LR-N13-0159, In-Service Inspection Activities - 90-Day Report

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In-Service Inspection Activities - 90-Day Report
ML13205A302
Person / Time
Site: Salem PSEG icon.png
Issue date: 07/24/2013
From: Jamila Perry
Public Service Enterprise Group
To:
Office of Nuclear Reactor Regulation, Document Control Desk
References
LR-N13-0159, N-532-4
Download: ML13205A302 (5)


Text

PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, NJ 08038-0236 0PSEG ASME Code Case N-532-4 JUL 24 2013 LR-N13-0159 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-001 Salem Nuclear Generating Station Unit 1 Renewed Facility Operating License DPR-70 NRC Docket No. 50-272

Subject:

In-Service Inspection Activities- 90-Day Report This letter submits the Owner's Activity Report for In-Service Inspection (lSI) activities conducted at the Salem Generating Station Unit 1 during the twenty-second refueling outage.

This report is submitted in accordance with Code Case N-532-4 "Repair/Replacement Activity Documentation Requirements and In-Service Summary Report Preparation and Submission Section XI, Division 1," and within its ninety (90) day reporting requirement. to this letter contains the required Salem Unit 1 Owner's Activity Report. There are no commitments contained in this letter.

Should you have any questions regarding this submittal, please contact C.M. Dahms at (856) 339-5456.

Sincerely, cj'thf! R.z John Perry Site Vice President -

  • alem Enclosures (1)

JUL 24 2013 Document Control Desk Page2 LR-Nl3-0159 C Mr. W. Dean, Administrator, Region I, NRC Mr. J. Hughley, Project Manager, NRC Mr. J. Hawkins, NRC Senior Resident Inspector, Salem Mr. P. Muligan, Manager IV, NJBNE Mr. L. Marabella, Corporate Commitment Tracking Coordinator Mr. T. Cachaza, Salem Commitment Tracking Coordinator Mr. Milton Washington, Chief Inspector- Occupational Safety and Health Bureau of Boiler and Pressure Vessel Compliance

Document Control Desk LR-Nl3-0159 Salem Unit 1 Owners Activity Report- S1R22 In Accordance With ASME Section XI Code Case N-532-4

FORM OAR-1 OWNER'S ACTIVITY REPORT ReportNumber S1RF022 Owner P SEGNuclear LLC, PO Box 236, Hancocks Bridge, NJ 08038 Plant Salem Gen erating Station UnitNo. 1 Commercial Service Date July 1, 1977 Refueling OutageNo. 22 Current Inspection Interval lSI- Fourth (4th) {CISI- S econd (2nd)}

Current Inspection Period lSI- First (1st) {CISI- First (1st)}

Edition and Addenda of Section XI Applicable to the inspection plan lSIand CISI- 2004 Edition Date and revision of inspection plan lSI- July 2012, Revision 1 {CISI- October 2010, Revision 0}

Code Cases used N-460, N-532-4, N-706-1 & N-722-1 CERTIFICATE O F CON FORMANCE

=

I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supportin the completion of S1RF022 eo quirement' of Section XI.

Signed Edley T. Giles I lSI Program Manager Owner or Owner's Designee, Title 07s;7Zt:J/ .3 Date CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and the State or Province of New Jersey and employed by Hartford Steam Boiler Ins:gection and Insurance Com:gany of C01mecticut have inspected the items described in this Owner's Activity Report, during the period November23, 2011 to May 27, 2013, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section X I.

By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report.

Furthermore, neither the Inspector nor his employer shall be liable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with this inspection.

Ross Goodwin ZJ&.. U .

Inspector's Signature Commissions NB 14086 A,N,I NJ955 National Board, State, Province, and Endorsements Date 6¥-1o/26l3

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FORM OAR-1 OWNER'S ACTIVITY REPORT TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Exam Item Item Description Evaluation Description Category Number Augmented Owner Containment Liner Plate, The technical evaluation of 5 inch by 2 inch mid wall (E-C) (E4.12) performed UT thickness plate lamination identified under notification 20603606.

measurements during Evaluation concluded that the lamination does not impact License Renewal the structural integrity of the liner as the stresses are examinations membrane stresses and the effective cross-sectional area is the same as the nominal plate cross-sectional area.

TABLE2 ABSTRACT OF REPAIR/REPLACEMENT ACTITIES REQUIRED FOR CONTINUED SERVICE Code Item Description Description ofWork Date Repair/

Class Completed Replacement Plan Number Through wall leak in 0.75 Replace 0.75 inch piping from No. 11 inch carbon steel schedule 40 Component Cooling Pump to Valve 05/15/2012 60102788 piping upstream of Valve Sl CC-11CC227 3 11CC227 Snubber 1MSSN12B serial Installed New Snubber number 0900610/006, Lisega 04/24/2013 50146649 M odel 309253RC4 failed 2 Tension Bleed Rate test.

No. 11 Steam Generator Steam Generator tubes plugged (both 05/08/2013 50132246 1 Tubing_Inspections ends)- 4 tubes.

No. 12 Steam Generator Steam Generator tubes plugged (both 05/08/2013 50132247 1 Tubing Inspections ends)- 3 tubes No. 13 Steam Generator Steam Generator tubes plugged (both 05/08/2013 50132263 1 Tubing Inspections ends)- 3 tubes No. 14 Steam Generator Steam Generator tubes plugged (both 05/09/2013 50132248 1 Tubing Inspections ends)- 3 tubes Containment Liner beneath Cleaned Containment Liner, performed insulation system had UT thickness measurements and 05/21/2013 60107638 degraded coatings (License repaired coatings.

MC Renewal examination) 2 inch Valve 12MS7 had Installed new plug and seal weld 05/16/2013 60110660 2 leak at 0.25 inch pipe plug No. 11 Safety Injection Replaced No. 11 Safety Injection Pump Pump Lube Oil Cooler End Lube Oil Cooler End Bells 08/16/2012 60105064 Bell through wall leakage 3 (lSJElOO)

No. 12 Safety Injection Replaced No. 12 Safety Injection Pump Pump Lube Oil Cooler End Lube Oil Cooler End Bells 08/20/2012 60105103 Bell through wall leakage 3 (lSJElOl )

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