ML19331B876

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LER 80-041/03L-0:on 800807,while Reviewing Maint Work Request (Packing Adjustment on Valve 1-CS-88278),determined Surveillance Requirements Not Current During Change from Mode 5 to Mode 4.Cause Unstated
ML19331B876
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 08/07/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19331B872 List:
References
LER-80-041-03L, LER-80-41-3L, NUDOCS 8008130466
Download: ML19331B876 (1)


Text

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EVENT DESCRIPTION AND PRCGABLE CONSEQUENCES h O 2 lWhile reviewing a Maintenance Work Request (packing' adjustment on 6/24/80 on valve [

! F6 I i'l i 1-CS-8827B) for functional acceptance at 1920 on 7-8-80, it was determined that the ]

I IOI41 Isurveillance requirements were not current during a plant = ode change (Mode 5 to 4. at l

. g o 3 3,- [ 0630 on 7-8-80) . T/S 3.6.3.1 requires that the valve be demonstrated operable'af ter  ;

g g l maintenance in Modes 1 through 4. The health / safety.of the 'public were not affected.

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44 CAUSE DESCRIPTION AND CCARECTIVE ACTIONS h l i j O l l The valve was subreouently satis f actorily tested per FNP-1-STP-16.7, " Containment Soravl y l System Valve Inservice Test". It was not noted on the work request that adiustine I t.

i,,7i l packing on valve 1-CS-8827B would require a retest. This. requirement is listed in I g l FNP-0-AP-52, " Equipment Status and Maintenance Authorization". The necessity of I li # 41 7 8 9

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