ML19257A935

From kanterella
Jump to navigation Jump to search
LER 79-073/03L-0:on 791204,after Completing Weekly Testing on Diesel Generator,Associated Sequence Initiate Alarm Did Not Clear.Caused by Binding Auxiliary Switch Which Would Not Return to Open Position.Switch Replaced
ML19257A935
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 01/04/1980
From: Bauer E, Lagiewski J
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19257A932 List:
References
LER-79-073-03L, LER-79-73-3L, NUDOCS 8001090429
Download: ML19257A935 (2)


Text

. llc I- OHM ;G6 IJ. 6. f4UCLE A9 M GOL ATOrtY CtM.uSSION (7-77) i LICENSEE EVENT REPORT CONTROL BLOCK: (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 l l l l l lh 6

o i l Ml Dl C C l Nl 1 l@l 0 l 0 l -l 0 l 0 l 0 l 0 ] 04 - l 0 l 025l@l 4 1 l 1 l 1 l 1 l@l$ 7 C lA T $8l g' 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 26 LIC.NSE TYPE JO CON'T -

?

0 1 8

S uRg l L l@l 0l 5 l 0 0 l 0 l 3 l 1 l 7 )@l 1 60 61 68 69 2EVENT l 0 DATE l 4 l 7 l 9 l@@ 74 75 0]DATE lREPORT 4l 8 0@ 80 DOCK ET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lo l>l I Af ter completion of weekly testing on #11 Diesel Generator (D.G.), it was  ;

10 l 3 l l observed that the associated " sequence initiate" alann did not clear. At l 0 4 1 1323, the 0.G. was removed from service to investigate the problem and l 0 s [ effect repairs on the output breaker. The breaker auxiliary switch was l l0 l6 l l found to be binding and would not return to the open position. l 0 7 l l 0 I a l 90 g g DE CO E SL8C E CO'.tPCNENT CODE SLac C'E S I DE O 9 S lH l@ [_EJ@ W@ l C l K ] T l B l R l K l@ y@ l Zl @

7 8 9 to 11 12 13 18 19 20 SEOLENTI AL OCCURRENCE HEPORT REVISION LER AO EVENT YEAR REPCRT NO. CODE TYPE NO.

O .y.g 17 l9 l

,,., 21 22 l-l 2J 24 0l7l3l 26 M

27 28 0 l3 l 29 lL 30

[_j 31 l0l 32 TA EN A O ON PL NT ET HOURS 22 SLS ITT FCRibuS. S PPLIE '.*A' F CTLRER l C l@[_Zj@

33 34

[Zj@

35 36 Z l@ l 01010l 0l 37 40 W@

41 W@ lAl@ lGl0 8 Olg 42 43 44 47 CAUSE DESCRIPTION AND COPRECTIVE ACTIONS i o i The faulty switch was replaced. O'odel dSBM Type 10 AX 01263). The procer I li li l I oneration of this switch can be observed durina the weekly functional test i li i 21 l of the Diesel Generators. Additionally, the breaker and its auxiliary j i 3 l ' switches are periodically inspected under the preventive maintenance l

[1j4j l program. l 7 8 9 80 STA $ '. P O.'. E R OT54ER STATUS IS O RY DISCOVERY OESCH:PTION i s E@l0 7l 0l@l" flA -

l lA l@l**

NA l

'diviTY CS: ENT

A'.*OUNT OF ACTIVITY LOC ATION CF RELE A0E 7

i 6 8 9

[1] ASE@D cF RELE ASELZj@l AELE 10 11 flA 44 l l 45 NA 80 l

PEMCN NEL EXPOSURES

, D. E R TYPE D E !O RIP TIO*J <

i 7 [ 0 ] 0 l 0j@l Z l@L flA j 7 8 9 11 12 13 U

nfd 9 F

]'

50 P M 7.'.E L l'. J'. A I E S

. . , cER DESCa.PfiON

]' ,5 L, 7

i -

8 9 l010101@l II 12 NA - -

23 l

LG S CF C9 OM.* AGE TO F ACILI TY

= ' " " "

7

, e 8 9 ri'igi 10 NA 1708 017 i E3 l l0j Ul.j61

< Tih.sN@ fiA 52 0 o 10 90 W; ; ; ;"; "; "; ; ; ; ; ; ; l :;

7 4 3 0 .s o

. oS

. A*.* E O F N E P AR E P

d. $. Lagiewski/E. R. Bauer g,. o., s (301):34-79*2/7255  ?,

LER NO. 79-73/3L DOCKET NO. 317 EVENT DATE 12/4/79 REPORT DATE 1/4/80 ATTACHMENT

- - CAUSE DESCRIPTION AND CORRECTIVE ACTION: (CONTINUED)

Since the switch remained closed, the associated sequencer logic was continually energized and would not have functioned in the assigned time period (no delay would have occurred). However, a redundant sequencer and associated ESFAS equipment remained operable throughout the event.

While the 0.G. was inoperative, the remaining A.C. power sources were checked in accordance with Technical Specification 3.8.1.1. #11 Diesel Generator was returned to service at 1510. This is not a repetitive occurrence.

CAUSE DESCRIPTION AND CORRECTIVE ACTION: (CONTINUED)

Therefore, no further action to prevent recurrence is considered necessary at this time.

1708 018 f