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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000382/LER-1999-014, :on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B1999-10-12012 October 1999
- on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B
05000382/LER-1999-013, :on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included1999-09-23023 September 1999
- on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included
05000382/LER-1999-012-01, :on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With1999-09-13013 September 1999
- on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With
05000382/LER-1999-011-01, :on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B1999-08-31031 August 1999
- on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B
05000382/LER-1999-009-01, :on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established1999-08-26026 August 1999
- on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established
05000382/LER-1999-010-01, :on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity1999-08-26026 August 1999
- on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity
05000382/LER-1999-008-01, :on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-021999-07-29029 July 1999
- on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-02
05000382/LER-1999-007-01, :on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff1999-07-23023 July 1999
- on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff
05000382/LER-1999-006-01, :on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With1999-07-14014 July 1999
- on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With
05000382/LER-1999-005-01, :on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested1999-06-24024 June 1999
- on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested
05000382/LER-1999-004-02, :on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing1999-05-14014 May 1999
- on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing
ML20205T2621999-04-22022 April 1999 LER 99-S02-00:on 990216,contract Employee Inappropriately Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Security Personnel Performed Review of Work & Work Area That Individual Was Involved with 05000382/LER-1999-003-02, :on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With1999-04-0909 April 1999
- on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With
05000382/LER-1999-002-03, :on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired1999-03-25025 March 1999
- on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired
ML20207F3491999-03-0505 March 1999 LER 99-S01-00:on 990203,contraband Was Discovered in Plant Protected Area.Bottle Was Determined to Have Been There Since Original Plant Construction.Bottle Was Removed & Security Personnel Performed Search of Area.With 05000382/LER-1999-001, :on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With1999-02-0404 February 1999
- on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With
05000382/LER-1998-020, :on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With1998-12-31031 December 1998
- on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With
05000382/LER-1998-016, :on 980730,failed to Meet TS Requirements for for RT Bypasses.Cause Not Determined Because of Age of condition.1E-4% Bistables for All for Channels of Excore Log Power Channels Were Declared Inoperable 9807301998-08-27027 August 1998
- on 980730,failed to Meet TS Requirements for for RT Bypasses.Cause Not Determined Because of Age of condition.1E-4% Bistables for All for Channels of Excore Log Power Channels Were Declared Inoperable 980730
ML20237B6831998-08-17017 August 1998 LER 98-S01-00:on 980723,discovered That Waterford 3 Physical Security Plan,Safeguards Document Was Not Under Positive Control of Authorized Person at All Times.Caused by Human Error/Inappropriate Action.Counseled Employee Involved 05000382/LER-1998-013, :on 980701,IST Valve Surveillances Were Missed. Caused by Inadequate Processing of Info Transferred Between Operations Procedure Group & Programs Engineering.Procedure Revised1998-07-30030 July 1998
- on 980701,IST Valve Surveillances Were Missed. Caused by Inadequate Processing of Info Transferred Between Operations Procedure Group & Programs Engineering.Procedure Revised
05000382/LER-1998-012, :on 980609,TS Channel Check for TS Surveillance 4.3.1.1 Was Missed.Caused by Human Error.Involved Employees Were Counseled & All Licensed Operators Were Apprised of Event1998-07-0909 July 1998
- on 980609,TS Channel Check for TS Surveillance 4.3.1.1 Was Missed.Caused by Human Error.Involved Employees Were Counseled & All Licensed Operators Were Apprised of Event
05000382/LER-1998-011, :on 980603,TS 3.0.3 Entry Was Noted.Caused by Component Cooling Water Makeup Check Valve Failing Ist. Operability of a Train of CCW Was Restored Immediately & Check Valve Internals Were Replaced1998-07-0202 July 1998
- on 980603,TS 3.0.3 Entry Was Noted.Caused by Component Cooling Water Makeup Check Valve Failing Ist. Operability of a Train of CCW Was Restored Immediately & Check Valve Internals Were Replaced
05000382/LER-1998-007, :on 980317,discovered That No Allowance for Instrument Loop Uncertainity Included in Surveillance for Chilled Water Outlet Temp.Caused by Failure to Consider Instrument Loop Uncertainty.Revised Task1998-04-16016 April 1998
- on 980317,discovered That No Allowance for Instrument Loop Uncertainity Included in Surveillance for Chilled Water Outlet Temp.Caused by Failure to Consider Instrument Loop Uncertainty.Revised Task
05000382/LER-1998-006, :on 980306,increased Differential Pressure for Feedwater Isolation Valves Occurred.Caused by Failure to Consider All Pressure Source Affecting Mfivs.Admin Controls Have Been Enacted Requiring Entry Into TS 3.6.31998-04-13013 April 1998
- on 980306,increased Differential Pressure for Feedwater Isolation Valves Occurred.Caused by Failure to Consider All Pressure Source Affecting Mfivs.Admin Controls Have Been Enacted Requiring Entry Into TS 3.6.3
05000382/LER-1998-005, :on 980312,missed Thermal Overload TS Surveillance Were Noted.Caused by Inadequate Review of 1992 Rev to TS 3.8.4.2 IAW GL 91-08.Thermal Overloads for 8 MOVs Were Subsequently Tested & Determined to Be Operable1998-04-13013 April 1998
- on 980312,missed Thermal Overload TS Surveillance Were Noted.Caused by Inadequate Review of 1992 Rev to TS 3.8.4.2 IAW GL 91-08.Thermal Overloads for 8 MOVs Were Subsequently Tested & Determined to Be Operable
05000382/LER-1998-004, :on 980304,TS 4.0.3 Condition - CPC Channel Functional Test,Was Concluded from Preliminary CEOG Rept. Caused by Human Error.Cpc Channels A,B & C Were Satisfactorily Tested1998-04-0303 April 1998
- on 980304,TS 4.0.3 Condition - CPC Channel Functional Test,Was Concluded from Preliminary CEOG Rept. Caused by Human Error.Cpc Channels A,B & C Were Satisfactorily Tested
05000382/LER-1998-003, :on 980302,inoperable Hydrogen Analyzers Were Noted Due to Undersized Thermal Overloads.Engineering Personnel Conducted all-hands Meetings to Discuss Management Expectations for Verifying Critical Design Inputs1998-04-0101 April 1998
- on 980302,inoperable Hydrogen Analyzers Were Noted Due to Undersized Thermal Overloads.Engineering Personnel Conducted all-hands Meetings to Discuss Management Expectations for Verifying Critical Design Inputs
05000382/LER-1998-002, :on 980215,brief Loss of Command Function in CR Occurred.Caused by Inappropriate Action (Human Error) on Part of Shift Superintendent.Ss Was Counseled IAW Corporate Discipline Policy1998-03-18018 March 1998
- on 980215,brief Loss of Command Function in CR Occurred.Caused by Inappropriate Action (Human Error) on Part of Shift Superintendent.Ss Was Counseled IAW Corporate Discipline Policy
05000382/LER-1998-001-01, :on 980214,TSs 3.0.3 Condition Occurred Due to Inoperable Charging Pumps.Replaced Failed SX-1 Relay1998-03-16016 March 1998
- on 980214,TSs 3.0.3 Condition Occurred Due to Inoperable Charging Pumps.Replaced Failed SX-1 Relay
ML20198K3921998-01-12012 January 1998 LER 97-S05-00:on 971210,emergency Vehicles Entered Into Protected Area W/O Proper Security Search.Caused by Misinterpretation of Security Procedure Requirement.Security Personnel Searched Areas Where Drill Occurred 05000382/LER-1997-033, :on 971205,change in HPSI Flow Measurement Exceeded 10CFR50.46 Acceptance Criteria.Caused by Inadequate Procedures.Sbloca ECCS Performance Analysis Was Performed Using S2M Evaluation Model1998-01-0505 January 1998
- on 971205,change in HPSI Flow Measurement Exceeded 10CFR50.46 Acceptance Criteria.Caused by Inadequate Procedures.Sbloca ECCS Performance Analysis Was Performed Using S2M Evaluation Model
05000382/LER-1997-030, :on 971114,noncompliance W/Ts 3.6.3 Was Noted. Caused by Design Error Associated W/Cars Containment Isolation Valves.Valve CAR-201B Was Declared Inoperable1997-12-15015 December 1997
- on 971114,noncompliance W/Ts 3.6.3 Was Noted. Caused by Design Error Associated W/Cars Containment Isolation Valves.Valve CAR-201B Was Declared Inoperable
05000382/LER-1997-027, :on 971110,discovered That Controller for Valve ACC-126A Was Inadvertently Left in Manual Position.Caused by Personnel Error.Operations Manager Conducted Event Debriefing,Performed Walkdown & Revised Procedure1997-12-10010 December 1997
- on 971110,discovered That Controller for Valve ACC-126A Was Inadvertently Left in Manual Position.Caused by Personnel Error.Operations Manager Conducted Event Debriefing,Performed Walkdown & Revised Procedure
05000382/LER-1997-026, :on 971105,single Failure Effects Condensate Storage Pool Inventory Occurred.Caused by Design Deficiency. Procedure Change Initiated1997-12-0505 December 1997
- on 971105,single Failure Effects Condensate Storage Pool Inventory Occurred.Caused by Design Deficiency. Procedure Change Initiated
05000382/LER-1997-025, :on 971017,gag for Valve CC-835B Was Partially Engaged Restricting Valve to Approx 80% Open.Caused by Inadequate Work Instructions.Gag Was Completely Disengaged on Valve CC-835B1997-11-17017 November 1997
- on 971017,gag for Valve CC-835B Was Partially Engaged Restricting Valve to Approx 80% Open.Caused by Inadequate Work Instructions.Gag Was Completely Disengaged on Valve CC-835B
05000382/LER-1996-015, :on 961024,failure to Isolate Containment Penetration 20 Occurred.Caused by Failure of CR Staff Discussing Clearance to Identify,Containment Isolation Would Not Be Adequate If Hung as-is.Expectations Reinforced1997-10-20020 October 1997
- on 961024,failure to Isolate Containment Penetration 20 Occurred.Caused by Failure of CR Staff Discussing Clearance to Identify,Containment Isolation Would Not Be Adequate If Hung as-is.Expectations Reinforced
05000382/LER-1997-016, :on 970515,potential for Inadvertent Recirculation & EFASs Allowed by Ts,Existed.Caused by Deficiency in Ts.Ts Change Request Will Be Revised & Resubmitted for EFAS1997-10-16016 October 1997
- on 970515,potential for Inadvertent Recirculation & EFASs Allowed by Ts,Existed.Caused by Deficiency in Ts.Ts Change Request Will Be Revised & Resubmitted for EFAS
05000382/LER-1997-024, :on 970528,emergency Diesel Generator Autostart Occurred Due to start-up Transformer Failure.Implemented Procedures OP-901-311,OP-901-511 & OP-901-5131997-08-19019 August 1997
- on 970528,emergency Diesel Generator Autostart Occurred Due to start-up Transformer Failure.Implemented Procedures OP-901-311,OP-901-511 & OP-901-513
05000382/LER-1997-023, :on 970708,EDG Fuel Sys Surveillance Was Missed Due to Failure of Personnel to Determine Intended Start & End Dates for SR 4.8.1.1.2.h.2 Interval.Submitted Application for Emergency Amend for Removal of SR1997-08-0707 August 1997
- on 970708,EDG Fuel Sys Surveillance Was Missed Due to Failure of Personnel to Determine Intended Start & End Dates for SR 4.8.1.1.2.h.2 Interval.Submitted Application for Emergency Amend for Removal of SR
ML20151L6561997-08-0404 August 1997 LER 97-S03-00:on 970704,discovered Undetected Entry Into Plant Vital Area.Caused by Inadequate Communication Re Proper Hpt Encl Controls When Normal Steam Flow Was Absent. Developed Security Directive to Address Configurations 05000382/LER-1997-022, :on 970614,RWSP Boron Concentration Was Lower than Rcs,In Volation of TS 3.7.6.2b.Caused by Incorrect Assumptions by Operations Dept Staff & Mgt.Waterford 3 Will Submit TS Change for TS 3.7.6.2b1997-07-18018 July 1997
- on 970614,RWSP Boron Concentration Was Lower than Rcs,In Volation of TS 3.7.6.2b.Caused by Incorrect Assumptions by Operations Dept Staff & Mgt.Waterford 3 Will Submit TS Change for TS 3.7.6.2b
ML20149E2951997-07-16016 July 1997 LER 97-S02-00:on 970616,determined That Two Individuals Inappropriately Entered Vital Area.Caused by Faulty Security Keycard Reader.Repaired Security Keycard & Search Vital Area Entered 05000382/LER-1997-018, :on 970428,voluntary LER for Dropped New Fuel Assembly Was Issued.Caused by Human Error.Sfhm Grappling Tool Was Inspected for Damage or Misalignment1997-06-27027 June 1997
- on 970428,voluntary LER for Dropped New Fuel Assembly Was Issued.Caused by Human Error.Sfhm Grappling Tool Was Inspected for Damage or Misalignment
05000382/LER-1997-019, :on 970529,non-compliance with TS 3.3.3.6 for Containment Isolation Valve Position Indication Was Noted. Caused by Misinterpretation of Requirements of RG 1.97. Revised Submittal to NRC1997-06-27027 June 1997
- on 970529,non-compliance with TS 3.3.3.6 for Containment Isolation Valve Position Indication Was Noted. Caused by Misinterpretation of Requirements of RG 1.97. Revised Submittal to NRC
05000382/LER-1997-017, :on 970515,control Room Emergency Filtration Unit Common Mode Failed.Caused by Inadequate Design.Both Crefu Trains Declared Inoperable & TS 3.7.6.2 Was Entered & Emergency Work Authorization,Initiated1997-06-19019 June 1997
- on 970515,control Room Emergency Filtration Unit Common Mode Failed.Caused by Inadequate Design.Both Crefu Trains Declared Inoperable & TS 3.7.6.2 Was Entered & Emergency Work Authorization,Initiated
05000382/LER-1997-016, :on 970515,potential for Inadvertent Recirculation Actuation Signal Allowed by TS Discovered. Caused by Deficiency in TS Since Original Issuance.Performed Review of Esfa Sys Instrumentation1997-06-16016 June 1997
- on 970515,potential for Inadvertent Recirculation Actuation Signal Allowed by TS Discovered. Caused by Deficiency in TS Since Original Issuance.Performed Review of Esfa Sys Instrumentation
05000382/LER-1997-012, :on 970404,programmatic Breakdown of Overtime Program Occurred.Caused by Lack of Mgt Oversight in Administering & Implementing Plants Working Hour Policy. Ltr Issued Reemphasizing Working Hour Policy1997-06-0404 June 1997
- on 970404,programmatic Breakdown of Overtime Program Occurred.Caused by Lack of Mgt Oversight in Administering & Implementing Plants Working Hour Policy. Ltr Issued Reemphasizing Working Hour Policy
ML20148D0271997-05-19019 May 1997 LER 97-S01-00:on 970418,improperly Authorized Individuals Were Granted Access to Plant Protected Area.Caused by Inadequate Work Process.Keycard Badges Were Inactivated for All Individuals Not Fully Employed 05000382/LER-1997-015, :on 970418,ultimate Heat Sink Did Not Incorporate Conservative Assumptions.Caused by Design Errors Associated W/Original Design of Ultimate Heat Sink. Operability Evaluation Completed on 9704041997-05-19019 May 1997
- on 970418,ultimate Heat Sink Did Not Incorporate Conservative Assumptions.Caused by Design Errors Associated W/Original Design of Ultimate Heat Sink. Operability Evaluation Completed on 970404
05000382/LER-1997-007, :on 970309,discovered Addl Refueling Water Storage Pool Instrument Uncertainty.Caused by Inadequate Design for Reference Leg of Level Transmitters.Recalibrated Rwsp Transmitters & Conducted Tests1997-05-16016 May 1997
- on 970309,discovered Addl Refueling Water Storage Pool Instrument Uncertainty.Caused by Inadequate Design for Reference Leg of Level Transmitters.Recalibrated Rwsp Transmitters & Conducted Tests
1999-09-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F2891999-10-13013 October 1999 Drill 99-08 Emergency Preparedness Exercise on 991013 05000382/LER-1999-014, :on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B1999-10-12012 October 1999
- on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B
ML20217G7211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Waterford 3 Ses. with 05000382/LER-1999-013, :on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included1999-09-23023 September 1999
- on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included
05000382/LER-1999-012-01, :on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With1999-09-13013 September 1999
- on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With
ML20211Q2141999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Waterord 3 Ses.With 05000382/LER-1999-011-01, :on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B1999-08-31031 August 1999
- on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B
05000382/LER-1999-010-01, :on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity1999-08-26026 August 1999
- on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity
05000382/LER-1999-009-01, :on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established1999-08-26026 August 1999
- on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established
ML20210Q6361999-07-31031 July 1999 Corrected Monthly Operating Rept for July 1999 for Waterford 3 ML20210S0581999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Waterford 3.With 05000382/LER-1999-008-01, :on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-021999-07-29029 July 1999
- on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-02
05000382/LER-1999-007-01, :on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff1999-07-23023 July 1999
- on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff
ML20210D8951999-07-23023 July 1999 Safety Evaluation Accepting First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 - ISI-020 05000382/LER-1999-006-01, :on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With1999-07-14014 July 1999
- on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With
ML20209H3781999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Waterford 3 Ses. with 05000382/LER-1999-005-01, :on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested1999-06-24024 June 1999
- on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested
ML20195J8951999-06-17017 June 1999 Safety Evaluation Granting Relief for Listed ISI Parts for Current Interval,Per 10CFR50.55a(g)(5)(iii) ML20195J9741999-06-16016 June 1999 Safety Evaluation Supporting Amend 152 to License NPF-38 ML20207E8631999-06-0303 June 1999 Safety Evaluation Accepting Licensee 990114 Submittal of one-time Request for Relief from ASME B&PV Code IST Requirements for Pressure Safety Valves at Plant,Unit 3 ML20195D5491999-06-0303 June 1999 Safety Evaluation Supporting Amend 151 to License NPF-38 ML20195K3391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Waterford 3 Ses.With ML20195C3041999-05-28028 May 1999 Annual Rept on ABB CE ECCS Performance Evaluation Models 05000382/LER-1999-004-02, :on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing1999-05-14014 May 1999
- on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing
ML20206S7401999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Waterford 3.With ML20205T2621999-04-22022 April 1999 LER 99-S02-00:on 990216,contract Employee Inappropriately Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Security Personnel Performed Review of Work & Work Area That Individual Was Involved with ML20206A9641999-04-21021 April 1999 Safety Evaluation Supporting Amend 150 to License NPF-38 05000382/LER-1999-003-02, :on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With1999-04-0909 April 1999
- on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With
ML20205N9671999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Waterford 3 Ses.With ML20205E8531999-03-30030 March 1999 Corrected Pages COLR 3/4 1-4 & COLR 3/4 2-6 to Rev 1, Cycle 10, Colr ML20205A6331999-03-25025 March 1999 SER Accepting Request to Use Mechanical Nozzle Seal Assemblies as an Alternative Repair Method,Per 10CFR50.55a(a)(3)(i) for Reactor Coolant Sys Applications at Plant,Unit 3 05000382/LER-1999-002-03, :on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired1999-03-25025 March 1999
- on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired
ML20204H1401999-03-23023 March 1999 Rev 1 to Engineering Rept C-NOME-ER-0120, Design Evaluation of Various Applications at Waterford Unit 3 ML20204H1231999-03-22022 March 1999 Rev 1 to Design Rept C-PENG-DR-006, Addendum to Cenc Rept 1444 Analytical Rept for Waterford Unit 3 Piping ML20204H2451999-03-22022 March 1999 Rev 2 to C-NOME-SP-0067, Design Specification for Mechanical Nozzle Seal Assembly (Mnsa) Waterford Unit 3 ML20204F0791999-03-17017 March 1999 Rev 1 to Waterford 3 COLR for Cycle 10 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207F3491999-03-0505 March 1999 LER 99-S01-00:on 990203,contraband Was Discovered in Plant Protected Area.Bottle Was Determined to Have Been There Since Original Plant Construction.Bottle Was Removed & Security Personnel Performed Search of Area.With ML20204B5141999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Waterford 3.With ML20203H8151999-02-17017 February 1999 Safety Evaluation Supporting Amend 149 to License NPF-38 ML20203H8591999-02-17017 February 1999 Safety Evaluation Accepting Licensee Second Ten Year ISI Program & Associated Relief Requests for Plant,Unit 3 05000382/LER-1999-001, :on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With1999-02-0404 February 1999
- on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With
ML20202H9161999-02-0202 February 1999 Safety Evaluation Supporting Amend 148 to License NPF-38 ML20199H6261999-01-21021 January 1999 Safety Evaluation Accepting Classification of Instrument Air Tubing & Components for Safety Related Valve Top Works.Staff Recommends That EOI Revise Licensing Basis to Permit Incorporation of Change 05000382/LER-1998-020, :on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With1998-12-31031 December 1998
- on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With
ML20199C9101998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Waterford 3.With ML20198F4691998-12-21021 December 1998 Safety Evaluation Supporting Amend 147 to License NPF-38 ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20206N4131998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Waterford 3.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program 1999-09-30
[Table view] |
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Operations
- - u ma le '. 6;3tPO D. F. Packer G.' r,.vce rA, mor nan, m..a ox G'.if e t f' WL13 W3F1-94-0058 A4.05 PR fiay 11, 1994 U.S. Nuc1 ear Regulatcry Commission Attn:
Document Control Desk Washington, D.C.
20555
Subject:
Waterford 3 SES Docket No. 50-382 License flo. f4PF-38 Reporting of Licensee Event Report Gentlemen:
Attached is Licensee Event Report fiumber LER-94-006-00 for Waterford Steam Electric Station Unit 3.
This Licensee Event Report is submitted in accordance with the requirements of 10CFR50.73(a)(2)(i)(B) and 10CFR50.36(c)(2).
Very truly you s, CM
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D.F. Packer General flanager Plant Operations DFP/RWP/ssf Attachment cc:
L.J. Callan, NRC Region IV G.L. florreich J.T. Wheelock - INPC Records Center R.B. McGehee N.S. Reynolds f1RC Resident Inspectors Office y
Administrator - LRPD
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ADSTRACT (Lim,t to 1400 spaces. t e, a;; proximate:y 15 mngle spaced typeetten kne?) (16)
On April 15, 1994, Waterford SES Unit 3 was shutdown for refueling in Mode 5 while conducting a compliance review check of previous Reactor Coolant System (RCS) leak rate calculations that were based on Attachment 10.4 of Revision 8 to Operating Procedure OP-903-024.
At this time it was determined that on Noverrber 3,1992, during the previous refueling outage (Refuel 5), that an unidentified RCS leak rate of >l GPM had occurred during Mode 5 before entering Mode 4, which constituted noncompliance with Technical Specification (TS) 3.0.4.
The root cause of this event was inadequate technical review of a change made to the RCS mass balance equation in Attachment 10.4 of Revision 8 to OP-903-024.
Immediate corrective action included a tetrporary approved change to Attachment 10.4, correcting the equation.
Action to prevent recurrence will be to have Operations personnel review this event.
The event did not compromise the health and safety of the public.
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00 um,.,,. w.....n.a. -..m-. m...., ec o+ um p n REPORTABLE OCCURRENCE On flovember 3,1992, during the previous refueling outage (Refuel 5), an unidentified RCS (EIIS Identifier AB) leak rate of 1.4424 GPM had occurred.
Due to incorrect calculational methods, the unidentified RCS leak rate at the time, during Refuel 5, was calculated to be <1 GPM; therefore, no action was taken to prevent from proceeding to Mode 4.
TS 3.0.4 states that entry into an operational mode shall not be made unless the conditions of the LCO are met without reliance on provisions contained in the action requirements.
Also, TS 3.4.5.2 states that RCS leakage shall be limited to 1 GPM unidentified leakage for Modes 1, 2, 3 and 4.
Therefore, upon entry into Mode 4, a condition prohibited by the plant's Technical Specifications had occurred; and, per 10CFR50.73(a)(2)(i)(B) and 10CFR50.36(c)(2) the event is reportable as an LER.
I INIT_IAL_COND1TIONS Plant Power 0%
Plant Operating Mode Mode 5 Procedures Being Performed Specific to this Event OP-903-024 1
Technical Specification LCO's in
'l Effect Specific to this Event 3.4.b.2 Major Equipment Out of Service l
Specific to this Event lione l
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LEQUE NT AL RE asioN NUMBER NUMBER i
Waterford Steam Electric Station 05000 382 03 OF 04 Unit 3 94
- - 006 00 i
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,6., o ww,m> v n EVENT SEQUENCE On April 11, 1994, during Refuel 6 while attempting to use Attachment 10.4 of OP-903-024 for an RCS leak rate calculation, it was realized that the i
results were ur, realistic for plant conditions that existel at the time.
On April 13, 1994, the results of an investigation revealed that the formula for the RCS mass balance equation (AGrcs), when T vg is <540*F, used in a
step 8.1.1.5 of Attachment 10.4 of OP-903-024 was in error.
The initial and final RCS inventories were reversed in the equation; i.e., the final I
inventory should have been subtracted from the initial inventory to obtain i
AG The investigation determined that this equation was revised by rcs.
Revision 8 to OP-903-024 on September 6, 1991.
The previous Revision 7 (dated February 13, 1990) equation was correct and the incorrect equation i
was introduced by Revision 8.
The investigation also recommended that a compliance review check be conducted of previous RCS leak rate calculations
{
that were based on Attachment 10.4 of Revision 8 to OP-903-024.
On April 15, 1994, at 1637 hours0.0189 days <br />0.455 hours <br />0.00271 weeks <br />6.228785e-4 months <br />, Waterford 3 was shutdown for refueling in Made 5 while conducting the recommended compliance review check when it was determined that on November 3, 1992, that an unidentified RCS leak rate of
>l GPM had occurred during Mode 5 before entering Mode 4.
CAUSAL _ FACTORS i
The root cause of this event was inadequate technical review of a change I
l made to the RCS mass balance equation in Attachment 10.4 of Revision 8 to
.l OP-903-024.
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FORWARD LICENSEE EVENT REPORT (LER)
CouuevTs REauoNo BURotN EsTuaTE To THE woRMATcN AND RECORD 3 MANAGEMENT ORANCH (MNB8 771dL U S. NUCLEAR TEXT CONTINUATION Recut 4Tosu CoMutssroN. wAsMiNoToN, oc resss-ooo1 ANa To THE PAPERW1DR< REDUCTON PROJECT (31504104, OFFICE 08 MANAGEMENT AND BUDGET. WASHINGTON DC 20503.
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Si;QUENTIAL hEV1LON ygg NUMBER NUMBER Waterford Steam Electric Station 05000 382 04 & 04 unit 3 94
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, E a w n. n...u.n.a.... m -., n m xm o n IMMEDIATE CORRECTIVE MEASURES Immediate corrective action for this event was to make a temporary approved change to Attachment 10.4 of OP-903-024 correcting the mass balance equation.
ACIIONS TO PREVENT RECURRENCE Given that Waterford 3 believes that this was an isolated case, action to prevent recurrence will be to have Operations personnel review this event.
1 This will be completed by June 15, 1994.
l
SAFETY SIGNIFICANCE
This event did not compromise the health and safety of the public because RCS components and support systems designed to accommodate RCS leakage were not burdened during the time frame that the leakage could have occurred.
Also, when the surveillances were conducted upon exiting Refuel 5 during Modes 1 through 4, which were based on correct calculations in Attachment 10.1 of OP-903-024, RCS unidentified leakage was within LCO limits.
The l
incorrect methodology in Attachment 10.4 of Revision 8 to OP-903-024 was l
used only once to determine RCS leak rate, which was on November 3, 1992 j
involving this event.
SIMILAR EVENTS
None I
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05000382/LER-1994-001-02, :on 940118,discovered That Component Cooling Water Valves Open Approx 30% Due to Lack of Work Instructions.Valve Operators for Affected Valves Adjusted to Close Valves & Valves Locked Closed |
- on 940118,discovered That Component Cooling Water Valves Open Approx 30% Due to Lack of Work Instructions.Valve Operators for Affected Valves Adjusted to Close Valves & Valves Locked Closed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | 05000382/LER-1994-002-01, :on 840808,determined That Five Radioactive Sources Had Not Been Leak Tested.Caused by Programmatic Deficiency.Radioactive Sealed Sources Leak Tested |
- on 840808,determined That Five Radioactive Sources Had Not Been Leak Tested.Caused by Programmatic Deficiency.Radioactive Sealed Sources Leak Tested
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000382/LER-1994-003-01, :on 940305,discovered Reactor Protection Inoperable Due to Missed Surveillances.Caused by Omission of Relevant Info from Procedures.Procedures Revised & Personnel Debriefed |
- on 940305,discovered Reactor Protection Inoperable Due to Missed Surveillances.Caused by Omission of Relevant Info from Procedures.Procedures Revised & Personnel Debriefed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(1) | 05000382/LER-1994-004-01, :on 940307,degraded CCW HX Discovered While Shutdown Due to Biological Fouling.Ccw HXs a & B Cleaned.W/ |
- on 940307,degraded CCW HX Discovered While Shutdown Due to Biological Fouling.Ccw HXs a & B Cleaned.W/
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) | 05000382/LER-1994-005-01, :on 940415,dicovered That Several Valves Were Not Being Tested Per Requirements of ASME Section Xi.Caused by Inappropriate Action.Corrective Action:Pump & Valve Team Has Been Formed to Perform in Depth Reviews |
- on 940415,dicovered That Several Valves Were Not Being Tested Per Requirements of ASME Section Xi.Caused by Inappropriate Action.Corrective Action:Pump & Valve Team Has Been Formed to Perform in Depth Reviews
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | 05000382/LER-1994-006, :on 940415,determined That on 921103, Unidentified RCS Leak Rate of Greater than 1 Gpm Occurred. Caused by Error in RCS Mass Balance Equation.Approved Temporary Change to Procedure OP-903-024 |
- on 940415,determined That on 921103, Unidentified RCS Leak Rate of Greater than 1 Gpm Occurred. Caused by Error in RCS Mass Balance Equation.Approved Temporary Change to Procedure OP-903-024
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | 05000382/LER-1994-007, :on 940426,automatic Reactor Trip Occurred Due to Low Pressurizer Pressure Core Protection Calculator Auxiliary Trip.Corrective Action:Replacing Faulty Relay & Removing Reactor Power System from Service |
- on 940426,automatic Reactor Trip Occurred Due to Low Pressurizer Pressure Core Protection Calculator Auxiliary Trip.Corrective Action:Replacing Faulty Relay & Removing Reactor Power System from Service
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(viii)(B) | 05000382/LER-1994-008, :on 940503,circuitry Problem Re Response Times of Temp Controllers & Time Delay Relays for ESF Filtration Unit Heaters.Caused by Personnel Missing Opportunities to Promptly Identify ESF Performance |
- on 940503,circuitry Problem Re Response Times of Temp Controllers & Time Delay Relays for ESF Filtration Unit Heaters.Caused by Personnel Missing Opportunities to Promptly Identify ESF Performance
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | 05000382/LER-1994-009-01, :on 940218,SRO Discovered Object Hanging from Spent Fuel Handling Machine.Caused by Inadequate Barriers. Power Strip to Computer Deengergized |
- on 940218,SRO Discovered Object Hanging from Spent Fuel Handling Machine.Caused by Inadequate Barriers. Power Strip to Computer Deengergized
| | 05000382/LER-1994-010-01, :on 940607,purge of Letdown RM Resulted in Inadvertent Boron Dilution in RCS Due to Inadequate Review of Station Mod Package (SMP-1817) Which Installed Subj Rm. Danger Tag Placed on Valve PMU-120 |
- on 940607,purge of Letdown RM Resulted in Inadvertent Boron Dilution in RCS Due to Inadequate Review of Station Mod Package (SMP-1817) Which Installed Subj Rm. Danger Tag Placed on Valve PMU-120
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | 05000382/LER-1994-011-01, :on 940720,addition of Improper Blend of Makeup Water to VCT Caused RCS Temp to Rise & Reactor Power to Increased.Caused by Personnel Error.Personnel Involved in Event Counseled |
- on 940720,addition of Improper Blend of Makeup Water to VCT Caused RCS Temp to Rise & Reactor Power to Increased.Caused by Personnel Error.Personnel Involved in Event Counseled
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) | 05000382/LER-1994-012-01, :on 940907,discovered Failure to Perform TS Surveillance Requirements.Caused by Misunderstanding & Inadequate Technical Reviews.Ts Bases for 3/4.8.1 Will Be Revised |
- on 940907,discovered Failure to Perform TS Surveillance Requirements.Caused by Misunderstanding & Inadequate Technical Reviews.Ts Bases for 3/4.8.1 Will Be Revised
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000382/LER-1994-013-01, :on 940819,undesired Boron Dilution of Reactor Coolant Sys Occurred.Caused by Failure of BAM-146 to Function properly.BAM-146 Replaced & Increasing Operator Awareness on Reactivity Mgt Significance |
- on 940819,undesired Boron Dilution of Reactor Coolant Sys Occurred.Caused by Failure of BAM-146 to Function properly.BAM-146 Replaced & Increasing Operator Awareness on Reactivity Mgt Significance
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | 05000382/LER-1994-014-01, :on 941006,HLIV Circuit Breaker Left in Open Position Due to Personnel Error.Cognizant CRS Has Been Counseled in Accordance W/Waterford 3 Improving Human Performance Program |
- on 941006,HLIV Circuit Breaker Left in Open Position Due to Personnel Error.Cognizant CRS Has Been Counseled in Accordance W/Waterford 3 Improving Human Performance Program
| | 05000382/LER-1994-015-01, :on 940916,boric Acid Addition to RCS Occurred. Caused by Personnel Error Due to Lack of Self Checking. Primary Nuclear Plant Operator Counseled Re Improving Human Performance Program |
- on 940916,boric Acid Addition to RCS Occurred. Caused by Personnel Error Due to Lack of Self Checking. Primary Nuclear Plant Operator Counseled Re Improving Human Performance Program
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | 05000382/LER-1994-016-01, :on 940721,informed by Cooper Energy Svcs (CES) That CES Could Not Locate Documentation to Prove That Lube Oil Flow to Cooper Model ET-18 Turbocharger Would Be Adequate Under Loss of Control Air |
- on 940721,informed by Cooper Energy Svcs (CES) That CES Could Not Locate Documentation to Prove That Lube Oil Flow to Cooper Model ET-18 Turbocharger Would Be Adequate Under Loss of Control Air
| 10 CFR 50.73(a)(2) 10 CFR 50.73(c)(2) | 05000382/LER-1994-017-01, :on 941122,load Rejection Testing Requirements for EDG Not Met Due to Inadequate Procedure Re Misunderstanding of 498 Kw HPSI Pump.Condition Rept (CR-94-1108) Was Generated |
- on 941122,load Rejection Testing Requirements for EDG Not Met Due to Inadequate Procedure Re Misunderstanding of 498 Kw HPSI Pump.Condition Rept (CR-94-1108) Was Generated
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000382/LER-1994-018-01, :on 941123,liquid Radwaste Released from Waste Condensate Tank a W/Incorrect & non-conservative Permit Release Setpoint on Liquid Waste Radiation Monitor.Caused by Human Error.Appropriate Personnel Counseled |
- on 941123,liquid Radwaste Released from Waste Condensate Tank a W/Incorrect & non-conservative Permit Release Setpoint on Liquid Waste Radiation Monitor.Caused by Human Error.Appropriate Personnel Counseled
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