LR-N22-0068, In-Service Inspection Activities - 90-Day Report
| ML22222A083 | |
| Person / Time | |
|---|---|
| Site: | Salem |
| Issue date: | 08/10/2022 |
| From: | Desanctis R Public Service Enterprise Group |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| LR-N22-0068, N-532-5 | |
| Download: ML22222A083 (5) | |
Text
August 10, 2022 LR-N22-0068 PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, NJ 08038-0236 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington DC 20555-0001
Subject:
Salem Generating Station Unit 1 Renewed Facility Operating License DPR-70 NRC Docket No. 50-272 In-Service Inspection Activities Day Report 0 PSEG Nudear [,!,(;
ASME Code Case N-532-5 This letter submits the Owner's Activity Report for In-Service Inspection (ISi) activities conducted at the Salem Generating Station Unit 1 during the twenty-eighth refueling outage.
This report is submitted in accordance with Code Case N-532-5 "Repair/Replacement Activity Documentation Requirements and In-Service Summary Report Preparation and Submission Section XI, Division 1," and within its ninety day reporting requirement. to this letter contains the required Salem Unit 1 Owner's Activity Report.
There are no commitments contained in this letter.
Should you have any questions regarding this submittal, please contact Ms. Bernadette Humphrey at 856-339-1308.
Sincerely, Richard J. Desanctis Plant Manager-Salem Salem Generating Station Enclosure
LR-N22-0068 Page 2 cc:
USNRC -Administrator-Region 1 USNRC -Licensing Project Manager-Salem USNRC Senior Resident Inspector Chief, NJBNE Salem Commitment Tracking Coordinator Corporate Commitment Tracking Coordinator Chief Inspector-Occupational Safety and Health Bureau of Boiler and Pressure Vessel Compliance LR-N22-0068 Salem Unit 1 Owner's Activity Report - S 1 R28 In Accordance With ASME Section XI Code Case N-532-5
FORM OAR-1 OWNER'S ACTIVITY REPORT Report Number -=S_,_1_,_R=2=8'----------------------------------
Plant Salem Generating Station Unit No. ___,__ ___ Commercial Seivice Date July 1, 1977 Refueling Outage no. ___ __,,2"'8,__ __ _
(If applicable}
Current Inspection lnteival ISi - Fifth (5th), CISI - Third (3rd)
(1st, 2nd, 3rd, -4th, other)
Current Inspection Period ISi - First (1st), CISI - First (1st)
(1st, 2nd, 3rd)
Edition and Addenda of Section XI Applicable to the Inspection Plans 2013 Edition, No Addenda Date and Revision of Inspection Plans ISl(CISI) Revision 2, February 2022 Edition and Addenda of Section XI Applicable to Repair/Replacement Activities, if different than the Inspection Plans __ _
Same as ISi (CISI) Plan Code Cases used for inspection and evaluation: N-532-5, N-716-1, N-729-6, N-805 & N-854 CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supporting the completion of S1 R28 Conform to the requirements of Section XI.
(Refueling outage number}
CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and employed by Hartford Steam Boiler Inspection and Insurance Company of Hartford, Connecticut have inspected the items described in this Owner's Activity Report, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.
By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report. Furthermore, neither the Inspector nor his employer shall be liable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with this inspection.
Commission NB16247,N, I, R / NJ1238 (National Board Number and Endo~ement)
FORMOAR1OWNERSACTIVITYREPORT
2
TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE
Exam Category Item Number ItemDescription EvaluationDescription none none none none
TABLE 2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE
Code Class Item Description DescriptionofWork Date Complete Repair/Replacement PlanNumber 1
Reactor Vessel Core Barrel Thermal Shield Support Block Bolt (TSSBB) degraded.
Prior S1R27 outage UT of TSSBBs identified one UT degraded (67 Right) and one non-testable (292 Left) TSSBB with one cycle evaluation order 70215189.
Visual inspection of TSSBBs during S1R28 outage identified one additional visually degraded (292 Right) TSSBB. Replaced 4 TSSBBs, 292 degree location right and left and 67 degree location right and left.
05/09/2022 60148962 2
Pinhole leak at the weld between 1PL3610 3/8 stainless steel tubing and valve 1CV299 to 13 Charging Pump discharge pressure local Indication.
Replaced 3/8 stainless steel tubing between valve 1CV299 and 1PL3610.
11/08/2021 60151939 2
3/8 stainless steel tubing sheared at downstream side of valve 1CV299 recently replaced under order 60151939.
Replaced 3/8 stainless steel tubing between valve 1CV299 and first coupling.
03/10/2022 60153199 3
A through-wall ASME leak on cement lined 10" carbon steel service water bay strainer blowdown and bearing cooling outlet line.
Base Metal weld repair on 10 45 degree carbon steel schedule 40 elbow.
06/06/2022 60149728 3
A through-wall ASME leak was identified on 3/4 inch carbon steel nipple off 12 chill water pump going to valve 12CH9.
Replaced 3/4 inch carbon steel nipple at upstream side of valve 12CH9.
02/24/2021 60148734 2
A through-wall ASME leak was identified on low side sensing line of transmitter 1FT523, the leak was at carbon steel panel penetration nipple.
Replaced carbon steel panel penetration nipple with stainless steel Union and 3/8 stainless steel tubing.
04/20/2021 60149499