ML19257D844

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LER 79-081/03L-0:on 791225,containment Air Particulate & Gaseous Radiation Monitor Pump Tripped Off Due to Low Air Flow.Cause Undetermined.Air Flows Realigned & Readjusted. Operating Instructions Being Modified
ML19257D844
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 01/25/1980
From: Davis S, Rizzo P
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19257D843 List:
References
LER-79-081-03L, LER-79-81-3L, NUDOCS 8002060598
Download: ML19257D844 (2)


Text

NRC FORM ,J66 U. S. NUCLEAR REGULATORY COMMISSION (170

  • LICENSEE EVENT REPORT CoNTRotStoCo l l 1 I I l@ (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI to 7

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REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 i At 0800 the contaiment air particulate and gaseous radiation monitor pump l RTT'l I tripped off due to low airflow. The air particulate monitor was bypassed I o 4 I and isolated in accordanCe with T.S. 3.4.6.1 in order to crovide adecuate l Io s l airflow to the caseous monitor. The air carticulate monitor was returned I o s l to service at 1410 on 12/26/79. The contaiment sumo level alarm and caseous I o 7 l monitor remained ocerable durino the event. This is not a recetitive occur- I o a i renc e. I 7 8 9 80 0E OE SU8C E COMPONENT CODE SUSCODE 5 E 7

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LER NO. 79-81/3L DOCKET NO. 50-317 EVEfiT DATE 1 2/25/79 REPORT DATE 01/ 25/80 ATTACHMENT CAUSE DESCRIPTION AND CORRECTIVE ACTIONS: (CONTINUED)

The initial cause of loss of flow was undetermined. Flow may decrease over time due to wear of sampler pJmp vanes or may Change due to systen lineups . Operators bypassed the particulate sampler to increase flow due to unfamiliarity with valve functions and sample skid component operation. Technicians were able to realign and adjust flows the following day.

To prevent recurrence, sample skid valves will be labled for identification and Operating Instructions are being modified to facilitate valve Lineup changes for contairment sampler components.

O 1928 033