ML19257A348

From kanterella
Jump to navigation Jump to search
LER 79-070/03L-0:on 791122,during Log Readings,Discovered That Reactor Protection Sys Channel C Containment Pressure Signal Had Deviated by Greater That 0.1 Volts from Other Channels.Caused by Faulty Isolator 1-E/E-5313C
ML19257A348
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 12/20/1979
From: Davis S
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19257A347 List:
References
LER-79-070-03L, LER-79-70-3L, NUDOCS 8001030797
Download: ML19257A348 (2)


Text

- - -- .-.

(7 77)i -

LICENSEE EVENT REPORT control block: l l l l l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 o i 8 9 lMIDlClClNl 1 l@l 010 l- 10 l0LICENSE 14 15 l 0 lNUMBER 0 l 0 l- [0 l 0 25l@l4 26 l1LICENSE l1 l1TYPE l 1JOl@l 57 CAT l 68 l@

7 LICENSEE CCOE con'T 7

o 1 3

"'[RE C

60 l l l@l 0 l 5 l DOCKET 61 0 l 0NUMBER l 0 l 3 l 1 68[ 7 69l@l 1EVENT l1 DATE 12 12 l 719 l@llREPCRT 74 75 1212 DATEl 017 80 9l@

EVENT DESCRIPTION AND PRCBABLE CONSEQUENCES h o 2 l At 1800 the Control Rcom Ocerator while takina 100 readings discovered I ola t reactor protection system channel "C" centainment pressure signal had l 0 4 [ deviated by 9reater than 0.1 volts from the other channels. The Channel I o s Iwas bvpassed in accordance with T.S. 3.3.1.1 to accommodate recairs. The I o s I three redundant channels remained ocerable durinc the event. Channel "C" I oi7 I containment cressure was returned to service at 1310 on 11/23/79. This l I is a recetitive occurrence for this tyre of instrument. I cis 80 7 8 9

'$'E '!Coe' sLeC$$E CCMPCNENT CCCE SL8C QE SU E 7

o 9 6

l I l 5 l@ [ E l@ l E l@ l Il NI S i Tl RI U l@ LE_J@ I 20z l @

3 10 11 12 13 18 19 SE QUENTI AL CCCLAAENCE AEPCRT AEVISiCN EVENT YEA R R EPORT NO. CCCE TYPE NO.

lea RO

@ AE j, 17 19 l l- 10 l7 10 l l/l l0l3l lL l l-l l Dl 21 22 23 24 ;6 27 28 29 30 31 32 TK N ACT C. CNP *T E HCURS S8 i FCR B. $LPPLI VANUFAC AER lz l@ 10l 0 01 Ol l Yl@ lA l@ l Tl 2 817 l@

l20A l@34 Fl@ 33l zl@ .

A, 3 ,' 40 41 l42Y l@ 43 44 47 CAUSE DESCRIPTION AND CCARECTIVE ACTICNS h i lo I Feund isolater 1-E/E-5313C to have a low cutrut for its inrut sicnal level, 1 ti ITne instr n ent cculd not be calibrated ard was vaniaced with a stocbd I

!, 2 1 scare. The instrument is a Tran7ation "Odel 230T isolatine transnitter. I ii i2 i Recent Transmation correscendence has succested the use of vil. Scec. I i A I cacacitcrs to decrease failure rate of this mcdel. 30 i

3 3 5  % POWER CTMER STATUS Di RY DiSCCVERY CESCRIPTION Is W @ l 01 6l Ol @ n N/A l l Bl@l Operator Observaticn l

' ' ' '2 a 4s 4 so A!nviTY CCRTENT RE4 SED CF REMA$E LOCATICN CF REGASE @

i e z l@ l' z!@l N/A AMOUNT OF "

ACTIVITYl N/A @l '

l

,E.sCNNELE4,CSSEs NuM.ER Tv,E CEsCRieriCN @

l i 7 l 010 I O l@l z l@l N/A '

,EasCNNEL m a iEs NuM.ER CEsCmeTiC~@ 1447 IUUI zn7 JUJ 7

4 3 3 10 Cl0l@l 11 12 N/A 80 l

6C53 CF CR OAMAGE TO FACILITY r Q

Lt_12]

7 4 3 TYPE l z l@l30 CESCRIPT!CN N/A @N )7 N 80 l

  • " ' "ac use c~'v .
10 ,,scE;@LLPT,2N I NI l N/a @  ! IlllIllIil!Ili a 3 :0 63 69 80 I u ,iE cy :,os.wsR S. ". Davis /P. I;. ciz2n pycyg; (3011234-7042  ?,

LER NO. 79-70/3L DOCKET NO. 50-317 EVENT DATE 11/22/79 REPORT DATE 12/20/79 ATTACH.'ENT CAUSE DESCRIPTICN AND CORRECTIVE ACTION: (C0tiTINUED)

Plant personnel are presently investigating best means to accerolish the change.

1667 304