ML18064A793

From kanterella
Jump to navigation Jump to search
Monthly Operating Rept for May 1995 for Palisades Nuclear Power Plant.W/950602 Ltr
ML18064A793
Person / Time
Site: Palisades Entergy icon.png
Issue date: 05/31/1995
From: Berles B, Anthony Williams
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9506130207
Download: ML18064A793 (5)


Text

....-*

/

consumers Power POWERiNii lllllCHlliAN'S PROliRE55 Palisades Nuclear Plant: 27780 Blue Star Memorial Highway; Covert. Ml 49043 June 2, 1995 US Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 LICENSEE REPORT OF MONTHLY OPERATING DATA DPR-20, DOCKET NO 50-255 Enclosed is a copy of the Monthly Operating Data and Summary of Operating Experience for the Palisades Nuclear Plant for the month of May, 1995.

If you have any questions or concerns, please feel free to contact me at (616) 764-8913, extension 0113.

Sincerely, AL Williams Reactor Engineer CC: RAVincent, Palisades Senior Resident Inspector, Palisades DRHahn, Div of Rad Health Services, Lansing, MI BWJorgenseri, Michigan Dept of Labor, Lansing, MI JPadgett, Michigan Public Service Commission Records Center, INPO, Atlanta, GA CWMain, Palisades SMMclntyre, Pl3-121 Region III Administrator, USNRC Document Control, 950*22*35*10/L Cycle ll Reports 9506130207 9$0531 jP~ll

.PDR ADOCK 05000255 R *.. PDR .

A GHS' ENERGY COMPANY

OPERATING DATA REPORT DOCKET NO 50-255 DATE 06-02-95 COMPLETED BY BIJBerles TELEPHONE (616)764-8913 OPERATING STATUS:

NOTES:

1. UNIT NAME Palisades 2, REPORTING* PERIOD: 950501-950531
3. LICENSED THERMAL POIJER.(MIJt) 2530.0
4. NAMEPLATE RATING (GROSS. MIJe) 811 .7
5. DESIGN ELECTRICAL RATING (NET MIJe) 805.0
6. MAXIMUM DEPENDABLE CAPACITY (GROSS MIJe) **770
7. MAXIMUM DEPENDABLE CAPACITY (NET MIJe) **730
8. IF CHANGES OCCUR IN CAPCITY RATINGS (ITEM NUMBERS 3 THROUGH ?AND 7) SINCE LAST REPORT, GIVE REASONS:
9. POIJER LEVEL TO IJHICH RESTRICTED, IF ANY (NET MIJe):.
10. REASONS FOR RESTRICTIONS, IF ANY:

This Month Yr-to-Date cumulative

11. HOURS IN REPORTING PERIOD 744.0 3623.0 205550.0
12. NUMBER OF HOURS REACTOR IJAS CRITICAL 515.2 3394.2 117706.2
13. REACTOR RESERVE SHUTDOIJN HOURS
14. HOURS GENERATOR ON-LINE 515.2 3394.2 113056.3
15. UNIT RESERVE SHUTDOIJN HOURS
16. GROSS THERMAL ENERGY GENERATED (MIJH) 1170744.0 8384257.. 0 246674908.0
17. GROSS ELECTRICAL ENERGY GENERATED (MIJH) 372341.0 2720389.0 78085180.0
18. NET ELECTRICAL ENERGY GENERATED* (MIJH) 352564.0 2587807.0 73684368.0
19. UNIT SERVICE FACTOR 69.2% 93. ?"!. 55.0%
20. *UNIT AVAILABILITY FACTOR 69.2% 93.7% 55.0%
21. UNIT CAPACITY FACTOR (USING MDC NET) 64.9% 97.8% 53.0%*
22. UNIT CAPACITY FACTOR (USING.DER NET) 58.9% 88.7% 44.5%

. 23. UNIT FORCED OUTAGE RATE . 23.2% 4.4% 29.2%

24. SHUTDOIJNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE, DATE AND DURATION OF EACH):

The 1995 Refueling Outage began on 5/22/95 and is scheduled for 92 days

25. IF SHUTDOIJN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

Forecast* Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

    • Based on condenser backpressure
  • IJeighted Average (635 MIJe used as MDC Net prior to October 1985)

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO 50-255 UNIT Palisades DATE 06/02/95 COMPLETED BY BWBerles MONTH _ _ _ _ MA_Y_ __ TELEPHONE (616)764-8913 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net) (MWe Net)

1. 776 17. 671
2. 775 . 18 .. 677
3. 776 . 19. 676
4. 775 20. 673
5. 774 21. 676
6. 773 22. 310
7. 769 23. 0
8. 771 24. 0
9. 768 25. 0
10. 580 26. 0
11. 426 27. 0
12. 546 28. 0
13. 565 29. 0
14. 631 30. 0
15. 642 - 31. 0
16. 662 INSTRUCTIONS:

On this format, list the average daily unit power level in MWe-NET for each day in the reporting month. Compute to the nearest whole megawatt.

SUMMARY

OF OPERATING EXPERIENCE FOR MAY 1995 The unit began the month operating at full power. On 5/10/95 at* 1300, the loss of Bus lG resulted in Cooling Tower Pump P-398 tripping. An emergency power reduction was made and the unit was stabilized at 55% power. Power was slowly raised to 88% by 5/16/95, where it remainded until 5/22/95. At 1105 on 5/22/95, 'A' Main Feedwater Pump tripped and an emergency power reduction was performed to approximately 50%. At 1110, 'B' Main Feedwater Pump also tripped, at which point the reactor was manually scrammed. The unit remained off-line and entered the Refueling Outage originally scheduled for 5/28/95.

DOCKET NO 50-255 UNIT Palisades DATE 06/02/95 COMPLETED BY _ _B::. :W.:. :B"'e.:. .r.:. :le=s REPORT MONTH ___M~A~Y~1~9~95_ __ TELEPHONE (616)764-8913 UNIT SHUTDOWNS AND POWER REDUCTIONS No. Date Type 1 Duration Method of Licensee System Component Cause & Corrective (Hours) Shutting Event Code 4 Code 5 Action to 3

Down Reactor Report # Prevent Recurrence 5/10/95 131 A-Cooling Tower Pump Trip Power reduction from 100% to 55% following CT trip. Power raised to 88% by 5/16/95.

2 5/22/95 F 155._8 A-Both Main 2 95-003 Loss of both Main Feedwater Feedwater Pumps P~mps in a 5 minute interval.

Tripped Rapid downpower from 88% to 60%. power, followed by manual scram from 60% power.

3 5/28/95 s c Refueling Outage scheduled to begin on 5/28/95 began on 5/22/95 due to #2.

l. 2. 3. 4. 5.

F: Forced Reason: Method: Exhibit G - Instructions Exhibit I - Same Source S: Scheduled A-Equipment Failure -(Explain) 1-Manual for Preparation of Data

  • B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling* 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-0ther (Explain) (NUREG-'0161)

E-Operator Training & License Examination F-Administrative G-Operational Error (Explain)

H-Other (Explain}