LR-N16-0025, In-Service Inspection Activities - 90-Day Report
| ML16057A316 | |
| Person / Time | |
|---|---|
| Site: | Salem |
| Issue date: | 02/26/2016 |
| From: | Carr E Public Service Enterprise Group |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| LR-N16-0025 | |
| Download: ML16057A316 (5) | |
Text
PSEG Nuclear LLC P.O. Box 236, Hancocks Btidge, NJ 08038?0236 February 26, 2016 LR-N 16-0025 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington DC 20555-0001 Salem Generating Station Unit 2 Renewed Facility Operating License DPR-75 NRC Docket No. 50-311 ASME Code Case N-532-4
Subject:
In-Service Inspection Activities Day Report This letter submits the Owner's Activity Report for In-Service Inspection (ISi) activities conducted at the Salem Generating Station Unit 2 during the twenty-first refueling outage. This report is submitted in accordance with Code Case N-532-4 "Repair/Replacement Activity Documentation Requirements and In-Service Summary Report Preparation and Submission Section XI, Division 1," and within its ninety day reporting requirement. to this letter contains the required Salem Unit 2 Owner's Activity Report.
There are no commitments contained in this letter.
Should you have any questions regarding this submittal, please contact Mr. Michael Phillips at 856-339-1873.
Eric Carr Plant Manager Salem Generating Station Enclosure
February 26, 2016 Page2 LR-N16-0025 cc:
Mr. D. Dorman, USNRC -Administrator-Region 1 Ms. C. Sanders, USNRC -Licensing Project Manager-Salem Mr. P. Finney, USNRC Senior Resident Inspector Mr. P. Mulligan, NJBNE Manager IV Mr. T. Cachaza, Salem Commitment Tracking Coordinator Mr. L. Marabella, Corporate Commitment Tracking Coordinator Mr. M. Washington, Chief Inspector - Occupational Safety and Health Bureau of Boiler and Pressure Vessel Compliance LR-N16-0025 Salem Unit 2 Owner's Activity Report - S2RF021 In Accordance With ASME Section XI Code Case N-532-4 i'
FORM OAR-1 OWNER'S ACTIVITY REPORT ReportNumberKS2RFL Plant Salem Generating Station Unit No. #2---- Commercial service date October 13, 1981 Refueling outage no. '21-----
(If applicable)
Current inspection interval !SI - Fourth (41\\ GISI - Second (2"'l
{1K!. 2nd, 3rd, 4lh, o1her)
Current inspection period IS! - First (1'1), GISI - Second (2"')
(1sL 2nd, 3fd)
Edition and Addenda of Section XI appllc"ble to the inspection plans 2004 Edition No Addenda Date and revision of Inspection plans !SI Revision 1, July 2015 (CISI Revision 1, July 2015)
Edition and Addenda of Section XI appllcable to repair/replacement activities, if different than the inspection plans ___
Same as ISi Plans Code Cases used for inspection and evaluation: N-460 N-532-5 N-706-1 N-722-1 and N-770-1 (If applicable, Including cases modified by Case N*532 and later revisions)
CERTIFICATE OF CONFORMANCE I certifythat(a)the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supporting the completion of +S2RF,021--
Confonn to the requirements of Section X
{reruellng outage number)
Signed _ _L;;-:Z:.2 !"""-#a._
__.EQld l"e'L[T_(cGillil-"esU1l l/S1._I !::'_
Pre>;orura!!]mJ_0(,2w;,mne"1r:_
Date /,Jo/(;,
CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission Issued by the National Board of Boiler and Pressure Vessel Inspectors and employed by Hartford Steam Boiler Inspection and Insurance Company of Connecticut have inspected the Items described in this Owner's Actlvity Report, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report In accordance wlth the requirements of Section XI.
By signing this certificate neither the Inspector-nor his employer makes any warranty, expressed or implied, concerning the repairfreplacement activities and evaluation described in th!s report. Furthermore, neither the \\nspector nor his employer shall be Hable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with this Inspection.
Robert Wineoarden Q,:
lnspeotor's Signature Date 2/ S"") 'Zo J <;
NB 12442 A N I IS (Natlonal Board Number and Endorsement)
Code Class I 3
3 1
2 FORM OAR-1 OWNER'S ACTIVITY REPORT TABLE1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Examination Category and Item Number Item Description Evaluation Description None None None TABLE2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Item Descrlpllon Date I
Repair/Replacement Description of Work Completed Plan Number 3/8" Tubing pin hole leak between Replaced tubing and I 12/11/2015 I 60122014 isolation valve 22S\\/V94 and pressure flange between valve device 2LP746 22SW94 and 2LP746 3/8" Tubing to insert adapter weld leak Replaced tubing and 1212912015 60126676 at outlet side of flanged isolation valve flange betvveen valve 2SW329, tubing to pressure device 2SW329 and PL9629 PL9629 Hanger 2C-CVCS -522 has become Fabricated & Installed 11/2012015 60126638 dislodged from It proper position replacement pipe clamp with modified structural wide flange 3/8" Pressurizer steam space sample Replaced portion of 11/2412015 60127025 line tubing just prior to where it exits containment at penetration 188 had a leaking tubing thru wall leak in the tubing bend PSEG Nuclear LLC P.O. Box 236, Hancocks Btidge, NJ 08038?0236 February 26, 2016 LR-N 16-0025 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington DC 20555-0001 Salem Generating Station Unit 2 Renewed Facility Operating License DPR-75 NRC Docket No. 50-311 ASME Code Case N-532-4
Subject:
In-Service Inspection Activities Day Report This letter submits the Owner's Activity Report for In-Service Inspection (ISi) activities conducted at the Salem Generating Station Unit 2 during the twenty-first refueling outage. This report is submitted in accordance with Code Case N-532-4 "Repair/Replacement Activity Documentation Requirements and In-Service Summary Report Preparation and Submission Section XI, Division 1," and within its ninety day reporting requirement. to this letter contains the required Salem Unit 2 Owner's Activity Report.
There are no commitments contained in this letter.
Should you have any questions regarding this submittal, please contact Mr. Michael Phillips at 856-339-1873.
Eric Carr Plant Manager Salem Generating Station Enclosure
February 26, 2016 Page2 LR-N16-0025 cc:
Mr. D. Dorman, USNRC -Administrator-Region 1 Ms. C. Sanders, USNRC -Licensing Project Manager-Salem Mr. P. Finney, USNRC Senior Resident Inspector Mr. P. Mulligan, NJBNE Manager IV Mr. T. Cachaza, Salem Commitment Tracking Coordinator Mr. L. Marabella, Corporate Commitment Tracking Coordinator Mr. M. Washington, Chief Inspector - Occupational Safety and Health Bureau of Boiler and Pressure Vessel Compliance LR-N16-0025 Salem Unit 2 Owner's Activity Report - S2RF021 In Accordance With ASME Section XI Code Case N-532-4 i'
FORM OAR-1 OWNER'S ACTIVITY REPORT ReportNumberKS2RFL Plant Salem Generating Station Unit No. #2---- Commercial service date October 13, 1981 Refueling outage no. '21-----
(If applicable)
Current inspection interval !SI - Fourth (41\\ GISI - Second (2"'l
{1K!. 2nd, 3rd, 4lh, o1her)
Current inspection period IS! - First (1'1), GISI - Second (2"')
(1sL 2nd, 3fd)
Edition and Addenda of Section XI appllc"ble to the inspection plans 2004 Edition No Addenda Date and revision of Inspection plans !SI Revision 1, July 2015 (CISI Revision 1, July 2015)
Edition and Addenda of Section XI appllcable to repair/replacement activities, if different than the inspection plans ___
Same as ISi Plans Code Cases used for inspection and evaluation: N-460 N-532-5 N-706-1 N-722-1 and N-770-1 (If applicable, Including cases modified by Case N*532 and later revisions)
CERTIFICATE OF CONFORMANCE I certifythat(a)the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supporting the completion of +S2RF,021--
Confonn to the requirements of Section X
{reruellng outage number)
Signed _ _L;;-:Z:.2 !"""-#a._
__.EQld l"e'L[T_(cGillil-"esU1l l/S1._I !::'_
Pre>;orura!!]mJ_0(,2w;,mne"1r:_
Date /,Jo/(;,
CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission Issued by the National Board of Boiler and Pressure Vessel Inspectors and employed by Hartford Steam Boiler Inspection and Insurance Company of Connecticut have inspected the Items described in this Owner's Actlvity Report, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report In accordance wlth the requirements of Section XI.
By signing this certificate neither the Inspector-nor his employer makes any warranty, expressed or implied, concerning the repairfreplacement activities and evaluation described in th!s report. Furthermore, neither the \\nspector nor his employer shall be Hable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with this Inspection.
Robert Wineoarden Q,:
lnspeotor's Signature Date 2/ S"") 'Zo J <;
NB 12442 A N I IS (Natlonal Board Number and Endorsement)
Code Class I 3
3 1
2 FORM OAR-1 OWNER'S ACTIVITY REPORT TABLE1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Examination Category and Item Number Item Description Evaluation Description None None None TABLE2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Item Descrlpllon Date I
Repair/Replacement Description of Work Completed Plan Number 3/8" Tubing pin hole leak between Replaced tubing and I 12/11/2015 I 60122014 isolation valve 22S\\/V94 and pressure flange between valve device 2LP746 22SW94 and 2LP746 3/8" Tubing to insert adapter weld leak Replaced tubing and 1212912015 60126676 at outlet side of flanged isolation valve flange betvveen valve 2SW329, tubing to pressure device 2SW329 and PL9629 PL9629 Hanger 2C-CVCS -522 has become Fabricated & Installed 11/2012015 60126638 dislodged from It proper position replacement pipe clamp with modified structural wide flange 3/8" Pressurizer steam space sample Replaced portion of 11/2412015 60127025 line tubing just prior to where it exits containment at penetration 188 had a leaking tubing thru wall leak in the tubing bend