IR 05000335/2022004

From kanterella
Jump to navigation Jump to search
– Integrated Inspection Report 05000335/2022004 and 05000389/2022004
ML23040A370
Person / Time
Site: Saint Lucie  
Issue date: 02/10/2023
From: David Dumbacher
Division Reactor Projects II
To: Coffey B
Florida Power & Light Co
References
IR 2022004
Download: ML23040A370 (14)


Text

SUBJECT:

ST LUCIE UNITS 1 & 2 - INTEGRATED INSPECTION REPORT 05000335/2022004 AND 05000389/2022004

Dear Bob Coffey:

On December 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at St Lucie Units 1 & 2 and discussed the results of this inspection with Robert Craven, Nuclear Site Vice President, St Lucie Power Plant and other members of your staff. The results of this inspection are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. One of these findings involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at St Lucie Units 1 & 2.

If you disagree with a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC Resident Inspector at St Lucie Units 1 & 2.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

February 10, 2023

Sincerely, David E. Dumbacher, Chief Reactor Projects Branch 3 Division of Reactor Projects Docket Nos. 05000335 and 05000389 License Nos. DPR-67 and NPF-16

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000335 and 05000389

License Numbers:

DPR-67 and NPF-16

Report Numbers:

05000335/2022004 and 05000389/2022004

Enterprise Identifier:

I-2022-004-0025

Licensee:

Florida Power & Light Company

Facility:

St Lucie Units 1 & 2

Location:

Jensen Beach, FL 34957

Inspection Dates:

October 01, 2022, to December 31, 2022

Inspectors:

J. Bundy, Senior Operations Engineer

P. Cooper, Senior Reactor Inspector

S. Downey, Senior Reactor Inspector

D. Lanyi, Senior Operations Engineer

T. Morrissey, Senior Resident Inspector

D. Orr, Senior Resident Inspector

S. Roberts, Resident Inspector

Approved By:

David E. Dumbacher, Chief

Reactor Projects Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at St Lucie Units 1 & 2, in accordance with

the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for

overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Unit 1 Manual Trip Due to Insufficient Feed Flow to 1A Steam Generator

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Initiating Events

Green

FIN 05000335/2022004-01

Open/Closed

None (NPP)

71153

A self-revealed Green finding was identified when the licensee failed to ensure condensate

flow controller (FIC-12-1) was classified in accordance with ER-AA-101, "Equipment

Reliability". Specifically, FIC-12-1 was classified non-critical, and its failure caused a

significant reduction in feedwater flow to steam generator 1A water level resulting in a manual

reactor trip.

Failed Unit 1 Emergency Core Cooling System (ECCS) Ventilation System Charcoal Filter

Testing Results

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Barrier Integrity

Green

NCV 05000335/2022004-02

Open/Closed

None (NPP)

71153

A self-revealed Green non-cited violation (NCV) of Technical Specification (TS) 6.8.1.a.,

Procedures and Programs, was identified for the licensees failure to develop and establish an

appropriate preventive maintenance schedule to replace charcoal adsorber units in the

emergency core cooling system (ECCS) ventilation system prior to methyl iodide efficiency

degrading to less than TS surveillance requirements (TSSR).

Additional Tracking Items

None.

PLANT STATUS

Unit 1 began the inspection period shut down in refueling outage, SL1-31. The unit was

restarted on October 3, 2022, and was returned to rated thermal power (RTP) on October 6,

2022. On November 14, 2022, the unit was down powered to 75 percent for a 1B drain cooler

tube leak repair and was returned to RTP on November 18, 2022, and remained at or near RTP

for the remainder of the inspection period.

Unit 2 operated at or near RTP for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix DProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 2515,</br></br>Appendix D" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated the adequacy of the overall preparations to protect risk-

significant systems from impending severe weather, Hurricane Nicole, on November

7 - 10, 2022.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

Unit 2 component cooling water (CCW) system while the 2B CCW pump was out of

service (OOS) for planned maintenance on October 19 - 20, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1)

Fire zone (FZ) 81, Unit 1 external control zones on October 6, 2022

(2)

FZ 7, Unit 2 external control zones on October 6, 2022

(3)

FZ 71, Unit 1 control room heating ventilation air conditioning area on October 26,

2022

(4)

FZs 42II and 42III, Unit 2 control room air conditioning room and control room

emergency air cleanup system room on October 26, 2022

(5)

FZ 2, Unit 2 pipe tunnel on October 26, 2022

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1)

The licensee completed the annual requalification operating examinations required to

be administered to all licensed operators in accordance with Title 10 of the Code of

Federal Regulations 55.59(a)(2), "Requalification Requirements," of the NRC's

"Operator's Licenses." During the week of January 2, 2023, the inspector performed

an in-office review of the overall pass/fail results of the individual operating

examinations and the crew simulator operating examinations in accordance with IP 71111.11, "Licensed Operator Requalification Program." These results were

compared to the thresholds established in Section 3.03, "Requalification Examination

Results," of IP 71111.11.

The inspectors reviewed and evaluated the licensed operator examination failure

rates for the requalification annual operating exam completed on December 20, 2022.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1

Sample)

(1)

The inspectors observed and evaluated licensed operator performance in the Control

Room during a Unit 1 reactor startup on October 3, 2022.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1)

The inspectors observed and evaluated a simulator licensed operator annual

operating examination on October 31, 2022.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components (SSCs) remain capable of performing their intended

function:

(1)

Action request (AR) 2429763, 1B2 emergency diesel generator (EDG) radiator

coolant leak, review completed on November 1, 2022

Aging Management (IP Section 03.03) (1 Sample)

The inspectors evaluated the effectiveness of the aging management program by reviewing

the following:

(1)

AR 2407701, Quarterly Review of License Renewal Internal Operating

Experience - 4th Quarter 2021

AR 2424155, Quarterly Review of License Renewal Internal Operating

Experience - 1st Quarter 2022

AR 2442435, Quarterly Review of License Renewal Internal Operating

Experience - 2nd Quarter 2022

Reviews were completed on December 1, 2022

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1)

Unit 1 elevated risk while the 1C auxiliary feedwater (AFW) pump was OOS for

unplanned maintenance on October 13, 2022

(2)

Unit 1 and Unit 2 elevated risk while the 1B EDG was OOS for planned maintenance

from October 24 - 25, 2022

(3)

Unit 1 and Unit 2 elevated risk while the 1A EDG was unavailable for a 24-hour

endurance run from November 28 - 29, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1)

AR 2439052, V09151, steam leak at hinge pin on check valve for AFW pump 1C

supply to SG 1A feedwater inlet, review completed on October 12, 2022

(2)

AR 2440216, Unit 2 RM-26-26, radiation monitor for Unit 2 containment atmosphere,

is causing nuisance alarms on the radiation monitoring computer system, review

completed on November 3, 2022

(3)

AR 2437929, 1C charging pump discharge piping leak and AR 2438397, charging

system piping leak downstream of MV-02-2, review completed on November 14, 2022

(4)

AR 2440221, Boric acid evaluation for Unit 2 RC-121-2B1 cold leg piping and reactor

vessel, review completed on November 30, 2022

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1

Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1)

Engineering Change (EC) 294435, 1A3 and 1B3 safety-related 4 kV switchgear,

replace SF6 breakers with vacuum breakers, review completed on October 5, 2022

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated the following post-maintenance testing activities to verify system

operability and/or functionality:

(1)

Work Order (WO) 40695460, 2B CCW pump overhaul, review completed on October

26, 2022

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated refueling outage SL1-31 activities from September 3, 2022,

to October 4, 2022.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability

and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (2 Samples)

(1)

1-OSP-69.14B, ESF-18 Month Surveillance for EDG Start on SIAS Without LOOP

and 24-Hour Load Run - Train B, reviewed on October 24 - 25, 2022

(2)

1-OSP-52.01A, Surveillance Test of Degraded Grid Voltage A Train, reviewed on

November 2, 2022

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS06: Emergency AC Power Systems (IP Section 02.05) (2 Samples)

(1)

Unit 1 (October 1, 2021, through September 30, 2022)

(2)

Unit 2 (October 1, 2021, through September 30, 2022)

MS07: High Pressure Injection Systems (IP Section 02.06) (2 Samples)

(1)

Unit 1 (October 1, 2021, through September 30, 2022)

(2)

Unit 2 (October 1, 2021, through September 30, 2022)

MS08: Heat Removal Systems (IP Section 02.07) (2 Samples)

(1)

Unit 1 (October 1, 2021, through September 30, 2022)

(2)

Unit 2 (October 1, 2021, through September 30, 2022)

MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)

(1)

Unit 1 (October 1, 2021, through September 30, 2022)

(2)

Unit 2 (October 1, 2021, through September 30, 2022)

MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)

(1)

Unit 1 (October 1, 2021, through September 30, 2022)

(2)

Unit 2 (October 1, 2021, through September 30, 2022)

71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (Section 03.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program

related to the following issues:

(1)

Several ARs related to previously identified structural deficiencies and areas of aging

related degradation associated with the Unit 1 and Unit 2 intake structure: AR

2408625, 2409095, 2409555, 2409612, 2410253, 2410259, and 2410333. These

ARs were selected for follow-up to verify the licensees corrective actions were

appropriate to maintain structural integrity of the intake structures and associated

appurtenances.

71153 - Follow Up of Events and Notices of Enforcement Discretion

Event Report (IP Section 03.02) (2 Samples)

H

The inspectors evaluated the following licensee event reports (LERs):

(1)

LER 050000335/2022-003-00, Manual Reactor Trip Due to Loss of Feedwater Pump.

(ADAMS Accession Number ML22301A127). The inspection conclusions associated

with this LER are documented in this report under Inspection Results Section 71153.

(2)

LER 050000335/2022-002-00, Condition Prohibited by Technical Specifications

(ADAMS Accession No. ML22301A124). The inspection conclusions associated with

this LER are documented in this report under Inspection Results Section 71153.

INSPECTION RESULTS

Unit 1 Manual Trip Due to Insufficient Feed Flow to 1A Steam Generator

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Initiating Events

Green

FIN 05000335/2022004-01

Open/Closed

None (NPP)

71153

A self-revealed Green finding was identified when the licensee failed to ensure condensate

flow controller (FIC-12-1) was classified in accordance with ER-AA-101, "Equipment

Reliability". Specifically, FIC-12-1 was classified non-critical, and its failure caused a

significant reduction in feedwater flow to steam generator 1A water level resulting in a manual

reactor trip.

Description: On September 2, 2022, St Lucie Unit 1 was down powered to begin refueling

outage SL1-31. After reaching approximately 45% rated thermal power, an operator was

assigned to manually control condensate flow to the single operating condensate pump using

the condensate recirculation valve (FCV-12-1) in accordance with procedure 1-GOP-123,

Turbine Shutdown - Full Load To Zero Load. When the local switch at condensate controller

FIC-12-1, was placed in manual, FCV-12-1 fully opened. FCV-12-1 fully opened caused a

substantial reduction in condensate flow to the operating main feedwater pump (MFP). The

MFP tripped on low suction pressure, resulting in a loss of steam generator feedwater flow.

Based on lowering and unrecoverable 1A steam generator water level, the reactor was

manually tripped by control room operators.

FIC-12-1 was infrequently used and, prior to being placed in service, was balanced by

adjusting a loader until a metal ball indicator was stable inside a visible switching zone. Once

balanced and switched to manual operation, there should be no FCV-12-1 movement until

the loader was adjusted. On September 2, 2022, the controller indicated balanced, but the

actual output of the manual controller was high resulting in FCV-12-1 going full open when

FIC-12-1 was transferred to manual.

The inspectors reviewed the root cause evaluation associated with this issue documented in

AR 2488832. The licensee determined that condensate flow controller FIC-12-1 is not

classified, maintained or pre-operational checked consistent with its actual functional

importance consistent with ER-AA-101, Equipment Reliability.

ER-AA-101, section 3.3, step 1, requires the licensee to implement the equipment reliability

process. ER-AA-101 Attachment 1, INPO AP-913, Equipment Reliability Process and

Objectives, references ER-AA-204-2006, Management of Critical Components and Single

Point Vulnerabilities (SPVs), for scoping, preventative maintenance, and continuing

improvement. ER-AA-204-2006, section 4.1, step 1, requires scoping and identification of

single point vulnerabilities and critical components to be accomplished using ER-AA-2006-

100001, Functional Importance Determination and ER Scoping. ER-AA-2006-100001,

section 7.0, step 2, part B, references Attachment 2, Criticality Criteria, to develop an initial

Functional Importance Determination (FID). A potential scram or large down power greater

than 20% should be classified as FID-1. FID-1 classification required recurring preventative

maintenance. FIC-12-1 was inappropriately classified as FID-N, i.e., a loss of a function will

not cause a significant impact on nuclear safety, production capability, or level of

consequence on other indicators of importance.

Corrective Actions: The licensee entered this issue into its corrective action program as AR

2435832. The licensee rebuilt FIC-12-1 and updated the FID for both Unit 1 and Unit 2 control

loop F-12-1 components. The licensee additionally initiated a procedural change to both units

[1,2]-GOP-123, Turbine Shutdown - Full Load To Zero, to maintain two condensate pumps in

operation during the down power to minimize the risk of FCV-12-1 spurious opening.

Corrective Action References: AR 2435832

Performance Assessment:

Performance Deficiency: The licensees failure to ensure controller FIC-12-1 was classified,

maintained or pre-operational checked consistent with its actual functional importance as

expected in ER-AA-101, Equipment Reliability, was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Equipment Performance attribute of the Initiating Events

cornerstone and adversely affected the cornerstone objective to limit the likelihood of events

that upset plant stability and challenge critical safety functions during shutdown as well as

power operations. Specifically, the licensee failed to ensure condensate recirculation valve

FIC-12-1 was classified in accordance with ER-AA-101, Equipment Reliability. FIC-12-1 was

classified non-critical, and its failure caused a reduction in steam generator 1A water level

resulting in a manual reactor trip.

Significance: The inspectors assessed the significance of the finding using IMC 0609

Appendix AProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609</br></br>Appendix A" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., The Significance Determination Process (SDP) for Findings At-Power. The

finding screened to very low safety significance (Green) because it did not cause a reactor

trip and the loss of mitigation equipment relied upon to transition the plant from the onset of

the trip to a stable shutdown condition (e.g., loss of main condenser or the loss of feedwater).

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to

this finding because the inspectors determined the finding did not reflect present licensee

performance.

Enforcement: Inspectors did not identify a violation of regulatory requirements associated

with this finding.

Failed Unit 1 Emergency Core Cooling System (ECCS) Ventilation System Charcoal Filter

Testing Results

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Barrier Integrity

Green

NCV 05000335/2022004-02

Open/Closed

None (NPP)

71153

A self-revealed Green non-cited violation (NCV) of Technical Specification (TS) 6.8.1.a.,

Procedures and Programs, was identified for the licensees failure to develop and establish

an appropriate preventive maintenance schedule to replace charcoal adsorber units in the

emergency core cooling system (ECCS) ventilation system prior to methyl iodide efficiency

degrading to less than TS surveillance requirements (TSSR).

Description: On September 3, 2022, the licensee received laboratory results for samples

taken from the ECCS ventilation system charcoal adsorber units, HVE-9A and HVE-9B. The

charcoal samples were obtained on August 31, 2022, and tested for methyl iodide penetration

in accordance with the Ventilation Filter Testing Program (VFTP) and TSSR 4.7.8.1.b. The

requirements of the VFTP are established in TS 6.8.4.k. and require the ECCS area

ventilation system charcoal adsorber units have a methyl iodide penetration less than or

equal to 2.5%. HVE-9A was at 6.05% and HVE-9B was at 3.26% methyl iodide

penetration. These results exceeded the TS maximum required limit of 2.5%. On September

3, 2022, the licensee declared both trains of ECCS ventilation system inoperable from August

31, 2022, which placed the unit in TS limiting condition for operation (LCO) 3.0.3. TS 3.0.3.

requires within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> that action shall be initiated to place the unit in a mode in which the

specification does not apply, which for this instance, required cold shutdown within the

subsequent 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Cold shutdown was established on September 3, 2022, at 1025 hours0.0119 days <br />0.285 hours <br />0.00169 weeks <br />3.900125e-4 months <br />

as part of the planned refuel outage, SL1-31, sequence. The licensee submitted LER 05000335/2022-002-00 to document this condition. The licensee entered this issue into the

corrective action program as ARs 2435856 and 2435857.

The inspectors reviewed LER 05000335/2022-002-00 and the associated corrective action

documents in ARs 2435856 and 2435857. The licensee concluded in its equipment failure

investigation reviews that although the charcoal is tested for methyl iodide penetration every

eighteen months, the charcoal efficiency cannot be trended with reliable

predictions. Additionally, the licensee did not have an appropriate replacement frequency for

the charcoal adsorber units to ensure the charcoal was replaced prior to unacceptable methyl

iodide penetration results. The charcoal adsorber units were 22 and 10 years in service for

HVE-9A and HVE-9B respectively, when replaced in October 2022.

Corrective Actions: The licensee replaced the charcoal adsorber units in HVE-9A and HVE-

9B during refuel outage SL1-31. The licensee also intended to replace all Unit 1 charcoal

adsorber units every 9 years and all Unit 2 charcoal adsorber beds every 10.5 years which

they judged to be conservative based on several years of VFTP results and site operating

experience. This corrective action was entered into the corrective action program as AR

2435856-09 on December 21, 2022.

Corrective Action References: ARs 2435856 and 2435857.

Performance Assessment:

Performance Deficiency: The licensees failure to implement a preventive maintenance

schedule to replace the charcoal adsorber units in the ECCS ventilation system prior to

efficiency degrading to less than technical specification surveillance requirements was a

performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the SSC and Barrier Performance attribute of the Barrier

Integrity cornerstone and adversely affected the cornerstone objective to provide reasonable

assurance that physical design barriers protect the public from radionuclide releases caused

by accidents or events. Specifically, the licensee failed to establish an appropriate preventive

maintenance schedule to replace charcoal adsorber units in the ECCS ventilation system

which caused methyl iodide efficiency to degrade below TS requirements.

Significance: The inspectors assessed the significance of the finding using IMC 0609

Appendix AProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609</br></br>Appendix A" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., The Significance Determination Process (SDP) for Findings At-Power. Using

Exhibit 3, Barrier Integrity, for "Control Room, Auxiliary, Reactor, or Spent Fuel Pool

Building," the inspectors determined the finding to be of very low safety significance (Green)

because the finding only represented a degradation of the radiological barrier function

provided for the control room, auxiliary building, spent fuel pool, SBGT system (BWR), or

EGTS system (PWR ice condenser).

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to

this finding because the inspectors determined the finding did not reflect present licensee

performance. The licensee since initial operation did not establish an appropriate

replacement schedule for charcoal adsorber units and the charcoal adsorber methyl iodide

test results were satisfactory for over ten years.

Enforcement:

Violation: St Lucie Unit 1 Technical Specification 6.8.1.a, stated in part, that written

procedures shall be established, implemented, and maintained covering the activities

referenced in the applicable procedures recommended in Appendix A, of Regulatory Guide 1.33, Revision 2, February 1978. Regulatory Guide 1.33, Revision 2, Appendix A, item 9,

Procedures for Performing Maintenance, subsection b, stated in part, preventive maintenance

schedules should be developed to specify replacement of such items as filters and

replacement of parts that have a specified lifetime. The Unit 1 ECCS ventilation system

charcoal adsorber units have a finite service life based on methyl iodide penetration

efficiency. Contrary to the above, from initial operation until December 21, 2022, the licensee

failed to establish a replacement schedule for the ECCS ventilation system charcoal adsorber

units.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On January 12, 2023, the inspectors presented the integrated inspection results to

Robert Craven, Nuclear Site Vice President, St Lucie Power Plant and other members of

the licensee staff.

THIRD PARTY REVIEWS

On November 16, 2022, the inspectors reviewed the Institute on Nuclear Power Operations

continuum report that was issued in October 2022.