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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:RO)
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A9151999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Shearon Harris Npp. with 991012 Ltr ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18017A8621999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Harris Nuclear Plant.With 990908 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18017A8361999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Shearon Harris Nuclear Power Plant.With 990811 Ltr ML18016B0151999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Shearon Harris Npp. with 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9851999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990614 Ltr ML18017A8981999-05-12012 May 1999 Technical Rept Entitled, Harris Nuclear Plant-Bacteria Detection in Water from C&D Spent Fuel Pool Cooling Lines. ML18016A9581999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990513 Ltr ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8941999-04-0505 April 1999 Revised Pages 20-25 to App 4A of non-proprietary Version of Rev 3 to HI-971760 ML18016A9101999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Shearon Harris Nuclear Power Plant.With 990413 Ltr ML18016A8661999-03-31031 March 1999 Shnpp Operator Training Simulator,Simulator Certification Quadrennial Rept. ML18017A8931999-02-28028 February 1999 Risks & Alternative Options Associated with Spent Fuel Storage at Shearon Harris Nuclear Power Plant. ML18016A8551999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Shearon Harris Npp. with 990312 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8531999-02-18018 February 1999 Non-proprietary Rev 3 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris SFP 'C' & 'D'. ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18022B0631999-02-0404 February 1999 Rev 0 to Nuclear NDE Manual. with 28 Oversize Uncodable Drawings of Alternative Plan Scope & 4 Oversize Codable Drawings ML20202J1161999-02-0101 February 1999 SER Accepting Relief Requests Associated with Second 10-year Interval Inservice Testing Program ML18016A8041999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Shearon Harris Nuclear Power Plant.With 990211 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7801998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Shearon Harris Npp. with 990113 Ltr ML18016A7671998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Shnpp,Unit 1.With 981215 Ltr ML18016A9731998-11-28028 November 1998 Changes,Tests & Experiments, for Harris Nuclear Plant.Rept Provides Brief Description of Changes to Facility & Summary & of SE for Each Item That Was Implemented Under 10CFR50.59 Between 970608-981128.With 990527 Ltr ML18016A8351998-11-28028 November 1998 ISI Summary 8th Refueling Outage for Shearon Harris Power Plant,Unit 1. ML18016A7411998-11-25025 November 1998 Rev 1 to Shnpp Cycle 9 Colr. ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A7071998-11-0303 November 1998 Rev 0 to Harris Unit 1 Cycle 9 Colr. ML18016A7201998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Shearon Harris Nuclear Power Plant.With 981113 Ltr ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves ML18016A6201998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Harris Nuclear Power Plant.With 981012 Ltr ML18016A5971998-09-21021 September 1998 Rev 1 to Harris Unit 1 Cycle 8 Colr. ML18016A5881998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Shnpp,Unit 1.With 980914 Ltr ML18016A5071998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Shearon Harris Nuclear Plant.W/980811 Ltr ML18016A9431998-07-0707 July 1998 Rev 1 to QAP Manual. ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A9371998-06-30030 June 1998 Technical Rept on Matl Identification of Spent Fuel Piping Welds at Hnp. ML18016A4861998-06-30030 June 1998 Monthly Operating Rept for June 1998 for SHNPP.W/980715 Ltr ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18016A4521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Shearon Harris Nuclear Power Plant.W/980612 Ltr ML18016A7711998-05-26026 May 1998 Non-proprietary Rev 2 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris Spent Fuel Pools 'C' & 'D'. 1999-09-30
[Table view] |
Text
j.v.
'. ACCELERATED DISJ IBUTION DEMONSTR10N SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8804060126 DOC.DATE: 88/03/29 NOTARIZED: NO DOCKET FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH. NAME AUTHOR AFFILIATION HOWE,A. Carolina Power & Light Co.
WATSON,R.A. Carolina Power & Light Co.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 88-001-01:on 880115,emergency operating procedure deficiency for switchover to recirculation discovered.
W/8 DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR NCL SIZE:
TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:Application for permit renewal filed. 05000400 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL A PD2-.1 LA 1 1 PD2-1 PD 1 1 BUCKLEY,B 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 AEOD/DOA 1 1 AEOD/DSP/NAS 1 1 AEOD/DSP/ROAB 2 2. AEOD/DSP/TPAB 1 1 ARM/DCTS/DAB 1 1' DEDRO 1 1 NRR/DEST/ADS 7E 0 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB7A 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/HFB10D 1 1 NRR/DLPQ/QAB10A 1 1 NRR/DOEA/EAB11E 1 1 NRR/DREP/RAB10A 1 1 NRR/DREP/RPB10A 2 2
-D - SIB9A1 1 1 NRR/PMAS/ILRB12 1 1 G 02 1 1 RES TELFORD,J 1 1 RES/DE/EIB 1 1 RES/DRPS DIR 1 1 RGN2 FILE 01 1 1 EXTERNAL EG&G GROHi M 4 FORD BLDG HOY,A 1 1 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC HARRIS,J 1 1 NSIC MAYS,G 1 1 8
A D
TOTAL NUMBER OF COPIES REQUIRED: LTTR 45 ENCL 44
NRC Forml388 U.S. NUCLEAR REQULATOAY COMMISSION
'94)3) APPAOVED OMB NO. 31604104 EXPIRES: 8/31/88 LICENSEE EVENT REPORT (LER)
FACILITY NAME (1) DOCKET NUMBER (2) PA E 3 SHEARON HARRIS NUCLEAR POWER PLANT UNIT ONE o 5 o o o4O ioFo6 EMERGENCY OPERATING PROCEDURE DEFICIENCY FOR SWITCHOVER TO RECIRCULATION AFTER A EVENT DATE (5) LER NUMBER (8) REPOAT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR Pgg: SEQUENTIAL ;S.'A'EYISKIN MONTH OAY YEAR FACILITYNAMES DOCKET,NUMBERISI xBr>>l NUMBER '<. 4 NUMBER 0 5 0 0 0 0 3 29 88 0 5 0 0 0 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 cFR (II ICheck onr or mott of thr follorflnpl (11(
OPERATINO MODE (8) 20.402(B) 20A06(c) 60.73(e) (2)Dv) 73.7)(B)
POWE R 20.406(e) l1) ll) 50M(c) (I ) 50.73(e) (2) (v) 73.71(c)
LEVEL (rill)(BI (10) 20A05(e) II)Dl) 50.38(c) (2) 60.73(e) (2)(v8) OTHER (Specify In Abstrect be/ore end In Text, HRC Form 20.406(e)(1) Dil) 50.73(e)(2) li) 60.73(e) (2) (rill)(AI 388AI 20A06(e)(1) I lv) 50.73(el (2) (8) 50,73 (e) (2)
>>rrrnr,'>> '4'N3>>>>>>v+>> 20.405(e)(1)(r) 50.73(e)(2) (IIII 50.73( ~ ) (2) (x)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE ANDREW HOWE SR. ENGINEER REGULATORY COMPLIANCE 919 362 2 719 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBEO IN THIS REPORT (13) 9' CAUSE SYSTEM COMPONENT MANUFAC.
TUAER REPORTABLE,':.
TO NPROS CAUSE SYSTEM COMPONENT MANUFAC.
TUAER EPORTA8 LE TO NPRDS INWIT PA%33('<
SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED SU 8 MISSION DATE (16)
YES (II yes, complrtr EXPECTED SUBhtlSSIDN DATEI No ABSTRACT It.imlt ro t400 sprees, I e., rppsoxlmetrly fiftrrn sinpleepece typervrittrn lines) (18)
On January 15, 1988, it was discovered that a procedure deficiency had previously existed in the Emergency Operating Procedures (EOPs) which could have resulted in the failure of the Emergency Core Cooling System (ECCS) during the recirculation phase of an accident, under a scenario of a single failure of one Residual Heat Removal Pump (RHRP). The deficiency involved an improper valve lineup which could cause a RHRP to exceed its design flow limit during ECCS recirculation, if one of the two RHRPs had failed during a loss of coolant accident (LOCA) leaving only one operating RHRP, and if the LOCA was sufficiently large to completely depressurize the Reactor Coolant System.
This procedure deficiency resulted from the failure to completely incorporate into plant procedures a change made to the Final Safety Analysis Report.
The deficiency existed beginning in December of 1986, when the EOP containing the error was approved, and initial operation of the plant began. When the safety significance of the discrepancy was discovered, the EOPs were revised to correct the error. This occurred on December 16, 1987.
Other FSAR changes made in this time period involving a change to procedures were reviewed to ensure they were properly implemented. Members of the Plant Nuclear Safety Committee have been advised of this situation and reminded of their responsibility regarding the reportability of such situations.
g(pZ2.
8804060126 Ii 05000400 880325'DR ADOCK 8 DCD
NRC Form ESSA V.S. NUCLEAR REOULATORY COMMISSION
($ 421 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVED OMS NO. 3(50&(04 EXPIRES: SI31/SS fACILITYNAME (11 DOCKET NUMSER (2l LER NVMSER LSI ~ AOE IS)
SHEARON HARRIS NUCLEAR POWER PLANT YE<<95 55QVENTIAL NVM ER R(vr5ION NVM 5R UNIT ONE OF 0 5 0 0 0 TEXT Ilfmoro N>>c>> II fffr(orE I>>f afrrR(N>>>>l IIRC Amr ~'fl (17(
DESCRIPTION:
Note'The following drawings supplement the narrative of this report:
Attachment A - ECCS Recirculation Flowpath Existing Prior to September 1986 Attachment B - ECCS Recirculation Flowpath Required in FSAR After September 1986 Attachment C ECCS Recirculation Flowpath Implemented in Procedures, December 1986 The switchover procedure for transferring the Emergency Core Cooling System (ECCS) from injection to recirculation is outlined in FSAR Table 6.3.2-6. The initial practice required closing isolation valves to separate the ECCS headers into two separate trains, thus providing protection for passive failures of the piping. The resulting valve lineup for recirculation is shown in Attachment A. On September 27, 1985, and on August 21, 1986, Westinghouse Electric Corporation, the Nuclear Steam Supply System designer for the Shearon Harris Nuclear Power Plant (SHNPP), issued letters (serial CQL-9018 and CQL-9445) to Ebasco Services, Inc., the architect/engineer for SHNPP. The letters documented recommendations for changes to the procedure described in FSAR Table 6.3.2-6 for the switchover. Westinghouse recommended deletion of the procedure steps which separated the two ECCS trains, since these steps did not provide complete passive failure protection, and since their elimination would allow a single RHRP to supply both CSIPs. In addition, the second correspondence identified the need for new check valves to be installed in the piping connecting the discharge of an RHRP to the CSIP suction, to prevent potential backflow through an idle RHRP during recirculation.
These proposed changes were approved for implementation at SHNPP, since they improved operational flexibility following an accident. In addition, a separate issue regarding requirements for local leak rate testing (LLRT) on ECCS containment penetrations was also resolved by implementing this proposed change.
NRCfORM 5454 *U S OPO:I SSS.DS24 SSSI455 NSSI
NRC form 30SA U.S. NUCLEAR REGULATORY COMMISSION (043)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OMS NO. 3150-0104 EXPIRES: 0/31/SS PACILITY NAME (1) OOCKET NUMBER LT) LER NUMSER (0) ~ AOE (31 SHEARON HARRIS NUCLEAR POWER PLANT YEAR SEQUENTIAL (
NVM E4 REVISION Q NVM E4 UNIT ONE o s o o o 400 88 001 0 1 0 3 oF0 6 TEXT /1/'moro <<oc>> /P nqvkrd, ver A//o)mo///RC Form 30143/ (17)
DESCRIPTION: (continued)
An FSAR change (serial HPOS"845) was initiated to incorporate these changes.
As part of the review of these changes, Technical Support determined that a single RHRP could not supply two CSIPs and both low pressure ECCS injection headers, as the proposed recirculation lineup required. However, by isolating one of the two low pressure safety injection (LPSI) header containment isolation valves, an acceptable configuration was created. This revised lineup demonstrated that the RHRP would not run out (Preoperational Test 2085-P-05, completed October 5, 1986). Therefore, the FSAR change included the new requirement to close one of the two LPSI containment isolation valves to ensure that runout of the RHRP would not occur during recirculation if the other RHRP failed.
This change was incorporated into the FSAR change which was approved on September 24, 1986. A letter was also submitted to the NRC describing this change.
The change required significant revisions be made to the EOPs; however, due to other commitments, revisions were already in progress. The additional changes required due to the FSAR change were not therefore formally identified and tracked. On December 22, 1986, Revision 2 to procedure EOP-EPP-010, Transfer to Cold Leg Recirculation, was issued. However, the revision did not fully implement the requirements of the FSAR in that the requirement to close one LPSI containment isolation valve, identified in FSAR change HPOS-845, was not included. The procedure change package references this FSAR change in its safety analysis, but the engineers developing the procedure revision were not fully cognizant of all the new requirements. h The SHNPP On-site Nuclear Safety (ONS) unit was responsible for the review of INPO Significant Event Reports (SER), and during review of SER 2-87, they identified the discrepancy between the FSAR and the EOPs. On July 10, 1987, an action item was established for the plant engineering department to evaluate the discrepancy to determine whether the procedure or the FSAR was inaccurate. On December 3, 1987, the engineering department confirmed the deficiency was in the EOPs.
NRC PORM 3OOA 4 U.S.OPO;1050 0 024 538/455 (043)
NRC FAIR 348A V.S. NVC( EAR REOVLATORY COMMISSION (04)3)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVED OMS NO, 3150&I 04 EXPIRES: 8/31/88 fACILITYNAME ll) DOCKET NUMSER (2) LER NUMSER (4) ~ AOE (3)
SEOVENTIAL REYIEION SHEARON HARRIS NUCLEAR POWER PLANT YEAR NVM ER NVM ER UNIT ONE 0 5 0 0 0 OF TEXT //m4m 4P444/I /44NPNL v44 A/4/444///RC Fo/m 38340) l)T)
DESCRIPTION: (continued)
Separately, Operations personnel noted that the Monitor Light Box (MLB) for ECCS recirculation was engraved to require one LPSI containment isolation valve to be close while the other was open. Believing this to be a simple engraving error, a Plant Change Request (PCR) (serial PCR-2384) was initiated on September 25, 1987, to change the engraving to require the valve to be open during recirculation, in agreement with the plant EOPs. The PCR was rejected by Technical Support personnel, since they were aware of the previous FSAR change requiring the valve to be closed to prevent RHR pump runout. The Operations engineer who initiated the PCR then wrote a feedback report (serial 305) in accordance with plant procedure OMM-001, Operations Conduct of Operations, on October 26, 1987. A procedure change was determined to be required, and was to be addressed in the next revision which was to be issued in the fall of 1988.
In both cases, personnel were not cognizant of the safety significance of the procedure deficiency.
However, when ONS received the response for INPO SER 2-87 from engineering on December 3, 1987, the ONS unit contacted Operations and made them aware of the serious nature of the deficiency. A change to procedure EOP-EPP-010 was issued on December 16, 1987, correcting the error and making the procedure consistent with the FSAR. In addition, procedure EOP-EPP-003, Loss of All AC Power Recovery with Safety Injection Required, which also addresses the recirculation lineup, was issued on January 6, 1988.
On January 15, 1988, this matter was discovered by Regulatory Compliance personnel. The situation existing for nearly one year in which the emergency operating procedures were in disagreement with the FSAR was investigated and determined to be reportable.
SAFETY SIGNIFICANCE:
The ECCS, and hence all procedures governing operation of this system, were required to be in place when the plant first entered Mode 4 in December of 1986, as per Technical Specification 3.5.3. In the event of a large break loss of coolant accident simultaneous with the single failure of an RHRP, when the recirculation phase of ECCS operation was initiated in accordance with plant procedures, the plant would have been in an unanalyzed condition'.
This conclusion was reached after a review of the significance of this event.
Technical Support and Engineering personnel reviewed the test data and evaluation that was done in 1986 which determined that one LPSI header must be isolated during recirculation. The result of this review confirmed that the earlier test did not demonstrate sufficient margin to allow flow to both LPSI headers during recirculation.
NRC FORM 344A 4 U.S.OPO:10884).824 838/488 IM3)
NRC PRIm 3SSA U.S. NUCLEAR REOULATORY COMMISSION
$ 43 l LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVEO OMB NO. 3150&I04 EXPIRES: 8/3l/88 PACILITY NAME ill OOCKET NUMBER l2l LER NUMBER ldl PACE l31 SHEARON HARRIS NUCLEAR POWER PLANT YEAR F<I. SEOVENTIAL :PII REV>>ION NVM ER NVM 44 UNIT ONE o so o o 40 088 001 0 1 OF TEXT // II>>m N>>4I /I IfEMPN/. vfr //I/444/I/RC P>>mI 3/4/A'4/ I17)
SAFETY SIGNIFICANCE: (continued)
The single operating RHRP could have exceeded its design flow limit under such a scenario, which would cause the RHRP to trip on overcurrent, subsequently causing the failure of the CSIPs, since these pumps rely on the RHRP as the source of water for recirculation operation. Operator action outside of plant procedures would have been required to recover the situation.
The following indications would have been available to the operator to alert him of the problem'.
Flow indication and alarms for the RHRP Motor amperage indication for 'the RHRP Alarms for the MLB due to the valve lineup error Alarm for the RHRP tripping Alarms for the CSIPs tripping It has been determined that restoration of a single RHRP without any operating CSIPs would be sufficient to ensure adequate post-LOCA cooling of the core, provided the flow is restored within approximately 3-4 minutes after interruption. The operator would have to reset the over current trip at the RHRP breaker, located one floor level below the control room, and restart the pump using the control switch.
The condition is reportable in accordance with 10CFR50.73(a)(2)(v) as a procedural error which could have prevented the fulfillment of the safety function of systems which mitigate the consequences of an accident.
CAUSE:
There is no single reason that this procedure deficiency came into existence, but the following contributed to the error.
- 1. Personnel responsible for the EOPs were aware of the Westinghouse proposals to revise the ECCS recirculation lineup, and when the FSAR was changed to implement this new lineup the additional requirement to close the LPSI isolation valve was not noted. The 'modification to close one of the two LPSI containment isolation valves affected only one page of a change package which was 32 pages in length, and the majority of this package discussed containment isolation valve design, not ECCS recirculation procedures.
NRC fORM $ 444 *U.S.OPO:1088&824 538'455 l843 I
1 U.S. NUCLEAR REOULATORY COMMISSION NRC Form 344A (94)3 I LICENSEE EVENT REPORT ILERI TEXT CONTINUATION APPROVED OMB NO, 3150&)(N EXPIRES: 8/31/88 FACILITYNAME (II DOCKET NUMBER l2) LER NUMBER (4) ~ AOE (3I YEAR SEQVENZIAL REVISION Pop SHEARON HARRIS NUCLEAR POWER PLANT NVMSER NVM ER UNIT ONE 0 8 8 0 10 106 OF 0 6 o s o o o 4 TExT ///more EPece /4 /e)/rkerL Ireo ~ //ooom/ /YRc Fonrr 3(ELi'e/ (17)
CAUSE: (continued)
- 2. Changes made to the FSAR, which would require changes to plant procedures, were not routinely identified and tracked prior to licensing of the plant due to the significant number of changes and due to the fact that procedures were being revised prior to initial use in preparation for the operation of the plant.
- 3. FSAR changes are not immediately made available in the copies of the FSAR, since updates are only required annually by regulations.
The discrepancy between the FSAR and EOPs was .identified by many groups during 1987. However, the technical issue as to which document was accurate was not obvious. Investigation of the discrepancy was not given appropriate urgency, given the potential consequences of the discrepancy. When the investigation was completed, the problem was corrected within a reasonable period of time, but the potential reportability of the situation was not identified.
No similar situations have previously occurred.
CORRECTIVE ACTIONS:
The EOPs were revised prior to the discovery of this situation.
I The events which led to this procedure deficiency occurred prior to licensing of the plant. Upon issuance of the operating license, many changes went into effect regarding how plant design changes are controlled:
Changes to the plant components which require a PCR receive a complete safety analysis in accordance with 10CFR50.59.
PCRs are reviewed by the appropriate units to determine the ,
impact on plant procedures for which they are responsible.
FSAR changes now follow, rather than precede, the changes made to the plant and/or procedures.
The following additional measures have been taken'.
Changes to the FSAR approved in 1986 have been reviewed to verify that those changes which alter procedures described in the FSAR were properly implemented in the plant. No similar situations were discovered.
Members of the Plant Nuclear Safety Committee have been informed of this event and reminded of their responsibility to ensure potentially reportable items are brought to the attention of management.
NRC SORM 344* *U.S.OPO:1988 0.524 538/455 l943)
LER 88-001-01 BIT ATTACHMENT A ECCS RECIRCULATION FLOVPATIL EXISTING PRIOR TO SEPTEMBER 1986 ffSl-COLD LEG 1B-SB HPSI-HGT LEG 1C-SAB INSIDE CONTAINMENT CONTAINMENT 1A-SA fPSI-RECIRCULATICN COLD LEG SUMPS CHARGING/Sl PUMP5 LPSI-COLD LEG 1B-SB LPSI-RHR PUMPS HOT LEG HX LPSI-OGLD LEG 1A-SA INSIDE CONTAINMENT
LER 88-001-01 ATTAC)IHENT B ECCS RECIRCULATION FLOMPATH II'Sl-REQUIRED IN FSAR AFTER COLD LES SEPTFJIBER 1986 1B-SB HPSI-HDT LEG 1C-SAB INSIDE CONTAINMENT 1A-SA CONTAINMENT RECIRCULATION IfSl-COLD LEB SUMPS CHARGI NGl S I PUMPS F
LPSI-COLDLES ISI-M1 1B-SB LPSI-HOT LEO RHR PUMPS LPSI-HX COLD LEO ISI-340 CONTAINMENT IA-SA INSIDE
LER 88-001-01 BIT ATTACIIHENT C ECCS RECIRCULATION FLOWPATH IHPLEHFNTED IN PROCEDURE, COLD LEB DECEHBER 1986 1B-SB HPSI-IIBT LEO lc-SAB INSIDE CONTAINMENT COIITAINHENT I A-SA 8'6l-RECIRCULATION COLD LEB SUt1PS CHARGl NG/S l PUMPS LPSI-COLD LEO IB-SB LPSI-HBT LEO RHR PUMPS LPSI-HX COLD LEO IA-SA INSIDE CONTAIIII1ENT
CARL Carolina Power 5 Light Company HARRIS NUCLEAR PROJECT P.O. Box 165 New Hill, NC 27562 Ooo File Number'. SHF/10-13510C Letter Number'HO-880080 (0)
U.S. Nuclear Regulatory Commission ATTN: NRC Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 LICENSEE EVENT REPORT 88-001-01 Gentlemen'.
In accordance with Title 10 to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted. The original report fulfills the requirement for a written report within thirty (30) days of a reportable occurrence and is in accordance with the format set forth in NUREG-1022, September, 1983.
Revision one provides additional information regarding the potential safety significance of the reported condition, based on further engineering evaluation.
Very truly yours, R. A. Watson Vice President Harris Nuclear Project MGW:ddl Enclosure cc'. Dr. J. Nelson Grace (NRC RII)
Mr. B. Buckley (NRR)
Mr. G. Maxwell (NRC SHNPP)
MEM/LER-88-001/1/OS1