|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000382/LER-1999-014, :on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B1999-10-12012 October 1999
- on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B
05000382/LER-1999-013, :on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included1999-09-23023 September 1999
- on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included
05000382/LER-1999-012-01, :on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With1999-09-13013 September 1999
- on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With
05000382/LER-1999-011-01, :on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B1999-08-31031 August 1999
- on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B
05000382/LER-1999-009-01, :on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established1999-08-26026 August 1999
- on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established
05000382/LER-1999-010-01, :on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity1999-08-26026 August 1999
- on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity
05000382/LER-1999-008-01, :on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-021999-07-29029 July 1999
- on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-02
05000382/LER-1999-007-01, :on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff1999-07-23023 July 1999
- on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff
05000382/LER-1999-006-01, :on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With1999-07-14014 July 1999
- on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With
05000382/LER-1999-005-01, :on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested1999-06-24024 June 1999
- on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested
05000382/LER-1999-004-02, :on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing1999-05-14014 May 1999
- on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing
ML20205T2621999-04-22022 April 1999 LER 99-S02-00:on 990216,contract Employee Inappropriately Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Security Personnel Performed Review of Work & Work Area That Individual Was Involved with 05000382/LER-1999-003-02, :on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With1999-04-0909 April 1999
- on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With
05000382/LER-1999-002-03, :on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired1999-03-25025 March 1999
- on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired
ML20207F3491999-03-0505 March 1999 LER 99-S01-00:on 990203,contraband Was Discovered in Plant Protected Area.Bottle Was Determined to Have Been There Since Original Plant Construction.Bottle Was Removed & Security Personnel Performed Search of Area.With 05000382/LER-1999-001, :on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With1999-02-0404 February 1999
- on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With
05000382/LER-1998-020, :on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With1998-12-31031 December 1998
- on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With
05000382/LER-1998-016, :on 980730,failed to Meet TS Requirements for for RT Bypasses.Cause Not Determined Because of Age of condition.1E-4% Bistables for All for Channels of Excore Log Power Channels Were Declared Inoperable 9807301998-08-27027 August 1998
- on 980730,failed to Meet TS Requirements for for RT Bypasses.Cause Not Determined Because of Age of condition.1E-4% Bistables for All for Channels of Excore Log Power Channels Were Declared Inoperable 980730
ML20237B6831998-08-17017 August 1998 LER 98-S01-00:on 980723,discovered That Waterford 3 Physical Security Plan,Safeguards Document Was Not Under Positive Control of Authorized Person at All Times.Caused by Human Error/Inappropriate Action.Counseled Employee Involved 05000382/LER-1998-013, :on 980701,IST Valve Surveillances Were Missed. Caused by Inadequate Processing of Info Transferred Between Operations Procedure Group & Programs Engineering.Procedure Revised1998-07-30030 July 1998
- on 980701,IST Valve Surveillances Were Missed. Caused by Inadequate Processing of Info Transferred Between Operations Procedure Group & Programs Engineering.Procedure Revised
05000382/LER-1998-012, :on 980609,TS Channel Check for TS Surveillance 4.3.1.1 Was Missed.Caused by Human Error.Involved Employees Were Counseled & All Licensed Operators Were Apprised of Event1998-07-0909 July 1998
- on 980609,TS Channel Check for TS Surveillance 4.3.1.1 Was Missed.Caused by Human Error.Involved Employees Were Counseled & All Licensed Operators Were Apprised of Event
05000382/LER-1998-011, :on 980603,TS 3.0.3 Entry Was Noted.Caused by Component Cooling Water Makeup Check Valve Failing Ist. Operability of a Train of CCW Was Restored Immediately & Check Valve Internals Were Replaced1998-07-0202 July 1998
- on 980603,TS 3.0.3 Entry Was Noted.Caused by Component Cooling Water Makeup Check Valve Failing Ist. Operability of a Train of CCW Was Restored Immediately & Check Valve Internals Were Replaced
05000382/LER-1998-007, :on 980317,discovered That No Allowance for Instrument Loop Uncertainity Included in Surveillance for Chilled Water Outlet Temp.Caused by Failure to Consider Instrument Loop Uncertainty.Revised Task1998-04-16016 April 1998
- on 980317,discovered That No Allowance for Instrument Loop Uncertainity Included in Surveillance for Chilled Water Outlet Temp.Caused by Failure to Consider Instrument Loop Uncertainty.Revised Task
05000382/LER-1998-006, :on 980306,increased Differential Pressure for Feedwater Isolation Valves Occurred.Caused by Failure to Consider All Pressure Source Affecting Mfivs.Admin Controls Have Been Enacted Requiring Entry Into TS 3.6.31998-04-13013 April 1998
- on 980306,increased Differential Pressure for Feedwater Isolation Valves Occurred.Caused by Failure to Consider All Pressure Source Affecting Mfivs.Admin Controls Have Been Enacted Requiring Entry Into TS 3.6.3
05000382/LER-1998-005, :on 980312,missed Thermal Overload TS Surveillance Were Noted.Caused by Inadequate Review of 1992 Rev to TS 3.8.4.2 IAW GL 91-08.Thermal Overloads for 8 MOVs Were Subsequently Tested & Determined to Be Operable1998-04-13013 April 1998
- on 980312,missed Thermal Overload TS Surveillance Were Noted.Caused by Inadequate Review of 1992 Rev to TS 3.8.4.2 IAW GL 91-08.Thermal Overloads for 8 MOVs Were Subsequently Tested & Determined to Be Operable
05000382/LER-1998-004, :on 980304,TS 4.0.3 Condition - CPC Channel Functional Test,Was Concluded from Preliminary CEOG Rept. Caused by Human Error.Cpc Channels A,B & C Were Satisfactorily Tested1998-04-0303 April 1998
- on 980304,TS 4.0.3 Condition - CPC Channel Functional Test,Was Concluded from Preliminary CEOG Rept. Caused by Human Error.Cpc Channels A,B & C Were Satisfactorily Tested
05000382/LER-1998-003, :on 980302,inoperable Hydrogen Analyzers Were Noted Due to Undersized Thermal Overloads.Engineering Personnel Conducted all-hands Meetings to Discuss Management Expectations for Verifying Critical Design Inputs1998-04-0101 April 1998
- on 980302,inoperable Hydrogen Analyzers Were Noted Due to Undersized Thermal Overloads.Engineering Personnel Conducted all-hands Meetings to Discuss Management Expectations for Verifying Critical Design Inputs
05000382/LER-1998-002, :on 980215,brief Loss of Command Function in CR Occurred.Caused by Inappropriate Action (Human Error) on Part of Shift Superintendent.Ss Was Counseled IAW Corporate Discipline Policy1998-03-18018 March 1998
- on 980215,brief Loss of Command Function in CR Occurred.Caused by Inappropriate Action (Human Error) on Part of Shift Superintendent.Ss Was Counseled IAW Corporate Discipline Policy
05000382/LER-1998-001-01, :on 980214,TSs 3.0.3 Condition Occurred Due to Inoperable Charging Pumps.Replaced Failed SX-1 Relay1998-03-16016 March 1998
- on 980214,TSs 3.0.3 Condition Occurred Due to Inoperable Charging Pumps.Replaced Failed SX-1 Relay
ML20198K3921998-01-12012 January 1998 LER 97-S05-00:on 971210,emergency Vehicles Entered Into Protected Area W/O Proper Security Search.Caused by Misinterpretation of Security Procedure Requirement.Security Personnel Searched Areas Where Drill Occurred 05000382/LER-1997-033, :on 971205,change in HPSI Flow Measurement Exceeded 10CFR50.46 Acceptance Criteria.Caused by Inadequate Procedures.Sbloca ECCS Performance Analysis Was Performed Using S2M Evaluation Model1998-01-0505 January 1998
- on 971205,change in HPSI Flow Measurement Exceeded 10CFR50.46 Acceptance Criteria.Caused by Inadequate Procedures.Sbloca ECCS Performance Analysis Was Performed Using S2M Evaluation Model
05000382/LER-1997-030, :on 971114,noncompliance W/Ts 3.6.3 Was Noted. Caused by Design Error Associated W/Cars Containment Isolation Valves.Valve CAR-201B Was Declared Inoperable1997-12-15015 December 1997
- on 971114,noncompliance W/Ts 3.6.3 Was Noted. Caused by Design Error Associated W/Cars Containment Isolation Valves.Valve CAR-201B Was Declared Inoperable
05000382/LER-1997-027, :on 971110,discovered That Controller for Valve ACC-126A Was Inadvertently Left in Manual Position.Caused by Personnel Error.Operations Manager Conducted Event Debriefing,Performed Walkdown & Revised Procedure1997-12-10010 December 1997
- on 971110,discovered That Controller for Valve ACC-126A Was Inadvertently Left in Manual Position.Caused by Personnel Error.Operations Manager Conducted Event Debriefing,Performed Walkdown & Revised Procedure
05000382/LER-1997-026, :on 971105,single Failure Effects Condensate Storage Pool Inventory Occurred.Caused by Design Deficiency. Procedure Change Initiated1997-12-0505 December 1997
- on 971105,single Failure Effects Condensate Storage Pool Inventory Occurred.Caused by Design Deficiency. Procedure Change Initiated
05000382/LER-1997-025, :on 971017,gag for Valve CC-835B Was Partially Engaged Restricting Valve to Approx 80% Open.Caused by Inadequate Work Instructions.Gag Was Completely Disengaged on Valve CC-835B1997-11-17017 November 1997
- on 971017,gag for Valve CC-835B Was Partially Engaged Restricting Valve to Approx 80% Open.Caused by Inadequate Work Instructions.Gag Was Completely Disengaged on Valve CC-835B
05000382/LER-1996-015, :on 961024,failure to Isolate Containment Penetration 20 Occurred.Caused by Failure of CR Staff Discussing Clearance to Identify,Containment Isolation Would Not Be Adequate If Hung as-is.Expectations Reinforced1997-10-20020 October 1997
- on 961024,failure to Isolate Containment Penetration 20 Occurred.Caused by Failure of CR Staff Discussing Clearance to Identify,Containment Isolation Would Not Be Adequate If Hung as-is.Expectations Reinforced
05000382/LER-1997-016, :on 970515,potential for Inadvertent Recirculation & EFASs Allowed by Ts,Existed.Caused by Deficiency in Ts.Ts Change Request Will Be Revised & Resubmitted for EFAS1997-10-16016 October 1997
- on 970515,potential for Inadvertent Recirculation & EFASs Allowed by Ts,Existed.Caused by Deficiency in Ts.Ts Change Request Will Be Revised & Resubmitted for EFAS
05000382/LER-1997-024, :on 970528,emergency Diesel Generator Autostart Occurred Due to start-up Transformer Failure.Implemented Procedures OP-901-311,OP-901-511 & OP-901-5131997-08-19019 August 1997
- on 970528,emergency Diesel Generator Autostart Occurred Due to start-up Transformer Failure.Implemented Procedures OP-901-311,OP-901-511 & OP-901-513
05000382/LER-1997-023, :on 970708,EDG Fuel Sys Surveillance Was Missed Due to Failure of Personnel to Determine Intended Start & End Dates for SR 4.8.1.1.2.h.2 Interval.Submitted Application for Emergency Amend for Removal of SR1997-08-0707 August 1997
- on 970708,EDG Fuel Sys Surveillance Was Missed Due to Failure of Personnel to Determine Intended Start & End Dates for SR 4.8.1.1.2.h.2 Interval.Submitted Application for Emergency Amend for Removal of SR
ML20151L6561997-08-0404 August 1997 LER 97-S03-00:on 970704,discovered Undetected Entry Into Plant Vital Area.Caused by Inadequate Communication Re Proper Hpt Encl Controls When Normal Steam Flow Was Absent. Developed Security Directive to Address Configurations 05000382/LER-1997-022, :on 970614,RWSP Boron Concentration Was Lower than Rcs,In Volation of TS 3.7.6.2b.Caused by Incorrect Assumptions by Operations Dept Staff & Mgt.Waterford 3 Will Submit TS Change for TS 3.7.6.2b1997-07-18018 July 1997
- on 970614,RWSP Boron Concentration Was Lower than Rcs,In Volation of TS 3.7.6.2b.Caused by Incorrect Assumptions by Operations Dept Staff & Mgt.Waterford 3 Will Submit TS Change for TS 3.7.6.2b
ML20149E2951997-07-16016 July 1997 LER 97-S02-00:on 970616,determined That Two Individuals Inappropriately Entered Vital Area.Caused by Faulty Security Keycard Reader.Repaired Security Keycard & Search Vital Area Entered 05000382/LER-1997-018, :on 970428,voluntary LER for Dropped New Fuel Assembly Was Issued.Caused by Human Error.Sfhm Grappling Tool Was Inspected for Damage or Misalignment1997-06-27027 June 1997
- on 970428,voluntary LER for Dropped New Fuel Assembly Was Issued.Caused by Human Error.Sfhm Grappling Tool Was Inspected for Damage or Misalignment
05000382/LER-1997-019, :on 970529,non-compliance with TS 3.3.3.6 for Containment Isolation Valve Position Indication Was Noted. Caused by Misinterpretation of Requirements of RG 1.97. Revised Submittal to NRC1997-06-27027 June 1997
- on 970529,non-compliance with TS 3.3.3.6 for Containment Isolation Valve Position Indication Was Noted. Caused by Misinterpretation of Requirements of RG 1.97. Revised Submittal to NRC
05000382/LER-1997-017, :on 970515,control Room Emergency Filtration Unit Common Mode Failed.Caused by Inadequate Design.Both Crefu Trains Declared Inoperable & TS 3.7.6.2 Was Entered & Emergency Work Authorization,Initiated1997-06-19019 June 1997
- on 970515,control Room Emergency Filtration Unit Common Mode Failed.Caused by Inadequate Design.Both Crefu Trains Declared Inoperable & TS 3.7.6.2 Was Entered & Emergency Work Authorization,Initiated
05000382/LER-1997-016, :on 970515,potential for Inadvertent Recirculation Actuation Signal Allowed by TS Discovered. Caused by Deficiency in TS Since Original Issuance.Performed Review of Esfa Sys Instrumentation1997-06-16016 June 1997
- on 970515,potential for Inadvertent Recirculation Actuation Signal Allowed by TS Discovered. Caused by Deficiency in TS Since Original Issuance.Performed Review of Esfa Sys Instrumentation
05000382/LER-1997-012, :on 970404,programmatic Breakdown of Overtime Program Occurred.Caused by Lack of Mgt Oversight in Administering & Implementing Plants Working Hour Policy. Ltr Issued Reemphasizing Working Hour Policy1997-06-0404 June 1997
- on 970404,programmatic Breakdown of Overtime Program Occurred.Caused by Lack of Mgt Oversight in Administering & Implementing Plants Working Hour Policy. Ltr Issued Reemphasizing Working Hour Policy
ML20148D0271997-05-19019 May 1997 LER 97-S01-00:on 970418,improperly Authorized Individuals Were Granted Access to Plant Protected Area.Caused by Inadequate Work Process.Keycard Badges Were Inactivated for All Individuals Not Fully Employed 05000382/LER-1997-015, :on 970418,ultimate Heat Sink Did Not Incorporate Conservative Assumptions.Caused by Design Errors Associated W/Original Design of Ultimate Heat Sink. Operability Evaluation Completed on 9704041997-05-19019 May 1997
- on 970418,ultimate Heat Sink Did Not Incorporate Conservative Assumptions.Caused by Design Errors Associated W/Original Design of Ultimate Heat Sink. Operability Evaluation Completed on 970404
05000382/LER-1997-007, :on 970309,discovered Addl Refueling Water Storage Pool Instrument Uncertainty.Caused by Inadequate Design for Reference Leg of Level Transmitters.Recalibrated Rwsp Transmitters & Conducted Tests1997-05-16016 May 1997
- on 970309,discovered Addl Refueling Water Storage Pool Instrument Uncertainty.Caused by Inadequate Design for Reference Leg of Level Transmitters.Recalibrated Rwsp Transmitters & Conducted Tests
1999-09-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F2891999-10-13013 October 1999 Drill 99-08 Emergency Preparedness Exercise on 991013 05000382/LER-1999-014, :on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B1999-10-12012 October 1999
- on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B
ML20217G7211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Waterford 3 Ses. with 05000382/LER-1999-013, :on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included1999-09-23023 September 1999
- on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included
05000382/LER-1999-012-01, :on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With1999-09-13013 September 1999
- on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With
ML20211Q2141999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Waterord 3 Ses.With 05000382/LER-1999-011-01, :on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B1999-08-31031 August 1999
- on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B
05000382/LER-1999-010-01, :on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity1999-08-26026 August 1999
- on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity
05000382/LER-1999-009-01, :on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established1999-08-26026 August 1999
- on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established
ML20210Q6361999-07-31031 July 1999 Corrected Monthly Operating Rept for July 1999 for Waterford 3 ML20210S0581999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Waterford 3.With 05000382/LER-1999-008-01, :on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-021999-07-29029 July 1999
- on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-02
05000382/LER-1999-007-01, :on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff1999-07-23023 July 1999
- on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff
ML20210D8951999-07-23023 July 1999 Safety Evaluation Accepting First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 - ISI-020 05000382/LER-1999-006-01, :on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With1999-07-14014 July 1999
- on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With
ML20209H3781999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Waterford 3 Ses. with 05000382/LER-1999-005-01, :on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested1999-06-24024 June 1999
- on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested
ML20195J8951999-06-17017 June 1999 Safety Evaluation Granting Relief for Listed ISI Parts for Current Interval,Per 10CFR50.55a(g)(5)(iii) ML20195J9741999-06-16016 June 1999 Safety Evaluation Supporting Amend 152 to License NPF-38 ML20207E8631999-06-0303 June 1999 Safety Evaluation Accepting Licensee 990114 Submittal of one-time Request for Relief from ASME B&PV Code IST Requirements for Pressure Safety Valves at Plant,Unit 3 ML20195D5491999-06-0303 June 1999 Safety Evaluation Supporting Amend 151 to License NPF-38 ML20195K3391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Waterford 3 Ses.With ML20195C3041999-05-28028 May 1999 Annual Rept on ABB CE ECCS Performance Evaluation Models 05000382/LER-1999-004-02, :on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing1999-05-14014 May 1999
- on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing
ML20206S7401999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Waterford 3.With ML20205T2621999-04-22022 April 1999 LER 99-S02-00:on 990216,contract Employee Inappropriately Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Security Personnel Performed Review of Work & Work Area That Individual Was Involved with ML20206A9641999-04-21021 April 1999 Safety Evaluation Supporting Amend 150 to License NPF-38 05000382/LER-1999-003-02, :on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With1999-04-0909 April 1999
- on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With
ML20205N9671999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Waterford 3 Ses.With ML20205E8531999-03-30030 March 1999 Corrected Pages COLR 3/4 1-4 & COLR 3/4 2-6 to Rev 1, Cycle 10, Colr ML20205A6331999-03-25025 March 1999 SER Accepting Request to Use Mechanical Nozzle Seal Assemblies as an Alternative Repair Method,Per 10CFR50.55a(a)(3)(i) for Reactor Coolant Sys Applications at Plant,Unit 3 05000382/LER-1999-002-03, :on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired1999-03-25025 March 1999
- on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired
ML20204H1401999-03-23023 March 1999 Rev 1 to Engineering Rept C-NOME-ER-0120, Design Evaluation of Various Applications at Waterford Unit 3 ML20204H1231999-03-22022 March 1999 Rev 1 to Design Rept C-PENG-DR-006, Addendum to Cenc Rept 1444 Analytical Rept for Waterford Unit 3 Piping ML20204H2451999-03-22022 March 1999 Rev 2 to C-NOME-SP-0067, Design Specification for Mechanical Nozzle Seal Assembly (Mnsa) Waterford Unit 3 ML20204F0791999-03-17017 March 1999 Rev 1 to Waterford 3 COLR for Cycle 10 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207F3491999-03-0505 March 1999 LER 99-S01-00:on 990203,contraband Was Discovered in Plant Protected Area.Bottle Was Determined to Have Been There Since Original Plant Construction.Bottle Was Removed & Security Personnel Performed Search of Area.With ML20204B5141999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Waterford 3.With ML20203H8151999-02-17017 February 1999 Safety Evaluation Supporting Amend 149 to License NPF-38 ML20203H8591999-02-17017 February 1999 Safety Evaluation Accepting Licensee Second Ten Year ISI Program & Associated Relief Requests for Plant,Unit 3 05000382/LER-1999-001, :on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With1999-02-0404 February 1999
- on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With
ML20202H9161999-02-0202 February 1999 Safety Evaluation Supporting Amend 148 to License NPF-38 ML20199H6261999-01-21021 January 1999 Safety Evaluation Accepting Classification of Instrument Air Tubing & Components for Safety Related Valve Top Works.Staff Recommends That EOI Revise Licensing Basis to Permit Incorporation of Change 05000382/LER-1998-020, :on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With1998-12-31031 December 1998
- on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With
ML20199C9101998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Waterford 3.With ML20198F4691998-12-21021 December 1998 Safety Evaluation Supporting Amend 147 to License NPF-38 ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20206N4131998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Waterford 3.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program 1999-09-30
[Table view] |
text
!
i Ref: 10CFR50.73(a)(2)(iv)
P l-Lo u i s s a m a ! WATERFORD 3 SES
W3A90-0145 A4.05 QA May 7,1990 U.S. Nuclear Regulatory Commission ATTENTION: Document Control Desk I
Washington, D.C.
20555 Subject: Waterford 3 SES l
Docket No. 50-382 License No. NPF-35 Reporting of Lice see Event Report l
Gentlemen Attached is Licensee Event Report Number LER-90-004-00 for Waterford Steam Electric Station Unit 3.
This Licensee Event Report is submitted pursuant to 10CFR50.73(a)(2)(iv).
Very truly yours,
'J.R.
McGaha Plant Manager - Nuclear JRM/KTW/rk (w/ Attachment) cci Messrs. R.D. Martin J.T. Wheolock - INPO Records Center E.L. Blake W.M. Stevenson D.L. Wigginton NRC Resident Inspectors Office 9005090344 900507 6DR ADOCK 05000382 l
s PDC q ZO "AN EQUAL OPPORTUNITY ER*LOYER"
/
.,..,C,,...
.. -, l _. t em... m_ _
o enavtDoMeNo simonit LICENSEE EVENT REPORT (LER)
' " Na t $ ' "
I I AcaLITV esAMt (H (MsCatt NUMalm tal 8 AG E d' Waterford Steam Elcetric Station _ Unit 3 0 lb 101010131812 1 l0Fl 014 14 T L t tel Inadvertent Emergency Feedwater System Actuation Due to Test Circuit Malfunction
__ SVGNT DATI 196 L t h IWOMBE R ($1 mt PDAT DATI (F1 OTHE M $ AOttlTit $,NVOLYt D Its MONTH DAV YE A81 YEAH
'IU$'M
du MDPJf 6e DAV tlAA
D0l ki ' NVV8t h'8' n
N/A 016l0l0l0l l l 0h 0l8 9 0 9l 0 0l0l4 0l0 0l5 0 l7 9l0 N/A 016l0g0l0l l l
~
~
tuis nicoat is eu MittiD ruasuANv vo tut at ovinm(Nr o, io C.
s ic,..
,,,,,,,..,,, w.,, o n "UDI #
]
20 4o2th) ac eoStal I to 736eittual 7 7i4bl po In to ammno so n im so n. urn.i n tu.i E*P 110 h re sosannia p osi.nsi so n.nsus otusa m m,,v - AA+
e
~
~~~
- - UI, '" " '" ' * ' '~'
so aamu.in p n.unno no n.nsn.. nAi to aainni.i en n. nan.n
.o n.nznn. nei to a nin.i se n. nan o non.nsn..
LICINtit CONT ACT FOn Th.) Lim tint NAVE 15 LLPHONE Nuv9t R AkiACDDL T.ll. Smith, Plant Engineering Superintendent 51014 41614 l -1311 1218 COMettit DNt LINI #0h I ACH COMPONINT f Altunt DttCnistD IN TMit RIPOnf 113.
" I,'g p',"g
C
"")['g,"U p',"h '
"I CiU$t tv57tv CouPONI NT Caust tv5f f v C0vtONINT g
1 I I i i i 1 i
i i i 1 I l
I l l l l !
I l ! l l l l SUPPLIME NT AL htPORT t kPICit D Het UDN1h Dev v t A81 Sv D M 'f*5 tC N
} u <<<,..,,,, a uscrio ave.nssio= oA rts
-]No o li yl4 9; 3 as s i e A C t n.-, o,. w.....,... -,,,..
,y. u-,,,,.
~n.
,...e n.>
At 0444 hours0.00514 days <br />0.123 hours <br />7.34127e-4 weeks <br />1.68942e-4 months <br /> on April 8, 1990, Waterford Steam Electric Station Unit 3 was operating at 100% power when a partial actuation of the Emergency Feedwater i
(EFW) system occurred during a scheduled functional test of the Plant Protection System (PPS).
This event is reportable an an unplanned Engineered Safety Feature (ESP) actuation. The actuation was not of sufficient duration to allow ErW flow to the Steam Generators (SG).
The root cause of this event is test circuit malfunction.
Inspection of the matrix test module relay hold pushbutton contact blocks and wiring revealed a higher than normal resistance across the early opening contacts.
The relay hold pushbutton assembly has been replaced and the PPS functional test has been l
completed satisfactorily. Further diagnostic testing of the relay hold pushbutton is planned to attempt to isolate the cause of the circuit malfunction.
11ecause the circuit malfunction was associated only with the test circuitry and i
the EFW System was capabic of responding in the safe direction, this event did I
not threaten the health and safety of the general public or plant personnel, i
+,e,,,. n.
a
o
=ac ee,.
A v exucumtivefony coMMissio=
LICENSEE EVENT REPORT (LER) TEXT CCNTINUATCN ue:.ovfo cus no mo-oio.
E xPIRES. S!$1/08 f #*1417 y NAMt (l)
DOCKtifdVM$tM(U tlR NUMSIR (si.
PA06 (31 ygan f l uvt NT ea k ef v stoN Waterford Steam Electric Station Unit 3 0l 0l 4 0 l5 l 0 l 0 l 0 l 3l8 l2 9 10 O l0 012 OF gl4 iEKT IN newe spece h reess eel arse enMaanelMC Form anWeb (1h At 0444 hours0.00514 days <br />0.123 hours <br />7.34127e-4 weeks <br />1.68942e-4 months <br /> on April 8, 1990, Waterford Steam Electric Station Unit 3 was operating at 100% power when a partial actuation of the Emergency Feedwater (EFW) (EIIS Identifier - DA) occurred during a scheduled functional test of the Plant Protection System (PPS) (EIIS Identifier - JC).
This event is reportable as an unplanned engineered safety feature (ESP) actuation.
While performing step 85 of operating procedure (0p) 903-107, " Plant Protection System Channel Functional Test," which involves pressing and-holding the PPS matrix relay hold pushbutton and verifying system response, all three EFW pumps (EIIS Identifier BA-P) and Steam Generator (SG) (EIIS Identifier-SG) Blowdown System Isolation Valves (EIIS Identifier WI-ISV) actuated.
The EFW to SG isolation valves did not open due to the short dura: ion of the actuation signal.
The functional test was terminated and EFW system components were returned to their normal configuration.
The inadvertent actuation could not be reproduced and the functional test was later reperformed with satisfactory results.
l l
The matrix relay hold pushbutton performs three functions.
- 1) It interrupts test power to the matrix test modules (EIIS Identifier - IMOD) not being tested.
- 2) It provides test power to the matrix relay bistable coils (EIIS Identifier - RIN/CL) through the use of early closure contacts (EIIS Identifier - CNTR) on the pushbutton.
- 3) It provides test power to the 1
matrix bistable relay opposing coils.
During the circuit test sequence. the relay hold pushbutton is depressed and l
I through use of the early closure contacts, applies test power to the aiding 1'
coils of the matrix trip path relays before the bistable relays are l
l deenergized.
If the bistabic relays deerergize the matrix trip path relay primary coils before the matrix relay aiding coils energize, an Emergency Feedwater Actuation Signal (EFAS) (EIIS Identifier BA-JE) will result.
N3 C FQ9tU 396A
'U'I' c-sa j
etRC Form 306A U $ NUC48 A3 ME;UL'.TOmv COMM606 l
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Aaenoveo out no mo-oios exeints. sinte p
8 ACILtTF hAMG til.
DoceLif NUMeth tv Lth NUMeth 16)
PAGE 01
- 5^a
" R't.W."
OJ.O Waterford Steam 0 l0l4 C10
({ 3 0F 0l4 Electric Station Unit 3 0 l6 l0 l0 l013 l 8l 2 9l 0 TEXT (# sure space 4 oversif, use esMepne 44C Fsym JNA N tth r
During troubleshooting performed on May 3, 1990, the relay hold pushbutton and contact blocks for the A-C matrix test module were examined and revealed a higher than normal resistance across the early opening contacts.
(Resistance measured in the range of 1.9 to 28 chms, compared to a normal resistanco of 0.2 ohms). This increased resistance may have allowed the bistable relays to deenergized before the matrix relay aiding coils fully energized, causing the EFAS.
I Based on the results of this inspection, the relay hold pushbutton and contacts were repinced and the A-C matrix was tested satisfactorily. Further diagnostic testing of the removed pushbutton is planned to attempt to isolate the cause of the circuit malfunction and evaluate to what degree the observed increase in contact resistance could have delayed the energitation of the aiding coils.
The possibility of carbon or corrosion product buildup on the contacts will also be explored. Based on the results of the diagnostic testing, the relay hold pushbutton assembly may be sent to the vendor (Combustion Engineering, Inc.) for further analysis. Appropriate long term corrective action will be taken as a result of this testing.
Consideration will also be given to examination of similar pushbutton assemblies to address any generic concerns that may arise from the collective test results.
If critical definitive information results from these analyses, a supplement to this report will be issued. The above mentioned testing is expected to be completed prior to December 28, 1990.
The circuit malfunction was limited to the PPS test circuitry and would not have impaired the ability of the EFW system or any other related safety systems to respond to an actual demand on the PPS if required. The functional test in progress at the time of the EFAS was later completed satisfactorily. For these reasons, the health and safety of the general public was not jeopardized during this event,
<, c eonw n a ux
.u.s. cm me-su-m e m u
(
WRC esem Sata -
U s. WuCLla2 ELOULAf omY COuulSeloN 4
~ ' ' '
UCENSEE EVENT REPORT (LER) TEXT CONTINUATION arenovto owo uo aino-oios txeints swas j
eaciun ausni pocniiwuusta m un aman m eaos m
==
=.n i
Waterford Steam Electric Station Unit 3 0 l5 l0 l0 l0 l 3lg l2 glo d ol 4 olo 0l4 OF glg
~~
ssxs wma,eme a w u,m oc w snuw on
Similar Events
None Plant Contact T.H. Smith, Plant Engineering Superintendent, 504/464-3128.
l l
l i
s l
l t
P r
l NAC eORM 356A eU.S. CFtw 1994 520*l0,r00070 C SJ)
|
---|
|
|
| | Reporting criterion |
---|
05000382/LER-1990-001, :on 900223,discovered Controlled Ventilation Area Sys Airlock Doors D-170 & D-171 Open.Caused by Inadequate Administrative Controls.Procedural Instructions Will Be Developed |
- on 900223,discovered Controlled Ventilation Area Sys Airlock Doors D-170 & D-171 Open.Caused by Inadequate Administrative Controls.Procedural Instructions Will Be Developed
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000382/LER-1990-002, :on 900322,reactor Trip Initiated by Plant Protection Sys When Two Control Element Assemblies Dropped to Fully Inserted Position.Caused by Connectors Damaged from Misalignment.Damaged Components Replaced |
- on 900322,reactor Trip Initiated by Plant Protection Sys When Two Control Element Assemblies Dropped to Fully Inserted Position.Caused by Connectors Damaged from Misalignment.Damaged Components Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000382/LER-1990-003, :on 900329,severe Transient on 230-KV Power Distribution Grid Resulted in Reactor Trip & Bus Tie Breaker B Opened Automatically,Deenergizing Safety Bus B.Caused by Grid Fault.Calibr Data Reviewed |
- on 900329,severe Transient on 230-KV Power Distribution Grid Resulted in Reactor Trip & Bus Tie Breaker B Opened Automatically,Deenergizing Safety Bus B.Caused by Grid Fault.Calibr Data Reviewed
| | 05000382/LER-1990-003-01, :on 900329,reactor Trip Occurred Due to Grid Disturbance.Caused by Severe Grid Voltage Transient on 230 Kv Sys.Util Investigating Protective Relay Performance of Industrial Loop & Maint Procedures |
- on 900329,reactor Trip Occurred Due to Grid Disturbance.Caused by Severe Grid Voltage Transient on 230 Kv Sys.Util Investigating Protective Relay Performance of Industrial Loop & Maint Procedures
| | 05000382/LER-1990-004-01, :on 900408,partial Actuation of Emergency Feedwater Sys Occurred During Scheduled Functional Test of Pps.Caused by Test Circuit Malfunction.Matrix Test Module Relay Hold Pushbutton Assembly Replaced |
- on 900408,partial Actuation of Emergency Feedwater Sys Occurred During Scheduled Functional Test of Pps.Caused by Test Circuit Malfunction.Matrix Test Module Relay Hold Pushbutton Assembly Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000382/LER-1990-004, :on 900408,partial Actuation of Emergency Feedwater Sys Occurred During Scheduled Test of Plant Protection Sys.Caused by Test Circuit Malfunction.Relay Hold Pushbutton Assembly Replaced |
- on 900408,partial Actuation of Emergency Feedwater Sys Occurred During Scheduled Test of Plant Protection Sys.Caused by Test Circuit Malfunction.Relay Hold Pushbutton Assembly Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000382/LER-1990-005, :on 900420,condenser Vacuum Pump Discharge Wide Range Gas Monitor Setpoint Discovered to Be Incorrect.Caused by Inadequate Change Procedure for Data Base Manual. Administrative Procedures Revised |
- on 900420,condenser Vacuum Pump Discharge Wide Range Gas Monitor Setpoint Discovered to Be Incorrect.Caused by Inadequate Change Procedure for Data Base Manual. Administrative Procedures Revised
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) | 05000382/LER-1990-006, :on 841218.determined That Shutdown Cooling Sys Relief Valve Setpoint Not Set,Per Tech Spec Requirement. Caused by Procedural Inadequacy.Procedure MM-007-006 Revised |
- on 841218.determined That Shutdown Cooling Sys Relief Valve Setpoint Not Set,Per Tech Spec Requirement. Caused by Procedural Inadequacy.Procedure MM-007-006 Revised
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(c)(2)(1) | 05000382/LER-1990-008-01, :on 900703,Tech Spec 3.0.3 Entered Due to Svcs Chill Water Trains Being Declared Inoperable.Caused by Reduction of Chill Water Loads Following Dropped Control Element Assembly.Event Discussed W/Personnel |
- on 900703,Tech Spec 3.0.3 Entered Due to Svcs Chill Water Trains Being Declared Inoperable.Caused by Reduction of Chill Water Loads Following Dropped Control Element Assembly.Event Discussed W/Personnel
| 10 CFR 50.73(a)(2)(1) | 05000382/LER-1990-009, :on 900606,missed Monthly & Quarterly Composite Analysis Occurred Due to Personnel Error.Technician Failed to Store Sample in Proper Location & Sample Subsequently Discarded.Procedure for Samples Developed |
- on 900606,missed Monthly & Quarterly Composite Analysis Occurred Due to Personnel Error.Technician Failed to Store Sample in Proper Location & Sample Subsequently Discarded.Procedure for Samples Developed
| 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000382/LER-1990-010, :on 900709,inconsistencies Discovered in Pump & Valve Inservice Test Program.Caused by Inadequate Review of ASME Section XI Inservice Test Requirements.Rev to Inservice Test Plan Being Submitted |
- on 900709,inconsistencies Discovered in Pump & Valve Inservice Test Program.Caused by Inadequate Review of ASME Section XI Inservice Test Requirements.Rev to Inservice Test Plan Being Submitted
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(e)(2)(1) | 05000382/LER-1990-011, :on 900721,ESF Control Room Ventilation Actuations Occurred Due to Equipment Malfunction.Cause Under Investigation.Insp of Radiation Monitor Performed |
- on 900721,ESF Control Room Ventilation Actuations Occurred Due to Equipment Malfunction.Cause Under Investigation.Insp of Radiation Monitor Performed
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(1) | 05000382/LER-1990-012-01, :on 900825,reactor Tripped Due to Lightning Strike.Station Mod Request Issued to Provide Uninterruptable Power Source for Steam Bypass Control Sys |
- on 900825,reactor Tripped Due to Lightning Strike.Station Mod Request Issued to Provide Uninterruptable Power Source for Steam Bypass Control Sys
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000382/LER-1990-013-01, :on 900903,unsampled Gas Released from Gaseous Waste Mgt Sys.Caused by Internal Leakage Past Discharge Isolation Valves.Administrative Controls in Place to Ensure That Gas Decay Tanks Sampled Prior to Release |
- on 900903,unsampled Gas Released from Gaseous Waste Mgt Sys.Caused by Internal Leakage Past Discharge Isolation Valves.Administrative Controls in Place to Ensure That Gas Decay Tanks Sampled Prior to Release
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) | 05000382/LER-1990-014-01, :on 900922,control Room Outside Air Isolation Due to Procedural Inadequacy |
- on 900922,control Room Outside Air Isolation Due to Procedural Inadequacy
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000382/LER-1990-015, :on 900929,inadvertent Control Room Ventilation Actuation Occurred Due to Equipment Malfunction |
- on 900929,inadvertent Control Room Ventilation Actuation Occurred Due to Equipment Malfunction
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) | 05000382/LER-1990-016-02, :on 901014,two Posted High Radiation Areas Greater than 1000 Mrems Discovered Not Locked Per Tech Spec 6.12.2.W/undated Ltr |
- on 901014,two Posted High Radiation Areas Greater than 1000 Mrems Discovered Not Locked Per Tech Spec 6.12.2.W/undated Ltr
| 10 CFR 50.73(a)(2)(1) | 05000382/LER-1990-017-01, :on 901116,missed Diesel Fuel Oil Sample Due to Not Following Required Procedure.Addl Sample Drawn to Support Investigation of New Diesel Fuel Oil Analysis.W/ |
- on 901116,missed Diesel Fuel Oil Sample Due to Not Following Required Procedure.Addl Sample Drawn to Support Investigation of New Diesel Fuel Oil Analysis.W/
| 10 CFR 50.73(a)(2)(1) | 05000382/LER-1990-018-03, :on 901206,discovered That Shutdown Cooling Sys Suction Line Relief Valves Not Demonstrated Operable Since Issuance of OL on 841218.Caused by Overlooking Configuration Since TS Written.Ts Change Will Be Sent |
- on 901206,discovered That Shutdown Cooling Sys Suction Line Relief Valves Not Demonstrated Operable Since Issuance of OL on 841218.Caused by Overlooking Configuration Since TS Written.Ts Change Will Be Sent
| 10 CFR 50.73(a)(2)(1) | 05000382/LER-1990-019-02, :on 901212,Tech Spec LCO 3.0.3 Entered When Both Trains of Control Room HVAC Sys Declared Inoperable Due to Breach in Control Room Envelope.Caused by Insufficient Documentation & Details of Boundary Seals |
- on 901212,Tech Spec LCO 3.0.3 Entered When Both Trains of Control Room HVAC Sys Declared Inoperable Due to Breach in Control Room Envelope.Caused by Insufficient Documentation & Details of Boundary Seals
| 10 CFR 50.73(a)(2)(1) | 05000382/LER-1990-019, :on 901212,both Trains of Control Room Heating Ventilation & Air Conditioning Sys Inoperable Due to Breach in Control Room Envelope.Caused by Air Flow Past Retaining Angle.Leakage Paths Repaired |
- on 901212,both Trains of Control Room Heating Ventilation & Air Conditioning Sys Inoperable Due to Breach in Control Room Envelope.Caused by Air Flow Past Retaining Angle.Leakage Paths Repaired
| 10 CFR 50.73(a)(2)(1) | 05000382/LER-1990-020-03, :on 901227,chlorine Gas Released from Local Chemical Plant.Alert Declared.Toxic Chemical Release & Emergency Procedures Entered.Event Voluntarily Reported.W/ |
- on 901227,chlorine Gas Released from Local Chemical Plant.Alert Declared.Toxic Chemical Release & Emergency Procedures Entered.Event Voluntarily Reported.W/
| |
|