LR-N19-0011, In-Service Inspection Activities - 90-Day Report

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In-Service Inspection Activities - 90-Day Report
ML19042A019
Person / Time
Site: Salem PSEG icon.png
Issue date: 02/11/2019
From: Martino P
Public Service Enterprise Group
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LR-N19-0011
Download: ML19042A019 (5)


Text

PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, NJ 08038-0236 PSEG J.Vnclear LLC fEB 1 1 2019 ASME Code Case N-532-5 LR-N 19-0011 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington DC 20555-0001 Salem Generating Station Unit 2 Renewed Facility Operating License DPR-75 NRC Docket No. 50-311

Subject:

In-Service Inspection Activities Day Report This letter submits the Owner's Activity Report for In-Service Inspection (lSI) activities conducted at the Salem Generating Station Unit 2 during the twenty-third refueling outage.

This report is submitted in accordance with Code Case N-532-5 "Repair/Replacement Activity Documentation Requirements and In-Service Summary Report Preparation and Submission Section XI, Division 1,"and within its ninety day reporting requirement. to this letter contains the required Salem Unit 2 Owner's Activity Report.

There are no commitments contained in this letter.

Should you have any questions regarding this submittal, please contact Mr. Thomas Cachaza at 856-339-5038.

Sincerely,

~

Patrick Martino Plant Manager- Salem Salem Generating Station Enclosure

LR-N19-0011 Page 2 cc: Mr. D. Dorman, USNRC -Administrator-Region 1 Mr. J. Kim, USNRC -Licensing Project Manager-Salem Mr. P. Finney, USNRC Senior Resident Inspector Mr. P. Mulligan, Chief, NJBNE Mr. T. Cachaza, Salem Commitment Tracking Coordinator Mr. L. Marabella, Corporate Commitment Tracking Coordinator Mr. M. Washington, Chief Inspector- Occupational Safety and Health Bureau of Boiler and Pressure Vessel Compliance LR-N 19-0011 Salem Unit 2 Owner's Activity Report- S2RF023 In Accordance With ASME Section XI Code Case N-532-5

FORM OAR-1 OWNER'S ACTIVITY REPORT ReportNumber~S=Z=R=F~0=2=3----------------~------------------------------------------

Piant Salem Generating Station Unit No . ......!2~------ Commercial service date October 13.1981 Refueling outage no.-=2:..::3..___ _ _ _ _ _ __

(If appHcable) current inspection interval lSI - Fourth (4th), CISI - Second (2nd)

(1~t. 2nd, 3rd, 4th, clhar)

Current inspection period lSI- Second (2nd) CISI- Third (3rd)

(1Sl, 2nd, 3rt1)

Edition and Addenda of Section XI applicable to the inspection plans 2004 Edition. No addenda Date and revision of inspection plans [SI Reyision 3. August 2018 (CIS I Revision 2. September 2018)

Edition and Addenda of Section XI applicable to repair/replacement activities, if different than the inspection plans _ _ __

Same as lSI Plans Code Cases used for inspection and evaluation: N~460. N-532-5 N-566-2. N-706-1. N-716-1. N-722-1. N-729-4 and N-770-2.

{"If applicable, Including casu mcdlllea by Casa N*532 ~nd later revisions)

CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code;Section XI; and (c) the repair/replacement activities and evaluations supporting the completion of ..!:::S:.:2~R!:!..F~0:.!::2~3~---

<retuellng outage number)

CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and employed by Hartford Steam Boiler of Hartford. CT have Inspected the Items described In this Owner's Activity Report, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.

By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described In this report. Furthermore, neither the Inspector nor his employer shafl be liable in any manner for any perso JUry or property e or a loss of any kind arising from or connected with this inspection .

. 1-

FORM OAR-1 OWNER'S ACTIVITY REPORT TABLEt ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Exam Item Item Description Evaluation Description Category Number B-P B15.10b S2CVC-2CV77 Body-to- Order 70203562, S2CVC-2CV77 Boric Acid Program Bon net inactive boric acid Evaluation was performed as well as a Body-to*

indication was observed Bonnet Stud Failure Evaluation. Valve was around the body to bonnet disassembled during S2R20 for seat replacement, seam during a scheduled ASME Section XI VT-2 bolting was good condition at that time. Current examination of class 1 evaluation is for one cycle, the valve will be bolted connection. disassembled during next refueling outage S2R24 for inspection.

TABLE2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Item Description of Date RepairiReplacement Code Class Description Work Completed Plan Number 3 Service Water leak was Replaced Service Water 09/04/2018 60139163 identified 21 SW header, header 2" branch pinhole leak was in 2" pipe connection.

connection on top of header.

MC License Renewal Performed weld overlay 01/22/2019 60135577 Containment Liner of 6 inch by 6 inch area inspections beneath to restore containment insulation system revealed liner thickness to design corrosion and wall loss requirements.

below minimum required wall thickness.

MC Containment IWE Removed moisture 01/22/2019 60135577 inspections of moisture barrier below concrete barrier at floor to floor grade to sound containment liner was metal, performed UT found degraded. thickness measurements and found a 3 inch by 10 foot long area of containment liner knuckle below design wall thickness, performed weld overlay to restore containment liner thickness to design requirements.