactorily passed dye penetrant tests. Thus, this tubing classification is considered to be classified as safety class 3. und the tubing would perform its design !
function.
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Waterford Steam viaa "g =,','. agf,W i Electric Station Unit 3 0 l5 lo j o l0 l 3l8 l2 8l 9 -
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TEXT M more apece m sovido4 ese saWooast NRC Form JEE4 W 1171 DE personnel reviewed Instrument Installation Detailed Drawing, LOU-1564-B430, to identify any valves with similar problems. The review identified ant additional 24 valves that have volume tanks to supply instrument air to the valve actuators in the event of a loss of instrument air. . Additionally, a review of the safety related portion of the nitrogen system (EIIS Identifier LK) that provides a backup to instrument air identified 34 safety related valves with nitrogen accumulators (EIIS Identifier LK-ACC). Nitrogen accumulators are used in some safety related applications as a backup to the instrument air system. ACME Section III class 3 tubing was installed from these nitrogen accumulators to the last isolation valve prior to connecting to the instrument air tubing assoc.iated with the valve topworks. At this point a class break was established from the nitrogen tubing to the instrument air tubing. That portion of the instrument air tubing from the class break to the valve topworks was installed per ANSI B31.1, seismically supported.
A walkdown and review of the above 58 valves has determined that their associated instrument air tubing was installed per the same standards as that of SI 602 A&B. The component walkdowns, documentation reviews, engineering analysia (performed by Gilbert / Commonwealth, Inc.), and safety assessment have established ANSI B31.1, Seismic Category 1, as the design criteria for pneumatic valve topworks for safety related valves at Waterford 3. DE personnel will revise design drawings to show this tubing to be safety class 3. This action is expected to be complete by September 30, 1990. The component walkdowns identified several other valve topworks related deficiencies which are summarized below:
l Unqualified Check Valves In IA Tubing CC-641 CCW to RCPs header isolation valve CC-710 CCW to RCPs inside containment isolation valve CC-713 CCW to RCPs outside containment isolation valve l
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W2terford' Steam Electric Station Unit 3 0 l5 !0 l0 l0131812 81 9 dd2 -
01 1 Ol 5 OF gh TEXT M mese spece 4 reewed amo eaWesset 44C #erm JeSMs/ HM Galvanized " Tee" Connection in IA Tubing to Accumulator SI-106A,B Refueling Water Storage Pool header isolation valves i IA tube track not supported / missing CVR-101,201 Containment Vacuun Relief butterfly valves MS-116A Atmospheric Dump Valve IA Tubing Not Seismically Supported CC-710 CCW to RCPs inside containment isolation valve Questionable Seismic Oualification of Compotients in I A tubing CS-125A,B Containment Spray Header Isolation Valve (air regulator and needle valve)
CC-114A B CCW pump suction cross-connect header isolation valve (air filter) ,
CC-115A,B CCW pump suction cross-connect header isolation valve (air filter)
CC-126A,B CCW pump diecharge cross-connect header isolation valve (air filter)
CC-127A,B CCW pump discharge cross-connect header isolation valve (air filter)
CC-200A,B CCW supply isolation valve (non-nuclear safety train A,B) (air filter)
CC-563 CCW return isolation valve (non-nuclear safety train B) (air filter)
CC-727 CCW return header isolation valve (non-nuclear safety train A)
(air filter)
MS-116A,B Atmospheric dump valves (3-way ball valves, hose and volume boosters)
NOTE: CCW = Component Cooling Water System (EIIS Identifier - CC)
CVR = Containment Vacuum Relief System (EIIS Identifier - BF)
RCP = Reactor Coolant Pump (EIIS Identifier AB - P)
MS = Main Steam System (EIIS Identifier - SB)
CS = Containment Spray System (EIIS Identifier - BE)
These deficiencies will be resolved prior to entering the mode in which the
, i cluipment is required to be operable during the third refueling outage !
(September - November 1989).
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LICENSEE EVENT REPORT (LER) TEXT C3NTINUATION urnovto ous wo mo-om !
, , o exrints: was 9 AclLITV NAME Hi DOCKti NUMSta (2) ctM NVMSER IS) PAGE (31 Waterford Steam %~. n om .u .ai v .o .
- p. Electric Station Unit 3 o [6 l0 lo lo l 3l8 l2 8l9 0 l0l 2 0l1 0 l6 or 0 l6 TEXT L mwe assec 4 #seemost, use eswooW MC Form W W (17)
A review of past LERs revealed one similar event. On November 28, 1988, LER 88-026 was submitted describing the lack of seismic qualification for Boric Acid Makeup Tank (BAMT) level indicator (EIIS Identifier CB-TK-LI) tubing and supports. The tubing and supports were installed as non-seismic during construction. An evaluation conducted after the installation determined this was acceptable because a break in both tubing runs and subsequent loss of fluid would not affect plant shutdown capability. However, on January 8, 1987, a Technical Specification (TS) change was issued to lower the required boron concentration of the BAMTs. This TS change made the qualification of the BAMT level indicator tubing unsatisfactory.
The BAMT event is described in LER 88-026 and recounts an unidentified safety class break in instrument tubing. LER 89-002-01 addresses a seismic qualification issue, which is unrelated to the class interface discrepancy reported in LER 88-026.
The classification discrepancy for SI 602A&B tubing was discovered by DE -
personnel as a result of a Safety System Functional inspection (SSFI) initiated by Waterford 3 management. This report was issued due to the lack of qualification documentation f1r the tubing. However, the walkdown, dye penetrant testing, and document reviews fot SI 602A&B have confirmed that l this tubing can be classified as safety class 3 and would perform its design function. The other 58 valves' instrument air tubing was installed in l
accordance with the same standards as that of SI 602A&B instrument air l
l tubing. Thus, this event did not adversely affect the health or safety of the public or plant personnel.
SIMILAR EVENTS LER 88-026 i
l PLANT CONTACT ,
T.P. Brennan, Design Engineering Manager, 504/464-3300, l-
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