IR 05000335/2020003

From kanterella
Jump to navigation Jump to search
Integrated Inspection Report 05000335/2020003 and 05000389/2020003
ML20304A326
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 10/30/2020
From: Randy Musser
NRC/RGN-II
To: Moul D
Florida Power & Light Co
References
IR 2020003
Download: ML20304A326 (9)


Text

October 30, 2020

SUBJECT:

ST. LUCIE UNITS 1 & 2 - INTEGRATED INSPECTION REPORT 05000335/2020003 AND 05000389/2020003

Dear Mr. Moul:

On September 30, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at St. Lucie Units 1 & 2. On October 19, 2020, the NRC inspectors discussed the results of this inspection with Mr. Dan DeBoer, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Randall A. Musser, Chief Reactor Projects Branch 3 Division of Reactor Projects

Docket Nos. 05000335 and 05000389 License Nos. DPR-67 and NPF-16

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000335 and 05000389

License Numbers:

DPR-67 and NPF-16

Report Numbers:

05000335/2020003 and 05000389/2020003

Enterprise Identifier: I-2020-003-0054

Licensee:

Florida Power & Light Company

Facility:

St. Lucie Units 1 & 2

Location:

Jensen Beach, FL 34957

Inspection Dates:

July 01, 2020 to September 30, 2020

Inspectors:

T. Morrissey, Senior Resident Inspector

S. Roberts, Resident Inspector

Approved By:

Randall A. Musser, Chief

Reactor Projects Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at St. Lucie Units 1 & 2, in accordance with

the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for

overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 began the inspection period at rated thermal power (RTP). On July 29, 2020, power was

lowered to approximately 81 percent RTP to support planned turbine valve testing and

maintenance. On July 31, 2020, Unit 1 was returned to RTP. On September 18, 2020, power

was rapidly lowered to approximately 50 percent RTP after a digital electric-hydraulic leak

developed on the intercept valve for the 1A moisture separator reheater. The leak was

repaired, and Unit 1 was returned to RTP on September 20, 2020. Unit 1 remained at RTP for

the remainder of the inspection period.

Unit 2 operated at or near RTP for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess licensee performance and compliance

with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President

of the United States on the public health risks of the coronavirus (COVID-19), resident and

regional inspectors were directed to begin telework and to remotely access licensee information

using available technology. During this time the resident inspectors performed periodic site

visits each week, increasing the amount of time on site as local COVID-19 conditions permitted.

As part of their onsite activities, resident inspectors conducted plant status activities as

described in IMC 2515, Appendix D; observed risk significant activities; and completed on site

portions of IPs. In addition, resident and regional baseline inspections were evaluated to

determine if all or portion of the objectives and requirements stated in the IP could be performed

remotely. If the inspections could be performed remotely, they were conducted per the

applicable IP. In some cases, portions of an IP were completed remotely and on site. The

inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated licensee readiness for impending adverse weather

conditions due to Hurricane Isaias approaching the site on July 30-August 2, 2020.

The site was under a hurricane warning; however, hurricane and tropical storm force

winds were not experienced on site.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

Unit 2, 2B emergency diesel generator (EDG) while the 2A EDG was out of service

(OOS) for a planned critical maintenance management (CMM) outage, on

July 7-11, 2020

(2)

Unit 1, 1B EDG and 1B3, 4,160-volt (V) engineered safeguards (ES) switch gear

while 1A EDG was OOS for a planned CMM outage on August 4-6, 2020

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1)

Unit 2, 2B EDG room, on July 8, 2020

(2)

Unit 1, fuel handling building 19.5-foot (ft) elevation, on July 15, 2020

(3)

Unit 2, high pressure safety injection (HPSI) and containment spray (CS) pump area,

on August 23, 2020

(4)

Unit 1, 1B EDG room, on August 31, 2020

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

(1)

Unit 2, 2A HPSI pump, 2A low pressure safety injection (LPSI) pump, and 2A CS

pump, flood area, on September 10, 2020

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1)

Unit 1, The inspectors observed and evaluated licensed operator performance in the

control room during a down power to 81 percent RTP to support turbine valve testing

and 4B feedwater heater level control repairs, on July 29, 2020

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1)

On August 24, 2020, the inspectors observed a licensed operator requalification

training evaluation on the control room simulator.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (3 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components (SSCs) remain capable of performing their intended

function:

(1)

Action Request (AR) 2357368, Unit 1 electrical equipment room fan damper failed

closed

(2)

Unit 1, intake cooling water (ICW) system health report

(3)

Unit 2, safety injection (SI) system health report

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed;

(1)

Unit 2, elevated risk while 2A EDG was OOS for a planned CMM outage, from

July 7-11, 2020

(2)

Unit 1, elevated risk while 1A EDG was OOS for a planned CMM outage, from

August 4-6, 2020

(3)

Unit 1, elevated risk while 1A LPSI was OOS for planned maintenance and 1A EDG

was OOS for planned surveillance testing, on August 31, 2020

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1)

AR 2363584, Unit 2, upper and lower grippers engaged on numerous rod control

element assemblies (CEAs), on August 13, 2020

(2)

AR 2363094, Unit 1, 1B LPSI pump casing vent valve, (V3674), seat leakage, on

August 12, 2020

(3)

AR 2365678, Unit 1, B ICW header pipe, (CW-90) has an area below minimum wall

thickness, on August 27, 2020

(4)

AR 2366911, Unit 1, oil leakage from 1C charging pump, on September 3, 2020

(5)

AR 2369432, Unit 2, reactor protection system (RPS) reactor coolant low flow

channel trip (failed relay), on September 29, 2020

(6)

AR 2368474, Unit 1, component cooling water (CCW) valve, (MV-14-2), has corroded

torque tube base, on September 24, 2020

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the following post maintenance test activities to verify system

operability and functionality:

(1)

Unit 2, Work Order (WO), 40724034, 2A EDG CMM outage, July 7-11, 2020

(2)

Unit 1, WO 40724032, 1A EDG CMM outage, August 4-6, 2020

(3)

Unit 2, WO 40640995, 2B LPSI pump SF-6 Breaker preventative maintenance,

August 17, 2020

(4)

Unit 1, WO 40714125, repack 1A charging pump, September 30, 2020

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01) (3 Samples)

(1)

Unit 2, 2-OSP-69.24, "Engineered Safeguards Relay Test Train A," on July 10, 2020

(2)

Unit 1, 1-OSP-22.04, "Unit 1 Semi Annual Turbine Valve Test," on July 29, 2020

(3)

Unit 1, 1-SMI-69.02, "Engineered Safeguards Actuation System - Channel Functional

Test," on August 10, 2020

Inservice Testing (IP Section 03.01) (2 Samples)

(1)

Unit 2, 2-OSP-09.01C, "2C Auxiliary Feedwater Pump Code Run," on August 6, 2020

(2)

Unit 2, 2-OSP-03.06B, "2B Low Pressure Safety Injection Pump Code Run," on

August 17, 2020

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1

Sample)

NOTE: The sample below was erroneously entered as a sample in integrated inspection

report 2020-002, ADAMS Accession No. (ML20212L728). This error was administrative in

nature. Therefore, inspection report 2020-002 was not amended to address the error.

The sample was removed and annotated from inspection report 2020-002 within the NRC's

reactor program system (RPS) inspection tracking system and correctly applied to this

report.

(1)

On July 21, 2020 the inspectors evaluated an emergency response drill that included

a loss of off-site power (LOOP), loss of the 2A EDG, and a cyber-attack on station

computers.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (2 Samples)

(1)

Unit 1, Safety System Functional Failures from July 1, 2019, through June 30, 2020

(2)

Unit 2, Safety System Functional Failures from July 1, 2019, through June 30, 2020

INSPECTION RESULTS

No findings were identified.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On October 19, 2020, the inspectors presented the integrated inspection results to

Mr. Dan DeBoer, Site Vice President, and other members of the licensee staff.