ML070440126

From kanterella
Jump to navigation Jump to search
IR 05000275-06-005, 05000323-06-005; 10/1/06 - 12/31/06; Diablo Canyon Power Plant Units 1 and 2; Maintenance Risk Assessments and Emergent Work Control, Problem Identification and Resolution, Operability Evaluations, and Other Activities
ML070440126
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 02/13/2007
From: Vincent Gaddy
NRC/RGN-IV/DRP/RPB-B
To: Keenan J
Pacific Gas & Electric Co
References
IR-06-005
Download: ML070440126 (53)


See also: IR 05000275/2006005

Text

February 13, 2007

John S. Keenan

Senior Vice President - Generation

and Chief Nuclear Officer

Pacific Gas and Electric Company

P.O. Box 770000

Mail Code B32

San Francisco, CA 94177-0001

SUBJECT: DIABLO CANYON POWER PLANT - NRC INTEGRATED INSPECTION

REPORT 05000275/2006005 AND 05000323/2006005

Dear Mr. Keenan:

On December 31, 2006, the U.S. Nuclear Regulatory Commission completed an inspection at

your Diablo Canyon Power Plant, Units 1 and 2, facility. The enclosed integrated report

documents the inspection findings that were discussed on January 10, 2007, with Ms. Donna

Jacobs and members of your staff.

This inspection examined activities conducted under your licenses as they relate to safety and

compliance with the Commission's rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

There were three NRC-identified findings and one self-revealing finding of very low safety

significance (Green) identified in this report. These findings involved violations of NRC

requirements. However, because of their very low risk significance and because they are

entered into your corrective action program, the NRC is treating these four findings as noncited

violations (NCVs) consistent with Section VI.A of the NRC Enforcement Policy. If you contest

any NCV in this report, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive, Suite

400, Arlington, Texas 76011-4005; the Director, Office of Enforcement, U.S. Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

Diablo Canyon Power Plant.

Pacific Gas and Electric Company -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document

system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Vince G. Gaddy, Chief

Project Branch B

Division of Reactor Projects

Dockets: 50-275

50-323

Licenses: DPR-80

DPR-82

Enclosure:

NRC Inspection Report 05000275/2006005

and 05000323/2006005

w/attachment: Supplemental Information

cc w/enclosure:

Donna Jacobs

Vice President, Nuclear Services

Diablo Canyon Power Plant

P.O. Box 56

Avila Beach, CA 93424

James R. Becker, Vice President

Diablo Canyon Operations and

Station Director, Pacific Gas and

Electric Company

Diablo Canyon Power Plant

P.O. Box 56

Avila Beach, CA 93424

Sierra Club San Lucia Chapter

ATTN: Andrew Christie

P.O. Box 15755

San Luis Obispo, CA 93406

Pacific Gas and Electric Company -3-

Nancy Culver

San Luis Obispo Mothers for Peace

P.O. Box 164

Pismo Beach, CA 93448

Chairman

San Luis Obispo County Board of

Supervisors

County Government Building

1055 Monterey Street, Suite D430

San Luis Obispo, CA 93408

Truman Burns\Robert Kinosian

California Public Utilities Commission

505 Van Ness Ave., Rm. 4102

San Francisco, CA 94102-3298

Diablo Canyon Independent Safety Committee

Robert R. Wellington, Esq.

Legal Counsel

857 Cass Street, Suite D

Monterey, CA 93940

Director, Radiological Health Branch

State Department of Health Services

P.O. Box 997414 (MS 7610)

Sacramento, CA 95899-7414

Antonio Fernandez, Esq.

Pacific Gas and Electric Company

P.O. Box 7442

San Francisco, CA 94120

City Editor

The Tribune

3825 South Higuera Street

P.O. Box 112

San Luis Obispo, CA 93406-0112

James D. Boyd, Commissioner

California Energy Commission

1516 Ninth Street (MS 34)

Sacramento, CA 95814

Pacific Gas and Electric Company -4-

Jennifer Tang

Field Representative

United States Senator Barbara Boxer

1700 Montgomery Street, Suite 240

San Francisco, CA 94111

Chief, Radiological Emergency

Preparedness Section

Oakland Field Office

Chemical and Nuclear Preparedness

and Protection Division

Department of Homeland Security

1111 Broadway, Suite 1200

Oakland, CA 94607-4052

Pacific Gas and Electric Company -5-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (RJC1)

Senior Resident Inspector (TWJ)

Branch Chief, DRP/B (VGG)

Senior Project Engineer, DRP/E (FLB2)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (MSH3)

DRS STA (DAP)

V. Dricks, PAO (VLD)

D. Cullison, OEDO RIV Coordinator (DGC)

ROPreports

DC Site Secretary (AWC1)

W. A. Maier, RSLO (WAM)

R. E. Kahler, NSIR (REK)

SUNSI Review Completed: __yes___ ADAMS: G Yes G No Initials: __vgg___

G Publicly Available G Non-Publicly Available G Sensitive G Non-Sensitive

R:\_REACTORS\_DC\2006\DC2006-05RP-TWJ.wpd

RIV:RI:DRP/B RI:DRP/B SRI:DRP/B C:DRS/OB

TAMcConnell MABrown TWJackson ATGody

T - VGGaddy T - VGGaddy T - VGGaddy /RA/

2/9/07 2/9/07 2/9/07 1/31/07

DRS:PSB DRS:EB1 DRS:EB2 C:DRP/B

MPShannon WBJones LJSmith VGGaddy

/RA/ /RA/ /RA/ /RA/

2/1/07 1/31/07 1/30/07 2/13/07

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets: 50-275, 50-323

Licenses: DPR-80, DPR-82

Report: 05000275/2006005

05000323/2006005

Licensee: Pacific Gas and Electric Company

Facility: Diablo Canyon Power Plant, Units 1 and 2

Location: 7 1/2 miles NW of Avila Beach

Avila Beach, California

Dates: October 1 through December 31, 2006

Inspectors: T. Jackson, Senior Resident Inspector

T. McConnell, Resident Inspector

M. Brown, Resident Inspector

M. Peck, Senior Resident Inspector - Callaway Plant

J. Dodson, Regional Operations Officer

J. Drake, Operation Engineer

P. Goldberg, Reactor Inspector

R. Kellar, Health Physicist

R. Lantz, Senior Emergency Preparedness Inspector

Approved By: V. G. Gaddy, Chief, Projects Branch B

Division of Reactor Projects

-1- Enclosure

TABLE OF CONTENTS

PAGE

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

REACTOR SAFETY

1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R07 Biennial Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R11 Licensed Operator Requalification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

1R13 Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 12

1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

1R17 Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

1R19 Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

1R23 Temporary Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

1EP1 Exercise Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

OTHER ACTIVITIES

40A1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

4OA5 Other . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

4OA6 Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 35

ATTACHMENT: SUPPLEMENTAL INFORMATION

Key Points of Contact . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

Items Opened, Closed and Discussed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

List of Documents Reviewed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

List of Acronyms . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-13

-2- Enclosure

SUMMARY OF FINDINGS

IR 05000275/2006-005, 05000323/2006-005; 10/1/06 - 12/31/06; Diablo Canyon Power Plant

Units 1 and 2; Maintenance Risk Assessments and Emergent Work Control, Problem

Identification and Resolution, Operability Evaluations, and Other Activities.

This report covered a 13-week period of inspection by resident inspectors and Region-based

health physics and reactor inspectors. Three NRC-identified and one self-revealing, Green,

noncited violations were identified. The significance of most findings is indicated by their color

(Green, White, Yellow, or Red) using Inspection Manual Chapter 0609 Significance

Determination Process. Findings for which the Significance Determination Process does not

apply may be Green or be assigned a severity level after NRC management review. The

NRCs program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Criterion III, Design Control, was identified for the failure to apply adequate

design control measures regarding the installation of thimble tubes with chrome-

plated bands. Specifically, Pacific Gas and Electric Company installed thimble

tubes with chrome-plated bands at the fuel assembly bottom nozzle/lower core

plate interface to address flow-induced vibration wear. Due to the failure of

engineering personnel to account for the chrome-plated bands in the thimble

tube relocation procedure, the chrome-plated band on Thimble Tube L-13 was

removed from its designed location at the fuel assembly bottom nozzle, thereby

increasing the potential for thimble tube through-wall wear. This issue was

entered into Pacific Gas and Electric Companys corrective action program as

Nonconformance Report N0002211.

The finding is greater than minor because it is associated with the Initiating

Events Cornerstone attribute of design control and affects the associated

cornerstone objective to limit the likelihood of those events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. Using the Inspection Manual Chapter 0609, Significance

Determination Process, Phase 1 Worksheet, the finding is determined to have

very low safety significance because, assuming the worst-case degradation, the

finding would not result in exceeding the Technical Specification limit for

identified reactor coolant system leakage or affect mitigating systems.

Specifically, the inspectors verified the worst-case leakage, i.e., guillotine break,

from a thimble tube at the fuel assembly bottom nozzle/lower core plate interface

to be approximately 7 gpm versus the Technical Specification reactor coolant

system identified leakage limit of 10 gpm. The finding has a crosscutting aspect

in the area of problem identification and resolution associated with the corrective

action program because Pacific Gas and Electric Company removed a corrective

action to prevent recurrence of significant thimble tube wear (Section 4OA5.5).

-3- Enclosure

Cornerstone: Mitigating Systems

Criterion XVI, Corrective Actions, was identified for the failure to promptly

correct a condition adverse to quality. Specifically, on October 15, 2006, Pacific

Gas and Electric Company implemented a temporary modification to Vital

Battery 1-1 contrary to American National Standards Institute/Institute of

Electrical and Electronics Engineers Standard 450-1995, "IEEE Recommended

Practice for Maintenance, Testing, and Replacement of Large Lead Storage

Batteries for Generating Stations and Substations. Additionally, surveillance

tests to monitor the condition of the degraded battery cell were adversely

affected by the installed temporary modification. This issue was entered into

Pacific Gas and Electric Companys corrective action program as Action

Request A0678820.

The finding is greater than minor because it is associated with the Mitigating

Systems Cornerstone attribute of equipment performance and affects the

associated cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Using the Manual Chapter 0609, Significance Determination

Process, Phase 1 Worksheet, the inspectors determined that this finding is of

very low safety significance because it did not represent an actual loss of safety

function of a single train for greater than its Technical Specification allowed

outage time. This finding has a crosscutting aspect in the area of problem

identification and resolution associated with the corrective action program in that

engineering staff did not thoroughly assess the operability of the battery and

correct a condition adverse to quality in a timely manner (Section 1R15).

Criterion III, Design Control, was determined for the failure of engineering

personnel to apply adequate design control measures. Specifically, on

February 9, 2006, engineering personnel changed the acceptance criteria in the

auxiliary saltwater pump surveillance test from greater than zero packing leak-off

to zero packing leak-off with packing gland temperature less than 120EF. The

acceptance criteria change was based on engineering judgment, even though

vendor documentation called for greater than zero packing leak-off to prevent

packing and pump shaft damage. This issue was entered into Pacific Gas and

Electric Companys corrective action program as Action Request A0684631.

The finding is greater than minor because it is associated with the Mitigating

Systems Cornerstone attribute of procedure quality and affects the associated

cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Using the Manual Chapter 0609, Significance Determination Process, Phase 1

Worksheet, the finding is determined to be of very low safety significance

because it did not represent an actual loss of system safety function, did not

represent an actual loss of a single train for greater than its Technical

-4- Enclosure

Specification allowed outage time, and the finding did not screen as potentially

risk significant due to a seismic, flooding, or severe weather initiating event. This

finding has a crosscutting aspect in the area of human performance associated

with resources because engineering personnel failed to provide up-to-date

design documentation to support a design change in surveillance test

acceptance criteria (Section 4OA2.2).

Cornerstone: Barrier Integrity

Criterion XVI, Corrective Actions, was determined for the failure of engineering

and operations personnel to promptly identify and correct a condition adverse to

quality. On two occasions between September 29 and November 9, 2006,

operations and engineering personnel: (1) failed to address operability when

using manual actions in place of automatic actions associated with the auxiliary

building ventilation system and (2) failed to fully address the impact of debris

between the circuit card and the panel connections of the auxiliary building

ventilation system. This issue was entered into Pacific Gas and Electric

Companys corrective action program as Action Request A0678429.

The finding is greater than minor because it is associated with the Barrier

Integrity Cornerstone attribute of structure, system, component, and barrier

performance and affects the associated cornerstone objective to provide

reasonable assurance that physical design barriers protect the public from

radionuclide releases caused by accidents or events. Using the Inspection

Manual Chapter 0609, "Significance Determination Process," Phase 1

Worksheet, the finding is determined to have very low safety significance

because the finding only represents a degradation of the radiological barrier

function provided for the auxiliary building. This finding has a crosscutting

aspect in the area of problem identification and resolution associated with the

corrective action program because operations and engineering personnel did not

adequately evaluate operability of the auxiliary building ventilation system due to

the failure to fully encompass all aspects of the degraded conditions and

corresponding compensatory measures (Section 1R13).

-5- Enclosure

REPORT DETAILS

Summary of Plant Status

Diablo Canyon Unit 1 began this inspection period at 100 percent power. On

November 26, 2006, operators reduced power to 50 percent for circulating water tunnel

cleaning. Upon completion of the maintenance, reactor power was returned to 100 percent on

December 1 and maintained that power level for the remainder of the inspection period.

Diablo Canyon Unit 2 began this inspection period at 100 percent power. On December 10,

operators reduced power and manually tripped the reactor due to indications of Reactor

Coolant Pump (RCP) 2-2 high stator temperature. Following repair activities, operators

restarted the Unit 2 reactor on December 11, entering Mode 2 (startup). On December 11,

while reactor power was being restored to 100 percent, Circulating Water Pump (CWP) 2-1

experienced an electrical short at the motor terminal leads, resulting in a reactor trip. Following

repair activities, operators restarted the Unit 2 reactor on December 12, entering Mode 2.

Reactor power was returned to 100 percent on December 19 and remained at that power level

for the remainder of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R05 Fire Protection (71111.05)

Quarterly Inspection

a. Inspection Scope

The inspectors walked down the six below listed plant areas to assess the material

condition of active and passive fire protection features and their operational lineup and

readiness. The inspectors: (1) verified that transient combustibles and hot work

activities were controlled in accordance with plant procedures; (2) observed the

condition of fire detection devices to verify they remained functional; (3) observed fire

suppression systems to verify they remained functional and that access to manual

actuators was unobstructed; (4) verified that fire extinguishers and hose stations were

provided at their designated locations and that they were in satisfactory condition;

(5) verified that passive fire protection features (electrical raceway barriers, fire doors,

fire dampers, steel fire proofing, penetration seals, and oil collection systems) were in a

satisfactory material condition; (6) verified that adequate compensatory measures were

established for degraded or inoperable fire protection features and that the

compensatory measures were commensurate with the significance of the deficiency;

and (7) reviewed the Final Safety Analysis Report (FSAR) Update to determine if Pacific

Gas and Electric Company (PG&E) identified and corrected fire protection problems.

  • October 3, 2006, Unit 1, Control Room Cable Spreading Room
  • October 3, 2006, Unit 2, Control Room Cable Spreading Room

-6- Enclosure

  • October 10, 2006, Unit 1, Diesel Engine Generator Rooms
  • October 10, 2006, Unit 2, Diesel Engine Generator Rooms
  • October 11, 2006, Units 1 and 2, 140' and 85' elevation fire equipment storage

lockers

  • December 28, 2006, Unit 1, 85' elevation turbine building

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed six samples.

b. Findings

No findings of significance were identified.

1R07 Biennial Heat Sink Performance (71111.07B)

.1 Performance of Testing, Maintenance and Inspection Activities

a. Inspection Scope

The inspectors selected three heat exchangers that were either directly or indirectly

connected to the safety-related service water system. The inspectors reviewed PG&E's

test and cleaning methodology for the following heat exchangers:

  • Containment Fan Cooler Units

In addition, the inspectors reviewed test data and inspection and cleaning records for

the heat exchangers and design and vendor-supplied information to ensure that the heat

exchangers were performing within their design bases. The inspectors also reviewed

chemical controls to avoid fouling, the heat exchanger test, and inspection and cleaning

results. Specifically, the inspectors reviewed design conditions, appropriate use of test

instrumentation, and appropriate accounting for instrument inaccuracies. Additionally,

the inspectors reviewed inspection and cleaning results and trending results, if available.

The inspectors reviewed the methods and results of heat exchanger inspection and

cleaning to verify that the methods used to inspect and clean were consistent with

industry standards. The results were found appropriately dispositioned such that the

final conditions were acceptable.

The inspectors completed three samples.

-7- Enclosure

b. Findings

No findings of significance were identified.

.2 Verification of Conditions and Operations Consistent with Design Bases

a. Inspection Scope

For the selected heat exchangers, the inspectors reviewed the documents listed in the

attachment to verify that PG&E established heat sink and heat exchanger condition and

that operation and test criteria were consistent with the design assumptions.

Specifically, the inspectors reviewed the applicable calculations to ensure that the

thermal performance test acceptance criteria for the heat exchangers were being

applied consistently throughout the calculations. The inspectors also reviewed

documents in order to verify that the appropriate acceptance values for fouling and tube

plugging for the heat exchangers cooled by the component cooling water heat

exchangers remained consistent with the values used in the design-basis calculations.

b. Findings

Introduction: An unresolved item (URI) was identified regarding inadequate design

control measures for verifying the adequacy of the safety-related RHR system heat

exchangers. PG&E stated that the RHR heat exchangers were not inspected and

cleaned, due to as low as is reasonably achievable (ALARA) considerations, and the

heat exchangers were not tested. Test Procedure STP V-13A, CCW Flow Balancing,

along with Calculation M-1017, Component Cooling Water System, were used by

PG&E to determine if the RHR heat exchanger would meet its design basis. The

calculation only establishes the flow balance for the component cooling water (CCW)

system based on PG&Es modeling assumptions. This issue is unresolved for both

significance and enforcement, since additional technical review by NRC was needed to

assess this issue.

Description: The inspectors reviewed Calculation M-1017, Component Cooling Water

System, Revision 3, and found that the purpose of the calculation was to compute the

flow rates in the CCW system for input into the accident analysis. The inspectors noted

that the calculation only established the flow balance of the CCW system based on

PG&Es modeling assumption. The calculation did not address the heat transfer

capability of any of the heat exchangers and the references listed did not appear to

provide heat transfer capability. The inspectors noted that the assumptions used by

PG&E could vary the results of the calculation. Some of the assumptions were: the

manufacturers pressure drop data for the CCW, RHR, and containment fan cooling

unit (CFCU) heat exchangers was assumed to be accurate; the RHR heat exchanger

throttle valve was assumed to be in the full open position without verification; and even

though the CCW systems of Units 1 and 2 are slightly different, PG&E concluded that

the results of Unit 1 were applicable for Unit 2. Any of these assumptions, if incorrect,

could change the results.

-8- Enclosure

The inspectors reviewed Surveillance Test Procedure STP-V13A, CCW Flow

Balancing, Revision 15. The purpose of the test is to adjust the CCW flow to assure

that the CCW system will supply sufficient flow to vital equipment without exceeding the

CCW design temperature limitations during the worst-case accident conditions. The

inspectors noted that the test was conducted with CCW flow to Vital Headers A and B.

The flow is balanced using the CFCU CCW throttling valve. Flow to each CFCU is

adjusted to establish a flow rate between the minimum and maximum flow limitations.

Based on the known hydraulics of the CCW system, when the CCW flow to each CFCU

is throttled to within the desired range, the overall header will be appropriately balanced.

The inspectors noted that, during the test, CCW flow to the RHR heat exchangers was

secured.

The inspectors reviewed Action Request (AR) A0588366, initiated on August 3, 2003,

which was written to develop a heat exchanger program to test and monitor heat

exchangers. Based on engineering judgement, PG&E decided that preventive

maintenance on the RHR heat exchangers could not be justified based on ALARA

concerns and dose considerations. The inspectors noted that performance monitoring

and trending were recommended to ensure that heat exchangers do not fail to perform

their safety function. However, the RHR heat exchangers were not recommended for

monitoring and trending. The inspectors found that the RHR heat exchangers were not

tested, not inspected and cleaned, and not monitored and trended. The inspectors

determined that PG&E had not demonstrated that the RHR heat exchangers would

meet their safety function.

PG&E stated that they would send additional material for the inspectors to review in

order to demonstrate that the RHR heat exchangers would perform their safety function.

Analysis: At the time of writing, PG&E had not demonstrated that the RHR heat

exchangers would meet their safety function. This issue is potentially more than minor

because it could affect the Mitigating Systems Cornerstone objective by causing the

safety-related RHR system to not transfer sufficient heat to the CCW system to support

the safety-related systems.

Enforcement: 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in

part, that design control measures shall provide for verifying or checking the adequacy

of the design, such as by the performance of design reviews, by the use of alternative or

simplified calculation methods, or by performance of a suitable testing program.

Additional review by NRC is needed to determine if the RHR heat exchangers would

meet their design safety function. Therefore, this item will be treated as a URI pending

additional review: URI 50-275; 323/06-05-01, Additional Review of Material to

Determine if the RHR Heat Exchangers Will Meet Their Safety Function.

-9- Enclosure

.3 Identification and Resolution of Problems

a. Inspection Scope

The inspectors verified that PG&E had entered significant heat exchanger/heat sink

performance problems into the corrective action program (CAP). The inspectors

reviewed 17 ARs.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11)

a. Inspection Scope

On November 28, 2006, the inspectors observed testing and training of senior reactor

operators and reactor operators to identify deficiencies and discrepancies in the training,

to assess operator performance, and to assess the evaluators critique. The training

scenario involved a volume control tank rupture, an auxiliary saltwater pump trip, an

earthquake, and an anticipated transient without scram. Documents reviewed by the

inspectors included:

  • Lesson FRS1-B, ATWS, Revision 10

Revision 34

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

.1 Routine Maintenance Effectiveness Inspection

a. Inspection Scope

The inspectors reviewed the one below listed maintenance activity to: (1) verify the

appropriate handling of structure, system, and component (SSC) performance or

condition problems; (2) verify the appropriate handling of degraded SSC functional

performance; (3) evaluate the role of work practices and common cause problems; and

(4) evaluate the handling of SSC issues reviewed under the requirements of the

Maintenance Rule, 10 CFR Part 50, Appendix B, and the Technical Specifications (TS).

-10- Enclosure

Valves FW-1-LCV-113/115

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Risk Assessments and Management of Risk

a. Inspection Scope

The inspectors reviewed the three below listed assessment activities to verify:

(1) performance of risk assessments when required by 10 CFR 50.65(a)(4) and PG&E

procedures prior to changes in plant configuration for maintenance activities and plant

operations; (2) the accuracy, adequacy, and completeness of the information

considered in the risk assessment; (3) that PG&E recognizes, and/or enters as

applicable, the appropriate risk category according to the risk assessment results and

PG&E procedures; and (4) PG&E identified and corrected problems related to

maintenance risk assessments.

  • October 4, 2006, Unit 1, Preventive maintenance on Auxiliary Saltwater Cross-tie

Valve SW-0-FCV-601, RCP undervoltage/under-frequency relay testing, and

Morro Bay - Diablo Canyon 230 kV line outage

  • October 9, 2006, Unit 2, Planned maintenance outage of condensate booster

pump

  • November 17, 2006, Unit 1, Installation of cell jumper on Vital Battery 1-1

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed three samples.

b. Findings

No findings of significance were identified.

-11- Enclosure

.2 Emergent Work

a. Inspection Scope

The inspectors: (1) verified that PG&E performed actions to minimize the probability of

initiating events and maintained the functional capability of mitigating systems and

barrier integrity systems; (2) verified that emergent work-related activities, such as

troubleshooting, work planning/scheduling, establishing plant conditions, aligning

equipment, tagging, temporary modifications, and equipment restoration did not place

the plant in an unacceptable configuration; and (3) reviewed the FSAR Update to

determine if PG&E identified and corrected risk assessment and emergent work control

problems.

  • September 26, 2006, Unit 1, Emergent failure of POV-1 ventilation logic cabinet
  • October 9, 2006, Unit 1, Emergent failure of a reactor protection channel
  • November 3, 2006, Units 1 and 2, 230 kV disconnect switch warm termination
  • November 22, 2006, Units 1 and 2, Hydrochloric acid developed by auxiliary

saltwater piping cathodic protection

  • December 18, 2006, Unit 2, Indication of nuclear fuel leak

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed five samples.

b. Findings

Introduction: A Green NRC-identified, noncited violation (NCV) of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Actions, was determined for the failure of

engineering and operations personnel to promptly identify and correct a condition

adverse to quality. On two occasions regarding poor circuit card connections in the

auxiliary building ventilation control panel, operations and engineering personnel:

(1) failed to address operability when using manual actions in place of automatic actions

and (2) failed to fully address the impact of debris between circuit card and panel

connections.

Description: On September 27, 2006, the Unit 1 Auxiliary Building Ventilation System

Train B control panel (POV-2) was de-energized for planned maintenance. Shortly

thereafter, the Train A control panel (POV-1) ac power controller tripped. At the time,

both cabinets were declared inoperable and TS 3.0.3 was entered. Control Panel

POV-2 panel was returned to service and operators moved from TS 3.0.3 to TS 3.7.12

for having one train of the auxiliary building ventilation system inoperable. To facilitate

troubleshooting and repairs, on September 29, maintenance personnel de-energized

both Panels POV-1 and POV-2. De-energizing the control panels placed the system

dampers in their safety-related position. Additionally, operators manually started one

-12- Enclosure

auxiliary building exhaust fan and planned to manually start the other exhaust fan if

needed during a design basis event. The controls for the auxiliary building exhaust fans

were located in the cable spreading room. Operators subsequently declared both trains

of the ventilation system operable and exited TS 3.7.12.

The inspectors questioned the decision to declare the train with the standby exhaust fan

fully operable by taking credit for manual actions to start the fan during a design basis

event. The attachment to Regulatory Information Summary 2005-20, Part 9900

Technical Guidance Operability Determinations & Functionality Assessments for

Resolution of Degraded or Nonconforming Conditions Adverse to Quality of Safety,

Section C.5, states that substitution of manual actions for automatic actions requires an

operability determination. However, an operability determination was not performed. In

response to NRC questioning, operators declared Control Panel POV-1 inoperable and

re-entered TS 3.7.12. The inspectors observed that operators would have been able to

start the standby exhaust fan had it been necessary; therefore, they would have been

able to produce an operability determination.

Subsequent troubleshooting revealed the cause of the Control Panel POV-1 power

supply to trip was oxidation buildup and dust collection on the terminals. An interlock

feature on the control panels de-energizes the panel if a circuit card becomes loose.

Control Panel POV-2 was also inspected and several loose cards were found and

cleaned. The extent of condition review by engineering personnel concluded that the

Unit 2 control panels were not affected due to the interlock feature being disabled.

Unit 2 Control Panel POV-1 was inspected on November 9, 2006, during a scheduled

card replacement. Nine cards were found to have loose connections, and these cards

were cleaned and reinstalled. Unit 2 Control Panel POV-2 was scheduled for inspection

in April 2007.

The inspectors concluded that engineering personnel had failed to adequately address

operability of the Units 1 and 2 auxiliary building ventilation system control panels.

Engineering and maintenance staff were aware that debris was being blown onto the

control panel circuit cards by the panels ventilation fans. The debris would work its way

between the circuit card and panel connection points and cause the poor connections.

During a design basis event, particularly a seismic event, the connections may not

provide an adequate circuit path. While engineering staff discussed the fact that the

interlock feature would not de-energize the control panels if a loose card were detected,

their assessment did not discuss the affect of the debris on other connection points and

what the impact that would have on the auxiliary building ventilation system. The

inspectors did observe that any loose connection would still provide an alarm to the

control room operators and failure of the control panels would move the dampers to their

safety-related position. Additionally, operators would be able to manually control the

exhaust fans. Therefore, engineering staff had a basis for determining that the control

panels were degraded but operable, but failed to provide this basis in a timely manner.

Analysis: The performance deficiency associated with this finding involved two

examples where PG&E personnel failed to perform an adequate operability

determination. The finding is greater than minor because it is associated with the

Barrier Integrity Cornerstone attribute of SSC and barrier performance and affects the

-13- Enclosure

associated cornerstone objective to provide reasonable assurance that physical design

barriers protect the public from radionuclide releases caused by accidents or events.

Using the Inspection Manual Chapter 0609, "Significance Determination Process,"

Phase 1 Worksheet, the finding is determined to have very low safety significance

because the finding only represents a degradation of the radiological barrier function

provided for the auxiliary building. This finding has a crosscutting aspect in the area of

problem identification and resolution associated with the CAP because operations and

engineering personnel did not adequately evaluate operability of the auxiliary building

ventilation system regarding use of manual actions and the full impact of debris on

circuit card connections.

Enforcement: 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires,

in part, that measures be established to assure that conditions adverse to quality are

promptly identified and corrected. Contrary to this, on two occasions between

September 29 and November 9, 2006, PG&E staff failed to promptly identify and correct

a condition adverse to quality when they failed to adequately evaluate operability of the

auxiliary building ventilation system. In the first example, operations personnel credited

manual actions in place of automatic safety actions without evaluating the capability of

those actions in an operability determination. In the second example, engineering

personnel failed to fully address the effect of debris between circuit card connections

and their impact on system operability. Because the finding is of very low safety

significance and has been entered into the CAP as AR A0678429, this violation is being

treated as an NCV consistent with Section VI.A of the Enforcement Policy:

NCV 50-275; 323/06-05-02, Failure to Adequately Evaluate Operability of Auxiliary

Building Ventilation Control Panels.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors: (1) reviewed plant status documents such as operator shift logs,

emergent work documentation, deferred modifications, and standing orders to

determine if an operability evaluation was warranted for degraded components;

(2) referred to the FSAR Update and design bases documents to review the technical

adequacy of the operability evaluations; (3) evaluated compensatory measures

associated with operability evaluations; (4) determined degraded component impact on

any TS; (6) used the Significance Determination Process to evaluate the risk

significance of degraded or inoperable equipment; and (5) verified that PG&E has

identified and implemented appropriate corrective actions associated with degraded

components.

  • October 17, 2006, Unit 2, Valves FW-2-LCV-111 and FW-2-LCV-115 placed in

manual due to 10 CFR Part 21 Notice

  • October 30, 2006, Unit 1, Diesel Engine Generator 1-3 slow to reach rated

speed during surveillance test

  • November 13, 2006, Unit 1, Vital Battery 1-1 Cell 15 low voltage

-14- Enclosure

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed three samples.

b. Findings

Introduction: An NRC-identified, NCV of 10 CFR Part 50, Appendix B, Criterion XVI,

Corrective Actions, was identified for the failure to promptly correct a condition adverse

to quality. Specifically, on October 15, 2006, PG&E implemented a temporary

modification to Vital Battery 1-1, contrary to American National Standards

Institute/Institute of Electrical and Electronics Engineers (ANSI/IEEE) Standard

450-1987, "IEEE Recommended Practice for Maintenance, Testing, and Replacement

of Large Lead Storage Batteries for Generating Stations and Substations. Additionally,

surveillance tests to monitor the condition of the degraded battery cell were adversely

affected by the installed temporary modification.

Description: The vital batteries are required to provide adequate power to loads

necessary for plant cooldown during a station blackout. The battery system consists of

three, 60-cell, 125 V battery banks with five battery chargers. Two chargers are capable

of charging Battery 1-1. However, in the event of a loss of vital 480 V Bus 1F, Battery

Charger 121 could be manually aligned to restore power to direct current (dc) loads

associated with Battery 1-1. In the event of a loss of vital 480 V Bus 1F, Battery 1-1

supplies the following risk significant loads: Diesel Engine Generator 1-2 engine panel

emergency source, solid-state protection system Train A; main steam isolation valves

and 10 percent steam dump circuitry, vital 120 V Inverter IY 1-1, and Diesel Engine

Generator 1-3 normal gage panel power. Calculation 235A-DC, Battery 11 Sizing,

Load Flow, Voltage Drop, Short Circuit and Charger Sizing, Revision 8, determined the

minimum number of cells for each operable bank to be 59 cells.

On October 3, 2006, Battery 1-1, Cell 15 indicated a low voltage of 2.093 V during the

performance of Surveillance Test Procedure STP M-11A, "Station Battery and Pilot Cell

Condition Monitoring," Revision 19. The TS 3.8.4 limit for cell voltage is 2.07 V. The

battery was subsequently placed on equalizing charge in an attempt to restore voltage.

This attempt was not successful and an individual cell equalizing charge was

commenced on October 11. On October 15, maintenance personnel installed an

individual cell charger on Cell 15 as a temporary modification. The charger was

adjusted to a float voltage charge of 2.25 V as a compensatory measure to ensure

battery operability.

On October 16, the inspectors engaged PG&E staff regarding the operability of

Battery 1-1, while an individual cell charger was installed to maintain Cell 15 at the

battery average voltage. In the event of a station blackout, the degraded cell could

adversely impact Battery 1-1 by becoming an additional load on the battery (i.e., reverse

polarizing). Engineering staff assumed that, during a battery discharge, Cell 15 voltage

would drop at the same rate as the other battery cells. Therefore, if the individual cell

charger maintained Cell 15 voltage at the same voltage level as the overall battery, the

cell would not become an additional load during battery discharge. However, the

-15- Enclosure

inspectors observed that engineering staff did not have analysis, test data, or other

information to support the assumption. In discussions with the battery vendor (C&D

Power Systems), engineering staff determined that it is not known at what point or how

much, if any, that having a degraded cell would affect battery performance. According

to ANSI/IEEE Standard 450-1987, "IEEE Recommended Practice for Maintenance,

Testing, and Replacement of Large Lead Storage Batteries for Generating Stations and

Substations," there are specified methods to correct battery cell deficiencies. This

industry standard stated that, if a cell is not recoverable through equalizing charges, it

should be removed from service. The inspectors noted that the staff had not provided

sufficient tests, analyses, or other evidence that supported the installation of a cell

charger for battery operability.

On November 17, Cell 15 was isolated electrically from Battery 1-1 by installing jumper

cables. This action restored Battery 1-1 to an analyzed, operable condition of 59 fully

functional cells. PG&E waited approximately 33 days to install the jumper cables since

they were waiting for a response on a license amendment request to extend the current

TS 3.8.4 allowed outage time from 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> to 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. On November 15, PG&E

received a one-time license amendment to extend the allowed outage time to 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

The evolution on November 17 took approximately 74 minutes, which was within the

original allowed outage time of 120 minutes. The inspectors also noted that prior mock-

ups of the jumper installation demonstrated that the evolution could be completed in less

than the TS allowed outage time.

Analysis: The performance deficiency associated with this finding involved the failure of

engineering personnel to properly implement measures to correct a condition adverse to

quality. The finding is greater than minor because it is associated with the Mitigating

Systems Cornerstone attribute of equipment performance and affects the associated

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences. Using the Manual

Chapter 0609, Significance Determination Process, Phase 1 worksheets, the

inspectors determined that this finding is of very low safety significance because it did

not represent an actual loss of safety function of a single train for greater than its TS

allowed outage time. This finding has a crosscutting aspect in the area of problem

identification and resolution associated with the CAP in that engineering staff did not

thoroughly assess the operability of the battery and correct a condition adverse to

quality in a timely manner.

Enforcement: 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that

measures be established to assure that significant conditions adverse to quality, such as

deficiencies, defective material and equipment, and nonconformances, are promptly

identified and corrected. Contrary to this requirement, from October 15 to

November 17, 2006, PG&E implemented a temporary modification that had not been

adequately analyzed for its effect on battery operability and was contrary to committed

industry standards. As a result, PG&E failed to correct a condition adverse to quality in

a timely manner. This finding is of very low safety significance and has been entered

into the CAP as AR A0678820. This violation is being treated as an NCV, consistent

with Section VI.A of the NRC Enforcement Policy: NCV 50-275/06-05-03, Inadequate

Temporary Modification to a Vital Battery.

-16- Enclosure

1R17 Permanent Plant Modifications (71111.17)

a. Inspection Scope

The inspectors reviewed key affected parameters associated with energy needs,

materials/replacement components, timing, heat removal, control signals, equipment

protection from hazards, operations, flowpaths, pressure boundary, ventilation

boundary, structural, process medium properties, licensing basis, and failure modes for

the one modification listed below. The inspectors verified that: (1) modification

preparation, staging, and implementation did not impair emergency/abnormal operating

procedure actions, key safety functions, or operator response to loss of key safety

functions; (2) postmodification testing maintained the plant in a safe configuration during

testing by verifying that unintended system interactions will not occur, SSC performance

characteristics still meet the design basis, the appropriateness of modification design

assumptions, and the modification test acceptance criteria has been met; and (3) PG&E

has identified and implemented appropriate corrective actions associated with

permanent plant modifications.

  • September 29, 2006, Unit 1, Modification of Excess Letdown Heat Exchanger

Outlet Valve Controller HCV-123 with a 60-ohm resistor

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors selected the four below listed postmaintenance test activities of risk-

significant systems or components. For each item, the inspectors: (1) reviewed the

applicable licensing basis and/or design basis documents to determine the safety

functions; (2) evaluated the safety functions that may have been affected by the

maintenance activity; and (3) reviewed the test procedure to ensure it adequately tested

the safety function that may have been affected. The inspectors either witnessed or

reviewed test data to verify that acceptance criteria were met, plant impacts were

evaluated, test equipment was calibrated, procedures were followed, jumpers were

properly controlled, the test data results were complete and accurate, the test

equipment was removed, the system was properly realigned, and deficiencies during

testing were documented. The inspectors also reviewed the FSAR Update to determine

if PG&E identified and corrected problems related to postmaintenance testing.

  • September 26, 2006, Unit 1, Excess letdown Heat Exchanger Valve HCV-123
  • October 3, 2006, Unit 1, Auxiliary Building Ventilation System, POV-1/POV-2

-17- Enclosure

  • October 4, 2006, Unit 1, Auxiliary Saltwater Unit Cross-tie Valve SW-0-FCV-601
  • November 1, 2006, Unit 1, Safety Injection Pump 1-1

Documents reviewed by the inspectors included:

  • Procedure LT 8-82, CVCS Excess Letdown Heat Exchanger Outlet HCV-123

Calibration, Revision 1

  • Procedure STP V-3F3, Exercising Valve FCV-601, Units 1 and 2 ASW

Cross-tie, Revision 16

  • Procedure PEP 23-01, Aux Building and Fuel Handling Building Ventilation

Systems Fan Failure Tests and Miscellaneous POV Tests, Revision 8

  • Procedure STP P-SIP-11, Routine Surveillance Test of Safety Injection

Pump 1-1, Revision 19

The inspectors completed four samples.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the FSAR Update, procedure requirements, and TS to ensure

that the two below listed surveillance activities demonstrated that the SSCs tested were

capable of performing their intended safety functions. The inspectors either witnessed

or reviewed test data to verify that the following significant surveillance test attributes

were adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;

(3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumpers; (7) test data;

(8) testing frequency and method demonstrated TS operability; (9) test equipment

removal; (10) restoration of plant systems; (11) fulfillment of American Society of

Mechanical Engineers Code requirements; (12) updating of performance indicator data;

(13) accuracy of engineering evaluations, root causes, and bases for returning tested

SSCs not meeting the test acceptance criteria; (14) reference setting data; and

(15) annunciators and alarm setpoints. The inspectors also verified that PG&E identified

and implemented any needed corrective actions associated with the surveillance testing.

  • November 1, 2006, Unit 1, Eagle-21 partial trip board activation test

Control Valve FW-2-LCV-113

Documents reviewed by the inspectors included:

-18- Enclosure

  • Procedure STP- I-36-S1EPT, Protection Set 1 Eagle-21 Partial Trip Board

Activation Test, Revision 12

  • Procedure STP V-3P6B, Exercising Valves LCV-115 and 113 Auxiliary

Feedwater Pump Discharge, Revision 13

The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors reviewed the FSAR Update, plant drawings, procedure requirements,

and TS to ensure that the one below listed temporary modification was properly

implemented. The inspectors: (1) verified that the modifications did not have an affect

on system operability/availability; (2) verified that the installation was consistent with

modification documents; (3) ensured that postinstallation test results were satisfactory

and that the impact of the temporary modifications on permanently installed SSCs were

supported by the test; (4) verified that the modifications were identified on control room

drawings and that appropriate identification tags were placed on the affected drawings;

and (5) verified that appropriate safety evaluations were completed. The inspectors

verified that PG&E identified and implemented any needed corrective actions associated

with temporary modifications.

  • November 16, 2006, Unit 1, Installation of jumper in Vital Battery 1-1

Documents reviewed by the inspectors included:

  • Work Order C0207140

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

-19- Enclosure

1EP1 Exercise Evaluation (71114.01)

Cornerstone: Emergency Preparedness

a. Inspection Scope

The inspectors reviewed the objectives and scenario for the 2006 biennial emergency

plan exercise to determine if the exercise would acceptably test major elements of the

emergency plan. The scenario simulated a large condenser tube leak, with a

subsequent failure of the reactor protection system to complete a reactor scram.

Multiple main steam isolation valve failures then resulted in initiation of a small release

of radioactivity to the environment. An initially small reactor coolant leak in containment

greatly increased, ultimately resulting in a loss of reactor vessel level, core uncovering

and damage of reactor fuel, with a rapid increase in the offsite release of radioactivity to

the environment.

The inspectors evaluated exercise performance by focusing on the risk-significant

activities of event classification, offsite notification, recognition of offsite dose

consequences, and development of protective action recommendations, in the simulator

control room and the following dedicated emergency response facilities:

  • Operations Support Center
  • Emergency Operations Facility

The inspectors also assessed recognition of and response to abnormal and emergency

plant conditions, the transfer of decision making authority and emergency function

responsibilities between facilities, onsite and offsite communications, protection of

emergency workers, emergency repair evaluation and capability, and the overall

implementation of the emergency plan to protect public health and safety and the

environment. The inspectors reviewed the current revision of the facility emergency

plan, and emergency plan implementing procedures associated with operation of the

above facilities and performance of the associated emergency functions. These

procedures are listed in the Attachment to this report.

The inspectors compared the observed exercise performance to the requirements in the

facility emergency plan, 10 CFR 50.47(b), 10 CFR Part 50, Appendix E, and to the

guidance in the emergency plan implementing procedures and other federal guidance.

The inspectors attended the post-exercise critiques in each of the above facilities to

evaluate the initial licensee self-assessment of exercise performance. The inspectors

also attended a subsequent formal presentation of critique items to plant management.

The inspectors completed one sample during this inspection.

b. Findings

No findings of significance were identified.

-20- Enclosure

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

a. Inspection Scope

The inspectors reviewed licensee evaluations for the three emergency preparedness

cornerstone performance indicators of Drill and Exercise Performance, Emergency

Response Organization Participation, and Alert and Notification System Reliability, for

the period October 1, 2005, through September 30, 2006. The definitions and guidance

of NEI 99-02, "Regulatory Assessment Indicator Guideline," Revisions 3 and 4, and the

licensee Emergency Plan Instruction 18, "Emergency Preparedness NRC Performance

Indicators," 6/15/2006, were used to verify the accuracy of the licensees evaluations for

each performance indicator reported during the assessment period.

The inspectors reviewed a sample of drill and exercise scenarios and licensed operator

simulator training sessions, notification forms, and attendance and critique records

associated with training sessions, drills, and exercises conducted during the verification

period. The inspectors reviewed selected emergency responder qualification, training,

and drill participation records. The inspectors reviewed alert and notification system

testing procedures, maintenance records, and a 100 percent sample of siren test

records. The inspectors also reviewed other documents listed in the Attachment to this

report.

The inspectors completed three samples during the inspection.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a daily screening of items entered into PG&Es CAP. This

assessment was accomplished by reviewing ARs and event trend reports and attending

daily operational meetings. The inspectors: (1) verified that equipment, human

performance, and program issues were being identified by PG&E at an appropriate

threshold and that the issues were entered into the CAP; (2) verified that corrective

actions were commensurate with the significance of the issue; and (3) identified

conditions that might warrant additional follow-up through other baseline inspection

procedures.

b. Findings

No findings of significance were identified.

-21- Enclosure

.2 Selected Issue Follow-Up Inspection

a. Inspection Scope

In addition to the routine review, the inspectors selected the one below listed issue for a

more in-depth review. The inspectors considered the following during the review of

PG&Es actions: (1) complete and accurate identification of the problem in a timely

manner; (2) evaluation and disposition of operability/reportability issues;

(3) consideration of extent of condition, generic implications, common cause, and

previous occurrences; (4) classification and prioritization of the resolution of the

problem; (5) identification of root and contributing causes of the problem;

(6) identification of corrective actions; and (7) completion of corrective actions in a timely

manner.

  • November 22, 2006, Units 1 and 2, Auxiliary Saltwater (ASW) Pump Shaft

Packing

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one sample.

b. Findings

Introduction: The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, for the failure of engineering personnel to apply adequate

design control measures. Specifically, engineering personnel changed the acceptance

criteria in the ASW pump surveillance test from greater than zero packing leak-off to

zero packing leak-off, with packing gland temperature less than 120EF. However, the

change was based on engineering judgment versus analysis or test data. If the

engineering judgment were incorrect, operability of the ASW pump could be impacted

and the pump may be unable to perform its safety function due to potential shaft

damage.

Description: The ASW systems safety function is to remove heat from the component

cooling water heat exchangers using the ultimate heat sink (Pacific Ocean). The system

consists of two pumps that take suction from the ocean and supply water to one or both

heat exchangers. The ASW pumps utilize packing to limit the amount of water escaping

the pump/shaft interface. The type of packing utilized in the ASW pumps is a Garlock

Type 1304 graphite-based packing. The stuffing box for the ASW pumps utilizes a

packing injection line, where the injection flow enters the box between an upper packing

and a lower packing. A portion of the injection flow travels upward, between the pump

shaft and the upper packing, and exits as visible packing leak-off at the top of the

packing gland. The rest of the injection flow travels downward, between the pump shaft

and the lower packing, and exits into the pump (i.e., nonvisible packing leak-off).

Operators observe evidence of visible packing leak-off on a daily basis to ensure that

there is adequate cooling for the packing. Inadequate cooling to the packing may result

in pump shaft seizure or damage to the packing gland and/or pump shaft. For more

-22- Enclosure

than 5 years, the ASW pump packing has been susceptible to sand and silt

accumulation from ocean water, resulting in zero packing leak-off. When operations

personnel found zero packing leak-off, the pump was declared inoperable and the pump

was repacked. In all cases where zero packing leak-off was observed, the pump had

just started versus when it had been running for some time.

Engineering personnel believed the ASW pumps were still operable without packing

leak-off since the packing gland was cool to touch in such cases. Therefore, on

February 9, 2006, engineering personnel developed a corrective action in AR A0657460

to modify the acceptance criteria in the ASW routine surveillance test procedures to

allow zero packing leak-off as long as the packing gland temperature is less than 120EF.

For example, the following procedures stated under Section 6, Acceptance Criteria,

that pump packing leakage is greater than zero drops per minute, or stuffing box

temperature is less than 120EF.

  • STP P-ASW-11, Routine Surveillance Test of Auxiliary Saltwater Pump 1-1,

Revision 23

  • STP P-ASW-12, Routine Surveillance Test of Auxiliary Saltwater Pump 1-2,

Revision 20

  • STP P-ASW-21, Routine Surveillance Test of Auxiliary Saltwater Pump 2-1,

Revision 22

  • STP P-ASW-22, Routine Surveillance Test of Auxiliary Saltwater Pump 2-2,

Revision 18

Prior revisions of these procedures required packing leakage to be greater than zero to

pass the surveillance test and for the pump to be considered operable.

The inspectors reviewed AR A0657460 and the bases for the procedure change. The

inspectors observed that licensee personnel based the change on engineering

judgment, since there was no industry or vendor-specific criteria for an allowable stuffing

box temperature. The inspectors also observed that Vendor Document 663030,

Sheet 17, Bingham Centrifugal Pumps - Instructions for Installation, Operation, and

Maintenance, Revision 18, stated that a slight amount of leakage was needed to

provide lubrication between the packing and the rotating element. If the leakage was

cut off too much, the heat generated by the friction between the packing and the rotating

element would destroy the packing and damage the rotating element. Engineering

personnel felt that, with the stuffing box temperature less than 120EF, neither the shaft

or packing would degrade and fail. The inspectors were concerned that there was no

data or experience to show that the packing would remain at a constant temperature

over time, particularly when the packing was full of sand and silt. Furthermore, the

procedure change did not require temperature surveillance of the stuffing box on a

periodic frequency if there was zero packing leak-off. Engineering personnel had

determined that shift walkdowns of the ASW pumps performed twice a day by operators

would be sufficient for monitoring. Again, there was no test data or experience to

demonstrate that the surveillance frequency would be sufficient.

-23- Enclosure

Analysis: The performance deficiency associated with this finding involved engineering

personnel failing to apply design control measures to a routine surveillance test

acceptance criteria that were commensurate with those applied to the original design.

The finding is greater than minor because it is associated with the Mitigating Systems

Cornerstone attribute of procedure quality and affects the associated cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Using the Manual Chapter 0609,

Significance Determination Process, Phase 1 Worksheet, the finding is determined to

be of very low safety significance, because it did not represent an actual loss of system

safety function, did not represent an actual loss of a single train for greater than its TS

allowed outage time, and the finding did not screen as potentially risk significant due to

a seismic, flooding, or severe weather initiating event. This finding has a crosscutting

aspect in the area of human performance associated with resources because

engineering personnel failed to provide up-to-date design documentation to support a

design change in surveillance test acceptance criteria.

Enforcement: 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in

part, that design control measures shall be applied to items such as acceptance criteria

for inspections and tests. Design changes, including field changes, shall be subject to

design control measures commensurate with those applied to the original design.

Contrary to this, on February 9, 2006, engineering personnel failed to apply design

control measures to a change in the routine surveillance test acceptance criteria that

were commensurate with the original design. Specifically, engineering personnel

modified the ASW pump routine surveillance test procedure acceptance criteria to allow

zero packing leak-off, although original vendor documentation required greater than

zero packing leak-off. Engineering personnel used judgment to justify the design

change rather than vendor information or test results, which would have been

commensurate with the original design. The corrective actions to restore compliance

included obtaining vendor documentation to justify zero packing leak-off from the

pumps. Because the finding is of very low safety significance and has been entered into

PG&Es CAP as AR A0684631, this violation is being treated as an NCV consistent with

Section VI.A of the Enforcement Policy: NCV 50-275; 323/06-05-04, Inadequate

Change to Auxiliary Saltwater Pump Routine Surveillance Test Acceptance Criteria.

.3 Semiannual Trend Review

a. Inspection Scope

The inspectors completed a semiannual trend review of repetitive or closely-related

issues documented in ARs to identify trends that might indicate the existence of more

safety-significant issues. The inspectors review consisted of the 6-month period of

July 1 to December 31, 2006. When warranted, some of the samples expanded beyond

those dates to fully assess the issue. The inspectors also reviewed corrective actions

associated with Emergency Action Level (EAL) Alert 2 and emergency core cooling

system (ECCS) piping voids. The inspectors compared and contrasted their results with

the results contained in PG&Es quarterly trend reports. Corrective actions associated

with a sample of the issues identified in PG&Es trend reports were reviewed for

adequacy. Documents reviewed by the inspectors are listed in the attachment.

-24- Enclosure

b. Findings

.1 EAL Alert 2

Procedure EP G-1, Emergency Classification and Emergency Plan Activation,

Revision 34, EAL Alert 2, describes the identification of fuel damage as shown

by: Confirmed Reactor Coolant System (RCS) sample > 300 µCi/cc of

equivalent I-131 specific activity OR equivalent fuel failure is measured by

exposure rate from systems carrying reactor coolant per EP RB-14A. During

the critique of the emergency drill on September 20, 2006, a concern was raised

regarding the ability to determine the extent of possible fuel damage using

Procedure EP RB-14A, Initial Detection of Core Damage, Revision 0.

AR A0678189 was written to capture this concern.

The inspectors observed that several ARs had been written since 2004

(A0616739, A0670612, A0670613, and A0675097) regarding the ability to

perform the requirements of EAL Alert 2 using Procedure EP RB-14A or through

confirmation of an RCS sample > 300 µCi/cc of equivalent I-131 specific activity.

Concerns included the high dose rates that would occur in the letdown heat

exchanger room, where piping dose rates would be taken, and the lack of

training for radiological protection personnel that would perform the procedure

during an event. Other concerns involved the use of the postaccident sampling

system for obtaining and analyzing RCS samples, since much of that system had

been abandoned in place. Some ARs were still open and others had been

closed without fully addressing the concerns.

PG&E stated that, in an event, Procedure RB-14A would be adequately briefed

and preparations made for taking dose rates. Also, portions of the postaccident

sampling system were maintained operable for taking RCS samples. However, it

was not until the NRC began to research the issue that PG&E adequately

addressed the concerns.

.2 ECCS Piping Voids

The inspectors reviewed Diablo Canyon Power Plant performance with respect

to ECCS piping voids. Within the past 6 years, both units exhibited voids at

ECCS suction piping that could adversely impact the ability of ECCS pumps to

perform their safety function. A notable area of ECCS voids was the cross-over

suction piping from the RHR system to the safety injection system. PG&E

believed that the voiding was caused by hydrogen gas coming out of solution at

the RCP seal injection system and migrating to this section of pipe. To eliminate

concerns of ECCS pipe voids at this location, PG&E installed an approximate

40 gallon void chamber (i.e., tank) to that section of pipe for both units. Gas

accumulating in that section of the pipe now travels up piping to the void

chamber. During monthly ECCS void surveillances, operators vent the void

chamber. Per design, the gas coming out of solution is removed from the piping

-25- Enclosure

and contained in the void chamber where it does not affect the performance of

safety-related pumps. The inspectors reviewed the performance of the void

chambers and found them to operate as designed, without any adverse impacts

to the plant.

The inspectors reviewed other operating experience at Diablo Canyon Power

Plant that may point to potential ECCS void concerns. The inspectors observed

that a section of RHR discharge piping in both units have experienced voiding in

the past. This section of discharge piping, Line 509, is located inside

containment, but outside the bioshield. In April 2001, AR A0528837 documented

the presence of a large void in Line 509 for Unit 1. The voiding was caused by

leakage of nitrogen-saturated water from Accumulator 1-3 into the RHR

discharge piping. Prior to this determination, operators noticed an increase in

RHR discharge pressure by a factor of four and a declining level in

Accumulator 1-3. To prevent the voiding from impacting operability of the RHR

system at that time, PG&E maintained high pressure on the RHR discharge

piping. Later, PG&E was able to correct the accumulator leakage and eliminate

the void. In May 2006, while performing an extent of condition review for a water

hammer that occurred on Accumulator 2-3 discharge piping, engineering

personnel discovered small void pockets in Unit 1 Line 509. As documented in

AR A0669488, the volume of the void was approximately 3 percent of the pipe

area, which was less than the 20 percent limit as described in

Calculation STA-108, ECCS Pump Suction Void Evaluation, Revision 0. PG&E

continued to monitor Line 509 for the next 6 months on Units 1 and 2 and were

able to vent at a maximum of 1/2 cup of gas during that time period for both units.

The inspectors reviewed PG&Es actions in regard to the voiding found inside

containment, including their monitoring efforts. The inspectors found that in both

cases the voids would not be a water hammer concern or impede core cooling

following a safety injection. The inspectors also found that PG&Es monitoring

efforts were consistent with industry practices. Specifically, PG&E would verify

the piping inside containment was full before restarting the reactor following a

refueling outage. Additionally, PG&E monitored RCS leakage and accumulator

levels and pressures to identify the potential for nitrogen or hydrogen gas coming

out of solution in ECCS piping.

4OA3 Event Followup (71153)

.1 Unit 2 Reactor Shutdown Due to Indicated High Stator Temperature for RCP 2-2

a. Inspection Scope

On December 10, 2006, operators received alarms for Unit 2 RCP 2-2 high stator

temperature. Using Procedures AR PK05-02, RCP No. 22, Revision 20, and

OP AP-28, Reactor Coolant Pump Malfunction, Revision 2, operators responded to the

alarm condition. Both procedures required a reactor trip if the RCP stator temperature

exceeded 300EF. Operators determined that a reactor shutdown was necessary as

indicated stator temperature was 249EF and increasing. Operators manually tripped the

-26- Enclosure

reactor when indicated stator temperature was 300EF. Just prior to the reactor trip, the

reactor was subcritical with keff less than 0.99; however, operators had not been able to

fully insert control rods as part of the reactor shutdown. Upon the manual reactor trip,

all control rods inserted. PG&E investigated the cause of the high stator temperature

alarm and identified a failed resistance temperature detector. An installed spare

resistance temperature detector in the RCP 2-2 stator was selected and operators

began actions to restart Unit 2 on December 11.

The inspectors responded at the time of the event and: (1) observed plant parameters

and status, (2) evaluated performance of mitigating systems and operators,

(3) confirmed that PG&E properly classified the event in accordance with EAL

procedures and made timely notifications to the NRC and state/local governments, and

(4) communicated the details of the events and conditions to NRC management as input

to determining the need for additional inspection effort.

b. Findings

No findings of significance were identified.

.2 Unit 2 Reactor Trip Due to Electrical Fault Associated With CWP 2-1

a. Inspection Scope

On December 12, 2006, an electrical fault occurred in Unit 2 CWP 2-1. The apparent

cause of the fault was the failure of an oil-filled surge capacitor located at the motor

terminal leads. As a result of the electrical fault, voltage on 12 kV nonvital Bus D

dropped to approximately 6.5 kV for less than a second. This bus supplies CWP 2-1, as

well as RCPs 2-2 and 2-4. Relay devices on Bus D sensed the degraded voltage and

opened the breakers for RCPs 2-2 and 2-4 per design. With two RCP breakers open,

the coincidence logic in the reactor protection system was met for a reactor trip.

Subsequently, the Unit 2 reactor tripped from 25 percent power.

The inspectors responded at the time of the event and: (1) observed plant parameters

and status, (2) evaluated performance of mitigating systems and operators,

(3) confirmed that PG&E properly classified the event in accordance with EAL

procedures and made timely notifications to the NRC and state/local governments, and

(4) communicated the details of the events and conditions to NRC management as input

to determining the need for additional inspection effort.

b. Findings

No findings of significance were identified.

-27- Enclosure

4OA5 Other

.1 Onsite Fabrication of Components and Construction of an Independent Spent Fuel

Storage Installation (ISFSI) (60853)

a. Inspection Scope

The inspectors witnessed portions of the ongoing ISFSI construction activities and

evaluated PG&Es performance in accordance with the criteria contained in Inspection

Procedure 60853. PG&E continued concrete placement activities for the cask transfer

facility (CTF) and the second ISFSI pad. Concrete was placed for the CTF on

August 9, 2006, and for the Transporter Seismic Anchors (TSAs) on

September 7, 2006. Concrete placement activities were completed for the second

ISFSI pad on August 23, 2006. The inspectors witnessed portions of the concrete

placement and testing activities for the CTF, TSAs, and the second ISFSI pad.

Grouted anchors were installed as part of the TSA design on October 31, 2006, to

securely anchor the transporter during a seismic event. The grouted anchors were

tensioned on November 6, 2006. The inspectors witnessed portions of the anchor

installation, grouting, and tensioning.

b. Findings

No findings of significance were identified.

.2 Temporary Instruction 2515/169, Mitigating Systems Performance Index

Verification (MSPI)

a. Inspection Scope

The inspectors verified that PG&E correctly implemented the Mitigating Systems

Performance Index (MSPI) guidance for reporting unavailability and unreliability of the

monitored safety systems. Monitored safety systems included emergency diesel

generators, RHR pumps, secondary heat removal pumps, cooling water pumps, and

high head safety injection pumps. During the inspection, the inspectors assessed the

following:

  • Accurate documentation of the baseline planned unavailability hours for the

MSPI systems

  • Accurate documentation of the actual unavailability hours for the MSPI systems
  • Accurate documentation of the actual unreliability information for each MSPI

monitored component

  • Significant errors in the reported data, which resulted in a change of the

indicated index color

-28- Enclosure

  • Significant errors in the basis document which resulted in: (1) a change of the

system boundary; (2) an addition of a monitored component; or (3) a change in

the reported index color

This temporary instruction is complete for Units 1 and 2.

b. Findings

No findings of significance were identified.

.3 (Closed) URI 05000275, 323/2006012-01, Oil Found in the Vicinity of RHR Pumps

In response to inspectors identifying the presence of oil in the vicinity of the drain plugs

of the motors for RHR Pumps 1-1, 2-1, and 2-2, PG&E monitored leakage from the

motors during subsequent pump runs and concluded that the RHR pumps would have

remained operable for their mission times. Additionally, PG&E staff evaluated the use of

a shortened cure time on the RHR pump motor oil drain plugs and determined that the

sealing capability of the plugs had not been adversely affected. These evaluations were

reviewed by the inspectors, no findings of significance were identified, and no violations

of NRC requirements were identified. PG&E documented the evaluations for presence

of the oil and the shortened sealant cure time in ARs A0670760 and A0675763. This

URI is closed.

.4 (Closed) URI 07200026/2006-01, Review the concrete compressive strength test results

to confirm that the concrete compressive strength of the CTF basemat and initial ISFSI

pad meet the specified compressive strength of 5,000 psi at 90 days.

During the concrete placement activities for the Diablo Canyon ISFSI, several minor

deviations were identified by the inspectors and those were not considered to be safety

significant as documented in NRC Inspection Report 05000275/2006008;

05000323/2006008; 07200026/2006001. The determination that the deviations were

not safety significant was based on the expectation that the concrete would meet or

exceed the required minimum compressive strength of 5,000 psi at the specified cure

period of 90 days. URI 07200026/2006-01 was opened to track and confirm that the

minimum concrete compressive strength was achieved.

PG&E transmitted the 90-day concrete compressive strength test results for the initial

ISFSI pad and the CTF basemat to the NRC on October 12, 2006. The 90-day concrete

compressive test results varied from a low of 7,420 psi to a high of 9,060 psi. The

arithmetic average of any three consecutive strength tests exceeded the required

minimum concrete compressive strength of 5,000 psi as required by Section 5.6.2.3 of

ACI 349, Code Requirements for Nuclear Safety Related Concrete Structures. There

were no maximum concrete compressive strength limitations associated with the Diablo

Canyon ISFSI. Based on satisfactory concrete compressive strength results for the

initial ISFSI pad and the CTF basemat, URI 07200026/2006-01 is considered closed.

-29- Enclosure

.5 (Closed) URI 05000323/2006004-03, Corrective Actions Regarding RCS Leakage

Through In-core Thimble Tube

a. Inspection Scope

On August 31, 2006, an approximate 1.5 gpm RCS leak occurred in Unit 2. The

location of the leakage was in the movable in-core detector system (MIDS) L-13 thimble

tube. The inspectors responded to the RCS leakage at the time of the event and

observed operator actions to identify, quantify, and mitigate the leakage. As discussed

in NRC Inspection Report 05000275; 323/2006004, the inspectors found that PG&E

staff took appropriate action in response to the leakage.

PG&E initiated Nonconformance Report (NCR) N0002211 to identify the root cause(s)

of the leakage and ensure that appropriate corrective actions were taken. Following the

RCS leakage on August 31, maintenance personnel began activities to repair the MIDS,

which had been damaged by water. On September 6, maintenance personnel noticed

leakage from the Path L-13 manual isolation valve at the threaded connection on the

high pressure side. The leakage was determined to be 4 to 6 drops per minute.

Maintenance personnel initially installed a freeze seal to isolate the leakage, and then

tighten the threaded connection three flats to stop the leakage. PG&E subsequently

continued with repair activities on the MIDS.

URI 05000323/2006004-03 was initiated in NRC Inspection Report 05000275;

323/2006004 in order to: (1) evaluate PG&Es root cause and corrective actions

following the RCS leakage and (2) evaluate PG&Es response to the leak on the

threaded connection on the high pressure side of the Path L-13 manual isolation valve.

The inspectors have completed the necessary actions to evaluate these two aspects.

Therefore, URI 05000323/2006004-03 is closed.

b. Findings

1. Failure to Preserve Corrective Action for Thimble Tube Wear

Introduction: A self-revealing, Green NCV of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, was identified for the failure to apply adequate

design control measures regarding the installment of thimble tubes with chrome-

plated bands. Specifically, PG&E installed thimble tubes with chrome-plated

bands at the fuel assembly bottom nozzle/lower core plate interface to address

flow-induced vibration wear. Due to engineering personnels failure to account

for the chrome-plated bands in the thimble tube relocation procedure, the

chrome-plated band on Thimble Tube L-13 was removed from its designed

location at the fuel assembly bottom nozzle, thereby increasing the potential for

thimble tube through-wall wear.

Background: Westinghouse pressurized-water reactors utilize MIDS to monitor

nuclear power distribution within the reactor core. MIDS consists of a detector

that travels inside the thimble tubes, with the thimble tubes inserted into select

fuel assemblies. The thimble tubes are constructed of 316 stainless steel with a

-30- Enclosure

typical outer diameter of 0.3 inches and a wall thickness of 0.049 inches. The

thimble tubes are flexible to allow withdrawal and re-insertion into fuel

assemblies during reactor refueling activities. Inside the reactor vessel, the

thimble tubes are supported by the fuel assembly instrument tube and the lower

reactor internals guide columns. The thimble tubes enter the reactor vessel at

the bottom of the vessel and are supported outside the reactor vessel by

permanently-mounted thimble guide tubes. The permanently-mounted thimble

guide tubes are welded at the bottom of the reactor vessel and stop at the in-

core seal table, where a high pressure seal prevents reactor coolant from

traveling between the thimble tube and thimble guide tube out of the RCS. The

thimble tube connects to a selector device that directs the detector into the

selected thimble tube. Since the thimble tube and thimble guide tube are

subjected to RCS pressure, they are considered an extended portion of the RCS

pressure boundary.

Description: On August 31, 2006, an approximate 1.3 gpm RCS leak occurred in

the Unit 2 MIDS L-13 thimble tube. NCR N0002211 identified a presumed root

cause and developed corrective actions to prevent recurrence. NCR N0002211

stated that the RCS leak was due to accelerated wear/wear-induced fatigue of

the L-13 thimble tube due to flow-induced vibration in combination with multiple

wear scars in a short length of tube, which was not prevented by the thimble tube

wear management program. Until the thimble tube is removed for examination

in the next refueling outage in early 2008, PG&E staff has classified the root

cause as presumed and not definite.

The inspectors reviewed operating experience associated with thimble tubes at

the Diablo Canyon Power Plant and in the nuclear industry. In 1987, NRC

Information Notice 87-44, Thimble Tube Thinning in Westinghouse Reactors,

was issued to discuss thimble tube wall thinning due to flow-induced vibration on

the exposed portion of thimble tubes at the bottom of fuel assemblies and the

lower core plate. In 1988, NRC Bulletin 88-09, Thimble Tube Thinning in

Westinghouse Reactors, requested that licensees establish an inspection

program to detect thimble tube wall thinning. For Unit 1, PG&E responded to

NRC Bulletin 88-09 via PG&E Letter DCL-89-280, dated November 10, 1989. In

the letter, PG&E noted that they found 20 of 58 thimble tubes exceeded the

60 percent through-wall degradation limit, with other tubes experiencing lesser

degrees of damage. PG&E subsequently replaced 28 thimble tubes and

repositioned the wear point on 17 other tubes by pulling up at least 1.5 inches on

the seal table end of the tube and cutting off the excess tube at the high

pressure seal. For Unit 2, PG&E responded in PG&E Letter DCL-90-094, dated

April 4, 1990, with the results of the Unit 2 thimble tube inspection. PG&E found

that 3 tubes, including Thimble Tube L-13, exceeded the acceptable wear limit,

and they were capped for future replacement. In 4 other tubes, PG&E

repositioned the wear points and kept the tubes in service, since the tube wall

degradation did not exceed the acceptable wear limit.

The inspectors found that PG&E continued to inspect the thimble tubes each

refueling outage using eddy current techniques. Thimble Tube L-13 remained

-31- Enclosure

capped and out of service until Refueling Outage 2R10 (May 2001), when it was

replaced. The new thimble tube included a 16-inch long chrome band to protect

the thimble tube from flow-induced vibration at the fuel assembly/lower core plate

interface. In Refueling Outage 2R11 (February 2003), Thimble Tube L-13

showed 16 percent wear at the upper tie plate area (located in the reactor vessel

lower internals). Since the wear was deemed acceptable per

Procedure STP R-22, Thimble Tube Inspection Program, Revision 5, PG&E did

not perform any corrective actions on the tube. In Refueling Outage 2R12

(November 2004), the wear on Thimble Tube L-13 indicated 46 percent at the

upper tie plate area, and maintenance personnel repositioned the tube by

5 inches. In Refueling Outage 2R13 (May 2006), the wear on Thimble

Tube L-13 again showed 46 percent through-wall, and maintenance personnel

repositioned the tube by another 5 inches. Thimble Tube L-13 began leaking

approximately 3 months later.

NCR N0002211 noted that, when maintenance personnel repositioned Thimble

Tube L-13 the second time in Refueling Outage 2R13, the tube had been

repositioned such that the chrome-plated band on the thimble tube was no

longer in its designed location. As a result of thimble tube wall-thinning

discovered in 1989 and 1990, NCR N0001325, Corrective Action to Prevent

Recurrence 3, called for implementation of a design change to eliminate or

greatly reduce flow-induced thimble tube wear rates. Westinghouse had

developed thimble tubes with chrome-plated bands which would be more

resistant to flow-induced thimble tube wear. PG&E installed these thimble tubes

in Refueling Outage 1R6 for Unit 1 and Refueling Outage 2R10 for Unit 2.

When the new thimble tube was installed at the L-13 position, the chrome-plated

band was 16 inches long, with approximately 9 inches above the fuel assembly

bottom nozzle and 7.5 inches below the lower core plate. The chrome-plated

band was placed in this location since operating experience had shown the fuel

assembly bottom nozzle/lower core plate interface to be a high wear-rate area.

As discussed in AR A0205526, engineering personnel observed that the chrome-

plated thimble tubes were an approved replacement part provided by

Westinghouse. Therefore, engineering staff did not implement a design change

for the new thimble tubes, but did have the drawings updated to reflect the

chrome band on the thimble tubes. Subsequently, Procedure STP R-22 was not

revised in order to restrict the amount of reposition for the chrome-plated thimble

tubes. Therefore, when maintenance personnel repositioned Thimble Tube L-13

in Refueling Outage 2R13, the tube had been repositioned a total of 10 inches

during its life. The final reposition moved a section of nonchrome-plated thimble

tube area to the fuel assembly bottom nozzle/lower core plate interface.

Analysis: The performance deficiency associated with this finding involved

engineering personnel failing to apply adequate design control measures, which

would have included necessary procedure changes to reflect the use of thimble

tubes with chrome bands. The finding is greater than minor because it is

associated with the Initiating Events Cornerstone attribute of design control and

affects the associated cornerstone objective to limit the likelihood of those events

that upset plant stability and challenge critical safety functions during shutdown

-32- Enclosure

as well as power operations. Using the Inspection Manual Chapter 0609,

Significance Determination Process, Phase 1 Worksheet, the finding is

determined to have very low safety significance because, assuming the worst-

case degradation, the finding would not result in exceeding the TS limit for

identified RCS leakage or affect mitigating systems. Specifically, the inspectors

verified the worst-case leakage, i.e. guillotine break, from a thimble tube at the

fuel assembly bottom nozzle/lower core plate interface to be approximately

7 gpm versus the TS RCS identified leakage limit of 10 gpm. The finding has a

crosscutting aspect in the area of problem identification and resolution

associated with the CAP because PG&E disabled a corrective action to prevent

recurrence of significant thimble tube wear.

Enforcement: 10 CFR Part 50, Appendix B, Criterion III, Design Control,

requires, in part, that design control measures shall provide for verifying or

checking the adequacy of design. Design changes, including field changes,

shall be subject to design control measures commensurate with those applied to

the original design. Contrary to this, on April 24, 2006, engineering personnel

removed a corrective action to prevent significant thimble tube wear when they

repositioned Thimble Tube L-13 such that the tube was no longer in its intended

location. Specifically, Thimble Tube L-13 was repositioned to the extent that its

chrome-plated band was no longer effectively covering the fuel assembly bottom

nozzle and lower core plate interface zone. The cause of the violation was the

failure of engineering personnel to update applicable procedures with information

that would prevent the chrome-plated bands from being removed from their

designed location during repositioning of thimble tubes. The corrective actions

to restore compliance included actions to update the applicable procedures to

provide repositioning limits on thimble tubes with chrome-plated bands and to

utilize thimble tubes with chrome-plated bands for the entire length of tube inside

the reactor vessel. Because the finding is of very low safety significance and

has been entered into PG&Es CAP as NCR N0002211, this violation is being

treated as an NCV consistent with Section VI.A of the Enforcement Policy:

NCV 50-323/06-05-05, Failure to Update Relocation Procedure for Thimble Tube

Chrome Band.

40A6 Management Meetings

Exit Meeting Summary

On October 27, 2006, the lead inspector presented the results of the biennial

emergency preparedness exercise inspection to Ms. D. Jacobs, Vice President, Nuclear

Services, and other members of her staff, who acknowledged the findings. The

inspector confirmed that proprietary information was not provided or examined during

the inspection.

On December 20, 2006, the inspectors presented the findings of the inspection on

biennial heat sink performance to Mr. L. Parker and other members of PG&E

management. PG&E acknowledged the inspection findings.

-33- Enclosure

The resident inspection results were presented on January 10, 2007, to Ms. D. Jacobs,

Vice President, Nuclear Services, Diablo Canyon and other members of PG&E

management. PG&E acknowledged the findings presented.

The inspectors asked PG&E whether any materials examined during the inspection

should be considered proprietary. Proprietary information was reviewed by the

inspectors and left with PG&E at the end of the inspection.

ATTACHMENT: SUPPLEMENTAL INFORMATION

-34- Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

PG&E Personnel

J. Becker, Vice President - Diablo Canyon Operations and Station Director

D. Burns, Operations Training Supervisor

C. Dougherty, Regulatory Services Senior Engineer

S. David, Operations Director

D. Fried, Emergency Planning Coordinator

M. Ginn, Emergency Planning Coordinator

J. Haynes, Training manager

J. Haynes, Licensing Services Manager

R. Hite, Manager, Radiation Protection

D. Jacobs, Vice President - Nuclear Services

S. Ketelsen, Manager, Regulatory Services

K. Langdon, Director, Operations Services

M. Lemke, Emergency Planning Principal

M. Meko, Director, Site Services

C. Over, Regulatory Services Supervisor

L. Parker, Regulatory Services Supervisor

K. Peters, Director, Engineering Services

J. Purkis, Director, Maintenance Services

P. Roller, Director, Performance Improvement

D. Taggart, Manager, Quality Verification

B. Terrell, Emergency Planning Supervisor

R. Waltos, Manager, Emergency Preparedness

M. Zawalick, Emergency Services, Senior Coordinator

S. Zawalick, Regulatory Services Engineer

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-275; 323/06-05-01 URI Additional Review of Material to Determine if the RHR

Heat Exchangers Will Meet Their Safety Function

(Section 1R07.2)

Opened and Closed

50-275; 323/06-05-02 NCV Failure to Adequately Evaluate Operability of Auxiliary

Building Ventilation Control Panels (Section 1R13)

50-275/06-05-03 NCV Inadequate Temporary Modification to a Vital Battery

(Section 1R15)

A-1 Attachment

50-275; 323/06-05-04 NCV Inadequate Change to Auxiliary Saltwater Pump Routine

Surveillance Test Acceptance Criteria (Section 4OA2.2)

50-323/06-05-05 NCV Failure to Preserve Corrective Action for Thimble Tube

Wear (Section 4OA5.5)

Closed

50-275; 323/06-12-01 URI Oil Found in the Vicinity of Residual Heat Removal Pumps

(Section 4OA5.3)

72-026/06-01-01 URI Review the Concrete Compressive Strength Test Results

to Confirm that the Concrete Compressive Strength of the

Cask Transfer Facility Basemat and Initial Independent

Spent Fuel Storage Installation Pad Meet the Specified

Compressive Strength of 5,000 psi at 90 days

(Section 4OA5.4)

50-323/06-04-03 URI Corrective Actions Regarding RCS Leakage Through In-

core Thimble Tube (Section 4OA5.5)

LIST OF DOCUMENTS REVIEWED

Section 1R05: Fire Protection

Procedures

Number Title Revision

A-6 Equipment Inspections 5

OM8.ID4 Control of Flammable and Combustible Materials 14

STP M-69A Monthly Fire Extinguisher Inspection 36

STP M-69B Monthly CO2 Hose Reel and Deluge Valve Inspection 14

STP M-70C Inspection/Maintenance of Doors 10

A-2 Attachment

Section 1R07: Biennial Heat Sink Performance (71111.07B)

Action Requests

A0341604 A0556717 A0600918 A0608887 A0617092 A0648128

A0391927 A0588366 A0608886 A0608888 A0640406 A0653252

A0380732 A0592857

Calculations

Number Title Revision

M-938 CCW Data Input for 1993 Containment Analysis Program 3

M-1017 Determine Flows in the CCW System 3

Procedures

Number Title Revision

STP M-93A Refueling Interval Surveillance - Containment Fan Cooler 18

STP M-13A CCW Flow Balancing 15

BIO D-5 Microfouling Sample Collections in Component Cooling 0A

Water Heat Exchangers

CAP O-6 Chemical Additions to the Closed Cooling Water Systems 16A

OP F-5:III Chemistry Control Limits and Action Guidelines for the 18

Plant Support Systems

PEP M-200 Flow Balancing CCW to Equipment on CCP Pump Skid 0

Miscellaneous Documents

Title Date/Revision

DCM No. S-23A, Design Criteria Memorandum Containment HVAC 18C

System

DCM No. S-10, Design Criteria Memorandum S-10 Residual Heat 13D

Removal System

A-3 Attachment

Title Date/Revision

DCM No. S-14, Design Criteria Memorandum Component Cooling Water 15E

System

Nonconformance Report N0002194, Void at CCP - SIP Suction Cross Tie 0

PG&E letter DCL 90-027 Jan. 26, 1990

Westinghouse Letter PGE 96-605 Sept. 3, 1996

Work Orders

C0193402 R0234221 R0258879 R0259792 R0259790 R0259627

R0259787 R0269129 R0269164 R0234221 R0244369 R0244367

Section 1R12: Maintenance Effectiveness (71111.12)

Action Requests

A0678838 A0681428 A0681464

Procedures

Number Title Revision

MP E-53.7 Maintenance of ITT, General Controls Hydramotor Actuator 9A

AD13.ID4 Post-Maintenance Testing 14

Section 1R13: Maintenance Risk Assessments and Emergent Work Control (71111.13)

Action Requests

A0610558 A0636037 A0637526 A0642790 A0660739 A0678429

A0678436 A0681559 A0683008 A0684812

Procedures

Number Title Revision

A-29 Protected Train Restrictions 3

A-4 Attachment

Number Title Revision

AD7.DC6 On-line Maintenance Risk Management 9

MA1.DC10 Troubleshooting 9

MA1.DC11 Risk Assessment 7

OP J-2:VIII Guidelines for Reliable Transmission Service for DCPP 10

OP1.DC17 Control of Equipment Required by the Plant Technical 11

Specifications or Other Designated Programs

OM7.ID12 Operability Determination 9

OP H-1:I Auxiliary Building Ventilation System - Make Available 9

and System Operation

Work Requests

C0202499 C0206797 C0208219

Section 1R15: Operability Evaluations (71111.15)

Action Requests

A0678820 A0680025 A0681006 A0682008

Calculations

Number Title Revision

235A-DC Battery 11 Sizing, Load Flow, Voltage Drop, Short Circuit 8

and Charger Sizing

369-DC Vital 125 VDC System Calculation for PRA System 1

Analysis (Station Blackout)

Drawings

Number Title Revision

437546 Single Line Meter and Relay Diagram 125 Volt DC System 39

445075 Single Line Meter and Relay Diagram 125 Volt DC System 156

A-5 Attachment

445076 Single Line Meter and Relay Diagram 125 Volt DC System 15

050024 List of Electrical Devices for Protection and Control Circuits 47

D-INV-4- Discharge Characteristics LCUN-33 1

88598

Procedures

Number Title Revision

MP E-67.6 Station Battery Preventive Maintenance 6

OP O-2 Operation of Hagan Controllers 10

STP M-11A Station Battery and Pilot Cell Condition Monitoring 20

STP M-11B Station Battery Condition Monitoring 26

STP M-21A Vital Station Battery Modified Performance Test 12

Work Requests

R0233847 R0213290

Miscellaneous Documents

Title Date/Revision

Amendment to Facility Operating License, Amendment No. 190, Nov. 15, 2006

License DPR-80

ASCO Letter, Potential Non-Conformances of Plunger Tubes Used In Sept. 15, 2006

Certain NH Series Hydramotor Pump and pump Kits

BCT-2000 Battery Load Test Report, Modified Performance Test Vital Oct. 27, 2005

Battery 1-1"

BCT-2000 Battery Load Test Report, Modified Performance Test Non- May 12, 2006

Vital Battery 2-5"

DCM No. T-42, Station Blackout 9

A-6 Attachment

Title Date/Revision

IEEE Standard 535-1986, Qualification of Class 1E Lead Storage

Batteries

Operations Shift Orders Oct. 17, 2006

Regulatory Guide 1.155, Station Blackout Aug. 1988

PG&E Letter DCL-06-120, Exigent License Amendment Request 06-08

Revision to Technical Specification 3.8.4, DC Sources-Operating, Oct. 18, 2006

Condition B

PG&E Letter DCL-06-126, Supplement to Exigent License Amendment

Request 06-08 Revision to Technical Specification 3.8.4, DC Sources- Oct. 18, 2006

Operating, Condition B

Section 1R17: Permanent Plant Modifications (71111.17)

Action Requests

A0678267

Documents

IB-129-154, Westinghouse Instruction bulletin, Remote/Manual Setpoint Station, dated

November 1968

Drawings

Number Title Revision

102032 Excess Letdown Heat Exchanger Outlet Loop Block Diagram, 148

Sheet 26

102032 Excess Letdown Heat Exchanger Outlet Loop Block Diagram, 116

Sheet 31

106725 Unit 1 Containment 109

448928 Electrical Diagram Connections Unit 1 Vertical Control 31

Board 1VB2

437930 Electrical Diagram Of Connections Penetration No. 24E 16

A-7 Attachment

Work Requests

C0206720

Section 1EP1: Emergency Plan Implementing Procedures (71114.01)

EP G-1 Revision 34 Emergency Classification and Emergency Plan Activation

EP G-2 Revision 31 Interim Emergency Response Organization

EP G-3 Revision 47 Emergency Notification of Off-Site Personnel

EP G-4 Revision 22 Assembly and Accountability

EP G-5 Revision 9A Evacuation of Nonessential Personnel

EP OR-3 Revision 6B Emergency Recovery

EP RB-1 Revision 5B Personnel Dosimetry

EP RB-2 Revision 5 Emergency Exposure Guides

EP RB-3 Revision 5 Stable Iodine Thyroid Blocking

EP RB-4 Revision 4A Access to and Establishment of Controlled Areas Under

Emergency Conditions

EP RB-5 Revision 6 Alternate Personnel Decontamination Facilities

EP RB-8 Revision 19 Instructions to Field Monitoring Teams

EP RB-9 Revision 11A Calculation Release Rate

EP RB-10 Revision 12 Protective Action Recommendations

EP RB-11 Revision 12 Emergency Offsite Dose Calculations

EP RB-12 Revision 6 Plant Vent Iodine and Particulate Sampling During

Accident Conditions

EP RB-14 Revision 8A Core Damage Assessment Procedure

EP RB-14A Revision 0 Initial Detection of Core Damage

EP RB-15 Revision 11 Post Accident Sampling System

EP RB-16 Revision 0 Operating Instructions for the EARS Computer Program

EP R-2 Revision 23 Release of Airborne Radioactive Materials Initial

Assessment

EP R-3 Revision 8C Release Of Radioactive Liquids

EP R-7 Revision 15A Off-Site Transportation Accidents

EP EF-1 Revision 33A Activation and Operation of the Technical Support Center

EP EF-2 Revision 28 Activation and Operation of the Operations Support

Center

EP EF-3 Revision 26A Activation and Operation of the Emergency Operations

Facility

EP EF-4 Revision 15 Activation of the Off-Site Emergency Laboratory

EP EF-9 Revision 10 Backup Emergency Response Facilities

EP EF-10 Revision 8 Activation and Operation of the Joint Media Center

TQ1 Revision 3 Personnel Training and Qualification

TQ1.ID3 Revision 5 Non-accredited Training Program Management

OM10.ID4 Revision 7 ERO Management

OM10.DC2 Revision 4 ERO On-Call

Exercise Evaluation Reports:

Drill Reports for 2004 and 2002 Biennial NRC Evaluated Exercise

All full-scale Exercise reports conducted in 2005-2006

A-8 Attachment

Summary List of Drill/Exercise Evaluation related Condition Reports, July 2004 through

September 2006

Emergency Plan, Revision 45

Section 4OA2: Problem Identification and Resolution (71152)

Action Requests

A0528837 A0631582 A0657460 A0669488 A0680274 A0685913

A0535731 A0636681 A0661341 A0672126 A0680773

A0558389 A0636984 A0664245 A0679011 A0684631

Procedures

Number Title Revision

STP M-89 (Unit 1) ECCS System Venting 46

STP P-ASW-11 Routine Surveillance Test of Auxiliary Saltwater Pump 1-1 23

STP P-ASW-12 Routine Surveillance Test of Auxiliary Saltwater Pump 1-2 20

STP P-ASW-21 Routine Surveillance Test of Auxiliary Saltwater Pump 2-1 22

STP P-ASW-22 Routine Surveillance Test of Auxiliary Saltwater Pump 2-2 18

Calculations

Number Title Revision

STA-108 ECCS Pump Suction Void Evaluation 0

Miscellaneous Documents

Title Date

Licensing Position - Definition of Full and Accessible for Performance of Sept. 4, 2001

Technical Specification (TS) Surveillance Requirement (SR) 3.5.2.3

(Revision 1)

A-9 Attachment

Title Date

NRC Information Notice 97-40, Potential Nitrogen Accumulation June 26, 1997

Resulting From Backleakage From Safety Injection Tanks

Vendor Document DC 663030-17-8, Page 69, Auxiliary Saltwater Pumps Dec. 24, 1969

Section 4OA1: Emergency Implementing Procedures (71151)

OM10.DC1, Emergency Preparedness Drills and Exercises, Revision2A

AWP EP-001, Emergency Preparedness Performance Indicators, Revision 5

EP G-3, Emergency Notification of Off-Site Agencies, Revision 43, Attachment

6.1, Instructions for the DCPP Emergency Notification Form

EP R-2, Release of Airborne Radioactive Materials Initial Assessment, Revision

23

EP RB-10, Protective Action Recommendations, Revision 11

Section 4OA3: Event Followup (71153)

Action Requests

A0132116 A0165736 A0342551 A0665509 A0684192 A0685056

A0164337 A0205526 A0623606 A0684170 A0684536 A0686189

Drawings

Number Title Revision

441227 Single Line Meter & Relay Diagram 12 kV System Bus 21

Section D & E

441284 Schematic Diagram - Circulating Water Pumps 31

441338 Schematic Diagram - Bus Potential and Synchronizing 16

12 kV System

441350 Schematic Diagram - 12 kV Bus Sections D & E Automatic 8

Transfer

A-10 Attachment

Procedures

Number Title Revision

AR PK05-02 RCP No. 22 20

EP G-1 Emergency Classification and Emergency Plan Activation 34

EP G-3 Emergency Notification of Off-Site Agencies 47

NDE ET-2 Eddy Current Examination of Heat Exchanger Tubing 5

OP AP-28 Reactor Coolant Pump Malfunction 2

STP R-22 Thimble Tube Inspection Program 5/6

Miscellaneous Documents

Title Date

DC-663102-24-2, Westinghouse Installation - Operation - Maintenance Jan. 4, 1985

Instructions for Types SSV-T and SSC-T Relays for Class 1E Application

Event Investigation Report 2006-001, Unit 2 Reactor Trip and Unusual Dec. 13, 2006

Event Due to CWP 2-1 Fault

Event Notification 42822 Aug. 31, 2006

Event Notification 43042 Dec. 10, 2006

Event Notification 43047 Dec. 12, 2006

Licensee Event Report 93-007-00, Manual Reactor Trip Initiated Due to June 26, 1993

High Stator Temperature on Reactor Coolant Pump

Nonconformance Report (NCR) DC1-89-TN-N096/2, Incore Thimble Jan. 30, 1991

Tubes (also titled NCR N0001325)

A-11 Attachment

Title Date

NCR N0002211, Root Cause Analysis Report - RCS Leak Through MIDS Oct. 18, 2006

Thimble Tube

NRC Bulletin 88-09, Thimble Tube Thinning in Westinghouse Reactors July 26, 1988

NRC Information Notice 87-44, Thimble Tube Thinning in Westinghouse Sept. 16, 1987

Reactors

PG&E Letter DCL-88-208, Thimble Tube Thinning in Westinghouse Aug. 26, 1988

Reactors

PG&E Letter DCL-89-280, Thimble Tube Thinning in Westinghouse Nov. 10, 1989

Reactors

PG&E Letter DCL-89-292, Thimble Tube Thinning Due to Flow-Induced Nov. 20, 1989

Vibration

PG&E Letter DCL-90-094, Thimble Tube Thinning April 4, 1990

PG&E Memorandum File No. 96, Licensing Position - TS 3.4.13 Oct. 5, 2006

Application for Threaded Connection Leakage

WCAP-12866, Bottom-Mounted Instrumentation Flux Thimble Wear Jan. 1991

Westinghouse Letter PGE-87-064, Flux Thimble Wear May 5, 1987

Westinghouse Letter PGE-90-537, BMI Thimble Tube Wear Evaluation Feb. 16, 1990

A-12 Attachment

LIST OF ACRONYMS

ac alternating current

ADAMS agency document and management system

ALARA As Low As is Reasonably Achievable

ANSI/IEEE American National Standards Institute/Institute of Electrical and Electronics

Engineers

AR action request

ASW auxiliary saltwater

CAP corrective action program

CCW component cooling water

CFR Code of Federal Regulations

CFCU containment fan cooling unit

CTF cask transfer facility

CWP circulating water pump

dc direct current

EAL emergency action level

ECCS emergency core cooling system

FSAR Final Safety Analysis Report

ISFSI Independent Spent Fuel Storage Installation

LER licensee event report

MIDS movable in-core detector system

MSPI Mitigating Systems Performance Index

NCR nonconformance report

NCV noncited violation

A-13 Attachment

NRC Nuclear Regulatory Commission

PG&E Pacific Gas and Electric Company

RCP reactor coolant pump

RCS reactor coolant system

RHR residual heat removal

SSC structure, system, and component

TS Technical Specifications

TSA transporter seismic anchor

URI unresolved item

A-14 Attachment