LR-N22-0068, In-Service Inspection Activities - 90-Day Report

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In-Service Inspection Activities - 90-Day Report
ML22222A083
Person / Time
Site: Salem PSEG icon.png
Issue date: 08/10/2022
From: Desanctis R
Public Service Enterprise Group
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LR-N22-0068, N-532-5
Download: ML22222A083 (5)


Text

PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, NJ 08038-0236 0 PSEG Nudear [,!,(;

ASME Code Case N-532-5 August 10, 2022 LR-N22-0068 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington DC 20555-0001 Salem Generating Station Unit 1 Renewed Facility Operating License DPR-70 NRC Docket No. 50-272

Subject:

In-Service Inspection Activities Day Report This letter submits the Owner's Activity Report for In-Service Inspection (ISi) activities conducted at the Salem Generating Station Unit 1 during the twenty-eighth refueling outage.

This report is submitted in accordance with Code Case N-532-5 "Repair/Replacement Activity Documentation Requirements and In-Service Summary Report Preparation and Submission Section XI, Division 1," and within its ninety day reporting requirement. to this letter contains the required Salem Unit 1 Owner's Activity Report.

There are no commitments contained in this letter.

Should you have any questions regarding this submittal, please contact Ms. Bernadette Humphrey at 856-339-1308.

Sincerely, Richard J. Desanctis Plant Manager- Salem Salem Generating Station Enclosure

LR-N22-0068 Page 2 cc: USNRC -Administrator-Region 1 USNRC -Licensing Project Manager-Salem USNRC Senior Resident Inspector Chief, NJBNE Salem Commitment Tracking Coordinator Corporate Commitment Tracking Coordinator Chief Inspector- Occupational Safety and Health Bureau of Boiler and Pressure Vessel Compliance LR-N22-0068 Salem Unit 1 Owner's Activity Report - S 1R28 In Accordance With ASME Section XI Code Case N-532-5

FORM OAR-1 OWNER'S ACTIVITY REPORT Report Number -=S_,_1_,_R=2=8'----------------------------------

Plant Salem Generating Station Unit No. _ _ _,___ _ _ Commercial Seivice Date July 1, 1977 Refueling Outage no. _ _ ___,,2"'8,_____

(If applicable}

Current Inspection lnteival ISi - Fifth (5 th ), CISI - Third (3 rd )

(1st, 2nd, 3rd, -4th, other)

Current Inspection Period ISi - First (1s t ), CISI - First (1s t )

(1st, 2nd, 3rd)

Edition and Addenda of Section XI Applicable to the Inspection Plans 2013 Edition, No Addenda Date and Revision of Inspection Plans ISl(CISI) Revision 2, February 2022 Edition and Addenda of Section XI Applicable to Repair/Replacement Activities, if different than the Inspection Plans _ __

Same as ISi (CISI) Plan Code Cases used for inspection and evaluation: N-532-5, N-716-1, N-729-6, N-805 & N-854 CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code, Section XI; and (c) the repair/replacement activities and evaluations supporting the completion of S1 R28 (Refueling outage number}

Conform to the requirements of Section XI.

CERTIFICATE OF INSERVICE INSPECTION I, the undersigned , holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and employed by Hartford Steam Boiler Inspection and Insurance Company of Hartford, Connecticut have inspected the items described in this Owner's Activity Report, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.

By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report. Furthermore, neither the Inspector nor his employer shall be liable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with this inspection.

Commission NB16247,N, I, R / NJ1238 (National Board Number and Endo~ement)

FORM OAR1 OWNERS ACTIVITY REPORT TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Exam Item Item Description Evaluation Description Category Number none none none none TABLE 2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Item Description of Work Date Repair/Replacement Code Class Description Complete Plan Number 1 Reactor Vessel Core Barrel Prior S1R27 outage UT of 05/09/2022 60148962 Thermal Shield Support Block TSSBBs identified one UT Bolt (TSSBB) degraded. degraded (67 Right) and one non-testable (292 Left) TSSBB with one cycle evaluation order 70215189.

Visual inspection of TSSBBs during S1R28 outage identified one additional visually degraded (292 Right) TSSBB. Replaced 4 TSSBBs, 292 degree location right and left and 67 degree location right and left.

2 Pinhole leak at the weld between Replaced 3/8 stainless steel 11/08/2021 60151939 1PL3610 3/8 stainless steel tubing between valve 1CV299 tubing and valve 1CV299 to 13 and 1PL3610.

Charging Pump discharge pressure local Indication.

2 3/8 stainless steel tubing Replaced 3/8 stainless steel 03/10/2022 60153199 sheared at downstream side of tubing between valve 1CV299 valve 1CV299 recently replaced and first coupling.

under order 60151939.

3 A through-wall ASME leak on Base Metal weld repair on 10 06/06/2022 60149728 cement lined 10" carbon steel 45 degree carbon steel service water bay strainer schedule 40 elbow.

blowdown and bearing cooling outlet line.

3 A through-wall ASME leak was Replaced 3/4 inch carbon steel 02/24/2021 60148734 identified on 3/4 inch carbon steel nipple at upstream side of valve nipple off 12 chill water pump 12CH9.

going to valve 12CH9.

2 A through-wall ASME leak was Replaced carbon steel panel 04/20/2021 60149499 identified on low side sensing line penetration nipple with stainless of transmitter 1FT523, the leak steel Union and 3/8 stainless was at carbon steel panel steel tubing.

penetration nipple.

2