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Category:Inspection Report
MONTHYEARIR 05000335/20250102024-10-21021 October 2024 Notification of St. Lucie Plant Units 1 & 2 Comprehensive Engineering Team Inspection - U.S. Nuclear Regulatory Commission Inspection Report 05000335/2025010 and 05000389/2025010 IR 05000335/20240112024-09-18018 September 2024 Biennial Problem Identification and Resolution Inspection Report 05000335/2024011 and 05000389/2024011 IR 05000335/20240052024-08-22022 August 2024 Updated Inspection Plan for St. Lucie, Units 1 & 2 - Report 05000335/2024005 and 05000389/2024005 IR 05000335/20240022024-08-13013 August 2024 Integrated Inspection Report 05000335-2024002 and 05000389-2024002 IR 05000335/20244012024-06-0303 June 2024 Security Baseline Inspection Report 05000335/2024401 and 05000389/2024401 IR 05000335/20240012024-05-10010 May 2024 Integrated Inspection Report 05000335/2024001 and 05000389/2024001 IR 05000335/20230062024-02-28028 February 2024 Annual Assessment Letter for St Lucie Units 1 & 2 - Report 05000335/2023006 and 05000389/2023006 IR 05000335/20230102024-01-26026 January 2024 NRC Quadrennial Focused Engineering Inspection (FEI) Commercial Grade Dedication Report 05000335/2023010 and 05000389/2023010 IR 05000335/20230042024-01-24024 January 2024 – Integrated Inspection Report 05000335/2023004 and 05000389/2023004 IR 05000335/20230032023-11-0606 November 2023 Integrated Inspection Report 05000335/2023003 and 05000389/2023003 IR 05000335/20233012023-09-20020 September 2023 NRC Operator License Examination Report 05000335/2023301 and 05000389/2023301 IR 05000335/20230022023-08-0707 August 2023 Integrated Inspection Report 05000335/2023002 and 05000389/2023002 IR 05000335/20234032023-06-29029 June 2023 Security Inspection Report 05000335/2023403 and 05000389/2023403 IR 05000335/20234022023-06-20020 June 2023 Security Baseline Inspection Report 05000335/2023402 and 05000389/2023402 IR 05000335/20234012023-05-16016 May 2023 Cyber Security Inspection Report 05000335/2023401 and 05000389/2023401 (Cover Letter) IR 05000335/20230012023-05-0909 May 2023 Integrated Inspection Report 05000335/2023001 and 05000389/2023001 IR 05000335/20234202023-03-21021 March 2023 Security Baseline Inspection Report 05000335/2023420 and 05000389/2023420 IR 05000335/20220062023-03-0101 March 2023 Annual Assessment Letter for St. Lucie Units 1 & 2 (Report 05000335/2022006 and 05000389/2022006) IR 05000335/20220042023-02-10010 February 2023 Integrated Inspection Report 05000335/2022004 and 05000389/2022004 IR 05000335/20220112022-12-27027 December 2022 Triennial Fire Protection Inspection Report 05000335/2022011 and 05000389/2022011 IR 05000335/20220032022-11-0404 November 2022 Integrated Inspection Report 05000335/2022003 and 05000389/2022003 ML22208A1762022-08-0404 August 2022 Review of the Fall 2021 Steam Generator Tube Inspection Report IR 05000335/20220022022-08-0101 August 2022 Integrated Inspection Report 05000335/2022002 and 05000389/2022002 ML22210A0782022-07-22022 July 2022 Stl 2022003 Document Request IR 05000335/20220122022-06-29029 June 2022 Biennial Problem Identification and Resolution Inspection Report 05000335 2022012 and 05000389 2022012 IR 05000335/20224012022-05-20020 May 2022 Security Baseline Inspection Report 05000335/2022401 and 05000389/2022401 IR 05000335/20220012022-05-12012 May 2022 Integrated Inspection Report 05000335/2022001 and 05000389/2022001 IR 05000335/20220102022-04-27027 April 2022 Design Basis Assurance Inspection (Programs) Inspection Report 05000335/2022010 and 05000389/2022010 IR 05000335/20214022022-04-0404 April 2022 Material Control and Accounting Program Inspection Report 05000335/2021402 and 05000389/2021402 - Public IR 05000335/20210062022-03-0202 March 2022 Annual Assessment Letter for St. Lucie, Units 1 & 2 (Report No. 05000335/2021006 and 05000389/2021006) IR 05000335/20210042022-02-14014 February 2022 Integrated Inspection Report 05000335/2021004 and 05000389/2021004 IR 05000335/20214032021-12-14014 December 2021 Security Baseline Inspection Report 05000335/2021403 and 05000389/2021403 IR 05000335/20210102021-12-0707 December 2021 Design Basis Assurance Inspection (Teams) Inspection Report 05000335/2021010 and 05000389/2021010 IR 05000335/20210032021-11-0303 November 2021 Integrated Inspection Report 05000335/2021003 and 05000389/2021003 IR 05000335/20210052021-08-25025 August 2021 Updated Inspection Plan for St. Lucie Plant Units 1 & 2 (Report 05000335/2021005 and 05000389/2021005) IR 05000335/20210022021-08-10010 August 2021 Integrated Inspection Report 05000335/2021002 and 05000389/2021002 IR 05000335/20214012021-06-23023 June 2021 Security Baseline Inspection Report 05000335/2021401 and 05000389/2021401 IR 05000335/20213012021-06-21021 June 2021 NRC Examination Report 05000335/2021301 and 05000389/2021301 IR 05000335/20210012021-05-12012 May 2021 Integrated Inspection Report 05000335/2021001 and 05000389/2021001 IR 05000335/20200062021-03-0303 March 2021 Annual Assessment Letter for St. Lucie Nuclear Plant, Unit 1 and Unit 2 Report 05000335/2020006 and 05000389/2020006 IR 05000335/20203012021-02-16016 February 2021 NRC Operator License Examination Report 05000335/2020301 and 05000389/2020301 IR 05000335/20200042021-02-0808 February 2021 Integrated Inspection Report 05000335/2020004 and 05000389/2020004 and Independent Spent Fuel Storage Installation (ISFSI) Inspection 07200061/2020002 IR 05000335/20204012021-01-0505 January 2021 Security Baseline Inspection Report 05000335/2020401 and 05000389/2020401 IR 05000335/20200112020-12-16016 December 2020 Triennial Inspection of Evaluation of Changes, Tests and Experiments Baseline Inspection Report 05000335/2020011 and 05000389/2020011 IR 05000335/20200032020-10-30030 October 2020 Integrated Inspection Report 05000335/2020003 and 05000389/2020003 ML20296A3732020-10-22022 October 2020 Security Inspection Report IR 05000335/20200052020-08-24024 August 2020 Updated Inspection Plan for St. Lucie Plant, Unit 1 and 2 (Report 05000335/2020005 and 05000389/2020005) IR 05000335/20200022020-07-29029 July 2020 St.Lucie Units 1 & 2 Integrated Inspection Report 05000335/2020002, 05000389/2020002, and Independent Spent Fuel Storage Installation Inspection (Lsfsi) 07200061/2020001 IR 05000335/20200102020-07-16016 July 2020 Biennial Problem Identification and Resolution Inspection Report 05000335/2020010 and 05000389/2020010 IR 05000335/20200012020-05-0505 May 2020 Integrated Inspection Report 05000335/2020001 and 05000389/2020001 and Exercise of Enforcement Discretion 2024-09-18
[Table view] Category:Letter
MONTHYEARIR 05000335/20250102024-10-21021 October 2024 Notification of St. Lucie Plant Units 1 & 2 Comprehensive Engineering Team Inspection - U.S. Nuclear Regulatory Commission Inspection Report 05000335/2025010 and 05000389/2025010 L-2024-085, Refueling Outage SL1-32 Low Pressure Turbine Rotor Inspection Results2024-10-15015 October 2024 Refueling Outage SL1-32 Low Pressure Turbine Rotor Inspection Results L-2024-165, Report of 10 CFR 50.59 Plant Changes, Tests and Experiments Made2024-10-14014 October 2024 Report of 10 CFR 50.59 Plant Changes, Tests and Experiments Made L-2024-118, Fleet License Amendment Request to Relocate Staff Qualifications from Technical Specifications to the Quality Assurance Topical Report (FPL-1)2024-10-0808 October 2024 Fleet License Amendment Request to Relocate Staff Qualifications from Technical Specifications to the Quality Assurance Topical Report (FPL-1) ML24255A3092024-09-30030 September 2024 SLRA - Revised SE Letter L-2024-155, Subsequent License Renewal Application, Third Annual Update2024-09-27027 September 2024 Subsequent License Renewal Application, Third Annual Update L-2024-158, Supplemental Information to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes2024-09-25025 September 2024 Supplemental Information to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes 05000335/LER-2024-001, Unplanned Reactor Scram2024-09-25025 September 2024 Unplanned Reactor Scram IR 05000335/20240112024-09-18018 September 2024 Biennial Problem Identification and Resolution Inspection Report 05000335/2024011 and 05000389/2024011 L-2024-136, Supplement to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes2024-09-16016 September 2024 Supplement to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes L-2024-138, License Amendment Request L-2024-138, Fuel Methodology Changes in Support of St. Lucie, Unit 2 Transition to 24-Month Fuel Cycles2024-09-11011 September 2024 License Amendment Request L-2024-138, Fuel Methodology Changes in Support of St. Lucie, Unit 2 Transition to 24-Month Fuel Cycles L-2024-148, Submittal of Offsite Dose Calculation Manual (Odcm), Revision 552024-09-0909 September 2024 Submittal of Offsite Dose Calculation Manual (Odcm), Revision 55 IR 05000335/20240052024-08-22022 August 2024 Updated Inspection Plan for St. Lucie, Units 1 & 2 - Report 05000335/2024005 and 05000389/2024005 L-2024-140, Cycle 28 Core Operating Limits Report2024-08-14014 August 2024 Cycle 28 Core Operating Limits Report L-2024-133, Snubber Program Plan Submittal2024-08-14014 August 2024 Snubber Program Plan Submittal IR 05000335/20240022024-08-13013 August 2024 Integrated Inspection Report 05000335-2024002 and 05000389-2024002 L-2024-132, 2024 Population Update Analysis2024-08-13013 August 2024 2024 Population Update Analysis L-2024-129, Relief Request (RR) 14. Limited Coverage Exams Due to Impractical Inservice Inspection Requirements - Fourth Ten-Year Inservice Inspection Program Interval2024-08-0707 August 2024 Relief Request (RR) 14. Limited Coverage Exams Due to Impractical Inservice Inspection Requirements - Fourth Ten-Year Inservice Inspection Program Interval ML24163A0012024-08-0505 August 2024 LTR-24-0119-1-1 Response to Nh Letter Regarding Review of NextEras Emergency Preparedness Amendment Review 05000389/LER-2024-003, Unplanned Reactor Scram2024-08-0505 August 2024 Unplanned Reactor Scram L-2024-121, Subsequent License Renewal Commitment 30 Revision2024-07-30030 July 2024 Subsequent License Renewal Commitment 30 Revision L-2024-123, Submittal of In-Service Inspection Program Owners Activity Report (OAR-1)2024-07-29029 July 2024 Submittal of In-Service Inspection Program Owners Activity Report (OAR-1) L-2024-125, Notice of Intent to Provide Supplemental Information to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes2024-07-24024 July 2024 Notice of Intent to Provide Supplemental Information to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes ML24184B2822024-07-16016 July 2024 – Request to Use a Later Code Edition and Addenda of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code, Section XI ML24193A2432024-07-12012 July 2024 – Interim Audit Summary Report in Support of Review of License Amendment Requests Regarding Fleet Emergency Plan L-2024-117, Safety Injection Tank Vent Through Wall Leakage2024-07-11011 July 2024 Safety Injection Tank Vent Through Wall Leakage L-2024-110, Environmental Protection Plan Report, Unusual or Important Environmental Event - Manatee in Intake2024-07-10010 July 2024 Environmental Protection Plan Report, Unusual or Important Environmental Event - Manatee in Intake L-2024-114, Quality Assurance Topical Report (FPL-1 Revision 31 Annual Submittal2024-07-10010 July 2024 Quality Assurance Topical Report (FPL-1 Revision 31 Annual Submittal L-2024-109, Schedule for Subsequent License Renewal Environmental Review2024-07-0303 July 2024 Schedule for Subsequent License Renewal Environmental Review ML24172A1562024-06-27027 June 2024 Relief Request - PSL2-I5-RR-01 Proposed Alternative to Amse Code XI Code Examination Requirements - System Leakage Test of Reactor Pressure Vessel Bottom Head and Class 1 and 2 Piping in Covered Trenches L-2024-104, Response to Request for Additional Information, St. Luce Relief Request (RR) 7, Proposed Alternative in Accordance with 10 CFR 50.55a(z)(1 Extension of Inspection Interval for Reactor Pressure Vessel Welds from 102024-06-26026 June 2024 Response to Request for Additional Information, St. Luce Relief Request (RR) 7, Proposed Alternative in Accordance with 10 CFR 50.55a(z)(1 Extension of Inspection Interval for Reactor Pressure Vessel Welds from 10 L-2024-097, Technical Specification Special Report2024-06-20020 June 2024 Technical Specification Special Report L-2024-102, Official Service List Update2024-06-19019 June 2024 Official Service List Update ML24149A2862024-06-12012 June 2024 NextEra Fleet - Proposed Alternative Frr 23-01 to Use ASME Code Case N-752-1, Risk-Informed Categorization and Treatment for Repair/Replacement Activities in Class 2 and 3 Systems Section X1, Division 1 (EPID L-2023-LLR-0009) - Letter L-2024-090, Revised Steam Generator Tube Inspection Reports2024-06-0404 June 2024 Revised Steam Generator Tube Inspection Reports IR 05000335/20244012024-06-0303 June 2024 Security Baseline Inspection Report 05000335/2024401 and 05000389/2024401 ML24135A0642024-05-17017 May 2024 Correction Letter - Amendment Nos. 253 and 208 Regarding Conversion to Improved Standard Technical Specifications L-2024-075, Notification of Improved Standard Technical Specifications (ITS) Implementation2024-05-13013 May 2024 Notification of Improved Standard Technical Specifications (ITS) Implementation IR 05000335/20240012024-05-10010 May 2024 Integrated Inspection Report 05000335/2024001 and 05000389/2024001 ML24127A0632024-05-0606 May 2024 Supplemental Information to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes L-2024-053, License Amendment Request L-2024-053, Updated Spent Fuel Pool Criticality Analysis2024-04-30030 April 2024 License Amendment Request L-2024-053, Updated Spent Fuel Pool Criticality Analysis L-2024-071, Cycle 27 Core Operating Limits Report2024-04-29029 April 2024 Cycle 27 Core Operating Limits Report L-2024-070, Cycle 32 Core Operating Limits Report2024-04-29029 April 2024 Cycle 32 Core Operating Limits Report ML24108A0632024-04-18018 April 2024 – Notification of Inspection and Request for Information for NRC Problem Identification and Resolution Inspection L-2024-064, Florida Power & Light Company - 10 CFR 50.46 - Emergency Core Cooling System SBLOCA 30-Day Report2024-04-17017 April 2024 Florida Power & Light Company - 10 CFR 50.46 - Emergency Core Cooling System SBLOCA 30-Day Report L-2024-056, Annual Radiological Environmental Operating Report for Calendar Year 20232024-04-17017 April 2024 Annual Radiological Environmental Operating Report for Calendar Year 2023 L-2024-054, 2023 Annual Environmental Operating Report2024-04-0909 April 2024 2023 Annual Environmental Operating Report ML24093A2612024-04-0202 April 2024 – Investigation Summary, Office of Investigations Case Number 2-2023-005 L-2024-047, Proposed Use of a Subsequent ASME Code Edition and Addenda2024-03-28028 March 2024 Proposed Use of a Subsequent ASME Code Edition and Addenda L-2024-045, Report of 10 CFR 72.48 Plant Changes2024-03-27027 March 2024 Report of 10 CFR 72.48 Plant Changes 2024-09-09
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UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 January 15, 2013 Mr. Mano Nazar Executive Vice President and Chief Nuclear Officer Florida Power and Light Company P.O. Box 14000 Juno Beach, FL 33408-0420
SUBJECT:
ERRATA ST. LUCIE NUCLEAR PLANT UNIT 1 - NRC INSPECTION PROCEDURE 95002 SUPPLEMENTAL INSPECTION REPORT 05000335/2012009 AND ASSESSMENT FOLLOW-UP LETTER FOR ST. LUCIE NUCLEAR PLANT UNIT 1 On November 16, 2012, the US Nuclear Regulatory Commission (NRC) issued the subject inspection report for St. Lucie Unit 1, ADAMS accession ML12321A239. The inspection and closure of a licensee event report (LER) entitled Unit 1 Reactor Trip on Turbine Trip was documented in the inspection report. The LER was incorrectly assigned the tracking number 05000335/2012-007-0. The correct LER tracking number is 05000335/2012-005-0.
Accordingly, we have revised pages 4 and 14 of the enclosure to Inspection Report 05000335/2012009 in order to document the necessary changes. Please replace pages 4 and 14 of the enclosure to the original report with the pages enclosed.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). The original report is available at ML12321A239. ADAMS is accessible from the NRC Web site at http://www.nrc.gov/readingrm/adams.html (The Public Electronic Reading Room).
I apologize for any inconvenience this error may have caused. If you have any questions, please contact me at (404) 562-4513.
Sincerely,
/RA/
Shane Sandal, Acting Chief Projects Branch 3 Division of Reactor Projects
Enclosure:
As stated cc w/encl: (See page 2)
_________________________ X SUNSI REVIEW COMPLETE G FORM 665 ATTACHED OFFICE RII:DRP RII:DRP SIGNATURE MJR /RA/ SRS /RA/
NAME MRiches SSandale DATE 01/14/2013 01/15/2013 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO M. Nazar 2 cc w/encl:
Joseph Jensen Bryan Koon Site Vice President Director St. Lucie Nuclear Plant Florida Division of Emergency Management Electronic Mail Distribution Electronic Mail Distribution Paul Freeman Donna Calabrese Vice President Emergency Preparedness Manager Organizational Effectiveness St. Lucie Plant Florida Power & Light Company Electronic Mail Distribution Electronic Mail Distribution J. Kammel Peter Wells Radiological Emergency Planning Vice President Administrator Outage Support CFAM Department of Public Safety Florida Power & Light Company Electronic Mail Distribution Electronic Mail Distribution Michael Baughman Robert J. Hughes Training Manager Plant General Manager St. Lucie Nuclear Plant St. Lucie Nuclear Plant Electronic Mail Distribution Electronic Mail Distribution Faye Outlaw Daniel D. DeBoer County Administrator Operations Site Director St. Lucie County St. Lucie Nuclear Plant Electronic Mail Distribution Electronic Mail Distribution James Petro Eric Katzman Managing Attorney-Nuclear Licensing Manager Florida Power & Light Company St. Lucie Nuclear Plant Electronic Mail Distribution Electronic Mail Distribution Jack Southard Larry Nicholson Director Director Public Safety Department Licensing St. Lucie County Florida Power & Light Company Electronic Mail Distribution Electronic Mail Distribution Alison Brown Nuclear Licensing Florida Power & Light Company Electronic Mail Distribution Cynthia Becker (Acting) Chief Florida Bureau of Radiation Control Department of Health Electronic Mail Distribution
M. Nazar 3 Letter to Mano Nazar from Shane Sandal dated January 15, 2013
SUBJECT:
ERRATA ST. LUCIE NUCLEAR PLANT UNIT 1 - NRC INSPECTION PROCEDURE 95002 SUPPLEMENTAL INSPECTION REPORT 05000335/2012009 AND ASSESSMENT FOLLOW-UP LETTER FOR ST. LUCIE NUCLEAR PLANT UNIT 1 Distribution w/encl:
C. Evans, RII L. Douglas, RII OE Mail RIDSNRRDIRS PUBLIC RidsNrrPMStLucie Resource
REPORT DETAILS
- 4. OTHER ACTIVITIES 4OA3 Follow-up of Events and Notices of Enforcement Discretion
.1 (Closed) Licensee Event Report (LER) 05000335/2012-003-00, 01, Manual Trip during Steam Bypass Control System Post-Modification Testing On March 31, 2012, while St. Lucie Unit 1 was at 10 percent reactor power and the licensee was performing preoperational testing of the SBCS, the reactor was manually tripped when a steam bypass control valve unexpectedly opened. Immediately following the reactor trip, the steam bypass control valve closed. Additionally, operators closed the main steam isolation valves in accordance with Emergency Operating Procedure (EOP-01), "Standard Post Trip Actions" due to steam generator pressure decreasing to less than 750 psia. During post trip recovery, EOP-05, "Excess Steam Demand" was entered as a result of not meeting Reactor Coolant System (RCS) average temperature between 525 and 535 degrees. EOP-05 was exited with no actions taken when temperature increased into the required band. The licensee documented this issue in the corrective action program as action request (AR) 1755493-01. The enforcement aspects associated with this LER are dispositioned in Section 4OA4.2.01 d.
.2 (Closed) LER 05000335/2012-005-00, Unit 1 Reactor Trip on Turbine Trip On June 2, 2012, Unit 1 automatically tripped from normal full power operation due to a turbine trip and loss of load following a failure of the TCS. There were no complications with the reactor trip. The reactor trip on turbine trip was caused by loss of communications in the recently installed Ovation TCS due to a failed fiber optic connection. The licensee documented this issue in the corrective action program as AR 01772644. The enforcement aspects associated with this LER are dispositioned in Section 4OA4.2.01 d.
4OA4 Supplemental Inspection (95002)
.1 Inspection Scope This supplemental inspection was conducted using Inspection Procedure (IP) 95002 to assess the licensees RCE associated with the four unplanned reactor trips described below that resulted in a degraded Initiating Events cornerstone in the reactor safety strategic performance area for Unit 1.
- 3rd Quarter 2011: Manual reactor trip from 100 percent power due to a large influx of jelly fish into the intake canal affecting the circulating water and intake cooling water systems. During the trip recovery, all main feedwater was lost. This was considered a complicated reactor trip. (AR 1679935)
- 4th Quarter 2011: Manual reactor trip from 100 percent power due to loss of circulating water pumps resulting in decreasing condenser vacuum. (AR 01697977)
Enclosure
SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT Licensee Personnel:
D. Andrews, Communications Manager C. Bible, Engineering Director E. Belizar, Projects Manager D. Calabreses, Emergency Preparedness Manager D. DeBoer, Operations Director R. Fillpeic, Engineering Design Manager J. Giampietro, Extended Power Uprate Engineering Manager M. Greer, Human Resources Manager T. Horton, Operations Assistant Manager B. Hughes, Plant General Manager J. Jenson, Site Vice President E. Katzman, Licensing Manager C. Martin, Radiation Protection Manager J. Ownes, PID Manager S. Redman, Communications Specialist M. Snyder, Quality Assurance Manager N. Sorensen, Business Operations Manager R. Webber, Unit Supervisor (95002 Lead)
T. Young, Security Manager NRC Personnel:
D. Rich, Chief, Branch 3, Division of Reactor Projects T. Hoeg, Senior Resident Inspector, St. Lucie Nuclear Plant R. Reyes, Resident Inspector, St. Lucie Nuclear Plant LIST OF REPORT ITEMS Opened and Closed 05000335/2012009-01 FIN Failure to Adequately Implement Design Changes Procedure (Section 4OA4.2.01 d)
Closed 05000335/2012-003-00 LER Manual Trip During Steam Bypass Control System and 2012-003-01 Post Modification Testing (Section 4OA3.1) 05000335/2012-005-00 LER Unit 1 Reactor Trip on Turbine Trip (Section 4OA3.2)
Attachment
REPORT DETAILS
- 4. OTHER ACTIVITIES 4OA3 Follow-up of Events and Notices of Enforcement Discretion
.1 (Closed) Licensee Event Report (LER) 05000335/2012-003-00, 01, Manual Trip during Steam Bypass Control System Post-Modification Testing On March 31, 2012, while St. Lucie Unit 1 was at 10% reactor power and the licensee was performing preoperational testing of the SBCS, the reactor was manually tripped when a steam bypass control valve unexpectedly opened. Immediately following the reactor trip, the steam bypass control valve closed. Additionally, operators closed the main steam isolation valves in accordance with Emergency Operating Procedure (EOP-01), "Standard Post Trip Actions" due to steam generator pressure decreasing to less than 750 psia. During post trip recovery, EOP-05, "Excess Steam Demand" was entered as a result of not meeting Reactor Coolant System (RCS) average temperature between 525 and 535 degrees. EOP-05 was exited with no actions taken when temperature increased into the required band. The licensee documented this issue in the corrective action program as action request (AR) 1755493-01. The enforcement aspects associated with this LER are dispositioned in Section 4OA4.2.01 d.
.2 (Closed) LER 05000335/2012-007-00, Unit 1 Reactor Trip on Turbine Trip On June 2, 2012, Unit 1 automatically tripped from normal full power operation due to a turbine trip and loss of load following a failure of the TCS. There were no complications with the reactor trip. The reactor trip on turbine trip was caused by loss of communications in the recently installed Ovation TCS due to a failed fiber optic connection. The licensee documented this issue in the corrective action program as AR 01772644. The enforcement aspects associated with this LER are dispositioned in Section 4OA4.2.01 d.
4OA4 Supplemental Inspection (95002)
.1 Inspection Scope This supplemental inspection was conducted using Inspection Procedure (IP) 95002 to assess the licensees RCE associated with the four unplanned reactor trips described below that resulted in a degraded Initiating Events cornerstone in the reactor safety strategic performance area for Unit 1.
- 3rd Quarter 2011: Manual reactor trip from 100 percent power due to a large influx of jelly fish into the intake canal affecting the circulating water and intake cooling water systems. During the trip recovery, all main feedwater was lost. This was considered a complicated reactor trip. (AR 1679935)
- 4th Quarter 2011: Manual reactor trip from 100 percent power due to loss of circulating water pumps resulting in decreasing condenser vacuum. (AR 01697977)
Attachment
SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT Licensee Personnel:
D. Andrews, Communications Manager C. Bible, Engineering Director E. Belizar, Projects Manager D. Calabreses, Emergency Preparedness Manager D. DeBoer, Operations Director R. Fillpeic, Engineering Design Manager J. Giampietro, Extended Power Uprate Engineering Manager M. Greer, Human Resources Manager T. Horton, Operations Assistant Manager B. Hughes, Plant General Manager J. Jenson, Site Vice President E. Katzman, Licensing Manager C. Martin, Radiation Protection Manager J. Ownes, PID Manager S. Redman, Communications Specialist M. Snyder, Quality Assurance Manager N. Sorensen, Business Operations Manager R. Webber, Unit Supervisor (95002 Lead)
T. Young, Security Manager NRC Personnel:
D. Rich, Chief, Branch 3, Division of Reactor Projects T. Hoeg, Senior Resident Inspector, St. Lucie Nuclear Plant R. Reyes, Resident Inspector, St. Lucie Nuclear Plant LIST OF REPORT ITEMS Opened and Closed 05000335/2012009-01 FIN Failure to Adequately Implement Design Changes Procedure (Section 4OA4.2.01 d)
Closed 05000335/2012-003-00 LER Manual Trip During Steam Bypass Control System and 2012-003-01 Post Modification Testing (Section 4OA3.1) 05000335/2012-007-00 LER Unit 1 Reactor Trip on Turbine Trip (Section 4OA3.2)
Attachment