ML20011F459

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LER 89-021-00:on 891116,emergency Diesel Generator a Declared Inoperable When Essential Svcs Chiller a Declared Inoperable W/O Verifying Availability of Offsite Ac Power. Caused by Personnel Error.Supervisor counseled.W/891218 Ltr
ML20011F459
Person / Time
Site: Waterford Entergy icon.png
Issue date: 12/18/1989
From: Mcgaha J, Starkey R
LOUISIANA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-89-021, LER-89-21, W3A89-0211, W3A89-211, NUDOCS 9003060066
Download: ML20011F459 (4)


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Louisiama P O W E R ' & L I G H T! WATERFOAD 3 SES

  • RO. DOX B'e KILLONA, LA 70066 0751 n 4 - EuSNtIysYdU W3A89-0211 A4.05-QA December 18, 1989~

U.S. Nuclear Regulatory Commission

' ATTENTION: Document Control Desk Washington,-D.C. 20555

Subject:

Waterford 3 SES

. Docket No.'50-382 License No. NPF-38 Reporting of Licensee Event Report i

,i Centlement Attached-'is Licensee Event Report Number LER-89-021-00 for Waterford Steam Electric Station Unit 3..This Licensee Event Report is submitted pursuant to 10CFR50.73(a)(2)(1). ]

'I Very truly yo,urs, j oc

' 3. . McGaha Plant Manager - Nuclear L

JRM/ PTS /rk (w/ Attachment) cc Messrs. R.D. Martin J.T. Wheelock - INPO Records Center l

.E.L. Blake l W.M. Stevenson D.L. Wigginton NRC Resident Inspectors Office I l

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W 8 NUCLE AR Rt0 ult,f0RV COMMISSION APPRovtD OMB NO 31eH104 LICENSEE EVENT REPORT (LER) ' " "'a ' * ' '8" eACILITV NAMt til DOCati NUMetR (28 PAGE (3'

-Waterford Steam Electric Station Unit 3 0l6l0toj0l31812 1 loFl 013 TITLE tes Fn i l tire e rs P3rform Off-site Power Verification Surveillance due to Personnel Error iVENT Daf t lll Lin NUMetR ten REPORY DAf t 171 OTHE R F ACILITit$ INYOLvtD iti MONTH day vtAR vtAR "[yy '4 , ((7M MONYM DAY vtAR Pacility Nauts DOCatT NUM8tRt31 N/A 0l6l01010; l l l 1! 1 1l 6 8 9 8l9 0l2 l 1 0l 0 1l 2 N8 8l 9 N/A 0 t 6 toloio; l l DPE R ATtNG THIS REPORT 16 5USMITTED PURSUANT TO TML PEQUIREMENTS OF 10 CF R l (Casca one se more of the tenew ps tiu 3 20 +0 mini 20 aosisi so.73isii2iiivi 72.71 *i to40RieH1H4 le 3eleHit to.73 tent 1Het 73.71tel fiel O 10 D 80 40*'eH1Hdi 50.886eH2) 50 73 inh 2H=al

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] $0.73teH2H6) 50 73teH2HeiuHA) redJ to 408(*H1H6vl 40.73teH2 Het 50.73teH2Hentitel to 406teH1 Het ' 50.73te H2HHil 60.734ent211al LICENEtt CONT ACT FOR TMit LER (121 NAME TELEPHONE NUMBER art A CQQt R.S. Starkey, Operations Superintendent 5 1014 4 6141-13 111314 COMPL ETE ONE LINE FOR I ACM COMPONENT F AILURE DESCRISID IN THIS REPORT 113 M^ 0R ,T A Lt " ORTe E CAUSE Sv87tM COMPONENT g$0' Tn CAust SvittM COMPONENT .

p g $C. pq I I I i l l l I I I f I I I i 1 l 1 l l i 1 I I ! l I I SUPPLEMENTAL REPORT EXPtCTED 114 MONTH DAY YEAR SV0MtSSION 4t$ lie pen. eemoiste RKPECTED SUOw$$lOnt DA TIJ NO l l l A.:T R ACT rum,, ,o eco =<*o e . e,emme., r n.ee e,* -<e ~~,.nemeu n et At 1025 hours0.0119 days <br />0.285 hours <br />0.00169 weeks <br />3.900125e-4 months <br /> on November 16, 1989, Waterford Steam Electric Station Unit 3 was in Mode 3 when Emergency Diesel Generator "A" was declared inoperable due to Essential Services Chiller "A" being declared inoperable. Technical Specification (TS) 3.8.1.1. action requirement b specifies verifying offsite AC power availability within one hour and every eight hours thereafter. The-first verificat1on was completed at 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br />. On November 17, 1989, at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, it was discovered that the verification required by 1845 hours0.0214 days <br />0.513 hours <br />0.00305 weeks <br />7.020225e-4 months <br /> on the previous day had not been performed. Failure to perform an action requirement is reportable as a condition prohibited by TS.

The root cause of this event is personnel error. While performing the procedures g required for a normal plant startup, this additional electrical verification F was not performed. To prevent recurrence the Operations Control Room Supervisor involved will be counselled on this event and a copy of this report will be required reading for all current Senior Reactor Operator License holders.

The offsite AC electrical power was verified available at 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br /> on November 17, 1989, and was~known to be available throughout this event; therefore, no threat to the health and safety of the public or plant personnel existed.

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"*' u.s. NUCLEA2 F EIULAToRY CoMMissloN o LICENSEE EVENT REPORT (LER) TEXT CONTINUATION uenovio oMe No. siso-oin i- - # ~ * ' ' ' =

EXPIRES: 8/314 f ActLtiv NAMt tu DOCKit NUMGER (21 Lim NUMSER (si PAGE (31 vtan St out NT s A4 Re v ech Waterford Steam- '*"" '*""

Electric Station Unit 3 TEXT (# snore spese e segunod, was eds,senaf 44C Form JOEA W (1M o l5 l0 l0 l0 l3 I8l 2 8l9 -

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On November 16, 1989, Waterford Steam Electric Station Unit 3 was in mode 3

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preparing for startup from Refuel 3. At 1025 hours0.0119 days <br />0.285 hours <br />0.00169 weeks <br />3.900125e-4 months <br />,. Emergency Diesel Generator l (EDG) "A" (EIIS Identifier EK-DG) was declared inoperable because Essential *

' Services Chiller "A" (EIIS Identifier 101) had been declared inoperable. This -

i action was necessary because Chiller "A" provides cooling for the Component Cooling Water (CCW) Pump "A" (EIIS Identifier CC-P) Room Cooler (EIIS Identifier VF-CLR) and CCW Pump "A" provides cooling for EDG "A". At that time Technical Specification (TS) 3.8.1.1. action requirement b was entered which requires verifying offsite AC power availability. Waterford 3 satisfies this action requirement by performance of Surveillance Procedure OP-903-066, " Electrical Breaker Alignment Check," within one hour of declaring an EDG inoperable and l

cach eight hours thereafter. The first performance of OP-903-066 was completed at 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br />. On November 17, 1989, at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, it was discovered that the surveillance required by 1845 hours0.0214 days <br />0.513 hours <br />0.00305 weeks <br />7.020225e-4 months <br /> on the previous day had not been performed.

Failure to perform an action requirement is reportable as a condition prnhibited by TS.

The root cause of this event is personnel error. While performing the other procedures required for a normal plant-startup, this additional electrical.

surveillance procedure was not performed. To prevent recurrence the Operations Control Room Supervisor involved will be counselled concerning the missed surveillance and a copy of this report will be required reading for all current Senior Reactor Operator License holders. These actions will be completed by January 1, 1990. The Operations Department will review and evaluate the current procedure and methodology for ensuring compliance with irregular / infrequent

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Limiting Condition for Operation (LCO) action requirements. Applicable results will be used to enhance the process and minimize the potential for recurrence.

This will be completed by February 1, 1990.

The offsite AC electrical pcwer was verified available at 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br /> on November 17, 1989, and was known to be available throughout this event; j therefore, no threat to the health and safety of the public or plant personnel

! existed.

l e NRC FORM MSA *U.S. GPoe 1988-520 589i00010 bk _i___________________________ _

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~* NRC Were 306A - U.S. NUCLEA3 KEIULATORY COMMISSION

' ' - ~ . ** LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APerovio OMS No. sino-aio4 ,

, EXPIRIS: $/31/m -

P ACILuv NAML til DOCKET NUAES6R (2) LER NUMSIR 644 PA06 (3) .

~Waterford Steam , " ' "

"0NI'a" SEI=U Electric Station-Unit 3 rex 7wso - . w . w m.m.asaaunn 0 15l0l0l013 l812 819 -

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SIMILAR EVENTS There was a similar event reported as LER-88-021 in which, after declaring an EDG inoperable, the initial electrical lineup verification required within one-s hour was overlooked by control room personnel. As in this case, offsite

-electrical power was known to be available throughout the event; therefore, no threat to the health and safety of the public or plant staff existed.

PLANT CONTACT R.S. Starkeyi Operations Superintendent, 504/464-3134.

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I o NIC PORM 3 eta 'U.S. GFoa 1988-520 589,00070 DM.