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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:RO)
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A9151999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Shearon Harris Npp. with 991012 Ltr ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18017A8621999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Harris Nuclear Plant.With 990908 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18017A8361999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Shearon Harris Nuclear Power Plant.With 990811 Ltr ML18016B0151999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Shearon Harris Npp. with 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9851999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990614 Ltr ML18017A8981999-05-12012 May 1999 Technical Rept Entitled, Harris Nuclear Plant-Bacteria Detection in Water from C&D Spent Fuel Pool Cooling Lines. ML18016A9581999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990513 Ltr ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8941999-04-0505 April 1999 Revised Pages 20-25 to App 4A of non-proprietary Version of Rev 3 to HI-971760 ML18016A9101999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Shearon Harris Nuclear Power Plant.With 990413 Ltr ML18016A8661999-03-31031 March 1999 Shnpp Operator Training Simulator,Simulator Certification Quadrennial Rept. ML18017A8931999-02-28028 February 1999 Risks & Alternative Options Associated with Spent Fuel Storage at Shearon Harris Nuclear Power Plant. ML18016A8551999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Shearon Harris Npp. with 990312 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8531999-02-18018 February 1999 Non-proprietary Rev 3 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris SFP 'C' & 'D'. ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18022B0631999-02-0404 February 1999 Rev 0 to Nuclear NDE Manual. with 28 Oversize Uncodable Drawings of Alternative Plan Scope & 4 Oversize Codable Drawings ML20202J1161999-02-0101 February 1999 SER Accepting Relief Requests Associated with Second 10-year Interval Inservice Testing Program ML18016A8041999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Shearon Harris Nuclear Power Plant.With 990211 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7801998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Shearon Harris Npp. with 990113 Ltr ML18016A7671998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Shnpp,Unit 1.With 981215 Ltr ML18016A9731998-11-28028 November 1998 Changes,Tests & Experiments, for Harris Nuclear Plant.Rept Provides Brief Description of Changes to Facility & Summary & of SE for Each Item That Was Implemented Under 10CFR50.59 Between 970608-981128.With 990527 Ltr ML18016A8351998-11-28028 November 1998 ISI Summary 8th Refueling Outage for Shearon Harris Power Plant,Unit 1. ML18016A7411998-11-25025 November 1998 Rev 1 to Shnpp Cycle 9 Colr. ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A7071998-11-0303 November 1998 Rev 0 to Harris Unit 1 Cycle 9 Colr. ML18016A7201998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Shearon Harris Nuclear Power Plant.With 981113 Ltr ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves ML18016A6201998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Harris Nuclear Power Plant.With 981012 Ltr ML18016A5971998-09-21021 September 1998 Rev 1 to Harris Unit 1 Cycle 8 Colr. ML18016A5881998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Shnpp,Unit 1.With 980914 Ltr ML18016A5071998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Shearon Harris Nuclear Plant.W/980811 Ltr ML18016A9431998-07-0707 July 1998 Rev 1 to QAP Manual. ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A9371998-06-30030 June 1998 Technical Rept on Matl Identification of Spent Fuel Piping Welds at Hnp. ML18016A4861998-06-30030 June 1998 Monthly Operating Rept for June 1998 for SHNPP.W/980715 Ltr ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18016A4521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Shearon Harris Nuclear Power Plant.W/980612 Ltr ML18016A7711998-05-26026 May 1998 Non-proprietary Rev 2 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris Spent Fuel Pools 'C' & 'D'. 1999-09-30
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I \
- Ac CE~ RATED D1SlBUTJ 0> DE M 04 STR+04 SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8903160060 DOC.DATE: 89/03/09 NOTARIZED- NO DOCKET I FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH. NAME AUTHOR AFFILIATION LEW,G.T; Carolina Power & Light Co.
WATSON,R.A. Carolina Power & Light. Co.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 89-004-00:on 890207,reactor trip/turbine trip on loss of condenser vacuum caused by loss of CCW circulation pumps.
W/8 ltr.
DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR ( ENCL SIZE:
TITLE: 50.73 Licensee Event Report (LER), Incident Rpt,Qetc.
NOTES:Application for permit renewal filed. 05000400/
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-1 LA 1 1 PD2-1 PD 1 1 BECKER, D 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 ARM/DCTS/DAB 1 1 DEDRO 1 1 ~
NRR/DEST/ADE 8H 1 1 NRR/DEST/ADS 7E 1 0 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/QAB 10 1 1 NRR/DOEA/EAB 11 1 1 NRR/DREP/RAB 10 1 1 NRR/DREP/RPB 10 2 2 RR/iggIS/SIB 9A 1 1 NUDOCS-ABSTRACT 1 1 REG FZQE~ 02 1 1 RES/DS IR/EIB 1 1 WSgDSR/PRAB 1 1 RGN2 FILE 01 1 1 EXTERNAL EG&G WILLIAMSI S 4 4 FORD BLDG HOY,A 1 1 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 S D
NCTE 'IO ALL "RZDS" RECIPIENIS:
S PIZASE HELP US 'IO RECCE WASTE.'XNZACZ 'IHE DOCUMENI'ONSOL DESK, RCCM Pl-37 (EXT. 20079)
LISTS FOR
~ EZZKCNATE YOUR NAME PBCH DISTIGBUTXGN DOCUMEMI'S YOU DGN~T HEED!
TOTAL NUMBER OF COPIES REQUIRED: LTTR 45 ENCL 44
NAC Form 355 UA. NUCLEAR REOULATOAY COMMISSION (04L) I APPROVED OMB NO. 31504104 EXPIRES: Sl31lSS LICENSEE EVENT REPORT ILER)
FACILITY NAME (1) DOCKET NUMBER (2) PAOE 3 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 0 5 0 0 04 0 0 1 OFO 6 REACTOR TRIP/TURBINE TRIP ON LOSS OF CONDENSER VACUUM CAUSED BY LOSS OF CONDENSOR COOLING WATER CIRCULATION PUMPS F VENT OAT E (Sl LER NUMBER (Sl REPORT DATE (7) OTHER FACILITIES INVOLVED (5)
MONTH OAY YEAR YEAR SEOUENTIAL &WE NUMBER RE~
NUMBER MONTH OAY YEAR FACILITYNAMES DOCKET NUMBER(S) 0 5 0 0 0 0 2 0 7 89 89 0 0 4 0 003 0 9 8 9 0 6 0 0 0 OPERATINO THIS REPORT IS SUBMITTED PURSUANT To THE AEQUIREMENTs oF 10 cFR ()r fcrrrc4 onr of mare of thr follorffnp) (11)
MODE (0) 20.402(bl 20.405(c) 50.73(e)(2)(lr) 73.71(b)
POWER 20AOS( ~ ) (1)(II SOM(cl (1) 50.73(e) 12)(rl 73.71(c)
LEVEI.
HO) 0 4 7 20.405(e) (I )(Q) 50.35(c) (2) 50,73(e) I 2) (rII) oTHER lsprclfy ln Aotrrct or/ore end In Text, NRC Form 20.405( ~ l(1)()Ill 50.73(e) (2)(l) 50.73(e)(2)(rllll(A) 388A) 20AOS(e)(1)(lr) 50.7 3(e) (2) (5 l 50.73( ~ l(2)(rIII)(Bl r', ..,c@ . g 20.405(e)(1)(rl 50.73(e) (2) (IIII 50.73( ~ l(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
NAME TEI.EPHONE NUMBER AREA CODE G. T. LEW PROJECT ENGINEER REGULATORY COMPLIANCE COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OESCAIBEO IN THIS AEPOAT (13)
'ijv'N' 'x:p xoyXc'cc CAUSE SYSTEM COMPONENT MANUFAC TUAER EPOATABLE TO NPADS CAUSE SYSTEM COMPONENT MANUFAC.
TUAER K 'PORTABLE TO NPRDS h lx y K K' MR A 62 5 N:<% Irm S SUPPLEMENTAL REPORT EXPECf ED (14) MONTH DAY YEAR EXPECTED SUBMISSION DATE (15)
YES llfyrr, complete EXPECTED SV84(ISSION DATE) No ABSTRACT (Limit to 1400 tpecer, l A, rpproxlmerrly flfrrrn tlnpfeepece typewritten linerl (15)
The plant was operating in Mode 1, Power Operation, with Main Feedwater Train "B" in service at 47X reactor power. At 1055 on February 7, 1989, the sudden loss of all three Circulating Water Pumps (CWPs) resulted in the loss of all flow to the Main Condenser. The plant tripped at 1058 as a result of a sudden loss of vacuum in the Main Condenser. The Low Pressure Turbine Rupture Disks ruptured as designed, a result of the loss of vacuum in the Main Condenser.
The Auxiliary Feedwater System actuated subsequent to the reactor trip as a result of trip of the only operating Main Feedwater Pump. Main Steam isolation valves were closed to limit plant cooldown and the plant stabilized in Hot Standby (Mode 3).
This event was caused by air entering the CWP's Seal Water System and causing the pumps to trip on loss of seal flow. Air entered the Seal Water System due to a failure in the level control system for the Potable Water Hydropneumatic Tank.
Corrective actions included repairing failed components in the Potable Water System, replacing the rupture disks for the turbine, identifying additional modifications for the Seal Water System and the Potable Water System.
There was no impact on plant safety. All systems functioned as expected.
This event is reported in accordance with 10CFR50.73(a)(2)(iv) as an Engineered Safety Feature actuation and a reactor protection system actuation.
- B9031C 00(' 890309 Z.5~~ I
]
PDR ADOCK 0 000400 NI (0
PDC
NRC Sorm 388A US. NUCLEAR REOULATORY COMMISSION (0831 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OMB NO. 3150M(CO EXPIRES: 8/31/88 SACILITY NAME (Il OOCKET NUMBER (11 LER NUMBER (51 PACE (31 YEAR :(~D> SEQVENTI*L -j) RSV>>ION NVM ER NVM OR SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 OF
//I'morpho>>ce 0 5 0 0 0 TEXT N reevke4 coo o(BOo>>////IC fcem 388AB/(17(
DESCRIPTION:
On February 7, 1989, the plant was operating in Mode 1, Power Operation, at 47X reactor power. Rod Control was in manual and Main Feedwater Train "B" (EIIS:SJ) was in service. Repairs to the Main Feedwater Pump "A" were in progress (refer to LER 89-03 for details).
EVENT:
At about 1030 the "CIRC WTR PUMP (EIIS:KB) A BEARING COOLING WATER LOW FLOW" Alarm was received in the Main Control Room. An operator was dispatched to investigate and check the pump valve line up. At about the same time, personnel in the Radwaste Control Room were investigating reports of air in the Potable Water (PW) System (EIIS:KK).
At 1055 all three Circulating Water Pumps (CWPs) tripped within 9 seconds of each other on low bearing water flow. Condenser (EIIS:SG) pressure began to increase and the operators started a turbine (EIIS:TA) runback at 40 MW per minute. Condenser Vacuum Pumps (EIIS:SH) subsequently tripped (probably due to high discharge temperatures) and were restarted several times over the next few minutes. The trip of the CWPs resulted in decreasing efficiency of the secondary plant. As a result, reactor power began to increase because the turbine was demanding increasing amounts of steam to maintain the selected turbine load.
At 1055:36 CWP."A" was restarted; a start attempt could not be performed until the pump's discharge valve was fully shut from the previous pump trip. The pump ran for only about one minute before tripping on low bearing water flow. An attempt was also made to start CWP "C", but an interlock prevented its start until 60 seconds after the CWP "A" starts Direction was given by the Shift Foreman to monitor condenser vacuum closely and to manually trip the plant when the Turbine Low Vacuum pretrip annunciator was received. The Shift Foreman also dispatched an operator to locally monitor vacuum from the gages located on the turbine's front standard and provide reports to the Main Control Room via radio.
At 1057:45. CWP "C" was started but this action was too late to avoid a plant trip. The turbine tripped automatically on low vacuum moments after the pretrip annunciator was received. The turbine trip was followed by an automatic reactor trip since reactor power was greater than the P-10 permissive of 10K. The Low Pressure Turbine Rupture Disks ruptured as a result of the rapid and sustained loss of circulating water flow and increasing condenser pressure. The plant responded to the trip as expected.
Main Feedwater Pump "B" tripped on low flow when the Main Feed Regulating Valves (EIIS:SJ) shut and the Auxiliary Feedwater System (EIIS:BA) subsequently actuated as required. Main Steam Isolation Valves (EIIS:SB) were NRC SORM 3OOA *U.S.GPO:10850824 538/455 (0831
NRC Form 358A UA. NUCLEAR REOULATORY COMMISSION (0431 LICENSEE EVENT REI5ORT ILER) TEXT CONTINUATION APPROVEO OMS NO. 3)50W104 EXPIRES: 8/31/88 FACILITY NAME 111 OOCKET NUMSER (1) LER NUMSER (8) PACE IS)
CCOVCNTIAL r)cvrcroN YEAR jj~ NVM CII .I NUM cn SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 OF 0 5 0 0 0 TEXT II!more 4/rece/4 /I)r/kraf, ore eO//R/One/I HRC %%drrn JRLCS/ 117)
EVENT: (continued) shut to limit plant cooldown. The turbine rupture disks were replaced. After completing the other repairs and calibrations discussed under cause, the plant was restarted and returned to service at 2204 on February 8, 1989.
CAUSE:
The initial plant design used the Potable Water System to provide seal and bearing water flow for starting a CWP. This flow was to satisfy an 11 gpm start permissive interlock. The CWP discharge is used to provide sufficient flow during normal operation (refer to attached drawing). The pump design included a trip when this seal water flow decreased below 6 gpm. The absence of 11 gpm also actuated a Main Control Board annunciator.
Historically, the design provided a marginal amount of seal flow. In 1988, it was documented that the flow available to satisfy the start permissive was marginal and often required jumpers to satisfy the start logic'. Local verification of the flow rates . was done during pump starts. 'he flow available from the CWP "A" and "B" discharge, was not adequate to keep the low flow annunciator out during normal operation. The potable water valves were throttled to clear these annunciators. This led to the situation where the CWPs operation was dependent on successful operation of the PW System.
Air binding of the PW System occurred on the morning of February 7 when a timing switch (Autocon Industries Part Number 56471300) in the Hydropneumatic Tank (EIIS:KK) level control circuit failed. The failure would not allow the Hydropneumatic Tank makeup pumps to start and supply makeup water to the Hydropneumatic Tank. Tank pressure is maintained at 35 to 60 psig by an air supply regulator that. is independent of the level control system. When the level control system failed, the air supply system kept pressure at the design point. As all the water was used up, air was introduced into the entire PW System including the CWP Seal System.
The indication available to the operators, system pressure, was normal throughout the event. There is no sight glass for the tank to assess adequate level. The first indication that the system was being filled with air came from other personnel in the plant.
While CWP "C" was not tied to the PW System, the seal flow is dependent on the discharge pressure of CWP "CNC All three pumps are cross tied via a common discharge block. There are no discharge check valves for these pumps. Each CWP has a motor operated butterfly valve which must close to prevent recirculation of flow through an idle pump. It was determined that CWP "C" tripped during the time when the discharge valves for CWPs "A" and "B" were going closed. During this time interval, the CWP "C" discharge pressure was too low to maintain its required seal flow because its flow was recirculating through CWP "A" and "B" NRC FORM SCCA n U.S.OPO:10884) 824 538/455 1083)
.~
NRC form 344A US. NUCLEAR REOULATORY COMMISSION (8431 LICENSEE EVENT REPORT ILER) TEXT CONTINUATION tVrfROVED OMB NO, 3(50&(04 EXPIRES: 8/31/88 fACILITYNAME Ol DOCKET NUMBER (3) LER NUMBER (41 ~ AOE (31 IE7Ã SEOVSNTIAL ~Q ASVISION SHEARON HARRIS NUCLEAR POWER PLANT yEAR ~a NVM 4ll o4. NVMSSII UNIT 1 o s o o o 400 89 0 04 0 0 0 4 oF 0 6 TEXT //I moro ofooo*rff/rorS uro I/4/orN////IC fomr 3//SAS/ (17(
CAUSE: (continued)
Subsequent to the plant trip, the accuracy of the Main Control Board indicators for condenser vacuum, local indicators for. condenser vacuum and the calibration of the pressure switches for the low condenser vacuum turbine trip were investigated. The investigation found that there were significant errors in these devices. The errors were such that the operators'ecision to trip the plant upon receipt of the pretrip annunciator, resulted in an automatic trip and rupture of the low pressure turbine rupture disks. However, these instrument errors would not have prevented the plant trip.
The cause for the error of the Main Control Board gages is that the instrument tubing from the condenser to the pressure transmitters is sloped such that moisture is trapped. This causes inaccurate readings and slow gage response. Experience had shown that the pressure transmitters and instrument tubing had to be drained every few hours to obtain reasonable readings. This problem had been identified in mid 1987. An effort to establish a formal program for conducting the draining was initiated in January 1989, but was not in effect.
r The investigation also revealed that all four low vacuum pressure switches had drifted out of calibration and were recalibrated.. The required setpoint is 5 inhg (abs) and the actual switch settings were found to range from 5.5 to 8.7 in hg (abs). The pretrip annunciator is taken from one of these pressure switches. Its normal setting is 4 inhg (abs) and it was presumed to have also been out of calibration since its trip setpoint for the pressure trip had drifted to 7.9 inhg (abs).
ANALYSIS:
There were no safety consequences as a result of this event. All plant systems responded as expected.
The Low Pressure Turbine Rupture Disks are designed to rupture and protect the turbine during an event of this nature, A higher initial power level would not significantly change the course of event. The event would have been shorter and still resulted in a plant trip.
This is the first time the plant has experienced a rapid vacuum .loss caused by an abrupt loss of Circulating Water Flow. In 1987 debris from damaged cooling tower fill material caused a gradual loss of Circulating Water Flow through the Main Condenser and a trip of the condensate pumps due to high discharge temperature. This event resulted in a manual plant trip. Refer to LER 87-,021.
This event is being reported in accordance with 10CFR50.73(a)(2)(iv) as an Engineered Safety System Feature (EIIS:JE) and" Reactor Protection System (EIIS:JC) Actuation.
NRC SORM 344A oU.S.GPO:108%%34 538/455 (9431
NRC Form 355A US. NUCLEAR REOULATORY COMMISSION
$ 431 LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVED OMS NO. 3150&105 EXPIRES: d/31/N FACILITYNAME 111 DOCKET NUMEER 121 LER NUMEER Idl PACE (31 YEAR P(( 55OVCNTIAL NVM ~ II gg IIEVISION NVM dN SHEARON HARRIS NUCLEAR POWER PLANT UNIT l 0 6 0 0 0 OF TEXT ///II>>rd <<>>ro /5 rddo/r<<L I/od <<//h/or>>IHRC Forrrr 3//SAE/117l CORRECTIVE ACTION:
1 ~ The Hydropneumatic Tank (Potable Water) level control circuit was repaired.
- 2. Air was purged from *the Potable Water and Seal Water Systems and the systems returned to service.
3~ Plant Change Requests were issued to provide the operator with indication of Potable Water level in the Hydropneumatic Tank.
'I 4~ Initiated design action to evaluate the Seal Water Supply to the Circulating Water Pumps to provide for an adequate and reliable source of water.
5 ~ A Temporary Modification was installed to establish an air purge flow to prevent condensation in the instrument sensing line. The Temporary Modification will be evaluated for subsequent incorporation as perma'nent change.
- 6. Replaced the Low Pressure Turbine Rupture Disks.
7 Repaired and recalibrated vacuum gages that indicated or responded incorrectly.
NIIC SOIIM SddA o U.SGPO: I Odd.Od2d-d38/5dd 15431
COOL I HG TOY/ER PCV 9576 SER'/ICE AIR I PRO (55 10 60 p8lg) 1PY/29
,ARIOUS LS)
YARD P.V!.
SER'/ICES 1P')V~2 W TOOTHEP. C. 0/. PUl"IPS kIYDROP tlEUt'IATIC TANK (6000 gal. POTABLE "/ATER) .
+ NOTE 5PY/1 Pl TYPICAL C. V'.
SEALS PUI"IP SEAL V/ATER ARRAHGt"IEHT BEARINGS .
SOURCE OF PUI IP FROI"I TRIP SIGNAL klYPOC HLOPI HATORS TO E 5, E CENTER FROt"I PUf"IP SYSTEH DESANDER DISCHARGE
" INTE: VALVES FOR PUI"IPS 'A'HD 4- Vi'ATER TREATI"IEHT BUI LDI tlG
'B'ARTIALLYOPEN TO t'IAI STAIN I'IltIIII'IUI1 SEAL C IRCULATII'!GWATER PUI'IPS AHD BEARING 9/ATER FLO'A'.
SEAL WATER SUPPL'( LER 89-004 Page 6 of 6
NAR 0 ~ $ S89 HARRIS NUCLEAR PROJECT P.O. Box 165 New Hill, NC 27562 File Number.'SHF/10-13510C Letter Number: H0-890032 (0)
U.S. Nuclear Regulatory Commission ATTN: NRC Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 LICENSEE EVENT REPORT 89-004-00 Gentlemen.'n accordance with Title 10 to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted. This report fulfills the requirement for a written report within thirty (30) days of a reportable occurrence and is in accordance with the format set forth in NUREG-1022, September 1983.
Very truly yours, v~3 R. A. Watson Vice President Harris Nuclear Project DLT:msb Enclosure cc: Mr. R. A. Becker (NRR)
Mr. W. H. Bradford (NRC SHNPP)
Mr. S. D. Ebneter (NRC RII)
/r/
MEM/LER-89-004/1/OS1
NRC Document Control Desk Page 2 bcc'Mr. R. H. Bassett Mr. C. H. Moseley, Jr.
Mr R. M. Coats Mr. W. R. Ponder Mri Jo M. Collins Mr. A. W. Powell Mr. C. W. Crawford Mr. C. E. Rose Mr. A. B. Cutter Mr. J. R. Sipp Mr. G. L. Forehand Mr. A. L. Stanley Mri C. R. Gibson Mr. D. L. Tibbitts Mrs J. G. Hammond Mr. R. B. Van Metre Mr. J. L. Harness Mr. D. C. Whitehead Mr M. D. Hill Mr, R. L. Winkler Mr. C. S. Hinnant INPO Mr. J. B. Hudson SHEEC Training Mr L. I. Loflin Reference Library Mr. R. E. Morgan SHNPP Reg. Compliance (2)
Mr. T. C. Morton NLS File: H-X-0523 Day File MEM/LER-89-004/2/OS1