ML13044A599

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IR 05000387-12-005, 05000388-12-005 10/01/2012 - 12/31/2012; Susquehanna Steam Electric Station, Units 1 and 2; Maintenance Effectiveness, Drill Evaluation, Problem Identification and Resolution, Follow-up of Events and Notices of Enforceme
ML13044A599
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 02/13/2013
From: Mel Gray
Reactor Projects Region 1 Branch 4
To: Rausch T
Susquehanna
GRAY, MEL
References
IR-12-005
Download: ML13044A599 (72)


See also: IR 05000387/2012005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

2100 RENAISSANCE BOULEVARD, SUITE 100

KING OF PRUSSIA, PENNSYLVANIA 19406-2713

February 13, 2013

Mr. Timothy S. Rausch

Senior Vice President and Chief Nuclear Officer

PPL Susquehanna, LLC

769 Salem Boulevard, NUCSB3

Berwick, PA 18603

SUBJECT: SUSQUEHANNA STEAM ELECTRIC STATION - NRC INTEGRATED

INSPECTION REPORT 05000387/2012005 AND 05000388/2012005

Dear Mr. Rausch:

On December 31, 2012, the U. S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Susquehanna Steam Electric Station (SSES) Units 1 and 2. The enclosed

inspection report (IR) presents the inspection results, which were discussed on January 25,

2013, with you and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents two NRC identified findings and one self-revealing finding of very low

safety significance (Green). Additionally, NRC inspectors identified two traditional enforcement

Severity Level IV violations. These findings were determined to involve violations of NRC

requirements. However, because of the very low safety significance and because all the

violations are entered into your correction action program (CAP), the NRC is treating the

findings as a non-cited violations (NCVs) consistent with Section 2.3.2 of the NRCs

Enforcement Policy. If you contest any NCV in this report, you should provide a response

within 30 days of the date of this IR, with the basis for your denial, to the Nuclear Regulatory

Commission, ATTN.: Document Control Desk, Washington, D.C. 20555-0001; with copies to

the Regional Administrator Region I; the Director, Office of Enforcement, U. St. Nuclear

Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the

Susquehanna Steam Electric Station. In addition, if you disagree with the cross-cutting aspect

of any finding in this report, you should provide a response within 30 days of the date of this IR,

with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC

Resident Inspectors at the SSES.

T. Rausch 2

In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any), will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mel Gray, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Docket Nos. 50-387; 50-388

License Nos. NPF-14, NPF-22

Enclosures: Inspection Report 05000387/2012005 and 05000388/2012005

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

ML13044A599

Non-Sensitive Publicly Available

SUNSI Review

Sensitive Non-Publicly Available

OFFICE RI/DRP RI/DRP RI/DRP

NAME PFinney/AAR for ARosebrook/AAR MGray/MG

DATE 02/ 12 /13 02/12 /13 02/ 13 /13

1

U.S NUCLEAR REGULATORY COMMISSION

REGION I

Docket No: 50-387, 50-388

License No: NPF-14, NPF-22

Report No: 05000387/2012005 and 05000388/2012005

Licensee: PPL Susquehanna, LLC (PPL)

Facility: Susquehanna Steam Electric Station, Units 1 and 2

Location: Berwick, Pennsylvania

Dates: October 1, 2012 through December 31, 2012

Inspectors: P. Finney, Senior Resident Inspector

J. Greives, Resident Inspector

R. Edwards, Acting Resident Inspector

A. Rosebrook, Senior Project Engineer

J. Richmond, Senior Reactor Inspector

J. Furia, Senior Health Physicist

J. Caruso, Senior Operations Engineer

A. Bolger, Reactor Engineer

R. Rolph, Health Physicist

C. Lally, Operations Engineer

Approved By: Mel Gray, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Enclosure

2

TABLE OF CONTENTS

SUMMARY OF FINDINGS ........................................................................................................... 3

REPORT DETAILS ....................................................................................................................... 6

1. REACTOR SAFETY ................................................................................................................. 6

1R01 Adverse Weather Protection ................................................................................... 6

1R04 Equipment Alignment ............................................................................................... 7

1R05 Fire Protection .......................................................................................................... 8

1R11 Licensed Operator Requalification Program ......................................................... 10

1R12 Maintenance Effectiveness ................................................................................... 11

1R13 Maintenance Risk Assessments and Emergent Work Control .............................. 16

1R15 Operability Determinations and Functionality Assessments .................................. 17

1R19 Post-Maintenance Testing ..................................................................................... 18

1R20 Refueling and Other Outage Activities .................................................................. 18

1R22 Surveillance Testing .............................................................................................. 20

1EP6 Drill Evaluation ...................................................................................................... 20

2. RADIATION SAFETY ............................................................................................................. 23

2RS6 Radioactive Gaseous and Liquid Effluent Treatment ............................................ 23

2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,

and Transportation ................................................................................................ 28

4. OTHER ACTIVITIES .............................................................................................................. 30

4OA1 Performance Indicator Verification ......................................................................... 30

4OA2 Problem Identification and Resolution ................................................................... 32

4OA3 Follow-up of Events and Notices of Enforcement Discretion ................................ 47

4OA5 Other Activities ....................................................................................................... 51

4OA6 Meetings, Including Exit ......................................................................................... 54

4OA7 Licensee-Identified Violations ................................................................................. 54

ATTACHMENT: SUPPLEMENTAL INFORMATION.................................................................. 54

SUPPLEMENTAL INFORMATION ........................................................................................... A-1

KEY POINTS OF CONTACT .................................................................................................... A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED ........................................................ A-2

LIST OF DOCUMENTS REVIEWED ....................................................................................... A-3

LIST OF ACRONYMS ............................................................................................................. A-13

Enclosure

3

SUMMARY OF FINDINGS

IR 05000387/2012005, 05000388/2012005 10/01/2012 - 12/31/2012; Susquehanna Steam

Electric Station, Units 1 and 2; Maintenance Effectiveness, Drill Evaluation, Problem

Identification and Resolution, Follow-up of Events and Notices of Enforcement Discretion.

The report covered a three-month period of inspection by resident inspectors and announced

inspections performed by regional inspectors. Inspectors identified two Severity Level IV non-

cited violations (NCVs) and three NCVs of very low safety significance (Green). The

significance of most findings is indicated by their color (i.e., greater than Green, or Green,

White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, Significance

Determination Process (SDP), dated June 2, 2011. Cross-cutting aspects are determined

using IMC 0310, Components Within Cross-Cutting Areas, dated October 28, 2011. All

violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement

Policy, dated June 7, 2012. The NRCs program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 4.

Cornerstone: Initiating Events

Green. A self-revealing Green NCV of 10 CFR 50 Appendix B, Criteria III, Design Control,

was identified related to a leak on the Unit 1 A reactor recirculation pump suction line

decontamination flange weld. Specifically, PPL personnel used an incorrect value for stress

intensification factor in the vibration analysis in 2004 to support an extended power uprate

(EPU). When the correct stress intensification factor was applied, American Society of

Mechanical Engineers (ASME) OM-3 code limits for endurance and fatigue stress were

exceeded. The weld failure resulted in pressure boundary leakage in excess of TS 3.4.4

limits from approximately June 16 through 19, 2012. PPL staff entered the problem in the

PPL corrective action program (CAP) as CR 1589390, repaired and modified the flange line,

and revised the calculation.

The inspectors reviewed the performance deficiency using NRC IMC 0612, Appendix B,

Issue Screening, and determined to be more than minor because it affected the Initiating

Events cornerstone attribute of design control. The issue adversely affected the associated

cornerstone objective of limiting the likelihood of those events that upset plant stability and

challenge critical safety functions during shutdown as well as power operations. The finding

was evaluated using Section A of IMC 609, Appendix A, Exhibit 1, Initiating Events

Screening Questions. Since the finding result could not have reasonably exceeded the

leak rate for a small loss of coolant accident (LOCA) and did not likely affect other systems

used to mitigate a LOCA resulting in a total loss of their function (e.g., inter-facing system

LOCA), the finding screened to very low safety significance (Green). This finding was

determined to not be indicative of current performance because the deficiency occurred in

2004 and procedures and training are in place that would have precluded the issue.

Therefore, no cross-cutting aspect is assigned. (Section 4OA2)

Enclosure

4

Cornerstone: Mitigating Systems

Green. Inspectors identified a Green NCV of 10 CFR 50.65(a)(2) for PPL staff not

demonstrating that the performance of the Unit 2 125 volt direct-current (VDC) system was

being effectively controlled through appropriate preventive maintenance. Specifically, PPL

did not properly classify a functional failure of the Unit 2 125 VDC system on November 23,

2011 as maintenance preventable until prompted by questions from the inspectors.

Consequently, PPL staff declared the functional failure as maintenance preventable,

determined a maintenance rule performance criteria was exceeded and moved the Unit 2

125 VDC system from a(2) to (a)(1) status in order to establish goals and monitoring as

required by 10 CFR 50.65. PPL staff entered this issue in their CAP as CRs 1496655 and

1643158.

This finding was more than minor because it was associated with the Equipment

Performance attribute of the Mitigating System cornerstone, and adversely affected the

cornerstone objective of ensuring the availability, reliability and capability of systems that

respond to initiating events to prevent undesirable consequences. Additionally, this finding

was similar to example 7.d of IMC 0612, Appendix E. Using Section A of Exhibit 2 of NRC

IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-

Power, inspectors determined this finding was of very low safety significance (Green)

because the finding did not represent an actual loss of function of one or more non-TS trains

of equipment designated as high safety-significant in accordance with PPLs maintenance

rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The inspectors determined that this finding had a

cross-cutting aspect in the area of Problem Identification and Resolution (PI&R), CAP,

because PPL staff did not thoroughly evaluate the Unit 2 125 VDC system functional failure

such that the resolution addressed the cause to include proper classification. The inspectors

determined that PPL staff not thoroughly evaluating the maintenance preventable aspects of

a functional failure was due to the CAP process evaluation not fully addressing the cause

such that appropriate classification under the maintenance rule could be made P.1(c)

(Section 1R12).

Cornerstone: Emergency Preparedness

Green. Inspectors identified a Green NCV associated with emergency preparedness

planning standard 10 CFR 50.47(b)(14) and the requirements of Section lV.F.2.g of

10 CFR 50, Appendix E. Specifically, PPL personnel did not identify an Emergency

Response Organization (ERO) performance weakness associated with an untimely

notification of an emergency declaration during their critique following the full-scale

emergency preparedness (EP) drill. In the case of ERO performance, simulator equipment

issues prevented the ability of drill controllers to satisfactorily evaluate performance of the

ERO and PPL staff did not identify that all off-site response organizations (OROs)

were not notified within fifteen minutes. The critique deficiency was entered into PPLs CAP

as CR 1648380.

The finding is more than minor because it is associated with the ERO attribute of the

Emergency Preparedness cornerstone and affected the cornerstone objective to ensure that

PPL staff are capable of implementing adequate measures to protect the health and safety

of the public in the event of a radiological emergency. The inspectors assessed the issue,

related to the failure to make a timely notification to the OROs, using NRC IMC 0609

Appendix B, Emergency Preparedness Significance Determination Process. PPL's drill

critique not identifying the untimely notification met the NRC's definition of a weakness in a

Enclosure

5

full-scale drill. However, because of the unique nature of the equipment failures associated

with the notification of the first ORO, inspectors determined that the failure to critique the drill

weakness only constituted a degradation of the planning standard (PS) function. Therefore

the finding is characterized as very low safety significance (Green). The finding is related

to the cross-cutting area of PI&R, CAP, in that PPL staff did not identify a risk significant

planning standard (RSPS) performance issue completely, accurately, and in a timely

manner commensurate with the safety significance. Specifically, during the critique of the

full-scale drill conducted on October 14, 2012, PPL staff did not recognize and critique that

an RSPS was not met and did not place this issue into the CAP until prompted by

inspectors. P.1(a) (Section 1EP6)

Cornerstone: Miscellaneous

Severity Level IV. Inspectors identified a SL IV NCV of 10 CFR 50.73 (a)(2)(vii) for PPLs

failure to submit a licensee event report (LER) of a common cause inoperability of two

independent trains of reactor protection system (RPS) electrical power monitoring

associated with several Unit 1 RPS breakers on May 8, 2012. PPL staff entered the issue

into the CAP as CR 1663785 and took action to issue the required LER.

This finding was evaluated using the traditional enforcement process because the failure to

accurately report events has the potential to impact or impede the regulatory process. The

finding was determined to be a Severity Level IV violation based on example 6.9.d.9 of the

NRC Enforcement Policy. This example states that a licensee failing to make a report

required by 10 CFR 50.72 or 10 CFR 50.73 is an example of a Severity Level IV violation.

Because this violation involves the traditional enforcement process and does not have an

underlying technical violation that would be considered more-than-minor, inspectors did not

assign a cross-cutting aspect to this violation in accordance with IMC 0612, Appendix B.

(Section 1R12)

Severity Level IV. The inspectors identified a SL IV NCV of 10 CFR 50.72(b)(3)(iv)(A) and

(B) when PPL operators did not report a valid actuation of the Unit 2 RPS on November 9,

2012 within eight hours of occurrence as required. The concern was entered into PPLs

CAP as CR 1643096 and an Emergency Notification System (ENS) report was submitted

restoring compliance.

This finding was evaluated using the traditional enforcement process because the failure to

accurately report events has the potential to impact or impede the regulatory process. The

finding was determined to be a Severity Level IV violation based on example 6.9.d.9 of the

NRC Enforcement Policy. This example states that a licensee failing to make a report

required by 10 CFR 50.72 or 10 CFR 50.73 is an example of a Severity Level IV violation.

Because this violation involves the traditional enforcement process and does not have an

underlying technical violation that would be considered more-than-minor, inspectors did not

assign a cross-cutting aspect to this violation in accordance with IMC 0612, Appendix B.

(Section 4OA3)

Enclosure

6

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at or near 100 percent power. On October 2, 2012,

operators reduced Unit 1 to 85 percent power to address potential problems with some low

pressure (LP) turbine blades consistent with their adverse condition monitoring plan (ACMP).

On October 6, Unit 1 was further reduced to 65 percent power in accordance with the ACMP.

On October 8, the ACMP supported a Unit 1 power increase to 75 percent. Unit 1 was shut

down from 75 percent power on October 19 and reached Mode 4 the following day in support of

a maintenance outage for the LP turbine blades. A reactor startup commenced on November 6,

and Unit 1 reached 100 percent power on November 12. Operators reduced Unit 1 power to 70

percent power on December 7, for a control rod sequence exchange and scram time testing.

Unit 1 returned to 100 percent power on December 9. On December 14, operators reduced

Unit 1 power to approximately 79 percent power in response to entry into TS 3.0.3, for problems

with both control room chilling units. After restoring a control room chiller, operators restored

Unit 1 to 100 percent later that day and remained at 100 percent for the remainder of the

inspection period.

Unit 2 began the inspection period at or near 100 percent power. On October 2, operators

reduced Unit 2 to 85 percent power to address potential problems with some low pressure (LP)

turbine blades consistent with their ACMP. On October 6, Unit 2 was further reduced to 65

percent power in accordance with the ACMP to mitigate potential degradation of LP turbine

blades in accordance with the ACMP. On October 8, the ACMP supported a Unit 2 power

increase to 75 percent. On November 9, operators manually scrammed Unit 2 due to a failure of

the integrated control system (ICS). Unit 2 remained shutdown for a maintenance outage on LP

turbine blades and reached Mode 4 on November 11. On November 18, operators commenced

a Unit 2 reactor startup. On November 19, operators placed the Unit 2 main turbine on the grid,

but commenced a reactor shutdown due to an electro-hydraulic control (EHC) fluid leak on a

main turbine bypass valve. Unit 2 reached Mode 4 on November 21. Operators commenced a

Unit 2 reactor startup on November 25, and reached approximately 10 percent power when

another EHC leak was identified. Operators shutdown Unit 2 and reached Mode 4 on November

26. Operators commenced a Unit 2 reactor startup on November 28, and reached 100 percent

power on December 3. On December 14, operators reduced Unit 2 to approximately 79 percent

power in response to entry into TS 3.0.3 for problems with both control room chilling units. After

restoring a control room chiller, operators restored Unit 2 to 100 percent later that day. On

December 16, an automatic reactor scram occurred during testing of the main turbine control

valves and Unit 2 entered Mode 3. On December 18, operators commenced a Unit 2 reactor

startup. On December 19, Unit 2 automatically scrammed at approximately 18 percent power

during a feedwater system mode shift. Operators commenced a Unit 2 reactor startup on

December 26, and reached approximately 90 percent power at the end of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01 - 2 samples)

.1 Readiness for Imminent Adverse Weather Conditions

Enclosure

7

a. Inspection Scope

The inspectors reviewed PPLs preparations in advance of and during warnings and

advisories issued by the National Weather Service. The inspectors performed

walkdowns of areas that could be potentially impacted by the weather conditions,

such as the emergency and station blackout (SBO) diesel generators (DGs), station

transformers, and switchyards, and verified that station personnel secured loose

materials staged for outside work prior to the forecasted weather. The inspectors

verified that PPL staff monitored the approach of adverse weather according to

applicable procedures and took appropriate actions as required. The inspectors

reviewed the Updated Final Safety Analysis Report (UFSAR), Technical Specifications

(TSs) control room logs, and the CAP to determine what temperatures or other seasonal

weather could challenge these systems, and to ensure PPL personnel had adequately

prepared for these challenges. The inspectors reviewed station procedures, including

PPLs seasonal weather preparation procedure and applicable operating procedures.

Documents reviewed for each section of this IR are listed in the Attachment.

Common, preparations for Hurricane Sandy

b. Findings

No findings were identified.

.2 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

The inspectors performed a review of PPLs readiness for the onset of seasonal low

temperatures. The review focused on the condensate system and the Engineering

Safeguards Service Water (ESSW) pump house. The inspectors reviewed the UFSAR,

TSs, control room logs, and the CAP to determine what temperatures or other seasonal

weather could challenge these systems, and to ensure PPL personnel had adequately

prepared for these challenges. The inspectors reviewed station procedures, including

PPLs seasonal weather preparation procedure and applicable operating procedures.

The inspectors performed walkdowns of the selected systems to ensure station

personnel identified issues that could challenge the operability of the systems during

cold weather conditions. Documents reviewed for each section of this IR are listed in

the Attachment.

Common, winter preparations

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial System Walkdowns (71111.04Q - 3 samples)

a. Inspection Scope

Enclosure

8

The inspectors performed partial walkdowns of the following systems:

Unit 2, Division II residual heat removal (RHR) during C emergency diesel

generator (EDG) inoperability

Common, 13.8 kilovolts (kV) offsite power during startup transformer T20 outage

Common, B emergency service water (ESW)

The inspectors selected these systems based on their risk-significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors reviewed

applicable operating procedures, system diagrams, the UFSAR, TSs, work orders

(WOs), CRs, and the impact of ongoing work activities on redundant trains of equipment

in order to identify conditions that could have impacted system performance of their

intended safety functions. The inspectors also performed field walkdowns of accessible

portions of the systems to verify system components and support equipment were

aligned correctly and were operable. The inspectors examined the material condition of

the components and observed operating parameters of equipment to verify that there

were no deficiencies. The inspectors also reviewed whether PPL staff had properly

identified equipment issues and entered them into the CAP for resolution with the

appropriate significance characterization.

b. Findings

No findings were identified.

.2 Full System Walkdown (71111.04S - 1 sample)

a. Inspection Scope

On November 20, 2012, the inspectors performed a complete system walkdown of

accessible portions of the common A EDG to verify the existing equipment lineup was

correct. The inspectors reviewed operating procedures, surveillance tests, drawings,

equipment line-up check-off lists, and the UFSAR to verify the system was aligned to

perform its required safety functions. The inspectors also reviewed electrical power

availability, component lubrication, equipment cooling, and operability of support

systems. The inspectors performed field walkdowns of accessible portions of the

systems to verify system components and support equipment were aligned correctly

and operable. The inspectors examined the material condition of the components and

observed operating parameters of equipment to verify that there were no deficiencies.

Additionally, the inspectors reviewed a sample of related CRs and WOs to ensure PPL

appropriately evaluated and resolved any deficiencies.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Resident Inspector Quarterly Walkdowns (71111.05Q - 5 samples)

a. Inspection Scope

Enclosure

9

The inspectors conducted tours of the areas listed below to assess the material

condition and operational status of fire protection features. The inspectors verified

that PPL controlled combustible materials and ignition sources in accordance with

administrative procedures. The inspectors verified that fire protection and suppression

equipment was available for use as specified in the area pre-fire plan, and passive fire

barriers were maintained in good material condition. The inspectors also verified that

station personnel implemented compensatory measures for out of service, degraded, or

inoperable fire protection equipment, as applicable, in accordance with procedures.

Unit 1, lower relay room (Fire Zone 0-24D) on December 12, 2012

Unit 1, lower cable spreading room, (Fire Zone 0-25E) on December 12, 2012

Unit 2, heat exchanger and pump access area (Fire Zone 2-3A) on October 23, 2012

Unit 2, containment access area (Fire Zone 1-4A-N, S, W) on November 9, 2012

Unit 2, high pressure coolant injection (HPCI) and reactor core isolation cooling

(RCIC) pump rooms (Fire Zones 2-1C, 2-1D) on December 17, 2012

b. Findings

No findings were identified.

.2 Fire Protection - Drill Observation (71111.05A - 1 sample)

a. Inspection Scope

The inspectors observed unannounced fire drills conducted on September 17 and

October 17, 2012, which involved fires in the Unit 1 EHC room and Unit 1 Remote

Shutdown room. The inspectors evaluated the readiness of the plant fire brigade to

fight fires. The inspectors verified that PPL personnel identified deficiencies, openly

discussed them in a self-critical manner at debriefs, and took appropriate corrective

actions as required. The inspectors evaluated specific attributes as follows:

Proper wearing of turnout gear and self-contained breathing apparatus (SCBA)

Proper use and layout of fire hoses

Employment of appropriate fire-fighting techniques

Sufficient fire-fighting equipment brought to the scene

Effectiveness of command and control

Search for victims and propagation of the fire into other plant areas

Smoke removal operations

Utilization of pre-planned strategies

Adherence to the pre-planned drill scenario

Drill objectives met

The inspectors also evaluated the fire brigades actions to determine whether these

actions were in accordance with PPLs fire-fighting strategies.

b. Findings

No findings were identified.

Enclosure

10

1R11 Licensed Operator Requalification Program (71111.11 - 4 samples)

.1 Quarterly Review of Licensed Operator Requalification Testing and Training

a. Inspection Scope

The inspectors observed licensed operator requalification examinations on October 10,

2012. The inspectors evaluated operator performance during the simulated event and

verified completion of risk significant operator actions, including the use of abnormal and

emergency operating procedures (EOPs). The inspectors assessed the clarity and

effectiveness of communications, implementation of actions in response to alarms and

degrading plant conditions, and the oversight and direction provided by the control room

supervisor. The inspectors verified the accuracy and timeliness of the emergency

classification made by the shift manager and the TS action statements entered by the

shift technical advisor. Additionally, the inspectors assessed the ability of the crew and

training staff to identify and document crew performance problems.

b. Findings

No findings of significance were identified.

.2 Quarterly Review of Licensed Operator Performance in the Main Control Room

a. Inspection Scope

The inspectors observed operator performance in the main control room during the

evolutions listed below. The inspectors observed infrequently performed test or

evolution briefings, pre-shift briefings, and reactivity control briefings to verify that the

briefings met the criteria specified in PPLs Operations Section Expectations Handbook

and PPLs Administrative Procedure OP-AD-004, Operations Standards for Error and

Event Prevention, Revision 25. Additionally, the inspectors observed test performance

to verify that procedure use, crew communications, and coordination of activities

between work groups similarly met established expectations and standards.

Unit 1, reactor shutdown for a maintenance outage on October 20, 2012 and

subsequent startup on November 6, 2012

Unit 2, operator response to reactor pressure vessel stratification on November 10,

2012

b. Findings

No findings were identified.

.3 Annual Review of Pass/Fail Results for Licensed Operator Requalification Exams

a. Inspection Scope

On December 6, 2012, NRC region-based inspectors conducted an in-office review of

results of PPL-administered annual operating tests and comprehensive written

examinations for 2012. The inspection assessed whether pass rates were consistent

Enclosure

11

with the guidance of NRC IMC 0609, Appendix I, Operator Requalification Human

Performance SDP. The inspectors verified that:

Crew pass rates were greater than 80 percent. (Pass rate was 100 percent)

Individual pass rates on the written examination were greater than 80 percent.

(Pass rate was 95.1 percent)

Individual pass rates on the job performance measures of the operating examination

were greater than 80 percent. (Pass rate was 100 percent)

Individual pass rates on the dynamic simulator test were greater than 80 percent.

(Pass rate was 93.4 percent)

Overall pass rate among individuals for all portions of the examination was greater

than or equal to 80 percent. (Overall pass rate was 90.2 percent)

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12 - 5 samples)

a. Inspection Scope

The inspectors reviewed the samples listed below to assess the effectiveness of

maintenance activities on structures, systems and components (SSCs) performance

and reliability. The inspectors reviewed system health reports, CAP documents,

maintenance WOs, and maintenance rule basis documents to ensure that PPL was

identifying and properly evaluating performance problems within the scope of the

maintenance rule. For each sample selected, the inspectors verified that the SSC was

properly scoped into the maintenance rule in accordance with 10 CFR 50.65 and verified

that the (a)(2) performance criteria established by PPLs staff was reasonable. As

applicable, for SSCs classified as (a)(1), the inspectors assessed the adequacy of goals

and corrective actions to return these SSCs to (a)(2). Additionally, the inspectors

ensured that PPLs staff was identifying and addressing common cause failures that

occurred within and across maintenance rule system boundaries.

Unit 1, RPS electrical power monitoring assembly failures on May 8, 2012

Unit 1, nuclear instrumentation (NI) equipment challenges during maintenance

shutdown from October 20 through November 6, 2012

Unit 2, rod position information system (RPIS) relay card failures on July 25,

August 8, and August 9, 2012

Common, ESW pinhole leaks on November 26 and November 28, 2012

Unit 2, RCIC inverter trip while placing 125V DC system in equalize charge on

November 23, 2011

b. Findings

.1 Introduction. Inspectors identified a Green NCV of 10 CFR 50.65(a)(2) for PPL staff not

demonstrating the performance of the Unit 2 125 VDC system was being effectively

controlled through appropriate preventive maintenance. Specifically, PPL staff did not

properly classify a functional failure of the Unit 2 125 VDC system on November 23,

2011 as maintenance preventable until prompted by questions from the inspectors.

Enclosure

12

Consequently, PPL staff declared the functional failure as maintenance preventable,

determined that a maintenance rule performance criteria was exceeded and moved the

Unit 2 125 VDC system from a(2) to (a)(1) status to establish goals and monitoring as

required by 10 CFR 50.65.

Description. On November 23, 2011, PPL operators placed the Unit 2 D 125 VDC

system battery charger to equalize as a standard maintenance practice after adding

water to a battery to maintain adequate electrolyte level. Immediately after placing the

battery charger in equalize, the main control room received alarms related to the Unit 2

RCIC system. In accordance with the alarm response procedure, PPL operators

confirmed that the RCIC inverter was de-energized. With the RCIC inverter de-

energized, there was no control power to the RCIC flow controller, and PPL operators

declared the RCIC system inoperable and unavailable. PPL staff further investigated

and determined that the D battery charger equalize voltage was not within the criteria

of 138 to 141 volts, as discussed in OP-202-001, 125V DC System, Section 2.4.

Subsequently, the D battery charger was placed to float and the RCIC inverter

immediately reset. PPL staff determined that the RCIC inverter tripped on the high

voltage setpoint during equalize charging of the D battery charger. RCIC was

unavailable for a total of 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 16 minutes prior to the automatic reset of the

inverter.

On March 28, 2012, PPL Engineering completed the ACE (CR 1496655), which

concluded that the November 23, 2011 issue was a maintenance rule function failure

(MRFF) of the 125 VDC system. This function is defined in the Maintenance Rule Basis

Document as the ability to energize channel A of the class 1E 125 VDC system. The

ACE also determined that the MRFF was not a maintenance preventable functional

failure (MPFF) because adequate tasks were already in place to identify and correct

setpoint drift of the RCIC inverter high voltage trip setpoint via a biennial calibration. On

October 25, 2012, PPLs Maintenance Rule Expert Panel (MREP) reviewed the Unit 2

125 VDC system functional failure and agreed with the MRFF and MPFF determinations

in the ACE.

The inspectors performed a review of the MRFF issue, including the ACE, the Expert

Panel meeting minutes, procedures NDAP-QA-0413, Maintenance Rule Program, and

OP-202-001, 125V DC System, Unit 2 RCIC inverter calibration data history, and

discussed the issue with PPL engineers and the Maintenance Rule Coordinator. PPL

staff had determined that an apparent cause of the Unit 2 RCIC inverter high voltage trip

was attributed to inadequate design margin between the operating range of the battery

chargers and the shutdown setpoint of the RCIC inverters. The ACE indicated that when

the charger is switched from float to equalize, the sudden change in potential to the

battery causes an initial voltage overshoot by the charger. The ACE also indicated that

the RCIC system Topaz-style inverters have exhibited up to a three-volt setpoint drift

decrease in the high voltage trip setpoint during routine as-found calibration testing. The

inspector review of historical as-found calibration data for a sample of PPLs Topaz-style

inverters found up to a six-volt setpoint decreasing drift. The inspectors determined that

PPLs operating experience review for Topaz-style inverter trips as a result of placing

batter chargers in equalize was appropriate, and noted that several examples were

identified, including past examples at Susquehanna. Corrective action item number 4 of

the ACE, which addressed the apparent cause, performed a change to the 125 VDC

system procedure to perform a quarter-turn decreasing voltage adjustment of the battery

charger equalizing potentiometer just prior to taking the switch from float to equalize.

Enclosure

13

The inspectors noted that NDAP-QA-0413, Maintenance Rule Program, step 7.4.2.b,

contains specific guidance that MRFFs due to incorrect maintenance procedures are

MPFFs.

Ultimately, the inspectors determined that the ACEs apparent cause incorrectly

described the failure as inadequate design margin with respect to the operating voltage

range of the battery chargers. Despite this, the inspectors concluded that the corrective

actions were appropriate. Specifically, revising the system procedural steps for placing

the battery on an equalizing charge, during a maintenance activity, ensured the

equipment was maintained and operated within the low design margin. The inspectors

determined that had the apparent cause been more accurately described, the evaluator

could have reasonably concluded that the MRFF was maintenance preventable, or the

MREP would have had sufficient information to challenge the MRFF classification.

The inspectors questioned PPL staff regarding the determination documented in the

ACE and confirmed by October 25, 2012 MREP, that the 125 VDC system functional

failure was not maintenance preventable. Specifically, the inspectors questioned

whether the November 23, 2011 action to place the Unit 2 D battery charger to equalize

would have been considered implementation of an incorrect maintenance procedure,

since the procedure was changed as a corrective action to address the apparent cause

of the problem. The inspectors also questioned whether PPLs staff were performing the

RCIC inverter calibration at a proper frequency to address the as-found calibration

testing examples of high voltage trip setpoint drift.

On December 13, 2012, PPL staff performed a second Maintenance Rule Expert Panel

review of the Unit 2 125 VDC system MRFF to consider the potential maintenance

preventable aspects, as identified by the inspectors. PPL staff determined that

additional changes to the 125 VDC system procedure would be appropriate, to provide

guidance on promptly switching the charger from equalize back to float to promptly

restore the RCIC inverter in the event of an inverter trip on high voltage, thereby

minimizing the duration of any adverse impact on the RCIC system. Based on the

maintenance preventable aspects associated with the Unit 2 125 VDC system steps

prior to the procedure changes, PPL staff determined that the MRFF did constitute a

MPFF. PPL staff determined that because the Unit 2 125 VDC system was scoped as a

high safety significant system under the Maintenance Rule, the system would be moved

from (a)(2) to (a)(1) per procedure NDAP-QA-0413, step 7.4.3.c. PPL staff determined

that an (a)(1) action plan would be developed under the original CR. Regarding the

examples of RCIC inverter as-found high voltage setpoint drift, PPL staff evaluated a

broad scope of historical data and determined that there was no obvious trend of low

setpoint drift. PPL staff did acknowledge that low setpoint drift could have contributed to

the MRFF and created an action to obtain the as-found data in the next two-year

calibration under WO 1434638 (ACE item 6). PPL staff entered these items in their CAP

under CRs 1496655 and 1643158.

The inspectors noted that NDAP-QA-0413, steps 4.7.4.a and step 4.8.2.a require that

MRFFs shall be presented to the Expert Panel within 60 days of the failure date. Step

7.1.4 allows for the control of extensions relative to the 60-day requirement and states

that extensions are controlled to ensure that the determination of (a)(1) classification

meets timeliness requirements. The inspectors questioned PPL staff on the

approximate 11-month gap between the November 23, 2011 MRFF and the October 25,

2012 initial expert panel review. PPL staff stated that this delay was attributed to a high

Enclosure

14

backlog of functional failures for expert panel review. See section 4OA2.2 of this

inspection report for further discussion of this adverse trend.

Additionally, inspectors noted that NDAP-QA-0413, section 7.1.3 states that CRs

involving MRFFs shall, as a minimum, be assigned the Apparent Cause evaluation type

defined in NDAP-QA-0702, Action Request and CR Process. Section 7.2.2 of NDAP-

QA-0413, which describes the requirements for processing MRFF CR evaluation reports

as it applies to the Maintenance Rule, states that the responsible system engineer shall

ensure that the CR evaluation report contains a determination of whether the failure

was/was not maintenance preventable and that this must be consistent with the

cause(s) of the failure. Based on this requirement, inspectors determined that the

ACE did not appropriately evaluate the issue to ensure the functional failure was

classified as maintenance preventable.

Analysis. The inspectors determined that PPL staff did not demonstrate performance of

the Unit 2 125 VDC system was being effectively controlled through the appropriate

preventive maintenance. Specifically, PPL staff did not properly classify a functional

failure of the Unit 2 125 VDC system as maintenance preventable, which when

appropriately classified, required establishing goals and monitoring the Unit 2 125 VDC

system in accordance with 10 CFR 50.65(a)(1). This finding was more than minor

because it was associated with the Equipment Performance attribute of the Mitigating

System cornerstone, and adversely affected the cornerstone objective of ensuring the

availability, reliability and capability of systems that response to initiating events to

prevent undesirable consequences. Additionally, this finding was similar to IMC 0612

Appendix E example 7.d. Specifically, PPL staff determined, based on inspector-

identified issues of concern, that equipment performance problems were such that

effective control of performance through appropriate preventive maintenance of the 125

VDC system under 10 CFR 50.65(a)(2) could not be demonstrated. The inspectors

evaluated this finding using Section A of Exhibit 2 of NRC IMC 0609 Appendix A, The

Significance Determination Process (SDP) for Findings At-Power, and determined this

finding was of very low safety significance (Green) because the finding did not represent

an actual loss of function of one or more non-TS trains of equipment designated as high

safety-significant in accordance with PPLs maintenance rule program for greater than

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The inspectors determined that this finding had a cross-cutting aspect in the area of

PI&R, CAP, because PPL staff did not thoroughly evaluate the Unit 2 125 VDC system

functional failure such that the resolution addressed the cause, to include proper

classification. Specifically, PPLs ACE identified and addressed 125 VDC system

procedural deficiencies. However, it did not consider the procedural deficiencies in the

MPFF determination until prompted by the inspectors questions. The inspectors

determined that PPLs failure to thoroughly evaluate the maintenance preventable

aspects of a functional failure was the result of a CAP failure to address the cause such

that appropriate classification under the maintenance rule could be made P.1(c).

Enforcement. 10 CFR 50.65(a)(1) requires, in part, that holders of an operating license

shall monitor the performance or condition of SSCs within the scope of the monitoring

programs as defined in 10 CFR 50.65(b) against licensee-established goals, in a manner

sufficient to provide reasonable assurance that such SSCs are capable of fulfilling their

intended functions. 10 CFR 50.65 (a)(2) requires, in part, that monitoring as specified in

10 CFR 50.65(a)(1) is not required where it has been demonstrated that the

performance or condition of an SSC is being effectively controlled through the perfor-

Enclosure

15

mance of appropriate preventive maintenance, such that the SSC remains capable of

performing its intended function. Contrary to the above, PPL staff did not demonstrate

that performance of the Unit 2 125 VDC system was being effectively controlled through

the performance of appropriate preventive maintenance in that an MPFF of 125 VDC

occurred on November 23, 2011. PPLs ACE determined the failure was not

maintenance preventable, a determination that was accepted at the October 25, 2012

maintenance rule expert panel meeting. This determination resulted in PPL staff not

placing the Unit 2 125 VDC system under 10 CFR 50.65(a)(1) for establishing goals and

monitoring against the goals until December 13, 2012 when the system was placed in

a(1) status. This violation is being treated as an NCV, consistent with section 2.3.2 of

the NRC Enforcement Policy because it was of very low safety significance and has

been entered into PPLs CAP under CRs 1496655 and 1643158. (NCV 05000388/

2012005-01, Failure to Demonstrate Effective Preventive Maintenance Under

50.65(a)(2))

.2 Introduction. Inspectors identified a SL IV NCV of 10 CFR 50.73 (a)(2)(vii) for PPL staff

not submitting an LER within 60 days of discovery of a common cause inoperability of

two independent trains of RPS electrical power monitoring.

Description. 10 CFR 50.73 (a)(2)(vii) requires, in part, that licensees submit an LER for

any event where a single cause or condition caused two independent trains or channels

to become inoperable in a single system designed to shut down the reactor within 60

days of discovering the event.

On May 8, 2012, three of eight RPS electrical power monitoring assemblies (EPA

breakers) did not trip open as required during TS required surveillance testing on Unit 1.

TS 3.3.8.2 requires two RPS EPA breakers to be operable for each in-service RPS

motor generator set or alternate power supply. The function of the breakers is to open

on under-voltage, over-voltage, or under-frequency conditions to prevent failures in the

safety-related RPS due to the non-safety related power supplies. Extended operation of

RPS in an under-voltage condition could result in the scram solenoids chattering and

potentially losing their pneumatic control capability, resulting in a loss of the primary

scram function. The inoperable breakers were sent to a vendor for failure analysis and

an ACE was initiated (CR 1570413).

Inspectors reviewed PPLs CAP and identified that condition report action (CRA)

1571200, which tracked the reportability follow-up determination, was closed on

September 5, 2012. PPL personnel had determined that the event was not reportable

because it did not result in a loss of safety function or condition prohibited by plant TSs.

This determination was based on completion of a past operability review (CRA 1572356)

which provided discussion that there was no evidence or past indication to support

degraded past operability prior to the point of discovery. It also discussed that, based

on which breakers were inoperable; there was no loss of safety function. Inspectors

determined that this information was sufficient and reasonable to support the condition

not being reportable as an event or condition that could have prevented fulfillment of a

safety function per 10 CFR 50.73(a)(2)(v) or as an operation or condition prohibited by

TSs per 10 CFR 50.73(a)(2)(i)(B). However, the past operability review stated that the

cause of the EPA breakers failing to trip is unknown (failed breakers have been returned

for evaluation). Based on this statement, inspectors determined that there was

insufficient evidence on September 5th to determine that the event was not reportable for

other reasons and the potential for common cause inoperability should have still been

considered.

Enclosure

16

By letter dated September 21, 2012, the vendor informed PPL staff that two of the three

breakers did not trip due to the calibration screws being out of adjustment on the under-

voltage relays (UVRs) which caused an, insufficient force balance between the torsional

spring and the plunger spring. This resulted in inadequate force being applied to trip

the breaker. Additionally, the vendor determined that, marginal calibrationover time

and cycling resulted in the UVR to lose calibration. The third breaker not tripping

could not be repeated in the laboratory and therefore its cause was indeterminate.

Inspectors reviewed the failure analysis and PPLs ACE and determined that the

condition constituted a common cause failure mode for independent trains, which

should have been reported to the NRC via an LER no later than November 20, 2012.

Analysis. The inspectors determined that PPL not reporting a common cause

inoperability of independent trains of TS required equipment was a performance

deficiency and impacted the NRCs ability to perform its regulatory function. The

finding was evaluated using the traditional enforcement process because the failure to

accurately report events has the potential to impact or impede the regulatory process.

The finding was determined to be a Severity Level IV violation based on example 6.9.d.9

of the NRC Enforcement Policy. This example states that a licensee failing to make a

report required by 10 CFR 50.72 or 10 CFR 50.73 is an example of a Severity Level IV

violation.

Because this violation involves the traditional enforcement process and does not have

an underlying technical violation that would be considered more-than-minor, inspectors

did not assign a cross-cutting aspect to this violation in accordance with IMC 0612,

Appendix B.

Enforcement. 10 CFR 50.73 (a)(2)(vii) requires, in part, that licensees submit an LER for

any event where a single cause or condition caused two independent trains or channels

to become inoperable in a single system designed to shut down the reactor within 60

days of discovering the event. Contrary to the above, PPL staff did not submit a report

within 60 days of September 21, 2012, after a failure analysis determined that two

independent trains of RPS electrical power monitoring were inoperable due to a common

cause or condition. PPL staff entered the deficiency into their CAP as CR 1663785 and

initiated action to submit the required LER. This violation is being treated as an NCV,

consistent with Section 2.3.2 of the Enforcement Policy because it was Severity Level IV

and was entered into the PPLs CAP. (NCV 05000387/2012005-02, Failure to Report

Common-Cause Inoperability of Independent Trains)

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 5 samples)

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the

maintenance and emergent work activities listed below to verify that PPL staff performed

the appropriate risk assessments prior to removing equipment for work. The inspectors

selected these activities based on potential risk significance relative to the reactor safety

cornerstones. As applicable for each activity, the inspectors verified that PPL personnel

performed risk assessments as required by 10 CFR 50.65(a)(4) and that the

assessments were accurate and complete. When PPL performed emergent work, the

inspectors verified that operations personnel promptly assessed and managed plant risk.

The inspectors reviewed the scope of maintenance work and discussed the results of

Enclosure

17

the assessment with the stations probabilistic risk analyst to verify plant conditions were

consistent with the risk assessment. The inspectors also reviewed the TS requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

Unit 1, yellow risk during division II RHR minimum flow valve work

Unit 2, yellow risk during the November 9, 2012 manual reactor scram

Common, risk assessment during startup transformer T20 maintenance

Common, B EDG room temperature calibration

Common, yellow risk during B ESW flow transmitter replacement

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments (71111.15 - 6 samples)

a. Inspection Scope

The inspectors reviewed operability determinations for the following degraded or non-

conforming conditions:

Unit 1, anomalous bypass valve (BPV) indications during plant shutdown

Unit 2, elevated suction pressure on RCIC

Unit 2, reactor pressure vessel (RPV) bottom head cooldown in excess of 100°

F/hour following the November 9, 2012, reactor scram and reactor vessel

stratification

Unit 2, 2A residual heat removal service water (RHRSW) pump in-service test

failure

Common, control structure (CS) boundary leak during testing

Common, compliance with TS surveillance requirement (SR) 3.4.2.1 for jet pump

operability

The inspectors selected these issues based on the risk significance of the associated

components and systems. The inspectors evaluated the technical adequacy of the

operability determinations to assess whether TS operability was properly justified and

the subject component or system remained available such that no unrecognized

increase in risk occurred. The inspectors compared the operability and design criteria in

the appropriate sections of the TSs and UFSAR to PPLs evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled by PPL. The

inspectors determined, where appropriate, compliance with bounding limitations

associated with the evaluations.

b. Findings

No findings were identified.

Enclosure

18

1R19 Post-Maintenance Testing (71111.19 - 7 samples)

a. Inspection Scope

The inspectors reviewed the post-maintenance tests for the maintenance activities listed

below to verify that procedures and test activities ensured system operability and

functional capability. The inspectors reviewed the test procedure to verify that the

procedure adequately tested the safety functions that may have been affected by the

maintenance activity, that the acceptance criteria in the procedure was consistent with

the information in the applicable licensing basis and/or design basis documents, and that

the procedure had been properly reviewed and approved. The inspectors also

witnessed the test or reviewed test data to verify that the test results adequately

demonstrated restoration of the affected safety functions.

Unit 1, standby liquid control (SBLC) planned maintenance

Unit 1, corrective maintenance on source range monitors (SRMs) and intermediate

range monitor (IRMs)

Unit 1, 1A reactor recirculation pump (RRP) seal replacement and motor-generator

set maintenance

Unit 2, division I core spray minimum flow valve maintenance

Unit 2, drywell cooler fan breaker repair following failure to start in slow speed

Unit 2, division II RHR planned maintenance

Common, planned maintenance on startup transformer T20

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities (71111.20 - 2 samples)

.1 Unit 1 Maintenance Outage for Low Pressure (LP) Turbine Blade Replacement

a. Inspection Scope

The inspectors reviewed the stations work schedule and outage risk plan for the Unit 1

maintenance outage, which was conducted on October 19 through November 6, 2012.

The inspectors reviewed PPLs development and implementation of outage plans and

schedules to verify that risk, industry experience, previous site-specific problems, and

defense-in-depth were considered. During the outage, the inspectors observed portions

of the shutdown and cooldown processes and monitored controls associated with the

following outage activities:

Configuration management, including maintenance of defense-in-depth

commensurate with the outage plan for the key safety functions and compliance with

the applicable technical specifications when taking equipment out of service

Implementation of clearance activities and confirmation that tags were properly hung

and that equipment was appropriately configured to safely support the associated

work or testing

Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication and instrument error accounting

Enclosure

19

Status and configuration of electrical systems and switchyard activities to ensure that

technical specifications were met

Monitoring of decay heat removal operations

Reactor water inventory controls, including flow paths, configurations, alternative

means for inventory additions, and controls to prevent inventory loss

Activities that could affect reactivity

Maintenance of secondary containment as required by technical specifications

Fatigue management

Tracking of startup prerequisites and startup and ascension to full power operation

Identification and resolution of problems related to refueling outage activities

b. Findings

No findings were identified.

.2 Unit 2 Maintenance Outage for LP Turbine Blade Replacement

a. Inspection Scope

The inspectors reviewed the stations work schedule and outage risk plan for the Unit 2

maintenance outage, which was conducted on November 9 through November 28, 2012.

The inspectors reviewed PPLs development and implementation of outage plans and

schedules to verify that risk, industry experience, previous site-specific problems, and

defense-in-depth were considered. The outage was commenced early due to a manual

reactor scram following an integrated control system failure. During the outage, the

inspectors observed portions of the shutdown and cooldown processes and monitored

controls associated with the following outage activities:

Configuration management, including maintenance of defense-in-depth,

commensurate with the outage plan for the key safety functions and compliance with

the applicable technical specifications when taking equipment out of service

Implementation of clearance activities and confirmation that tags were properly hung

and that equipment was appropriately configured to safely support the associated

work or testing

Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication and instrument error accounting

Status and configuration of electrical systems and switchyard activities to ensure that

technical specifications were met

Monitoring of decay heat removal operations

Reactor water inventory controls, including flow paths, configurations, alternative

means for inventory additions, and controls to prevent inventory loss

Activities that could affect reactivity

Maintenance of secondary containment as required by technical specifications

Fatigue management

Tracking of startup prerequisites and startup and ascension to full power operation

Identification and resolution of problems related to refueling outage activities

b. Findings

No findings were identified.

Enclosure

20

1R22 Surveillance Testing (71111.22 - 4 samples)

a. Inspection Scope

The inspectors observed performance of surveillance tests and/or reviewed test data of

selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR,

and PPL procedure requirements. The inspectors verified that test acceptance criteria

were clear, tests demonstrated operational readiness and were consistent with design

documentation, test instrumentation had current calibrations and the range and accuracy

for the application, tests were performed as written, and applicable test prerequisites

were satisfied. Upon test completion, the inspectors considered whether the test results

supported that equipment was capable of performing the required safety functions. The

inspectors reviewed the following surveillance tests:

Unit 1, RCIC comprehensive flow surveillance

Unit 2, main turbine valve testing

Unit 2, fuel pool cooling (FPC) system flow test

Unit 2, quarterly calibration of RPV pressure channels for low pressure

emergency core cooling system permissive signals

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation (71114.06 - 1 sample)

a. Inspection Scope

The inspectors evaluated the conduct of a routine PPL emergency drill on November 13,

2012 to identify weaknesses and deficiencies in the classification, notification, and

protective action recommendation development activities. The inspectors observed

emergency response operations in the simulator to determine whether the event

classifications, notifications, and protective action recommendations were performed in

accordance with procedures. The inspectors also attended the station drill critique to

compare inspector observations with those identified by PPL staff in order to evaluate

PPLs critique and to verify whether the PPL staff was properly identifying weaknesses

and entering them into the CAP.

Common, green team full-scale drill on November 13, 2012

b. Findings

Introduction. The NRC identified a Green NCV associated with emergency

preparedness planning standard 10 CFR 50.47(b)(14) and the requirements of Section

lV.F.2.g of 10 CFR 50 Appendix E. Specifically, PPL staff did not identify a performance

weakness related to a RSPS during their critique following the full-scale EP drill.

Description. 10 CFR 50.47(b)(14) requires that periodic drills be conducted to develop

and maintain key skills, and deficiencies identified as a result of exercises or drills be

Enclosure

21

corrected.Section IV.F.2.g of 10 CFR 50 Appendix E requires that all exercises, drills,

and training that provide performance opportunities to develop, maintain, or demonstrate

key skills include a formal critique in order to identify weak or deficient areas that need

correction. Additionally, it requires that any weaknesses or deficiencies be corrected.

On November 13, 2012, inspectors observed PPLs full-scale EP drill. In accordance

with the drill scenario, the Control Room Emergency Director declared an Unusual Event

(UE) at 8:28 a.m. Inspectors observed performance of the initial notification to offsite

response organizations (OROs). The stations emergency plan specifies three OROs

that PPL has responsibility to notify: Pennsylvania Emergency Management Agency

(PEMA), Luzerne County Emergency Management Agency (LCEMA), and Columbia

County Emergency Management Agency (CCEMA). Inspectors noted two observations

of significance with respect to performance of this notification.

First, in accordance with PPL emergency planning procedure EP-PS-126, Emergency

Plan Communicator: Emergency Plan Position Specific Instruction, Revision 28, the

communicator attempted to make contact with the OROs via a bridge line, which

simultaneously dials all three OROs, and then attempted to dial the OROs individually.

These attempts were unsuccessful because the phone had no dial tone. The lead drill

controller contacted a phone technician who restored some connectivity. It was

subsequently determined that at the start of the drill, the crew manipulated the setup of

the handset and portable headset. In doing this, the operator mistakenly disconnected

the handset that was required to be used by the communicator for ORO notifications.

The phone technician resolved this issue and the communicator was able to attempt to

continue the notification process. Again, notification via the bridge was unsuccessful

and the communicator asked the lead drill controller for guidance. The drill controller

prompted the communicator to continue with the procedure and attempt to dial the

OROs individually. This attempt was successful and the communicator made initial

contact with PEMA at 8:43 a.m., fifteen minutes after the UE declaration.

Secondly, inspectors observed that not all OROs were notified within 15 minutes of the

declared UE. Specifically, though initial contact was made with PEMA at 8:43 a.m.,

initial contact was not initiated with LCEMA and CCEMA until 22 minutes and 24 minutes

after the emergency declaration, respectively.

Inspectors observed the drill critique conducted on November 14, 2012 and noted these

deficiencies were not adequately captured. Specifically, Drill Objective 1.5 for the

control room emergency plan communicator states to perform timely notifications to

offsite authoritiesuntil relieved of this duty by the TSC and was evaluated by the

drill controllers as Met. CR 1643107 was generated stating that phone problems

challenged the ability of the emergency plan communicator to make the required

15 minute notification. However, the CR also mentioned that the notification to outside

agencies was successfully initiated just within the 15-minute time limit. Additionally,

inspectors reviewed the drill and exercise performance (DEP) PI opportunities for the

drill and noted that drill controllers evaluated the DEP PI opportunity for timely

notification of the UE as successful. There was no mention in the CR or drill critique

presentation that the second and third OROs were not notified within fifteen minutes

of the declared emergency or that equipment performance or controller intervention

potentially interfered with adequate observation of ERO performance.

Enclosure

22

For the first observation, inspectors reviewed NEI 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 6, and noted that page 46 of the guidance

states for sites with multiple agencies to notify, the notification is considered to be

initiated when contact is made with the first agency to transmit the initial notification

information. However, inspectors were concerned that the level of interaction between

the drill controller and the ERO member was sufficient to prevent adequate observation

and evaluation of performance. In particular, NEI 99-02 page 47 states that if a

controller intervenes (e.g., coaching, prompting) with the performance of an individual to

make an independent and correct classification, notification, or PAR, then that DEP PI

opportunity shall be considered a failure. In this case, inspectors determined, after

consultation with regional EP specialists, that it was incorrect for the evaluators to

determine the DEP PI opportunity was successful when controller intervention was

required to resolve the equipment failures. Inspectors reviewed the nature of the

equipment failures and determined that they were unique to the simulator such that there

was reasonable assurance the same deficiency could not exist in the plant control room

during an actual emergency.

For the second observation, inspectors determined the CR and the drill critique did not

correctly document that the crew had not met regulatory requirements associated with

notification of the second and third OROs following the emergency declaration.

Specifically, 10 CFR 50.47(b)(5) requires, in part, that procedures be established for

notification by the licensee of State and local response organizations. Additionally, 10

CFR 50, Appendix E, Section IV.D.3 requires, in part, that a licensee have the capability

to notify responsible State and local governmental agencies within 15 minutes of

declaring an emergency. IMC 0609 Appendix B classifies the function of notifying

OROs as a RSPS. This RSPS is further described in PPLs emergency plan and EP

implementing procedures and the OROs are defined as PEMA, LCEMA, and CCEMA.

Since initial notification was not made with all OROs within fifteen minutes of the

declared emergency, inspectors determined that an ERO performance deficiency

existed which was not adequately assessed and critiqued. PPL staff entered the critique

weakness into their CAP as CR 1648380.

Analysis. Inspectors determined that PPL staff not identifying a drill weaknesses related

to emergency notification during their drill critique was a performance deficiency that was

reasonably within their ability to foresee and prevent. The finding is more than minor

because it is associated with the ERO performance attribute of the EP corner-stone and

affected the cornerstone objective to ensure that the licensee is capable of implementing

adequate measures to protect the health and safety of the public in the event of a

radiological emergency. Specifically, PPL staff did not effectively identify a drill

weakness associated with an RSPS and caused a missed opportunity to identify and

correct a drill-related performance weakness.

The inspectors assessed the issue using the NRC IMC 0609 Appendix B, Emergency

Preparedness Significance Determination Process. Inspectors noted two examples

provided in IMC 0609 Appendix B table 5.14-1 that were similar to the performance

deficiency. First, an example of a loss of planning standard (PS) function occurs when

the critique process fails to identify a weakness associated with an RSPS that is

determined by the NRC to be a DEP Pl opportunity failure during a full-scale drill.

Second, an example of a degradation of PS function occurs when the critique process

fails to identify a weakness associated with a RSPS that is determined by the NRC to be

a DEP Pl successful opportunity during a full-scale drill. PPL not critiquing the untimely

Enclosure

23

notification met the NRC's definition of a weakness in a full-scale drill. However,

because of the unique nature of the equipment failures associated with the notification of

the first ORO, inspectors determined that not identifying and critiquing the drill weakness

only constituted a degradation of the PS function. Therefore the finding is characterized

as very low safety significance (Green).

The finding is related to the cross-cutting area of PI&R, CAP, in that PPL did not identify

an RSPS issue completely, accurately, and in a timely manner commensurate with the

safety significance. Specifically, during the critique of the full-scale drill conducted on

October 14, 2012, PPL staff did not recognize and critique that an RSPS was not met

and did not place this issue into the CAP until prompted by the inspectors questions.

P.1(a)

Enforcement. 10 CFR 50.54(q)(2) requires, in part, that a licensee shall follow and

maintain the effectiveness of an emergency plan that meets the requirements in

10 CFR 50, Appendix E and, for nuclear power reactor licensees, the planning standards

of 10 CFR 50.47(b). 10 CFR 50.47(b)(14) requires, in part, that periodic drills be

conducted to develop and maintain key skills, and deficiencies identified as a result of

drills be corrected. 10 CFR Part 50, Appendix E, section lV.F.2.g requires that all

training, including drills, shall provide for formal critiques in order to identify weak or

deficient areas that need correction. Additionally, it requires that any identified

weaknesses or deficiencies be corrected.

Contrary to the above, during the November 14, 2012, critique of the November 13,

2012, Susquehanna Steam Electric Station full-scale emergency drill, PPL did not

identify performance weaknesses. Specifically, PPL did not identify that timely

notification was not made with two of the OROs as required by regulatory requirements

and the SSES Emergency Plan. Additionally, PPL evaluated a performance indicator

opportunity as a success despite drill controller action precluding satisfactory

observation of ERO performance. PPL entered the drill critique deficiency into their

CAP as CR 1648380 and initiated action to correct the performance indicator deficiency.

Because this violation is of very low safety significance (Green) and PPL entered this

into their CAP, this violation is being treated as an NCV consistent with Section 2.3.2 of

the NRC Enforcement Policy. (NCV 05000387;388/2012005-03: Failure of Full-Scale

Drill Critique to Identify an RSPS Weakness)

2. RADIATION SAFETY

Cornerstone: Occupational/Public Radiation Safety (PS)

2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06 - 1 sample)

a. Inspection Scope

From November 5 to 9, 2012, the inspectors verified that gaseous and liquid effluent

processing systems are maintained so radiological discharges are properly reduced,

monitored, and released. The inspectors also verified the accuracy of the calculations

for effluent releases and public doses.

The inspectors used the requirements in 10 CFR Part 20; 10 CFR 50.35(a) TSs; 10 CFR

Part 50 Appendix A - Criterion 60, Control of Release of Radioactivity to the

Enclosure

24

Environment, and Criterion 64, Monitoring Radioactive Releases; 10 CFR 50

Appendix I, Numerical Guides for Design Objectives and Limiting Condition for

Operations (LCOs) to Meet the Criterion As Low as is Reasonably Achievable (ALARA)

for Radioactive Material in Light-Water-Cooled Nuclear Power Reactor Effluents;

10 CFR 50.75(g), Reporting and Recordkeeping for Decommissioning Planning;

40 CFR Part 141, Maximum Contaminant Levels for Radionuclides; 40 CFR Part 190,

Environmental Radiation Protection Standards for Nuclear Power Operations;

Regulatory Guide (RG) 1.109, Calculation of Annual Doses to Man from Routine

Releases of Reactor Effluents; RG 1.21, Measuring, Evaluating, Reporting Radioactive

Material in Liquid and Gaseous Effluents and Solid Waste; RG 4.1, Radiological

Environmental Monitoring for Nuclear Power Plants; RG 4.15, Quality Assurance for

Radiological Monitoring Programs; NUREG-1301 or 1302, Offsite Dose Calculation

Manual (ODCM) Guidance: Standard Radiological Effluent Controls; applicable Industry

standards; and PPL procedures required by Susquehannas TSs/ODCM as criteria for

determining compliance.

Inspection Planning and Program Reviews

Event Report and Effluent Report Reviews

The inspectors reviewed the SSES Radiological Effluent Release Reports for 2010 and

2011 to determine if the reports were submitted as required by the Offsite Dose

Calculation Manual (ODCM) and TSs. The inspectors reviewed anomalous results,

unexpected trends, and abnormal releases that were identified. The inspectors

determined if these effluent results were evaluated, were entered in the CAP, and were

adequately resolved.

The inspectors identified radioactive effluent monitor operability issues reported in

the Annual Radioactive Effluent Release Reports, and reviewed these issues and

determined if the issues were entered into the CAP and were adequately resolved.

ODCM and UFSAR Review

The inspectors reviewed the SSES UFSAR descriptions of the radioactive effluent

monitoring systems, treatment systems, and effluent flow paths to identify system design

features and required functions.

The inspectors reviewed changes to the SSES station ODCM made by PPL, since the

last inspection. When differences were identified, the inspectors reviewed the technical

basis or evaluations of the change and determined whether they were technically

justified and maintained effluent releases ALARA.

The inspectors reviewed documentation to determine if any non-radioactive systems that

have become contaminated were disclosed either through an event report or the ODCM.

The inspectors reviewed selected 10 CFR 50.59 evaluations and made a determination

if any newly contaminated systems had an unmonitored effluent discharge path to the

environment. The inspectors also reviewed whether it required revisions to the ODCM

to incorporate these new pathways and whether the associated effluents were reported

in accordance with RG 1.21.

Enclosure

25

Groundwater Protection Initiative (GPI) Program

The inspectors reviewed reported groundwater monitoring results and changes to PPLs

written program for identifying and controlling contaminated spills/leaks to groundwater.

Procedures, Special Reports, and Other Documents

The inspectors reviewed licensee event reports (LERs), event reports and/or special

reports related to the effluent program issued since the previous inspection to identify

any additional focus areas for the inspection based on the scope/breadth of problems

described in these reports.

The inspectors reviewed effluent program implementing procedures, including those

associated with effluent sampling, effluent monitor set-point determinations, and dose

calculations.

The inspectors reviewed copies of third party (independent) evaluation reports of the

effluent monitoring program since the last inspection to gather insights into the

effectiveness of the program.

Walkdowns and Observations

The inspectors walked down selected components of the gaseous and liquid discharge

systems to verify that equipment configuration and flow paths align with the descriptions

in the UFSAR and to assess equipment material condition. Special attention was made

to identify potential unmonitored release points, building alterations which could impact

airborne, or liquid, effluent controls, and ventilation system leakage that communicate

directly with the environment.

The inspectors reviewed effluent system material condition surveillance records, as

applicable, for equipment or areas associated with the systems selected for review that

were not readily accessible due to radiological conditions.

The inspectors walked down filtered ventilation systems to verify there are no degraded

conditions associated with high efficiency particulate air/charcoal banks, improper

alignment, or system installation issues that would impact the performance or the

effluent monitoring capability of the effluent system.

As available, the inspectors observed selected portions of the routine processing and

discharge of radioactive gaseous effluent to verify that appropriate treatment equipment

was used and the processing activities align with discharge permits.

The inspectors determined that PPL had not made any changes to their effluent release

paths.

As available, the inspectors observed selected portions of the routine processing and

discharge of liquid waste. The inspectors verified that appropriate effluent treatment

equipment is being used and that radioactive liquid waste is being processed and

discharged in accordance with procedures.

Enclosure

26

Sampling and Analyses

The inspectors selected three effluent sampling activities, and assessed whether

adequate controls have been implemented to ensure representative samples were

obtained.

The inspectors selected three effluent discharges made with inoperable effluent

radiation monitors to verify that controls are in place to ensure compensatory sampling

is performed consistent with the TSs/ODCM and that those controls are adequate to

prevent the release of unmonitored liquid and gaseous effluents.

The inspectors determined whether the facility is routinely relying on the use of

compensatory sampling in lieu of adequate system maintenance, based on the

frequency of compensatory sampling since the last inspection.

The inspectors reviewed the results of the inter-laboratory and intra-laboratory

comparison program to verify the quality of the radioactive effluent sample analyses.

The inspectors also assessed whether the intra- and inter-laboratory comparison

program includes hard-to-detect isotopes, as appropriate.

Instrumentation and Equipment

Effluent Flow Measuring Instruments

The inspectors reviewed the methodology that PPL uses to determine the effluent stack

and vent flow rates to verify that the flow rates are consistent with TSs/ODCM and

UFSAR values. The inspectors reviewed the differences between assumed and actual

stack and vent flow rates to ensure that they do not affect the calculated results of public

dose.

Air Cleaning Systems

The inspectors assessed whether surveillance test results for TS-required ventilation

effluent discharge systems meet TS acceptance criteria.

Dose Calculations

The inspectors reviewed all significant changes in reported dose values compared to the

previous radioactive effluent release report to evaluate the factors which may have

resulted in the change.

The inspectors reviewed more than three radioactive liquid and no gaseous waste

discharge permits, as no batch releases were made, to verify that the projected doses to

members of the public were accurate and based on representative samples of the

discharge path. The inspectors reviewed the analysis of continuous releases.

The inspectors evaluated the methods used to ensure that all radionuclides in the

effluent stream source term are included, within detectability standards. The review

included the current waste stream analyses to ensure hard-to-detect radionuclides are

included in the effluent releases.

Enclosure

27

The inspectors reviewed changes in PPL methodology for offsite dose calculations since

the last inspection to verify the changes are consistent with the ODCM and RG 1.109.

The inspectors reviewed meteorological dispersion and deposition factors used in the

ODCM and effluent dose calculations to ensure appropriate dispersion/deposition factors

are being used for public dose calculations.

The inspectors reviewed the latest Land Use Census to verify changes that affect public

dose pathways have been factored into the dose calculations and environmental

sampling/analysis program.

The inspectors evaluated whether the calculated doses are within 10 CFR 50, Appendix I,

Numerical Guides for Design Objectives and Limiting Condition for Operations (LCOs) to

Meet the Criterion As Low as is Reasonably Achievable (ALARA) for Radioactive

Material in Light-Water-Cooled Nuclear Power Reactor Effluents; and TS dose criteria.

The inspectors reviewed records of any abnormal gaseous or liquid tank discharges to

ensure the abnormal discharge was monitored by the discharge point effluent monitor.

Discharges made with inoperable effluent radiation monitors, or unmonitored leakages

were reviewed to ensure that an evaluation was made of the discharge to account for

the effluent release and were included in the calculated doses to the public.

Groundwater Protection Initiative (GPI) Implementation

The inspectors reviewed monitoring results of the voluntary Nuclear Energy Institute GPI

to determine if PPL has implemented the GPI as intended.

For anomalous results or missed samples, the inspectors assessed whether PPL has

identified and addressed deficiencies through its CAP.

The inspectors reviewed identified leakage or spill events and entries made into PPL's

decommissioning files. The inspectors reviewed evaluations of leaks or spills, and

reviewed the effectiveness any remediation actions. The inspectors reviewed onsite

contamination events involving contamination of groundwater and assessed whether the

source of the leak or spill was identified and isolated/terminated.

For unmonitored spills, leaks, or unexpected liquid or gaseous discharges, the

inspectors assessed whether an evaluation was performed to determine the type and

amount of radioactive material that was discharged by: assessing whether sufficient

radiological surveys were performed to evaluate the extent of the contamination and

assessing whether a survey/evaluation has been performed; and determining whether

PPL completed offsite notifications, as provided in its GPI implementing procedures.

The inspectors did not review any evaluation of discharges from onsite surface water

bodies as none currently exist at the site.

The inspectors assessed whether on-site groundwater sample results and a description

of any significant on-site leaks/spills into groundwater for each calendar year are

documented in the Annual Radioactive Effluent Release Report.

For significant, new effluent discharge points, such as significant or continuing leakage

to groundwater that continues to impact the environment, the inspectors evaluated

Enclosure

28

whether the licensees ODCM was updated to include the dose calculation method for

the new release point and the associated dose calculation methodology.

Problem Identification and Resolution

Inspectors assessed whether problems associated with the effluent monitoring and

control program were being identified by the PPL staff at an appropriate threshold and

properly addressed for resolution in the PPLs licensee CAP. In addition, the inspectors

evaluated the appropriateness of the corrective actions for a selected sample of

problems documented.

b. Findings

No findings were identified.

2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and

Transportation (71124.08 - 1 sample)

a. Inspection Scope

This area was inspected to verify the effectiveness of PPLs programs for processing,

handling, storage, and transportation of radioactive material. The inspectors used the

requirements of 10 CFR Parts 20, 61, and 71, and 10 CFR Part 50, Appendix A, -

Criterion 63, Monitoring Fuel and Waste Storage, and PPL procedures required by the

TSs/Process Control Program (PCP) as criteria for determining compliance.

The inspectors reviewed the solid radioactive waste system description in the FSAR,

the PCP, and the recent radiological effluent release report for information on the types,

amounts, and processing of radioactive waste disposed.

The inspectors reviewed the scope of quality assurance (QA) audits performed for this

area since the last inspection. The inspectors reviewed the results of the audits

performed since the last inspection of this program and evaluated the adequacy of

PPLs corrective actions for issues identified during those audits.

The inspectors observed areas where containers of radioactive waste were stored, and

verified that the containers were labeled in accordance with 10 CFR 20.1904, Labeling

Containers, or controlled in accordance with 10 CFR 20.1905, Exemptions to Labeling

Requirements, as appropriate.

The inspectors verified that the radioactive materials storage areas were controlled

and posted in accordance with the requirements of 10 CFR Part 20, Standards for

Protection Against Radiation. For materials stored or used in the controlled or

unrestricted areas, the inspectors verified that they were secured against unauthorized

removal and controlled in accordance with 10 CFR 20.1801, Security of Stored

Material, and 10 CFR 20.1802, Control of Material not in Storage, as appropriate.

The inspectors verified that PPL had established a process for monitoring the impact of

long-term storage (e.g., buildup of any gases produced by waste decomposition,

chemical reactions, container deformation, loss of container integrity, or re-release of

free-flowing water) sufficient to identify potential unmonitored, unplanned releases, or

Enclosure

29

nonconformance with waste disposal requirements. The inspectors verified that there

were no signs of swelling, leakage, or deformation.

The inspectors walked down accessible portions of liquid and solid radioactive waste

processing systems to verify and assess that the current system configuration and

operation agree with the descriptions in the FSAR, offsite dose calculation manual,

and PCP.

The inspectors identified radioactive waste processing equipment that was not

operational and/or was abandoned in place, and verified that PPL had established

administrative and/or physical controls to ensure that the equipment would not contribute

to an unmonitored release path and/or affect operating systems or be a source of

unnecessary personnel exposure. The inspectors verified that PPL had reviewed the

safety significance of systems and equipment abandoned in place in accordance with

10 CFR 50.59, Changes, Tests, and Experiments.

The inspectors reviewed the adequacy of any changes made to the radioactive waste

processing systems since the last inspection. The inspectors verified that changes from

what was described in the FSAR were reviewed and documented in accordance with

10 CFR 50.59, as appropriate.

The inspectors identified processes for transferring radioactive waste resin and/or sludge

discharges into shipping/disposal containers. The inspectors verified that the waste

stream mixing, sampling procedures, and methodology for waste concentration

averaging were consistent with the PCP, and provided representative samples of the

waste product for the purposes of waste classification as described in 10 CFR 61.55,

Waste Classification.

For those systems that provide tank recirculation, the inspectors verified that the tank

recirculation procedure provided sufficient mixing.

The inspectors verified that the licensees PCP correctly described the current methods

and procedures for dewatering waste.

The inspectors identified radioactive waste streams, and verified that PPLs radio-

chemical sample analysis results were sufficient to support radioactive waste

characterization as required by 10 CFR Part 61, Licensing Requirements for Land

Disposal of Radioactive Waste. The inspectors verified that PPLs use of scaling

factors and calculations to account for difficult-to-measure radionuclides was technically

sound and based on current 10 CFR Part 61 analyses.

For the waste streams identified above, the inspectors verified that changes to plant

operational parameters were taken into account to (1) maintain the validity of the waste

stream composition data between the annual or biennial sample analysis update, and

(2) verified that waste shipments continued to meet the requirements of 10 CFR Part 61.

The inspectors verified that PPL had established and maintained an adequate QA

program to ensure compliance with the waste classification and characterization

requirements of 10 CFR 61.55, Waste Classification and 10 CFR 61.56, Waste

Characteristics.

Enclosure

30

The inspectors reviewed the records of shipment packaging, surveying, labeling,

marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping

papers provided to the driver, and verification of shipment readiness. The inspectors

verified that the requirements of any applicable transport cask certificate of compliance

had been met. The inspectors verified that the receiving licensee was authorized to

receive the shipment packages.

The inspectors determined that the shippers were knowledgeable of the shipping

regulations and that shipping personnel demonstrated adequate skills to accomplish the

package preparation requirements for public transport with respect to PPLs response to

NRC Bulletin 79-19, Packaging of Low-Level Radioactive Waste for Transport and

Burial, and 49 CFR Part 172, Hazardous Materials Table, Special Provisions,

Hazardous Materials Communication, Emergency Response Information, Training

Requirements, and Security Plans, Subpart H, Training. The inspectors verified that

PPLs training program provided training to personnel responsible for the conduct of

radioactive waste processing and radioactive material shipment preparation activities.

The inspectors identified non-excepted package shipment records and verified that the

shipping documents indicate the proper shipper name; emergency response information

and a 24-hour contact telephone number; accurate curie content and volume of material;

and appropriate waste classification, transport index, and shipping identification number.

The inspectors verified that the shipment placarding was consistent with the information

in the shipping documentation.

The inspectors verified that problems associated with radioactive waste processing,

handling, storage, and transportation, were being identified by PPL at an appropriate

threshold, were properly characterized, and were properly addressed for resolution in

PPLs CAP. The inspectors verified the appropriateness of the corrective actions for

a selected sample of problems documented by PPL that involve radioactive waste

processing, handling, storage, and transportation. PPL generated six CRs to document

material condition deficiencies identified during this inspection.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification) (71151 - 8 samples)

.1 Mitigating Systems Performance Index (MSPI) (4 samples)

a. Inspection Scope

The inspectors reviewed PPLs submittal of the MSPI for the following systems for the

following systems for the period of October 1, 2011 through September 30, 2012:

Units 1 and 2, emergency alternating current power systems (MS06)

Units 1 and 2, RHR systems (MS09)

Enclosure

31

To determine the accuracy of the performance indicator data reported during those

periods, the inspectors used definitions and guidance contained in Nuclear Energy

Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6. The inspectors also reviewed PPLs operator narrative logs,

CRs, mitigating systems performance index derivation reports, event reports, and

NRC integrated IRs to validate the accuracy of the submittals.

b. Findings

No findings were identified.

.2 Radiological Effluent TS/Offsite Dose Manual (ODCM) Radiological Effluent

Occurrences (1 sample)

a. Inspection Scope

During November 5-9, 2012, the inspectors sampled PPL submittals for the radiological

effluent TS/ODCM radiological effluent occurrences PI (PR01) for the period from the 1st

quarter 2011 through 4th quarter 2011. The inspectors used PI definitions and guidance

contained in the Nuclear Energy Institute Document 99-02, Regulatory Assessment PI

Guideline, Revision 6, dated October 2009, to determine if the PI data was reported

properly during this period.

The inspectors reviewed PPLs corrective action report (AR) database and selected

individual reports generated since this indicator was last reviewed to identify any

potential occurrences such as unmonitored, uncontrolled, or improperly calculated

effluent releases that may have impacted offsite dose. The inspectors reviewed

gaseous and liquid effluent summary data and the results of associated offsite dose

calculations for selected dates between 1st quarter 2011 through 4th quarter 2011, to

determine if indicator results were accurately reported. The inspectors also reviewed

PPLs methods for quantifying gaseous and liquid effluents and determining effluent

dose.

b. Findings

No findings were identified.

.3 Emergency Preparedness (3 samples)

a. Inspection Scope

The inspectors reviewed data for the three EP Performance Indicators (PI), which are:

(1) Drill and Exercise Performance (ER01); (2) Emergency Response Organization Drill

Participation (ER02); and, (3) Alert and Notification System Reliability (ER03). The last

NRC EP inspection at Susquehanna was conducted in the fourth quarter of 2011.

Therefore, the inspectors reviewed supporting documentation from EP drills and

equipment tests from the fourth quarter of 2011 through the third quarter of 2012 to

verify the accuracy of the reported PI data. The review of the PIs was conducted in

accordance with NRC Inspection Procedure 71151. The acceptance criteria

documented in NEI 99-02, Regulatory Assessment Performance Indicator Guidelines,

Revision 6, was used as reference criteria.

Enclosure

32

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution (71152)

.1 Routine Review of Problem Identification & Resolution (PI&R) Activities

a. Inspection Scope

As required by Inspection Procedure (IP) 71152, Problem Identification and Resolution,

the inspectors routinely reviewed issues during baseline inspection activities and plant

status reviews to verify that PPL entered issues into the CAP at an appropriate

threshold, gave adequate attention to timely corrective actions, and identified and

addressed adverse trends. In order to assist with the identification of repetitive

equipment failures and specific human performance issues for follow-up, the inspectors

performed a daily screening of items entered into the CAP and periodically attended CR

screening meetings.

b. Findings

No findings were identified.

.2 Semi-Annual Trend Review (1 sample)

a. Inspection Scope

The inspectors performed a semi-annual review of site issues, as required by IP 71152,

Problem Identification and Resolution, to identify trends that might indicate the

existence of more significant safety issues. In this review, the inspectors included

repetitive or closely-related issues that may have been documented by PPL staff outside

of the CAP, such as trend reports, performance indicators, major equipment problem

lists, system health reports, maintenance rule assessments, and maintenance or CAP

backlogs. The inspectors also reviewed PPLs CAP database for the third and fourth

quarters of 2012 to assess CRs written in various subject areas (equipment problems,

human performance issues, etc.), as well as individual issues identified during the NRCs

daily CR review (Section 4OA2.1). The inspectors reviewed PPL staffs quarterly trend

reports for the first three quarters of 2012, conducted under NDAP-QA-0710, Station

Trending Program, to verify that PPL personnel were appropriately evaluating and

trending adverse conditions in accordance with applicable procedures.

b. Findings and Observations

Evaluation of Trends Related to CAP Evaluations (P.1(c)).

PPL staff has designated CAP as a gap to excellence and a subset of the metrics PPL

uses to monitor CAP progress are attributable to the P.1(c) Evaluation substantive

cross-cutting issue (SCCI). Additionally, PPL completed an evaluation (CR 1633700)

after the NRCs 2012 mid-cycle assessment letter (ML12248A066), dated September 4,

2012, continued the SCCI. The evaluation concluded there were no additional

performance gaps that have not been identified and addressed with corrective actions.

Enclosure

33

The evaluation used three performance indicators (PIs) (discussed below) to confirm

PPL staffs conclusion. The inspectors performed a review of these metrics, and other

PIs deemed by the inspectors to be pertinent to the SCCI, to determine what standards

PPL had established and whether corrective actions were identified as a result of PPLs

monitoring of their internal metrics.

Quality of CARB Reviewed CR Evaluations (SL52) - This metric measures the

quality of CARB-reviewed root cause analyses (RCAs) and ACEs and plots both

the six-month average and the monthly percent rejection rate. The metric has

been White for the duration of 2012. In September, PPL concluded that the

improving trend had stalled the past several months. In October and December,

PPL concluded that the trend was slowly and consistently improving. During

review, the inspectors questioned the rise in evaluation rejection rate from 12.5

percent in both July and August, to 25 percent in September, to 50 percent for

October and November, without a corresponding decline in overall metric

performance. PPL examined the input data to the PI and determined that the

metric was incorrect. PPL entered this issue into their CAP (CR 1657686). The

PI was revised and while the trend for rejection rate percentages changed, the

overall metric color did not change.

Effectiveness Review Results (GWE40) - This metric was Green for October

after being White since January 2012. October data showed 9 of 10

effectiveness reviews rated as being effective. PPL changed the thresholds in

June 2011 to be more challenging and the rolling average was reduced from 12

to 6 months. In response to inspector questioning of SL52 accuracy, PPL also

reviewed the data for this PI and identified that this PI was also incorrect. PPL

incorporated additional effectiveness reviews that had been unaccounted for,

including five effectiveness reviews rated as being ineffective. The incorporation

of this data caused the revised PI to be changed from Green to Yellow. PPL

entered this issue into their CAP (CR 1659032).

Repeat of Significant Events (SL90) - This PI is based on the same root cause

occurring twice in a three-year rolling period and has been White for 2012. The

PI is based, in part, on a cognitive review of root causes and is expected to be

reduced to a one-year rolling average in 2013.

CAP Engagement (SL82) - This metric, covering Performance Improvement

Review Board (PIRB), CAP Health, Management Review Committee (MRC), and

CARB meeting attendance by senior management, has been consistently Green.

Notwithstanding, PPL staffs November update documented that senior

leadership struggles during outage periods for oversight of screening, MRC,

CARB, and CAP recovery meetings. The update stated that while this metric is

monitored during outages, it does not have any bearing on establishing a

recovery plan since the metric is extremely impacted by outages. The

inspectors noted that a substantial amount of 2012 was spent in outages to

include the Unit 1 refueling and Unit 2 maintenance outages in the spring, the

Unit 1 shutdown for pressure boundary leakage in the summer, fall maintenance

outages on both Units, and two Unit 2 reactor scrams in December. Additionally,

the inspectors noted that PIRB and CAP Health were consistently above the

average and most often had a score over 200 percent while MRC, a daily

meeting, was consistently less than 100 percent. MRC engagement remained

Enclosure

34

less than the goal at 26 percent in October and 68 percent in November. PPL

staff documented that no recovery plan is necessary.

Operability Determinations - The inspectors observed that PPL does not have

metrics to monitor effectiveness of Operability Determinations. The inspectors

noted that weaknesses in Operability Determinations resulted in several NRC

findings with a P.1(c) cross cutting aspect that contributed to the SCCI and

corrective actions have been developed to address weakness in this area.

Finally, both the Biennial PI&R inspection and a fourth quarter inspection sample

identified ACEs that did not evaluate deeper than the direct cause, contrary to station

procedures. Despite this, Departmental Corrective Action Review Board (DCARB)

scores were relatively high, none of the DCARBs were cross-functional, and all five

ACEs were not reviewed by CARB. PPL subsequently identified two additional ACEs

with similar issues. PPL has implemented cross-functional DCARBs as an interim

measure that will be evaluated for effectiveness.

Review of Trend Related to Procedure Quality (H.2(c))

At the station level, PPL staff has designated procedure quality, use, and adherence as

a gap to excellence. A subset of the metrics PPL uses to monitor progress in this area is

attributable to the procedure quality (H.2.(c)) substantive cross-cutting issue. The

inspectors performed a review of the applicable metrics to determine what standards

PPL had established and whether corrective actions were identified as a result of PPLs

monitoring of their internal metrics.

Procedure Request Average Age by Priority (SL104) - This metric is based on

priority 1 and 2 requests exceeding 180 days. The metric was Red from July

through October 2012. Of the four levels of Operations Procedure Group (OPG)

priority levels, there was a rise in the number of Level 3 and Level 4 requests by

age and a drop in the monthly number of Level 2 requests by age. Of the four

levels of Maintenance Procedure Group (MPG) priority levels, there was a

general rise in the number of Level 2 requests by age and general stability

without reduction in the number of Level 3 and 4 requests by age. Recovery

plans for this metric include procedure action item burndown curves that target a

total of 590 procedure requests by June 2013 and 350 by the end of 2013. The

recovery plan for the MPG concluded that resource issues and a large number of

incoming items resulted in the high percentage of high priority items. There were

also open positions in the organization that PPL management anticipated would

assist in backlog reduction, once filled.

Incoming Procedure Change Request (SL106) - This metric is based on the total

number of change requests with a distinct mechanism that each procedure

affected by a request is counted individually. The metric has been consistently

Green with a threshold of 100 change requests.

Procedure Quality Issues Identified (SL109) - This metric was changed in June

2012 to represent both technical and quality procedure issues. The metric has

been predominantly Red based on technical quality procedure issues exceeding

60 per month. The BOP procedures were not yet prioritized and incorporated

into this PI. The Green threshold is less than or equal to 40 per month. PPL

Enclosure

35

staff generated OPG and MPG recovery plans that consist of burndown curves

through the end of 2013.

Procedure Request Total Backlog Quantity (SL110) - This metric has been Red

from June through October 2012 based on the total backlog (technical, quality,

enhancement, and editorial) exceeding 1500. PPL staffs assessment stated that

the industry average for a two-unit site is 1200 items. The BOP procedures were

not yet prioritized and incorporated into this PI.

Emerging Trend in Work Control (H.3(a))

There was one NRC finding in each of the first three quarters of 2012 in this cross-

cutting area. In response, PPL staff conducted a common-cause analysis (CCA) (CR

1616738) that was not CARB-approved by the end of the inspection period. The

inspectors had one observation regarding the corrective actions planned.

The stations lowest work levels, work lists, were partly responsible for two of the three

NCVs. The lower threshold of these work list items enabled some work activities to

initiate without appropriate management or programmatic review. Corrective actions

regarding these work lists are due greater than a year from when the initial NCV with an

H.3(a) aspect was issued.

Emerging Trend in Preparations for Adverse Weather

During a winter readiness inspection sample, the inspectors noted that the preparatory

checklist in NDAP-00-0024, Winter Operation Preparations, Revision 18, had not been

completed by November 1 of each year, as required, from 2008 through 2012 (CRs

1088314, 1198388, 1323433, 1489677, and 1638078). Additionally, the summer

operations preparation procedure, NDAP-00-0334, was not completed prior to May 15,

2012 as required (CR 1575139). Finally, in the 2012 third quarter inspection report, the

NRC issued a Green NCV regarding an inadequate procedure for high winds. The

inspectors concluded that there is an adverse trend in PPL personnel preparing for

seasonal and adverse weather conditions in a timely manner.

Emerging Trend in CAP- Problem Identification (P.1(a))

The inspectors observed an issue with respect to problems being identified and placed

into the CAP based on recent inspection results.

During implementation of Temporary Instruction (TI)-187 and TI-188, inspector obser-

vations during a walkdown of the Unit 2 HPCI room floor degradations were initially

assessed by Engineering as not warranting CAP entry. Inspectors reviewed NDAP-QA-

0702, Action Request and Condition Report Process, and determined the issues met the

station defined threshold for CR generation. Following additional discussions with PPL

staff, the items were entered in the CAP.

Three NCVs in 2012 had aspects of problem identification. The first had a cross-cutting

aspect in P.1.(a) based on personnel not entering issues into the CAP when they

discovered a lack of procedural guidance, qualification, and non-compliance with

instructions associated with the motor-operated valve program (NCV 2012002-01).

Enclosure

36

The second had a cross-cutting aspect in P.1(a) based on PPL not entering procedural

issues into the CAP during a periodic procedure review or after inspectors provided the

issues to PPL staff (NCV 2012004-01). The third had a cross-cutting aspect in P.1(a)

and is documented in this report (Section 1EP6). Based on having three findings with

the same cross-cutting aspect in a four quarter period, PPL generated CR 1664721 to

perform a CCA on the collective issues.

Inspectors identified a missed risk assessment when one division of ESW was removed

from service on an operable EDG to support testing. The issue was communicated to

the work week manager who confirmed that the item had not been included in the

stations risk assessment; however, when it was added, the overall risk to the station

remained Green. Since this issue was a minor violation of 10 CFR 50.65(a)(4), it was

required to be entered into the stations CAP by PPLs CAP procedures. The issue was

not entered into the CAP until inspectors discussed the issue with senior PPL

management.

Inspectors reviewed an ACE on TS SR 3.4.2.1 requirements that concluded that the

stations performance was not in strict compliance with the SR. No CR was generated

to ensure corrective actions were taken to restore compliance until identified by the

inspectors. PPL staff took subsequent actions to revise the ACE.

Emerging Trend in Maintenance Rule Program Implementation

The inspectors noted challenges in PPL staffs implementation of the Maintenance Rule.

Maintenance Rule Expert Panel (MREP) backlog - In August 2012, the

inspectors became aware of a 17-item backlog in MRFFs that required MREP

review and that no MREP meetings occurred from April through August 2012.

PPL staff attributed the cause to extended plant outages and limited, qualified

expert panel members. This condition had existed from July 2011 when CR

1437589 documented the same situation. Additionally, PPL staff identified that

the station routinely failed to generate actions to track MREP review of the

MRFFs. In response, PPL management took action to qualify additional MREP

members and held six MREP meetings from September to the end of 2012.

Notwithstanding, the inspectors concluded the problem has not been sufficiently

resolved. For example, there were still five MRFFs requiring MREP review that

were in excess of the 60-day procedural requirement. This included one MRFF

on an inboard D MSIV LLRT with an MREP due date ten months after

identification. Inspectors identified two additional MRFFs that both exceeded the

60 day guideline and did not have associated action item for MREP review.

Scoping - Inspectors identified that the ability to substitute the E EDG for other

EDGs was not scoped into the Maintenance Rule despite being used in EOPs

(CR 1630387).

Timeliness of 10 CFR 50.65(a)(1) classification - In the discussion of the

Maintenance Rule NCV in Section 1R12 of this report, there was approximately a

year delay for a RCIC system issue designated as a MRFF to be reviewed by the

MREP. As a result, it took over a year before the system was reclassified as

(a)(1). Additionally, in the summer of 2012, the inspectors identified that PPL

staff had not classified Unit 2 RCIC as an a(1) system despite meeting the

Enclosure

37

performance criteria in the summer of 2011 (CR 1619848). The system was

subsequently presented to MREP in September of 2012 where it was classified

as (a)(1). In both cases, the delays in the review of issues by the MREP resulted

in actions to reclassify the systems to a(1) and establishment of goals as

required by 10 CFR 50.65(a)(1) to be untimely.

Quality of MPFF determinations - This report documents an NRC-identified

violation of 10 CFR 50.65(a)(2) which occurred when a MRFF was

inappropriately classified as not maintenance preventable in Section 1R12.

Additionally, inspectors reviewed an ACE for a gasket failure in the control room

emergency outside air supply (CREOAS) system which concluded that no vendor

guidance for periodic replacement existed and determined the MRFF was not

maintenance preventable. Inspectors reviewed the vendor manual and identified

that it did in fact provide recommendations for inspection and periodic

replacement. This resulted in the issue becoming an MPFF and required a

revision to the ACE. The CREOAS system remained in a(2); therefore, the issue

was determined to be of minor safety significance.

.3 Annual Sample - 1A Reactor Recirculation Pump Suction Decontamination Flange

Weld Though-Wall Leak (1 Sample)

a. Inspection Scope

The inspectors assessed the adequacy of and associated corrective actions from the

root cause analysis (RCA) for the development of a through wall leak of the Unit 1 A

reactor recirculation pump suction decontamination flange weld VRR-B31-1-14F. The

inspectors reviewed the RCA report (CR 1589390), to determine the root cause and

contributing causes for the through wall leak, and the adequacy and status of corrective

actions.

The inspectors assessed PPL staffs problem identification threshold, cause analyses,

extent of condition reviews, compensatory actions, and the prioritization and timeliness

of corrective actions to determine whether PPL staff was appropriately identifying,

characterizing, and correcting problems associated with this issue and whether the

planned or completed corrective actions were appropriate. The inspectors compared

the actions taken to the requirements of PPLs CAP and 10 CFR 50 Appendix B. In

addition, the inspectors conducted interviews with the root cause team leader, and

other engineering and operations personnel who were familiar with the event and the

investigation.

b. Findings

Introduction. A self-revealing Green NCV of 10 CFR 50, Appendix B, Criterion III,

Design Control, was identified related to the development of a through-wall leak of

the Unit 1 A reactor recirculation pump suction line decontamination flange weld. This

through-wall leak resulted in an unexpected increase in unidentified drywell leak rate and

a shutdown of Unit 1 on June 19, 2012, in order to make repairs. Specifically, PPL

personnel used an incorrect value for stress intensification factor in the vibration analysis

in 2004 to support an extended power uprate (EPU). When the correct stress intensi-

fication factor was used, American Society of Mechanical Engineers (ASME) OM-3 code

limits for endurance and fatigue stress were exceeded. The through-wall leak resulted in

Enclosure

38

pressure boundary leakage in excess of TS 3.4.4 limits from approximately June 16 to

June 19, 2012.

Discussion. Operators commenced a reactor startup for Susquehanna Unit 1 from a

refueling outage on June 7, 2012. From plant startup until June 15, the drywell

unidentified leak rate slowly increased to 0.13 gallons per minute (gpm). On June 16,

operators observed a step increase in the unidentified leak rate from 0.13 to 0.50 gpm

was observed. Unidentified leak rate continued to trend upward over the next several

days to a maximum of 1.80 gpm. On June 18, PPL management made the decision to

conduct a controlled plant shutdown of Unit 1 due to this increasing trend in unidentified

drywell leakage and drywell pressure. On June 19, Unit 1 was shutdown and a through-

wall crack was identified on 1A reactor recirculation pump suction decontamination

flange weld, VRR-B31-1-14F. Investigation revealed that a through-wall cyclic fatigue-

driven circumferential crack measuring 3 1/8 outside diameter (OD) and 2 5/8 inside

diameter (ID), initiated from the outside diameter, was the source of the leakage. In

addition, an axial, intergranular stress corrosion and cracking (IGSCC)-driven crack was

also found. However, that crack had been arrested in the weld material and was not

through-wall.

The decontamination line is a flanged connection provided to facilitate decontamination

of the recirculation system. Connections are provided in each recirculation loop on the

suction and discharge side of the pump inboard of the pump suction and discharge

valves. These connections are arranged for attachment of temporary piping to permit

flushing and decontamination of the pump and adjacent piping. The suction line

connection was an unsupported four inch flanged line.

PPL calculated the natural frequency of this line to be 129.6 Hz and the primary

frequency of vibration is 128.5 Hz. These frequencies are in the range of vibrations

experienced at the high end of the design operating range of the reactor recirculation

pumps. At these frequencies, the decontamination flange pipe is exposed to large

bending moments and stresses in the decontamination pipe branch connection. The

primary concern is the five-times (5X) vane passing frequency developed from the

recirculation pump when operating at pump speeds greater than 1515 rpm and system

flow rates greater than 103 Mlbm/hr.

In 1995, following the Unit 1 stretch power uprate (5 percent), flow rates of up to 108

Mlbm/hr were included in the new power to flow envelope. General Electric (GE) testing

programs in June 1994 following the same power uprate on Unit 2, identified abnormal

increases in RCS system vibrations at recirculation pump speed of 1570 to 1580 rpm.

These vibrations were generated by the 5X vane pass frequency of the recirculation

pumps. This was the subject of NRC Information Notice (IN) 95-16, Vibration Caused

by Recirculation Flow in a Boiling Water Reactor. However prior to 2001, recirculation

pumps were not operated above 1480 rpm by procedure. Following a power uprate in

2001, PPLs procedures were revised to authorize flow rates of up to 104 Mlbm/hr.

The PPL RCA team discovered, in 2004, PPL had contracted an outside engineering

firm to recalculate the vibrations stresses on the RCS piping systems in preparation for

an EPU. PPL provided the weld profiles for the welds within the reactor recirculation

piping system to the contractor to perform this analysis. PPL procedure, NDAP-QA-

1208, Control of Welding, contained the PPL specifications for the weld and the

specifications for in-service inspection (ISI) of girth butt welds which required welds in

Enclosure

39

stainless steel material to be essentially flush. Weld detail P5 of NDAP-QA-1208

illustrated the specification. However, the weld profile for weld VRR-B31-1-14F was not

consistent with this specification. This weld did not meet the ASME design requirements

for a flush weld; therefore, a stress intensification factor of 1.8 vice 1.1 needed to be

applied to determine the stresses felt by the weld. However, the PPL RCA team

discovered that the contractor did not identify that the weld was not flush and used the

incorrect stress intensification factor. This resulted in an incorrect conclusion that

alternating stresses due to vibrations were within specification and ASME code fatigue

curve values at 1011 cycles were also within specification yielding an infinite life with an

input frequency of 128.5 Hz.

The decontamination lines were instrumented for post EPU testing and vibrations limits

were established based upon the 2004 piping stress calculations. In July of 2010,

measured peak acceleration exceeded the level 2 vibration limits established. However,

the action for exceeding level 2 limits was to review the measured accelerations data

and resulting stresses against the stress limits established in the 2004 calculation. As a

result PPL determined the test data to have been within limits which supported

continued operations.

Following the discovery of the through-wall leak in 2012, PPL contracted a vendor and

provided them with the 2004 weld profile and specifications and requested that they

recalculate the stresses for VRR-31-1-14F and compare the results to the data taken

during the 2010 EPU. Using the proper stress intensification factor, the vendor

determined the ASME OM-S/G-2009 Part 3 stress limit was 10,880 psi, and the stresses

measured during EPU acceptance testing were 13,674 psi (approximately 26 percent

greater than the endurance limit). Likewise, the ASME fatigue curve values at 1011

cycles was recalculated for the measured stresses which calculated an expected lifetime

of only 4.9 years at a frequency of 128.5 Hz. These results would not have justified

continued operation in 2010 and corrective actions would have had to be taken. Correct

calculations could have precluded the weld failure.

PPLs corrective actions included, modifying the length of the 1A reactor recirculation

pump suction decontamination flange to change the natural frequency of the line such

that it was no longer within the operating range of the reactor recirculation pumps, the

1B reactor recirculation was also modified. Unit 2s reactor recirculation pump suction

decontamination flanges were reviewed and their natural frequencies were found to be

above the operating range of the reactor recirculation pumps and the post EPU testing

data confirmed this. Extent of condition reviews included identifying other susceptible

components, conducting volumetric examinations of those welds, reviewing the piping

stress analysis weld data to determine if any addition welds were mischaracterized as

being flush.

The crack resulted in an unidentified leak rate of 1.8 gpm at the time the unit was

shutdown. The critical flaw size for structural integrity of the flange was calculated to be

a crack measuring 7.7 and the crack discovered was 3 1/8 long. The TS limit for

unidentified leakage is 5.0 gpm; however, a through-wall leak from a weld is considered

pressure boundary leakage and the TS limit for pressure boundary leakage is zero.

Thus, Susquehanna Unit 1 had operated in a condition prohibited by TSs. Notwith-

standing, PPLs evaluation determined that the flaw characterization was such that

complete failure could not have resulted in leakage that exceeded the leak rate for a

small break loss of coolant accident (LOCA).

Enclosure

40

Analysis. PPL not identifying weld VRR-B31-1-14F was not flush and applying the

improper stress intensification factor in accordance with the ASME code in 2004 was a

performance deficiency within PPLs ability to foresee and correct. The performance

deficiency was reviewed using IMC 0612, Appendix B, Issue Screening, and was

determined to be more than minor because it affected the Initiating Events Cornerstone

attribute of design control. The issue adversely affected the associated cornerstone

objective of limiting the likelihood of those events that upset plant stability and challenge

critical safety functions during shutdown as well as power operations. The finding was

evaluated using Section A of IMC 0609 Appendix A, Exhibit 1, Initiating Events

Screening Questions. Since the finding result could not have reasonably exceeded the

leak rate for a small LOCA and did not likely affect other systems used to mitigate a

LOCA resulting in a total loss of their function (e.g., Interfacing System LOCA), the

finding screened to very low safety significance (Green). This finding was determined to

not be indicative of current performance since the performance deficiency occurred in

2004 and procedures and training are in place that would have precluded the issue.

Thus no cross-cutting aspect is assigned.

Enforcement. 10 CFR 50 Appendix B, Criterion III, Design Control, states, in part,

measures shall be established to assure that applicable regulatory requirements and

the design basis, as defined in 10 CFR 50.2 and as specified in the license application,

for those structures, systems, and components to which this appendix applies are

correctly translated into specifications, drawings, procedures, and instructions.

Additionally, Criterion III states that design control measures shall be applied to items

such as the following: reactor physics, stress, thermal, hydraulic, and accident analyses;

compatibility of materials; accessibility for in-service inspection, maintenance, and repair;

and delineation of acceptance criteria for inspections and tests. TS 3.4.4, RCS

Operational LEAKAGE, states, in part, RCS operational LEAKAGE shall be limited

to: (a) No pressure boundary LEAKAGE; and (b) < 5 gpm unidentified LEAKAGE.

Contrary to the above from 2004 until June 19, 2012, PPL failed to accurately translate

design basis requirements to ensure Unit 1 RCS piping systems met ASME Code

requirements to pipe stress analysis calculations and acceptance criteria due to using an

incorrect stress intensification factor. The weld in question subsequently failed resulting

in pressure boundary leakage in excess of Technical Specification 3.4.4 limits from

June 16 to June 18, 2012. PPL took action to make repairs to the piping and review

other areas for extent of condition. Because of the very low safety significance of this

finding and because the finding was entered into PPLs CAP as CR 1589390, this

violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC

Enforcement Policy. (NCV 05000387/2012005-04, Improper Stress Intensification

Factor Results in RCS Pressure Boundary Leak)

c. Observations

The inspectors assessed PPLs problem identification threshold, cause analyses, extent

of condition reviews, compensatory actions, and the prioritization and timeliness of

PPLs corrective actions to determine whether PPLs was appropriately identifying,

characterizing, and correcting problems associated with this issue and whether the

planned or completed corrective actions were appropriate. The inspectors compared the

actions taken to the requirements of PPLs corrective action program and 10 CFR 50,

Appendix B. The inspectors concluded that PPLs evaluations and corrective actions for

this issue were timely and appropriate. The RCA (CR 1589390, Revision 1) for the issue

identified the causes of the through-wall leak, developed appropriate extent of condition

and extent of cause reviews and the corrective actions were timely and reasonable.

Enclosure

41

.4 Annual Sample: Failure to Report Changes in Medical Conditions as Required by 10

CFR 50.74, Notification of Change in Operator or Senior Operator Status (1 sample)

a. Inspection Scope

In February 2012, PPL staff commenced a root cause investigation (CR 15167640) in

response to a series of NRC findings from 2007 to present involving required NRC

notifications not being made that affected license conditions of licensed operators. The

root cause report was issued on April 17, 2012. As a result of PPLs review, on July 20,

2012, PPL submitted ten medical updates to the NRC. Four of the ten submittals

reported permanent changes in medical conditions that were not submitted in a timely

manner as required and six others were submitted to the NRC as Information Only.

On August 28 to 29, 2012, inspectors conducted a Problem Identification and Resolution

(PI&R) inspection. Since there had been a history of unreported medical issues at

Susquehanna dating back four years, the focus of this inspection was to determine the

site process for conducting the 10 CFR 55 required biennial licensed operator medical

exams. The inspectors reviewed appropriate medical documents, PPL procedures and

conducted interviews with PPL Staff, the PPL Medical Reviewing Officer (MRO) and

other knowledgeable individuals. This inspection also evaluated PPLs actions to restore

compliance and address SLIV NOV 50-387 & 388 2011-004-01. However, due to the

additional issues discovered and discussed below, the NOV could not be closed.

b. Findings

Introduction. The inspectors identified an unresolved item (URI) related to licensed

operator medical examinations and qualifications required by 10 CFR 55.53 and 10 CFR

55.21. Specifically, over a period of approximately four years, a number of licensed

operators developed potentially disqualifying medical conditions which were not properly

evaluated by PPL in accordance with ANSI/ANS-3.4-1983, American National Standard

Medical Certification and Monitoring of Personnel Requiring Operator Licenses for

Nuclear Power Plants. In addition, during this same time frame, there were a number

of cases (i.e., both historical and current) where PPL potentially failed to notify the NRC

of a change in medical condition within 30 days as required by 10 CFR 55.25. The

inspectors concluded that there are a number of recently submitted submittals of PPL

medical status updates that will require independent evaluation by the NRCs contract

physicians before the NRC is able to determine whether the medical issues represented

disqualifying conditions and; therefore, would constitute a violation of NRC requirements.

Description. In February 2012, PPL launched a root cause evaluation (CR 15167640)

in response to a series of NRC findings from 2007 to present involving required NRC

notifications not being made that affected license conditions of licensed operators. The

root cause report was issued on April 17, 2012. As a result of this evaluation, on July

20, 2012, PPL submitted ten medical updates to the NRC. Four of the ten submittals

reported permanent changes in medical conditions that were not submitted in a timely

manner as required and six others were submitted to the NRC as Information Only.

PPL later resubmitted three of the six Information Only submittals adding conditions to

the licenses after follow-up questioning from the NRC contract doctor. Examples of

license conditions included Solo Operations is Not Authorized and Shall Submit

Medical Status Report Every 12 Months.

Enclosure

42

In addition, PPL staff initiated CR 1597808 on July 12, 2012, when PPLs interviews

conducted with the MRO and site nurse as part of a root cause corrective action (CRA

1567782) revealed they are not adequately familiar with regulatory responsibilities

contained in 10 CFR 55.23, ANSI 3.4, and the NRC Medical FAQs. During the week of

July 16, 2012, the inspectors conducted a follow-up interview with the Licensed Operator

Requalification Training (LORT) supervisor who was assigned overall responsibility for

follow-up to the root cause investigation and corrective actions. On July 17, 2012, the

inspectors asked the LORT supervisor why neither the primary root cause

(Susquehanna lacks a formal process to maintain NRC licensed operator status to

ensure appropriate notifications are made) or causal factors pointed to the inadequate

training and oversight of the MRO and examining physician or assigned corrective

actions to address these issues. On July 18, 2012, PPL revised the root cause (CRA

1600109) to include training of the MRO and nurse as a root cause and assigned

corrective actions to address this issue.

On August 16, 2012, the MRO called the NRC inspectors to discuss questions that had

been previously posed to PPL staff by the inspectors. The MRO stated that he was

assigned to his position in 2008. The MRO stated that he was not given any turnover or

training regarding ANSI 3.4 or 10 CFR 55 requirements and that he relied on the in-

house nurse for her experience and insights. Through this discussion, the inspectors

identified that licensed operator medical examinations were coordinated by the site

nurse but the examinations were actually conducted at the Berwick Hospital by another

physician.

The site nurse, the MRO of record, and the doctor that actually performed the medical

examinations at Berwick Hospital were interviewed by the inspectors to determine their

process for conducting these examinations and for notifying the NRC when a change in

medical condition requires the operators license to be conditioned. The interviews also

established their prior understanding of the ANSI standard and 10 CFR 55. As a result

of their interviews the inspectors identified the following information which was not

identified in PPLs Root Cause Analysis:

The inspectors confirmed that the MRO was not provided a turnover or training

regarding ANSI 3.4 or 10 CFR 55 but learned by on-the-job performance as

discussed in the August 16 call with NRC inspectors.

The inspectors identified that the MRO does not actually perform the operator

medical examinations and, as a rule, he does not actually meet with or examine the

licensed operators during the medical exam process. The exams were actually

performed by a physician and his staff at Berwick Hospital and then the records were

faxed back to the nurse for later review by the nurse and the MRO.

The inspectors identified that the NRC Form 396s, Certification of Medical

Examination by Facility Licensee, sent to the NRC had not been completed

accurately in the past since the physicians name that had actually performed the

medical examinations was not entered on the part A of the form as required.

The inspectors identified that, in April 2010, Susquehanna Form 4294, Licensed

Operator Medical Requirements, was incorrectly revised by the MRO (i.e., the

revisions did not accurately reflect disqualifying conditions as indicated in ANSI/ANS-

3.4-1983). This Form was given to the physician actually performing the medical

examinations at Berwick Hospital as a checklist to highlight ANSI disqualifying

medical conditions.

Enclosure

43

The inspectors identified that the doctor at Berwick Hospital, who had been

performing the physical examinations for the past twenty years, had not been trained

on either ANSI 3.4 or 10 CFR 55.

The licensed operator medical issues identified in the past four years (i.e., both current

as well as historical) appear to be associated with PPLs failure to properly train and

provide oversight for their MRO and the Berwick examining physician regarding

compliance with the requirements of ANSI/ANS-3.4-1983 and 10 CFR 55. The medical

issues identified during this time frame appear to be related to a lack of knowledge and

inadequate oversight. The inspectors noted the following guidance applies:

ANSI/ANS-3.4-1983, states in part, 3. Health Evaluation Responsibility, 3.1 General

Aspects. The primary responsibility for assuring that qualified personnel are on duty

rests with the facility operator. The health requirements set forth herein are

considered the minimum necessary to determine that the physical condition and

general health of the individual are not such as might cause operational errors

endangering public health and safety. The designated medical examiner shall be

conversant with this standard and should have a general understanding of activities

required of a nuclear reactor operator.

Susquehanna Procedure, NTP-QA-31.12, Revision 5, Preparation and Submission

of NRC Form 396 - Certification of Medical Examination by facility Licensee and

NRC Form 398 - Personal Qualifications Statement - Licensee, section 6.3.11,

states in part, The Consulting Physician reviews the results against the medical

standards set forth in ANSI/ANS 3.4 -1983completes the medical section of Form

NRC- 396 for employees seeking Initial Licensure and Six-Year License Renewal or

any change in medical condition. Consulting Physician may also request a "waiver"

or a "specifically limited approval" when an employee's general medical condition

does not meet the minimum standard, i.e., wear corrective lenses. These requests

are documented on Form NRC-396 and other medical history and pertinent medical

documentation are attached.

NRC Form 396, Certification of Medical Examination by Facility Licensee, Part A,

Medical Examination Information, provides the physicians name, license number,

and most recent biennial medical examination date for the applicant that was

examined and states in part, I certify that in reaching this determination the

guidance in the ANSI standardwas followed, and that documentation is available

for review by the NRC. In addition, page two of the Instructions for NRC FORM

396, states in part, ...the physician has the ultimate responsibility for certifying that

the medical examination was conducted in accordance with the ANSI standard and

the applicant meets the medical requirements.

The inspectors concluded that PPLs failure to properly identify potentially disqualifying

medical conditions resulted in failure to notify the NRC of these changes in medical

conditions within 30 days, and in some cases may have affected the operators ability to

comply with operator license conditions that should have been in affect while standing

watch. This was a performance deficiency within PPLs ability to foresee and correct

and should have been prevented. The NRC has issued conditioned individual operator

licensees which address the potentially disqualifying conditions for the operators.

Enclosure

44

PPL has recently submitted several PPL medical status updates for the cases in

question that will require independent evaluation by the NRCs contract physicians. The

inspectors determined that these concerns represent a URI. Completion of an

independent evaluation by the NRC contract doctors is required before the NRC is able

to determine whether medical issues represented disqualifying conditions and, therefore,

would constitute a violation of NRC requirements. (URI 05000387;388/2012005-05,

Concerns Regarding PPLs Program for Conducting Biennial Medical Exams for

Licensed Operators and Reporting Changes in Medical Conditions).

.5 Annual Sample: Instances of Inoperable Main Steam Safety Relief Valves (SRVs)

(1 sample)

a. Inspection Scope

The inspectors performed an in-depth review of PPL's evaluations and corrective actions

associated with CR 1587108, for main steam SRV test failures. Specifically, during the

2012 Unit 1 refueling outage, two out of 5 SRVs tested did not meet the setpoint criteria

of +3 to -5 percent set forth in TS 3.4.3. Both SRVs actuated at a setpoint less than the

-5 percent criteria.

The inspectors assessed PPL's problem identification threshold, problem analysis,

extent of condition reviews, compensatory actions, and the prioritization and timeliness

of PPL's corrective actions to determine whether PPL was appropriately identifying,

characterizing, and correcting problems associated with this issue and whether the

planned or completed corrective actions were appropriate. The inspectors compared the

actions taken to the requirements of PPL's CAP and 10 CFR 50 Appendix B. The

inspectors interviewed engineering and licensing personnel to assess the effectiveness

of the implemented corrective actions, the reasonableness of the planned corrective

actions, and to evaluate the extent of any ongoing SRV problems. Specific documents

reviewed are listed in the attachment to this report.

b. Findings and Observations

No findings of significance were identified.

PPL staff determined the cause of the lower actuation was attributed to valve internal

misalignment. PPL staff determined the event to be a common cause inoperability of

independent trains or channels and reportable under 10 CFR 50.73(a)(2)(vii). However,

both SRVs would have relieved pressure before exceeding +3 percent. Therefore, the

SRV safety function, described in UFSAR 5.2.2.1.1, to prevent over-pressurization of the

reactor coolant pressure boundary, was not adversely impacted. In addition, TS 3.4.3

required the safety function of 14 of the 16 SRVs to be operable. With both SRVs

outside of their allowable TS setpoint criteria, 14 SRVs still remained operable and there

was no TS violation. PPL staff coordinated with the SRV vendor to address the

misalignment issues.

The inspectors determined PPL staffs overall response to the issue was commensurate

with the safety significance and included conservative decision-making and appropriate

engineering analysis. The inspectors determined that the actions taken or planned were

reasonable to resolve the identified SRV issues.

Enclosure

45

.6 Annual Sample: Evaluation of PPLs Corrective Action Plans to Address Substantive

Cross-Cutting Issues P.1(c), Evaluation of Identified Problems, and H.2(c), Procedure

Quality.

a. Inspection Scope

The inspectors reviewed PPLs corrective actions to address substantive cross-cutting

issues P.1(c), Evaluation of Identified Problems, and H.2(c), Procedure

Quality/Procedure Use and Adherence. The inspectors evaluated PPL staffs

performance in addressing the P.1(c) and H.2(c) SCCI and corrective action plan

implementation. The standards applied to the inspection are the performance attributes

contained within NRC inspection procedure 71152, Problem Identification and

Resolution, as related to corrective action implementation and effectiveness reviews.

Documents reviewed are listed throughout the body of the report and in the Attachment.

The P.1(c) cross-cutting theme was first identified in the 2010 Annual Assessment Letter

(ML110620317), dated March 4, 2011, and remained open as documented in the 2011

End-of-cycle Assessment (ML12061A021) and 2012 Mid-cycle Assessment

(ML12248A066) letters. The H.2(c) cross-cutting theme was first identified in the 2011

Mid-cycle Assessment Letter (ML112430469), dated September 1, 2011, and remained

open as documented in the 2012 Mid-cycle Assessment Letter (ML12248A066).

b. Findings and Observations

No findings were identified.

PPL Corrective Actions Related to CAP - Evaluations (P.1(c))

PPL staff implemented corrective actions to address the P.1(c) substantive cross-cutting

issue as identified in their Performance Improvement Integrated Matrix (PIIM). This

document describes seven elements intended to improve PPLs CAP performance. The

inspectors determined that PPL made progress in implementing corrective actions with

the following observations:

In 2011, PPL staff identified a significant contributing cause to for quality issues

with corrective action program (CAP) evaluations was insufficient staff skill and

understanding of process for performing root cause, apparent cause and lower

level cause evaluations. To correct this, since 2011, PPL implemented

qualification-based CAP training to employees and supervisors responsible for

performing evaluations. The training was developed to improve evaluation

quality and enhance staff knowledge on how to perform, review, and approve

CAP evaluations. Corrective actions to improve evaluation quality are in

progress and include PPLs actions to discuss evaluation quality in leadership

and all-hands meetings, increased management participation in corrective action

review boards (CARBs), and Training Needs Analyses (1547326) to make

adjustments to evaluation training as needed.

Since May 2011, PPL instituted Departmental Corrective Action Review Boards

(DCARBs), which are intended to improve evaluation quality before the

evaluations are submitted to the stations CARB for approval. The inspectors

reviewed PPL procedure NDAP-00-0761, Departmental Corrective Action

Enclosure

46

Review Board, and determined that PPL engineering department staff did not

adhere to the procedure requirement (step 2.2.2) for sampling level 3 evaluations

at DCARB. The inspectors determined this issue was a performance deficiency

and a minor finding related to PPLs procedural requirements. However, this

issue is not a violation of NRC requirements. PPL staff entered this issue into

the CAP (1651434).

PPL staff completed an evaluation (1502875) of the quality of operability

determinations, which determined that the appropriate level of rigor was not

being consistently applied in the performance of initial operability determinations

by operations personnel. In response, PPL staff completed a training needs

analysis (1383039). Full training for senior reactor operators (SROs) on

operability determinations has not yet been completed due to the availability of

the desired training vendor. In the interim, PPL staff has provided supplemental

training on operability determinations to SROs, and instituted additional peer

checks of operability determinations. Self assessments completed since the

interim training began (1521473) have concluded there is improvement in

operability evaluation quality. The inspector also noted there were no NRC

findings related to Operability Determinations over the last two quarters.

In December 2011, PPL staff determined that from a risk perspective, many

Level 3 CR evaluations within the stations backlog did not require evaluations

but were important to include in the CAP for trending. Corrective Action Program

Coordinator - Performance Improvement Coordinators (CAPCO PICs) review

these items periodically (CAP Health Days) and have determined many of the

items could be rescreened to a lower significance level in accordance with site

procedures. PPL staff also determined that many CRs were written with

insufficient problem descriptions, which made it difficult for the evaluators and the

Management Review Committee (MRC) screening team to understand the scope

of the problem. PPL staff has rescreened many of these CRs in accordance with

site procedures. Additionally, PPL staff instituted training for evaluators and

supervisors to improve upon the problem descriptions in CRs they approve.

These actions are attributed to a reduction in backlog with over 1030 corrective

actions closed since May 2012.

PPL Corrective Actions Related to Procedure Quality (H.2(c))

PPL implemented corrective actions to address procedure quality issues as identified in

the PIIM, which is intended to improve procedure quality, usage, and adherence.

Included in these corrective actions is the establishment of a site procedure group and a

procedure upgrade project. These items were inspected by the NRC during the conduct

of the NRC 95002 supplemental inspection follow-up in November 2012. The inspection

results for the site procedure group and procedure upgrade project are documented in

NRC inspection report 05000387/2012011.

The inspector determined that PPL has made progress in creating and implementing

corrective actions to address the H.2(c) substantive cross-cutting issue; however, some

items in the plan are in their early stages. The inspector noted the following

observations:

Enclosure

47

In April 2011, PPL completed a root cause evaluation (1389530) that determined

the station had less than adequate procedures due to a failure to incorporate

best industry guidance for procedure quality. Additionally, the root cause

evaluation identified that PPL had less than adequate management oversight in

reinforcing expectations for procedure use and adherence. Training sessions

conducted in January 2012 on procedure use and adherence revealed that many

supervisors were not adhering to or were not knowledgeable of existing

procedure usage standards (verifying current revision, place-keeping, signoffs,

use of not applicable, and general adherence requirements). A four-hour

classroom-based course was created and given to over 1000 PPL employees,

which focused on establishing rules and standards for procedure use to ensure

safe, effective control of work activities.

PPL evaluated the sites progress in procedure use and adherence through

effectiveness reviews, CR trending, and the use of Observation Way (an

employee observation database). Since January 2012, PPL has completed

15 effectiveness reviews which have shown through interviews that personnel

are being more critical, are demonstrating the desired procedure use and

adherence behaviors, and are identifying procedure issues during their work

activities. CR trending data shows that a total of 1589 CRs have been issued

since January 2012 which identify procedure issues for action and evaluation.

Additionally, 581 more procedure issues have been identified in 2012 than in

2011. The CRs also indicate that the number of procedure noncompliance

events have decreased from 32 events in the 3rd quarter 2011 to 11 events in the

3rd quarter 2012.

Observation Way data indicated a difference in behaviors associated with

procedure use and adherence fundamentals. In 2012, 1019 observations were

made of individuals who demonstrated a questioning attitude and stopped a job

when unsure about a procedure issue. PPL staff has interpreted this data as

evidence that the corrective actions from the root cause evaluation (1389530)

have resulted in the station personnel identifying more issues related for

procedure quality while procedures are in use in the field, and initiating actions

to address those issues vice working around procedure issues.

The inspectors reviewed the progress of the site procedure upgrade group to improve

procedure quality and found that at the time of the inspection the station had completed

333 procedure upgrades of the 700 high priority procedures. The station currently has

more than 4000 additional procedures that are being considered for upgrade over the

next several years. Though many of these non-upgraded procedures are in use in the

field, comments in Observation Way and interviews with plant personnel indicate

employees are raising concerns about existing procedures that have quality and usage

issues. PPL has corrective actions in place to continue reviewing and upgrading the

balance of the procedures.

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153 - 6 samples)

.1 Plant Events

a. Inspection Scope

Enclosure

48

For the plant events listed below, the inspectors reviewed and/or observed plant

parameters, reviewed personnel performance, and evaluated performance of mitigating

systems. The inspectors communicated the plant events to appropriate regional

personnel, and compared the event details with criteria contained in IMC 0309,

Reactive Inspection Decision Basis for Reactors, for consideration of potential reactive

inspection activities. As applicable, the inspectors verified that PPLs operators made

appropriate emergency classification assessments and properly reported the event in

accordance with 10 CFR Parts 50.72 and 50.73. The inspectors reviewed follow-up

actions related to the events to assure that PPL staff implemented appropriate corrective

actions commensurate with their safety significance.

Unit 2, Manual reactor scram following failure of the integrated control system on

November 9, 2012

Unit 2, Automatic reactor scram during control valve testing on December 16, 2012

Unit 2, Automatic reactor scram during plant startup on December 19, 2012

b. Findings

Introduction. Inspectors identified a Severity Level IV NCV of 10 CFR 50.72(b)(3)(iv)(A)

and (B) when PPL operators did not report a valid actuation of the Unit 2 reactor

protection system (RPS) on November 9, 2012 within eight hours of occurrence as

required.

Description. On November 9, 2012 at 1:17 a.m., Unit 2 was manually scrammed

following a failure in the integrated control system (ICS) and a subsequent lowering of

reactor water level. This failure rendered the control of reactor feedwater and

recirculation pump speed ineffective. Following the scram, reactor water level lowered,

the RCIC and HPCI systems automatically initiated, reactor recirculation pumps tripped

and containment isolations occurred as designed. Operators entered the appropriate

procedures. The operators overrode HPCI to prevent its injection, and restored reactor

water level using RCIC to a band of 13 to 30 inches in accordance with station

procedures.

During the post-transient response, a reactor operator was controlling RCIC using a

wide range reactor vessel level indicator in the vicinity of the RCIC control station. As

reactor temperature and pressure decreased due to cooldown, the level indications

displayed on wide range and narrow range began to diverge due to the fact these

instruments are calibrated under hot and full pressure conditions. At 4:20 a.m., while

wide range reactor water level indicated 24, narrow range level reached approximately

15 inches, and an automatic RPS scram was generated. Investigation determined that

the low reactor water level scram switches are conservatively calibrated to 15 inches.

Operators again entered applicable procedures and completed the scram response

actions. Although no rod motion occurred due to all rods having been previously

inserted, a valid reactor scram was initiated and the system responded as required.

PPL submitted a four-hour report in accordance with 10 CFR 50.72(b)(2)((iv)(A) and (B)

at 03:03 on November 9 (EN 48496) for the original scram as required. However, the

following day the inspectors questioned whether PPL operators had made an eight-hour

report regarding the second reactor scram and associated containment isolation signals.

10 CFR 50.72 (b)(3)(iv)(A) requires an eight hour report for any valid actuation of the

RPS system unless part of a preplanned test or in accordance with a procedure (such

Enclosure

49

as reactor shutdown). The inspectors raised the concern to the PPL management and

PPL staff determined that a second report had not been made, and as a result of the

inspectors questions determined a report one was required. PPL staff subsequently

submitted the report at 4:20 p.m. on November 10, 2012 (EN 48500).

The inspectors noted that NUREG 1022 Revision 2, Event Reporting Guidelines: 10

CFR 50.72 and 50.73, clarifies that the event was reportable. Examples listed for RPS

actuation include a scram signal generated with the plant in mode 3. An ENS

notification and LER are both required because, although the systems' safety functions

had already been completed, the RPS scram and primary containment isolation signals

were valid and the actuations were not part of the planned procedure. The automatic

signals were valid because they were generated from the sensor by measurement of an

actual physical system parameter that was at its set point.

The NRC was aware of both scrams, and no regulatory decisions were impacted due to

the report for the second scram being made late.

Analysis. Not making a timely eight hour notification in accordance with 10 CFR 50.72

was a performance deficiency within PPLs ability to foresee and correct. The per-

formance deficiency was evaluated in accordance with IMC 0612, Appendix B, and

traditional enforcement was determined to apply because this was a reporting failure

and therefore had the potential to impact the regulatory process. The issue was

evaluated using the Enforcement Policy and determined to be similar to example 6.9.d.9,

a licensee fails to make a report required by 10 CFR 50.72 or 10 CFR 50.73. This is

an example of a Severity Level IV violation.

Because this violation involves the traditional enforcement process and does not have

an underlying technical violation that would be considered more-than-minor, inspectors

did not assign a cross-cutting aspect to this violation in accordance with IMC 0612,

Appendix B.

Enforcement. 10 CFR 50.72(b)(3)(iv)(A) requires, in part, that any event or condition

that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) of this

section shall be reported within eight hours, except when the actuation results from and

is part of a pre-planned sequence during testing or reactor operation. 10 CFR

50.72(b)(3)(B) states, in part, The systems to which the requirements of paragraph

(b)(3)(iv)(A) of this section apply are: (1) Reactor protection system (RPS) including:

Reactor scram and reactor trip. Contrary to the above, PPL did not make a timely

notification within eight hours of a valid RPS actuation, which occurred on November 9,

2012. Because this violation was of very low safety significance, was not repetitive or

willful, and was entered into PPLs CAP (CR 1643098), this violation is being treated as

an NCV consistent with the NRC Enforcement Policy. (NCV 05000388/2012005-06,

Failure to Make a Timely Report for a Valid Actuation of RPS)

.2 (Closed) Licensee Event Report (LER) 05000387/2012-005-00: Valve Internal

Misalignment resulting in Multiple Inoperable Main Steam SRVs

a. Inspection Scope

In April 2012, during the Unit 1 outage, two main steam SRVs failed to meet the setpoint

criteria of +3 to -5 percent set forth in TS 3.4.3. Both SRVs actuated at a setpoint less

Enclosure

50

than the -5 percent criteria. The cause of the lower actuation was attributed to valve

internal misalignment. PPL determined the event to be a common cause inoperability

of independent trains or channels and reportable under 10 CFR 50.73(a)(2)(vii). Both

SRVs would have relieved pressure before exceeding +3 percent. Therefore, the SRV

safety function, described in UFSAR 5.2.2.1.1, to prevent over-pressurization of the

reactor coolant pressure boundary, was not violated. In addition, TS 3.4.3 required the

safety function of 14 of the 16 SRVs to be operable. With both SRVs outside of their

allowable TS setpoint criteria, 14 SRVs still remained operable. There were no actual

adverse consequences as a result of this event.

The inspectors reviewed this LER, including PPL's evaluations and associated corrective

actions. The inspectors did not identify any additional performance deficiencies related

to this issue. This LER is closed.

b. Findings

No findings were identified.

.3 (Closed) Licensee Event Report (LER) 05000387/2012-007-00 and LER

05000387/2012-007-01: Unplanned Shutdown due to Unidentified Drywell Leakage

a. Inspection Scope

On June 19, 2012, PPL conducted a reactor shutdown of Unit 1 and entered the drywell

to investigate the source of an increasing trend in drywell unidentified leakage. PPL

discovered that the source of the leakage was from a through-wall crack on the A

reactor recirculation loop decontamination connection. The crack was determined to

have been a fatigue-related failure due to cyclic vibration. LER 50-387/2012-007-00 was

issued on Aug 17, 2012 and LER 50-387/2012-007-01 was issued November 20, 2012

to update the original LER with the results of the RCA.

The inspectors reviewed this LER, including PPL's evaluations and associated corrective

actions. The inspectors did not identify any additional issues during the review of the

LERs. These LERs are closed.

b. Findings

A self-revealing Green NCV was identified and is discussed in section 4OA2 of this

report.

.4 (Closed) Licensee Event Report (LER) 05000388/2011-002-01: Condition Prohibited by

Technical Specification due to Unknown RCIC lnoperability

a. Inspection Scope

On June 29, 2011, during startup from a refueling outage, operations personnel

conducted the Unit 2 reactor core isolation cooling (RCIC) system quarterly flow

surveillance. During the testing, RCIC tripped on overspeed. Subsequent trouble-

shooting determined the problem to be failure of the ramp generator signal converter

(RGSC). An engineering evaluation determined that RCIC had been inoperable as a

result of the RGSC problem on June 27, 2011 when the plant exceeded 150 psig and

Enclosure

51

the RCIC LCO became applicable. This constituted a condition prohibited by plant TSs

and was reported to the NRC as LER 05000388/2011-002-00. This LER reported the

apparent cause as unexpected, random failure of the RGSC. The NRC reviewed this

LER and closed it in inspection report 05000388/2011005 with a Green NCV that

identified the failure was maintenance induced. Revision 1 to this LER was submitted in

May 2012 with results of a revised RCA.

The inspectors reviewed this LER, PPL's revised RCA, and associated corrective

actions. This LER is closed.

b. Findings

No findings were identified.

4OA5 Other Activities

.1 (Closed) NRC Temporary Instruction (TI) 2515/187 - Inspection of Near-Term Task

Force Recommendation 2.3 Flooding Walkdowns

a. Inspection Scope

Inspectors verified that the PPLs walkdown packages for 1) ESSW pump house Area 55

elevation 685 and 660, 2) EDG building Area 43 elevation 660, 3) Unit 1 Reactor

Building (RB) Area 25 elevation 645, and 4) E EDG building Area 81 elevation 656,

contained the elements as specified in NEI 12-07 Walkdown Guidance document:

The inspectors accompanied PPL staff on their walkdown of both Unit 1 RB Area 25

elevation 645 and E EDG building Area 81 elevation 656 and verified that PPL staff

confirmed the following flood protection features:

Visual inspection of the flood protection feature was performed if the flood protection

feature was relevant. External visual inspection for indications of degradation that

would prevent its credited function from being performed was performed.

Critical SSC dimensions were measured.

Available physical margin, where applicable, was determined.

Flood protection feature functionality was determined using either visual observation

or by review of other documents.

The inspectors verified that noncompliance with current licensing requirements, and

issues identified in accordance with the 10 CFR 50.54(f) letter, Item 2.g of Enclosure 4,

were entered into PPL's CAP. In addition, issues identified in response to Item 2.g that

could challenge risk significant equipment and PPLs ability to mitigate the

consequences will be subject to additional NRC evaluation.

b. Findings

No findings were identified.

.2 (Closed) NRC Temporary Instruction (TI) 2515/188 - Inspection of Near-Term Task

Force Recommendation 2.3 Seismic Walkdowns

Enclosure

52

a. Inspection Scope

The inspectors accompanied PPL on their seismic walkdowns of 1) Unit 2 Reactor

Building 645 on August 15, 2012, 2) Unit 1 Reactor Building 719 on September 25, 3)

Unit 2 Reactor Building 670 on September 26, and 4) Unit 2 Control Structure 771 on

September 21, and verified that PPL confirmed that the following seismic features

associated with the Unit 2 HPCI Steam Supply Valve (HV255F001), Unit 1 120 VAC

Instrument Distribution Panel (1Y236), Unit 2 ESS Division I 480V MCC (2B219), and

Unit 2 RHR/RCIC Relay Panel Division 2 (2C618), respectively, were free of potential

adverse seismic conditions as applicable:

Anchorage was free of bent, broken, missing or loose hardware.

Anchorage was free of corrosion that is more than mild surface oxidation.

Anchorage was free of visible cracks in the concrete near the anchors.

Anchorage configuration was consistent with plant documentation.

SSCs will not be damaged from impact by nearby equipment or structures.

Overhead equipment, distribution systems, ceiling tiles and lighting, and masonry

block walls are secure and not likely to collapse onto the equipment.

Attached lines have adequate flexibility to avoid damage.

The area appears to be free of potentially adverse seismic interactions that could

cause flooding or spray in the area.

The area appears to be free of potentially adverse seismic interactions that could

cause a fire in the area.

The area appears to be free of potentially adverse seismic interactions associated

with housekeeping practices, storage of portable equipment, and temporary

installations (e.g., scaffolding, lead shielding).

The inspectors independently performed walkdowns of the following equipment and

verified they were free of the above listed adverse seismic conditions, as applicable:

Unit 1, 1D653A, 250VDC engineering safeguard system (ESS) Division I Battery

Charger A, in the Control Structure, on November 21, 2012

Common, HD07812B, CREOAS Inboard Air Supply Damper, in the Control

Structure, on November 21, 2012

Common, 0E506B, EDG B Lube Oil Cooler, in the Diesel Generator building, on

November 21, 2012

Observations made during the walkdown that could not be determined to be acceptable

were entered into PPLs CAP for evaluation.

PPL personnel determined that there were no items that could allow the spent fuel pool

(SFP) to drain down rapidly. No items from the SFP were added to the SWEL.

b. Findings and Observations

No findings were identified.

Enclosure

53

.3 (Closed) Unresolved Item (URI) 05000387;388/2011005-05, RCIC Low Pressure

Surveillance Requirement (SR)

a. Inspection Scope

Inspectors reviewed URI 05000388/2011005-05. This URI was initiated to determine

whether PPLs implementation of TS SR 3.5.3.4 appropriately verified RCIC system

operability. Specifically, the implementing procedure, SO-250-005, 24 Month RCIC

Flow Verification, Revision 17, did not initiate RCIC with its flow controller in automatic

at reactor pressure of 150 psig and verify the RCIC pump provided rated flow within 30

seconds. This procedure tested the RCIC system in manual at 150 psig and in

automatic at rated pressure. Inspectors reviewed PPLs evaluations and operability

determinations, the UFSAR, power uprate analysis and discussed the potential issue

with Nuclear Reactor Regulation staff (NRR).

b. Findings

No findings were identified.

Based on a conference call with NRR technical staff and inspectors on October 11,

2012, inspectors determined that PPL did not establish the conditions assumed in the

accident analysis in their implementing procedure SO-250-005, 24 Month RCIC Flow

Verification, Revision 17, for the low pressure RCIC surveillance test. This

determination was based, in part, on the UFSAR and power uprate analysis which

assume that the RCIC system will start automatically. These requirements were

translated into power uprate test criteria which states that the average RCIC pump

discharge flow shall be equal to or greater than the 100% rated value within 30 seconds

from automatic initiation at any reactor pressure between 150 psig and rated.

The inspectors identified a violation of 10 CFR 50, Appendix B, Criterion XI, Test

Control, which states, in part, that a test program shall be established to assure that all

testing required to demonstrate that SSCs will perform satisfactorily in service is

identified and performed in accordance with written test procedures which incorporate

the requirements and acceptance limits contained in applicable design documents.

Contrary to this, PPL did not ensure that test conditions specified in TS SR implementing

procedures were consistent with conditions assumed in the UFSAR accident analysis

and test the RCIC system in automatic at both 150 psig and rated pressure. Inspectors

determined this violation was not more than minor based on review of PPLs operability

determination, which provided reasonable assurance of operability for the short period of

exposure that the issue covered (reactor pressure of at approximately 150 psig which

only occurs during plant startup and shutdown.) Additionally, PPL staff subsequently

revised the surveillance procedure and satisfactorily performed the low-pressure

surveillance test with the flow controller in automatic on each unit. This failure to comply

with 10 CFR 50, Appendix B, Criterion XI, constitutes a minor violation that is not subject

to enforcement action in accordance with the NRCs Enforcement Policy. This URI is

closed.

Enclosure

54

4OA6 Meetings, Including Exit

On January 25, 2013, the inspectors presented the inspection results to Mr. T. Rausch,

Chief Nuclear Officer (CNO), and other members of the PPL staff. PPL acknowledged

the findings. No proprietary information is contained in this report.

4OA7 Licensee-Identified Violations

No findings were identified.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

A-1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

A. Alley, Medical review Officer

T. Case, Licensing Engineer

M. Crowthers, Manager, Licensing

N. Davis, Senior Engineer, Performance Improvement

R. Edwards, Mechanical Engineer

C. Goff, Training Director

J. Goodbred, Jr., Operations Manager

K. Griffith, Licensed Operator Requalification Program Lead

J. Grisewood, Manager, Performance Improvement

D. Hackenberg, Mechanic Leader

J. Helsel, Site Vice President (Acting), Plant General Manager

F. Hickey, Senior Health Physicist, Chemistry

C. Hoffman, Manager, Nuclear Fuels

T. Iliadis, General Manager, Nuclear Operations

J. Jennings, Manager, Performance Improvement

G. Kanouse, Medical Doctor, Berwick Hospital

T. Magrone, Chemistry Technician

M. Micca, Radwaste Shipper

S. Muntzenberger, Supervisor, Mechanical Engineering

B. ORourke, Licensing Engineer

C. Parks, Site Nurse

G. Pennycoff, Chemistry Technician

J. Petrilla, III, Supervisor, Regulatory Affairs

B. Rigotti, Senior Engineer

C. Ringer, Instrument and Control (I&C) Technician - Level II

R. Rodriguez-Gilroy, Radiological Operations Supervisor

R. Thomann, Support Engineer

R. Thompson, Simulator Instructor

J. Tripoli, Manager Regulatory Affairs

J. Seroka, System Engineer, Ventilation

K. Spako, McCarls Worker

R. Stigers, Radwaste Specialist

R. Streeper, Operations Training Manager

NRC Personnel

K. Hoffman, Materials Engineer

K. Mangan, Senior Reactor Inspector

Attachment

A-2

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000387;388/2012005-05 URI Concerns Regarding PPLs Program for

Conducting Biennial Medical Examinations for

Licensed Operators and Reporting Changes in

Medical Conditions (Section 4OA2)

Opened/Closed

05000388/2012005-01 NCV Failure to Demonstrate Effective Preventive

Maintenance Under 50.65(a)(2) (Section 1R12)05000387/2012005-02 NCV Failure to Report Common-Cause Inoperability of

Independent Trains (Section 1R12)

05000387;388/2012005-03 NCV Failure of Full-Scale Drill Critique to Identify an

RSPS Weakness (Section 1EP6)05000387/2012005-04 NCV Improper Stress Intensification Factor Results in

RCS Pressure Boundary Leak (Section 4OA2)05000388/2012005-06 NCV Failure to Make a Timely Report for a Valid

Actuation of RPS (Section 4OA3)

Closed

05000387/2012-005-00 LER Valve Internal Misalignment resulting in Multiple

Inoperable Main Steam SRVs

05000387/2012-007-00 LER Unplanned Shutdown due to Unidentified Drywell

Leakage

05000387/2012-007-01 LER Unplanned Shutdown due to Unidentified Drywell

Leakage

05000388/2011-002-01 LER Condition Prohibited by Technical Specification

due to Unknown RCIC lnoperability

05000387;388/2011-005- URI RCIC Low Reactor Pressure SR

05

Discussed

05000387;388/2011-004-01 NOV Failure to Report a Disqualifying Operator

Medical Condition (Section 4OA2)

Attachment

A-3

LIST OF DOCUMENTS REVIEWED

(Not Referenced in the Report)

Section 1R01: Adverse Weather Protection

Procedures:

ON-104-001, Unit 1 Response to Loss of All Offsite Power, Revision 20

ON-000-002, Natural Phenomena, Revision 28

NDAP-00-0030, Severe Weather Preparations (Winter Storm, Hurricane), Revision 3

NDAP-QA-0024, Winter Operation Preparations, Revision 18

Condition Reports:

1522033, 1634874, 1654254*, 1654346, 1653636, 1640160*, 1639176, 1638800*, 1649975,

1647930, 1644298, 1644295, 1632320, 1631176, 1635181, 1635281, 1635250,

1617475, 1619820, 1624490, 1631176, 1612958, 1606545

Work Order:

1578318

Section 1R04: Equipment Alignment

Procedures:

CL-003-0011, Common 13.8kV System, Revision 2

CL-003-0012, Startup Transformers T10 and T20 (OX103 and OX 104), Revision 4

OP-003-003, Startup Bus 20 0A104 T20 Outage and Restoration, Revision 1

CL-054-0012, Common ESW System Mechanical, Revision 19

CL-054-0014, Unit 1 ESW System Mechanical, Revision 17

OP-054-001, ESW System, Revision 35

OP-249-001, RHR System, Revision 41

SO-249-001, Monthly RHR Alignment Check, Revision 25

CL-249-0015, Unit 2 RHR System - Division II Mechanical, Revision 18

CL-249-0018, Unit 2 RHR System - Common Mechanical, Revision 12

CL-249-0014, Unit 2 RHR System - Division II Electrical, Revision 11

OP-024-001, DG, Revision 64

SO-024-001A, Monthly DG A Operability Test, Revision 12

Condition Reports (* NRC identified):

1638800*, 1644374, 1524795, 1524808, 1610241, 1355642, 1425464, 1528173

Drawings:

M-134, Sheet 1, Common P&ID A, B, C, D DG Auxiliaries, Revision 49

M-134, Sheet 2, P&ID A-D Diesel Auxiliaries - Starting Air, Revision 18

M-134, Sheet 3, P&ID A-D Diesel Auxiliaries - Starting Air, Revision 16

M-134, Sheet 4, P&ID A-D Diesel Auxiliaries - Jacket Water and Lube Oil Storage Systems,

Revision 9

Miscellaneous:

Operations Logs for Units 1 and 2, dated October 27 - 30, 2012

TM-OP-024-ST, EDG A-D, Revision 11

TM-OP-024-ST, EDGs A-D, Revision 12

Attachment

A-4

Section 1R05: Fire Protection

Procedures:

OP-234-002, RB Heating, Ventilation, and Air Conditioning (HVAC) Zones 2 and 3, Revision 44

ON-013-001, Response to Fire, Revision 33

FP-213-245, HE and Pump Access Area (Fire Zone 2-3A), Elevation 683, Revision 5

FP-113-113, Containment Access Area (I-401, I-404, I-405) Fire Zones 1-4A-N, -S, -W,

Elevation 719

FP-013,139, Unit 1 Lower Relay Room C-203 Fire Zone O-24D, Elevation 698-0, Revision 8

FP-013-150, Unit 1 Lower Cable Spreading Room C-300 Fire Zone 0-25E, Elevation 714-),

Revision 6

FP-213-239, RCIC Pump Room (II-12), Fire Zone 2-10, Elevation 6450, Revision 7

FP-213-238, HPCI Pump Room (II-11), Fire Zone 2-1C, Elevation 6450, Revision 5

Section 1R11: Licensed Operator Requalification Program

Procedures:

EO-100-102, RPV Control, Revision 8

EO-100-103, Primary Containment Control, Revision 9

EO-100-112, Rapid Depressurization, Revision 7

GO-100-002, Plant Startup, Heatup, and Power Operation, Revision 79

GO-100-005, Plant Shutdown to Hot/Cold Shutdown, Revisions 55 and 56

GO-100-004, Plant Shutdown to Minimum Power, Revision 60

Miscellaneous:

10CFR55.46, 49, 59, 55.45a(2) - a(3)

RG 1.149

NUREG 1021

OP002-406

OP002-310

Startup Control Rod Sequence A1, Unit 1, Cycle 18

Section 1R12: Maintenance Effectiveness

Procedures:

OP-202-001, 125V DC System, Revision 19

NEPM-GA-1170, Through Wall Leakage in Class 3 Rain Water Systems, Revision 1

SI-178-201D, Weekly Functional test of Intermediate Range Monitor (IRM) Channel 1D,

Revision 6

Condition Reports:

1570413, 627323, 793337, 725347, 1571290, 1571862, 1571988, 1572356, 1571200, 1575809,

1636870, 1636945, 1083716, 725352, 1571862, 1571290, 1083716, 1468821, 1571988,

1091728, 1496655, 1498290, 1575062, 1501084, 1649605, 1646629, 1647950,

1647156, 1648135, 1646704, 1646788, 1646629, 1646792*,1646005, 1646237,

1286903, 1138347, 1636752*, 1636746, 1635356, 1634937, 1635728, 1634551,

1635356, 1632988, 1637562, 1633113, 1633341, 1633101, 1527146, 1602279,

1607032, 1607178, 1603839, 1602376, 1602373, 1607037

Work Orders:

1497855, 1497848, 1511889, 1527055, 1638746, 1577438, 1496680, 1643158, 1643161

Attachment

A-5

Miscellaneous:

Engineering Work Request (EWR) 1643161

Maintenance Rule Expert Panel Meeting Minutes, Meeting Number 2012-1025

MRFF Evaluation Summary, MRFF CR Number: 1496655/1501084, October 25, 2012 Expert

Panel

Maintenance Rule Basis Document - System 02, 125V DC, dated October 9, 2012

Maintenance Rule Basis Document - System 50, RCIC, dated October 9, 2012

ASME Code Case N-513-3, Evaluation Criteria for Temporary Acceptance of Flaws in

Moderate Energy Class 2 or 3 Piping,Section XI, Division I

M&P Laboratory Report QR-0297, dated March 9, 2006

GE SIL 496, Electrical Protection Assembly Performance, Revision 1

Maintenance Rule Basis Document, System 58, RPS

Maintenance Rule Basis Document, System 78, Nuclear Instrumentation

TM-OP-056A-ST, Reactor Manual Control System, Revision 5

Maintenance Rule Basis Document, System 56, Control Rod Manual Control

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures:

NDAP-QA-0340, Protected Equipment Program, Revision 18

NDAP-QA-1902, Integrated Risk Management, Revision 9

NDAP-QA-1902, Integrated Risk Management, Revision 9

Condition Reports (* NRC-identified):

162875, 1634526*

Action Request:

1510008

Work Orders:

1468533, 1603991, 1101487, 1376695, 1440681, 1616046, 1599832

Miscellaneous:

PEPETF for 149F007B

Equipment-Out-of-Service (EOOS) Run for Unit 1, October 15, 2012

Sapphire 8 Spar Model

PEPETF for B ESW

EOOS Run for Unit 1 and Unit 2, October 17, 2012

Section 1R15: Operability Evaluations

Procedures:

NDAP-QA-0703, Operability Assessments and Requests for Enforcement Discretion,

Revision 21

NDAP-QA-0423, Station Pump and Valve Testing Program, Revision 24

SO-216-A03, Quarterly RHRSW Flow Verification Division I, Revision 6

AR-208-001, RCIC System 2C601, Revision 21

SO-250-002, Quarterly RCIC Flow Verification, Revision 43

SO-100-007, Revisions 56 and 57

SO-200-007, Revisions 55 and 56

RE-ITP-023, Revision 11

Attachment

A-6

RE-ITP-024, Revision 10

NDAP-QA-0752, Cause Analysis, Revision 16

SO-200-011, Reactor Vessel Temperature and Pressure Recording, November 11, 2012,

Revision 18

Calculations:

EC-062-0573, Study to Support the Bases Section of TS 3.4.10, Revision 1

EC-062-1072, Revised Pressure Temperature Curves for Units 1 and 2, Revision 0

EC-062-0595, Evaluation of Out of Limit Reactor Pressure Vessel (RPV) Cooldown and Heatup

Rate Occurring on February 12, 1989

Condition Reports (* NRC-identified):

1626384, 1627430, 1625663, 1632998, 1633011, 1633216, 1594228, 1594716, 1632238,

1444679, 1632488, 1549881, 1599794, 1499803, 1599447, 1514292, 1630823*,

1622882*, 1537511, 1639429*, 1639432*, 1639428*, 1639403*, 1636681, 1584097*,

1643198*

Work Orders:

154772, 1643156

Miscellaneous:

Operations Logs Assistant Operations Manager Directive 12-04

IOM 182, CS, RB, TB, and RW Building Supply and Exhaust Filters, Revision 15

TS and TSB 3.7.3, 5.5.7, 5.5.14

FSAR Chapter 6, 15, and 915

ML040300694

NEI 99-03, Control Room Habitability Assessment, June, 2001

RG 1.197

PLA-3654, Response to RAI: Enforcement Action 89-042

TS 3.4.10, TSB 3.4.10

GE SIL 430, RPV Temperature Monitoring

GE-SIL 251, Control of RPV Bottom Head Temperatures and Supplement 1

NRC IR 05000387;388/1991-18

Section 1R19: Post-Maintenance Testing

Procedures:

MT-GE-005, Westinghouse 15KV Circuit Breaker and Switchgear Inspection and Maintenance,

Revision 31

SO-153-004, October 4, 2012

MT-GM-011, Valve Packing/Live Loading/Investigation, Revision 25

NDAP-QA-0515, Control and Calibration of Plant Measuring and Test Equipment (M&TE),

Revision 8

OP-164-001, Reactor Recirculation System, Revision 64

NDAP-QA-0482, Post-Maintenance Testing, Revision 6

MT-64-013, N-7500 Reactor Recirculating Pump Seal Installation and Removal, Revision 5

SO-260-001, Quarterly LOCA Test of Drywell Area Unit Coolers/Fans, Revisions 11, 12,

and 13

SO-249-805, Quarterly RHR LOOP B Valve Exercising, Revision 12

SO-249-802, Quarterly RHR System Flow Verification, Division II, Revision 17

Attachment

A-7

Condition Reports (*NRC-identified):

1627252, 1627553, 1627632, 1627635, 1628266, 1630826, 1629644, 1629159, 1634913,

1634440, 1634485, 1638291*, 1639382*, 1630214, 1631025, 1611369, 208309,

207934, 1527004, 1640858, 1639840, 1646899*, 1643759, 1643087*

Work Orders:

1068151, 1078195, 1538898, 1595917, 1451837, 1042880, 1046251, 1597911, 1635411,

1631976, 1630834, 11630223, 1632384, 1640404, 1640974, 1605927, 1640859,

1437034, 897318, 1527017, 1635559

Drawings:

E-224, Sheet 4, Unit 2 Schematic Diagram Drywell Area Cooling Fans , Revision 20

Miscellaneous:

Field test Evaluation HV252F031A, October 9, 2012

Unit 1 Operations Logs, October 26, 2012

ASME Section XI IWA-4540 and IWA 5243, 1995 Edition with 1997 Addenda and 1998 Edition

with 2000 Addenda, ML 092740004

TS and TSB 3.6.1.5, 3.6.3.2

FSAR 9.4.5, 6.2.5

Section 1R20: Refueling and Other Outage Activities

Procedures:

GO-100-002, Plant Startup, Heatup, and Power Operation, Revision 79

GO-100-005, Plant Shutdown to Hot/Cold Shutdown, Revisions 55 and 56

GO-100-004, Plant Shutdown to Minimum Power, Revision 60

GO-200-004, Plant Shutdown to Minimum Power, Revision 58

GO-200-005, Plant Shutdown to Hot/Cold Shutdown, Revision 54

OP-249-002, RHR Shutdown Cooling, Revision 52

Condition Reports (*NRC identified):

1637660*, 1637564, 1637558*, 1633107, 1633109, 1633108, 1633256, 1633295, 1633074,

1633307, 1628763, 1628764, 1644287

Miscellaneous:

Startup Control Rod Sequence A1, Unit 1, Cycle 18

Section 1R22: Surveillance Testing

Procedures:

SE-235-301, Revision 9

Non-Destructive Examination (NDE)-Visual Examination (VT)-002, Revision 4

SI-280-301, Quarterly Calibration of Reactor Vessel Pressure Channels (Core Spray System

and LPCI Permissive) Reactor Pressure Greater Than Setting (420 psig)

SO-150-006, RCIC Comprehensive Flow Verification, Revision 10

SO-150-002, RCIC Quarterly Flow Verification, Revision 47

SO-150-004, RCIC Quarterly Flow, Valve Exercising, Revision 29

SO-293-001, Quarterly Turbine Valve Cycling, Revisions 37, 38, and 39

Attachment

A-8

Condition Reports (* NRC identified):

1629100, 1230833, 1230823, 1217911, 162470, 1620757, 1652315, 1652821

Miscellaneous:

BOP-VT-12-209, October 1, 2012

SSES Switching Order, dated December 18, 2012

Section 1EP6: Drill Evaluation

Procedure:

EP-PS-126, Emergency Plan (EP) Communicator: EP-Position Specific Instructions,

Revision 28

Condition Reports:

1641893, 1641933, 1641944, 1643229, 1641405, 1641923, 1641902, 1641881, 1641878,

1641860, 1641932, 1642144, 1642137, 1641923, 1641907, 1641860, 1649645,

1643107, 1643092, 1643184, 1641934, 1642205, 1641940

Miscellaneous:

NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6

IN 2012-18, Failure to Properly Augment Emergency Response Organizations (ERO)

Section 2RS6: Radioactive Gaseous and Liquid Effluent Treatment

Procedures:

CH-ON-001, SPING Alarm Response, Revision 18

CH-ON-003, Chemistry Requirements for Plant Events, Revision 25

CH-RC-032, Tritium Analysis - Sample Preparation and Analysis, Revision 13

CH-RC-076, Gamma Spectral Analysis, Revision 11

CH-YS-014, SPING Data Collection and System Monitoring, Revision 15

ODCM-QA-003, Effluent Monitor Setpoints, Revision 7

ODCM-QA-008, Radiological Environmental Monitoring Program, Revision 14 and 15

NDAP-QA-1180, Radiological Effluent Monitoring and Control, Revision 7

SC-069-001, Liquid Radwaste Sampling and Pre-Release Analysis, Revision 21

SC-070-001, Standby Gas Treatment Vent Iodine and Particulate Activity, Revision 18

SC-070-002, Standby Gas Treatment Vent Iodine and Particulate Activity, Revision 16

SC-133-101, Unit-1 Turbine Building Vent Iodine and Particulate Activity, Revision 16

SC-133-102, Unit-1 Turbine Building Vent Tritium and Noble Gas Grab Sample Analysis,

Revision 13

SC-134-101, Unit-1 RB Vent Iodine and Particulate Activity, Revision 16

SC-134-102, Unit-1 RB Vent Tritium and Noble Gas Grab Sample Analysis, Revision 13

SC-233-101, Unit-2 Turbine Building Vent Iodine and Particulate Activity, Revision 16

SC-233-102, Unit-2 Turbine Building Vent Tritium and Noble Gas Grab Sample Analysis,

Revision 16

SC-234-101, Unit-2 RB Vent Iodine and Particulate Activity, Revision 16

SC-234-102, Unit-2 RB Vent Tritium and Noble Gas Grab Sample Analysis, Revision 15

Condition Reports:

1348108, 1376390, 1485588, 1491557, 1507526

Attachment

A-9

Audits, Self-Assessments, and Surveillances

QA Audit 1343694, Chemistry/ Effluents Audit Report

Updated Hydrogeologic Investigation Report, January 2011

Release Permits:

2011013, 2011028, 2011071, 2011087, 2011097, 2011141

Release Permits (with out-of-service radiation monitors)

2011003, 2011004. 2012006, 2012077, 2012076, 2012106, 2012109

Section 2RS8: Radioactive Solid Waste Processing and Radioactive Material Handling,

Storage, and Transportation

Procedures:

NDAP-QA-0646, Solid Radioactive Waste Process Control Program, Revision 12

WM-PS-150, 10CFR61 Non-Process Waste Stream Sampling, Revision 2

WM-PS-155, 10CFR61 Sample Shipping and Correlation Factor Determination, Revision 4

WM-PS-160, Radioactive Waste Curie Calculations, Revision 4

Condition Reports (* NRC identified):

1321067; 1351082; 1401530; 1447145; 1488491; 1527095; 1605044; 1508719; 1579742;

1578509; 1543806; 1629175; 1380959; 1505160; 1406109; 1504510; 1402236;

1543803; 1633075; 1633077; 1633078; 1633080; 1633089; 1633091

Miscellaneous:

Radioactive Material Shipments Nos.12-011; 12-015;12-025; 12-064;12-076

Teledyne Brown Engineering Report of Analysis for: control rod drives (CRDs); dry active waste;

condensate bead resin; liquid radwaste filter media; reactor water clean-up; condensate

filtration system backwash media; U-1 SPF clean-up; U-2 SPF clean-up

Quality Assurance Audit #1340786, dated 3/25/11, RP/Solid Radwaste Report

Walkup Assessment of Low Level Radioactive Waste Holding Facility, dated 2/16/12 & 3/2/12

PPL Audit No. 23091, February 15-16, 2011, Toxco Materials Management Center

Nuclear Utilities Procurement Issues Council (NUPIC) Audits:

  1. 22876, December 13-16, 2011, Studsvik Processing Facility - Erwin, LLC
  1. 22572; 22698; 22603; 22601; 22600, April 13-29, 2010, EnergySolutions
  1. 22937, January 24-27, 2011, Teledyne Brown Engineering
  1. 22873, November 14-18, 2011, GEL Laboratories, LLC

Training Material:

HP230, Revision 1, HAZMAT Training for Health Physics (HP) Technicians

HS053, Revision 2, HAZMAT Training for Container Handlers

EF009, Revision 2, Load Securement Training

Section 4OA1: Performance Indicator Verification

Condition Reports (* NRC identified):

1656747*, 1517915, 1357297, 1656747*

Attachment

A-10

Miscellaneous:

NEI 99-02, Regulatory Assessment PI Guideline, Revision 6

PL-NF-06-002, MSPI Basis Document, Revision 6

NDAP-QA-0737, Reactor Oversight Process (ROP) Performance Indicators, Revision 9

EP-AD-022, Nuclear Emergency Planning Performance Indicators, Revision 3

Alert and Notification System Reliability PI Data, October 2011 - September 2012

Drill and Exercise Performance PI Data, October 2011 - September 2012

Emergency Response Organization Drill Participation PI Data, October 2011 - September 2012

Section 4OA2: Identification and Resolution of Problems

Procedures:

OP-AD-010, Control of Licensed Operator License Status, Restrictions and Requirements,

Revision 6

NTP-QA-31.12, Preparation and Submission of NRC Form 396 - Certification of Medical

Examination by Facility Licensee and NRC Form 398 - Personal Qualifications

Statement - Licensee, Revision 5

ANSI/ANS-3.4-1983, American National Standard Medical Certification and Monitoring of

Personnel Requiring Operator Licenses for Nuclear Power Plants

NDAP-00-0761, Departmental Corrective Action Review Board, Revision 2

NDAP-QA-0702, Action Request and Condition Report Process, Revision 38

OP-023-001, Diesel Fuel Oil System, Revision 32

OP-023-001, Diesel Fuel Oil System, Revision 33

Condition Reports (* NRC identified):

1630609*, 1632818*, 1633719*, 1633700*, 1639335*, 1563931, 1587108, 1602093,

1602094, 1632000, 1632281, 16511165*, 1651391*, 1651419*, 1651434*, 1651844,

1651311, 1651824, 1502875, 1521513, 1602210, 1651434*, 1651844, 1651311,

1651824, 1502875, 1521513, 1602210, 1521488, 1582719 , 1549115, 1619762,

1634551, 1633700, 1406091, 1461742, 1541936, 1541933, 1601934, 1643405,

1641039, 1635196, 1446224, 1642609, 1344049, 1575787 , 1464711, 1629414,

1629416, 1547326, 1619762, 1651119, 1650638, 1650638, 1650020, 1456122,

1570413, 1557151, 1554948, 1557394, 1549033, 1538286, 1383039, 1521473,

1389530, 1653022*, 1653454*

Licensing and Design Basis Documents

Susquehanna Operating License Amendment and NRC Safety Evaluation Report (SER) to

Revise SRV Setpoint Tolerance from +/-1 percent to +/-3 percent (ML020520018), dated

March 7, 2002

Susquehanna Operating License Amendment and NRC SER to Revise SRV Setpoint Tolerance

from +/-3 percent to +3 percent, -5 percent (ML11291A137), dated November 17, 2011

TS 3.4.3 Basis, Safety/Relief Valves, Revision 4

TS 3.4.3, Safety/Relief Valves, Amendment 246

UFSAR Section 5.2.2, Overpressure Protection, Revision 64

UFSAR Section 7.7.1.12Nuclear Pressure Relief System, Revision 64

UFSAR Table 15C.0-2, Input Parameters & Initial Conditions for Transients, Unit 1 Cycle 16,

Revision 64

Calculations, Analysis, and Engineering Evaluations

Apparent Cause Evaluation (ACE) for CR 1399810, Revision 1

ACE for CR 1587108, Revision 0

Attachment

A-11

Miscellaneous:

LaSalle Operating License Amendment and NRC SER to Allow Surveillance of the Relief Mode

of SRV Operation with the Relief-Mode Actuator Uncoupled (ML013170087), dated

December 13, 2001

LER 50-387/2012-005-00, Valve Internal Misalignment Resulting in Multiple Inoperable Main

Steam SRVs, dated August 2, 2012

LER 50-388/2009-001-00, Multiple Test Failures of Main Steam SRVs, dated October 12, 2009

LER 50-388/2011-001-00, Multiple Inoperable Main Steam SRVs, dated July 1, 2011

Main Steam SRV Test Results History from 1985 to 2012

Maintenance Rule Basis Document, Unit 1 Main Steam System, dated September 12, 2012

NRC IR 05000387/2009003 AND 05000388/2009003, dated August 11, 2009

NRC IR 05000387/2010006 AND 05000388/2010006, dated March 15, 2010

NRC IR 05000387/2011005 AND 05000388/2011005, dated February 14, 2012

River Bend Operating License Amendment and NRC SER to Revise SRV Setpoint Tolerance

from +/-3 percent to +3 percent, -5 percent, and Allow Surveillance of the Relief Mode of

SRV Operation with the Relief-Mode Actuator Uncoupled (ML030450307), dated

February 13, 2003

Wyle Labs Test Records for SRVs Serial Numbers N63790-00-0019-112 and

N63790-00-0019-133, dated April 24, 2012 and February 25, 2012, Respectfully

OP002 CSI, Licensed Operator Requalification Program (Training Material), dated May 4,

2012

AD281, Justification of Interim Operation - Operability and Functionality Processes (Training

Material), dated July 23, 2012

AD264, Procedure and Work Instruction Use and Adherence, dated March 17, 2012

AD260, Procedure Writer Training, dated March 15, 2012

Procedure Quality/Procedure Use and Adherence PIIM, dated December 7, 2012

Procedure Quality/Procedure Use and Adherence PIIM, dated November 19, 2012

Station CAP PIIM, dated December 7, 2012

Station CAP PIIM, dated November 5, 2012

Station PIIM, dated September 4, 2012

Quick Hit Self-Assessment, Procedure Use and Adherence, dated September 12, 2012

Susquehanna Station Quarterly Trend Report, 3rd Quarter, 2012

Section 4OA3: Event Followup

Procedures:

EO-200-102, Reactor Vessel Level Control, Revision 8

ON-200-001, Reactor Scram, Reactor Scram Imminent, Revision 23

OP-AD-001, Operations Standards for System and Equipment Operation, Revision 49

OP-AD-327, Post Reactor Transient/Scram/Shutdown Elevation, Revision 26

OP-245-001, RFP and Lube Oil System, Revision 66

AR-204-001, RPS Division 2 2C651, Revision 32

ON-200-101, Scram, Scram Imminent, Revision 23

OP-AD-338, Reactivity Manipulations Standards and Communication Requirements,

Revision 19

GO-200-002, Plant Startup, Heatup, and Power Operation, Revision 67

SO-293-001, Quarterly Turbine Valve Cycling, Revision 37

SI-264-503, 24 Month Logic System Functional Test (LSFT) - Reactor Recirculation Pump Trip

System, Revision 11

SI-264-303, 24 Month Calibration - Reactor Vessel Low Low Level Channels (ATWS - RPT

and ARI), Revision 16

Attachment

A-12

Condition Reports:

1641025, 1643210, 1643098*, 1643098*, 1652339, 1652338, 1652507, 1652316, 1652377,

1652357, 1652391, 1652494, 1652316, 1652315, 1653679, 1653477, 1653479,

1455447, 1655159, 1654635, 1654555, 1654037, 1654158, 1653480, 1653762,

1655563, 1654991, 1654915, 1654258, 1653477, 1654235*, 1653633, 1148033,

1421109

Calculations:

EC-INST-1955, I&C Maintenance Calculation for LISB212N025D, Revision 0

EC-INST-1956, I&C Maintenance Calculation for LISB212N025D, Revision 0

Work Order:

1456387

Drawings:

E-129, Sheet 1, FW RFP Discharge and Bypass Valves, Revision 14

E-129, Sheet 2, FW RFP Discharge and Bypass Valves, Revision 9

M-2142, Sheet 1, Unit 2 P&ID Nuclear Boiler Vessel Instrumentation, Revision 48

MI-B31-275, Sheet 8, Reactor Recirculation Pump and MG Set, Revision 12

M1-B31-275, Sheet 7, Reactor Recirculation Pump and MG Set, Revision 15

Miscellaneous:

NUREG 1022, Event Reporting Guidelines: 10 CFR 50.72 and 50.73, Revision 2

EN 48496 dated November 09, 2012

EN 48500 dated November 10, 2012

Administrative Directive 12-07

TM-OP-045I-ST, Reactor Feedwater Level Control System (ICS/DCS), Revision 03

Startup Control Rod Sequence A1, Unit 2, Cycle 16

Engineering Journal, System 64, Journal ID 1316

Section 4OA5: Other Activities

Condition Reports:

1637421, 1635348, 1635279, 1635281, 1634516, 1634527, 1634536, 1634540, 1634541,

1634557, 1634560, 1634561, 1634562, 1634563, 1634544, 1634554, 1634555,

1634550, 1634559, 1632786, 1631806, 1630573, 1631474, 1630575*, 1630573,

1628346, 1627138*, 1623021, 1623016, 1601043, 1599743, 1599747, 1599726,

1599748, 1596549, 1599391, 1609708*, 1625702*, 1624965*, 1625645*, 1623008*,

1623018*, 1623022*, 1626973*, 1624965*, 1646231*, 1644480*, 16326521624541,

1613781, 1613752, 1613734, 1610459, 1609310, 1609332, 1609320, 1587132,

1618860, 1618312, 1613774, 1613798, 1613805, 1624632, 1624541, 1606132,

1644480*, 1659709

Miscellaneous:

Seismic Walkdown Checklist for: 0E506B, 1D653A, HV255F001, 2C618, 2B219, 1Y236,

HD07812B

Flooding Walkdown Record for: Unit 1 Reactor Building Penetrations on X-25-1 Sh.2

Section A-A, E EDG Building Penetrations on X-81-1 Sh.1 Section A-A

Attachment

A-13

LIST OF ACRONYMS

AC Alternating Current

ACE Apparent Cause Evaluation

ACMP Adverse Condition Monitoring Plan

ADAMS Agencywide Document and Access Management System

ALARA As Low As Is Reasonably Achievable

ANS Alert and Notification System

AR Action Report

ASME American Society of Mechanical Engineers

CAP Corrective Action Program

CAPCO-PIC Corrective Action Program Coordinator - Performance Improvement

Coordinators

CARB Corrective Action Review Board

CCA Common Cause Analysis

CCEMA Columbia County Emergency Management Agency

CFR Code of Federal Regulations

CNO Chief Nuclear Officer

CR Condition Report

CRA Condition Report Action

CRD Control Rod Drive

CREOAS Control Room Emergency Outside Air Supply

CS Control Structure

DCARB Departmental Corrective Action Review Boards

DEP Drill and Exercise Performance

DG Diesel Generator

DH Decay Heat

EAL Emergency Action Level

EDG Emergency Diesel Generator

EHC Electrohydraulic Control

ENS Emergency Notification System

EOOS Equipment Out-of-Service

EOP Emergency Operating Procedure

EP Emergency Preparedness

EPA Electrical Protective Assembly

EPU Extended Power Uprate

ERO Emergency Response Organization

ESS Engineering Safeguard System

ESW Emergency Service Water

ESSW Engineering Safeguards Service Water

EWR Engineering Work Request

FIN Finding

FPC Fuel Pool Cooling

GE General Electric

HP Health Physics

HPCI High Pressure Coolant Injection

HVAC Heating, Ventilation and Air-Conditioning

HX Heat Exchanger

ICS Integrated Control System

I&C Instrumentation and Controls

Attachment

A-14

IN Information Notice

IMC Inspection Manual Chapter

IP Inspection Procedure

IR NRC Inspection Report

ISI Inservice Inspection

JP Jet Pump

kV Kilovolts

LCEMA Luzerne County Emergency Management Agency

LCO Limiting Condition for Operation

LER Licensee Event Report

LOCA Loss of Coolant Accident

LOOP Loss of Offsite Power

LP Low Pressure

LSFT Logic System Functional Test

MPFF Maintenance Preventable Functional Failure

MPG Maintenance Procedure Group

MRC Management Review Committee

MREP Maintenance Rule Expert Panel

MRFF Maintenance Rule Functional Failures

MRO Medical Review Officer

MSPI Mitigating Systems Performance Index

M&TE Measuring and Test Equipment

NCV Non-Cited Violation

NDAP Nuclear Department Administrative Procedure

NDE Non-Destructive Examination

NEI Nuclear Energy Institute

NI Nuclear Instrumentation

NRC Nuclear Regulatory Commission

OA Other Activities

ODCM Offsite Dose Calculation Manual

ODM Operational Decision Making

OE Operating Experience

ORO Off-site Response Organization

PARS Publicly Available Records

PCP Process Control Program

PEMA Pennsylvania Emergency Management Agency

PI [NRC] Performance Indicator

PI&R Problem Identification and Resolution

PIIM Performance Improvement Integrated Matrix

PIM Plant Issues Matrix

PIRB Performance Improvement Review Board

PMT Post-Maintenance Test

PPL PPL Susquehanna, LLC

PS Planning Standard

QA Quality Assurance

RB Reactor Building

RCA Radiologically Controlled Area

RCA Root Cause Analysis

RCIC Reactor Core Isolation Cooling

RCS Reactor Coolant System

RG [NRC] Regulatory Guide

Attachment

A-15

RHR Residual Heat Removal

RHRSW Residual Heat Removal Service Water

RMA Risk Management Actions

ROP Reactor Oversight Process

RP Radiation Protection

RPIS Rod Position Information System

RPS Reactor Protection System

RPV Reactor Pressure Vessel

RSPS Risk Significant Planning Standard

SBO Station Blackout

SCBA Self-Contained Breathing Apparatus

SCCI Substantive Cross-Cutting Issue

SDP Significance Determination Process

SFP Spent Fuel Pool

SRM Source Range Neutron Monitoring

SRO Senior Reactor Operator

SRV Safety Relief Valve

SSC Structures, Systems and Components

SSES Susquehanna Steam Electric Station

SW Service Water

TI Temporary Instruction

TS Technical Specifications

T20 T20 Startup Transformer

UFSAR Updated Final Safety Analysis Report

UVR Under-Voltage Relay

VDC Volt Direct-Current

VT Visual Examination

WO Work Order

Attachment