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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20202J0181999-02-0303 February 1999 SER Accepting Changes in Quality Assurance Program,Which Continues to Meet Requirements of App B to 10CFR50 ML20202J1161999-02-0101 February 1999 SER Accepting Relief Requests Associated with Second 10-year Interval Inservice Testing Program ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves ML20153F9871998-09-17017 September 1998 Safety Evaluation Accepting 980225 Proposed Rev 26 to Illinois Power Nuclear Program Qam ML20237E3991998-08-27027 August 1998 SER Accepting Licensee Response to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode, for Clinton Power Station ML20237A1521998-08-0707 August 1998 SER Re Mgt Services Agreement at Clinton Power Station. Approval Under 10CFR50.80 Not Required ML20217H5771998-03-27027 March 1998 Safety Evaluation Concluding That No Significant Safety Hazards Introduced at CPS for Net 32% Ampacity Derating Factor for 1 H & 3 H Conduit Fire Barrier Sys & 1 H Cable Tray Fire Barrier Sys.Requests Response Addressing Issue ML20199F6751998-01-26026 January 1998 Safety Evaluation Accepting 971209 Proposed Change to CPS USAR Which Will Impact Commitments Made in CPS QAP Description ML20141K6321997-05-27027 May 1997 Safety Evaluation Accepting Relief Requests for Inservice Testing Program for Plant ML20135D1191996-12-0404 December 1996 Safety Evaluation of First Ten Year Interval Inservice Inspection Program Plan for Illinois Power Co,Clinton Power Station ML20149L7951996-11-12012 November 1996 Safety Evaluation Related to Licensee 960729 Requests for Relief from Requirements of Section XI of ASME Boiler & Pressure Vessel Code,1980 Edition Through Winter 1981 Addenda ML20116G8771992-10-29029 October 1992 Safety Evaluation Supporting Licensee Method of Coping W/Sbo Except W/Respect to Initial Room Temp Used in Control Room heat-up Calculation ML20059H0671990-08-24024 August 1990 SER Accepting Licensee Response to Generic Ltr 88-01, NRC Position on IGSCC in BWR Austentic Stainless Steel Piping, W/Exception of Licensee Position on Frequency of Leakage Monitoring ML20064A2611990-08-20020 August 1990 Generic SER Re Mark III Containment Hydrogen Control. Hydrogen Injection Rate Strongly Influenced by Background Gas Concentrations ML20246B6311989-08-17017 August 1989 Safety Evaluation Supporting Amend 25 to License NPF-62 ML20245F3471989-08-0404 August 1989 SER Accepting Util 841001,871118 & 880609 Responses to Generic Ltr 83-28,Item 2.1,Parts 1 & 2 Re Evaluation of Reactor Trip Sys Equipment Classification & Vendor Interface,Respectively ML20244D6351989-06-0707 June 1989 Safety Evaluation Supporting Licensee Response to Generic Ltr 83-28,Item 4.5.3 Re Reactor Trip Sys Reliability ML20247B8791989-05-15015 May 1989 Safety Evaluation Concluding That Licensee Combinatory Qualitative Event Analysis Adequately Addresses NRC Concerns Re Loss of Electric Power to nonsafety-related Control Sys ML20246C2301989-05-0303 May 1989 Safety Evaluation Accepting Uitl Response to Generic Ltr 83-28,Item 4.5.2 Re Periodic on-line Testing of Backup Scram Valves & Commitment to Test Backup Scram Valves Independently During Each Refueling Outage ML20244C5671989-04-10010 April 1989 Safety Evaluation Supporting Amend 21 to License NPF-62 ML20247E8831989-03-27027 March 1989 Safety Evaluation Supporting Amend 20 to License NPF-62 ML20206M5561988-11-21021 November 1988 Evaluation Concluding That Basis Provided by Licensee for Justifying Relief Requests for Replacement Parts Sufficient & Relief Requests 5003 & 5044 Acceptable.Licensee Should Certify Compliance W/Commitments When Replacements Complete ML20151N4701988-07-28028 July 1988 Safety Evaluation Supporting Rev to Position Re Nuclear Sys Protection Sys self-test Sys Failure Detection & Indication for Facility ML20147H7651988-03-0101 March 1988 Safety Evaluation Re First ten-year Interval Inservice Insp Program.Grants Relief from ASME Code Section XI Requirements for Requests 4002,4001 & 4003 & Denies Requests 5001 & 5002. Program Acceptable & in Compliance w/10CFR50.55a(g) ML20195G5461987-08-21021 August 1987 Safety Evaluation Accepting Proposed Util Tech Specs Change to Increase Max Allowed Enrichment of Reload Fuel to 4.2 Weight % U-235 ML20214F5641987-05-18018 May 1987 Safety Evaluation Supporting Util Compliance W/Atws Rule 10CFR50.62, Requirements for Reduction of Risk from ATWS Events for Light-Water-Cooled Nuclear Power Plants ML20137L7111986-01-22022 January 1986 Technical Evaluation Re HVAC Duct Work & Support Sys.Overall Structural Design of HVAC Sys Adequate & Provides Sufficient Margin of Safety to Failure Under Normal & DBA Conditions ML20138H1261985-10-18018 October 1985 Supplemental Safety Evaluation Accepting Use of Rev 2 to NCIG-01, Visual Weld Acceptance Criteria for Structural Welding at Nuclear Power Plants. Criteria Appropriate & Meet Requirements of GDC 1 to App a to 10CFR50 ML20137G7181985-06-30030 June 1985 Safety Evaluation Accepting Util Request for Elimination of Arbitrary Intermediate Breaks as Justified Deviation from Section 3.6.2 of SRP ML20204F6171981-11-0303 November 1981 Safety Evaluation Supporting Amends 1,1,1 & 1 to Construction Permits CPPR-158,CPPR-159,CPPR-160 & CPPR-161, Respectively 1999-02-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr U-603277, Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With ML18017A9151999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Shearon Harris Npp. with 991012 Ltr ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18017A8621999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Harris Nuclear Plant.With 990908 Ltr U-603267, Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18017A8361999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Shearon Harris Nuclear Power Plant.With 990811 Ltr U-603245, Monthly Operating Rept for Jul 1999 for CPS Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for Jul 1999 for CPS Unit 1.With ML20211C9621999-07-26026 July 1999 ISI Summary Rept U-603232, Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted1999-07-0909 July 1999 Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted ML18016B0151999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Shearon Harris Npp. with 990713 Ltr U-603233, Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9851999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990614 Ltr U-603222, Monthly Operating Rept for May 1999 for Clinton Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Clinton Power Station.With ML18017A8981999-05-12012 May 1999 Technical Rept Entitled, Harris Nuclear Plant-Bacteria Detection in Water from C&D Spent Fuel Pool Cooling Lines. ML20210K8391999-05-11011 May 1999 British Energy Annual Rept & Accounts 1998-99 ML20206H1231999-05-0505 May 1999 Illinois Power Co CPS Main CR Simulator Certification Rept ML18016A9581999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990513 Ltr U-603210, Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With U-603204, Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR211999-04-30030 April 1999 Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR21 ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8941999-04-0505 April 1999 Revised Pages 20-25 to App 4A of non-proprietary Version of Rev 3 to HI-971760 ML18016A9101999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Shearon Harris Nuclear Power Plant.With 990413 Ltr ML18016A8661999-03-31031 March 1999 Shnpp Operator Training Simulator,Simulator Certification Quadrennial Rept. U-603192, Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With U-603182, Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue1999-03-12012 March 1999 Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue ML18017A8931999-02-28028 February 1999 Risks & Alternative Options Associated with Spent Fuel Storage at Shearon Harris Nuclear Power Plant. U-603176, Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With ML18016A8551999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Shearon Harris Npp. with 990312 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8531999-02-18018 February 1999 Non-proprietary Rev 3 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris SFP 'C' & 'D'. ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML20207F2031999-02-10010 February 1999 Rev 1 to CPS COLR for Reload 6 Cycle 7 ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18022B0631999-02-0404 February 1999 Rev 0 to Nuclear NDE Manual. with 28 Oversize Uncodable Drawings of Alternative Plan Scope & 4 Oversize Codable Drawings ML20202J0181999-02-0303 February 1999 SER Accepting Changes in Quality Assurance Program,Which Continues to Meet Requirements of App B to 10CFR50 ML20202J1161999-02-0101 February 1999 SER Accepting Relief Requests Associated with Second 10-year Interval Inservice Testing Program ML18016A8041999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Shearon Harris Nuclear Power Plant.With 990211 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7801998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Shearon Harris Npp. with 990113 Ltr U-603223, Illinova Corp 1998 Annual Rept. with1998-12-31031 December 1998 Illinova Corp 1998 Annual Rept. with U-603144, Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With U-603115, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components1998-12-0404 December 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components 1999-09-30
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~. .._-m _. _ _ _ _ . . . _ _ _ _ _ _ _ . . _ - _ - __ _ . _ _ . _
f **%1 UNITED STATES i
y g j NUCLEAR REGULATORY COMMISSION o WASHINGTON, D.C. 30896-0001
- SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION INSERVICE TESTING PROGRAM RELIEF REQUEST ILLINOIS POWER COMPANY CLINTON POWER STATION
' NCKET NO. 50-461 1
INTRODUCTION The Code of Federal Regulations,10 CFR 50.55a, requires that inservice testing (IST) of certain ASME Code Class 1,2, and 3 pumps and valves be performed in accordance with Section XI of the ASME Boiler and Pressure Vessel Code and applicable addenda, except where relief has been requested and granted or proposed altematives have been authorized by
' the Commission pursuant to 10 CFR 50.55a (f)(6)(i), (a)(3)(i), or (a)(3)(ii). In order to obtain 4 authorization or relief, the licensee must demonstrate that: (1) conformance is impractical for its facility; (2) the proposed attemative provides an acceptable level of quality and safety; or (3) compliance would result in a hardship or unusual difficulty without a compensating increase in 4
the level of quality and safety. Section 50.55a'(f)(4)(iv) provides that inservice tests of pumps l and valves may meet the requirements set forth in subsequent editions and addenda that are incorporated by reference in 10 CFR 50.55a(b), subject to the limitations and modifications listed, and subject to Commission approval. NRC guidar,ce contained i. Generic Letter (GL) 89-04, " Guidance on Developing Acceptable Inservice Testing Programs," provided attematives to the Code requirements determined to be acceptable to the staff and authorized the use of the alternatives in Positions 1,2,6,7,9, and 10 provided the licensee follow the guidance delineated in the applicable position. When an attemative is proposed which is in accordance with GL 89-04 guidance and is documented in the IST program, no further evaluation is required; however, implementation of the altemative is subject to NRC inspection.
l
- Section 50.55a authorizes the Commission to grant relief from ASME Code requirements or to approve proposed altematives upon making the necessary findings. The NRC staffs findings
'. with respect to granting or not granting the relief requested or authorizing the proposed attemative as part of the licensee's IST program are contained in this Safety Evaluation (SE).
This relief request references the first 10-year interval for the Clinton Power Station (CPS),
stating that the IST program is based on the 1980 edition through Winter 1981 addenda of
- - ASME Section XI. CPS had implemented the requirements of OMa-1988, Part 10, Section
! 4.2.2.3 for leak rate testing of Category A valves in accordance with the guidance in NUREG-l 1482. The licensee's relief request was transmitted to the staff in a letter dated Jrne 18,1998, and supplemented by a letter dated September 4,1998.
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s 2 Relief Recuejil The licensee has requested relief from the requirements of OMa-1983, Part 10, Section 4.2.2.3.
This section defines the frequency for leak rate testing of Category A valves. A one-time extension of the 2-year test interval is requested for leak rate testing of the 21 valves listed below; 1E12-F008 1E12-F009 1E12-F023 1E12-F041 A 1E12-F0418 1E12-F041C 1E12-F042A 1E12-F0428 1E12-F042C 1Ei2 F050A 1E12 F050B 1E12-F053A 1E12-F053B lE21-F005 1E21-F006 1E22-F004 1E22-F005 1E51-F013 1E51-F066 1821-F001 1821-F002 Relief is requested to extend the test interval for each valve until the next refueling outage.
Licensee's Basis for Reauestina Relief The licensee states:
As a result of the current extended outage, the 2.-yearlimit for some of the valves may be exceeded prior to plant startup. In any case, the limit will be exceeded for all of the valves before the next scheduled refueling outage. Extension of the test interval would preclude the necessity of testing the valves twice during the current outage and instead allow the next required test to be performed during the next refueling outage scheduled for CPS.
All of the valvas were tested with high pressure (1000 psig) water between October 29, 1996, and January 28,1997. CPS has been in Mode 4 (cold shutdown) or Mode 5 (refueling) since before this testing was performed. Thus, the valves have not been exposed to operating conditions or the typical degradation pr.ocesses associated with a cycle of operation. Therefore, little additional as-surance of these valves' ability to perform their leakage safety functicn would be gained by reperformance at this time.
Reperformance of these tests at this time places an additional burden on CPS with no compensating increase in the level of quality and safety. Nearly all of these valves are located in high radiation areas, and therefore, leak testing these valves again would result in unnecessary radiation exposure for test personnel. In addition to the time required for test preparation, valve lineups, equipment setup, test performance, and post-test restoration, testing of several of these valves would require significant manipulations of plant equipment, including removal of the drywe:1 head.
3 i 3 Altemative Testino Some of the 21 pressure isolation valves are also containment isolation valves. As such, these valves will be leak rate tested in accordance with the requirements of 10 CFR 50, Appendix J (Type C test) prior tc startup, using air at 9.0 psig as the test medium. The following valves are included:
i 1E12 F008 1E12-F009 1E12-F023 1E12-F042A 1E12 F042B 1E12-F042C 1E12-F053A 1E12-F053B 1E21-F005 1E22-F004 1E51-F013 l
The frequency for performing high pressure water tests of the containment isolation valves will '
return to once per refueling outage after completion of testing during the next refueling outage, 1 which will occur approximately 18 months after startup from the current plant shutdown. _
EVALUATION Pressure isolation valves (PlVs) are defined as two normally closed valves in series that function to isolate the reactor coolant system from an attached low pressure system. Valves ,
J' which are defined as conta!nment isolation valves, have additional safety functions for isolation l or functioning of s. system such as emergency core cooling, or train separation of a safety system to prevent diversion of flow. The Code requires that these Category A valves be seat-leakage tested at a frequency of once every 2 years. i l
Six of the valves for which relief is requested (1E12-F008,1E12-F009,1E12-F050A,1E12- I '
, F053A,1E12 F050B,1E12-F0538) are required for establishing the residual heat removal shutdown cooling (SDC) mode. When testing these valves, the normal method for SDC is lost.
An alternate method to remove decay heat is the use of the reactor water cleanup system. This system is powered from a non-safety auxiliary power bus.
Currently, the licensee is performing maintenance activities in the switchyard. With the .
resulting breaker configuration, an e'setrical anomaly on the transmission line would cause the 4160 volt and 6900 voit non-safety buses to be lost. The loss of non-safety buses would cause a loss of the reactor water cleanup system which, if it was in service as the decay heat removal system, would result in a loss of SDC. Loss of decay heat removal capability represents an unnecessary nsk to the plant.
The valves 1E51-F013 and 1E51-F066 are located on the reactor head spray piping.1821-F001 and 1821-F002 are on the reactor vessel head vent line to the drywell.1E12-F023 is a !
. connection from the B train of residual heat removal to the reactor core isolation cooling system. Testing of these valves would involve removal of the drywell head and disassembly of the reactor vessel head spray and vent piping. The estimated dose that would be received by licensee personne! in performance of these tests is significant.
l The remaining valves,1E12-F041A,1E12-F042A,1Ef 2-F0418,1E12-F042B,1E12-F041C, 1E12-F042C,1E21-F005,1E21-F006,1E22-F004, and 1E22-F005, are located on the injection lines of the five emergency core cooling systems. These valves serve as the injection lira motor-operated shutoff valves and check valves.
f_,...
k 4 All of the valves for which the licensee requests relic f have successfully passed their Category A tests which were performed near the beginning of the extended outage. Since that time, they have not been irs service at normal operating temperature or pressure. All of the valves, with the exception of 1821-F001 and 1821-F002, are constructed from carbon steel with stellite seat rings and discs.1821-F001 and 1821-F002 have hard faced seats and discs made of cobalt based alloy A567. These materials are corrosion resistant. The materials of construction combined with the valves not being exposed to ncrmal deDradation processes provides sufficient assurance of their operational readiness.
Results from the past six leak rate tests performed on the valves were provided. All the measured leakage values were well below acceptance criteria of 5 gpm with the exception of the latest test of valve 1E12-F0538. However,1E12-F053B also serves as a containment isolation valve and therefore will undergo Appendix J testing prior to startup. Minimalleakage
, during Appendix J testing would provide reasonable assurance of the valve's operational
- readiness.
Compliance with the Code would result in hardship without a compensating increase in safety.
Reasonable assurance exists of the operational readiness of the valves due to their materials of construction, their testing history, and the fact that they have not been exposed to normal
, degradation processes associated with power operation. Therefore, the licensee is authorized to defer testing until the next refueling outage.
. CONCLUSION On the basis of the above evaluation. re staff concludes that the proposed alternative to the '
requirements of OMa-1988, Part 10, Section 4.2.2.3 for the 21 Category A reactor coolant system pressure isolation valves is authorized pursuant to 10 CFR 50.55a (a)(3)(ii) based on the determination that compliance with the specified requirementsfesults in a hardship without a compensating increase in the level of quality and safety. The alternative is authorized for an interim period from the date of the SE until the end of the 7th refueling outage.
Principal Contribuior: M. Kotzalas .
Date: October 6, 1998